IR 05000341/2017003: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(4 intermediate revisions by the same user not shown)
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:November 13, 2017
{{#Wiki_filter:UNITED STATES ember 13, 2017


==SUBJECT:==
==SUBJECT:==
FERMI POWER PLANT, UNIT 2-NRC INTEGRATED INSPECTION REPORT 05000341/2017003
FERMI POWER PLANT, UNIT 2NRC INTEGRATED INSPECTION REPORT 05000341/2017003


==Dear Mr. Polson:==
==Dear Mr. Polson:==
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Fermi Power Plant, Unit 2 (Fermi 2). On October 17, 2017, the NRC inspectors discussed the results of this inspection with Mr. M. Caragher and other members of your staff. The inspectors documented the results of this inspection in the enclosed inspection report. Based on the results of this inspection, the NRC has identified two issues, one that was evaluated under the risk significance determination process as having very low safety significance (Green) and one evaluated under the traditional enforcement process as a Severity Level IV violation. Both of these issues involved violations of NRC requirements. Because the licensee initiated condition reports to address these issues, these violations are being treated as Non-Cited Violations (NCVs), consistent with Section 2.3.2 of the Enforcement Policy. These NCVs are described in the subject inspection report. If you contest the violations or significance of the Non-Cited Violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to: (1) the Regional Administrator, Region III; (2) the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Fermi 2 Power Plant. In addition, if you disagree with the cross-cutting aspect assignment to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Fermi 2 Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Fermi Power Plant, Unit 2 (Fermi 2). On October 17, 2017, the NRC inspectors discussed the results of this inspection with Mr. M. Caragher and other members of your staff. The inspectors documented the results of this inspection in the enclosed inspection report.
 
Based on the results of this inspection, the NRC has identified two issues, one that was evaluated under the risk significance determination process as having very low safety significance (Green) and one evaluated under the traditional enforcement process as a Severity Level IV violation. Both of these issues involved violations of NRC requirements. Because the licensee initiated condition reports to address these issues, these violations are being treated as Non-Cited Violations (NCVs), consistent with Section 2.3.2 of the Enforcement Policy. These NCVs are described in the subject inspection report.
 
If you contest the violations or significance of the Non-Cited Violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to: (1) the Regional Administrator, Region III; (2) the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Fermi 2 Power Plant.
 
In addition, if you disagree with the cross-cutting aspect assignment to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Fermi 2 Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.


Sincerely,
Sincerely,
/RA/
/RA/
Billy Dickson, Chief Branch 2 Division of Reactor Projects  
Billy Dickson, Chief Branch 2 Division of Reactor Projects Docket No. 50-341 License No. NPF-43 Enclosure:
Inspection Report 05000341/2017003 cc: Distribution via LISTSERV


Docket No. 50-341 License No. NPF-43
=SUMMARY=
Inspection Report 05000341/2017003; 07/01/2017 - 09/30/2017; Fermi Power Plant, Unit 2;


Enclosure: Inspection Report 05000341/2017003 cc: Distribution via LISTSERV
Operability Determinations and Functionality Assessments.


=SUMMARY=
This report covers a 3-month period of inspection by the resident inspectors. One Green finding, with an associated Non-Cited Violation (NCV) of U.S. Nuclear Regulatory Commission (NRC) regulations, and one Security Level IV NCV of NRC regulations were identified. The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process, dated April 25, 2015. Cross-cutting aspects are determined using IMC 0310, Aspects within the Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, dated July 201
Inspection Report 05000341/2017003; 07/01/2017 - 09/30/2017; Fermi Power Plant, Unit 2; Operability Determinations and Functionality Assessments. This report covers a 3-month period of inspection by the resident inspectors. One Green finding, with an associated Non-Cited Violation (NCV) of U.S. Nuclear Regulatory
 
Commission (NRC) regulations, and one Security Level IV NCV of NRC regulations were identified. The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," dated April 25, 2015. Cross-cutting aspects are determined using IMC 0310, "Aspects within the Cross-Cutting Areas," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," dated July 2016.


===NRC-Identified===
===NRC-Identified===
and Self-Revealed Findings  
and Self-Revealed Findings


===Cornerstone: Mitigating Systems ===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
The inspectors identified a Non-Cited Violation (NCV) of Technical Specification (TS) 3.8.7 "Distribution Systems - Operating," for the licensee's failure to either restore inoperable Division 1 and Division 2 AC electrical power distribution subsystems to operable status within 8 hours or be in Mode 3 in 12 hours. Specifically, electrical power distribution subsystems required by the above limiting condition for operation were inoperable due to their respective subdivisions of Residual Heat Removal (RHR) switchgear room ventilation systems being out of service and therefore unavailable to provide the technical specification support function of attendant cooling that was needed for the associated electrical systems to perform their specified safety functions. The licensee entered the issue into its corrective action program as CARD 17-26749. The failure to comply with TS 3.8.7 by either restoring inoperable electrical power subsystems to operable status within 8 hours, or be in Mode 3 in 12 hours was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the Configuration Control attribute of the Mitigating Systems Cornerstone, and adversely affected the associated cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined that the finding was of very low safety significance (Green) because it did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time, or two separate safety systems out-of-service for greater than its technical specification allowed outage time. The inspectors determined that the violation had a cross-cutting aspect in the area of human performance, resources, because the licensee failed to ensure that the RHR Complex Heating and Ventilation procedure was adequate to support nuclear safety (H.1). (Section 1R15b.2)
The inspectors identified a Non-Cited Violation (NCV) of Technical Specification (TS) 3.8.7 Distribution Systems - Operating, for the licensees failure to either restore inoperable Division 1 and Division 2 AC electrical power distribution subsystems to operable status within 8 hours or be in Mode 3 in 12 hours. Specifically, electrical power distribution subsystems required by the above limiting condition for operation were inoperable due to their respective subdivisions of Residual Heat Removal (RHR) switchgear room ventilation systems being out of service and therefore unavailable to provide the technical specification support function of attendant cooling that was needed for the associated electrical systems to perform their specified safety functions. The licensee entered the issue into its corrective action program as CARD 17-26749.
 
The failure to comply with TS 3.8.7 by either restoring inoperable electrical power subsystems to operable status within 8 hours, or be in Mode 3 in 12 hours was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the Configuration Control attribute of the Mitigating Systems Cornerstone, and adversely affected the associated cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined that the finding was of very low safety significance (Green) because it did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time, or two separate safety systems out-of-service for greater than its technical specification allowed outage time. The inspectors determined that the violation had a cross-cutting aspect in the area of human performance, resources, because the licensee failed to ensure that the RHR Complex Heating and Ventilation procedure was adequate to support nuclear safety (H.1). (Section 1R15b.2)


===Other Findings===
===Other Findings===
Severity Level IV. The inspectors identified a Severity Level IV NCV of the NRC's reporting requirements Title 10 of the Code of Federal Regulations (CFR), Part 50.73(a)(1), "Licensee Event Report [LER] System.The licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery on March 24, 2017, of a condition that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system. The licensee entered this issue into its corrective action program to evaluate the cause for its failure to satisfy the reporting requirements and to identify appropriate corrective actions.
Severity Level IV. The inspectors identified a Severity Level IV NCV of the NRCs reporting requirements Title 10 of the Code of Federal Regulations (CFR), Part 50.73(a)(1), Licensee Event Report [LER] System. The licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery on March 24, 2017, of a condition that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system. The licensee entered this issue into its corrective action program to evaluate the cause for its failure to satisfy the reporting requirements and to identify appropriate corrective actions.


Subsequently, the licensee made a telephone notification on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859). Consistent with the guidance in IMC 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening," dated September 7, 2012, the inspectors determined the performance deficiency was of minor significance based on "No" answers to the more-than-minor screening questions. In accordance with Section 6.9.d.9 of the NRC
Subsequently, the licensee made a telephone notification on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).


Enforcement Policy, this violation was categorized as Severity Level IV because the licensee failed to report as required by 10 CFR 50.73(a)(1). No cross-cutting aspect is associated with this traditional enforcement violation because the associated performance deficiency was determined to be of minor significance and therefore not a finding. (Section 1R15.b.1)4
Consistent with the guidance in IMC 0612, Power Reactor Inspection Reports,
Appendix B, Issue Screening, dated September 7, 2012, the inspectors determined the performance deficiency was of minor significance based on No answers to the more-than-minor screening questions. In accordance with Section 6.9.d.9 of the NRC Enforcement Policy, this violation was categorized as Severity Level IV because the licensee failed to report as required by 10 CFR 50.73(a)(1). No cross-cutting aspect is associated with this traditional enforcement violation because the associated performance deficiency was determined to be of minor significance and therefore not a finding. (Section 1R15.b.1)


=REPORT DETAILS=
=REPORT DETAILS=
Summary of Plant Status Fermi 2 Power Plant was operated at or near 100 percent power during the inspection period with the following exceptions:
 
===Summary of Plant Status===
 
Fermi 2 Power Plant was operated at or near 100 percent power during the inspection period with the following exceptions:
* On August 5, the licensee reduced power to about 80 percent to perform a control rod pattern adjustment and turbine stop and control valve testing. The unit was returned to full power the following day.
* On August 5, the licensee reduced power to about 80 percent to perform a control rod pattern adjustment and turbine stop and control valve testing. The unit was returned to full power the following day.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}}
{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
{{IP sample|IP=IP 71111.01}}
Line 65: Line 75:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the design, material condition, and procedures for coping with the design basis probable maximum flood. The evaluation included a review to check for deviations from the descriptions provi ded in the Updated Final Safety Analysis Report (UFSAR) for features intended to mitigate the potential for flooding from external factors. As part of this evaluation, the inspectors checked for obstructions that could prevent draining, checked that the roofs did not contain obvious loose items that could clog drains in the event of heavy precipitation, and determined that barriers required to mitigate the flood were in place and operable. Additionally, the inspectors performed a walkdown of the protected area to identify any modification to the site which would inhibit site drainage during a probable maximum precipitation event or allow water ingress past a barrier. The inspectors also walked down underground bunkers/manholes subject to flooding that contained multiple train or multiple function risk-significant cables. The inspectors also reviewed the abnormal operating procedure for mitigating the design basis flood to ensure it could be implemented as written. This inspection constituted one external flooding sample as defined in Inspection Procedure (IP) 71111.01.
The inspectors evaluated the design, material condition, and procedures for coping with the design basis probable maximum flood. The evaluation included a review to check for deviations from the descriptions provided in the Updated Final Safety Analysis Report (UFSAR) for features intended to mitigate the potential for flooding from external factors. As part of this evaluation, the inspectors checked for obstructions that could prevent draining, checked that the roofs did not contain obvious loose items that could clog drains in the event of heavy precipitation, and determined that barriers required to mitigate the flood were in place and operable. Additionally, the inspectors performed a walkdown of the protected area to identify any modification to the site which would inhibit site drainage during a probable maximum precipitation event or allow water ingress past a barrier. The inspectors also walked down underground bunkers/manholes subject to flooding that contained multiple train or multiple function risk-significant cables. The inspectors also reviewed the abnormal operating procedure for mitigating the design basis flood to ensure it could be implemented as written.
 
This inspection constituted one external flooding sample as defined in Inspection Procedure (IP) 71111.01.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 Readiness for Impending Adverse Weather Conditions-Thunderstorms and High===
===.2 Readiness for Impending Adverse Weather ConditionsThunderstorms and High===


Temperatures
Temperatures


====a. Inspection Scope====
====a. Inspection Scope====
Since thunderstorms and high temperatures were forecasted for the week of September 18-22, the inspectors evaluated the licensee's overall preparations and protection for the expected weather conditions focusing on the emergency diesel generators (EDGs) and off-site power switchyards. The inspectors reviewed plant 5 specific design features and implementation of procedures for responding to or mitigating the effects of thunderstorms and high temperature conditions on the operation of plant systems. The inspectors observed housekeeping practices surrounding the switchyards and material condition and operating status of the EDGs in case of a loss of off-site power. The inspectors also discussed potential compensatory measures with plant operators. In addition, the inspectors verified adverse weather protection problems were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected Condition Assessment Resolution Documents (CARDs) were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted one readiness for impending adverse weather condition inspection sample as defined in IP 71111.01.
Since thunderstorms and high temperatures were forecasted for the week of September 18-22, the inspectors evaluated the licensees overall preparations and protection for the expected weather conditions focusing on the emergency diesel generators (EDGs) and off-site power switchyards. The inspectors reviewed plant specific design features and implementation of procedures for responding to or mitigating the effects of thunderstorms and high temperature conditions on the operation of plant systems. The inspectors observed housekeeping practices surrounding the switchyards and material condition and operating status of the EDGs in case of a loss of off-site power. The inspectors also discussed potential compensatory measures with plant operators.
 
