ML20203D558

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Insp Rept 50-416/97-21 on 971019-1129.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20203D558
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 12/05/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20203D508 List:
References
50-416-97-21, NUDOCS 9712160224
Download: ML20203D558 (18)


See also: IR 05000416/1997021

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.: 50-416

License No.: NPF 29

Report No.: 50 416/97 21

Licensee: Entergy Operations, Inc.

Facility: Grand Gulf Nuclear Station

Lncation: Waterloo Road

Port Gibson, Mississippi 39150

Dates: October 19 through November 29,1997

inspectors: J. Dixon Herrity, Senior Resident inspector

K. Weaver, Resident inspector

Approved By: D. Kirsch, Chief, Project Branch F

Division of Reactor Projects

Attachment: Supplemental Information

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9712160224

DR 971205

ADOCK 05000416

PDR

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EXECUTIVE SUMMARY

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Grand Gulf Nuclear Station l

NRC Inspection Report 50 416/97 21

Qeerations ,

  • Operations shift turnovers were thorough and conducted professionally

(Section 01.1).

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  • (Jonlicensed operators were knowledgeable of the equipment and their duties and j

responsibilities (Section 01.2).  !

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Maintenance

-* Workers were knowledgeable of equipment and tha scope of the planned work  ;

activities. Foreign material exclusion controls were good during work activities in

and around the spent fuel pool area (Section M1.1).

* The licensee identified a second maintenance preventable functional failure on the -

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Division 2 standby diesel generator due to the failure of the jacket water couplings

(Section M1.1).

  • Control roorn operators demonstrated good independert verifications, self checking

techniques, and communications during the observed s Jrveillance testing activities

(Section M1.2).

  • One example of a violation was identified for the failure to ensure that a -

procedurally required clearance between scaffolding and safety-related equipment

was either maintained or approved by engineering (Section M4.1). 1

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  • Reactor engineering personnel provided continuous oversight and good support

during the irradiated control rod blade processing (Section M1.1).

Plant Support

  • In general, housekeeping and component material condition in the plant were good.

_However, housekeeping and combustible material controls were in need of much

improvement in the hot machine shop (Section M2,1).

  • Health physics provided good support during the waste processing in and around

the spent fuel pool area. Workers appropriately adhered to radiological work permit

requirements and demonstrated good radiation worker practices (Section R1.1).

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  • A second example of a violation was identified regarding the failure to obtain

engineering approval prior to securing three steel stanchions to an overhead

safety-related cable tray and its associated supports (Section R1.2).

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fleport Details

Summarv of Plant Status

The plant remained at or near 100 percent power throughout this inspection period.

I, Opergligng

01 Conduct of Operatiort

01.1 General Comments (71707)

The inspectors conducted frequent reviews of ongoing plant operations, attanded

daily operations shif t turnovers, plan-of the-day meetings, and performed plant

tours. Daily operations shift turnovers were thorough and conducted professionally.

However, the inspectors observed that, generally, numerous telephone calls came

into the control room during shift turnovers. Operations management had

determined that shift turnover times were to be considered quiet time end had

directed the plant staff to refrain from contacting the control room during these

periods. The inspectors discussed this concern with the operations superintendent.

During one of these observations, the superintendent observed and recognized the

same concern and stated that management was discussing plans on how to

eliminate these distractions.

01.2 Nonlicensed Operator Rgynds (71707)

On November 9,1997, the inspectors accompanied the nonficensed operators in

charge of the outside areas on their routine rounds to the plant radial well pump

houses, switchyard, and meteorological tower. The inspectors found the

nonlicensed operators knowledgeable of the equipment and their duties and

responsibilities. The nonlicensed operators appropriately documented all equipment

parameters and instrument readings in accordance with procedures. The inspectors

found that housekeeping and material condition in the switchyard and

j meteorological tower areas were good.

01.3 Conclusions

Operations shift turnovers were thorough and conducted professionally.

Nonlicensed operators were knowledgeable of the equipment and their duties and

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responsibilities.

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07 Quality Assurance in Operations

07.1 Safety Review Committee Meetino (71707)

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On October 21,1997, the inspectors attended a safety review committee meeting.

