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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20153H3141998-09-28028 September 1998 SE Accepting Util Proposed Alternatives as Contained in Relief Requests 3-SPT-3 & 3-SPT-4 for Second Interval & Code Case N-546 ML20247M1901998-05-20020 May 1998 Safety Evaluation Related to Browns Ferry,Unit 3 Nuclear Power Plant Individual Plant Exam ML20217E5431997-09-22022 September 1997 Safety Evaluation Re Flaw Evaluation of Core Spray Internal Piping for Plant,Unit 3 ML20217C2191997-09-11011 September 1997 Safety Evaluation Supporting Amend 249 to License DPR-52 ML20149L2301997-07-28028 July 1997 Safety Evaluation Accepting License Relief Request from Certain ASME Code Requirements Delineated in Change to 10CFR50.55a for Plant,Units 1,2 & 3 ML20148U3291997-07-0808 July 1997 Safety Evaluation Denying Relief Request 3-ISI-1.Based on Review,Nrc Concludes That Licensee Does Not Have Sufficient Basis for Relief from Code Required Successive Exam ML20136D7831997-03-10010 March 1997 Safety Evaluation Authorizing Use of ASME Code Case N-416-1 ML20132B2701996-12-11011 December 1996 Safety Evaluation Accepting Licensee Emi/Rfi site-survey Consistent W/Industry Stds & Practice ML20058K2411993-12-0707 December 1993 Supplemental Safety Evaluation Supporting Structural Steel Thermal Growth Design Critera at Plant ML20058J1091993-12-0303 December 1993 Safety Evaluation Accepting Licensee 921228 Submittal of Suppl Response to GL 88-01, NRC Position on Intergranular Stress Corrosion Cracking (IGSCC) in BWR Austenitic Stainless Steel Piping ML20059C2451993-10-22022 October 1993 Safety Evaluation Accepting IST Program Requests for Relief ML20246M3891989-05-0909 May 1989 Safety Evaluation Supporting Util 890317 Proposed long-term Solution to Correct Rust Problems in Containment Spray Headers ML20245H3371989-05-0101 May 1989 Safety Evaluation Re Generic Ltr 83-28,Item 2.1 (Part 2) About Vendor Interface Program ML20245D5711989-04-19019 April 1989 Safety Evaluation Re Rust in Lower Containment Spray Header Due to Leaking Isolation Valves ML20247K5561988-09-23023 September 1988 Safety Evaluation Supporting Amends 155,151 & 126 to Licenses DPR-33,DPR-52 & DPR-68,respectively ML20154H2721988-04-19019 April 1988 Safety Evaluation Describing Relationship of Util Nuclear Performance Plan,Vol 3,Part Ii,Section 2.6, QA to TVA-TR75-1A, QA Program Description for Design,Const... W/Proper Implementation,Qa Program Description Acceptable ML20148K9051988-03-23023 March 1988 Safety Evaluation Supporting Util Responses to Generic Ltr 83-28,Items 3.1.1,3.1.2,3.2.1 & 3.2.2, Post-Maint Testing of Reactor Trip Sys & All Other Safety-Related Components ML20246M2341988-02-29029 February 1988 Safety Evaluation Supporting Amends 145,141 & 116 to Licenses DPR-33,DPR-52 & DPR-68,respectively ML20214H9091987-05-13013 May 1987 Safety Evaluation Supporting Amends 133,129 & 104 to Licenses DPR-33,DPR-52 & DPR-68,respectively ML20206L9821986-06-20020 June 1986 Safety Evaluation Supporting Requests for Establishment of Common Date to Implement Inservice Insp Program Requirements.Start Date of 880301 Accepted for Second 10-yr Insp Interval ML20127D6641985-06-17017 June 1985 Safety Evaluation Re Licensee Response to Item 1.1 of Generic Ltr 83-28 on post-trip Review Program & Procedures. Post-trip Review Program & Procedures Acceptable ML18029A5381985-05-0606 May 1985 Safety Evaluation Re Mark I Containment long-term Program Pool Dynamic Loads Review for Plant.Pool Dynamic Loads Meet Acceptance Criteria of NUREG-0661 or Alternative Criteria Acceptable ML18029A5401985-05-0606 May 1985 Safety Evaluation Re Mark I Containment long-term Program Structural Review for Plant.Mods Follow NUREG-0661 Guidelines & Acceptable.Analyses Verified & Approved ML20148T7811980-12-0101 December 1980 Generic Safety Evaluation Re BWR Scram Discharge Sys ML20062A4221978-09-29029 September 1978 Safety Evaluation Rept Supporting Amend 43 to Lic DPR-33 Covering Pump Seizure Accident,Inadvertent Cold Loop Startup Transient & Monitoring of Safety Margins for 1 Loop Oper ML20247C1721976-02-23023 February 1976 Safety Evaluation Supporting Operation of Plant After Restoration & Mods of Facilities Following 750322 Fire 1999-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION LICENSEE RESPONSE TO GENERIC LETTER 95-07. " PRESSURE LOCKING AND THERMAL BINDING OF SAFETY-RELATED POWER-OPERATED GATE VALVES" BROWNS FERRY NUCLEAR PLANT. UNITS 2 AND 3 DOCKET NUMBERS 50-260 AND 50-296
