ML20214A141

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Insp Rept 50-416/87-10 on 870314-0417.Violations Noted: Failure to Document Identified Deficiency,To Implement SSW Basin Acid Addition Sys Per Temporary Alteration & to Install Control Rod Hydraulic Control Units
ML20214A141
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 04/29/1987
From: Butcher R, Dance H, Will Smith
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20214A112 List:
References
50-416-87-10, NUDOCS 8705190289
Download: ML20214A141 (13)


See also: IR 05000416/1987010

Text

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                                                UNITED STATES
                                    ' NUCLEAR REGULATORY COMMISSION
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       [[pn 8ttgo n                              REGION 11
       g            j                      101 MARIETTA STREET, N.W.
       *            t                       ATLANTA, GEORGI A 30323
        %,...../
         Report No.: '50-416/87-10
         Licensee:      System Energy Resources, Inc.
                        Jackson, MS 39205
         Docket No.:    50-416                                       License No.: NPF-29
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         Facility Name: Grand Gulf Nuclear Station
         Inspection Conducted: March 14 through April 17, 1987
          Inspect s:           /['                                              2f V7
                  w R.C Butt:her, Senior Resident Inspector                 Date S~1gned
                             P. Adn             ,
                       W.F. Sm th Resident Inspector
                                                                             Adn
                                                                            Date Signe
         Approve'd by:              A*                                           27 N
                        H.C. Dance, Section Chief, Division                 Date Signed
                        of Reactor Projects
                                          SUMMARY'
          Scope:   This routine inspection was conducted by 'the resident inspectors at
          the site in the areas. of Licensee Action on Previous Enforcement Matters,
         Operational Safety Verification, Maintenance Observation, Surveillance Observa-
          tion, Reportable Occurrences, Inspector Followup and Unresolved Items, and
         Design Changes and Modifications.
          Results:    Three violations were identified: Failure to document an identified ~
         deficiency, failure to implement the SSW basin acid addition system per the
          temporary alteration and failure to install control rod hydraulic control units
          per design drawings.

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             8705190289 870429 6
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                                                                       REPORT DETAILS
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        1.  Licensee Employees Contacted
            J.E. Cross,GGNS Site Director
           *C.R. Hutchinson, GGNS General Manager
            R.F. Rogers, Manager, Unit 1 Projects
            A.S. McCurdy,' Manager, olant Operations
           *J.D. Bailey, Compliance Coordinator
            M.J. Wright, Manager, Plant Support
            L.F. Daughtery, Compliance Superintendent
            D.G. Cupstid, Start-up Supervisor
            R.H. McAnuity, Electrical Superintendent
           *J.P. Dimmette, Manager, Plant Maintenance
            W.P. Harris, Compliance Coordinator
           *J.L Robertson, Licensing Superintendent
            L.G. Temple, I & C Superintendent
            *J.H. Mueller, Mechanical Superir,tendent
            L.B. Moulder, Operations Superintendent
           *S.F. Tanner, Manager, Nuclear Site QA
            J.V. Parrish, Chemistry / Radiation Control Superintendent
           *J.W. Yelverton, Acting Manager, Plant Operations
           *F.W. Titus, Director, Nuclear Plant Engineering
           *S.M. Feith,- Director, QA
            Other licensee employees contacted included technicians, cperators,
            security force members, and office personnel.
           * Attended exit interview
        2.  Exit Interview (30703)
            The inspection scope and findings were summarized on April 17, 1987, with
            those persons indicated in paragraph-1 above. The licensee did not
            identify as proprietary any of the materials provided to or reviewed by
            the inspectors during this inspection. The licensee had no comment on che
            following inspection findings:
                  416/87-10-01, Inspector Followup Item, Diesel Generator fuel oil
                  valve pit cover design change.                                 (paragraph 4)
                  416/87-10-02, Inspector Followup Item, Determine source of water on
                  SSW basin floor. (paragraph 4)
                  416/87-10-03, Inspector Followup Item, Failure of mechanics to
                  properly assemble a relief valve. (paragraph 5)

