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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20217D8361999-10-11011 October 1999 Provides NRC with Summary of Activities at TMI-2 During 3rd Quarter of 1999 ML20217F8271999-10-0707 October 1999 Forwards Pmpr 99-13, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990828- 0924.Diskette Containing Pmpr in Wordperfect 8 Is Encl. All Variances Are Expressed with Regard to Current Plans ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20216J6581999-09-28028 September 1999 Provides Info as Requested of Licensees by NRC in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A2101999-09-13013 September 1999 Forwards Rev 3 of Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2, Including Changes Made During 1998.Description of Changes Provided on Page 2 ML20216G4151999-09-0909 September 1999 Forwards Pmpr 99-12, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990731- 0827.All Variances Expressed with Regard to Current Operations Plans ML20211M5861999-09-0202 September 1999 Forwards non-proprietary & Proprietary Response to NRC 990708 RAI Re TS Change Request 272,reactor Coolant Sys Coolant Activity.Proprietary Encl Withheld ML20211M6591999-09-0101 September 1999 Forwards Errata Page to 990729 Suppl to TS Change Request 274,to Reflect Proposed Changes Requested by . Page Transmitted by Submitted in Error ML20211L2401999-09-0101 September 1999 Submits Response to NRC AL 99-02, Operator Reactor Licensing Action Estimates ML20211H3731999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI LAR 285 & TMI-2 LAR 77 Re Changes Reflecting Storage of TMI-1 Radioactive Matls in TMI-2 Facility.Revised License Page mark-up,incorporating Response,Encl ML20211H4001999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI-1 LAR 285 & TMI-2 LAR 77 Re Changes to Clarify Authority to Possess Radioactive Matls Without Unit Distinction.Revised License Page mark-up, Incorporating Response Encl ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211H5041999-08-20020 August 1999 Forwards Proprietary & non-proprietary Rept MPR-1820,rev 1, TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis. Affidavit Encl.Proprietary Rept Wihheld 05000289/LER-1999-007, Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface1999-08-20020 August 1999 Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20211H3571999-08-19019 August 1999 Forwards Itemized Response to NRC 990712 RAI Re TS Change Request 248 Re Remote Shutdown Sys,Submitted on 981019 ML20211A3931999-08-12012 August 1999 Requests NRC Concurrence with Ongoing Analytical Approach as Described in Attachment,Which Is Being Utilized by Gpu Nuclear to Support Detailed License Amend Request to Revise Design Basis for TMI-1 Pressurizer Supports ML20210R4691999-08-11011 August 1999 Forwards Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2.Update 3 Revises SAR to Reflect Current Plant Configuration & Includes Minor Editorial Changes & Corrections.Revised Pages on List of Effective Pages ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210L3831999-07-30030 July 1999 Responds to NRC 990617 RAI Re OTSG Kinetic Expansion Region Insp Acceptance Criteria That Was Used for Dispositioning Indications During Cycle 12 Refueling (12R) Outage ML20210K7371999-07-30030 July 1999 Forwards Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp LOCA, Which Corrects Evaluation Model for Mk-B9 non- Mixing Vane Grid Previously Reported in Util to Nrc,Per 10CFR50.46 ML20210L1151999-07-28028 July 1999 Confirms Two Senior Management Changes Made within Amergen Energy Co,Per Proposed License Transfer & Conforming Administrative License Amends for TMI-1 05000289/LER-1999-009, Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section1999-07-22022 July 1999 Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section ML20216D4001999-07-22022 July 1999 Provides Summary of Activities at TMI-2 During 2nd Quarter of 1999 ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20210G9471999-07-15015 July 1999 Forwards Pmpr 99-10, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990605- 0702.Diskette Containing Pmpr in Wordperfect 8 Format Is Also Encl ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days 05000289/LER-1999-008, Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public1999-07-0202 July 1999 Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public ML20196J3981999-07-0101 July 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for TMI-1 Encl ML20209C1131999-07-0101 July 1999 Forwards Signed Agreement as Proposed in NRC Requesting Gpu Nuclear Consent in Incorporate TMI-1 Thermo Lag Fire Barrier Final Corrective Action Completion Schedule Commitment of 000630 Into Co Modifying License 1999-09-09
