ML20214A141
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ML20214A141 | |
Person / Time | |
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Site: | Grand Gulf |
Issue date: | 04/29/1987 |
From: | Butcher R, Dance H, Will Smith NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20214A112 | List: |
References | |
50-416-87-10, NUDOCS 8705190289 | |
Download: ML20214A141 (13) | |
See also: IR 05000416/1987010
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i * ' UNITED STATES ' NUCLEAR REGULATORY COMMISSION i [[pn 8ttgo n REGION 11 g j 101 MARIETTA STREET, N.W. * t ATLANTA, GEORGI A 30323 %,...../ Report No.: '50-416/87-10 Licensee: System Energy Resources, Inc. Jackson, MS 39205 Docket No.: 50-416 License No.: NPF-29 ' Facility Name: Grand Gulf Nuclear Station Inspection Conducted: March 14 through April 17, 1987 Inspect s: /[' 2f V7 w R.C Butt:her, Senior Resident Inspector Date S~1gned P. Adn , W.F. Sm th Resident Inspector Adn Date Signe Approve'd by: A* 27 N H.C. Dance, Section Chief, Division Date Signed of Reactor Projects SUMMARY' Scope: This routine inspection was conducted by 'the resident inspectors at the site in the areas. of Licensee Action on Previous Enforcement Matters, Operational Safety Verification, Maintenance Observation, Surveillance Observa- tion, Reportable Occurrences, Inspector Followup and Unresolved Items, and Design Changes and Modifications. Results: Three violations were identified: Failure to document an identified ~ deficiency, failure to implement the SSW basin acid addition system per the temporary alteration and failure to install control rod hydraulic control units per design drawings.
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8705190289 870429 6 PDR ADOCK 0500 G
- >, , REPORT DETAILS t 1. Licensee Employees Contacted J.E. Cross,GGNS Site Director *C.R. Hutchinson, GGNS General Manager R.F. Rogers, Manager, Unit 1 Projects A.S. McCurdy,' Manager, olant Operations *J.D. Bailey, Compliance Coordinator M.J. Wright, Manager, Plant Support L.F. Daughtery, Compliance Superintendent D.G. Cupstid, Start-up Supervisor R.H. McAnuity, Electrical Superintendent *J.P. Dimmette, Manager, Plant Maintenance W.P. Harris, Compliance Coordinator *J.L Robertson, Licensing Superintendent L.G. Temple, I & C Superintendent *J.H. Mueller, Mechanical Superir,tendent L.B. Moulder, Operations Superintendent *S.F. Tanner, Manager, Nuclear Site QA J.V. Parrish, Chemistry / Radiation Control Superintendent *J.W. Yelverton, Acting Manager, Plant Operations *F.W. Titus, Director, Nuclear Plant Engineering *S.M. Feith,- Director, QA Other licensee employees contacted included technicians, cperators, security force members, and office personnel. * Attended exit interview 2. Exit Interview (30703) The inspection scope and findings were summarized on April 17, 1987, with those persons indicated in paragraph-1 above. The licensee did not identify as proprietary any of the materials provided to or reviewed by the inspectors during this inspection. The licensee had no comment on che following inspection findings: 416/87-10-01, Inspector Followup Item, Diesel Generator fuel oil valve pit cover design change. (paragraph 4) 416/87-10-02, Inspector Followup Item, Determine source of water on SSW basin floor. (paragraph 4) 416/87-10-03, Inspector Followup Item, Failure of mechanics to properly assemble a relief valve. (paragraph 5)
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. - . * - . . ' 2 416/87-10-04, Violation, Failure to document an identified deficiency. (paragraph 5) 416/87-10-05, Inspector Followup Item, Standby Liquid Control surveillance procedure improvement. (paragraph 6) 416/87-10-06, Inspector Followup Item, Standby Diesel Generator (SDG) 12 start pushbutton troubleshooting. .(paragraph 6) 416/87-10-07, Inspector Followup-Item, Method of venting air pressure from SDG air start lines. (paragraph 6) 416/87-10-08, Inspector Followup Item, Required SDG fuel oil tank levels. (paragraph 6) 416/87-10-09, Violation, Failure to implement the SSW basin acid addition system per the temporary alteration. (paragraph 9) 416/87-10-10, Violation, Failure to install hydraulic control units per design drawings. (paragraph 8) 3. Licensee Action on Previous Enforcement Matters (92702) (Closed) Violation 416/84-54-01. The licensee has issued Nuclear Produc- tion Department Procedure 1.14, Verification and Certification of Submittals and Information, to establish a method to be used for review of any information that is to be submitted to the NRC. Attachment II to Procedure 1.14 provides guidelines for verification and certification of submittals and information. This action should ensure future submittals are accurate. 4. Operational Safety Verification (71707) The inspectors kept themselves informed on a daily basis of the overall plant status and any significant safety matters related to plant opera - tions. Daily discussions were held with plant management and various members of the plant operating staff. The inspectors made frequent visits to the control room such that it was visited at least daily when an inspector was on site. Observations included instrument readings, setpoints and recordings, status of operating systems, tags and clearances on equipment controls and switches, annunciator alarms, adherence to limiting conditions for operation, temporary alterations in effect, daily journals and data sheet entries,
