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| I. BACKGROUND During the startup and initial operation of Turkey Point Units 3 and 4, a significant number of Fischer and Porter Company Electronic Differential Pressure Transmitters, Model 2495 and Model 2496, were found to have failed internally. After the startup of Turkey Point Unit No. 4 in June, 1973, the high level of maintenance required to keep these transmitters operational became of concern to staff and plant personnel of Florida Power and Light Company. A meeting was held on. August 1, 1973 with Fischer and Porter Company personnel to discuss the cause of the high failure rate and corrective action. | | I. BACKGROUND During the startup and initial operation of Turkey Point Units 3 and 4, a significant number of Fischer and Porter Company Electronic Differential Pressure Transmitters, Model 2495 and Model 2496, were found to have failed internally. After the startup of Turkey Point Unit No. 4 in June, 1973, the high level of maintenance required to keep these transmitters operational became of concern to staff and plant personnel of Florida Power and Light Company. A meeting was held on. August 1, 1973 with Fischer and Porter Company personnel to discuss the cause of the high failure rate and corrective action. |
| At this meeting it was agreed that Florida Power and Light Company would provide Fischer and Porter Company with five failed units which would be disassembled completely at the factory and evaluated to determine what had caused the failure. | | At this meeting it was agreed that Florida Power and Light Company would provide Fischer and Porter Company with five failed units which would be disassembled completely at the factory and evaluated to determine what had caused the failure. |
| In a letter dated October 1, 1973, Florida Power and Light Company was advised by Fischer and Porter Company that all five of the failed | | In a {{letter dated|date=October 1, 1973|text=letter dated October 1, 1973}}, Florida Power and Light Company was advised by Fischer and Porter Company that all five of the failed |
| * transmitters had lost their fill fluid and failed. The through-bolts on the process flanges for these five transmitters were not torqued to the manufacturer's recommended torque value. The postulated failure mechanism is an elongation of the through-bolts due to inadequate bolt torque, with a subsequent loss of fill fluid under process pressures.- | | * transmitters had lost their fill fluid and failed. The through-bolts on the process flanges for these five transmitters were not torqued to the manufacturer's recommended torque value. The postulated failure mechanism is an elongation of the through-bolts due to inadequate bolt torque, with a subsequent loss of fill fluid under process pressures.- |
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| : 2. Three of ten 1500 psig working pressure transmitters were found properly torqued to the manufacturer's recommended torque of forty foot-pounds. The average torque values were greater than one-half of the recommended torque on all transmitters. | | : 2. Three of ten 1500 psig working pressure transmitters were found properly torqued to the manufacturer's recommended torque of forty foot-pounds. The average torque values were greater than one-half of the recommended torque on all transmitters. |
| : 3. On November 7, 1973, the five transmitters that were evaluated by Fischer and Porter Company personnel were returned to the Turkey Point Plant after repair. The as-received torque was racasured by plant personnel. All four of the 3000 psig working pressure transmitters were found below the required torque of eighty foot-pounds; the one 1500 psig working pressure transmitter was found torqued satisfactorily. | | : 3. On November 7, 1973, the five transmitters that were evaluated by Fischer and Porter Company personnel were returned to the Turkey Point Plant after repair. The as-received torque was racasured by plant personnel. All four of the 3000 psig working pressure transmitters were found below the required torque of eighty foot-pounds; the one 1500 psig working pressure transmitter was found torqued satisfactorily. |
