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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARL-95-089, Special Rept:On 950517,Standby Feedwater Pump B Removed from Svc & Returned to Operable Status 950710.Caused by Prime Mover for B Standby Feedwater Pump Being Changed from Electric Motor to Diesel Driver Per Amend 164/1581995-04-21021 April 1995 Special Rept:On 950517,Standby Feedwater Pump B Removed from Svc & Returned to Operable Status 950710.Caused by Prime Mover for B Standby Feedwater Pump Being Changed from Electric Motor to Diesel Driver Per Amend 164/158 ML20235M9971989-02-23023 February 1989 Special Rept:Fire Protection Sys Impaired for Greater than 7 Days.On 890118,rust Holes Noted on Fire Door 67-2.On 890121,repair Required for Thermolog Insulation.Caused by Time Deterioration.Fire Patrols Established L-87-140, Special Rept:On 870225,electric Driven Fire Pump Exceeded 7- Day Tech Spec Limit for Permissible Time Pump May Remain Out of Svc W/O NRC Notification.Caused by Leakage of Bearing Grease Past Seal.Shaft,Sleeves & Bearings Replaced1987-03-27027 March 1987 Special Rept:On 870225,electric Driven Fire Pump Exceeded 7- Day Tech Spec Limit for Permissible Time Pump May Remain Out of Svc W/O NRC Notification.Caused by Leakage of Bearing Grease Past Seal.Shaft,Sleeves & Bearings Replaced L-87-141, RO 87-03:on 870315,NRC Notified of Intention to Remove IAEA Seals on Equipment Hatch & Reactor Missile Shields.Caused by Performance of Maint & Insps on Reactor Head.Addl Work Will Be Performed When Reactor Head Removed1987-03-25025 March 1987 RO 87-03:on 870315,NRC Notified of Intention to Remove IAEA Seals on Equipment Hatch & Reactor Missile Shields.Caused by Performance of Maint & Insps on Reactor Head.Addl Work Will Be Performed When Reactor Head Removed ML20210D1791987-01-30030 January 1987 RO 87-01:on 870127,area Lights in Spent Fuel Pool Burnt Out. Caused by Low Wattage Bulbs.Bulbs Replaced W/Longer Life Bulbs.Area Lights Will Be Verified Once Per Day L-86-500, Ro:Fire Barriers Breached for More than 7 Days.Caused by App R Work Which Still Remains to Be Completed.Compensatory Measures Implemented.Affected Fire Barrier/Conduit Seals Listed1986-12-0808 December 1986 Ro:Fire Barriers Breached for More than 7 Days.Caused by App R Work Which Still Remains to Be Completed.Compensatory Measures Implemented.Affected Fire Barrier/Conduit Seals Listed L-86-485, Special Rept:On 861030,electric Driven Fire Pump Out of Svc for More than 7-day Tech Spec Limit.Caused by Independent Failure of Low Pressure Start Switch & Flow Indicator, Resulting in Unscheduled Maint.Bearing Seal Replaced1986-12-0101 December 1986 Special Rept:On 861030,electric Driven Fire Pump Out of Svc for More than 7-day Tech Spec Limit.Caused by Independent Failure of Low Pressure Start Switch & Flow Indicator, Resulting in Unscheduled Maint.Bearing Seal Replaced L-86-456, Special Rept:Fire Barriers Breached for Longer than 7 Days. Caused by App R Work in Progress.Breached Barriers Listed1986-11-0606 November 1986 Special Rept:Fire Barriers Breached for Longer than 7 Days. Caused by App R Work in Progress.Breached Barriers Listed L-86-377, Special Rept:On 860819,condenser Air Ejector High Range Noble Gas Effluent Monitor Exceeded 7 Day Outage Reportability Limitations Established in Tech Spec Table 3.5-5.Caused by Water Intrusion Into Casing of Detector1986-09-18018 September 1986 Special Rept:On 860819,condenser Air Ejector High Range Noble Gas Effluent Monitor Exceeded 7 Day Outage Reportability Limitations Established in Tech Spec Table 3.5-5.Caused by Water Intrusion Into Casing of Detector L-86-283, RO 86-3:on 860708 & 10,loss of Lighting in Spent Fuel Pool Occurred.Caused by Deenergization of 4-kV Bus 4C.Bus Realigned to Normal Power Supply.Work Plans Discussed in 860708 Telcon1986-07-11011 July 1986 RO 86-3:on 860708 & 10,loss of Lighting in Spent Fuel Pool Occurred.Caused by Deenergization of 4-kV Bus 4C.Bus Realigned to Normal Power Supply.Work