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control room manning, and access controls. This inspection activity
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included numerous informal discussions with operators and their seper-
[ visors. 4
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. . . , 3 Weekly, when the inspectors were onsite, selected Engineered Safety Feature (ESF) systems were confirmed . operable. The confirmation is made :by verifying the following: Accessible valve flow path alignment, power supply breaker and fuse status, major component leakage, lubrication, cooling and general condition, and instrumentation. General plant tours were conducted on at least a biweekly basis. Portions of the control building, turbine building, auxiliar'y building and outside areas were visited. Observations included safety related tagout verifica- tions, shift turnover, sampling program, housekeeping and general plant conditions, fire protection equipment, control of activities in progress, radiation protection controls, physical security, problem identification systems, and containment isolation. At least monthly, the licensee's onsite emergency response facilities were toured to determine facility readiness. The folicwing comments were noted: On April 1, 1987, the. inspectors noted that the valve pits for the Divisions 1, 2 and 3 diesel generator fuel oil tanks were nearly full of water. Licensee personnel were in the process of pumping the water out. This condition was previously identified in NRC Inspection Report 86-20 when an ESF walkdown was conducted. At that time the Division 3 valve pit was found full of water due to the design of the cover. The licensee enlarged the covers to overlap the opening of the pit, however the new design has since proved itself to be inadequate as evidenced by the presence of water. The licensee is presently working on a solution. This shall be Inspector Followup Item 416/87-10-01. While touring the Standby Service Water (SSW) basins the inspectors noted the following discrepancies: Basin A SSW pump motor (P41C001A) had a junction box on the motor housing with the cover off and hanging by a restraining chain. Several loose wires were hanging out of the junction box and a loose screw was laying inside the junction box. On the wall behind the High Pressure Core Spray (HPCS) service water pump motor (P41C002C), a junction box cover was loose and hanging by only one screw. The floor in both areas was completely covered in water. Basin B SSW pump motor (P41C0018) had a similar junction box on the motor housing as P41C001A. It also had the cover off with several loose wires hanging down. The floor in the B basin arca was dry. The licensee was notified of the above discrepancies and took corrective action. The inspectors questioned the source of tha excessive water on the SSW basin floor since there was no obvious source. The source of water inside the SSW pump rooms will be Inspector Followup Iten 416/87- 10-02. ,
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. - . . * . ' 4 -The inspectors ' noticed, on repeated occasions, water on the floor in the RCIC/RWCU mezzanine on auxiliary building level _119. The water appeared to be leaking from the steam tunnel floor piping penetrations above. The-
. operators explained that due to leakage in the steam tunnel, water must be
. drained from the steam tunnel floor every shift or it overflows through the penetrati.ons to the area below. One of the areas where water is collecting _ on the floor is a high contamination area and leakage seems to persist ' independent of- draining the steam tunnel floor. The inspectors expressed concern that it is a . poor radiological work practice to allow this leakage to exist uncollected and uncontrolled. The licensee has corrected this condition by collecting the water and directing it to a drain. No violations or deviations were identified. 5. Maintenance Observation (62703) . During the report period, the inspectors observed portions of the maintenance activities listed below. The observations included a review of the work documents for adequacy, adherence to procedure, proper tagouts, adherence to technical specifications, radiological controls,
- observation of all or part of the actual work and/or retesting in
progress, specified retest requirements, and adherence to the appropriate quality controls.