In addition, the inspectors verified adverse weather protection problems were entered into the licensees corrective action program with the appropriate characterization and significance. Selected Condition Assessment Resolution Documents (CARDs) were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted one readiness for impending adverse weather condition inspection sample as defined in IP 71111.01.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
Line 89: Line 104:
* Division 2 Residual Heat Removal (RHR) during planned maintenance on Division 1 RHR;
* Division 2 Residual Heat Removal (RHR) during planned maintenance on Division 1 RHR;
* Division 2 EDGs during planned maintenance on EDG 12; and
* Division 2 EDGs during planned maintenance on EDG 12; and
* Reactor Core Isolation Cooling during planned maintenance on High Pressure Coolant Injection (HPCI). The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones. The inspectors reviewed operating procedures, system diagrams, technical specification (TS) requirements, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and were available. The inspectors observed operating parameters and examined the material condition of the equipment to verify there were no obvious deficiencies. In addition, the inspectors verified problems associated with plant equipment alignment were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted three partial system walkdown inspection samples as defined in IP 71111.04.
* Reactor Core Isolation Cooling during planned maintenance on High Pressure Coolant Injection (HPCI).
 
The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones. The inspectors reviewed operating procedures, system diagrams, technical specification (TS) requirements, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and were available. The inspectors observed operating parameters and examined the material condition of the equipment to verify there were no obvious deficiencies.
 
In addition, the inspectors verified problems associated with plant equipment alignment were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted three partial system walkdown inspection samples as defined in IP 71111.04.


====b. Findings====
====b. Findings====
Line 97: Line 118:


====a. Inspection Scope====
====a. Inspection Scope====
From August 28 through September 16, the inspectors performed a complete system alignment inspection of the Control Center Heating, Ventilation, and Air Conditioning (CCHVAC) system to verify the functional capability of the system. This system was selected because it was considered risk significant from an initiating events perspective. The inspectors walked down the system to review mechanical and electrical equipment lineups; electrical power availability; system pressure and temperature indications, as appropriate; component labeling; component lubrication; component and equipment cooling; hangers and supports; operability of support systems; and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding work orders (WOs)  
From August 28 through September 16, the inspectors performed a complete system alignment inspection of the Control Center Heating, Ventilation, and Air Conditioning (CCHVAC) system to verify the functional capability of the system. This system was selected because it was considered risk significant from an initiating events perspective. The inspectors walked down the system to review mechanical and electrical equipment lineups; electrical power availability; system pressure and temperature indications, as appropriate; component labeling; component lubrication; component and equipment cooling; hangers and supports; operability of support systems; and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding work orders (WOs)was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the corrective action program database to ensure system equipment alignment problems were being identified and appropriately resolved.


was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the corrective action program database to ensure system equipment alignment problems were being identified and appropriately resolved. These activities constituted one complete system walkdown inspection sample as defined in IP 71111.04.
These activities constituted one complete system walkdown inspection sample as defined in IP 71111.04.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
Line 112: Line 132:
The inspectors conducted fire protection walkdowns focusing on the availability, accessibility, and condition of firefighting equipment in the following risk-significant plant areas:
The inspectors conducted fire protection walkdowns focusing on the availability, accessibility, and condition of firefighting equipment in the following risk-significant plant areas:
* Reactor Building First Floor - Mezzanine;
* Reactor Building First Floor - Mezzanine;
* Auxiliary Building Basement - "T" Room;
* Auxiliary Building Basement - T Room;
* Residual Heat Removal Complex - Division 2 EDGs and Switchgear/Ventilation Rooms;
* Residual Heat Removal Complex - Division 2 EDGs and Switchgear/Ventilation Rooms;
* Turbine Building Basement - Standby Feedwater Area; and
* Turbine Building Basement - Standby Feedwater Area; and
* Auxiliary Building Fifth Floor - Division 2 CCHVAC. The inspectors reviewed these fire areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and implemented adequate compensatory measures for out-of-service, degraded, or inoperable fire 7 protection equipment, systems, or features in accordance with the licensee's Fire Protection Plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events (IPEEE) Report with later additional insights, their potential to impact equipment that could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event. The inspectors verified fire hoses and extinguishers were in their designated locations and available for immediate use; fire detectors and sprinklers were unobstructed; transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. In addition, the inspectors verified problems associated with plant fire protection were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted five quarterly fire protection inspection samples as defined in IP 71111.05Q.
* Auxiliary Building Fifth Floor - Division 2 CCHVAC.
 
The inspectors reviewed these fire areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and implemented adequate compensatory measures for out-of-service, degraded, or inoperable fire protection equipment, systems, or features in accordance with the licensees Fire Protection Plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events (IPEEE) Report with later additional insights, their potential to impact equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. The inspectors verified fire hoses and extinguishers were in their designated locations and available for immediate use; fire detectors and sprinklers were unobstructed; transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition.
 
In addition, the inspectors verified problems associated with plant fire protection were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted five quarterly fire protection inspection samples as defined in IP 71111.05Q.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
==1R11 Licensed Operator Requalification Program==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
{{IP sample|IP=IP 71111.11}}
Line 126: Line 151:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed licensed operators during simulator training on September 12, conducted partially in response to licensee-identified corrective actions intended to improve overall operating crew performance. The inspectors assessed the operators' performance of simulated tasks focusing on alarm response, command and control of crew activities, communication practices, and procedural adherence. The inspectors also observed the operations training staff's post-evaluation critique to assess the ability of the licensee's evaluators to identify performance deficiencies. The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. This inspection constituted one quarterly licensed operator requalification program simulator inspection sample as defined in IP 71111.11.
The inspectors observed licensed operators during simulator training on September 12, conducted partially in response to licensee-identified corrective actions intended to improve overall operating crew performance. The inspectors assessed the operators performance of simulated tasks focusing on alarm response, command and control of crew activities, communication practices, and procedural adherence. The inspectors also observed the operations training staffs post-evaluation critique to assess the ability of the licensees evaluators to identify performance deficiencies. The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements.
 
This inspection constituted one quarterly licensed operator requalification program simulator inspection sample as defined in IP 71111.11.


====b. Findings====
====b. Findings====
Line 133: Line 160:
===.2 Resident Inspector Quarterly Observations During Periods of Heightened Activity or Risk===
===.2 Resident Inspector Quarterly Observations During Periods of Heightened Activity or Risk===


(71111.11Q)
      (71111.11Q)


====a. Inspection Scope====
====a. Inspection Scope====
On August 5 and 6, the inspectors observed licensed operators in the control room perform power maneuvers for a rod pattern adjustment, main steam valve testing, and turbine stop valve testing. Then, on August 18, the inspectors observed licensed 8 operators in the control room perform turbine low pressure stop and intercept valve testing. These activities required heightened awareness, additional detailed planning, and involved increased operational risk. The in spectors evaluated the following areas:
On August 5 and 6, the inspectors observed licensed operators in the control room perform power maneuvers for a rod pattern adjustment, main steam valve testing, and turbine stop valve testing. Then, on August 18, the inspectors observed licensed operators in the control room perform turbine low pressure stop and intercept valve testing. These activities required heightened awareness, additional detailed planning, and involved increased operational risk. The inspectors evaluated the following areas:
* licensed operator performance;
* licensed operator performance;
* crew's clarity and formality of communications;
* crews clarity and formality of communications;
* ability to take timely actions in the conservative direction;
* ability to take timely actions in the conservative direction;
* prioritization, interpretation, and verification of annunciator alarms;
* prioritization, interpretation, and verification of annunciator alarms;
Line 144: Line 171:
* control board (or equipment) manipulations;
* control board (or equipment) manipulations;
* oversight and direction from supervisors; and
* oversight and direction from supervisors; and
* ability to identify and implement appropriate TS actions. The performance in these areas was compared to pre-established operator action expectations, procedural compliance, and task completion requirements. In addition, the inspectors verified problems related to licensed operator performance were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted one quarterly licensed operator heightened activity/risk inspection sample as defined in IP 71111.11.
* ability to identify and implement appropriate TS actions.
 
The performance in these areas was compared to pre-established operator action expectations, procedural compliance, and task completion requirements.
 
In addition, the inspectors verified problems related to licensed operator performance were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted one quarterly licensed operator heightened activity/risk inspection sample as defined in IP 71111.11.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}
Line 160: Line 192:
* CARD 17-21106; Review Reactor Pressure System (RPS) for Maintenance Rule (a)(1) Classification.
* CARD 17-21106; Review Reactor Pressure System (RPS) for Maintenance Rule (a)(1) Classification.


9 The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the SSCs. Specifically, the inspectors independently verified the licensee's handling of SSC performance or condition problems in terms of:
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the SSCs. Specifically, the inspectors independently verified the licensee's handling of SSC performance or condition problems in terms of:
* appropriate work practices;
* appropriate work practices;
* identifying and addressing common cause failures;
* identifying and addressing common cause failures;
Line 168: Line 200:
* trending key parameters (condition monitoring);
* trending key parameters (condition monitoring);
* 10 CFR 50.65(a)(1) or (a)(2) classification and reclassification; and
* 10 CFR 50.65(a)(1) or (a)(2) classification and reclassification; and
* appropriateness of performance criteria for SSC functions classified (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSC functions classified (a)(1). In addition, the inspectors verified problems associated with the effectiveness of plant maintenance for risk-significant SSCs were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted four quarterly maintenance effectiveness inspection samples as defined in IP 71111.12.
* appropriateness of performance criteria for SSC functions classified (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSC functions classified (a)(1).
 
In addition, the inspectors verified problems associated with the effectiveness of plant maintenance for risk-significant SSCs were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted four quarterly maintenance effectiveness inspection samples as defined in IP 71111.12.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R13}}
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
Line 182: Line 217:
* Planned maintenance during the week of August 7-11 including the EDG 12 safety system outage;
* Planned maintenance during the week of August 7-11 including the EDG 12 safety system outage;
* Planned maintenance during the week of August 21-25 including the HPCI safety system outage;
* Planned maintenance during the week of August 21-25 including the HPCI safety system outage;
* Emergent maintenance on Division 1 Standby Gas flow high out of specification; 10
* Emergent maintenance on Division 1 Standby Gas flow high out of specification;
* Planned maintenance during the week of September 18-22 including Division 2 CCHVAC; and
* Planned maintenance during the week of September 18-22 including Division 2 CCHVAC; and
* Emergent maintenance on Division 1 service water pump room ventilation dampers and planned maintenance during the week of September 25-29 including the turbine building closed cooling water west heat exchanger replacement. These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each of the above activities, the inspectors reviewed the scope of maintenance work in the plant's daily schedule, reviewed control room logs, verified plant risk assessments were completed as required by 10 CFR 50.65(a)(4) prior to commencing maintenance activities, discussed the results of the assessment with the licensee's probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were consistent with the risk assessment assumptions. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid, redundant safety-related plant equipment necessary to minimize risk was available for use, and applicable requirements were met. In addition, the inspectors verified maintenance risk-related problems were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted seven maintenance risk assessment and emergent work control inspection samples as defined in IP 71111.13.
* Emergent maintenance on Division 1 service water pump room ventilation dampers and planned maintenance during the week of September 25-29 including the turbine building closed cooling water west heat exchanger replacement.
 
These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each of the above activities, the inspectors reviewed the scope of maintenance work in the plants daily schedule, reviewed control room logs, verified plant risk assessments were completed as required by 10 CFR 50.65(a)(4) prior to commencing maintenance activities, discussed the results of the assessment with the licensees probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were consistent with the risk assessment assumptions. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid, redundant safety-related plant equipment necessary to minimize risk was available for use, and applicable requirements were met.
 