[Table view] Category:NRC TO PUBLIC ENTITY/CITIZEN/ORGANIZATION/MEDIA
MONTHYEARML20056A3691990-07-30030 July 1990 Discusses Office of Investigations Rept 1-87-008 Re Observation of Sleeping or Appearance of Sleeping on Duty & Forwards Notice of Violation ML20055F4161990-07-0909 July 1990 Final Response to FOIA Request.App a Record Encl & Available in PDR ML20247E0681989-07-20020 July 1989 Forwards Board Decision Approving Method for Disposing of accident-generated Water at Plant,Per Recipient Petition. Appeal of Decision Presently Before Appeal Board.W/O Encl. Related Correspondence NUREG-0557, Final Response to FOIA Request.Records Available Through Gpo1989-06-26026 June 1989 Final Response to FOIA Request.Records Available Through Gpo ML20245E9571989-06-26026 June 1989 Final Response to FOIA Request.Records Available Through Gpo ML20245G0301989-06-22022 June 1989 Responds to Re Offsite Radiation Monitoring & Emergency Warning Sys in Vicinity of TMI-2.NRC Opinion That Existing Real Time Monitoring Sys Will Remain Operational for at Least Next Several Yrs Expressed ML20246M2231989-05-0808 May 1989 Responds to Raising Concerns Re Actuation of Emergency Warning Signal in York,Pa on 890317.Emergency Brochure Issued to All Local Residents Adequate.Actuation Was Isolated Malfunction of One Signal ML20235N1981989-02-23023 February 1989 Final Response to FOIA Request for Records.Forwards Document Listed in App A.App a Document Available in PDR ML20206D9201988-11-0909 November 1988 Responds to Re NRC 880331 Response to Questions Raised Concerning Conditions at Plants & Recipient Proposal to Station Senior Operator in Control Room at All Nuclear Plants to Oversee Plant Operations ML20195G2121988-11-0808 November 1988 Final Response to FOIA Request for Documents.Forwards App D Document & Releasable Portions of Documents E/1 Through E/3. App D & Releasable Portions of Documents E/4 Through E/6 Available in Pdr.Portions Withheld (Ref FOIA Exemption 5) ML20154L0711988-09-20020 September 1988 Provides Response to TMI Alert,Inc/Susquehanna Valley Alliance Interrogatory 31(ii) Re NRC Experience &/Or Tests Performed on Moisture Separators & Vapor Superheaters. Related Correspondence ML20207E8801988-08-0303 August 1988 Forwards Programmatic EIS for TMI-2 & Suppls 2 & 3.W/o Encls ML20195E8821988-06-15015 June 1988 Third Partial Response to FOIA Request for Documents.App C, E,F & G Documents Encl & Available in Pdr.App D Documents Available in Pdr.Portions of Records Subj to Request Withheld (Ref FOIA Exemptions 4,5,6 & 7) ML20195F8041988-06-15015 June 1988 First Partial Response to FOIA Request for Documents. Forwards Apps B & C Documents.Documents Available in Pdr.App a Documents Also Available in Pdr.Apps D Through G Documents Withheld (Ref FOIA Exemption 5).Releasable Portion Encl ML20151M6061988-04-19019 April 1988 Responds to FOIA Request for Info Re Scores of Reactor Operators & Senior Reactor Operators.Forwards Requalification Exam Summary Source Sheets Listed in Encl App W/Personal Privacy Info Deleted ML20149G0731988-02-10010 February 1988 Responds to Re Announced Reorganization of NRC at TMI-2.NRC Personnel Stationed at Site,Region I & NRC Headquaters Will Continue to Provide Effective Regulatory Oversight of Cleanup Activities ML20147E2561988-01-15015 January 1988 Partial Response to FOIA Request for Documents Re Environ Qualification at Facility.Forwards Documents Listed in App C.Documents Also Available in PDR ML20149E9901988-01-11011 January 1988 Partial Response to FOIA Request Re MOU Between NRC & Dept of Labor.Forwards App B Documents.Apps a & B Documents Available in Pdr.App C Documents Totally Withheld (Ref FOIA Exemption 5) ML20147D4821988-01-0606 January 1988 Partial Response to FOIA Request for Documents.Forwards App B Documents.Documents Also Available in Pdr.Portions of App B Documents Withheld (Ref FOIA Exemptions 6 & 7) ML20237C5961987-12-17017 December 1987 Final Response to FOIA Request for Documents Re Plant. Article from NRC 1979 Annual Rept & Listing of NUREG Repts Re Plant Encl.Nureg Repts May Be Purchased from Pdr.All Encls Available in Pdr.W/O Encl IA-87-834, Final Response to FOIA Request for Documents Re Plant. Article from NRC 1979 Annual Rept & Listing of NUREG Repts Re Plant Encl.Nureg Repts May Be Purchased from Pdr.All Encls Available in Pdr.W/O Encl1987-12-17017 December 1987 Final Response to FOIA Request for Documents Re Plant. Article from NRC 1979 Annual Rept & Listing of NUREG Repts Re Plant Encl.Nureg Repts May Be Purchased from Pdr.All