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                        416/87-10-04,                       Violation,      Failure to document an                         identified
                        deficiency.                       (paragraph 5)
                        416/87-10-05, Inspector Followup Item, Standby Liquid Control
                        surveillance procedure improvement. (paragraph 6)
                        416/87-10-06, Inspector Followup Item, Standby Diesel Generator (SDG)
                        12 start pushbutton troubleshooting. .(paragraph 6)
                        416/87-10-07, Inspector Followup-Item, Method of venting air pressure
                        from SDG air start lines. (paragraph 6)
                        416/87-10-08, Inspector Followup Item, Required SDG fuel oil tank
                        levels. (paragraph 6)
                        416/87-10-09, Violation, Failure to implement the SSW basin acid
                        addition system per the temporary alteration. (paragraph 9)
                        416/87-10-10, Violation, Failure to install hydraulic control units
                        per design drawings.                           (paragraph 8)
             3. Licensee Action on Previous Enforcement Matters (92702)
                (Closed) Violation 416/84-54-01. The licensee has issued Nuclear Produc-
                tion Department Procedure 1.14, Verification and Certification of
                Submittals and Information, to establish a method to be used for review
                of any information that is to be submitted to the NRC. Attachment II to
                Procedure 1.14 provides guidelines for verification and certification of
                submittals and information. This action should ensure future submittals
                are accurate.
             4. Operational Safety Verification (71707)
                The inspectors kept themselves informed on a daily basis of the overall
                plant status and any significant safety matters related to plant opera -
                tions.           Daily discussions were held with plant management and various
                members of the plant operating staff.
                The inspectors made frequent visits to the control room such that it was
                visited at least daily when an inspector was on site.                                                  Observations
                included instrument readings, setpoints and recordings, status of
                operating systems, tags and clearances on equipment controls and switches,
                annunciator alarms, adherence to limiting conditions for operation,
                temporary alterations in effect, daily journals and data sheet entries,

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                control room manning, and access controls. This inspection activity

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                included numerous informal discussions with operators and their seper-

[ visors. 4

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          Weekly, when the inspectors were onsite, selected Engineered Safety
          Feature (ESF) systems were confirmed . operable.                      The confirmation is made
         :by verifying the following: Accessible valve flow path alignment, power
          supply breaker and fuse status, major component leakage, lubrication,
          cooling and general condition, and instrumentation.
          General plant tours were conducted on at least a biweekly basis. Portions
          of the control building, turbine building, auxiliar'y building and outside
          areas were visited. Observations included safety related tagout verifica-
          tions, shift turnover, sampling program, housekeeping and general plant
          conditions, fire protection equipment, control of activities in progress,
          radiation protection controls, physical security, problem identification
          systems, and containment isolation.                         At least monthly, the licensee's
          onsite emergency response facilities were toured to determine facility
          readiness.
          The folicwing comments were noted:
          On April 1,       1987, the. inspectors noted that the valve pits for the
          Divisions 1, 2 and 3 diesel generator fuel oil tanks were nearly full of
          water.      Licensee personnel were in the process of pumping the water out.
          This condition was previously identified in NRC Inspection Report 86-20
          when an ESF walkdown was conducted. At that time the Division 3 valve pit
          was found full of water due to the design of the cover. The licensee
          enlarged the covers to overlap the opening of the pit, however the new
          design has since proved itself to be inadequate as evidenced by the
          presence of water. The licensee is presently working on a solution. This
          shall be Inspector Followup Item 416/87-10-01.
          While touring the Standby Service Water (SSW) basins the inspectors noted
          the following discrepancies:
                  Basin A SSW pump motor (P41C001A) had a junction box on the motor
                  housing with the cover off and hanging by a restraining chain.
                  Several loose wires were hanging out of the junction box and a loose
                  screw was laying inside the junction box.                      On the wall behind the
                  High Pressure Core Spray (HPCS) service water pump motor (P41C002C),
                  a junction box cover was loose and hanging by only one screw.                       The
                  floor in both areas was completely covered in water.
                  Basin B SSW pump motor (P41C0018) had a similar junction box on the
                  motor housing as P41C001A.          It also had the cover off with several
                  loose wires hanging down. The floor in the B basin arca was dry.
          The licensee was notified of the above discrepancies and took corrective
          action. The inspectors questioned the source of tha excessive water on
           the SSW basin floor since there was no obvious source. The source of
          water inside the SSW pump rooms will be Inspector Followup Iten 416/87-
            10-02.
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             -The inspectors ' noticed, on repeated occasions, water on the floor in the
             RCIC/RWCU mezzanine on auxiliary building level _119.                     The water appeared
             to be leaking from the steam tunnel floor piping penetrations above. The-