In addition, the inspectors verified maintenance risk-related problems were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted seven maintenance risk assessment and emergent work control inspection samples as defined in IP 71111.13.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R15}}
{{a|1R15}}
==1R15 Operability Determinations and Functionality Assessments==
==1R15 Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}
Line 199: Line 239:
* CARD 17-00767; Diesel Fire Pump Failed to Start;
* CARD 17-00767; Diesel Fire Pump Failed to Start;
* CARD 17-26749; NRC Question Operability of EDG Switchgear with No Ventilation Available; and
* CARD 17-26749; NRC Question Operability of EDG Switchgear with No Ventilation Available; and
* CARD 17-27936; RHR Division 1 Pump Room Dampers Indicating Closed. The inspectors selected these potential operability/functionality issues based on the safety significance of the associated components and systems. The inspectors verified the conditions did not render the associated equipment inoperable/non-functional or result in an unrecognized increase in plant risk. When applicable, the inspectors verified the licensee appropriately applied TS limitations, appropriately returned the affected 11 equipment to an operable or functional status, and reviewed the licensee's evaluation of the issue with respect to the regulatory reporting requirements. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. When applicable, the inspectors also verified the licensee appropriately assessed the functionality of SSCs that perform specified functions described in the UFSAR, Technical Requirements Manual, Emergency Plan, Fire Protection Plan, regulatory commitments, or other elements of the current licensing basis when degraded and/or nonconforming conditions were identified. In addition, the inspectors verified problems associated with the operability or functionality of safety-related and risk-significant plant equipment were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted six operability determination and functionality assessment inspection samples as defined in IP 71111.15.
* CARD 17-27936; RHR Division 1 Pump Room Dampers Indicating Closed.
 
The inspectors selected these potential operability/functionality issues based on the safety significance of the associated components and systems. The inspectors verified the conditions did not render the associated equipment inoperable/non-functional or result in an unrecognized increase in plant risk. When applicable, the inspectors verified the licensee appropriately applied TS limitations, appropriately returned the affected equipment to an operable or functional status, and reviewed the licensees evaluation of the issue with respect to the regulatory reporting requirements. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. When applicable, the inspectors also verified the licensee appropriately assessed the functionality of SSCs that perform specified functions described in the UFSAR, Technical Requirements Manual, Emergency Plan, Fire Protection Plan, regulatory commitments, or other elements of the current licensing basis when degraded and/or nonconforming conditions were identified.
 
In addition, the inspectors verified problems associated with the operability or functionality of safety-related and risk-significant plant equipment were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted six operability determination and functionality assessment inspection samples as defined in IP 71111.15.


====b. Findings====
====b. Findings====
: (1) Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations
: (1) Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment     Isolation Valve Actuations


=====Introduction:=====
=====Introduction:=====
The inspectors identified a Severity Level IV Non-Cited Violation of the NRC's reporting requirements in 10 CFR 50.73(a
The inspectors identified a Severity Level IV Non-Cited Violation of the NRCs reporting requirements in 10 CFR 50.73(a)(1), Licensee Event Report System.
)(1), "Licensee Event Report System.The licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery on March 24, 2017, of a condition that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system.
 
The licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery on March 24, 2017, of a condition that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system.


=====Description:=====
=====Description:=====
While performing testing during the refueling outage on March 24 with the unit in Mode 5 (refueling), an electrical perturbation occurred when synchronizing EDG 12 with offsite power. The electrical perturbation caused a loss of RPS channel A power  
While performing testing during the refueling outage on March 24 with the unit in Mode 5 (refueling), an electrical perturbation occurred when synchronizing EDG 12 with offsite power. The electrical perturbation caused a loss of RPS channel A power and a loss of power to nuclear steam supply shutoff system (NSSSS) channels A and C.


and a loss of power to nuclear steam supply shutoff system (NSSSS) channels A and C. Several equipment/component actuations occurred including an RPS A half-scram, Division 1 NSSSSs actuation; auto start of the Division 1 standby gas treatment subsystem; trip of the reactor building heating, ventilation, and air conditioning system; and isolation of drywell pneumatics. CARD 17-22500 was written to evaluate the event.
Several equipment/component actuations occurred including an RPS A half-scram, Division 1 NSSSSs actuation; auto start of the Division 1 standby gas treatment subsystem; trip of the reactor building heating, ventilation, and air conditioning system; and isolation of drywell pneumatics. CARD 17-22500 was written to evaluate the event.


The licensee determined the bus tie breaker was apparently closed with the EDG slightly out-of-phase with offsite power, which caused an electrical voltage and current transient.
The licensee determined the bus tie breaker was apparently closed with the EDG slightly out-of-phase with offsite power, which caused an electrical voltage and current transient.


The licensee correctly concluded none of the equipment/component actuations met the reporting requirements in 10 CFR 50.72, "Immediate Notification Requirements for Operating Nuclear Power Reactors;" however , it did not subsequently review the event with respect to the 10 CFR 50.73 reporting requirements.
The licensee correctly concluded none of the equipment/component actuations met the reporting requirements in 10 CFR 50.72, Immediate Notification Requirements for Operating Nuclear Power Reactors; however, it did not subsequently review the event with respect to the 10 CFR 50.73 reporting requirements.


The inspectors reviewed the licensee's initial evaluation of the event and raised questions with the licensee to better understand which primary containment isolation valves actuated as a result of the Division 1 NSSSS actuation and whether the reporting requirements in 10 CFR 50.73 were satisfied since it appeared containment isolation valves in more than one system received isolation signals. The inspectors reviewed the control room logs and noted that in addition to the drywell pneumatics valves, the drywell 12 floor and equipment drain valves also isolated. Although the containment isolation was not required due to the actual plant conditions, the invalid actuation of containment valves in more than one system would be reportable under 10 CFR 50.73(a)(2)(iv)(A). In response to the inspectors' questions, the licensee initiated CARD 17-25005, "10 CFR 50.73 Reportability Review of CARD 17-22500 Not Documented Within 60 Days," and completed an evaluation of the event with respect to the 10 CFR 50.73 reporting requirements. The licensee determined this event should have been reported since Division 1 primary containment isolation valves actuated (closed) in three systems (drywell pneumatics, drywell floor and equipment drains, and torus water management). The licensee made a telephone notification on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).
The inspectors reviewed the licensees initial evaluation of the event and raised questions with the licensee to better understand which primary containment isolation valves actuated as a result of the Division 1 NSSSS actuation and whether the reporting requirements in 10 CFR 50.73 were satisfied since it appeared containment isolation valves in more than one system received isolation signals. The inspectors reviewed the control room logs and noted that in addition to the drywell pneumatics valves, the drywell floor and equipment drain valves also isolated. Although the containment isolation was not required due to the actual plant conditions, the invalid actuation of containment valves in more than one system would be reportable under 10 CFR 50.73(a)(2)(iv)(A).
 
In response to the inspectors questions, the licensee initiated CARD 17-25005, 10 CFR 50.73 Reportability Review of CARD 17-22500 Not Documented Within 60 Days, and completed an evaluation of the event with respect to the 10 CFR 50.73 reporting requirements. The licensee determined this event should have been reported since Division 1 primary containment isolation valves actuated (closed) in three systems (drywell pneumatics, drywell floor and equipment drains, and torus water management). The licensee made a telephone notification on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).


=====Analysis:=====
=====Analysis:=====
The inspectors determined the licensee's failure to report the invalid primary containment isolation valve actuations in accordance with the requirements in 10 CFR 50.73 was a licensee performance deficiency warranting a significance evaluation. Consistent with the guidance in IMC 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening," dated September 7, 2012, the inspectors determined the performance deficiency was not a finding of more than minor significance based on "No" answers to the more-than-minor screening questions. The inspectors also reviewed the examples of minor issues in IMC 0612, Appendix E, "Examples of Minor Issues," dated August 11, 2009, and found no examples related to this issue. Violations of 10 CFR 50.73 are dispositioned using the traditional enforcement process because they are considered to be violations that potentially impede or impact the regulatory process. This violation was also associated with a performance deficiency that has been evaluated as having minor safety significance by the significance determination process (SDP). The SDP, however, does not specifically consider regulatory process impact. Thus, although related to a common regulatory concern, it is necessary to address the violation and performance deficiency using different processes to correctly reflect both the regulatory importance of the violation and the safety significance of the associated performance deficiency. In accordance with Section 6.9.d.9 of the NRC Enforcement Policy, this violation was categorized as Severity Level IV because the licensee failed to make a report to the NRC as required by 10 CFR 50.73(a)(1). No cross-cutting aspect is associated with this traditional enforcement violation because the associated performance deficiency was determined to be of minor safety significance and therefore not a finding.
The inspectors determined the licensees failure to report the invalid primary containment isolation valve actuations in accordance with the requirements in 10 CFR 50.73 was a licensee performance deficiency warranting a significance evaluation. Consistent with the guidance in IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated September 7, 2012, the inspectors determined the performance deficiency was not a finding of more than minor significance based on No answers to the more-than-minor screening questions. The inspectors also reviewed the examples of minor issues in IMC 0612, Appendix E, Examples of Minor Issues, dated August 11, 2009, and found no examples related to this issue.
 
Violations of 10 CFR 50.73 are dispositioned using the traditional enforcement process because they are considered to be violations that potentially impede or impact the regulatory process. This violation was also associated with a performance deficiency that has been evaluated as having minor safety significance by the significance determination process (SDP). The SDP, however, does not specifically consider regulatory process impact. Thus, although related to a common regulatory concern, it is necessary to address the violation and performance deficiency using different processes to correctly reflect both the regulatory importance of the violation and the safety significance of the associated performance deficiency. In accordance with Section 6.9.d.9 of the NRC Enforcement Policy, this violation was categorized as Severity Level IV because the licensee failed to make a report to the NRC as required by 10 CFR 50.73(a)(1).
 
No cross-cutting aspect is associated with this traditional enforcement violation because the associated performance deficiency was determined to be of minor safety significance and therefore not a finding.


=====Enforcement:=====
=====Enforcement:=====
Title 10 CFR 50.73(a)(1) requires, in part, that the licensee submit an LER for any event of the type described in this paragraph within 60 days after the discovery of the event. Title 10 CFR 50.73(a)(2)(iv)(A) requires, in part, that the licensee report any event or condition that resulted in manual or automatic actuation of any of the systems listed in Paragraph (a)(2)(iv)(B). Title 10 CFR 50.73(a)(2)(iv)(B)(2) lists general containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves. Contrary to the above, the licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery of a condition on March 24, 2017, that resulted in the invalid actuation of containment isolation signals affecting 13 containment isolation valves in more than one system as required by 10 CFR 50.73(a)(2)(iv)(A). The condition involved the invalid automatic actuation of the primary containment isolation logic for Groups 12, 13, and 18 primary containment isolation valves on March 24, 2017. In accordance with Section 6.9.d.9 of the Enforcement Policy, this violation was classified as a Severity Level IV Violation. Because this violation was not repetitive or willful, and was entered into the licensee's corrective action program, it is being treated as a Non-Cited Violation consistent with Section 2.3.2.a of the NRC Enforcement Policy. (NCV 05000341/2017003-01, Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations) The licensee entered this issue into its corrective action program (CARD 17-25005) to evaluate the cause for its failure to satisfy the reporting requirements and to identify appropriate corrective actions. Subsequently, the licensee made a notification call on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).
Title 10 CFR 50.73(a)(1) requires, in part, that the licensee submit an LER for any event of the type described in this paragraph within 60 days after the discovery of the event. Title 10 CFR 50.73(a)(2)(iv)(A) requires, in part, that the licensee report any event or condition that resulted in manual or automatic actuation of any of the systems listed in Paragraph (a)(2)(iv)(B). Title 10 CFR 50.73(a)(2)(iv)(B)(2) lists general containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves.
: (2) Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service  The inspectors identified a non-cited violation (NCV) of TS 3.8.7 "Distribution Systems - Operating," for the licensee's failure to restore inoperable Division 1 and Division 2 AC electrical power distribution subsystems to operable status within 8 hours, or be in Mode 3 in 12 hours. Specifically, on multiple occasions, electrical power distribution subsystems required by the above limiting condition for operation were inoperable due to their respective subdivisions of RHR switchgear room ventilation systems being out of service and therefore unavailable to provide the technical specification support function of attendant cooling that is needed for the associated electrical systems to perform their


specified safety functions. The RHR switchgear room ventilation systems are required by the licensee's Updated Final Safety Analysis Report to be operable when the safety-related equipment in the associated room is required to be operable.
Contrary to the above, the licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery of a condition on March 24, 2017, that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system as required by 10 CFR 50.73(a)(2)(iv)(A). The condition involved the invalid automatic actuation of the primary containment isolation logic for Groups 12, 13, and 18 primary containment isolation valves on March 24, 2017.
 
