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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212G2241999-09-27027 September 1999 Safety Evaluation Supporting Amend 221 to License DPR-68 ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr 05000259/LER-1999-001-01, :on 990115,inoperable CR Emergency Ventilation Sys During Post Maint Testing Was Noted.Caused by Failure of Procedure Writers & Reviewers.Returned a Crev to Operable State & Revised B Crev Train Procedures.With1999-02-12012 February 1999
- on 990115,inoperable CR Emergency Ventilation Sys During Post Maint Testing Was Noted.Caused by Failure of Procedure Writers & Reviewers.Returned a Crev to Operable State & Revised B Crev Train Procedures.With
ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept 1999-09-30
[Table view] |
Text
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RZDS)
ACCESSZOH NBR:9907190071 DOC.DATE: 99/07/12 NOTARIZED: NO DOCKET FACIL:50-260 Browns Ferry Nuclear Power Station, Unit 2, Tennessee 05000260 AUTH. NAME AUTHOR AFFILIATION MOODY,G.F. Tennessee Valley Authority HERRON,J.T. "
Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 99-005-00:on 990617,ESF actuation c HPCI declared inoperable. Caused by personnel error.HPCZ reset &. sys returned to operable status with 25 minutes.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL LPD2-2 PD 1 1 LONG,W 1 1 INTERNAL: ACRS 1 1 E ENTE 1 1 NRR/DIPM/IOLB 1 1 NRR/DRIP/REXB 1' ERR/DSSA/SPLB 1 1 RES/DET/ERAB 1 1 RES/DRAA/OERAB 1 ~ 1 RGN2 ,FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LMZTCO MARSHALL 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS NRC PDR 1 1 NUDOCS FULL TXT '1 1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LIS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTE DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 16 ENCL 16
II ~I Tennessee Valfey Authority. Post Office Box 2000, Decatur, Atabarna 36609 July 12, 1999
'U.S. Nuclear Regulatory Commission 10 .CFR 50. 73 ATTN: Document Control Desk Washington, D.. C. 20555
Dear Sir:
TENNESSEE VALLEY AUTHORITY BROWNS, FERRY NUCLEAR PLANT (BFN)
UNIT 2' DOCKET 50-260 FACILITY OPERATING LICENSE DPR 52 LICENSEE EVENT REPORT. (LER) 50-260/1999-005-000
. The enclosed report provides detai;ls concerning an Engineered Safety Feature Actuation and the Unit 2 High Pressure Coolant Injection syst;em being declared inoperable due to personnel error during surveillance testing.
TVA i: s reporting this event pursuant to 10CFR50.73(a)(2)(iv) as an event or condit;ion,that resulted in an automatic actuation of an Engineered Safety Feature and 10CFR50.73(a),(2,)-(v) as a condition that alone could have prevented the fulfillment of the safety. function of a structure or system needed to mitigate, the consequences of an acci'dent.
Sincerely, J hn T. Herron In crim Site Vice President See page 2 9907i9007i 990712 PDR ADOCK OS000260 8 PDR
0
'I
U.S. Nuclear Regulatory Commission Page 2 July 12, 1999 Enclosure cc (Enclosure):
Mr. William O. Long, Senior Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852 Mr. Paul E. Fredrickson, Branch Chief U.S. Nuclear Regulatory Commission Region II Atlanta Federal Center 61 Forsyth Street, SW, Suite .23T85 Atlanta, Georgia 30303-3415 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611
I!
I
NRC FORIVI 366
'0 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXFIRES oersonoot
{6-1998) Estimated burden per response to comp)y with this mandatory information collection request: 50 hrs. Reported lessons learned are Incorporated into the licensing process and,fed back to industry. Forward comments regarding LICENSEE EVENT'REPORT (LER) burden estimate to the Records Marogernent Branch (TA F33), U.S. Nuclear Regulatory Commission, Washington. DC 20555400( and to the Paperwork
~
(See reverse for required number of Reduction Project (31500)04), Office of Management and Budget.
Washington, DC 20503. If an information collection does not display a digits/characters for each block) currently valid OMB control number, the NRC may not conduct or sponsor.
and a person is not required to respond to. the Informatkxl cot(ection.
FACIUTY NAME (I) DOCKET NUMBER (2) PAOE IS)
Browns Ferry Nuclear Plant Unit.2 05000260 1of7 TITLE (4)
Engineered Safety Feature (ESF) Actuation and High Pressure Coolant Injection (HPCI) Inoperable Due To Personnel Error.