E 1653 M71253, Repair, resetting and retesting of Standby Liquid Control
System Pump A discharge relief valve C41-F029A. MWO EL3567, General Maintenance Instruction 07-S-12-71, Revision 3, calibration checks of Time Delay Relays. MWO E71482, Replace Time Delay Relay Block.
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- MWO E71202, Install chart recorder and monitor points on Division 1
and 2 diesel generators related to previous Division 1 diesel
, generator output breaker trip. . On March 12, 1987, the inspectors witnessed the restoration to service and
retesting of relief valve C41-F029A. When the operator opened the Standby Liquid Control pump suction valve, water leaked profusely out of the relief valve gagging screw plug. The operator immediately shut the suction valve to stop the leakage. The inspectors noted that this was not an ordinary mechanical joint leak, but rather, the gagging screw plug was not properly installed when the valve was reassembled in the shop. The leak was corrected by maintenance tightening the plug, and then the valve passed the retest. When the NRC inspector questioned a QA inspector who was present for the retest if a deficiency report or other document was initiated to document the deficiency, the response was negative, nor did
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_ .- . . . , 5 he indicate any intention to do so, because he stated he did not consider the official retest as having started. The operator failed to d]cument the deficiency also. This is a failure to comply with GGNS Administrative Procedure (AP) 01-S-03-2, Quality Deficiency Reports (QDRs). Section- 6.1.1 requires all quality deficier.cies, unless identified on another deficiency document, to be documented in accordance with this procedure. The inspectors reviewed MWO 71253 to determine if adecuate instructions existed to ensure the valve was properly reassembled. There were no detailed instructions nor was the vendor manual-referenced, thus the work instruction appeared to be inadequate. The inspector expressed concern to the licensee over the way this job was handled, with particular emphasis on a QA representative's reluctance to insure that the apparent deficiency , was documented. Subsequently the licensee issued two QDRs (144-87 and 145-87) which identified a lack of knowledge on the part of the mechanic reassembling the valve and failure of MWO 71253 to provide adequate instructions. Upon investigating, the licensee deternined and r ported to the inspectors that the applicable vendor manual was used for the work on the relief valve, although not referenced in the MWO. The licensee stated that failure of the mechanics to properly assemble the relief valve was indicative of a training deficiency, and that appropriate corrective actions will be documented as 00Rs 144-87 and 145-87 are processed. Followup inspection of actions taken shall be tracked under Inspector Followup Item 416/87-10-03. Section 16.0 of the licensee's NRC-approved Operational Quality Assurance Manual, MPL-TOPICAL-1, Revision 5, requires, in part, that measures shall be established to ensure that conditions adverse to quality, such as deficiencies, are promptly identified and corrected. AP 01-S-03-2 established this measure. Failure to pronptly document the deficient reassembly of C41-F029A as evidenced-by the gagging screw plug being left loose is a violation of this requirement (416/87-10-04). QDR 168-87 was initiated by the licensee to identify the failure to document a defi- ciency, and corrective measures are being taken to ensure that such deficiencies are recognized and documented in the future. 6. Surveillance Observation (61726) The inspectors observed the performance of portions of the surveillances listed below. The observation included a review of the procedure for technical adequacy, conformance to Technical Specifications (TSs), verification of test instrument calibration, observation of all or part of the actual surveillances, removal from service and return to service of the system or components affected, and review of the data for accept- ability based upon the acceptance criteria. 06-0P-1C41-M-0001, Revision 25, Standby Liquid Control System Operability.