In accordance with Section 6.9.d.9 of the Enforcement Policy, this violation was classified as a Severity Level IV Violation. Because this violation was not repetitive or willful, and was entered into the licensees corrective action program, it is being treated as a Non-Cited Violation consistent with Section 2.3.2.a of the NRC Enforcement Policy.
 
    (NCV 05000341/2017003-01, Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations)
The licensee entered this issue into its corrective action program (CARD 17-25005) to evaluate the cause for its failure to satisfy the reporting requirements and to identify appropriate corrective actions. Subsequently, the licensee made a notification call on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).
: (2) Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service The inspectors identified a non-cited violation (NCV) of TS 3.8.7 Distribution Systems -
Operating, for the licensees failure to restore inoperable Division 1 and Division 2 AC electrical power distribution subsystems to operable status within 8 hours, or be in Mode 3 in 12 hours. Specifically, on multiple occasions, electrical power distribution subsystems required by the above limiting condition for operation were inoperable due to their respective subdivisions of RHR switchgear room ventilation systems being out of service and therefore unavailable to provide the technical specification support function of attendant cooling that is needed for the associated electrical systems to perform their specified safety functions. The RHR switchgear room ventilation systems are required by the licensees Updated Final Safety Analysis Report to be operable when the safety-related equipment in the associated room is required to be operable.


=====Description:=====
=====Description:=====
The licensee's Updated Final Safety Analysis Report, in Section 3.11.4.4, "Residual Heat Removal Complex Safety-Related Ventilation Systems," states, in part, to maintain conditions below the limits specified in Table 3.11-4, each diesel generator  
The licensees Updated Final Safety Analysis Report, in Section 3.11.4.4, Residual Heat Removal Complex Safety-Related Ventilation Systems, states, in part, to maintain conditions below the limits specified in Table 3.11-4, each diesel generator room, switchgear room, and pump room is ventilated with two 50 percent-capacity supply air fans. They are not required unless the equipment served is required, and are designed to start when the associated diesel generator starts, or a preset high room temperature is reached. The switchgear in the RHR switchgear rooms are required to be operable in Modes 1, 2, and 3, as described in TS 3.8.7. On August 10, 2017, the inspectors questioned the licensee on the operability of RHR switchgear when the ventilation supply fans were out of service. The licensed operators stated that Precaution and Limitation 3.2 of station technical and operating procedure 23.420, RHR Complex Heating and Ventilation, Revision 35, allowed RHR Pump Room and Switchgear Room equipment to remain operable without the applicable ventilation system being returned to normal operable status as long as temperatures do not exceed 104 degrees Fahrenheit (F) in the area, or for 24 hours if temperature exceeds 104 degrees F. The procedure referred to design calculation (DC)-4953, RHR Complex Abnormal Operation-Damper Lineups, dated December 20, 2002, which was incorporated into procedure 23.420 on January 26, 2003.
 
The purpose of the design calculation states, in part, that it is to determine acceptable damper configurations based upon outside air temperature to maintain RHR complex design temperatures. The purpose further states, in part, that the results of the calculation should only be utilized in the event the motor operated dampers are unable to perform their design function and a spare operator is not readily available.


room, switchgear room, and pump room is ventilated with two 50 percent-capacity supply air fans. They are not required unless the equipment served is required, and are designed to start when the associated diesel generator starts, or a preset high room temperature is reached. The switchgear in the RHR switchgear rooms are required to be operable in Modes 1, 2, and 3, as described in TS 3.8.7. On August 10, 2017, the inspectors questioned the licensee on the operability of RHR switchgear when the ventilation supply fans were out of service. The licensed operators stated that Precaution and Limitation 3.2 of station technical and operating procedure 23.420, "RHR Complex Heating and Ventilation," Revision 35, allowed RHR Pump Room and Switchgear Room equipment to remain operable without the applicable ventilation system being returned to normal operable status as long as temperatures do not exceed 104 degrees Fahrenheit (F) in the area, or for 24 hours if temperature exceeds 104 degrees F. The procedure referred to design calculation (DC)-4953, "RHR Complex Abnormal Operation-Damper Lineups," dated December 20, 2002, which was incorporated into procedure 23.420 on January 26, 2003.
The licensee documented the issue in its corrective action program as CARD 17-26749 and took interim actions using Nuclear Generation Memo NPOP-17-0067 to outline department guidance to not use the guidance of DC-4953 until an engineering technical evaluation was completed. The subsequent technical evaluation concluded that that the condition where both ventilation supply fans were out of service does not support operability of the AC distribution systems (i.e., 4160 kV and 480 V buses) in the RHR switchgear rooms. Additional licensee corrective actions planned include, but are not limited to, modification of procedure 23.420, RHR Complex Heating and Ventilation, to reflect the technical evaluation results.


14 The purpose of the design calculation states, in part, that it is to determine acceptable damper configurations based upon outside air temperature to maintain RHR complex design temperatures. The purpose further states, in part, that the results of the calculation should only be utilized in the event the motor operated dampers are unable to perform their design function and a spare operator is not readily available. The licensee documented the issue in its corrective action program as CARD 17-26749 and took interim actions using Nuclear Generation Memo NPOP-17-0067 to outline department guidance to not use the guidance of DC-4953 until an engineering technical evaluation was completed. The subsequent technical evaluation concluded that that the condition where both ventilation supply fans were out of service does not support operability of the AC distribution systems (i.e., 4160 kV and 480 V buses) in the RHR switchgear rooms. Additional licensee corrective actions planned include, but are not limited to, modification of procedure 23.420, "RHR Complex Heating and Ventilation," to reflect the technical evaluation results. Based on the licensee's evaluation and a review of operating history since the procedure change in 2003, the inspectors concluded that on numerous occasions, between September 10, 2014, and August 9, 2017, the requirements of TS 3.8.7 were not met for the RHR switchgear room ventilation systems.
Based on the licensees evaluation and a review of operating history since the procedure change in 2003, the inspectors concluded that on numerous occasions, between September 10, 2014, and August 9, 2017, the requirements of TS 3.8.7 were not met for the RHR switchgear room ventilation systems.


=====Analysis:=====
=====Analysis:=====
The inspectors determined that the licensee's failure to comply with TS 3.8.7 by either restoring inoperable electrical power subsystems to operable status within 8 hours, or be in Mode 3 in 12 hours was a per formance deficiency. Specifically, the inspectors identified numerous occasions, between September 10, 2014, and August 9, 2017, where safety-related RHR switchgear ventilation systems were removed from service without restoring these systems within 8 hours or taking action to place the unit in Mode 3 within 12 hours. The performance deficiency was determined to be more-than-minor because it was associated with the Configuration Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. In accordance with IMC 0609, Attachment 4, "Initial Characterization of Findings," issued October 7, 2016, and Exhibit 2 of IMC 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," issued June 19, 2012, the inspectors determined that this finding was of very low safety significance (Green) because it did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time, or two separate safety systems out-of-service for greater than its technical specification allowed outage time. That answer was based on reference material in the recent technical evaluation that showed that without the RHR switchgear room ventilation in operation for the probabilistic risk analysis mission time of 24-hours, the switchgear inside the room would still be able to perform its safety function. The inspectors determined that the violation had a cross-cutting aspect in the area of human performance, resources, because the licensee failed to ensure that the RHR Complex Heating and Ventilation procedure was adequate to support nuclear safety. H(1)
The inspectors determined that the licensees failure to comply with TS 3.8.7 by either restoring inoperable electrical power subsystems to operable status within 8 hours, or be in Mode 3 in 12 hours was a performance deficiency. Specifically, the inspectors identified numerous occasions, between September 10, 2014, and August 9, 2017, where safety-related RHR switchgear ventilation systems were removed from service without restoring these systems within 8 hours or taking action to place the unit in Mode 3 within 12 hours.
 
The performance deficiency was determined to be more-than-minor because it was associated with the Configuration Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
 
In accordance with IMC 0609, Attachment 4, Initial Characterization of Findings, issued October 7, 2016, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012, the inspectors determined that this finding was of very low safety significance (Green)because it did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time, or two separate safety systems out-of-service for greater than its technical specification allowed outage time. That answer was based on reference material in the recent technical evaluation that showed that without the RHR switchgear room ventilation in operation for the probabilistic risk analysis mission time of 24-hours, the switchgear inside the room would still be able to perform its safety function. The inspectors determined that the violation had a cross-cutting aspect in the area of human performance, resources, because the licensee failed to ensure that the RHR Complex Heating and Ventilation procedure was adequate to support nuclear safety. H(1)


=====Enforcement:=====
=====Enforcement:=====
Technical Specification (TS) 3.8.7, "Distribution Systems - Operating," requires, in part, that Division 1 and Division 2 AC and DC electrical power distribution 15 subsystems shall be operable in Modes 1, 2 and 3. Technical Specification 3.8.7 requires that if one or more required AC electrical power distribution subsystems is inoperable for more than 8 hours, action must be taken to place the unit in Mode 3 within 12 hours. Contrary to the above, on numerous occasions between September 10, 2014, and August 9, 2017, the licensee removed safety-related RHR switchgear ventilation systems from service without restoring these systems within 8 hours or taking action to place the unit in Mode 3 within 12 hours. Because the violation was of very low safety significance and was entered into the licensee's CAP, this violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement policy. (NCV 05000341/2017003-02, Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service)
Technical Specification (TS) 3.8.7, Distribution Systems - Operating, requires, in part, that Division 1 and Division 2 AC and DC electrical power distribution subsystems shall be operable in Modes 1, 2 and 3. Technical Specification 3.8.7 requires that if one or more required AC electrical power distribution subsystems is inoperable for more than 8 hours, action must be taken to place the unit in Mode 3 within 12 hours. Contrary to the above, on numerous occasions between September 10, 2014, and August 9, 2017, the licensee removed safety-related RHR switchgear ventilation systems from service without restoring these systems within 8 hours or taking action to place the unit in Mode 3 within 12 hours. Because the violation was of very low safety significance and was entered into the licensee's CAP, this violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement policy. (NCV 05000341/2017003-02, Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service)
{{a|1R19}}
{{a|1R19}}
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
Line 249: Line 314:
* HPCI Safety System Outage - Final Post Maintenance Test;
* HPCI Safety System Outage - Final Post Maintenance Test;
* WO 45095048; Inspect/Lube Blower and Motor, Replace Belts for CCHVAC Control Room North Division 1 Multizone Air Supply Unit; and
* WO 45095048; Inspect/Lube Blower and Motor, Replace Belts for CCHVAC Control Room North Division 1 Multizone Air Supply Unit; and
* WO 48734267; Troubleshoot/Repair of EDG 13 Output Breaker Tripping. The inspectors reviewed the scope of the work performed and evaluated the adequacy of the specified post-maintenance testing. The inspectors verified the post-maintenance testing was performed in accordance with approved procedures, the procedures contained clear acceptance criteria that demonstrated operational readiness and the acceptance criteria were met, appropriate test instrumentation was used, the equipment was returned to its operational status following testing, and the test documentation was properly evaluated. In addition, the inspectors verified problems associated with post-maintenance testing activities were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted four post-maintenance testing inspection samples as defined in IP 71111.19.
* WO 48734267; Troubleshoot/Repair of EDG 13 Output Breaker Tripping.
 
The inspectors reviewed the scope of the work performed and evaluated the adequacy of the specified post-maintenance testing. The inspectors verified the post-maintenance testing was performed in accordance with approved procedures, the procedures contained clear acceptance criteria that demonstrated operational readiness and the acceptance criteria were met, appropriate test instrumentation was used, the equipment was returned to its operational status following testing, and the test documentation was properly evaluated.
 