The inspectors observed good discussions among safety review committee

members on the presentations made during the meeting. Contractors on the

committee were appropriately critical of the licensee's actions. The members met

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the quorum requirements specified by the Technical Specifications. The inspectors

concluded that the safety review committee activities were effective.

II. Maintenance

M1 Conduct of Maintenance

M1.1 General Maintenance Comments

a. Insoection Scoce (62707)

The inspectors observed portions of maintenance activities, as specified by the

following work orders (WOs):

levelindication bubbler tube

  • WO 00197427 Troublerhoot/ replace Division 2 standby diesel

generator solenoid Valves 1P75F537B and 1P75F538B

  • WO 00196569 Perform Division 2 standby diesel generator pneumatic

control simulated engine run

  • WO 00194183 Process, package, and ship for d;sposal: irradiated

control rod blades, incore detecto.s, jet pump beams,

etc.

  • WO 00197629 Division 2 standby diesel generator jacket water

coupling leak repair

b. Observations and Findinns

in general, the inspectors found this work to be well planned and performed

satisfactorily. Workers were knowledgeable of the equipment and the scope of the

work activities. In general, foreign material exclusion controls were good during the

processing of the irradiated control rod blades in and around the spent fuel pool

area. However, the licensee did identify, and document in Condition Report

(CR) 19971150, that an unmarked clear plastic wrapping was found in the spent

fuel pool area during the evolution. Reactor engineering personnel proWed

l continuous oversight and good support during the irradiated control rod plade

processing.

During the postmaintenance test of the Division 2 standby diesel generator,

operators identified that the jacket water couplings on the diesel were leaking

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approximately 80 drops per minute. The operators had maintenance personnel

tighten the couplings, then started the diesel for a surveillance run. The leakage

increased to approximately a pint to a quart per minute. The operators secured the

diesel. The licensee identified this event as a valid maintenance preventable

functional failure of the diesel. The inspectors observed the replacement of the

coupling on November 12,1997. The licensee replaced the coupling with a

modified coupling from the same manuf acturer that had better sealing capability.

This was the second maintenance preventable functional failure identified on the

Division 2 standby diesel generator due to Jacket water coupling leakage. The first

maintenance preventable functional failure was described in NRC Inspection

Report 50-410/97 12. The licensee ran the Division 1 standby diesel generator to

verify that there was not a potential for common mode failure. The operators

observed that there was no leakage from the Jacket water couplings. The licensee

plans to replace all of the jacket water couplings through a design change in the

near future; however, the parts had not arrived at the site at the time of this failure,

c. Conclusions

Workers were knowledgeable of equipment and the scope of the planned work

activities. Foreign material exclusion controls were good during work activities in

and around the spent fuel pool area. Reactor engineering personnel provided

continuous oversight and good support during the irradiated control rod blade

processing. The licensee identified a second maintenance preventable functional

failure on the Division 2 standby diesel generator due to the failure of the Jacket

water couplings.

M1.2 General Surveillance Comments

a. Inspection Scone (617_231

The inspectors observed the performance of portions of the surveillance test,

Procedure 06 JP-1E21-0 0006, " Low Pressure Core Spray Quarterly Functional

Test," Revision 100,

b. Observations and Findinas

Control room operators performed well during the surveillance tests. Good

communications were observed between personnel in the field and the control room

operators. independent verifications were properly performed. All equipment

acceptance criteria specified in the test procedure were verified to be in compliance

with Technical Specifications and were met with no discrepancies,

c. Conclusions

Control room operators demonstrated good independent verifications, self-checking

techniques, and communications during the observed surveillance activities.

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M2 Maintenance and Material Condition of Faci" ties and Equ'.pment

M2.1 General Plant Tours

a. Inspection Scope (71750)

During tours of the plant, the inspectors reviewed the areas for proper

housekeeping, components for material condition, and any nonconforming

conditions.

b. Observations and Findinat

The general housekeeping and material condition continued to be good throughout

the plant. However, during a tour of the hot machine shop in the turbine building

on November 9,1997, the inspectors found weaknesses regarding housekeeping in

the area. For example, bags of contaminated and noncontaminated trash had not

been removed from the area. In addition, work incomplete tags, used cotton

gloves, plastic material, and various trash were scattered on the floor and in the

surrounding area. A container of liquid combustible material was found lef t

unattended with no matenal safety data sheet label. The inspectors had previously

found weak housekeeping in this area and documented this concern in NRC

inspection Report 50 416/97-06. The inspectors notified maintenance personnel

and CR 19971158 was initiated. The area was subsequently cleaned and a 1

material safety data sheet label with the combustible classification was affixed to

the container.

