ML20148D450
ML20148D450 | |
Person / Time | |
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Site: | Grand Gulf ![]() |
Issue date: | 05/27/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20148D420 | List: |
References | |
50-416-97-06, 50-416-97-6, NUDOCS 9705300211 | |
Download: ML20148D450 (15) | |
See also: IR 05000416/1997006
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ENCLOSURE 2
U.S. NUCLEAR REGULATORY COMMISSION
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REGION IV
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Docket No. 50-416
License No.- NPF-29
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Report No.- 50-416/97-06
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Licensee: Entergy Operations, Inc.
Facility: Grand Gulf Nuclear Station
Location: Waterloo Road
Port Gibson, Mississippi
Dates: March 23 through May 10,1997
Inspectors: K. Weaver, Resident inspector
D. Proulx, Resident inspector, River Bend Station
S. Freeman, Resident inspector Trainee
Approved By: P. Harrell, Chief, Project Branch D
Division of Reactor Projects
ATTACHMENT: Supplemental Information
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9705300211 970527 i
PDR ADOCK 05000416 i
G PDR
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EXECUTIVE SUMMARY
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Grand Gulf Nuclear Station j
NRC Inspection Report 50-416/97-06 '
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The inspectors evaluated aspects of licensee operations, maintenance, engineering, and
plant support activities. This report covers a 6-week period of resident inspection.
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Operations
Plant operations was conducted both safely and professionally (Section 01.1).
Operations personnel conservatively suspended on-going work activities and took !
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appropriate precautionary measures during severe weather conditions
(Section 01.2)
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The inspectors identified poor implementation of procedure requirements while
observing operators in the simulator. The operators f ailed to complete the required
emergency procedure steps for the appropriate reactor core isolation cooling (RCIC)
system alignment (Section 05.1).
Maintenance
Performance of observed maintenance work was satisfactory. Workers were
knowledgeable of the equipment and the scope of work that was performed
(Section M1.1). !
Instrumentation and control technicians performing surveillance activities
appropriately stopped work, consulted with their supervisor, and obtained further
information, when it was not clear where to install a jumper. The instrumentation
and control technicians had established good communications with the control room
operators (Section M1.3).
Severe corrosion and flaking of the Standby Service Water (SSW) Loops A and B
return piping to Cooling Towers A and B was noted (Section M2.1).
Enaineerina
Tho licensee implemented appropriate corrective actions for Condition Report
(CH) 97-0295 and performed a techically sound engineering evaluation. A prompt
operability determination was made and prompt corrective actions were
implemented (Section E1.1).
System engineering had intented that a standing order be immediately issued by
operations to all on-shift personnel for the increase in the wait time from 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />
to 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> before running the standby fresh air units prior to commencing painting
activities in the control building. No standing order was issued, and operators
remained unaware of the increased waiting period approximately 1 week later
(Section E1.2).
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Plant Support
Poor housekeeping was noted in the auxiliary building hot machine shop
(Section M2.1).
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A health physics technician demonstrated poor performance by not checking out a
count rate meter and by not returning the meter to the health physics laboratory in
accordance with the established controls, which resulted in the meter exceeding its
j calibration check period while lef t in the auxiliary building (Section R1.2).
Failure to ensure that a qualified individual was available to respond for the
emergency organization (ERO) position of Offsite Emergency Coordinator was a
violation (Section P1.1).
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Report Details
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Summarv of Plant Status
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4 The plant remained at or near 100 percent power throughout this inspection period.