. operators explained that due to leakage in the steam tunnel, water must be

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             drained from the steam tunnel floor every shift or it overflows through
             the penetrati.ons to the area below. One of the areas where water is
             collecting _ on the floor is a high contamination area and leakage seems to
             persist ' independent of- draining the steam tunnel floor. The inspectors
             expressed concern that it is a . poor radiological work practice to allow
              this leakage to exist uncollected and uncontrolled. The licensee has
              corrected this condition by collecting the water and directing it to a
             drain.
              No violations or deviations were identified.
          5. Maintenance Observation (62703)                                                          .
              During the report period, the inspectors observed portions of the
              maintenance activities listed below. The observations included a review
              of the work documents for adequacy, adherence to procedure, proper
              tagouts, adherence to technical specifications, radiological controls,
observation of all or part of the actual work and/or retesting in
              progress, specified retest requirements, and adherence to the appropriate
              quality controls.

E 1653 M71253, Repair, resetting and retesting of Standby Liquid Control

                      System Pump A discharge relief valve C41-F029A.
                      MWO EL3567, General Maintenance Instruction 07-S-12-71, Revision 3,
                      calibration checks of Time Delay Relays.
                      MWO E71482, Replace Time Delay Relay Block.

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MWO E71202, Install chart recorder and monitor points on Division 1
                      and 2 diesel generators related to previous Division 1 diesel

, generator output breaker trip. . On March 12, 1987, the inspectors witnessed the restoration to service and

              retesting of relief valve C41-F029A. When the operator opened the Standby
              Liquid Control pump suction valve, water leaked profusely out of the
              relief valve gagging screw plug.             The operator immediately shut the
               suction valve to stop the leakage. The inspectors noted that this was not
              an ordinary mechanical joint leak, but rather, the gagging screw plug was
              not properly installed when the valve was reassembled in the shop. The
               leak was corrected by maintenance tightening the plug, and then the valve
              passed the retest. When the NRC inspector questioned a QA inspector who
              was present for the retest if a deficiency report or other document was
               initiated to document the deficiency, the response was negative, nor did

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           he indicate any intention to do so, because he stated he did not consider
           the official retest as having started. The operator failed to d]cument
           the deficiency also. This is a failure to comply with GGNS Administrative
           Procedure (AP) 01-S-03-2, Quality Deficiency Reports (QDRs).        Section-
           6.1.1 requires all quality deficier.cies, unless identified on another
           deficiency document, to be documented in accordance with this procedure.
           The inspectors reviewed MWO 71253 to determine if adecuate instructions
           existed to ensure the valve was properly reassembled. There were no
           detailed instructions nor was the vendor manual-referenced, thus the work
           instruction appeared to be inadequate. The inspector expressed concern to
           the licensee over the way this job was handled, with particular emphasis
           on a QA representative's reluctance to insure that the apparent deficiency
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           was documented. Subsequently the licensee issued two QDRs (144-87 and
           145-87) which identified a lack of knowledge on the part of the mechanic
           reassembling the valve and failure of MWO 71253 to provide adequate
           instructions.
           Upon investigating, the licensee deternined and r ported to the inspectors
           that the applicable vendor manual was used for the work on the relief
           valve, although not referenced in the MWO. The licensee stated that
           failure of the mechanics to properly assemble the relief valve was
           indicative of a training deficiency, and that appropriate corrective
           actions will be documented as 00Rs 144-87 and 145-87 are processed.
           Followup inspection of actions taken shall be tracked under Inspector
           Followup Item 416/87-10-03.
           Section 16.0 of the licensee's NRC-approved Operational Quality Assurance
           Manual, MPL-TOPICAL-1, Revision 5, requires, in part, that measures shall
           be established to ensure that conditions adverse to quality, such as
           deficiencies, are promptly identified and corrected.         AP 01-S-03-2
           established this measure. Failure to pronptly document the deficient
           reassembly of C41-F029A as evidenced-by the gagging screw plug being left
           loose is a violation of this requirement (416/87-10-04).      QDR 168-87 was
           initiated by the licensee to identify the failure to document a defi-
           ciency, and corrective measures are being taken to ensure that such
           deficiencies are recognized and documented in the future.
        6. Surveillance Observation (61726)
           The inspectors observed the performance of portions of the surveillances
            listed below. The observation included a review of the procedure for
            technical adequacy, conformance to Technical Specifications (TSs),
           verification of test instrument calibration, observation of all or part of
           the actual surveillances, removal from service and return to service of
            the system or components affected, and review of the data for accept-
           ability based upon the acceptance criteria.
                   06-0P-1C41-M-0001, Revision 25,     Standby Liquid Control   System
                   Operability.