| a All transmitters were retorqued to the correct value in accordance with Maintenance Procedure 0707.3. The Fischer and Porter Company was notified of the results of the torque check in a letter dated November 9, 1973. | | a All transmitters were retorqued to the correct value in accordance with Maintenance Procedure 0707.3. The Fischer and Porter Company was notified of the results of the torque check in a {{letter dated|date=November 9, 1973|text=letter dated November 9, 1973}}. |
| Followup investigation and testing was performed as follows: | | Followup investigation and testing was performed as follows: |
| : 1. On November 10,'1973, a Fischer and Porter Company Model 10B2496PB electronic differential pressure transmitter (3000 psig working pressure) was tested at Turkey Point Plant as follows: | | : 1. On November 10,'1973, a Fischer and Porter Company Model 10B2496PB electronic differential pressure transmitter (3000 psig working pressure) was tested at Turkey Point Plant as follows: |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARL-95-089, Special Rept:On 950517,Standby Feedwater Pump B Removed from Svc & Returned to Operable Status 950710.Caused by Prime Mover for B Standby Feedwater Pump Being Changed from Electric Motor to Diesel Driver Per Amend 164/1581995-04-21021 April 1995 Special Rept:On 950517,Standby Feedwater Pump B Removed from Svc & Returned to Operable Status 950710.Caused by Prime Mover for B Standby Feedwater Pump Being Changed from Electric Motor to Diesel Driver Per Amend 164/158 ML20235M9971989-02-23023 February 1989 Special Rept:Fire Protection Sys Impaired for Greater than 7 Days.On 890118,rust Holes Noted on Fire Door 67-2.On 890121,repair Required for Thermolog Insulation.Caused by Time Deterioration.Fire Patrols Established L-87-140, Special Rept:On 870225,electric Driven Fire Pump Exceeded 7- Day Tech Spec Limit for Permissible Time Pump May Remain Out of Svc W/O NRC Notification.Caused by Leakage of Bearing Grease Past Seal.Shaft,Sleeves & Bearings Replaced1987-03-27027 March 1987 Special Rept:On 870225,electric Driven Fire Pump Exceeded 7- Day Tech Spec Limit for Permissible Time Pump May Remain Out of Svc W/O NRC Notification.Caused by Leakage of Bearing Grease Past Seal.Shaft,Sleeves & Bearings Replaced L-87-141, RO 87-03:on 870315,NRC Notified of Intention to Remove IAEA Seals on Equipment Hatch & Reactor Missile Shields.Caused by Performance of Maint & Insps on Reactor Head.Addl Work Will Be Performed When Reactor Head Removed1987-03-25025 March 1987 RO 87-03:on 870315,NRC Notified of Intention to Remove IAEA Seals on Equipment Hatch & Reactor Missile Shields.Caused by Performance of Maint & Insps on Reactor Head.Addl Work Will Be Performed When Reactor Head Removed ML20210D1791987-01-30030 January 1987 RO 87-01:on 870127,area Lights in Spent Fuel Pool Burnt Out. Caused by Low Wattage Bulbs.Bulbs Replaced W/Longer Life Bulbs.Area Lights Will Be Verified Once Per Day L-86-500, Ro:Fire Barriers Breached for More than 7 Days.Caused by App R Work Which Still Remains to Be Completed.Compensatory Measures Implemented.Affected Fire Barrier/Conduit Seals Listed1986-12-0808 December 1986 Ro:Fire Barriers Breached for More than 7 Days.Caused by App R Work Which Still Remains to Be Completed.Compensatory Measures Implemented.Affected Fire Barrier/Conduit Seals Listed L-86-485, Special Rept:On 861030,electric Driven Fire Pump Out of Svc for More than 7-day Tech Spec Limit.Caused by Independent Failure of Low Pressure Start Switch & Flow Indicator, Resulting in Unscheduled Maint.Bearing Seal Replaced1986-12-0101 December 1986 Special Rept:On 861030,electric Driven Fire Pump Out of Svc for More than 7-day Tech Spec Limit.Caused by Independent Failure of Low Pressure Start Switch & Flow Indicator, Resulting in Unscheduled Maint.Bearing Seal Replaced L-86-456, Special Rept:Fire Barriers Breached for Longer than 7 Days. Caused by App R Work in Progress.Breached Barriers Listed1986-11-0606 November 1986 Special Rept:Fire Barriers Breached for Longer than 7 Days. Caused by App R Work in Progress.Breached Barriers Listed L-86-377, Special Rept:On 860819,condenser Air Ejector High Range Noble Gas Effluent Monitor Exceeded 7 Day Outage Reportability Limitations Established in Tech Spec Table 3.5-5.Caused by Water Intrusion Into Casing of Detector1986-09-18018 September 1986 Special Rept:On 