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J 1. Operations
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) O1 Conduct of Operations
i 01.1 General Comments
The inspectors conducted frequent reviews of ongoing plant operations, attended
plan-of-the-day meetings, and performed plant tours. The inspectors found that
j plant operations were conducted both safely and professionally.
l 01.2 Operations Performance Durina Severe Weather
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j a. Inspection Scoce (71707)
- The inspectors observed operator performance during severe weather conditions.
b. Observations
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On April 22,1997, the inspectors observed operators enter
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Procedure 05-1-02-VI-2, " Hurricanes, Tornados, and Severe Weather,"
Revision 101, because of impending severe weather reported from the Pine Bluff
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dispatcher. The inspectors reviewed this procedure and noted that operators had
performed all the required procedure steps. The inspectors noted that operators
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continuously monitored the severe weather and appropriately announced on the
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plant communication system to all personnel of the impending severe weather. The
inspectors also noted that the shift superintendent had conservatively suspended
on-going work activities until the severe weather had ceased and passed out of the
immediate area.
c. Conclusions
Operators conservatively suspended on-going work activities and took appropriate
precautionary measures during severe weather conditions.
01.3 Locked Valve Proaram
a. Inspection Scope
The inspectors evaluated the locked valve program to ascertain if the program met
regulatory requirements and commitments. This evaluation included a review of
Procedure 02-S-01-2 " Conduct of Operations," Revision 28.
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b. Observations and Findinas
The inspectors noted that Procedure 02-S-01-2, Attachment 111, " Component
Verification," provided directions for locking valves. This attachment states that red
colored tie-wraps of a substantial material were to be placed on throttle valves.
Blue colored tie-wraps were to be placed on valves fully opened or closed. The
inspectors toured the facility to determine the effectiveness of this methodology.
The inspectors noted that for most valves the tie-wraps provided an effective
method for controlling locked valves. The inspectors noted that severallocked
valves were located approximately 20 feet above floor level in the overhead. The
licensee had placed tie-wraps on the valve chains such that the tie wraps were not
required to be disturbed to operate these valves. The inspectors questioned if these
valves could be considered locked since the locking devices provided no barriers to
preclude inadvertent operation. Further, the inspectors noted that this method
would not indicate whether or not the valves had been tampered with. The licensee
stated that the tie-wraps for locked valves were not intended to secure the valve in
place or serve as a barrier to prevent inadvertent operation. The licensee further
stated that the locked valve program served to inform employees that certain valves
were important and should only be operated under special care. Therefore, the
licensee stated that their methodology for locking valves in the overhead was
sound.
The inspectors questioned the licensee's interpretation of the purpose of locked
valves. _ Technical Specification (TS) Surveillance Requirements (SR) 3.5.1.2
and 3.7.1.3 require the licensee to verify, on a monthly basis, that each valve in the
emergency core cooling and SSW systems that is not locked, sealed, or otherwise
secured in oosition is in its correct position. The bases for these TSs indicate that
the locked or sealed valves need not be verified because they were verified and
secured in position prior to installation of the locking or sealing device.
The inspectors expressed concern that, because valves in the overhead could be
operated without removing the tie-wraps, the licensee could not ensure that the
valves were not tampered with or inadvertently operated. The inspectors concluded
that further evaluation of the treatment of locked valves in the overhead was
warranted in that the locking methodology did not secure the valve in position or
provide indication that personnel did not tamper with the valve. This further
evaluation is considered an unresolved item (50-416/9706-01),
c. Conclusions
The method of locking valves located in the overhead and operated by chain falls
warranted further evaluation. The inspectors noted that placing tie-wraps on the
chains did not secure the valves in position or provide positive indication that the
position of the valve had not been changed since verification.
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01.4 Taaout Walkdown (71707)
The inspectors walked down Clearance GG-97-0611 to verify that all tags were
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attached to the proper components, that components were in the correct position
and that the tags were not defaced. No discrepancies were identified. ,
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05 Operator Training and Qualification
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! 05.1 Sirnulator Observations Durina Emeraency Drill Scenario
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a. inspection Scope (71707)
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The inspectors observed operator performance in the simulator during an emergency
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b. Observations l
During an emergency drill conducted on April 9,1997, the inspectors observed
operator performance in the simulator. The inspectors noted that the drill scenario
included a loss of offsite power. The inspectors had previously reviewed
Procedure 05-S-01-EP-2, " Reactor Pressure Vessel Control," Revision 24, and noted
that the procedure required that reactor pressure vessel water level be maintained
by the RCIC system with suction from the condensate storage tank. The inspectors
also noted that Procedure 05-S-0-EP 2, Attachment 1, " Defeating RCIC High
Suppression Pool Water Level Suction Transfer Interlock," provided instructions to I
defeat the RCIC high suppression pool water level suction transfer interlock by
removing Relay E51 A-K79. The procedure also required operators to open
Valve E51-F010, RCIC pump suction from condensate storage tank, and to close
Valve E51-F031, RCIC pump suction from suppression pool.