The inspectors contacted fire protection personnel to ascertain whether the trash

and combustibles could exceed the fire protection heat load calculations for the

area. Fire protection personnel walked down the area on November 10 and

determined that the heat load calculations for the area had not been exceeded.

The fire protection personnel performed a walkdown of the area again on

November 18 and found (1) weaknesses in housekeeping with rubber gloves, rubber

mats, and plastic bag material scattered on the floor, (2) paint spray cans with no

combustible permits, (3) polyethylene plastic combustible material with no permit,

and (4) two fire extinguishers that had not had a monthly inspection. The fire

protection personnel initiated CR 1997-1212 to document these concerns. The

licensee determined that CR 1997 1212 should be classified as a station level CR,

which would require a formal root cause evaluation in accordance with their

corrective action process.

During a tour of the auxiliary building on November 10,1997, the inspectors

identified a paper suit that had been inappropriately discarded in a cable tray with

energized cables in the Division 2 safety 4 elated switchgear room. The inspectors

notified health physics personnel and the paper suit was removed and surveyed for

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contamination. The inspectors were informed that no contamination was found on

the suit.

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c. Conclusion 1 k

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In general, housekeeping and component material condition in the plant were good;

however, housekeepir,g and combustible material controls in the hot machine shop

were in need of improvement.

M.4 Maintenance Staff Knowledge and Performance

M4.1 Scaffold Constructed Next to Safetv Related Comoonent

a. Inmoeolon Scope (627071

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The inspectors reviewed equipment material condition related to maintenance during

tours of the plant.

b. Observations and Findinns

On October 28,1997, the inspectors observed that one member of a scaffold built

under electrical penetrations on the 166-foot level of the auxiliary building contacted

the insulation of a small gauge pipe just under containment atmosphere sample inlet

Valve 1P33F572A, a safety-related valve. The inspectors reviewed

Procedure 15-S-01-106, " Scaffolding Erection," Revision 0, and

Standard GGNS-CS-05, " Standard for Erection of Scaffolding in Safety-Related

Areas," Revision O. These procedures required nuclear plant engineering approval

for scaffolding with clearances less than 6 inches from safety-related systems or

components.

The inspectors discussed the concern with modification and construction personnel

and requested a copy of the engineering evaluation performed. The inspectors

observed that the evaluation did not address the concern identified and that the

independent inspection required by Procedure 15 S-01 106, Step 7.4, for

Seismic 11/1 scaffolding had not been signed off on the scaffold roquest form. The

inspectors discussed the concerns with a modification and construction supervisor.

The supervisor explained that the carpenters were aware that an evaluation had

been performed and thought that the proximity to safety-related equipment had

already been addressed. The supervisor initiated CR 1997 1129 to document and

resolve the conccrns.

The inspectors discussed the general process of scaffolding construction and

approval with engineering personnel. The nuclear plant engineer, who approved

deviating from Standard No. GGNS-CS-05, walked down the area with modification

and construction personnel to plan the scaffold. However, there was no

requirement for the engineer who approved the deviation to review the scaffold

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af ter it was constructed to ensure it met the plans. The inspectors observed that

this was a potential weakness in the licensee's program, i

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-The licensee acknowledged that the clearances between the scaffold and the valve

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should have been evaluated by engineering. The licensee had the scaffold modified

to provide 6 inches of clearance from safety-related equipment and performed a >

review of all scaffolding that was erected at the site. The remaining scaffolding

was constructed in accordance with the procedure.

The inspectors determined that the failure to build the scaffold in accordance with

Procedure 15 S-01 106 was the first example of a violation of 10 CFR Part 50,-

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Appendix B, Criterion V (50 416/9721-01). The second example is identified in

Section R1.2. ,

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c. Conclusions

! One example of a violation was identified for the failure to ensure that a

procedurally required clearance between scaffolding and safety related equipment

was either maintained or approved by engineering.