In addition, the inspectors verified problems associated with post-maintenance testing activities were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.
 
This inspection constituted four post-maintenance testing inspection samples as defined in IP 71111.19.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R22}}
 
{{a|1R22}}
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}
Line 261: Line 330:
The inspectors reviewed surveillance testing results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety functions and to verify testing was conducted in accordance with applicable procedural and TS requirements:
The inspectors reviewed surveillance testing results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety functions and to verify testing was conducted in accordance with applicable procedural and TS requirements:
* 24.204.01; Division 1 Low Pressure Coolant Injection and Suppression Pool Cooling/Spray Pump and Valve Operability Test;
* 24.204.01; Division 1 Low Pressure Coolant Injection and Suppression Pool Cooling/Spray Pump and Valve Operability Test;
* 24.307.16; Emergency Diesel Generator 13-Start and Load Test;
* 24.307.16; Emergency Diesel Generator 13Start and Load Test;
* 27.109.01; Turbine Steam Valves Test; and
* 27.109.01; Turbine Steam Valves Test; and
* 44.030.155; Emergency Core Cooling System - HPCI Torus Level Functional Test. The inspectors observed selected portions of the test activities to verify the testing was accomplished in accordance with plant procedures. The inspectors reviewed the test methodology and documentation to verify equipment performance was consistent with safety analysis and design basis assumptions, test equipment was used within the required range and accuracy, applicable prerequisites described in the test procedures were satisfied, test frequencies met TS requirements to demonstrate operability and reliability, and appropriate testing acceptance criteria were satisfied. When applicable, the inspectors also verified test results not meeting acceptance criteria were addressed  
* 44.030.155; Emergency Core Cooling System - HPCI Torus Level Functional Test.
 
The inspectors observed selected portions of the test activities to verify the testing was accomplished in accordance with plant procedures. The inspectors reviewed the test methodology and documentation to verify equipment performance was consistent with safety analysis and design basis assumptions, test equipment was used within the required range and accuracy, applicable prerequisites described in the test procedures were satisfied, test frequencies met TS requirements to demonstrate operability and reliability, and appropriate testing acceptance criteria were satisfied. When applicable, the inspectors also verified test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable.
 
In addition, the inspectors verified problems associated with surveillance testing activities were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.


with an adequate operability evaluation or the system or component was declared inoperable. In addition, the inspectors verified problems associated with surveillance testing activities were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled. This inspection constituted one in-service test and three routine surveillance tests, for a total of four surveillance testing inspection samples as defined in IP 71111.22.
This inspection constituted one in-service test and three routine surveillance tests, for a total of four surveillance testing inspection samples as defined in IP 71111.22.


====b. Findings====
====b. Findings====
Line 271: Line 344:


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
===.1 Mitigating Systems Performance Index-Heat Removal System===
===.1 Mitigating Systems Performance IndexHeat Removal System===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed a sample of plant records and data against the reported Mitigating Systems Performance Index (MSPI) Heat Removal System Performance 17 Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in Nuclear Energy
The inspectors reviewed a sample of plant records and data against the reported Mitigating Systems Performance Index (MSPI) Heat Removal System Performance Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, LERs, and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator.


Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, LERs, and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator. This inspection constituted one MSPI-Heat Removal System Performance Indicator verification inspection sample as defined in Inspection Procedure (IP) 71151.
This inspection constituted one MSPIHeat Removal System Performance Indicator verification inspection sample as defined in Inspection Procedure (IP) 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 Mitigating Systems Performance Index-Residual Heat Removal System===
===.2 Mitigating Systems Performance IndexResidual Heat Removal System===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed a sample of plant records and data against the reported MSPI- Residual Heat Removal System (RHR) Systems Performance Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, Licensee Event Reports (LERs), and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator. This inspection constituted one MSPI-RHR Syst ems Performance Indicator verification inspection sample as defined in IP 71151.
The inspectors reviewed a sample of plant records and data against the reported MSPI Residual Heat Removal System (RHR) Systems Performance Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, Licensee Event Reports (LERs), and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator.
 
This inspection constituted one MSPIRHR Systems Performance Indicator verification inspection sample as defined in IP 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.3 Mitigating Systems Performance Index-Cooling Water Systems===
===.3 Mitigating Systems Performance IndexCooling Water Systems===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed a sample of plant records and data against the reported MSPI Cooling Water Systems Performance Indicator. To determine the accuracy of the 18 performance indicator data reported, performance indicator definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline,"
The inspectors reviewed a sample of plant records and data against the reported MSPI Cooling Water Systems Performance Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, LERs, and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator.
Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, LERs, and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator. This inspection constituted one MSPI Cooling Water Systems Performance Indicator verification inspection sample as defined in IP 71151.
 
This inspection constituted one MSPI Cooling Water Systems Performance Indicator verification inspection sample as defined in IP 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|4OA2}}
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
Line 307: Line 382:


====a. Inspection Scope====
====a. Inspection Scope====
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensee's corrective action program at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Some minor issues were entered into the licensee's corrective action program as a result of the inspectors' observations; however, they are not discussed in this report. This inspection was not considered to be an inspection sample as defined in IP 71152.
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensees corrective action program at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Some minor issues were entered into the licensees corrective action program as a result of the inspectors observations; however, they are not discussed in this report.
 
This inspection was not considered to be an inspection sample as defined in IP 71152.


====b. Findings====
====b. Findings====
Line 316: Line 393:
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected the following issues for in-depth review:
The inspectors selected the following issues for in-depth review:
* CARD 13-24841; EDG Steady State Voltage and Frequency Technical Specification Ranges. As appropriate, the inspectors verified the following attributes during their review of the licensee's corrective actions for the above CARD and other related CARDs:
* CARD 13-24841; EDG Steady State Voltage and Frequency Technical Specification Ranges.
* complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery; 19
 
As appropriate, the inspectors verified the following attributes during their review of the licensee's corrective actions for the above CARD and other related CARDs:
* complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery;
* consideration of the extent of condition, generic implications, common cause, and previous occurrences;
* consideration of the extent of condition, generic implications, common cause, and previous occurrences;
* evaluation and disposition of operability/functionality/reportability issues;
* evaluation and disposition of operability/functionality/reportability issues;
* classification and prioritization of the resolution of the problem commensurate with safety significance;
* classification and prioritization of the resolution of the problem commensurate with safety significance;
* identification of the root and contributing causes of the problem; and
* identification of the root and contributing causes of the problem; and
* identification of corrective actions, which were appropriately focused to correct the problem. The inspectors discussed the corrective actions and associated evaluations with licensee personnel. This inspection constituted one annual in-depth review inspection samples as defined in IP 71152.
* identification of corrective actions, which were appropriately focused to correct the problem.
 
The inspectors discussed the corrective actions and associated evaluations with licensee personnel.
 
This inspection constituted one annual in-depth review inspection samples as defined in IP 71152.


====b. Findings====
====b. Findings====
Line 330: Line 413:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a review of the licensee's corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors' review was focused on component mispositionings, but also considered the results of daily inspector corrective action program item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors' review nominally considered the 6-month period of January 2017 through June 2017, although some examples expanded beyond those dates where the scope of the trend warranted. The review also included issues documented outside the corrective action program in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensee's corrective action program trending reports. Corrective actions associated with a sample of the issues identified in the licensee's trending reports were reviewed for adequacy. This review constituted one semi-annual trend review inspection sample as defined in IP 71152.
The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on component mispositionings, but also considered the results of daily inspector corrective action program item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the 6-month period of January 2017 through June 2017, although some examples expanded beyond those dates where the scope of the trend warranted.
 
The review also included issues documented outside the corrective action program in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees corrective action program trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.
 
This review constituted one semi-annual trend review inspection sample as defined in IP 71152.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|4OA3}}
 
{{a|4OA3}}
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
{{IP sample|IP=IP 71153}}
{{IP sample|IP=IP 71153}}
===.1 Retraction of Event Notification 52724:===
===.1 Retraction of Event Notification 52724: Unanalyzed Condition Combustion Turbine===
Unanalyzed Condition Combustion Turbine Generator 11-1
 
Generator 11-1


====a. Inspection Scope====
====a. Inspection Scope====
On May 2, 2017, the licensee submitted Event Notification 52724, "Unanalyzed Condition CTG 11-1," to the NRC for a condition discovered by the licensee that could not have ensured the applicable Appendix R success criteria under all of the postulated scenarios described in the Updated Final Safety Analysis Report (UFSAR) for Combustion Turbine Generator (CTG) 11-1. From December 21, 2016, until March 18, 2017, when Mode 4 was entered, CTG 11-1 was determined to be in a configuration where it could not be started from the dedicated shutdown panel although it could be started locally. One of the specific scenarios for Appendix R in the UFSAR credits CTG 11-1 to support a safe shutdown based on an assumed time required to start CTG 11-1 and then provide flow to the reactor pressure vessel using the Standby Feedwater System. On May 19, the licensee retracted Event Notification 52724. A time validation study was performed verifying operator actions could have been completed within the time described in the UFSAR for initiating Standby Feedwater flow to the reactor pressure vessel to ensure Appendix R safe shutdown capability under the plant conditions during the relevant time period. The inspectors reviewed the basis for the retraction including the time validation study. The inspectors concurred with the conclusion that operators would have sufficient time  
On May 2, 2017, the licensee submitted Event Notification 52724, Unanalyzed Condition CTG 11-1, to the NRC for a condition discovered by the licensee that could not have ensured the applicable Appendix R success criteria under all of the postulated scenarios described in the Updated Final Safety Analysis Report (UFSAR) for Combustion Turbine Generator (CTG) 11-1. From December 21, 2016, until March 18, 2017, when Mode 4 was entered, CTG 11-1 was determined to be in a configuration where it could not be started from the dedicated shutdown panel although it could be started locally. One of the specific scenarios for Appendix R in the UFSAR credits CTG 11-1 to support a safe shutdown based on an assumed time required to start CTG 11-1 and then provide flow to the reactor pressure vessel using the Standby Feedwater System.
 
On May 19, the licensee retracted Event Notification 52724. A time validation study was performed verifying operator actions could have been completed within the time described in the UFSAR for initiating Standby Feedwater flow to the reactor pressure vessel to ensure Appendix R safe shutdown capability under the plant conditions during the relevant time period.
 
The inspectors reviewed the basis for the retraction including the time validation study.
 
The inspectors concurred with the conclusion that operators would have sufficient time to manually start CTG 11-1 and initiate the Standby Feedwater System in compliance with the UFSAR and Appendix R requirements.


to manually start CTG 11-1 and initiate the Standby Feedwater System in compliance with the UFSAR and Appendix R requirements. This inspection constituted one event follow-up inspection sample as defined in IP 71153.
This inspection constituted one event follow-up inspection sample as defined in IP 71153.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Management Meetings==
==4OA6 Management Meetings==


===.1 Exit Meeting Summary On October 17, 2017, the inspectors presented the inspection results to Mr. M. Caragher and other members of the licensee staff.===
===.1 Exit Meeting Summary===
The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary. On November 9, 2017, the inspectors presented the results of the finding associated with the "Technical Specification Allowed Outage Time Exceeded for Electrical Power 
 
On October 17, 2017, the inspectors presented the inspection results to Mr. M. Caragher and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.