During the observation, the inspectors noted that the RCIC system maintained
reactor vessel water level with suction from the suppression pool instead of the
condensate storage tank. The inspectors questioned the assigned evaluator
concerning why the RCIC system was not aligned in accordance with
Procedure 05-S-01-EP-2. The evaluator investigated and replied that this was
considered a weakness and would be included in the critique following the drill.
The inspectors subsequently interviewed operations management concerning the
failure of the operators to appropriately perform Procedure 05-S-01-EP-2,
Attachment 1. Operations management investigated the error and concluded that
the operators had requested that Attachment 1 be performed but had not actually
read the attachment; therefore, they were not aware that further actions were
required to be performed on the simulator control panels. Operations management
stated that, in the future during emergency procedure training conducted on the
simulator., operators would be required to retrieve, read and request that emergency
procedure attachments be performed.
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b. Conclusions
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A weakness was identified during the operations simulator observations in that
operators failed to complete the required emergency procedure steps for the
appropriate RCIC system alignment,
ll. Maintenance
M1 Conduct of Maintenanco l
M 1.1 General Maintenance Comments
, a. Insoection Scoce (62703)
The inspectors observed portions of maintenance activities, as specified by the
following work orders (WOs):
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- WO 00185429: Room Cooler 1T4680018: Thermal Performance Test
b. Observations and Findinas
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observed was conducted in accordance with the instructions and procedures
provided in the work packages. Workers were knowledgeable of the equipment and
the scope of work that was performed. in addition workers appropriately adhered
to radiation work permit requirements and demonstrated good radiological
contamination controls.
M.1.2 Incorrect Confinuration of Rosemount Transmitters (71707)
On Apnl 15,1997, the inspectors noted that Rosemount Transmitters N00-3A and
N00-38, which are nonsafety-related transmitters installed in the fuel pool cleanup
system, had plastic shipping plugs installed in their spare conduit ports. The
conduit ports of Rosemount Transmitters contain plastic plugs for foreign material
exclusion during shipping. The licensee was required to discard the plastic plugs
and replace them with stainless steel plugs, upon installation, to preclude moisture
intrusion into the transmitters. The licensee initiated a condition identification and
replaced the plastic plugs. The licensee also performed walkdowns of safety-related
areas and identified no further concerns with Rosemount Transmitters. The
inspectors concluded that although this issue was not safety significant, this issue
indicated weak personnel knowledge of transmitter configuration.
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M1.3 General Surveillance Comments
a. Insnection Scope (61726)
The inspectors observed the performance of portions of the surveillance tests listed
below:
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Procedure 06-lC-1C51-R-0004, " Average Power Range Monitor (APRM)
Reactor Protect;on System (RPS) Response Time Test and 6-second Thermal
Power Time Constant Verification"
Procedure 06-OP-1E22-O-0005, "High Pressure Core Spray Pump Quarterly
Functional Test
- Procedure 06-EL-1 R21-M-0001-02, "4.16 KV Degraded Voltage Functional
Test and Calibration Division 2 Bus 16AB"
b. Observations and Findinas l
The inspectors noted that in general, the test procedures provided clear guidance
and properly implemented TS requirements. However, the inspectors noted that i
during the performance of Procedure 06-IC-1C51-R-0004, the instrumentation and I
control technicians performing the test stopped work at Step 5.5.5. Step 5.5.5 of i
Procedure 06-IC-1C51-R-0004 required removing the Thermal Trip Unit card from l
the average power range monitor and connecting a jumper in the circuit card. The
instrumentation and control technicians did not utearly understand from the
statement in Step 5.5.5 where to install the jumper. The instrumentation and i
control technicians appropriately stopped work and obtained a figure from another I
procedure, which clearly identified the jumper termination. An instrumentation and
control supervisor stated that Procedure 06-IC-1C51-R-0004 would be revised to
include this figure. The inspectors noted that the measuring and test equipment l
was within calibration. The instrumentation was removed from service, applicable l
limiting conditions for operation entered, and properly returned to service.