M8 Miscellaneous Maintenance issues (92902)

M8.1 (Closed) Violation 50-416/9617-02: f ailure to revise work packages in accordance

with procedures on work scope. An electricien was efectrically shocked as a result

of the failure to revise the work package to reflect the current equipment status in

the plant. The licenseo determined that this event resulted from the failure to

update the work packegn, an inadequate prejob briefing, and a failure to thoroughly

check the panel to verify n at it was deenergized. % addition, the licensee

determined that the perwnnel had failed to follow the procedure for flagging

temporarily onergized equipment and that a temporary alteration package should

have been used to route temporary power in this case, rather than a temporary

procedure.

The inspectors reviewed the corrective actions taken and discussed how the

corrective action would prevent recurrence with the electrical and instrumentation

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superintendent. The licensee had determined that the barriers to prevent recurrence

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included insuring that the temporary alteration process was used in the future. The

licensee revised Procedure 01 S-07-1, " Control of Work on Plant Equipment and

Facilities," Revision 31, to require the impact statement be revised to reflect

changes in work scope or plant conditions. With the information provided by the

temporary alteration process, supervisors reviewing packages to be placed on the

schedule would be able to identify changes and would be required to have the '

packages revised. The prejob briefing procen was changed to require a 30 minute

supervisor turnover time. F.lectrical maintenance personnel were given training to

stress tho importance of voltage checks and flagging. The inspectors concluded

that the licensee's corrective actions were acceptable.

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111. Enoineerina

E8 Miscellaneous Engineering issues (92903)

E8.1 (Closed) Violation 50-416/9606-02: unsecured locker in remote shutdown p nel

room. The licensee determined that Procedure 01 S-07-43, " Safe Handling o1

Loose items inside the Plant," did not contain adequate direction for ensuring that

safety-related equipment would not be affected by loose, nonsafety-related items in

the plant. The licensee conducted an extensive tour and identified 59 different

items which did not meet the criteria specified in the procedure. The inspectors

reviewed the corrective actions taken in response to these items and concluded that

the loose items had been acceptably addressed. The inspectors reviewed the

revised procedure and performed walkdowns of the plant to determine if the

corrective actions were effective. Although the inspectorr, identified no similar

loose items, as documented in NRC Inspection Report 50-416/9712 and

Section R1.2 in this report, the failure to ensure an engineering evaluation is

conducted prior to securing items tn safety related equipmt,nt was still a concern.

The inspectors concluded that the corrective actions taker adequately addressed

the concern of leaving items unsecured in the plant.

E8.2 (Closed) Unresolved item 50-416/9703 02: evaluation of licensee conformance

with regulatory guide. This item was opened to further evaluate the licensee's

conformance with Technical Specification 5.5.7 for testing of ventilation filters and

to review the Office of Nuclear Reactor Regulation's response to the licensee's

request for an interpretation of the wording in Regulatory Guide 1.52, " Design,

Testing and Maintenance Criteria for Post Accident Engineered-Safety-Feature

Atmosphere Cleanup System Air Filtration and Adsorption Units of

Light-Water-Cooled Nuclear Power Plants." The inspectors reviewed the response

from the Office of Nuclear Reactor Regulation to Mr. Jerrold Dewease dated

September 11,1997. In the letter, the staff determined that the licensees were

expected to develop interpretations of the terms in regulatory guides to limit the

high efficiency particulate air and charcoal filter testing to situations which have the

potential to degrade engineered safety featurre filtration system efficiency. The

interpretations must be based on a well-documented, sound, and conservative

technical basis. The staff also documented that painting, fire, or chemical release is

not comrnunicating with a ventilation system if the ventilation system is not in

operation and the isolation dampers for the system are closed and leak tight,

thereby preventing air from passing through the filter.