1.0 INTRODUCTION
{
Pressure locking and thermal binding represent potential common-cause failure mechanisms that can render redundant safety systems incapable of performing their safety functions. The identification of susceptible valves and the determination of when the phenomena might occur require a thorough knowledge of components, systems, and plant operations. Pressure locking occurs in flexible-wedge and double-disk gate valves when fluid becomes pressurized inside the valve bonnet and the actuator is not capable of overcoming the additional thrust requirements resulting from the differential pressure created across both valve disks by the pressurized fluid in the valve bonnet. Tnermal binding is generally associated with a wedge gate valve that is closed while the system is hot and then is allowed to cool before an attempt is made to open the valve.
Pressure locking or thermal binding occurs as a result of the valve design characteristics (wedge and valve body configuration, flexibility, and material thermal coefficients) when the !
valve is subjected to specific pressures and temperatures during various modes of plant <
operation. Operating experience indicates that these situations were not always considerer in many plants as part of the design basis for valves.
2.0 REGULATORY REQUIREMENTS Title 10, Code of Federal Regulations (10 CFR) Part 50 (Appendix A, General Design Criteria 1 and 4) and plant licensing safety analyses require or commit (or both) that licensees design and test safety-related components and systems to provide adequate assurance that those systems can perform their safety functions. Other individual criteria in Appendix A to 10 CFR Part 50 apply to specific systems. In accordance with those regulations and licensing commitments, and under the additional provisions of 10 CFR Part 50 (Appendix B, Criterion XVI), licensees are expected to act to ensure that safety-related power-operated gate valves susceptible to pressure locking or thermal binding are capable of performing their required safety functions.
On August 17,1995, the U.S. Nuclear Regulatory Commission (NRC) issued Generic Letter (GL) 95-07, " Pressure Locking and Thermal Binding of Safety-Related Power-Operated Gate '
Valves," to request thr' licensees take certain actions to ensure that safety-related power-operated gate valves inat are susceptible to pressure locking or thermal binding are capable of performing their safety functions within the current licensing bases of the facility. GL 95-07 requested that each licensee, within 180 days of the date of issuance of the generic letter i 9906290334 990623 PDR ADOCK 05000259 P PDR 1
i, (1) evaluate the operational configurations of safety-related power-operated gate valves in its l plant to identify valves that are susceptible to pressure locking or thermal binding, and (2) '
perform further analyses and take needed corrective actior.s (orjustify longer schedules) to ensure that the susceptible valves, identified in (1.0) above, are capable of performing their !
intended safety funutions under all modes of plant operation, including test configuration. In )
addition, GL 95-07 requested that licensees, within 180 days of the date of issuance of the l generic letter, provide to the NRC a summary description of (1) the susceptibility evaluation ,
used to determine that valves are or are not susceptible to pressure locking or thermal binding, (2) the results of the susceptibility evaluation, including a listing of the susceptible valves identified, and (3) the corrective actions, or other dispositioning, for the valves identified as susceptible to pressure locking or thermal binding. The NRC issued GL 95-07 as a
" compliance backfit" pursuant to 10 CFR 50.109(a)(4)(i) because modification may be necessary to bring facilities into compliance with the rules of the Commission referenced
- above, in a letter of February 13,1996, Tennessee Valley Authority (TVA) submitted its 180-day response to GL 95-07 for Browns Ferry Nuclear Plant, Units 2 and 3. In a letter dated March 15,1996, the licensee supplemented its 180-day response to GL 95-07. The NRC staff reviewed the licensee's submittels and requested additional information in a letter dated June 17,1996. In a letter of July 30,1996, the licensee provided the additionalinformation. In a letter of February 19,1999, the licensee supplemented its 180-day response to GL 95-07.