c. Conclusions
instrumentation and control technicians appropriately stopped work, consulted with
their supervisor, and obtained further information, when it was not clear where to
install a jumper as described in the procedure. The inspectors found the technicians
knowledgeable of the applicable equipment. The instrumentation and control
technicians had also established good communications with the control room
operators.
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' M 1.4 Surveillance of SSW Fans
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a. Inspection Scope (61726)
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The inspectors reviewed Surveillance Procedure 06-OP-1P41-M-004 " Standby
Service Water Loop A Operability," to determine if the surveillance properly !
implemented TS SR 3.7.1.2.
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b. Observations and Findinas
The inspectors noted that the surveillance implemented the TS as written; however,
the inspectors identified that Procedure 06-OP-1P41-M-0004 did not include all of
the tests as stated in the TS bases. The bases for TS SF.: 3.7.1.2 states that
operating each cooling tower fan for greater than 15 minates ensures that fan or l
, motor f ailure or excessive vibration can be detected for corrective action. However, i
. Procedure 06-OP-1P41-M-0004 only required the user to start the fans, run them
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for 15 minutes, and then secure them. No vibration monitoring or other predictive
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- The inspectors discussed this observation with operations management and the
, system engineer. The licensee stated that this description in the basis for TS
1 SR 3.7.1.2 was incorporated using the generic improved TSs and was not intended
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to require any additional site-specific action. The licensee took the position that the
- phrase in the bases for TS 3.7.1.2, " vibration can be detected," provided
l permission but did not dictate requirements. in addition, the licensee stated that
i the surveillance detected failures of the SSW cooling tower fans but not degrading
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performance identified by predictive maintenance.
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The inspectors concluded that further evaluation of the licensees position and the
TS bases for TS SR 3.7.1.2 was warranted to ensure that the current testing of the
SSW cooling tower fans met the intent of the TS SR. This is considered an
unresolved item (50-416/9706-02).
c. Conclusions
Further evaluation of the licensee's position and the bases for TS SR 3.7.1.2 was
identified as an inspection followup item to ensure that the current testing of the
SSW cooling tower fans met the intent of the TS SR.
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M2 Maintenance and Material Condition of Facilities and Equipment
i .: General Plant Tours
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a. Insoection Scope (71750)
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During tours of the plant, the inspectors reviewed the areas for proper
housekeeping, components for material condition, and other nonconforming
conditions.
b. Observations and Findinas
During plant tours, the inspectors noted that in general housekeeping continued to
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be good throughout the plant. However, the inspectors noted poor housekeeping in
3 the auxiliary building hot machine shop. In this area the inspectors identified pink
plastic wrap, which was used to wrap contaminated objects, on a shelf wadded up
with a piece of rope and other debris inside. The inspectors also noted several
pieces of soiled muslin, used cotton and surgical gloves, and discarded work
incomplete tags laying on the floor in the surrounding area. The inspectors also
noted soiled wet towels, which had been placed underneath equipment in the area.
The inspectors contacted health physics who surveyed the items for contamination.
The inspectors were notified that no contamination was found. The area was
subsequently cleaned and the debris appropriately discarded.
The inspectors interviewed maintenance management personnel to ascertain why
poor housekeeping conditions were found in the hot machine shop. The licensee
stated that personnel were removing tools and materials out of the area for
upcoming painting activities. The licensee further stated that a trash container was
subsequently placed in the area. During subsequent tours, the inspectors identified
no further problems with housekeeping in this area.