The inspectors had identified that the licensee did not have a basis for the 1.5-hour

required wait time that they identified for the standby fresh air system and that the

licensee had no controls over the amount of paint that was being used in the areas

that communicated with the filtration systems. The licensee changed the 1.5-hour

wait time to 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> and instituted controls to limit the amount of paint or volatile

organic compounds that could be taken into the areas to an amount that would not

degrade the filtration systems. The inspectors found that the dampers on the

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standby gas treatment system were not leak tight and questioned whether the

filters could be affected by painting. The licensee addressed this concern and

documented their response to the letter in a package titled, " Programs Package for

Control of Volatile Organic Compounds in the Control Building." The package

documented that the auxiliary building was maintained at a negative pressure in

relation to the outside. The leakage past the dampers was coming from the

discharge vent from the outside, through the filter, and out a drain valve. The

inspectors reviewed the system drawings and concluded that this was the case and

that volatile organic compounds released during painting would not have the

opportunity to pass through the filters.

The inspectors reviewed the results of all of the past tests conducted on the

charcoal. The charcoalin the filtration units has passed tests performed every

18 months, indicating that there is no buildup due to volatile organic compounds.

The inspectors determined that the lack of controls that the licensee had in place

prior to the concerns being identified did not have a safety significant effect on the

plant due to the rewits of past tests. The inspectors concluded that the programs

that the licensee recently put in place, to address Regulatory Guide 1.52, were

appropriate.

E8.3 LQ1gaml) Unresolved item 50-416/9720-02: discrepancies identified with

containment electrical penetration nitrogen supply pressure. This item was opened

to review the purpose of Updated Final Safety Analysis Report Table 6.219,

" Primary Reactor Containment Penetration and Containment isolation Valve Leakage

Rate Test List," Note 14, and its relation to the electrical penetrations. The

inspectors discussed the concerns with the Office of Nuclear Reactor Regulation

and determined that the note could be interpreted to mean that the electrical

penetrations only had to be continuously pressurized at > P, when leak rate testing

was being performed. Although the electrical penetrations were designed to allow

continuous monitoring, the Updated Final Safety Analysis Report does nit address

this function. The Office of Nuclear Reactor Regulation agreed that the inner two

o rings are the safety related seals required for containment isolation and the outer

two o-rings and the nitrogen supply system are nonsafety-related and were installed

to allow testing of the inner two o rings. Maintaining the penetrations pressurized

served no safety related function. The licensee initiated CR 19971024. The

inspectors concluded that the concern was nonsafety-related and would

appropriately be addressed by CR 1997-1024.

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IV. Plant Support

Ri Radiological Protection and Chemistry Controls

R1,1 Eackaaina of Irradiated Waste

a. Inspection Scope (71750)

The inspectors attended the crew prejob briefing for Radiation Work Permit

(RWP) 9710-001 which was written for the packaging of the irradiated waste in

the spent fuel pool performed under WO 00194183.

b. Observations and Findinas

The crew prejob briefing performed on November 5,1997, for RWP 97-10-001 was

thorough, and the RWP covered all the necessary information. Workers adhered to

the RWP requirements and demonstrated good radiation worker practices in high

contamination areas and high radiation areas during the work activities. Dedicated

health physics personnel continuously monitored the work activities performed

under RWP 97-10-001. In addition, health physics personnel installed additional

area radiation monitors on the fuel handling platform are on the fuel pool heat

exchanger prior to processing the control ro:! blades.

c. Conclusions

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Good health physics support was provided during the waste processing in and

around the spent fuel pool area. Workers appropriately adhered to RWP

requirements and demonstrated good radiation worker practices.

R1.2 HecIth Physics Eauipment Found Susoended From Safetv-Related Plant

Eauinment (71750)

a. Insocction Scope (71750)

The inspectors frequently performed walkdowns of the radiological controlled

access area and assessed radiological postings and worker adherence to protective

clothing requirements,

b. Observations and Findings

in general, radiological areas were properly posted, and area survey maps were

appropriately updated. During a 2 aur of the 139-foot elevation of the auxiliary

b'silding on NovemLer 10,1997, the insps.ctors identified three health physics

stanchions suspended . ; proximately 2 feet from the floor. The stanchions, each

weighing approximately 40 lbs., were tied with a rope to a Division 1 safety-related

cable tray and its associated supports in the overhead. The inspectors questioned

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contract workers in the area to ascertain the reason for securing the three

stanchions to safety related equipment. The contract workers stated that they were

preparing the auxiliary building floor for painting activities and that health physics

personnel had directed them to hang the stanchions from overhead < Jpment in

order to retain the posted radiation area boundary. Nuclear plant w< ating had

not been required to evaluate the praciice. The inspectors informec e a contract

workers and health physics personnel that plant procedures did not allow securing

loose items in the plant to safety-related equipment without nuclear plant

engineering approval. The stanchions were subsequently removed from the safety-

related equipment and CR 1997 1181 was initiated.