Plans Discussed in 860708 Telcon L-85-146, Special Rept:On 850308,diesel Driven Fire Pump Declared Out of Svc as Result of Inoperable Immersion Heater in Diesel Cooling Sys.Caused by Defective Thermostat Switch.Immersion Heater Assembly Replaced1985-04-0808 April 1985 Special Rept:On 850308,diesel Driven Fire Pump Declared Out of Svc as Result of Inoperable Immersion Heater in Diesel Cooling Sys.Caused by Defective Thermostat Switch.Immersion Heater Assembly Replaced ML20079Q8771983-10-0505 October 1983 RO 251-83-016:discovered Containment Spray Pumps 4A & B on Both Manual Discharge Valves 4-891A & B Locked in Closed Position.Investigation in Progress.Related Info Encl ML20084B7041978-08-25025 August 1978 Ro:On 780813,metal Impact Monitoring Sys Alarmed Six Times in 1 H.Caused by Acoustic Emissions Produced by Reactor Vessel During Periods of Changing Pressure & Temp.Tubesheet Photographs of Steam Generators Verified ML20084F2561975-12-0505 December 1975 RO 251-75-3 Re Leak of Spent Fuel Pit Concrete Wall. V-shaped Stainless Steel Drain Trough Installed on Concrete Wall of Fuel Transfer Tube.Mod of Spent Fuel Storage Sys Under Consideration ML20084F3211975-12-0505 December 1975 RO 250-75-3:on 751105,spring Hanger on Main Steam Line 3A Inside Containment Found Distorted.Cause Unknown.Plant Change/Mod Being Generated to Provide New Hanger Design to Withstand Spurious Closure Load & Hydro & Test Loads ML20084F7161975-08-18018 August 1975 ROs 250-75-2 & 251-75-2 Re Several Malfunctions of Spent Fuel Pit (SFP) Cooling Pumps.Cause Not Determined.Excessive Internal Stress Suspected as Cause.Redundant Cooling Pump to Be Installed in Each SFP Cooling Sys ML20084F5861975-07-0707 July 1975 RO 251-75-1 Re ECCS Analysis.Audit by Westinghouse of Calculations of ECCS Analysis for Large Break Spectrum Cycle 2 Has Shown Value for Peak Clad Temp in Error.Caused by Using Fuel Design Data for Unit 3 ML20084F6971975-04-14014 April 1975 RO 250-75-1 Re Apparent Discrepancy Between Measured Control Rod Worth & Vendor Predictions.Cause Not Stated.Fuel Vendor Recalculated Predictions & Results Are Now Consistent W/Util Predicted Values ML20084C1321974-12-20020 December 1974 RO 251-74-6:on 741201,w/planned Shutdown in Progress,Turbine Tripped.Caused by Failure of Turbine Control Valve Spring Adjusting Bolt.Defective Bolt Replaced & Zyglo Testing of Remaining Three Bolts Performed ML20084C0921974-11-26026 November 1974 RO 74-5:on 741126,filling of Spent Fuel Pit & Reactor Refueling Cavity During Refueling Revealed Leaks in Stainless Steel Liners of Both Structures.Cause Under Investigation.Small Head Tank Installed as Temporary Action ML20084C6411974-08-0808 August 1974 RO 250-74-5:abnormally High Failure Rates Occurred in Teledyne/Philbrick-Nexus Type 140801 Operational Amplifiers Used in Upper & Lower Flux Deviation Circuits.Cause Unknown. Investigation to Recommend Solution to Be Performed ML20084C6651974-07-15015 July 1974 ROs 250-74-3 & 251-74-3:capacitor Failures in Rod Control Power Supply Filter Assemblies Caused Control Rod Drops, Initiating Turbine Runbacks.Cause Unknown.Investigation in Process by Vendor ML20084C6461974-07-0101 July 1974 ROs 250-74-4 & 251-74-4:numerous Failures Experienced W/ Sample Suction Pumps Employed in Tracerlab Containment Gaseous & Air Particulate Radiation Monitoring Sys.Cause Unknown.Re Evaluation of Leak Detection Sys in Progress ML20084C6931974-05-31031 May 1974 Ro:On 740425,generators in Both Units Tripped When Both Generator Circuit Breaker Protection Sys Relays Energized During Functional Testing of Unit 4 Startup Transformer Protection Sys Relays.No Equipment Damage or AO Resulted ML20084C7061974-05-30030 May 1974 RO 250-74-2 & 251-74-2:while Conducting Normal Shutdown on Unit 3,turbine Stop Valves Failed to Close.Caused by Phosphate Deposits Between Valve Shafts & Bushings.Phosphate Buildup Problems Also Found W/Unit 4 ML20084D0571974-04-0202 April 1974 Suppl to Special Maint Rept 73-1:on 731211,investigation Conducted Re Torque Check of Fischer & Porter Co Electronic Differential Pressure Transmitters Due to High Failure Rate. Caused by Inadequate Clamping Force ML20084D2311973-12-11011 December 1973 Special Maint Rept 73-1:on 731023-25 & 1103-05,during Startup & Initial Operation,Fischer & Porter Co Electronic Differential Pressure Transmitters,Models 2495 & 2496 Found to Fail Internally.Caused by through-bolts Not Torqued 1995-04-21