During Surveillance Testing "EVENT DATE {5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR SEQUENTIAL 'EVISION MONTH DAY FACIUTY NAME DOCKET NUMBER NUMBER NUMBER NA DOCKET NUMBER 06 17 1999 1999 005 000 07 '12 1999 NA OPERATING THIS REPORT IS SUBMITTED PURSUA NT To-THE REQUIREMENTS OF 10 CFR II: (Check ono or more)
MODE (9) 20.2201 {b) 20.2203(a)(2)(v) 50.73(a) (2) (i) 50.73(a) (2)(viii
)
POWER 20.2203(a)(1) 20.2203(a)(3) (i) 50.73(a)(2)(iil 50.73(a)(2){x)
LEVEL (10) ,1 00 20.2203(a) (2)(i) 20.2203(a)(3)(ii) 50.73(a) (2) (iii) '3.71 20.2203(a)(2){ii) 20.2203(a) (4) X 50.73(a)(2)(iv) OTHER 20.2203(a) (2) (iii) 50.36(c) (1) X 50.73(a)(2)(v) Specify in Abstract below or ln NRC Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a) (2) (vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Area Code)
- Gerald F. Moody; Licensing Project Manager 256-729-7534 COMPLETE ONE LINE FOR EACH. COMPONENT FAILURE DESCRIBED IN THIS REPORT {13)
CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED {14) EXPECTED MONTH, OAY YES X NO SUBNIISSION (If yes, complete EXPECTED SUBMISSION DATE) DATE (15) YEAR'BSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) {16)
On June 17, 1999, at approximately 1337 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.087285e-4 months <br /> Central daylight Time.(CDT) during the performance of a regularly scheduled surveillance on a Unit 2 Core and Containment Cooling System Analog Trip Unit (ATU), an unexpected isolation of the HPCI System occurred. The HPCI system was immediately declared inoperable. Upon investigation, it was determined that the isolation was due to personnel error. Specifically, contact inhibits (boots) were incorrectly placed on a relay during the, surveillance. Section 7.15 of this procedure was being performed which is used to demonstrate operability of the HPCI isolation function on high steam line flow. The inhibits were removed, the HPCI isolation was reset and the system was returned to operable status. During this event, HPCI was inoperable less than 1/2 hour of the 14 days allowed by the Technical Specification LCO. Also, during the period the HPCI system was inoperable, all other required alternate safety systems were operable and would have performed their design function if called upon. Accordingly, there was no significant reduction in the degree of protection provided to public health and safety. Furthermore, the safety of the plant, its personnel, and the public was not compromised.
r This report is submitted pursuant to 10 CFR 50.73 (a) (2) (iv) as an event or condition that resulted in an automatic actuation of an engineered safety feature (ESF) and 10CFR50.73(a)(2)(v) as a condition that alone could have prevented the fulfillment of the safety function of a structure or system needed to mitigate the consequences of an accident.
NRC FORM 366B {6-199BI
0 0 NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION IS-ISSSI LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 2 of 7 Browns Ferry Nuclear Plant - Unit 2 05000260 1999 005 000 TEXT (lf more space is required, use additional copies of'NRC Form 366Ai I17l I. PLANT CONDITION(S)
At the time of the event, Unit 2 was in mode 1 at 100 percent pow'er, approximately 3456 megawatts
'thermal. Unit 3 was in mode 1 at 100 percent power, approximately 3456 megawatts thermal. Unit 1 was shutdown and defueled.
II. DESCRIPTION OF EVENT A. Event:
On June 17, 1999, at approximately 1217 hours0.0141 days <br />0.338 hours <br />0.00201 weeks <br />4.630685e-4 months <br /> Central Daylight Time (CDT) surveillance test Core and Containment Cooling Systems Analog Trip Unit (2-SR-3.3.5.1.2 (ATU C)) was started.
Section 7.15 of this procedure was being performed which is used to demonstrate operability of the HPCl.isolation function on high steam line flow. At approximately 1337 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.087285e-4 months <br /> CDT, the Unit 2 control room operators observed the High Pressure Coolant Injection (HPCI) [BJj system inboard and outboard containment isolation valves closing which was contrary to the SR requirement. The surveillance was stopped and HPCI was declared inoperable. As required by Technical Specifications, Browns Ferry Unit 2 entered a fourteen day Limiting Condition for Operation (LCO) for an inoperable HPCI.system.
At 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br /> it was determined that the HPCI isolation had been caused by the craftsmen (utility, non-licensed) performing this surveillance inhibiting the wrong contacts on a relay. At 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br />, Operations personnel directed the craftsmen to remove the trip signal in order to de-energize
'the relay so that the HPCI isolation could be reset. This was done and the contact inhibits were removed. The HPCI isolation was reset, the surveillance was satisfactorily completed without further incident, and the system was returned to an operable status at approximately 1402 hours0.0162 days <br />0.389 hours <br />0.00232 weeks <br />5.33461e-4 months <br /> CDT.