Procedure 01-S-07-43, " Safe Handling of Loose items inside the Plant," Revision 1,

Paragraph 5,11, stated in part, that equipmant; pioing; conduit; tubing; cable trays;

instrumentation; heating, ventilation, and air conditioning; and their associated

supports (safety-related and nonsafety related) are npj considered structural

elements ano cannot be used for securing loose items without nuclear plant

engineering approval.

The failure of health physics personnel to obtain nuclear plant engineering approval

prior to securing the three stanchions to the overhead safety related cable tray and

its associated supports was a second example of a violation of 10 CFR Part 50,

Appendix B, Criterion V (50-416/97021-01). The first example is addressed in

Section M4.1.

The inspectors identified a similar violation ia NRC Inspection Report 50-4?6/97-12.

The violation is discussed in Section R8.1 of this report.

c, Conclusionn

Radiological areas were properly posted and area survey maps were appropriately

updated. However, a second example of a violation was identified regarding the

failure to obtain engineering approval prior to securing three steel stanchions to the

overhead safety-related cable tray and its associated supports.

R1.3 Contamination Event and Unmonitored Release

a. insnection Scope (93702)

The inspectors reviewed the circumstances surrounding the unmonitored release

and contamination event and monitored the licensee's interim corrective actions and

cleanup activities.

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INSPECTION PROCEDURES USED

61726 Surveillance Observations

62707 Maintenance Observation

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71707 Plant Operations

71750- Plant Support Activities

92902 Followup Maintenance

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- 92903 Followup - Engineering

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' 92904 Followup - Plant Support

93702 Prompt Onsite Response to Events at Operating Power Reactors

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ITEMS OPENED CLOSED, AND DISCUSSED

Onened

, 97021 01 VIO Failure to ensure clearance from safety-related equipment

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was evaluated (Section M4.1) and is!!ure to evaluate the

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attachment of steel stanchions to a safety-related cable

r tray and the associated supports (Section R1.2)

97021 02 IFl Further review of the licensees investigation, the cause and

the licensee's corrective actions associated with the

unmonitored release and contamination event

(Section R1,3)

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b. 9_bservations and Findinus

At approximately 6 p.m. on November 24,1997, two workers who wera exiting the

protected area, alarmed the portal monitors at the security access point. The

individuals had contamination on their shoes.

Licensee investigation traced the contamination to the area around the condensate

storage tank, where a skid mounted hydrolaser was set up. This hydrolaser was

being used to provide wash water in the cask wash area of tt.e spent fuel pool. The

licensee determined that contaminated water was siphoned from the spent fuel pool

on November 21,1997. The hydrolaser wand had been lowered to the bottom of

the cask wash area and pressurized water was supplied to the wand to stir up

sediment in order that it could be vacuumed from the cask wash area. At one

point, the wand began floating towards the surface. As an emergency action

measure, personnel involved secured the pressurized water for about a two minute

time period until the wand could be removed from the cask wash down area. The

licensee believed that during this two minute period, the static head from the spent

fuel pool may have caused a siphon effect to occur. The licensee estimated that

the amount of contaminated water from the spent fuel pool that could have

migrated outside the radiological controlled access area onto the concrete and

gravel area was apprcximately 1.5 gallons.

Surveys of the area found contamination levels as high as 60,000 counts per

minute. This was the result of a direct frisk of a foot pedal for the hydrolaser skid.

The smearable contamination level for this pedal was approximately 30,000

disintegrations per minute. The licensee roped off the area as a contamination area.

Surveys detected contamination in a gravel area at a nearby storm drain. Upon

opening the drain cover and performing a large area survey in the drain, the licensee

detected contamination levels in the range of 1,500 disintegrations per minute.