21 Distribution Systems Due to Auxiliary Equipment Out of Service," (Section 1R15b.2) to Mr. L. Bennett and other members of the licensee staff. The licensee acknowledged the issues presented and confirmed that none of the potential report input was considered  
On November 9, 2017, the inspectors presented the results of the finding associated with the Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service, (Section 1R15b.2) to Mr. L. Bennett and other members of the licensee staff. The licensee acknowledged the issues presented and confirmed that none of the potential report input was considered proprietary.


proprietary. ATTACHMENT:
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 363: Line 456:


===Licensee Personnel===
===Licensee Personnel===
: [[contact::L. Anderson]], Manager, Radiological Emergency Response Preparedness (incoming)  
: [[contact::L. Anderson]], Manager, Radiological Emergency Response Preparedness (incoming)
: [[contact::N. Avrakotos]], Manager, Radiological Emergency Response Preparedness (outgoing)  
: [[contact::N. Avrakotos]], Manager, Radiological Emergency Response Preparedness (outgoing)
: [[contact::L. Bennett]], Director, Nuclear Operations  
: [[contact::L. Bennett]], Director, Nuclear Operations
: [[contact::R. Breymaier]], Manager, Performance Engineering and Fuels  
: [[contact::R. Breymaier]], Manager, Performance Engineering and Fuels
: [[contact::M. Brooks]], Principal Technical Expert  
: [[contact::M. Brooks]], Principal Technical Expert
: [[contact::M. Caragher]], Executive Director, Nuclear Production  
: [[contact::M. Caragher]], Executive Director, Nuclear Production
: [[contact::W. Colonnello]], Director, Nuclear Project Management  
: [[contact::W. Colonnello]], Director, Nuclear Project Management
: [[contact::K. Dittman]], Acting Manager, Plant Support Engineering  
: [[contact::K. Dittman]], Acting Manager, Plant Support Engineering
: [[contact::D. Domski]], Engineer, Plant Systems Engineering  
: [[contact::D. Domski]], Engineer, Plant Systems Engineering
: [[contact::M. Donigian]], Supervisor, Operations Training  
: [[contact::M. Donigian]], Supervisor, Operations Training
: [[contact::J. Haas]], Supervisor, Licensing  
: [[contact::J. Haas]], Supervisor, Licensing
: [[contact::D. Hemmele]], Superintendent, Nuclear Operations  
: [[contact::D. Hemmele]], Superintendent, Nuclear Operations
: [[contact::E. Kokosky]], Director, Organization Effectiveness  
: [[contact::E. Kokosky]], Director, Organization Effectiveness
: [[contact::R. Laburn]], Manager, Radiation Protection  
: [[contact::R. Laburn]], Manager, Radiation Protection
: [[contact::K. Locke]], General Supervisor - Electrical, Plant Systems Engineering  
: [[contact::K. Locke]], General Supervisor - Electrical, Plant Systems Engineering
: [[contact::S. Maglio]], Manager, Licensing  
: [[contact::S. Maglio]], Manager, Licensing
: [[contact::K. Mann]], Supervisor, Regulatory Compliance  
: [[contact::K. Mann]], Supervisor, Regulatory Compliance
: [[contact::R. Matuszak]], Manager, Plant Systems Engineering  
: [[contact::R. Matuszak]], Manager, Plant Systems Engineering
: [[contact::D. Noetzel]], Director, Nuclear Engineering  
: [[contact::D. Noetzel]], Director, Nuclear Engineering
: [[contact::K. Polson]], Senior Vice President and Chief Nuclear Officer  
: [[contact::K. Polson]], Senior Vice President and Chief Nuclear Officer
: [[contact::W. Raymer]], Director, Nuclear Maintenance  
: [[contact::W. Raymer]], Director, Nuclear Maintenance
: [[contact::B. Rumans]], General Supervisor, Radiation Protection Technical Services  
: [[contact::B. Rumans]], General Supervisor, Radiation Protection Technical Services
: [[contact::P. Southwell]], General Supervisor, Radiation Protection ALARA  
: [[contact::P. Southwell]], General Supervisor, Radiation Protection ALARA
: [[contact::U.S. Nuclear Regulatory Commission B. Dickson. Chief]], Reactor Projects Branch 2
U.S. Nuclear Regulatory Commission
: [[contact::B. Dickson. Chief]], Reactor Projects Branch 2


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==


===Opened===
===Opened===
: 05000341/2017003-01 NCV Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations
: 05000341/2017003-01     NCV   Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations (Section 1R15.b.1)
(Section 1R15.b.1)  
: 05000341/2017003-02     NCV   Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service (1R15.b.2)
: 05000341/2017003-02 NCV Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary
Equipment Out of Service (1R15.b.2)  


===Closed===
===Closed===
: 05000341/2017003-01 NCV Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations
: 05000341/2017003-01     NCV   Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations (Section 1R15.b.1)
(Section 1R15.b.1)  
: 05000341/2017003-02     NCV   Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service (1R15.b.2)
: 05000341/2017003-02 NCV Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary
Equipment Out of Service (1R15.b.2)


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
The following is a partial list of documents reviewed during the inspection.
 
: Inclusion on this list does not imply the NRC inspectors reviewed the documents in their entirety, but rather, selected
}}
}}

Latest revision as of 07:54, 19 December 2019

NRC Integrated Inspection Report 05000341/2017003
ML17318A053
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 11/13/2017
From: Billy Dickson
NRC/RGN-III/DRP/B2
To: Polson K
DTE Energy
References
IR 2017003
Download: ML17318A053 (35)


Text

UNITED STATES ember 13, 2017

SUBJECT:

FERMI POWER PLANT, UNIT 2NRC INTEGRATED INSPECTION REPORT 05000341/2017003

Dear Mr. Polson:

On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Fermi Power Plant, Unit 2 (Fermi 2). On October 17, 2017, the NRC inspectors discussed the results of this inspection with Mr. M. Caragher and other members of your staff. The inspectors documented the results of this inspection in the enclosed inspection report.

Based on the results of this inspection, the NRC has identified two issues, one that was evaluated under the risk significance determination process as having very low safety significance (Green) and one evaluated under the traditional enforcement process as a Severity Level IV violation. Both of these issues involved violations of NRC requirements. Because the licensee initiated condition reports to address these issues, these violations are being treated as Non-Cited Violations (NCVs), consistent with Section 2.3.2 of the Enforcement Policy. These NCVs are described in the subject inspection report.

If you contest the violations or significance of the Non-Cited Violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to: (1) the Regional Administrator, Region III; (2) the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Fermi 2 Power Plant.

In addition, if you disagree with the cross-cutting aspect assignment to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Fermi 2 Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Billy Dickson, Chief Branch 2 Division of Reactor Projects Docket No. 50-341 License No. NPF-43 Enclosure:

Inspection Report 05000341/2017003 cc: Distribution via LISTSERV

SUMMARY

Inspection Report 05000341/2017003; 07/01/2017 - 09/30/2017; Fermi Power Plant, Unit 2;

Operability Determinations and Functionality Assessments.

This report covers a 3-month period of inspection by the resident inspectors. One Green finding, with an associated Non-Cited Violation (NCV) of U.S. Nuclear Regulatory Commission (NRC) regulations, and one Security Level IV NCV of NRC regulations were identified. The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process, dated April 25, 2015. Cross-cutting aspects are determined using IMC 0310, Aspects within the Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, dated July 201

NRC-Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Non-Cited Violation (NCV) of Technical Specification (TS) 3.8.7 Distribution Systems - Operating, for the licensees failure to either restore inoperable Division 1 and Division 2 AC electrical power distribution subsystems to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or be in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Specifically, electrical power distribution subsystems required by the above limiting condition for operation were inoperable due to their respective subdivisions of Residual Heat Removal (RHR) switchgear room ventilation systems being out of service and therefore unavailable to provide the technical specification support function of attendant cooling that was needed for the associated electrical systems to perform their specified safety functions. The licensee entered the issue into its corrective action program as CARD 17-26749.

The failure to comply with TS 3.8.7 by either restoring inoperable electrical power subsystems to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, or be in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the Configuration Control attribute of the Mitigating Systems Cornerstone, and adversely affected the associated cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined that the finding was of very low safety significance (Green) because it did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time, or two separate safety systems out-of-service for greater than its technical specification allowed outage time. The inspectors determined that the violation had a cross-cutting aspect in the area of human performance, resources, because the licensee failed to ensure that the RHR Complex Heating and Ventilation procedure was adequate to support nuclear safety (H.1). (Section 1R15b.2)

Other Findings

Severity Level IV. The inspectors identified a Severity Level IV NCV of the NRCs reporting requirements Title 10 of the Code of Federal Regulations (CFR), Part 50.73(a)(1), Licensee Event Report [LER] System. The licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery on March 24, 2017, of a condition that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system. The licensee entered this issue into its corrective action program to evaluate the cause for its failure to satisfy the reporting requirements and to identify appropriate corrective actions.

Subsequently, the licensee made a telephone notification on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).

Consistent with the guidance in IMC 0612, Power Reactor Inspection Reports,

Appendix B, Issue Screening, dated September 7, 2012, the inspectors determined the performance deficiency was of minor significance based on No answers to the more-than-minor screening questions. In accordance with Section 6.9.d.9 of the NRC Enforcement Policy, this violation was categorized as Severity Level IV because the licensee failed to report as required by 10 CFR 50.73(a)(1). No cross-cutting aspect is associated with this traditional enforcement violation because the associated performance deficiency was determined to be of minor significance and therefore not a finding. (Section 1R15.b.1)

REPORT DETAILS

Summary of Plant Status

Fermi 2 Power Plant was operated at or near 100 percent power during the inspection period with the following exceptions:

  • On August 5, the licensee reduced power to about 80 percent to perform a control rod pattern adjustment and turbine stop and control valve testing. The unit was returned to full power the following day.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with the design basis probable maximum flood. The evaluation included a review to check for deviations from the descriptions provided in the Updated Final Safety Analysis Report (UFSAR) for features intended to mitigate the potential for flooding from external factors. As part of this evaluation, the inspectors checked for obstructions that could prevent draining, checked that the roofs did not contain obvious loose items that could clog drains in the event of heavy precipitation, and determined that barriers required to mitigate the flood were in place and operable. Additionally, the inspectors performed a walkdown of the protected area to identify any modification to the site which would inhibit site drainage during a probable maximum precipitation event or allow water ingress past a barrier. The inspectors also walked down underground bunkers/manholes subject to flooding that contained multiple train or multiple function risk-significant cables. The inspectors also reviewed the abnormal operating procedure for mitigating the design basis flood to ensure it could be implemented as written.

This inspection constituted one external flooding sample as defined in Inspection Procedure (IP) 71111.01.

b. Findings

No findings were identified.

.2 Readiness for Impending Adverse Weather ConditionsThunderstorms and High

Temperatures

a. Inspection Scope

Since thunderstorms and high temperatures were forecasted for the week of September 18-22, the inspectors evaluated the licensees overall preparations and protection for the expected weather conditions focusing on the emergency diesel generators (EDGs) and off-site power switchyards. The inspectors reviewed plant specific design features and implementation of procedures for responding to or mitigating the effects of thunderstorms and high temperature conditions on the operation of plant systems. The inspectors observed housekeeping practices surrounding the switchyards and material condition and operating status of the EDGs in case of a loss of off-site power. The inspectors also discussed potential compensatory measures with plant operators.

In addition, the inspectors verified adverse weather protection problems were entered into the licensees corrective action program with the appropriate characterization and significance. Selected Condition Assessment Resolution Documents (CARDs) were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted one readiness for impending adverse weather condition inspection sample as defined in IP 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • Division 2 EDGs during planned maintenance on EDG 12; and

The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones. The inspectors reviewed operating procedures, system diagrams, technical specification (TS) requirements, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and were available. The inspectors observed operating parameters and examined the material condition of the equipment to verify there were no obvious deficiencies.

In addition, the inspectors verified problems associated with plant equipment alignment were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted three partial system walkdown inspection samples as defined in IP 71111.04.

b. Findings

No findings were identified.

.2 Semi-Annual Complete System Walkdown

a. Inspection Scope

From August 28 through September 16, the inspectors performed a complete system alignment inspection of the Control Center Heating, Ventilation, and Air Conditioning (CCHVAC) system to verify the functional capability of the system. This system was selected because it was considered risk significant from an initiating events perspective. The inspectors walked down the system to review mechanical and electrical equipment lineups; electrical power availability; system pressure and temperature indications, as appropriate; component labeling; component lubrication; component and equipment cooling; hangers and supports; operability of support systems; and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding work orders (WOs)was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the corrective action program database to ensure system equipment alignment problems were being identified and appropriately resolved.