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
[Table view] |
Text
. P.C. BOX 3100 MIAMI. f tORIDA 33101
.-...-g FLORtDA PO'AER & LIGHT COMPANY April 14, 1975 Mr. Benard C. Rusche, Director Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Washington, D. C. 20555
Dear Mr. Rusche:
UNUSUAL EVENT NO. 250-75-1 TURKEY POINT UNIT NO. 3 APPARENT DISCREPANCY BETWEEN MEASURED -
CONTROL ROD WORTH AND VENDOR PREDICTIONS A. DESCRIPTION OF EVENT During physics tes. ting following Unit 3 Cycle II refueling, a comparison of measured control rod worths to the predicted worths, furnished by the vendor indicated ' discrepancy of approximately 19% for total control rod bank worth. The measured val-ucs were lower than predicted which gave some concern as to required shutdown margin at beginning-of-cycle. Further testing verified that adequate shutdown margin existed so normal operation of the unit was initiated.
B. APPAR$NT CAUSE AND ANALYSIS OF EVENT An investigation into the apparent discrepancy was initiated by Florida Power & Light Company to determine its cause and extent.
The fuel vendor was requested to reconfirm the predicted values for Cycle II operation. In addition, Florida Power & Light Company engineers performed independent calculations of beginning-of-cycle physics parameters. The Florida Power & Light Company calculations indicate that the measured control rod worths are within 6% of predicted values for beginning-of-cycle conditions.
Further, end-of-cycle calculations indicate that adequate shut-down margin will be available.
C. CORRECTIVE ACTION The fuel vendor has recalculated his predictions and the results, included as Table 1, are consistent with Florida Power &-Light Company predicted values. Based on this recalculation and our a: ~~'
'i 8304210244 750414 PDR ADOCK 05000250 S PDR TAWhM't&JtuT" ^
<_o
O O
Mr. Benard C. Rusche, Director Page Two April 14, 1975 L- independent calculations, adequate control rod capability and {
L-shutdown margin exist throughout Cycle II.
Very truly yours,
- l II pM A. D. Schmidt
.Vice President .
Power Resources PJW/cpc Enclosure ,
cc: Mr. Norman C. Moseley ,
Jack R. Newman, Esquire 6
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'O. O 1 TABLE 1 i
u '
TURKEY POINT UNIT NO. 3 - CYCLE 2 l
END OF CYCLE SHUTDOWN REQUIREMENTS AND MARGINS 1
I REVISED ITEM CYCLE 1 CYCLE 2 Control Rod Worth at HZP (%Ap)
" 'All Full Length Rods Inserted 7.71 7.23
. All Full Length Rods Inserted Less Worst Stuck Rod (F-14) 6.47 6.01 (1) Less 10% S.82 5.41 Control Rod Requirements (%Ap)
Power Defect (Combined Doppler, Tavg, Void and Redistribution ertects) 3.07 2.61 Rod Insertion Allowance 0.70 0.70 (2) Tota,1 Requirement 3.77 3.31 Shutdown Margin [(1) - (2)] (%Ap) 2.05 2.10 Required Shutdown Margin (%Ap) 1.77 ,
1.77 Excess 0.28 0.33 The revised control rod worth is based on the end of Cycle 1 critical boron and an adjustment to the radial reflector cross-section to provide better agreement with power distribution measure- .
ments. The revised power defect is based on a more accurate evaluation at the Cycle 2 plant operating conditions for a core average moderator temperature of 567.3*F at a system pressure of 1,900 psia, as pre-viously documented in the Unit No. 3 Design Report.
Based on this revised analysis, the calculated N-1 rod worth at BOC II is within 6.7% of the measured value. In addition, at BOC II the reanalysis provides good agreement between the calculated and measured power distribution and the HFP and HZP critical boron concen-trations.
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