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6 06-0P-1P75-M-0002, Revision 32, Standby Diesel Generator (SDG) 12 Functional Test. 06-IC-SD17-R-1025, Revision 22, Ef fluent System Flow Rate Monitor Calibration (Turbine Building Exhaust Radiation Monitor). 09-S-06-12, Revision 1,102.5% Core Flow Flux Controller High Limit Setting Verification. 06-0P-1P75-M-0001, Revision 32, Standby Diesel Generator (SDG) 11 Functional Test. During conduct of SLCS surveillance procedure 06-0P-1C41-M-0001 listed above, the inspectors noted that the precision test gauge connected at IC43R003 (SLCS pump discharge pressure) was oscillating violently as pressure was increased. At full discharge pressure the fluctuations from this positive displacement pump were so wide the end of the gauge pointer broke off. The operator experienced considerable difficulty in trying to maintain discharge pressure by throttling C41-F016 and at the same time throttling the pressure gauge isolation valve to dampen the oscillations. It was evident that he had marginal control over the system, and the probability of lifting the relief was high. The inspector expressed concern to the licensee that failure to obtain more positive control over this system during testing could lead to damage or unsatisfactory test results. The licensee indicated that the procedure will be changed to ensure better control, by the next time this quarterly surveillance is due, and that hardware ' changes are under consideration. This shall be tracked by Inspector Followup Item 416/87-10-05. During conduct of SDG 12 functional test 06-0P-1P75-M-0002 above, the diesel failed to start when the control room operator depressed the start pushbutten. i.fter reverifying prerequisites and finding no problems, a second attempt was made and the SDG started and came up to speed as required by the Technical Specifications. The Shift Superintendent informed the inspectors that a Maintenance Work Order (MWO) was initiated te troubleshoot the pushbutton. The inspectors will follow up to verify that the failure is identified and corrected as appropriate. This shall be Inspector Followup Item 416/87-10-06. Also during the SDG 12 surveillance above, the procedure required that the drain plugs be removed and reinstalled in the isolated air start strainers to depressurize the air start lines (steps 5.1.7 and 5.2.7). Since this section of piping gets pressurized over 200 psig, the mechanic satisfied this requirement by first loosening an instrument fitting to depressurize the piping so that the plug could be safely removed. This appeared to be stretching the intent of the procedure because the procedure does not specifically authorize the breaking of an additional air pressure boundary. The inspectors discussed this with the licensee who indicated that the procedure would be reviewed and revised as appropriate. This shall be Inspector Followup Item 416/87-10-07.
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* . 7 Following' the SDG surveillance the inspectors reviewed surveillance procedure 06-0P-IP75-M-0002, Revision 32. The procedure requires the operator verify that the fuel oil day tank contains a minimum of 220 gallons of fuel as indicated by at least 12 inches on fuel oil day tank level indicator LI-R607B on panel 1H13-P864. The inspector reviewed the control room round sheet and it required a minimum of 22 inches on LI-R607P. The inspector then reviewed several documents for fuel oil day tank and storage tank minimum level requirements and found the following numbers specified: Division 1 and 2 SDGs Day Tank Storage Tank [ l Yellow marking on control room 22 inches 6.2 feet level indicator Control room round sheet 22 inches 8.7 feet . . Alarm Response Instruction 23 inches 8 feet 8 04-1-02-1H22-P400-1A-C1 inches ~ DG Functional Test (06-0P-1P75- 12 inches 8 feet 8 M-0001/0002) inches Division 3 SDG (HPCS) Yellow marking on control room 10 inches 5.4 feet level indicator Control room round sheet 10 inches 6.3 feet Alarm Response Instruction 9.5 inches 76 inches 04-1-02-1H13-P870-5A-El DG Functional Test (06-0P-1P81- 12 inches 5 feet 11 M-0002) inches The Division 1 and 2 SOG day tank fuel oil level meters on the local panels read in 1/8th tank increments. When observed on April 3,1987, during a surveillance test, the Division 1 meter read 3/4 full when the control room indicator read 28 inches (out of 60 inch span). Discussions with the licensee indicate that the day tank level (for all three divisions) mest be a minimum of 12 inches to satisfy TS requirements. This would indicate that the HPCS SDG day tank level could be less than TS requirements on several indicators noted above and would be considered acceptable. Since there is an automatic fuel oil transfer pump for maintaining the day tank level well above TS limits, there is little possibility of being below TS limits during actual operation. The licensee was requested to evaluate the numerous values noted, determine the appropriate value and revise the SDG fuel oil level requirements to be consistent with TS limits. This will be Inspector Follow-up Item 416/87-10-08. _ _ _ _ _ _ _ _ _ _ _