During another plant tour, the inspectors noted that a heavy lifting cart was secured
to a permanent plant Carbon Dioxide fire protection line. The licensee was notified
and, subsequently, removed the lifting cart. The licensee stated that the contractor
personnel involved were counseled on properly securing temporary equipment in the
plant for seismic purposes. The inspectors concluded that this occurrence was
isolated and not indicative of how plant personnel normally secure temporary
equipment.
During a tour of the SSW system on May 1, the inspectors noted severe corrosion
and flaking of the SSW Loop A return piping to Cooling Tower A. The inspectors
also toured the SSW B system and found the same corrosion and flaking of the
SSW Loop B return piping to Cooling Tower B. The inspectors notified the licensee.
Corrosion and flaking of the SSW A discharge piping was previously identified and
documented in NRC Inspection Report 50-416/97-03. The licensee had initiated
CR 97-0251 and had performed an ultrasonic test on the SSW A discharge piping
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identified in NRC Inspection Report 50-416/97-03 and had found the pipe wall
thickness to be greater then pipe minimum wall thickness. The licensee stated that
as part of the corrective action for CR 97-0251 a walkdown and a visual and ultra
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sonic examination of the SSW Loop A and SSW Loop B piping penetrations would
be performed.
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The licensee implemented appropriate actions to address poor housekeeping and
incorrectly secored temporary equipment identified by the inspectors.
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111. Enaineerina
E1 Conduct of Engineering
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E1.1 Seismic Qualification of Soare 480 Vac ITE K-600S Circuit Breakers
a. Insoection Scope (37551)
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The inspectors reviewed the corrective actions for CR 97-0295. This CR identified
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that several spare 480 Vac load center breakers were found in the fully racked out
position but were not previously evaluated for seismic qualification in that position.
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b. Observations and Findinas
This CR documented that the licensee found Breakers 52-15605,52-15502,
52-15504, and 52-16504 not in the connect, test, or disconnect position. These
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were spare ITE K-600S 480 Vac breakers located on safety-related load centers.
i The licensee promptly restored the breakers to the disconnect position. The
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licensee determined the as-found breaker position was not previously evaluated for
i a seismic event and entered Procedure 01-S-06-44, " Operability Determination,"
3 Revision 101. Subsequently, the licensee determined a seismic event would not
have resulted in a common mode failure of the load centers nor significantly
affected other components such that plant safety would be compromised. The
licensee did not declare any components inoperable.
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The inspectors reviewed Procedure 01-S-06-44 and the engineering evaluation to
assess the operability conclusion in the CR. The procedure followed the guidance
of Generic Letter 91-18 in dealing with operability and restoration of qualification
separately. The inspectors did not identify any deficiencies in the operability
determination and concluded that the determination was timely.
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c. Conclusions
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The inspectors concluded that licensee actions in handling CR 97-0295 were
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that the licensee had made a prompt operability determination and took prompt l
corrective action,
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E1.2 Failure To implement immediate Corrective Actions for the Standbv Fresh Air Units
(71707. 37551) i
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As documented in NRC Inspection Report 50-416/97-03, the inspectors had
identified a lack of administrative controls for painting activities in areas that
communicated with the engineered safety feature ventilation systems. As part of
the corrective action for CR 97-0195, system engineering determined that the
waiting period following painting of 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> before running the standby fresh air
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units was inappropriate and would be changed to 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. System engineering
personnel informed the inspectors that this corrective action would be implemented
prior to commencing painting in the control building.
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The system engineering manager verbally requested that operations issue a standing
order until the permanent plant procedure was updated. However, approximately 1
week later after noticing painting in the control building, the inspectors interviewed
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operators concerning the applicable wait time for running the standby fresh air units
following painting. The operators indicated that the wait time was 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. The
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inspectors questioned operations management as to why the new requirements
l were not promulgated to the operators. The manager indicated that the request I
was not performed immediately and, subsequently, was forgotten. A standing ,
order was immediately issued. The licensee initiated CR 97-0446 to address '
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possible programmatic deficiencies for implementation of the immediate corrective
actions. The inspectors determined that no violation of regulatory requirements I
occurred since the ventilation units had not been operated within 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> of the
painting.
