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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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Text
CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
'ACCESSION NBR:9902250072 DOC.DATE: 99/02/12 NOTARIZED: NO DOCKET
'FACIE:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee 05000296 AUTHNAME, AUTHOR AFFILIATION ROGERS,A.T. Tennessee Valley Authority SINGER,K.W. Tennessee Valley Authority RECIP.NAME ~
RECIPIENT AFFILIATION
SUBJECT:
LER 99-001-00:on 990114,Unit 3 HPCI was noted inoperable.
Caused by oil leak on stop valve. Corrective maint was performed to repair oil leak. With 990212 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), ncident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3-PD 1 1 ~
DEAGAZIO, A 1 1 INTERNAL: ACRS 1 1 AEOD/SPD/RAB 2 2 AEOD/SPD/RRAB 1 1 1 1 NRR/DRCH/HOHB 1 1 /HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L 'ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOMIC POORE,W. 1, 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 U
N WASTETH NOTE TO ALL '"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19
Tennessee Valley Authority, Post Office Box 2000, Decatur, Alabama 35609.2000 Karl W. Singer Vice President, Browns Feny Nuclear Plant February 12, 1999 U.S. Nuclear Regulatory Commission 10 CFR 50.73 ATTN,: Document Control Desk Washington, D. C. 20555
Dear Sir:
BROWNS FERRY NUCLEAR PLANT (BFN) UNIT 3 DOCKET NO. 50-296 FACILITY OPERATING LICENSE DPR-68 LICENSEE EVENT REPORT (LER) 50-296/1999001 The enclosed'eport provides details concerning Unit 3 High Pressure Coolant Injection System becoming inoperable during surveillance testing.
This report is submitted in accordance with 10 CFR 50.73 (a)(2)(v)(D) as a condition that alone could have prevented the fulfillment of the safety function of a structure or system needed to mitigate the consequences of an accident.
Sincerely, Karl W. Singer cc: See page 2 9902250072 9902i2 PDR ADOCK 0500029b 8 PDR
41 U.S. Nuclear Regulatory Commission Page 2 February 12, 1999 Enclosure cc (Enclosure):
Mr. Paul Fredrickson, Branch Chief U.S. Nuclear Regulatory Commission Region II Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303-3415 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611 Mr. L. Raghavan, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739
li NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150.0104 EKPIRES (6-1998) 0 e/30/20 0 1 Estimated burden per response to comply with this mandatory information collection request: 50 hrs. Reported lessons learned are incorporated into LICENSEE EVENT REPORT (LER) the licensing process and fed back to Industry. Forward comments regs/ding burden estunate to the Records Management Branch (TW F33), U.S.
Nudear Regulatory Commission, Washington, DC 20555400)."and to the (See reverse for required number of Papetwo/k Reduction Project (31500104), Office of Management and digits/characters for each block) Budget, Washington, OC 20503. If an information collection does not display a current)y valid OMB control number, the NRC may not conduct or sponsor. and a person is not requi/ed to respond to. the information coEection.
FACIUTY NAME l1) DOCKET NUMBER I2) PAOE l3)
Browns ferry Nuclear Plant Unit 3 05000296 1 of 5 TITLE t4)
Unit 3 High Pressure Coolant Injection Inoperable As A Result Of An Oil Leak On The Stop Valve EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEQUENTIAL REVISION ACIU N DOCKET NUMBER NUMBER NUMBER DOCKET NUMBER 01 14 99 1999 001 00 02 12 99 NA OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)
MODE (9) 20.2201(b) 20.2203(a)(2)(v) 50.73(a) (2) (I) (B) 50.73(a) (2) (viii)
POWER 20.2203(a)(1) 20.2203(a)(3) (i) 50.73(a)(2)(ii) 50.73(a)(2)(x)
LEVEL (10), 100 20.2203(a) (2)(i) 20.2203(a)(3) (ii) 50.73(a) (2) (iii) 73.71 20.2203(a) (2)(ii) 20.2203(a) (4) 50.73(a)(2)(iv) OTHER
- 20. 2203(a) (2) (iii) 50.36(c)(1) 50.73(a)(2)(v) Specify in Abstract below or in NRC Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER gnclude Area Code)
Anthony T. Rogers, Senior Licensing Project Manager (256) 729-2977 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER REPOATABLE TO CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE NPRDS TO NPIIDS B ~ BJ SHV S075 NA SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH OAY YEAR YEs NO SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On January 14, 1999, at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br /> CST, during routine surveillance testing, the Unit 3 High Pressure Coolant Injection (HPCI) [BJ] system was declared inoperable as a result of an oil leak on the HPCI turbine inlet stop valve. As required by Technical Specifications, Browns Ferry entered a fourteen day Limiting Condition for Operation for an inoperable HPCI system. Following corrective maintenance and subsequent surveillance testing, the HPCI system was returned to an operable status at 1907 hours0.0221 days <br />0.53 hours <br />0.00315 weeks <br />7.256135e-4 months <br /> on January 15, 1999.