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         06-0P-1P75-M-0002, Revision 32, Standby Diesel Generator (SDG) 12
         Functional Test.
         06-IC-SD17-R-1025, Revision 22, Ef fluent System Flow Rate Monitor
         Calibration (Turbine Building Exhaust Radiation Monitor).
         09-S-06-12, Revision 1,102.5% Core Flow Flux Controller High Limit
         Setting Verification.
         06-0P-1P75-M-0001, Revision 32, Standby Diesel Generator (SDG) 11
         Functional Test.
  During conduct of SLCS surveillance procedure 06-0P-1C41-M-0001 listed
  above, the inspectors noted that the precision test gauge connected at
  IC43R003 (SLCS pump discharge pressure) was oscillating violently as
  pressure was increased. At full discharge pressure the fluctuations from
  this positive displacement pump were so wide the end of the gauge pointer
  broke off. The operator experienced considerable difficulty in trying to
  maintain discharge pressure by throttling C41-F016 and at the same time
  throttling the pressure gauge isolation valve to dampen the oscillations.
  It was evident that he had marginal control over the system, and the
  probability of lifting the relief was high.       The inspector expressed
  concern to the licensee that failure to obtain more positive control over
  this system during testing could lead to damage or unsatisfactory test
  results.    The licensee indicated that the procedure will be changed to
  ensure better control, by the next time this quarterly surveillance is
  due, and that hardware ' changes are under consideration. This shall be
  tracked by Inspector Followup Item 416/87-10-05.
  During conduct of SDG 12 functional test 06-0P-1P75-M-0002 above, the
  diesel failed to start when the control room operator depressed the start
  pushbutten. i.fter reverifying prerequisites and finding no problems, a
  second attempt was made and the SDG started and came up to speed as
  required by the Technical Specifications.       The Shift Superintendent
  informed the inspectors that a Maintenance Work Order (MWO) was initiated
  te troubleshoot the pushbutton. The inspectors will follow up to verify
  that the failure is identified and corrected as appropriate. This shall
  be Inspector Followup Item 416/87-10-06.
  Also during the SDG 12 surveillance above, the procedure required that the
  drain plugs be removed and reinstalled in the isolated air start strainers
  to depressurize the air start lines (steps 5.1.7 and 5.2.7). Since this
  section of piping gets pressurized over 200 psig, the mechanic satisfied
  this requirement by first loosening an instrument fitting to depressurize
  the piping so that the plug could be safely removed. This appeared to be
  stretching the intent of the procedure because the procedure does not
  specifically authorize the breaking of an additional air pressure
  boundary. The inspectors discussed this with the licensee who indicated
  that the procedure would be reviewed and revised as appropriate. This
  shall be Inspector Followup Item 416/87-10-07.
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     Following' the SDG surveillance the inspectors reviewed                                                                        surveillance
     procedure 06-0P-IP75-M-0002, Revision 32.                                                                     The procedure requires the
     operator verify that the fuel oil day tank contains a minimum of 220
     gallons of fuel as indicated by at least 12 inches on fuel oil day tank
     level indicator LI-R607B on panel 1H13-P864.                                                                      The inspector reviewed
     the control room round sheet and it required a minimum of 22 inches on
     LI-R607P. The inspector then reviewed several documents for fuel oil day
     tank and storage tank minimum level requirements and found the following
     numbers specified:
     Division 1 and 2 SDGs                                                                                  Day Tank        Storage Tank
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     Yellow marking on control room                                                                         22 inches         6.2 feet
         level indicator
     Control room round sheet                                                                               22 inches         8.7 feet      .
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     Alarm Response Instruction                                                                             23 inches         8 feet 8
     04-1-02-1H22-P400-1A-C1                                                                                                  inches
                                                                                                                                                  ~
     DG Functional Test (06-0P-1P75-                                                                        12 inches         8 feet 8
     M-0001/0002)                                                                                                             inches
      Division 3 SDG (HPCS)
      Yellow marking on control room                                                                        10 inches         5.4 feet