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." . . 8 No violations or deviations were identified. ' . 7. Reportable Occurrences (90712 & 92700) The below listed event reports were reviewed.to determine if the informa- tion ' provided met the _ NRC . reporting requirements. The determination included adequacy of event description ' and corrective action taken or planned, existence of potential generic problems and the relative safety significance of each event, Additional inplant reviews and discussions with plant personnel . as appropriate were conducted .for the reports indicated by an asterisk. The event reports were reviewed using the - guidance of the general policy and procedure for NRC enforcement actions, regarding licensee identified violations: The following license Event Reports (LERs) are closed. LER No. Event Date Event ' *85-033 August 30, 1985 Unit 2 ultimate heat sink components required for Unit 1 operability. *86-027 August 15, 1986 Fire watches exceed TS required frequency. The event of LER 86-027 was addressed in Inspection Report 416/86-24. LER 85-033 reported that portions of the Unit 2 SSW system required to support the seismic qualification of_the Unit 1 SSW system were not under the operational -control of the plant. Other Unit 1/ Unit 2 interface concerns were subsequently identified. In lieu of updating this LER the licensee submitted a Special . Report, Unit 1/ Unit 2 Interface (AECM-87/ 0077) to provide a comprehensive review of actions taken and planned. This LER is closed and the Unit 1/ Unit 2 interface concern will be tracked under violation 416/86-17-03 2nd the special report update. Due to the number of problems associated with the Standby Service Water (SSW) system and their potential safety impact, an enforcement conference was held in the NRC Region II office on February 4,1987, as documented in Inspection Report 416/87-03. Report 416/87-03 and LER 86-029 stated the licensee would initiate an independent design review of the SSW system. On March 18, 1987, the licensee reported that during the SSW design review it was determined that a postulated single failure could cause the loss of the SSW system / Ultimate Heat Sink (VHS) 30 day water inventory. A loss of power from Motor Control Center (MCC) 15B61 would leave valves P41F125 and P41F066A open which could allow the flow of SSW from the A SSW train to the Plant Service Water (PSW) system through 3 inch cross connect piping. This would result in the loss of cooling water to the A train control room air conditioning condenser but the B train would still be available. The
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. - . 9 loss of SSW water through the cross connect piping would eventually result in the excessive loss of UHS inventory. As interim corrective action the licensee issued night orders to tag close PSW to SSW cross connect valves P41F125 and P41F189 with SSW supplying the operable control room air conditioner (PSW normally supplies control room air conditioner cooling water). Tne licensee conducted a safety evaluation to assess the ability of the SSW/ UHS to meet established design criteria with the design deficiency noted above but with the implementation of appropriate administrative controls for operator action. The safety evaluation determined that with appropriate operator action within 7 hours, no unreviewed safety question exists. Off-Normal Event Procedure (ONEP) 05-1-02-I-4, Loss of Offsite Power and ONEP 05-1-02-V-11, Loss of Plant Service Water, were revised to incorporate the recommended administrative controls. Based on the above actions, the licensee secured the SSW system and returned the PSW/SSW isolation valves to their normal lineup. (Closed) P2184-07, Bonney Forge Non-Conforming Material . Based on a request from Nuclear Plant Engineering (NPE), Bechtel Power Corporation conducted a review of materials supplied to the licensee which originated from Bonney Forge. It was determined that no materials having the heat numbers identified as potential problem material were used in the construction of any Unit I nuclear piping systems. Based on the study results, the licensee determined no action was required. (Closed) P2185-01, Containment Purge Valve. Based on a Henry Pratt Information Letter, Nuclear Plant Engineering recommended to Plant Staff that Locktite be used on all four sides of the shaft key during reassembly on any Pratt valve and Limitorque operator. The valve driven gear spline adapter and key are secured to the valve shaft by a force fit together with the use of Locktite. Based on NPE recommendations the plant staff revised Maintenance Section Procedure 07-S-08-510, Installation, Reinstal- lation, Disassembly and Reassembly of valves, to require the use of Locktite grade 242 or 271 as recommended. No further action was required. Subsequently, 07-S-08-510 was superseded by Plant Modification and Construction Section Procedure 15-S-02-502 which also incorporated the above recommendativn. (Closed) P2186-02. The Electro-Motive Division of General Motors reported that upper connecting rod bearings had been found with mislocated dowel holes. Morrison-Knudsen Company, manufacturers of the High Pressure Core Spray (HPCS) diesel generator system notified General Electric (GE) which supplied the HPCS diesel to SERI. GE informed SERI that only connecting rod bearings purchased between November 1985 and April 1986 were suspect and require inspection. GE records indicate they neither purchased nor supplied any connecting rod bearings to MP&L (now SERI) for the Grand Gulf Plant during this time frame and no further action is required. __ _ . . . _ . _ ._. _