860819,condenser Air Ejector High Range Noble Gas Effluent Monitor Exceeded 7 Day Outage Reportability Limitations Established in Tech Spec Table 3.5-5.Caused by Water Intrusion Into Casing of Detector L-86-283, RO 86-3:on 860708 & 10,loss of Lighting in Spent Fuel Pool Occurred.Caused by Deenergization of 4-kV Bus 4C.Bus Realigned to Normal Power Supply.Work Plans Discussed in 860708 Telcon1986-07-11011 July 1986 RO 86-3:on 860708 & 10,loss of Lighting in Spent Fuel Pool Occurred.Caused by Deenergization of 4-kV Bus 4C.Bus Realigned to Normal Power Supply.Work Plans Discussed in 860708 Telcon L-85-146, Special Rept:On 850308,diesel Driven Fire Pump Declared Out of Svc as Result of Inoperable Immersion Heater in Diesel Cooling Sys.Caused by Defective Thermostat Switch.Immersion Heater Assembly Replaced1985-04-0808 April 1985 Special Rept:On 850308,diesel Driven Fire Pump Declared Out of Svc as Result of Inoperable Immersion Heater in Diesel Cooling Sys.Caused by Defective Thermostat Switch.Immersion Heater Assembly Replaced ML20079Q8771983-10-0505 October 1983 RO 251-83-016:discovered Containment Spray Pumps 4A & B on Both Manual Discharge Valves 4-891A & B Locked in Closed Position.Investigation in Progress.Related Info Encl ML20084B7041978-08-25025 August 1978 Ro:On 780813,metal Impact Monitoring Sys Alarmed Six Times in 1 H.Caused by Acoustic Emissions Produced by Reactor Vessel During Periods of Changing Pressure & Temp.Tubesheet Photographs of Steam Generators Verified ML20084F2561975-12-0505 December 1975 RO 251-75-3 Re Leak of Spent Fuel Pit Concrete Wall. V-shaped Stainless Steel Drain Trough Installed on Concrete Wall of Fuel Transfer Tube.Mod of Spent Fuel Storage Sys Under Consideration ML20084F3211975-12-0505 December 1975 RO 250-75-3:on 751105,spring Hanger on Main Steam Line 3A Inside Containment Found Distorted.Cause Unknown.Plant Change/Mod Being Generated to Provide New Hanger Design to Withstand Spurious Closure Load & Hydro & Test Loads ML20084F7161975-08-18018 August 1975 ROs 250-75-2 & 251-75-2 Re Several Malfunctions of Spent Fuel Pit (SFP) Cooling Pumps.Cause Not Determined.Excessive Internal Stress Suspected as Cause.Redundant Cooling Pump to Be Installed in Each SFP Cooling Sys ML20084F5861975-07-0707 July 1975 RO 251-75-1 Re ECCS Analysis.Audit by Westinghouse of Calculations of ECCS Analysis for Large Break Spectrum Cycle 2 Has Shown Value for Peak Clad Temp in Error.Caused by Using Fuel Design Data for Unit 3 ML20084F6971975-04-14014 April 1975 RO 250-75-1 Re Apparent Discrepancy Between Measured Control Rod Worth & Vendor Predictions.Cause Not Stated.Fuel Vendor Recalculated Predictions & Results Are Now Consistent W/Util Predicted Values ML20084C1321974-12-20020 December 1974 RO 251-74-6:on 741201,w/planned Shutdown in Progress,Turbine Tripped.Caused by Failure of Turbine Control Valve Spring Adjusting Bolt.Defective Bolt Replaced & Zyglo Testing of Remaining Three Bolts Performed ML20084C0921974-11-26026 November 1974 RO 74-5:on 741126,filling of Spent Fuel Pit & Reactor Refueling Cavity During Refueling Revealed Leaks in Stainless Steel Liners of Both Structures.Cause Under Investigation.Small Head Tank Installed as Temporary Action ML20084C6411974-08-0808 August 1974 RO 250-74-5:abnormally High Failure Rates Occurred in Teledyne/Philbrick-Nexus Type 140801 Operational Amplifiers Used in Upper & Lower Flux Deviation Circuits.Cause Unknown. Investigation to Recommend Solution to Be Performed ML20084C6651974-07-15015 July 1974 ROs 250-74-3 & 251-74-3:capacitor Failures in Rod Control Power Supply Filter Assemblies Caused Control Rod Drops, Initiating Turbine Runbacks.Cause Unknown.Investigation in Process by Vendor ML20084C6461974-07-0101 July 1974 ROs 250-74-4 & 251-74-4:numerous Failures Experienced W/ Sample Suction Pumps Employed in Tracerlab Containment Gaseous & Air Particulate Radiation Monitoring Sys.Cause Unknown.Re Evaluation of Leak Detection Sys in Progress ML20084C6931974-05-31031 May 1974 Ro:On 740425,generators in Both Units Tripped When Both Generator Circuit Breaker Protection Sys Relays Energized During Functional Testing of Unit 4 Startup Transformer Protection Sys Relays.No Equipment Damage or AO Resulted ML20084C7061974-05-30030 May 1974 RO 250-74-2 & 251-74-2:while Conducting Normal