      level indicator
      Control room round sheet                                                                              10 inches         6.3 feet
      Alarm Response Instruction                                                                            9.5 inches        76 inches
      04-1-02-1H13-P870-5A-El
      DG Functional Test (06-0P-1P81-                                                                       12 inches          5 feet 11
      M-0002)                                                                                                                  inches
      The Division 1 and 2 SOG day tank fuel oil level meters on the local
      panels read in 1/8th tank increments. When observed on April 3,1987,
      during a surveillance test, the Division 1 meter read 3/4 full when the
      control room indicator read 28 inches (out of 60 inch span). Discussions
      with the licensee indicate that the day tank level (for all three
      divisions) mest be a minimum of 12 inches to satisfy TS requirements.
      This would indicate that the HPCS SDG day tank level could be less than TS
       requirements on several indicators noted above and would be considered
      acceptable. Since there is an automatic fuel oil transfer pump for
      maintaining the day tank level well above TS limits, there is little
       possibility of being below TS limits during actual operation.                                                                          The
       licensee was requested to evaluate the numerous values noted, determine
       the appropriate value and revise the SDG fuel oil level requirements to be
       consistent with TS                          limits.                                        This will         be  Inspector Follow-up
       Item 416/87-10-08.
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       No violations or deviations were identified.
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    7. Reportable Occurrences (90712 & 92700)
       The below listed event reports were reviewed.to determine if the informa-
       tion ' provided met the _ NRC . reporting requirements.   The determination
       included adequacy of event description ' and corrective action taken or
       planned, existence of potential generic problems and the relative safety
       significance of each event, Additional inplant reviews and discussions
       with plant personnel . as appropriate were conducted .for the reports
       indicated by an asterisk.     The event reports were reviewed using the -
       guidance of the general policy and procedure for NRC enforcement actions,
       regarding licensee identified violations:
       The following license Event Reports (LERs) are closed.
       LER No.               Event Date                           Event
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       *85-033           August 30, 1985                    Unit 2 ultimate
                                                            heat sink
                                                            components
                                                            required for Unit
                                                            1 operability.
       *86-027           August 15, 1986                    Fire watches
                                                            exceed TS required
                                                            frequency.
       The event of LER 86-027 was addressed in Inspection Report 416/86-24.
       LER 85-033 reported that portions of the Unit 2 SSW system required to
       support the seismic qualification of_the Unit 1 SSW system were not under
       the operational -control of the plant. Other Unit 1/ Unit 2 interface
       concerns were subsequently identified. In lieu of updating this LER the
       licensee submitted a Special . Report, Unit 1/ Unit 2 Interface (AECM-87/
       0077) to provide a comprehensive review of actions taken and planned.
       This LER is closed and the Unit 1/ Unit 2 interface concern will be tracked
       under violation 416/86-17-03 2nd the special report update.
       Due to the number of problems associated with the Standby Service Water
       (SSW) system and their potential safety impact, an enforcement conference
       was held in the NRC Region II office on February 4,1987, as documented in
        Inspection Report 416/87-03. Report 416/87-03 and LER 86-029 stated the
        licensee would initiate an independent design review of the SSW system.
       On March 18, 1987, the licensee reported that during the SSW design review
        it was determined that a postulated single failure could cause the loss of
        the SSW system / Ultimate Heat Sink (VHS) 30 day water inventory. A loss of
        power from Motor Control Center (MCC) 15B61 would leave valves P41F125 and
        P41F066A open which could allow the flow of SSW from the A SSW train to
        the Plant Service Water (PSW) system through 3 inch cross connect piping.
       This would result in the loss of cooling water to the A train control room
        air conditioning condenser but the B train would still be available. The