The oil leak was attributed to an overload failure of one of the four stud bolts which attach the pilot relay valve to the stop valve (Model J53) cylinder supplied by Schutte and Koerting. The failed stud bolt was subsequently determined to be fabricated from improper material in the original installation. Corrective actions included replacing the stud bolts on the Unit 3 HPCI system stop valve with ASTM A193 Grade B7 which has a higher strength and ductility than the original bolts. TVA plans to replace the stud bolts on the Unit 2 HPCI system stop valve as soon as practicable.
This condition is reportabie in accordance with 10 CFR 50.73(a)(2)(v)(D) as a condition that alone could have prevented the fulfillment of the safety function of a structure or system needed to mitigate the consequences of an accident.
NRC FORM 366B (6-1998)
0 NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 2 of 5 Browns Ferry Nuclear Plant - Unit 3 05000296 1999 001 pp TEXT (llmore space is required, use additional copies of AIRC Form 366A j i17)
I.'LANTCONDITION(S)
At the time of the discovery of this condition, Unit 2 and Unit 3 were operating at 100 percent power, and Unit 1 was shutdown and defueled.
II. DESCRIPTION OF EVENT A. Event:
On January 14, 1999, at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br /> CST, during routine surveillance testing, the Unit 3 High Pressure Coolant Injection (HPCI) [BJ] system was declared inoperable as a result of an oil leak on the HPCI turbine inlet stop valve supplied by Schutte and Koerting. As required by Technical Specifications, Browns Ferry entered a fourteen day Limiting Condition for Operation (LCO) for an inoperable HPCI system. Following corrective maintenance and subsequent surveillance testing, the HPCI system was returned to an operable status at 1907 hours0.0221 days <br />0.53 hours <br />0.00315 weeks <br />7.256135e-4 months <br /> on January 15, 1999.
This condition is reportable in accordance with 10 CFR 50.73(a)(2)(v)(D) as a condition that alone could have prevented the fulfillment of the safety function of a structure or system needed to mitigate the consequences of an accident.
B. Ino erable Structures Com onents orS stems that Contributedtothe Event:
None.
C. Dates and A roximate Times of Ma or Occurrences:
Ja'nuary 14, 1999, 1357 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.163385e-4 months <br /> CST Unit 3 HPCI system declared inoperable to perform surveillance test (prior to oil leak).
1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br /> CST An oil leak on a fitting between the HPCI pilot relay valve and stop valve cylinder was observed.
Consequently, an LCO was entered retroactive to the start of the surveillance test.
1926 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.32843e-4 months <br /> CST Made four hour non-emergency notification to the NRC.
January 15, 1999, 1907 hours0.0221 days <br />0.53 hours <br />0.00315 weeks <br />7.256135e-4 months <br /> CST. Following corrective maintenance and testing, Unit 3 HPCI system declared operable and LCO exited.
D. Other S stems or Seconda Functions Affected None.
E. Method of Discove Personnel in the immediate area observed the oil leak during the performance of routine surveillance testin .
NRc FORM 366 l6-1998)
ji NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I6-1998I LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REViSiON NUMBER 3 of 5 Browns Ferry Nuclear Plant - Unit 3 05000296 1999 001 pp TEXT (If more speceis required, use edditionel copies of hfRC Form 366AJ i17i F. 0 erator Actions Operators secured the HPCI system and stopped the auxiliary oil pump once the HPCI pump shaft had coasted,to a stop.
G. Safet S stem Res onses None.
III. CAUSE OF THE EVENT A. Immediate Cause The immediate cause of this event was an oil leak resulting from the failure of a stud bolt securing the pilot valve to the stop valve cylinder.
B. Root Cause The root cause of this event was attributed to the stud bolt being fabricated from improper bolting material.
IV. ANALYSIS OF THE EVENT The HPCI system was being tested during the quarterly performance of Surveillance Procedure, 3-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated Reactor Pressure.
When the HPCI system was initially started, an oil leak developed at a fitting between the pilot relay valve and the stop valve. The stop valve is located in the steam supply line close to the HPCI turbine. The primary function of the stop valve is to close quickly and stop the flow of steam to the HPCI turbine when a trip signal is received. The stop valve is hydraulically operated using a nominal 36 to 38 psig oil system to actuate the pilot relay valve and a 100 psig oil system to actuate'the twelve inch hydraulic cylinder to open the stop valve. As a result, the HPCI system may not have been able to perform its safety function if required.