.This report is being submitted pursuant to.10CFR 50.73 (a) (2) (iv) as an event or condition that resulted in an automatic actuation of an engineered safety feature (ESF) and 10CFR50.73(a)(2)(v) as a condition that alone could have prevented the fulfillment of the safety function of a structure or system needed to mitigate the consequences of an accident.
B. Ino erable Structures Com onents or S stems that Contributed to the Event:
None.
C. Dates and A roximate Times of Ma or Occurrences:
June 17, 1999, 1217 hours0.0141 days <br />0.338 hours <br />0.00201 weeks <br />4.630685e-4 months <br /> CDT Surveillance 2-SR-3.3.5.1.2 (ATU C) Core and Containment Cooling Systems Analog Trip Unit Functional Test Started.
June 17, 1999, 1337 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.087285e-4 months <br /> CDT HPCI isolation occurred due to improper contacts being booted and HPCI was declared inoperable.
NRC FORM 366B I6-1998)
ll 4l NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I6-1998)
LICENSEE EVENT REPORT (LER).
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE I3 YEAR SEQUENTIAL REVISION NUMBER 3of7 Browns Ferry Nuclear Rant - Unit 2 05000260 1999 005 - 000 TEXT illmore space is required, use additional copies of hfRC Form 366Ai I17I June 17, 1999, 1402 hours0.0162 days <br />0.389 hours <br />0.00232 weeks <br />5.33461e-4 months <br /> CDT The isolation was reset and HPCI was returned to an operable status.
June 17, 1999, 1627 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.190735e-4 months <br /> CDT A 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> Non-Emergency notification was made to the NRC in accordance with 10 CFR 50.72 (b) (2) (ii) and 10 CFR 50.72 (b) (2) (iii).
D. Other S stems or Seconda Functions Affected None.
E. Method. of Discove During the performance of the surveillance,'Unit 2 Control Room Operators noticed the HPCI inboard and outboard isolation.valves closing.
F. 0 erator Actions No operator actions contributed to this event.
G. Safet S stem Res onses Safety system response was as. expected under the circumstances described in this report.
III. CAUSE OF THE EVENT A. Immediate Cause The immediate cause of this event was personnel error (installing the inhibit boots on the wrong contacts).
B. Root Cause The craftsmen (utility, non-lichnsed) involved in performing this surveillance installed the relay contact inhibits on the incorrect contacts. This was due in partto their familiarity with the test which led,them to rely on, memory in order to determine the placement of the contact inhibits instead of illustrations provided in the surveillance procedure.
C. Contributin Factors It was determined that the surveillance procedure could have'been more clearly written due to the fact that it allowed craftsmen to reference the illustration "as necessary" to determine proper placement of the contact inhibits. In addition, the numbering scheme used in the illustration may have contributed to the confusion.
NRC FORM'366 I6-1996)
II NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6. I 998)
LICENSEE:EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME'(1 DOCKET LER NUMBER 6 PAGE (3 YEAR SEQUENTIAL REVISION NUMBER 4o(7 Browne Ferry NUclear Plant - Unit 05000260 2'EXT 1999 005 000 (If moro space is required, use additional copies of PiRC Form 366A J (17)
IV. ANALYSIS OF THE EVENT
. Instrument Maintenance Craftsmen (utility, non-licensed) performing this surveillance relied on memory instead'of available resources to identify the relay contacts to be inhibited. On this type of relay (General Electric Company type HFA) [RLY] (see Figure on page 7) the contact positions are numbered from left to right when facing the relay from the front of the panel. where the craftsmen were working. The craftsmen performing the test inappropriately. counted the positions from right to left and installed the inhibits on the two left most set of contacts instead of the two right most set of contacts. The surveillance procedure contained an HFA relay illustration showing the relay layout. The appropriate relay contacts to be inhibited were illustrated. The craftsmen performing the surveillance did not refer to the illustration to ensure the correct contacts were inhibited. Because the craftsmen were familiar with the test, they relied on memory to determine which contacts to inhibit rather than use the illustration. This surveillance is a quarterly test that has been performed numerous times without incident. The fact that the surveillance steps included the HFA relay contact position numbers in addition to the actual contact numbers (which are numbered in the reverse sequence from the "position" numbers-see attached figure labeled HFA relay for clarification) and that the action steps directed the personnel performing the test to refer to the illustration "as necessary" was found to be a contributing factor.