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     loss of SSW water through the cross connect piping would eventually result
     in the excessive loss of UHS inventory. As interim corrective action the
     licensee issued night orders to tag close PSW to SSW cross connect valves
     P41F125 and P41F189 with SSW supplying the operable control room air
     conditioner (PSW normally supplies control room air conditioner cooling
     water).
     Tne licensee conducted a safety evaluation to assess the ability of the
     SSW/ UHS to meet established design criteria with the design deficiency
     noted above but with the implementation of appropriate administrative
     controls for operator action. The safety evaluation determined that with
     appropriate operator action within 7 hours, no unreviewed safety question
     exists. Off-Normal Event Procedure (ONEP) 05-1-02-I-4, Loss of Offsite
     Power and ONEP 05-1-02-V-11, Loss of Plant Service Water, were revised to
     incorporate the recommended administrative controls. Based on the above
     actions, the licensee secured the SSW system and returned the PSW/SSW
     isolation valves to their normal lineup.
     (Closed) P2184-07, Bonney Forge Non-Conforming Material . Based on a
     request from Nuclear Plant Engineering (NPE), Bechtel Power Corporation
     conducted a review of materials supplied to the licensee which originated
     from   Bonney Forge.     It was determined that no materials having the
     heat numbers identified as potential problem material were used in the
     construction of any Unit I nuclear piping systems. Based on the study
     results, the licensee determined no action was required.
     (Closed) P2185-01, Containment Purge Valve. Based on a Henry Pratt
     Information Letter, Nuclear Plant Engineering recommended to Plant Staff
     that Locktite be used on all four sides of the shaft key during reassembly
     on any Pratt valve and Limitorque operator. The valve driven gear spline
     adapter and key are secured to the valve shaft by a force fit together
     with the use of Locktite. Based on NPE recommendations the plant staff
     revised Maintenance Section Procedure 07-S-08-510, Installation, Reinstal-
     lation, Disassembly and Reassembly of valves, to require the use of
     Locktite grade 242 or 271 as recommended. No further action was required.
     Subsequently, 07-S-08-510 was superseded by Plant Modification and
     Construction Section Procedure 15-S-02-502 which also incorporated the
     above recommendativn.
     (Closed) P2186-02. The Electro-Motive Division of General Motors reported
     that upper connecting rod bearings had been found with mislocated dowel
     holes. Morrison-Knudsen Company, manufacturers of the High Pressure Core
     Spray (HPCS) diesel generator system notified General Electric (GE) which
      supplied the HPCS diesel to SERI. GE informed SERI that only connecting
     rod bearings purchased between November 1985 and April 1986 were suspect
     and require inspection. GE records indicate they neither purchased nor
      supplied any connecting rod bearings to MP&L (now SERI) for the Grand Gulf
     Plant during this time frame and no further action is required.
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     (Closed) P2186-04, BBC Brown Boveri, Inc. K600/K800 Circuit Breakers Wire
     Harness.   On June 30, 1986, the NRC was notified of a 10 CFR Part 21
     report identifying a condition in the type K600S circuit breakers stpplied
     by BBC Brown Boveri, wherein a control wire harness came into direct
     contact with a racking gear inside the breaker. The gear teeth had worn
     through the protective cover and severed a wire causing a grounded
     condition. The licensee was also notified in June 1986. During the first
     refueling outage (October 1986 thru January 1987) the plant staff
     inspected 26 out of 26 E5F breakers scheduled and 40 out of 60 balance of
     plant breakers scheduled for inspection and found no damage to the wiring
     harness.   The remaining breakers will be inspected during the normal
     inspection program. General Maintenance Instruction 07-S-12-50, Inspec-
     tion and Calibration of.480V ITE K600S-K1600S Breakers, has been updated
     to inspect breakers for this problem.
     No violations or deviations were identified.
  8. Inspector Followup and Unresolved Items (92701)
     (Closed) Inspector Followup Item 416/85-05-01. This item was addressed in
     Inspection Report 416/87-06 and was inadvertently listed as an open item
     when it should have been closed. This is to document the closure of
     416/85-05-01.
     (Closed) Inspector Followup Item 416/86-39-03.      Correction of records on
     G.N. Bettis valve actuator seal replacements.        The licensee issued a
     Quality Deficiency Report (QOR) to formally identify the problem and
      implement appropriate corrective actions. The inspectors reviewed the
     actions taken which included correction of the records by issuance of a
     record supplement and issuance of a memorandum to mechanical personnel
     frcm the Mechanical Maintenance Superintendent emphasizing their
     responsibilities as they relate to work documentation.
     The records, however, were not adequately corrected. The inspectors noted
     that in an effort to correct the record for valve E61-F009 (Task Card No.
     ME0027), the licensee added another copy of the erroneous material ticket
      instead of deleting or annotating that it was not applicable to E61-F009.
     The inspectors have since verified that this has been corrected. QA issued