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10 (Closed) P2186-04, BBC Brown Boveri, Inc. K600/K800 Circuit Breakers Wire Harness. On June 30, 1986, the NRC was notified of a 10 CFR Part 21 report identifying a condition in the type K600S circuit breakers stpplied by BBC Brown Boveri, wherein a control wire harness came into direct contact with a racking gear inside the breaker. The gear teeth had worn through the protective cover and severed a wire causing a grounded condition. The licensee was also notified in June 1986. During the first refueling outage (October 1986 thru January 1987) the plant staff inspected 26 out of 26 E5F breakers scheduled and 40 out of 60 balance of plant breakers scheduled for inspection and found no damage to the wiring harness. The remaining breakers will be inspected during the normal inspection program. General Maintenance Instruction 07-S-12-50, Inspec- tion and Calibration of.480V ITE K600S-K1600S Breakers, has been updated to inspect breakers for this problem. No violations or deviations were identified. 8. Inspector Followup and Unresolved Items (92701) (Closed) Inspector Followup Item 416/85-05-01. This item was addressed in Inspection Report 416/87-06 and was inadvertently listed as an open item when it should have been closed. This is to document the closure of 416/85-05-01. (Closed) Inspector Followup Item 416/86-39-03. Correction of records on G.N. Bettis valve actuator seal replacements. The licensee issued a Quality Deficiency Report (QOR) to formally identify the problem and implement appropriate corrective actions. The inspectors reviewed the actions taken which included correction of the records by issuance of a record supplement and issuance of a memorandum to mechanical personnel frcm the Mechanical Maintenance Superintendent emphasizing their responsibilities as they relate to work documentation. The records, however, were not adequately corrected. The inspectors noted that in an effort to correct the record for valve E61-F009 (Task Card No. ME0027), the licensee added another copy of the erroneous material ticket instead of deleting or annotating that it was not applicable to E61-F009. The inspectors have since verified that this has been corrected. QA issued another QDR (87-1073) to document the incorrect records correction and actions taken to ensure that record supplements are more carefully screened in the future. (Closed) Unresolved Item 416/87-01-04. Resolution of missing fasteners on control rod drive Hydraulic Control Units (HCU's). This item was previously addressed in NRC Inspection Reports 416/87-01 and 416/87-05. On February 6, 1987, during a tour of the containment the inspectors found that one fastener required for securing HCU 36-13 to the foundation was missing. It was apparent to the inspectors that the fastener had never been installed, and thus a concern was raised as to the as-built condition, and thus the seismic qualification of the other 192 HCUs. The licensee was requested to provide documentation that supports this and any
. - . 11 other deficient HCU installations. There was no ' documentation on file which would allow the fastener to be missing from HCU 36-13. The fastener was replaced, a 100% inspection was conducted on the other HCUs and other deficient fastener installations were corrected, confirmed acceptable by review of previous documentation, or accepted in their as-found condition by additional engineering analysis. From the results of these actions, it appeared that about 36 HCUs were operated in an unanalyzed, deficient condition with regard to seismic qualification from plant licensing until February 1987. A major effort was implemented by the licensee to review HCU installation records, to accurately document the as-found condition of the 193 HCUs and to perform proper engineering analyses of the condition as-found and after repairs (as-left). As was reported in NRC Inspection Report 416/87-05, the inspectors expressed concern that the licensee had not probed this problem to the depth necessary when the concern was initially raised. As a result, the licensee also implemented a review of program requirements for handling such problems. On April 10, 1987 the licer.see presented a documentation package containing the investigation results and disposition of deficiencies found on HCU mounting fasteners. The inspectors met with the 1.censee to _ discuss the package and then reviewed it for accuracy and completeness. Based on the information provided in the package and independent observa- tions made on the equipment by the inspectors, it appears that prior to