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IV. Plant Support
R1 Radiological Protection and Chemistry Controls
R1.1 General Comments (71750)
The inspectors frequently toured the radiological controlled area and assessed
radiological postings and worker adherence to protective clothing requirements. In
general, radiological meas were properly posted, and locked high radiation doors
were properly Ic0Ked. Workers adhered to radiation work permit requirements and
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displayed good radiological worker practices. However, the inspectors identified
two frisker probes in the hot machine shop face down instead of the face up as
required.
R1.2 Out of Service Instrument Found in Auxiliarv Buildina
a. Inspection Scoce (71750)
The inspectors evaluated the licensee process for controlling radiation protection I
meters.
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b. Observations and Findinas
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During a tour of the auxiliary building on April 8,1997, the inspectors found a
LM12 count rate meter, which had last been calibration checked on April 5. The
count rate meter was required to be calibration checked daily. The inspectors
questioned maintenance workers, who were working in a contaminated area in
close proximity to the raeter, if they had used the meter. The workers responded
that they had not used the meter nor were they aware that it was in the area. The
inspectors questioned health physics personnel as to why the count rate meter was
in the auxiliary building since its calibration check was past due. The health physics i
technicians immediately removed the meter from the area. Also, the health physics
technicians stated that this count rate meter was previously identified as missing
and out of service and that they had previously searched for the meter.
The inspectors reviewed the health physics calibration check sheet to verify that
this count rate meter was previously identified as missing and out of service.
Procedure 08-S-01-70, " Health Physics Instrumentation," Revision 100, required
that instruments outside their calibration che::k be bagged and tagged as out of
service or placed out of service at the health physics laboratory. The inspectors
interviewed health physics personnel concerning their administrative controls for
their instruments and questioned why this count rate meter had not been returned
to the health physics laboratory for a calibration check in accordance with
Procedure 08-S-01-70. The inspectors found that health physics maintained a
computer database, and management expected technicians to check out
instrumentation prior to use. During interviews with radiation protection
management the inspectors found that a qualified health physics technician had
taken the meter from the laboratory without following the established expectations,
in addition, the same health physics technician left the meter in the auxiliary
building until the inspectors subsequently found the meter.
c. Conclusions
The inspectors concluded that the health physics technician demonstrated poor
performance by not checking out the instrument in accordance with the established
administrative controls and by not returning the meter to the health physic '
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laboratory after use. The inspectors determined that no violation of regulatory
requirements occurred since no one had used the meter with an out of date source
check, and the procedure did not require checkout or return of the meter.
P1 Conduct of EP Activities
P1.1 Failure to Provide a Qualified Individual to Fill the ERO Position of Offsite Emeraency
Coordinator
. a. Insoection Scope (71750)
During this inspection period, the inspectors reviewed CR 97-0429, which
documented that the licensee was unable to fill the ERO position of Offsite
Emergency Coordinator for approximately 7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
b. Observations and Findinas
On April 24,1997, licensee management personnel went to the NRC Region IV
Office in Arlington, Texas, for a meeting. Because of the number of managers
away from the site, it was questioned whether they could fill the ERO position of
Offsite Emergency Coordinator with a qualified individual. The inspectors i
determined that three individuals were qualified to fill this position. However, two
of the individuals were in Arlington, Texas, at the meeting and the other individual
was also unavailable. Procedure 01-S-10-6, " Emergency Response Organization,"
Revision 7, required that personnel assigned to the ERO must, during the scheduled
on call period, ensure that they are available to respond within the required time. In I
addition, Procedure 01-S-10-6 required that personnel assigned to the ERO must, if !
circumstances prohibit response within the required times, ensure that an alternate
(from the same ERO position) has agreed to and is available for emergency response j
coverage. This alternate must notify Emergency Preparedness of the arrangements
made.