     another QDR (87-1073) to document the incorrect records correction and
     actions taken to ensure that record supplements are more carefully
      screened in the future.
      (Closed) Unresolved Item 416/87-01-04.      Resolution of missing fasteners
     on control rod drive Hydraulic Control Units (HCU's).        This item was
     previously addressed in NRC Inspection Reports 416/87-01 and 416/87-05.
     On February 6, 1987, during a tour of the containment the inspectors
      found that one fastener required for securing HCU 36-13 to the foundation
     was missing.    It was apparent to the inspectors that the fastener had
      never been installed, and thus a concern was raised as to the as-built
      condition, and thus the seismic qualification of the other 192 HCUs. The
      licensee was requested to provide documentation that supports this and any
                 .
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                   other deficient HCU installations. There was no ' documentation on file
                   which would allow the fastener to be missing from HCU 36-13. The fastener
                   was replaced, a 100% inspection was conducted on the other HCUs and other
                   deficient fastener installations were corrected, confirmed acceptable by
                   review of previous documentation, or accepted in their as-found condition
                   by additional engineering analysis. From the results of these actions, it
                   appeared that about 36 HCUs were operated in an unanalyzed, deficient
                   condition with regard to seismic qualification from plant licensing until
                   February 1987. A major effort was implemented by the licensee to review
                   HCU installation records, to accurately document the as-found condition of
                   the 193 HCUs and to perform proper engineering analyses of the condition
                   as-found and after repairs (as-left). As was reported in NRC Inspection
                   Report 416/87-05, the inspectors expressed concern that the licensee
                   had not probed this problem to the depth necessary when the concern was
                   initially raised. As a result, the licensee also implemented a review of
                   program requirements for handling such problems.
                   On April 10, 1987 the licer.see presented a documentation package
                   containing the investigation results and disposition of deficiencies found
                   on HCU mounting fasteners. The inspectors met with the 1.censee to
                                _
                   discuss the package and then reviewed it for accuracy and completeness.
                   Based on the information provided in the package and independent observa-
                   tions made on the equipment by the inspectors, it appears that prior to
                   discovery of the missing fastener on HCU 36-13 on February 6, 1987, 150 of
                   the 193 HCUs had an average of about three fasteners (of eleven) with less
                   than the recommended torque shown on drawing 767E800, Hydraulic Control
                   Unit, five HCUs had a mounting bolt missing without having in its place
                   the equivalent weld required by Bechtel Supplier Deviation Disposition
                   Request (SDDR) M-316.0-016 and General Electric Field Deviaticn Disposi-
                   . tion Request JB1-471. There were also a few isolated instances of missing
                   washers, broken bolts, missing nuts, and welds which were the incorrect
                   size. It was erroneously presumed by the licensee, however, that as of
                   May 30, 1982, all HCOs were mounted properly by the subcontractor, Reactor
                   Controls, Incorporated (RCI), in accordance with the applicable drawings
                   and specifications, and that any missing bolts had an equivalent weld, as
                   approved by the above SDDR. Therefore the system was operated in an
                   unanalyzed condition until after February 6,     1987, when the deficient,
                   as-found condition was corrected as much as practicable and as- corrected
                   analysis was performed by Nuclear Plant Engineering. 10 CFR Part 50,
                   Appendix B, Criterion V states, in part, that activities affecting quality
                    shall be accomplished in accordance with documented instructions and
                   drawings of a type appropriate to circumstances. Contrary to this, 156 of
                    193 HCUs were not mounted in accordance with the applicable drawings and
                    specifications during plant operation.     This is a violation. (416/87-
                    10-10).
                   The licensee performed a safety analysis of the HCUs in the as-found
                    condition. The analysis assumed that no fasteners were torqued to provide
                    the preload recommended, the various configurations of missing fasteners
                   were considered, welding provided under the above SDDR was conservatively
                    neglected in the calculation, and fasteners that were not fully seated
                   were assumed to be missing. The results of that analysis concluded that
                    the as-founJ conditions did not result in safety concerns which would
                    have jeopardized the integrity of the reactor coolant pressure boundary,