These activities constituted one complete system walkdown inspection sample as defined in IP 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Routine Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns focusing on the availability, accessibility, and condition of firefighting equipment in the following risk-significant plant areas:

  • Reactor Building First Floor - Mezzanine;
  • Auxiliary Building Basement - T Room;
  • Turbine Building Basement - Standby Feedwater Area; and
  • Auxiliary Building Fifth Floor - Division 2 CCHVAC.

The inspectors reviewed these fire areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and implemented adequate compensatory measures for out-of-service, degraded, or inoperable fire protection equipment, systems, or features in accordance with the licensees Fire Protection Plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events (IPEEE) Report with later additional insights, their potential to impact equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. The inspectors verified fire hoses and extinguishers were in their designated locations and available for immediate use; fire detectors and sprinklers were unobstructed; transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

In addition, the inspectors verified problems associated with plant fire protection were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted five quarterly fire protection inspection samples as defined in IP 71111.05Q.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification

a. Inspection Scope

The inspectors observed licensed operators during simulator training on September 12, conducted partially in response to licensee-identified corrective actions intended to improve overall operating crew performance. The inspectors assessed the operators performance of simulated tasks focusing on alarm response, command and control of crew activities, communication practices, and procedural adherence. The inspectors also observed the operations training staffs post-evaluation critique to assess the ability of the licensees evaluators to identify performance deficiencies. The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements.

This inspection constituted one quarterly licensed operator requalification program simulator inspection sample as defined in IP 71111.11.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Observations During Periods of Heightened Activity or Risk

(71111.11Q)

a. Inspection Scope

On August 5 and 6, the inspectors observed licensed operators in the control room perform power maneuvers for a rod pattern adjustment, main steam valve testing, and turbine stop valve testing. Then, on August 18, the inspectors observed licensed operators in the control room perform turbine low pressure stop and intercept valve testing. These activities required heightened awareness, additional detailed planning, and involved increased operational risk. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of procedures;
  • control board (or equipment) manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions.

The performance in these areas was compared to pre-established operator action expectations, procedural compliance, and task completion requirements.

In addition, the inspectors verified problems related to licensed operator performance were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted one quarterly licensed operator heightened activity/risk inspection sample as defined in IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated the licensee's handling of selected degraded performance issues involving the following risk-significant structures, systems, and components (SSCs):

  • CARD 17-24655; E1150F068B Division 2 RHR Heat Exchanger Service Water Outlet Flow Control Valve Failed to Open;
  • CARD 17-25769; Division 2 CCHVAC Make Up Air Rad Monitor Flow Switch Pegged High;
  • CARD 17-27857; Combustion Turbine Generator (CTG) 11-3 Unit Trouble Alarm (11D58) due to High Stator Temperature; and
  • CARD 17-21106; Review Reactor Pressure System (RPS) for Maintenance Rule (a)(1) Classification.

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the SSCs. Specifically, the inspectors independently verified the licensee's handling of SSC performance or condition problems in terms of:

  • appropriate work practices;
  • identifying and addressing common cause failures;
  • characterizing SSC reliability issues;
  • tracking SSC unavailability;
  • trending key parameters (condition monitoring);
  • appropriateness of performance criteria for SSC functions classified (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSC functions classified (a)(1).

In addition, the inspectors verified problems associated with the effectiveness of plant maintenance for risk-significant SSCs were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted four quarterly maintenance effectiveness inspection samples as defined in IP 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for maintenance and emergent work activities affecting risk-significant and/or safety-related equipment listed below to verify the appropriate risk assessments and risk management actions were performed prior to removing equipment for work:

  • Planned maintenance during the week of July 17-21 including the Division 1 RHR/RHR Service Water maintenance outage;
  • Planned maintenance during the week of July 31-August 4 including the 65F under voltage and EDG 14 slow start tests and emergent maintenance on the East Gland Seal Exhauster;
  • Planned maintenance during the week of August 7-11 including the EDG 12 safety system outage;
  • Planned maintenance during the week of August 21-25 including the HPCI safety system outage;
  • Emergent maintenance on Division 1 Standby Gas flow high out of specification;
  • Planned maintenance during the week of September 18-22 including Division 2 CCHVAC; and
  • Emergent maintenance on Division 1 service water pump room ventilation dampers and planned maintenance during the week of September 25-29 including the turbine building closed cooling water west heat exchanger replacement.

These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each of the above activities, the inspectors reviewed the scope of maintenance work in the plants daily schedule, reviewed control room logs, verified plant risk assessments were completed as required by 10 CFR 50.65(a)(4) prior to commencing maintenance activities, discussed the results of the assessment with the licensees probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were consistent with the risk assessment assumptions. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid, redundant safety-related plant equipment necessary to minimize risk was available for use, and applicable requirements were met.

In addition, the inspectors verified maintenance risk-related problems were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted seven maintenance risk assessment and emergent work control inspection samples as defined in IP 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed the following issues:

  • CARD 17-22500; Electrical Perturbation Occurred While Restoring Bus 64C to Offsite per 24.321.09;
  • CARD 17-23600; Unable to Remote Start CTG 11-1 During Surveillance Testing;
  • CARD 17-23029; Snubber T23-I2837-36-G56 Failed Functional Test; and
  • CARD 17-00767; Diesel Fire Pump Failed to Start;
  • CARD 17-26749; NRC Question Operability of EDG Switchgear with No Ventilation Available; and
  • CARD 17-27936; RHR Division 1 Pump Room Dampers Indicating Closed.

The inspectors selected these potential operability/functionality issues based on the safety significance of the associated components and systems. The inspectors verified the conditions did not render the associated equipment inoperable/non-functional or result in an unrecognized increase in plant risk. When applicable, the inspectors verified the licensee appropriately applied TS limitations, appropriately returned the affected equipment to an operable or functional status, and reviewed the licensees evaluation of the issue with respect to the regulatory reporting requirements. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. When applicable, the inspectors also verified the licensee appropriately assessed the functionality of SSCs that perform specified functions described in the UFSAR, Technical Requirements Manual, Emergency Plan, Fire Protection Plan, regulatory commitments, or other elements of the current licensing basis when degraded and/or nonconforming conditions were identified.

In addition, the inspectors verified problems associated with the operability or functionality of safety-related and risk-significant plant equipment were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted six operability determination and functionality assessment inspection samples as defined in IP 71111.15.

b. Findings

(1) Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations
Introduction:

The inspectors identified a Severity Level IV Non-Cited Violation of the NRCs reporting requirements in 10 CFR 50.73(a)(1), Licensee Event Report System.

The licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery on March 24, 2017, of a condition that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system.

Description:

While performing testing during the refueling outage on March 24 with the unit in Mode 5 (refueling), an electrical perturbation occurred when synchronizing EDG 12 with offsite power. The electrical perturbation caused a loss of RPS channel A power and a loss of power to nuclear steam supply shutoff system (NSSSS) channels A and C.

Several equipment/component actuations occurred including an RPS A half-scram, Division 1 NSSSSs actuation; auto start of the Division 1 standby gas treatment subsystem; trip of the reactor building heating, ventilation, and air conditioning system; and isolation of drywell pneumatics. CARD 17-22500 was written to evaluate the event.

The licensee determined the bus tie breaker was apparently closed with the EDG slightly out-of-phase with offsite power, which caused an electrical voltage and current transient.

The licensee correctly concluded none of the equipment/component actuations met the reporting requirements in 10 CFR 50.72, Immediate Notification Requirements for Operating Nuclear Power Reactors; however, it did not subsequently review the event with respect to the 10 CFR 50.73 reporting requirements.

The inspectors reviewed the licensees initial evaluation of the event and raised questions with the licensee to better understand which primary containment isolation valves actuated as a result of the Division 1 NSSSS actuation and whether the reporting requirements in 10 CFR 50.73 were satisfied since it appeared containment isolation valves in more than one system received isolation signals. The inspectors reviewed the control room logs and noted that in addition to the drywell pneumatics valves, the drywell floor and equipment drain valves also isolated. Although the containment isolation was not required due to the actual plant conditions, the invalid actuation of containment valves in more than one system would be reportable under 10 CFR 50.73(a)(2)(iv)(A).

In response to the inspectors questions, the licensee initiated CARD 17-25005, 10 CFR 50.73 Reportability Review of CARD 17-22500 Not Documented Within 60 Days, and completed an evaluation of the event with respect to the 10 CFR 50.73 reporting requirements. The licensee determined this event should have been reported since Division 1 primary containment isolation valves actuated (closed) in three systems (drywell pneumatics, drywell floor and equipment drains, and torus water management). The licensee made a telephone notification on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).

Analysis:

The inspectors determined the licensees failure to report the invalid primary containment isolation valve actuations in accordance with the requirements in 10 CFR 50.73 was a licensee performance deficiency warranting a significance evaluation. Consistent with the guidance in IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated September 7, 2012, the inspectors determined the performance deficiency was not a finding of more than minor significance based on No answers to the more-than-minor screening questions. The inspectors also reviewed the examples of minor issues in IMC 0612, Appendix E, Examples of Minor Issues, dated August 11, 2009, and found no examples related to this issue.

Violations of 10 CFR 50.73 are dispositioned using the traditional enforcement process because they are considered to be violations that potentially impede or impact the regulatory process. This violation was also associated with a performance deficiency that has been evaluated as having minor safety significance by the significance determination process (SDP). The SDP, however, does not specifically consider regulatory process impact. Thus, although related to a common regulatory concern, it is necessary to address the violation and performance deficiency using different processes to correctly reflect both the regulatory importance of the violation and the safety significance of the associated performance deficiency. In accordance with Section 6.9.d.9 of the NRC Enforcement Policy, this violation was categorized as Severity Level IV because the licensee failed to make a report to the NRC as required by 10 CFR 50.73(a)(1).

No cross-cutting aspect is associated with this traditional enforcement violation because the associated performance deficiency was determined to be of minor safety significance and therefore not a finding.

Enforcement:

Title 10 CFR 50.73(a)(1) requires, in part, that the licensee submit an LER for any event of the type described in this paragraph within 60 days after the discovery of the event. Title 10 CFR 50.73(a)(2)(iv)(A) requires, in part, that the licensee report any event or condition that resulted in manual or automatic actuation of any of the systems listed in Paragraph (a)(2)(iv)(B). Title 10 CFR 50.73(a)(2)(iv)(B)(2) lists general containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves.

Contrary to the above, the licensee failed to submit a required LER or provide a telephone notification within 60 days after discovery of a condition on March 24, 2017, that resulted in the invalid actuation of containment isolation signals affecting containment isolation valves in more than one system as required by 10 CFR 50.73(a)(2)(iv)(A). The condition involved the invalid automatic actuation of the primary containment isolation logic for Groups 12, 13, and 18 primary containment isolation valves on March 24, 2017.

In accordance with Section 6.9.d.9 of the Enforcement Policy, this violation was classified as a Severity Level IV Violation. Because this violation was not repetitive or willful, and was entered into the licensees corrective action program, it is being treated as a Non-Cited Violation consistent with Section 2.3.2.a of the NRC Enforcement Policy.

(NCV 05000341/2017003-01, Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations)

The licensee entered this issue into its corrective action program (CARD 17-25005) to evaluate the cause for its failure to satisfy the reporting requirements and to identify appropriate corrective actions. Subsequently, the licensee made a notification call on July 14, 2017 to the NRC Operations Center via the Emergency Notification System to report the event (Event Notice 52859).

(2) Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service The inspectors identified a non-cited violation (NCV) of TS 3.8.7 Distribution Systems -

Operating, for the licensees failure to restore inoperable Division 1 and Division 2 AC electrical power distribution subsystems to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, or be in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Specifically, on multiple occasions, electrical power distribution subsystems required by the above limiting condition for operation were inoperable due to their respective subdivisions of RHR switchgear room ventilation systems being out of service and therefore unavailable to provide the technical specification support function of attendant cooling that is needed for the associated electrical systems to perform their specified safety functions. The RHR switchgear room ventilation systems are required by the licensees Updated Final Safety Analysis Report to be operable when the safety-related equipment in the associated room is required to be operable.