Shutdown on Unit 3,turbine Stop Valves Failed to Close.Caused by Phosphate Deposits Between Valve Shafts & Bushings.Phosphate Buildup Problems Also Found W/Unit 4 ML20084D0571974-04-0202 April 1974 Suppl to Special Maint Rept 73-1:on 731211,investigation Conducted Re Torque Check of Fischer & Porter Co Electronic Differential Pressure Transmitters Due to High Failure Rate. Caused by Inadequate Clamping Force ML20084D2311973-12-11011 December 1973 Special Maint Rept 73-1:on 731023-25 & 1103-05,during Startup & Initial Operation,Fischer & Porter Co Electronic Differential Pressure Transmitters,Models 2495 & 2496 Found to Fail Internally.Caused by through-bolts Not Torqued 1995-04-21
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
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FLORD A N MR & b+1 C 4 Turkey Point Plant December 11, 1973 Mr. John F. O' Leary, Director .( N Directorate of Licensing N Office of Regulation " N U.S. Atomic Energy Commission IN.b ]}V 8fP Q(\
Washington, D. C. 20545 f-DECl? 197.4 4
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TURKEY POINT UNITS No. 3 AND 4 DOCKET NUMBERS 50-250 AND 50-251
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SPECIAL MAINTENANCE REPORT No. 73-1 \ I' jgf TORQUE CHECK OF FISCHER AND PORTER COMPANY mt_.
ELECTRONIC DIFFERENTIAL PRESSURE TRANSMITTERS
Dear Mr. O' Leary:
This report is submitted in accordance with Technical Specification 6.6.3.d, Operating License Numbers DPR-31 and DPR-41. The special maintenance was performed on October 23-25, 1973, for Unit No. 3, and on November 3-5, 1973, for Unit No. 4.
I. BACKGROUND During the startup and initial operation of Turkey Point Units 3 and 4, a significant number of Fischer and Porter Company Electronic Differential Pressure Transmitters, Model 2495 and Model 2496, were found to have failed internally. After the startup of Turkey Point Unit No. 4 in June, 1973, the high level of maintenance required to keep these transmitters operational became of concern to staff and plant personnel of Florida Power and Light Company. A meeting was held on. August 1, 1973 with Fischer and Porter Company personnel to discuss the cause of the high failure rate and corrective action.
At this meeting it was agreed that Florida Power and Light Company would provide Fischer and Porter Company with five failed units which would be disassembled completely at the factory and evaluated to determine what had caused the failure.
In a letter dated October 1, 1973, Florida Power and Light Company was advised by Fischer and Porter Company that all five of the failed
- transmitters had lost their fill fluid and failed. The through-bolts on the process flanges for these five transmitters were not torqued to the manufacturer's recommended torque value. The postulated failure mechanism is an elongation of the through-bolts due to inadequate bolt torque, with a subsequent loss of fill fluid under process pressures.-
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COPY SENT REGION _,
i PTP
December 11, 1973 Page 2
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II. CORRECTIVE E11NTENANCE ACTION TAKEN The initial corrective action taken was to measure the torque on the through-bolts of all Fischer and Porter Company electronic dif ferential pressure transmitters. Maintenance Procedure 0707.3 was written and approved to conduct the torque check. The Unit No. 3 transmitters were checked during a maintenance shutdown on October 23-25, 1973, and the Unit No. 4 transmitters were checked during a maintenance shutdown on November 3-5, 1973. The arithmetic average torque for the four through-bolts on each transmitter was calculated and the following luformation obtained:
- 1. Three of ninety-four 3000 psig working pressure transmitters were found properly torqued to the manufacturer's recommended torque of eighty foot-pounds. Approximately seventy per cent (70%)
of the transmitters had torque values less than one half (1/2) of the recommended torque. The lowest average torque measured was 19.2 foot-pounds.
- 2. Three of ten 1500 psig working pressure transmitters were found properly torqued to the manufacturer's recommended torque of forty foot-pounds. The average torque values were greater than one-half of the recommended torque on all transmitters.