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    reduced capability to achieve and maintain reactor shutdown, or reduced
    capability to prevent or mitigate the consequences of an accident. The
    licensee has indicated that corrective actions for this violation will
    include a review of other safety related work performed by RCI and will
    provide documentation as to results and additional actions if appropriate.
 9. Design, Design Changes and Modifications (37700)
    The inspector reviewed the licensee's program for temporary alterations.
    Administrative Procedure (AP) 01-S-06-3, Control of Temporary Alterations,
    Revision 20, was reviewed to verify controls were in accordance with
    TSs,10 CFR 50.59 and the approved QA program, MPL-TOPICAL-1. Adequate
    controls are specified in tne procedure to ensure independent verifica-
    tion, modification status, proper restoration, and records retention and
    periodic verification of outstanding alterations. The Temporary Altera-
    tion log was reviewed and several Temporary Alterations were verified.
    The inspector had the following comments:
          Temporary Alteration 87-0005. The Temporary Alteration Request Form
          (Attachment I to 01-S-06-3) did not have the tag numbers entered
          and the installed tags did not have individual numbers. The Shift
          Supervisor initiated a QDR to correct the tag numbers.
          Temporary Alteration 86-0034. The installation of an acid storage
          tank and related piping to add chemicals to the Standby Servi e Water
          (SSW) basins was accomplished by this alteration. A Temparary
          Alteration Request Addendum, Attachment III to 01-S-06-3, shows
          the installation details for this temporary alteration. A visual
          inspection of the actual installation showed that the installed
          piping and valves did not agree with the temporary alteration. At
          each basin the installed piping divided into two lines with an
          installed valve in each line. Additionally the inspector observed
          the following discrepancies.
          Valve FTA6, fill line to the acid tank, was broken off and laying in
          the tank pit area.
          Valve FTA4B had no handle and no identification (temporary altera-
          tion) tag attached.
          The 4 inch drain line from the acid tank berm to the SSW B basin was
          disconnected between the berm and the first isolation valve (FTA7)
          which provided a leak path directly to the ground.
    TS 6.8.1 requires written procedures to be established, implemented and
    maintained covering the procedures recommended in Appendix A of Regulatory
    Guide 1.33, Revision 2, February 1978. Appendix A of Regulatory Guide
     1.33 recommends procedures covering the bypass of safety functions and
    jumper control. Administrative Procedure 01-S-06-3, paragraph 6.1,
    requires temporary alterations to be documented and controlled using
    temporary alteration forms (Attachments I and III).         The failure to
     implement the installation of the SSW basin acid storage tank and related
    piping in accordance with the approved temporary alteration is a
    violation. This is violation 416/87-10-09.
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