Description:

The licensees Updated Final Safety Analysis Report, in Section 3.11.4.4, Residual Heat Removal Complex Safety-Related Ventilation Systems, states, in part, to maintain conditions below the limits specified in Table 3.11-4, each diesel generator room, switchgear room, and pump room is ventilated with two 50 percent-capacity supply air fans. They are not required unless the equipment served is required, and are designed to start when the associated diesel generator starts, or a preset high room temperature is reached. The switchgear in the RHR switchgear rooms are required to be operable in Modes 1, 2, and 3, as described in TS 3.8.7. On August 10, 2017, the inspectors questioned the licensee on the operability of RHR switchgear when the ventilation supply fans were out of service. The licensed operators stated that Precaution and Limitation 3.2 of station technical and operating procedure 23.420, RHR Complex Heating and Ventilation, Revision 35, allowed RHR Pump Room and Switchgear Room equipment to remain operable without the applicable ventilation system being returned to normal operable status as long as temperatures do not exceed 104 degrees Fahrenheit (F) in the area, or for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if temperature exceeds 104 degrees F. The procedure referred to design calculation (DC)-4953, RHR Complex Abnormal Operation-Damper Lineups, dated December 20, 2002, which was incorporated into procedure 23.420 on January 26, 2003.

The purpose of the design calculation states, in part, that it is to determine acceptable damper configurations based upon outside air temperature to maintain RHR complex design temperatures. The purpose further states, in part, that the results of the calculation should only be utilized in the event the motor operated dampers are unable to perform their design function and a spare operator is not readily available.

The licensee documented the issue in its corrective action program as CARD 17-26749 and took interim actions using Nuclear Generation Memo NPOP-17-0067 to outline department guidance to not use the guidance of DC-4953 until an engineering technical evaluation was completed. The subsequent technical evaluation concluded that that the condition where both ventilation supply fans were out of service does not support operability of the AC distribution systems (i.e., 4160 kV and 480 V buses) in the RHR switchgear rooms. Additional licensee corrective actions planned include, but are not limited to, modification of procedure 23.420, RHR Complex Heating and Ventilation, to reflect the technical evaluation results.

Based on the licensees evaluation and a review of operating history since the procedure change in 2003, the inspectors concluded that on numerous occasions, between September 10, 2014, and August 9, 2017, the requirements of TS 3.8.7 were not met for the RHR switchgear room ventilation systems.

Analysis:

The inspectors determined that the licensees failure to comply with TS 3.8.7 by either restoring inoperable electrical power subsystems to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, or be in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> was a performance deficiency. Specifically, the inspectors identified numerous occasions, between September 10, 2014, and August 9, 2017, where safety-related RHR switchgear ventilation systems were removed from service without restoring these systems within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or taking action to place the unit in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

The performance deficiency was determined to be more-than-minor because it was associated with the Configuration Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

In accordance with IMC 0609, Attachment 4, Initial Characterization of Findings, issued October 7, 2016, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012, the inspectors determined that this finding was of very low safety significance (Green)because it did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time, or two separate safety systems out-of-service for greater than its technical specification allowed outage time. That answer was based on reference material in the recent technical evaluation that showed that without the RHR switchgear room ventilation in operation for the probabilistic risk analysis mission time of 24-hours, the switchgear inside the room would still be able to perform its safety function. The inspectors determined that the violation had a cross-cutting aspect in the area of human performance, resources, because the licensee failed to ensure that the RHR Complex Heating and Ventilation procedure was adequate to support nuclear safety. H(1)

Enforcement:

Technical Specification (TS) 3.8.7, Distribution Systems - Operating, requires, in part, that Division 1 and Division 2 AC and DC electrical power distribution subsystems shall be operable in Modes 1, 2 and 3. Technical Specification 3.8.7 requires that if one or more required AC electrical power distribution subsystems is inoperable for more than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, action must be taken to place the unit in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to the above, on numerous occasions between September 10, 2014, and August 9, 2017, the licensee removed safety-related RHR switchgear ventilation systems from service without restoring these systems within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or taking action to place the unit in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Because the violation was of very low safety significance and was entered into the licensee's CAP, this violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement policy. (NCV 05000341/2017003-02, Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service)

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance testing activities to verify procedures and test activities were adequate to ensure system operability and functional capability:

  • WO 44741403; Perform 24 Month Post Maintenance Tasks on EDG 12 and R30P343C;
  • HPCI Safety System Outage - Final Post Maintenance Test;
  • WO 45095048; Inspect/Lube Blower and Motor, Replace Belts for CCHVAC Control Room North Division 1 Multizone Air Supply Unit; and

The inspectors reviewed the scope of the work performed and evaluated the adequacy of the specified post-maintenance testing. The inspectors verified the post-maintenance testing was performed in accordance with approved procedures, the procedures contained clear acceptance criteria that demonstrated operational readiness and the acceptance criteria were met, appropriate test instrumentation was used, the equipment was returned to its operational status following testing, and the test documentation was properly evaluated.

In addition, the inspectors verified problems associated with post-maintenance testing activities were entered into the licensee's corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted four post-maintenance testing inspection samples as defined in IP 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed surveillance testing results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety functions and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • 27.109.01; Turbine Steam Valves Test; and

The inspectors observed selected portions of the test activities to verify the testing was accomplished in accordance with plant procedures. The inspectors reviewed the test methodology and documentation to verify equipment performance was consistent with safety analysis and design basis assumptions, test equipment was used within the required range and accuracy, applicable prerequisites described in the test procedures were satisfied, test frequencies met TS requirements to demonstrate operability and reliability, and appropriate testing acceptance criteria were satisfied. When applicable, the inspectors also verified test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable.

In addition, the inspectors verified problems associated with surveillance testing activities were entered into the licensees corrective action program with the appropriate characterization and significance. Selected CARDs were reviewed to verify corrective actions were appropriate and implemented as scheduled.

This inspection constituted one in-service test and three routine surveillance tests, for a total of four surveillance testing inspection samples as defined in IP 71111.22.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Mitigating Systems Performance IndexHeat Removal System

a. Inspection Scope

The inspectors reviewed a sample of plant records and data against the reported Mitigating Systems Performance Index (MSPI) Heat Removal System Performance Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, LERs, and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator.

This inspection constituted one MSPIHeat Removal System Performance Indicator verification inspection sample as defined in Inspection Procedure (IP) 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance IndexResidual Heat Removal System

a. Inspection Scope

The inspectors reviewed a sample of plant records and data against the reported MSPI Residual Heat Removal System (RHR) Systems Performance Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, Licensee Event Reports (LERs), and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator.

This inspection constituted one MSPIRHR Systems Performance Indicator verification inspection sample as defined in IP 71151.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance IndexCooling Water Systems

a. Inspection Scope

The inspectors reviewed a sample of plant records and data against the reported MSPI Cooling Water Systems Performance Indicator. To determine the accuracy of the performance indicator data reported, performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, was used. The inspectors reviewed the MSPI derivation reports, Control Room logs, Maintenance Rule database, LERs, and maintenance and test data from July 2016 through June 2017 to validate the accuracy of the performance indicator data reported. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's corrective action program database to determine if any problems had been identified with the performance indicator data collected or transmitted for this performance indicator.

This inspection constituted one MSPI Cooling Water Systems Performance Indicator verification inspection sample as defined in IP 71151.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensees corrective action program at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Some minor issues were entered into the licensees corrective action program as a result of the inspectors observations; however, they are not discussed in this report.

This inspection was not considered to be an inspection sample as defined in IP 71152.

b. Findings

No findings were identified.

.2 Annual In-depth Review Samples

a. Inspection Scope

The inspectors selected the following issues for in-depth review:

  • CARD 13-24841; EDG Steady State Voltage and Frequency Technical Specification Ranges.

As appropriate, the inspectors verified the following attributes during their review of the licensee's corrective actions for the above CARD and other related CARDs:

  • complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery;
  • consideration of the extent of condition, generic implications, common cause, and previous occurrences;
  • evaluation and disposition of operability/functionality/reportability issues;
  • classification and prioritization of the resolution of the problem commensurate with safety significance;
  • identification of the root and contributing causes of the problem; and
  • identification of corrective actions, which were appropriately focused to correct the problem.

The inspectors discussed the corrective actions and associated evaluations with licensee personnel.

This inspection constituted one annual in-depth review inspection samples as defined in IP 71152.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on component mispositionings, but also considered the results of daily inspector corrective action program item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the 6-month period of January 2017 through June 2017, although some examples expanded beyond those dates where the scope of the trend warranted.

The review also included issues documented outside the corrective action program in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees corrective action program trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

This review constituted one semi-annual trend review inspection sample as defined in IP 71152.

b. Findings

No findings were identified.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 Retraction of Event Notification 52724: Unanalyzed Condition Combustion Turbine

Generator 11-1

a. Inspection Scope

On May 2, 2017, the licensee submitted Event Notification 52724, Unanalyzed Condition CTG 11-1, to the NRC for a condition discovered by the licensee that could not have ensured the applicable Appendix R success criteria under all of the postulated scenarios described in the Updated Final Safety Analysis Report (UFSAR) for Combustion Turbine Generator (CTG) 11-1. From December 21, 2016, until March 18, 2017, when Mode 4 was entered, CTG 11-1 was determined to be in a configuration where it could not be started from the dedicated shutdown panel although it could be started locally. One of the specific scenarios for Appendix R in the UFSAR credits CTG 11-1 to support a safe shutdown based on an assumed time required to start CTG 11-1 and then provide flow to the reactor pressure vessel using the Standby Feedwater System.

On May 19, the licensee retracted Event Notification 52724. A time validation study was performed verifying operator actions could have been completed within the time described in the UFSAR for initiating Standby Feedwater flow to the reactor pressure vessel to ensure Appendix R safe shutdown capability under the plant conditions during the relevant time period.

The inspectors reviewed the basis for the retraction including the time validation study.

The inspectors concurred with the conclusion that operators would have sufficient time to manually start CTG 11-1 and initiate the Standby Feedwater System in compliance with the UFSAR and Appendix R requirements.

This inspection constituted one event follow-up inspection sample as defined in IP 71153.

b. Findings

No findings were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary

On October 17, 2017, the inspectors presented the inspection results to Mr. M. Caragher and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

On November 9, 2017, the inspectors presented the results of the finding associated with the Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service, (Section 1R15b.2) to Mr. L. Bennett and other members of the licensee staff. The licensee acknowledged the issues presented and confirmed that none of the potential report input was considered proprietary.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

L. Anderson, Manager, Radiological Emergency Response Preparedness (incoming)
N. Avrakotos, Manager, Radiological Emergency Response Preparedness (outgoing)
L. Bennett, Director, Nuclear Operations
R. Breymaier, Manager, Performance Engineering and Fuels
M. Brooks, Principal Technical Expert
M. Caragher, Executive Director, Nuclear Production
W. Colonnello, Director, Nuclear Project Management
K. Dittman, Acting Manager, Plant Support Engineering
D. Domski, Engineer, Plant Systems Engineering
M. Donigian, Supervisor, Operations Training
J. Haas, Supervisor, Licensing
D. Hemmele, Superintendent, Nuclear Operations
E. Kokosky, Director, Organization Effectiveness
R. Laburn, Manager, Radiation Protection
K. Locke, General Supervisor - Electrical, Plant Systems Engineering
S. Maglio, Manager, Licensing
K. Mann, Supervisor, Regulatory Compliance
R. Matuszak, Manager, Plant Systems Engineering
D. Noetzel, Director, Nuclear Engineering
K. Polson, Senior Vice President and Chief Nuclear Officer
W. Raymer, Director, Nuclear Maintenance
B. Rumans, General Supervisor, Radiation Protection Technical Services
P. Southwell, General Supervisor, Radiation Protection ALARA

U.S. Nuclear Regulatory Commission

B. Dickson. Chief, Reactor Projects Branch 2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000341/2017003-01 NCV Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations (Section 1R15.b.1)
05000341/2017003-02 NCV Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service (1R15.b.2)

Closed

05000341/2017003-01 NCV Failure to Satisfy 10 CFR 50.73 Reporting Requirements for Primary Containment Isolation Valve Actuations (Section 1R15.b.1)
05000341/2017003-02 NCV Technical Specification Allowed Outage Time Exceeded for Electrical Power Distribution Systems Due to Auxiliary Equipment Out of Service (1R15.b.2)

LIST OF DOCUMENTS REVIEWED