- 3. On November 7, 1973, the five transmitters that were evaluated by Fischer and Porter Company personnel were returned to the Turkey Point Plant after repair. The as-received torque was racasured by plant personnel. All four of the 3000 psig working pressure transmitters were found below the required torque of eighty foot-pounds; the one 1500 psig working pressure transmitter was found torqued satisfactorily.
a All transmitters were retorqued to the correct value in accordance with Maintenance Procedure 0707.3. The Fischer and Porter Company was notified of the results of the torque check in a letter dated November 9, 1973.
Followup investigation and testing was performed as follows:
- 1. On November 10,'1973, a Fischer and Porter Company Model 10B2496PB electronic differential pressure transmitter (3000 psig working pressure) was tested at Turkey Point Plant as follows:
(a) The four through-bolts on the process flanges were loosened and then carefully torqued to eighty foot-pounds.
(b) The transmitter was pressurized to the hydrostatic test pressure recommended by the manufacturer, 4100 psig, for a period of ten minutes.
(c) The hydrostatic test pressure was released and the torque was measured. The torque had reduced to seventy foot-pounds on all four bolts.
l 1
l
.PTP Mr. John F. O'Lfy Page 3 p';
December 11,19't ' '-
- 2. On November 11, 1973, the stainless steel through-bolts on the same transmitter were replaced with high tensile strength bolts fabricated from A.I.S.I. Type 4130 low alloy carbon steel. The test performed on November 10, 1973, was repeated; the through-bolt torque remained eighty foot-pounds.
- 3. A review of the instrument records was performed to determine the failure rate of the differential pressure transmitters in various pressure environments. The following results were obtained for operations subsequent to August, 1971:
Design Number of Number of Pressure Environment Pressure Units Installed Units Failed Reactor Coolant System 2485 psig 22 11 Charging System 2735 psig 8 3 Safety Injection System 1750 psig 8 0 Feedwater System 1525 psig 12 6 Steam Generator System 1200 psig 36 15 Residual Heat Removal System 600 psig 2 0 Low Pressure Letdown System 500 psig 2 1 Component Cooling System 150 psig 4 1 Boric Acid Tank Level atmospheric 3 0 There were five transmitters that failed during prestartup checks (prior to September, 1971)
The postulated failure machanism of elongating the through-bolts under pressure appears to be credible in view of the results of the testing to date. The decision en final corrective action will be determined after the Fischer and Porter Company has completed testing and has recommended corrective action.
III. EVALUATION OF SAFETY IMPLICATIONS All transmitters affected had failed in the safe (tripped) condition upon loss of fill fluid. The steam generator level transmitters failed to maximum output and caused a single channel Hi-Hi Steam Generator Level Turbine Trip signal, which would trip the turbine and reactor if the second trip signal occured and tripped the 2/3 logic matrix.
All other transmitters failed to zero output and caused a single channel trip signal for either Low Reactor Coolant Flow, Low Steam Generator Feedwater Flow, or Low Steam Generator Steam Flow. There are no trip signals associated with the remaining transmitters.
V.
SUMMARY
OF THE SPECIAL MAINTENANCE
- 1. High maintenance was experienced on Fischer and Porter Company Electronic Differential Pressure Transmitters due to internal failures. ,
- 2. An evaluation by Fischer and Porter Company factory personnel revealed that the failures are due to inadequate torque on the through-bolts for the process flanges of the transmitter. The postulated cause is an elongation of the through-bolts under pressure. ,
PTP .
Mr. John F. O'Lff Page 4 ,
December 11, 197s/
- 3. The torque on the through-bolts of all Fischer and Porter Company Electronic Differential Pressure Transmitters at the Turkey Point Plant was checked and found to be below the required torque value for nearly all transmitters, including those transmitters recently received from the factory. All through-bolts were torqued to the manufacturer's recommended torque value. Fischer and Porter Company representives have been notified of the results of the torque check.
- 4. Testing at Turkey Point Plant subsequent to the torque check confirmed that the through-bolts are clongating.
- 5. The final corrective maintenance will be determined after the manufacturer's recommendations have been received.
- 6. This special maintenance has not resulted in any danger to the public health and safety, nor has safe operation of the reactor been jeapordized.
We will keep you advised of progress on this problem and of final corrective action.
hk1H~
A. D. Schmidt
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GEL / ldh cc: Mr. Norman C. Moseley
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