This indicated that there was likely an unmonitored release from the radiological

controlled access area. The drain flows to a hold up basin and eventually flows to

the river. Upon further investigation, the licensee found that the contamination was

contained inside the storm drain piping upstream of the basin. The licensee had

implemented interim measures in anticipation of rain. These measures included

sealing the concrete surfaces by painting and digging up and removing

contaminated rocks and gravel around the drain.

At the end of this inspection period, the licensee had establisi.ed a significant event

review team to perform an investigation of this event to determine the root cause

and corrective actions to prevent recurrence. Further review of the licensee's

investigation, the cat.=e, and the ricensee's corrective actions will be conducted

through an inspection Followup Item (50-416/9721-02h

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R8 Miscellaneous Radiological Protection & Chemistry issues (92904)

R8.1 1 Closed) Violation 50-416/9712-01: failure to perform a required engineering

evaluation prior to resting an extension ladder on a safety-related cable tray. In

reviewing the violation, the inspectors noted that Procedure 01-S-07-43, may have

contributed to the violation in that the requirement to obtain engineering approval

could only be found by reading a note in the definition section of the procedure.

The inspectors considered this to be a weakness in the procedure and discussed it

with the licensee. Subsequent to the discussion, the licensee issued an addendum

to its initial response. The addendum was dated October 2,1997, and committed

to enhance the procedure by putting the note in a more visible section of the

procedure.

While reviewing the issue discussed in Section R1.2 of this report, the inspectors

reviewed the changes made to Procedure 01-S 07-43. The licensee had added

Step 6.10, titled " Scaffolding and Portable Ladders," and had placed the note under

this step. The inspectors interviewed the personnel involved in the situation

discussed in Scction R1.2 and determined that the individuals were not aware of

the requirement in Procedure 01-S-07-43 nor did Step 6.10 address securing " loose

items" such as the three stanchions identified in violation 50-416/97021-01. The

inspectors considered that the corrective actions taken in response to Violation 50-

416/97012-01 were too narrowly focused and were not effective in preventing

recurrence of the violation discussed in Section R1.2. Review of this issue will be

included in t'u followup to violation 50 416/97021-01.

P8 Miscellaneous Emergency Preparedness issues (92904)

P8.1 IClosed) Violation 50-416/9706-03: failure to have a qualified individual for the

offsite emergency coordinator position available. The licensee determined that the

root cause for this event was personnel error. The individuals involved and the

emergency preparedness staff were counseled. The inspectors concluded that the

licensee's corrective actions were acceptable.

V. Manaaement Meetinas

X1 Exit Meeting Summary

The inspectors presented the :nspection results to members of licensee management on

December 2,1997, following the conclusion of the inspection. The licensee acknowledged

the findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary ;o propri6tary information was identified.

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ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED '

Licensee -

D. Bost, Director, Nuclear Plant Engineering

_

C. Bottemiller, Superintendent, Plant Licensing .

J. Burton, Technical Assistant, Performance and System Engineering

L. Dale, Director,' Plant Projects and Support '

J. Hagan, Vice President, Plant Operations

C. Hayes, Director, Quality Programs

C. Holifield, Licensing Engineer, Plant Licensing

K. Hughey, Director, Nuclear Safety and Licensing

D. Janecek, Director, Training

E. Langley, Technical Assistant, Maintenance

T. Kriesel, Radiation Control Supervisor, Radiation Protection

L. Robertson,- Outage Management, Maintenance

C. Stafford, Operations Assistant, Plant Operation

- J. Venable, Manager, Operations

HEC

J. Donahew, NRR Project Manager

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3-

Closed

96006-02 VIO Unsecured locker in remote shutdown panel room

(Section E8.1)

96017-02 VIO Failure to revise work packages in accordance with

procedures on work scopo (Section M8.1)

97006-03 VIO Failure to have a qualified individual for the offsite

emergency coordinator position available (Section P8.1)

97003-02 URI Evaluation of licensee conformance with regulatory guide

(Section E8.2)

97012-01 VIO Failure to perform a required engineering evaluation prior to

resting an extension ladder on a safety-related cable tray

(Section R8.1)

97020-02 URI Discrepancies identified with containment electrical

penetration nitrogen supply pressure (Section E8.3)

97012 01 VIO Failure to perform a required engineering evaluation prior to

resting an extension ladder on a safety-related cable tray

(Section R8.1)