3.0 STAFF EVALUATION 3.1 - Scope of Licensee's Review GL 95-07 requested that licensees evaluate the operational configurations of safety-related power-operated gate valves in their plants to identify valves that are susceptible to pressure locking or thermal binding - The TVA letters of February 13, March 15, and July 30,1996, and February 19,1999, described the scope of valves evaluated in response to GL 95-07. Reactor Core isolation Cooling (RCIC) Injection valves,2/3 FCV-71-39, are not included in the licensee's GL 95-07 Program. However, the licensee stated in a letter dated January 6,1997, that its RClC motor operated valves would be included within its GL 89-10, " Safety-Related Motor-Operated Valve Testing and Surveillance," Program in response to an NRC evaluation of its GL 89-10 scope. These valves were evaluated for pressure locking and thermal binding to ensure their capability to open for mitigation of certain licensing basis events. The NRC staff has reviewed the scope of the licensee's susceptibility evaluation performed in response to GL 95-07 and found it complete and acceptable.
3.2 Corrective Actions GL 95-07 requested that licensees, within 180 days, perform further analyses as appropriate, and take appropriate corrective actions (orjustify longer schedules), to ensure that the susceptible valves identified are capable of performing their intended safety function under all modes of plant operation, including test configuration. The licensee's submittals discussed proposed corrective actions to address potential pressure-locking and thermal-binding problems. The staff's evaluation of the licensee's actions is discussed in the following paragraphs:
l L.-.o
e
- a. The licensee stated that the following valves were modified to eliminate the potential for pressure locking:
2,3 FCV-74-53 Low Pressure Coolant injection 2,3 FCV-74-67 Low Pressure Coolant injection 2,3 FCV-75-25 Core Spray injection 2,3 FCV-75-53 Core Spray injection The staff finds that physical modification to valves susceptible to pressure locking is an appropriate corrective action to ensure operability of the valves and is thus acceptable.
l The licensee stated that the RCIC pump injection valves,2/3 FCV 71-39, were susceptible to pressure locking and that the valves would be modified to eliminate the potential for pressure locking during the Unit 2 refueling outage scheduled for Spring 2001 and the Unit 3 refueling
- outage scheduled for Fall 2000. In the interim, plant procedures require that the RCIC system be vented and the valves stroked on a monthly interval in order to verify that they will operate during pressure locking conditions. The staff finds that these interim corrective actions are ;
acceptable because they provide assurance that pressure locking conditions are promptly identified and corrected. The long-term corrective actions to modify the valves are acceptable l because the potential for pressure locking will be eliminated.
l
- c. The licensee stated that procedures were modified to cycle the high pressure coolant injection steam admission valves,2,3 FCV-73-16, following evolutions that could potentially create a j thermal binding condition. The staff finds that the licensee's i procedural changes to require cycling the valves as corrective actions provide assurance that thermal binding conditions are ,
eliminated, and are thus acceptable. I l
- d. The licensee stated that all flexible and solid wedge gate valves in the ;
scope of GL 95-07 were evaluated for thermal binding. When !
evaluating whether valves were susceptible to thermal binding, the l licensee assumed that thermal binding would not occur below specific temperature thresholds. The screening criteria used by the licensee appear to provide a reasonable approach to identify those valves that might be susceptible to thermal binding. Until more definitive industry criteria are developed, the staff concludes that the licensee's actions to address thermal binding of gate valves are acceptable.
4.0 CONCLUSION
On the basis of this evaluation, the NRC staff finds that the licensee has performed appropriate evaluations of the operational configurations of safety-related power-operated gate valves to identify valves at the Browns Ferry Nuclear Plant, Units 2 and 3, that are susceptible to pressure locking or thermal binding. In addition, the NRC staff finds that the licensee has taken, or is scheduled to take, appropriate corrective actions to ensure that these valves are capable of performing their intended safety functions. Therefore, the staff concludes that the licensee has adequately addressed the requested actions discussed in GL 95-07.
Principal Contributor: S. Tingen, NRR Date: June 23, 1999