V. ASSESSMENT OF THE SAFETY CONSEQUENCES The HPCI system is provided to assure that the reactor is adequately cooled to limit fuel cladding temperature in the event of a small pipe break in the nuclear system and loss of coolant which does not result in rapid depressurization of the reactor vessel. The HPCI system permits the nuclear plant to be shut down, while maintaining sufficient reactor vessel water inventory until the reactor vessel is depressurized. The HPCI system continues to operate until the reactor vessel is below the pressure at which Low Pressure Coolant Injection (LPCI) [BO] operation or Core Spiay (CS) [SM] operation maintains core cooling.'In the event HPCl,is not available or not sufficient to maintain reactor water level, the Automatic Depressurization System (ADS) [SB] functions to reduce reactor pressure so that flow from the LPCI and CS enters the reactor vessel in time to cool the core and limit fuel cladding temperature.
BFN Technical Specifications allow continued reactor operation for up to 14 days if HPCI is inoperable, provided ADS, CS, LPCI, and Reactor Core Isolation Cooling (RCIC) [BN] systems are operable. RCIC provides an alternate supply of high pressure makeup while ADS would depressurize the reactor to allow CS and LPCI to provide adequate low pressure ECCS makeup'o the reactor. The availability of these redundant and diversified systems provides adequate assurance of core cooling while the HPCI system is inoperable. For this event, HPCI was inoperable. less than 1I2 hour of the 14 days allowed by the LCO. During the period the HPCI system was inoperable, these required systems were operable and it is expected they would have performed their design function if called upon.
Accordingly, there was no significant reduction in the degree of protection provided tq public health and safety. Furthermore, the safety of the plant, its personnel, and the public was not compromised.
NRC FORM '366 (6-1998)
t 4l
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 5 or 7 Browne Ferry Nuclear Plant - Unit 2 05000260 1999 - 005 000 TEXT fffmore space is required, use additional copies of NRC Form 366A/ I 17)
VI. CORRECTIVE ACTIONS A. Immediate Corrective Actions The HPCI isolation was detected immediately and the cause of the isolation was determined within 3 minutes of the isolation. Actions were immediately initiated to return the system to standby readiness. The HPCI isolation was reset and the system was returned to operable status within 25 minutes.
B. Corrective Actions to Prevent Recurrence Information concerning this incident was communicated to plant personnel through stand down briefings.
I Craftsmen involved in the performance of this surveillance will receive personnel corrective action in accordance with TVA policy.
instructions are being reviewed to enhance guidance (where warranted) for
'urveillance individuals performing these tests.
'II
~ ADDITIONALINFORMATION A. Failed Com onents:
None.
B. Previous LERs on Similar Even'ts:
review of previous events for the past two years revealed one LER that was the result of an unplanned Engineered Safety Feature Actuation due to improperly'placed jumpers or contact inhibits.
LER 260/1997-005-000 was written to document an unexpected Engineered Safety Feature Actuation caused by personnel closing the wrong relay during a surveillance test. This action was inadvertent and the corrective actions for this event did not address a failure to follow work instructions. Accordingly, the corrective actions taken would not have precluded this event.
'VAdoes not consider these corrective actions regulatory commitments. The completion of these items will be tracked in TVA's Corrective Action Program.
NRC FORM 366 I6-1996)
II II NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6. I 998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 6 ol7 Browns Feiry NUclear Plant - Unit 2 05000260 1999 005 - 000 TEXT (lf more space is required, use additional copies of NRC Form 366A J I17)
C. Additional.Information:
None.
D. Safet S stem Functional Failure:
This event does not meet the criteria for a safety system functional failure as described in NEI 99-02 because it was immediately recognized that the HPCI system was inoperable.
The condition was not caused by an equipment failure and the isolation was reset within 25 minutes.
Vill. COMMITMENTS None.
NRC FORM 366 I6-199BI
0
NRC FORIVI 366A U.S.
I6.1998) NUCLEAR'REGULATORY'COMMISSION'ACILITY LICENSEE EVENT REPORT (LER).
TEXT CONTINUATION NAME 1 DOCKET LER NUIVIBER 6 PAGE 3)
YEAR SEQUENTIAl REVISION,
'NUMBER .7of7 Browns Ferry Nuclear Plant - Unit,2 05000260 1999 005 - 000 TEXT'fifmore space is required, use addi rionai copies of hfRC Form 366AJ f17)
.FIGURE HFA RELAY Contacts 3-4 Contacts 1-2 (Contact position 5) (Contact position 6) 0 '"'i::
F:
NRC FORM 366 f6-1998)
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