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During interviews, the inspectors found that an individual who was " provisionally" l
qualified was available and was notified by the licensee to be on standby for this !
period. The inspectors reviewed Procedure 01-S-04-21, " Emergency Preparedness
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Training Program", Revision 101, and noted that this procedure stated that all ;
personnel who respond as part of the GGNS Emergency Plan shall be qualified in j
accordance with this procedure. Further, all personnel who are designated to '
augment station staffing (On-Call ERO) in accordance with Procedure 01-S-10-6
shall meet all qualification requirements of assigned position before being placed on
call. The licensee stated that the individual had completed the required training but i
did not have the appropriate qualification card reviews and signatures and the j
responsible reviewer was not available.
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p Failure to ensure that a qualified individual was available to respond for the ERO
position of Offsite Emergency Coordinator is a violation of Procedure 01-S-10-6 ,
(50-416/9706-03).
S1 . Conduct of Security and Safeguards Activities -
I' S 1.1 ' General Comments (71750)
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[ The inspectors accompanied security personnel during.a routine survey of the
security lighting system on April 10. The inspectors found security personnel '
i' knowledgeable of the security lighting requirements for the isolation zones and all
j exterior areas. No problems were identified with the exception that, during the
survey, security personnel and the inspectors found a worker who appeared to be
i sleeping inside a vehicle. The inspectors reviewed Procedure 01-S-11-10, "GGNS
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Employees' Security Responsibilities," which governed the controls for vehicles
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inside the protected area. The procedure required the vehicle to be attended by an
j -- employee with unescorted access. However, no procedural requirements existed
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depicting how attentive the individual must be. Based on review of
j Procedure 01-S-11-10, the inspectors concluded that no procedural violations had
j occurred. ;
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V. Manaaement Meetinas
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- X1 - Exit Meeting Summary
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The inspectors presented the inspection'results to members of licensee management at the ,
i conclusion of the inspection on May 15,1997. The licensee acknowledged the findings )
j. presented,
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The inspectors asked the licensee whether any materials examined during the inspection
i should be considered proprietary. No propnetary information was identified.
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ATTACHMENT
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PARTIAL LIST OF PERSONS CONTACTED '
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Licensee
D. Bost, Director, Nuclear Plant Engineering
R. Brinkman, Senior Reactor Operator, Plant Operations
W. Deck, Superintendent, Security
- B. Eaton, General Manager, Plant Operations
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, C. Elisaesser, Manager, Performance and System Engineering
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J. Hagan, Vice President of Operations l
C. Hayes, Director, Quality Programs
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j W. Hughey, Director, Plant 1.icensing i
i T. Kriesel, Radiation Protection Manager
- R. Moomaw, Maintenance Manager, Maintenance
A. Morgan, Manager, Emergency Preparedness
, J. Venable, Operations Manager, Plant Operations
NRC .
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, J. Donahew, NRR Project Manager i
j INSPECTION PROCEDURES USED l
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37551 Onsite Engineering l
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61726 Surveillance Observations
62707 Maintenance Observation
71707 Plant Operations
- 71750 Plant Support Activities
, ITEMS OPENED, CLOSED, AND DISCUSSED
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Opened
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50-416/9706-01 UNR Further evaluation of the treatment of locked valves in the
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overhead (Section 01.3)
50-416/9706-02 UNR Further evaluation of the bases for testing the SSW cooling
tower f ans (Section M1.4)
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50-416/9706-03 VIO Failure to have a qualified individual for the Offsite
Emergency Coordinator position available (Section P1.1)
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LIST OF ACRONYMS USED
CR condition report ,
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ERO emergency response organization j
IFl inspection followup item
NRC Nuclear Regulatory Commission
NRR Nuclear Reactor Regulation j
RCIC reactor core isolation cooling
SR Surveillance Requirement
SSW standby service water i
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TS Technical Specification
WO work order
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