discovery of the missing fastener on HCU 36-13 on February 6, 1987, 150 of the 193 HCUs had an average of about three fasteners (of eleven) with less than the recommended torque shown on drawing 767E800, Hydraulic Control Unit, five HCUs had a mounting bolt missing without having in its place the equivalent weld required by Bechtel Supplier Deviation Disposition Request (SDDR) M-316.0-016 and General Electric Field Deviaticn Disposi- . tion Request JB1-471. There were also a few isolated instances of missing washers, broken bolts, missing nuts, and welds which were the incorrect size. It was erroneously presumed by the licensee, however, that as of May 30, 1982, all HCOs were mounted properly by the subcontractor, Reactor Controls, Incorporated (RCI), in accordance with the applicable drawings and specifications, and that any missing bolts had an equivalent weld, as approved by the above SDDR. Therefore the system was operated in an unanalyzed condition until after February 6, 1987, when the deficient, as-found condition was corrected as much as practicable and as- corrected analysis was performed by Nuclear Plant Engineering. 10 CFR Part 50, Appendix B, Criterion V states, in part, that activities affecting quality shall be accomplished in accordance with documented instructions and drawings of a type appropriate to circumstances. Contrary to this, 156 of 193 HCUs were not mounted in accordance with the applicable drawings and specifications during plant operation. This is a violation. (416/87- 10-10). The licensee performed a safety analysis of the HCUs in the as-found condition. The analysis assumed that no fasteners were torqued to provide the preload recommended, the various configurations of missing fasteners were considered, welding provided under the above SDDR was conservatively neglected in the calculation, and fasteners that were not fully seated were assumed to be missing. The results of that analysis concluded that the as-founJ conditions did not result in safety concerns which would have jeopardized the integrity of the reactor coolant pressure boundary,
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12 reduced capability to achieve and maintain reactor shutdown, or reduced capability to prevent or mitigate the consequences of an accident. The licensee has indicated that corrective actions for this violation will include a review of other safety related work performed by RCI and will provide documentation as to results and additional actions if appropriate. 9. Design, Design Changes and Modifications (37700) The inspector reviewed the licensee's program for temporary alterations. Administrative Procedure (AP) 01-S-06-3, Control of Temporary Alterations, Revision 20, was reviewed to verify controls were in accordance with TSs,10 CFR 50.59 and the approved QA program, MPL-TOPICAL-1. Adequate controls are specified in tne procedure to ensure independent verifica- tion, modification status, proper restoration, and records retention and periodic verification of outstanding alterations. The Temporary Altera- tion log was reviewed and several Temporary Alterations were verified. The inspector had the following comments: Temporary Alteration 87-0005. The Temporary Alteration Request Form (Attachment I to 01-S-06-3) did not have the tag numbers entered and the installed tags did not have individual numbers. The Shift Supervisor initiated a QDR to correct the tag numbers. Temporary Alteration 86-0034. The installation of an acid storage tank and related piping to add chemicals to the Standby Servi e Water (SSW) basins was accomplished by this alteration. A Temparary Alteration Request Addendum, Attachment III to 01-S-06-3, shows the installation details for this temporary alteration. A visual inspection of the actual installation showed that the installed piping and valves did not agree with the temporary alteration. At each basin the installed piping divided into two lines with an installed valve in each line. Additionally the inspector observed the following discrepancies. Valve FTA6, fill line to the acid tank, was broken off and laying in the tank pit area. Valve FTA4B had no handle and no identification (temporary altera- tion) tag attached. The 4 inch drain line from the acid tank berm to the SSW B basin was disconnected between the berm and the first isolation valve (FTA7) which provided a leak path directly to the ground. TS 6.8.1 requires written procedures to be established, implemented and maintained covering the procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Appendix A of Regulatory Guide 1.33 recommends procedures covering the bypass of safety functions and jumper control. Administrative Procedure 01-S-06-3, paragraph 6.1, requires temporary alterations to be documented and controlled using temporary alteration forms (Attachments I and III). The failure to implement the installation of the SSW basin acid storage tank and related piping in accordance with the approved temporary alteration is a violation. This is violation 416/87-10-09. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _
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