The pilot relay valve is attached to the stop valve using four 5/8 inch diameter stud bolts. Investigation found that one of the four stud bolts had fractured. The failed stud bolt and three remaining intact stud bolts were sent to TVA Central Laboratories for metallurgical evaluation. Visual examination. using a stereo microscope revealed a relatively flat fracture surface with the failure initiating in the threaded area of the stud bolt. Scanning electron microscopy (SEM) analysis of the fracture surface of the fractured stud bolt revealed a transgranular brittle fracture with the fracture consisting almost entirely of cleavage. There were also a few ductile pockets observed on the fracture surface, but these ductility pockets accounted for less than five percent of the fracture surface. A low magnification SEM macrograph also showed that the fracture initiated in the root of a thread and progressed rapidly across the surface of the stud bolt. The microstructure in the longitudinal direction of the failed stud bolt consisted of ferrite and pearlite with manganese sulfide stringers present throughout the structure. The results of the chemical analyses performed on the stud bolts showed that the failed stud bolt and one of the intact stud bolts were not NRC FORM 366 I6-1998)
0 I>
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I6-1998I LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 4 of 5 Browns Ferry Nuclear Plant - Unit 3 05000296 1999 001 pp TEXT (If more space is required, use additional copies of NRC Form 366AJ i17)
IV. ANALYSIS OF THE EVENT (continued) consistent with the vendor's specified bolting material requirements. These two stud bolts met the chemical requirements of ASTM A108 Grade 1215 material. This material is a free machining grade steel which has been resulfurized and rephosphorized. Additional sulfur is added to improve machinability of a free machining grade steel. The addition of phosphorus in this type of steel increases strength of the steel but decreases the ductility of ferrite. Steels which are high in phosphorus are notoriously notch sensitive. As a result, these two stud bolts were more susceptible to this type of failure than the material specified by the vendor.'he other two stud bolts (ASTM A108 Grade 1022), while not fully consistent with the requirements specified by the vendor (ASTM A108 Grade 1020), would exhibit similar characteristics as those specified by the vendor.'VA reviewed the maintenance history involving the HPCI system and found no documentation which indicates that the stud bolts were ever replaced. Therefore, these stud bolts were most likely a part of the originally supplied equipment. AII four hex nuts that were used on the stud bolts were tested and found to be consistent with the vendor supplied information. The valve supplier, Schutte and Koerting, has been notified of these findings.
Field observations identified marks and chipped paint on all four hex nuts which could have been caused by tightening the hex nuts to reduce oil seepage. This additional torquing coupled with a small flaw could have exacerbated this failure. However, this possible additional torque should not have resulted in bolt failure during system operation if the stud bolts had been fabricated from suitable material.
V. ASSESSMENT OF SAFETY CONSEQUENCES The HPCI system is provided to assure that the reactor is adequately cooled to limit fuel cladding temperature in the event of a small pipe break in the nuclear system and loss of coolant which, does not result in rapid depressurization of the reactor vessel. The HPCI system permits the nuclear plant to be shut down, while maintaining sufficient reactor vessel water inventory until the reactor vessel is depressurized.
The HPCI system continues to operate. until the reactor vessel pressure is below the pressure at which Low Pressure Coolant Injection (LPCI) [BO] operation or Core Spray (CS) [SM] System operation maintains core cooling. In the event HPCI is not.available'or not sufficient to maintain reactor water level, the Automatic Depressurization System (ADS) [SB] functions to reduce reactor pressure so that flow from the LPCI and the CS systems enter the reactor vessel in time to cool the core and limit fuel cladding temperature.
BFN TS allow continued reactor operation for up to fourteen days, if HPCI is inoperable, provided ADS, CS, LPCI, and Reactor Core Isolation Cooling (RCIC)[BN]systems are operable. RCIC provides an alternate supply of high pressure makeup while ADS would depressurize the reactor to allow CS and RHR to provide adequate low pressure ECCS makeup to the reactor. The availability of these redundant and diversified systems provides adequate assurance of core cooling while the HPCI system is inoperable.
During the period that the HPCI system was inoperable, these required systems were operable and would have performed their designed function, if called upon. Additionally, had the HPCI system been required to mitigate the consequences of an accident prior to this event, the HPCI system would have initiated and operated for a limited period prior to the loss of oil pressure resulting from the leak.
Accordingly, there was no major reduction in the degree of protection provided to public health and safety.
Furthermore, the safety of the plant, its personnel, and the public was not compromised.
NRC FORM 366 t6-1999)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 5 of 5 Browns Ferry Nuclear Plant - Unit 3 05000296 1999 001
,pp TEXT (If more space is required, use additional copies of NRC Form 366A) I17)
VI. CORRECTIVE ACTIONS A. Immediate Corrective Actions Corrective maintenance was performed to repair the oil leak.
B. Corrective Actions to Prevent Recurrence The failed stud bolts were replaced with a higher strength and more ductile bolting material than the current specified bolting material. The vendor has provided documentation stating that this change in material for the subject stud bolts is acceptable.
Stud bolts in this application on the Unit 2 HPCI system stop valve will be replaced as soon as practicable.'II.
ADDITIONALINFORMATION A. Failed Com onents The failed component was a 5/8 inch diameter stud bolt manufactured from ASTM A108 Grade 1215 material. These stud bolts attach the pilot relay valve to the HPCI system hydraulically operated stop valve (Model J53) which was supplied by Schutte and Koerting.
B. Previous LERs on Similar Events There have been no previous LERs involving the inoperability of HPCI due to a stud bolt failure.
C. Additional Information None.
Vill. COMMITMENTS None.
'VAdoes not consider this corrective action a regulatory commitment. The completion of this item will be tracked in TVA's Corrective Action Program.
NRC FORM 366 I6-1998)