Encls Available in Pdr.W/O Encl ML20235V1381987-10-13013 October 1987 Final Response to FOIA Request for Records.App a Document, Consisting of Dj Collins 870721 Memo to Wd Travers Re Testing of Processed Water Encl & Available in PDR ML20235R8521987-09-30030 September 1987 Responds to Re EIS for Meltdown of Large Reactors & NRC Compliance W/Nepa.As Result of TMI-2 Accident on 790329,NRC Included Class 9 Accidents in Assessments in Fes Re Licensing of Plants.Related Info Encl ML20216D4921987-06-22022 June 1987 Responds to 870610 Motion Requesting That ASLB Reconsider 870521 Decision Re Leak Rate Falsification at Plant. Comments Re Decision Should Be Sent to NRC Staff.Served on 870623 ML20214S0691987-06-0202 June 1987 Forwards Rd Parks Notice of Deposition.Deposition Period of 870622-24 Confirmed.Certificate of Svc Encl.Related Correspondence ML20209H0531987-04-29029 April 1987 Partial Response to FOIA Request for Documents Re INPO Accreditation of Training Programs.Forwards App B Document. Document Also Available in PDR ML20206T6591987-04-20020 April 1987 Forwards Transcript of Recipient 870410 Deposition,For Review.Any Corrections Should Be Made in Tabular Format as Indicated on Attached Sheet.W/O Transcript.Related Correspondence ML20206U0981987-04-20020 April 1987 Forwards Transcript of Recipient 870409 Deposition,For Review.Any Corrections Should Be Made in Tabular Format as Indicated on Encl Sheet.W/O Transcript.Related Correspondence DD-87-03, Advises That Time for Commission to Review Director'S Decision DD-87-03 Expired on 870331.Commission Declined Review.Served on 8704031987-04-0202 April 1987 Advises That Time for Commission to Review Director'S Decision DD-87-03 Expired on 870331.Commission Declined Review.Served on 870403 ML20205A3211987-03-24024 March 1987 Final Response to FOIA Request for IE Inspectors Failure to Rept Info Re 790328 Hydrogen Explosion at TMI-2. App a Document Available in PDR IA-87-163, Final Response to FOIA Request for IE Inspectors Failure to Rept Info Re 790328 Hydrogen Explosion at TMI-2. App a Document Available in PDR1987-03-24024 March 1987 Final Response to FOIA Request for IE Inspectors Failure to Rept Info Re 790328 Hydrogen Explosion at TMI-2. App a Document Available in PDR ML20212K5181987-03-0606 March 1987 Forwards Director'S Decision 87-03 Denying Remaining Portion of 830323 Petition to Halt All Work Based on Rd Parks Allegations & Fr Notice.Portion of Petition Re Polar Crane Load Test Previously Denied in Director'S Decision 83-18 ML20213A0101987-01-29029 January 1987 Final Response to FOIA Request for Documents Re Plant. Forwards App G Document.Documents Also Available in PDR ML20212R6291987-01-27027 January 1987 Forwards Transcript of 870113 Deposition.Review & Signature Requested.W/O Encl.Related Correspondence NUREG-1019, Forwards Response to 860915 & 30 Questions Re Steam Generator Tube Rupture & Turbine Bypass Valve1987-01-13013 January 1987 Forwards Response to 860915 & 30 Questions Re Steam Generator Tube Rupture & Turbine Bypass Valve ML20211Q7551986-12-18018 December 1986 Final Response to FOIA Request for Insp Rept 50-289/86-14 on 860825-0905.App a Document Available in PDR ML20214P4751986-11-26026 November 1986 Responds to 860919 Request That Filter Be Installed on Condenser Offgas Sys Line at TMI-1 to Reduce Possible Radioactive Releases to Environ.Nrc Does Not Believe Placing Filter on Sys Will Provide Measurable Improvement in Safety ML20214A6351986-11-14014 November 1986 Forwards Three Draft Documents to Be Discussed at 861117 Meeting in Buena Park,Ca.W/O Encls.Related Correspondence ML20215H9741986-10-22022 October 1986 Requests to Be Contacted to Arrange Appearance as Witness in Commission Inquiry Into Leak Rate Data Falsifications at Facilities in 1978-1979,per 860806 Subpoena.Served on 861023 ML20215L1871986-10-0909 October 1986 Responds to Appeal Re Denial of FOIA Request for Three Categories of Records Concerning Equipment Qualification at Facility.Forwards Documents 14-16 Listed on App.Documents 1- 13,17 & 20-22 Withheld (Ref FOIA Exemption 5) ML20210U4431986-10-0202 October 1986 Forwards Info Requested at 860923 SALP I Meeting,Including Clarification of Apps Listed in Table in Ref to 10CFR50 & Listing of Subjs of Amends 111-117 to License DPR-50 ML20214Q1991986-09-19019 September 1986 Forwards Response to 860616 & 0710 Ltrs Re Tube Failure in once-through Steam Generator on Reinjection of Emergency Feedwater During TMI-2 Accident Possibly Causing Primary to Secondary Leaks & Large Release of Iodine ML20212P6521986-08-29029 August 1986 Confirms 860828 Telcon Re Agreement to Appear as Witness in Commission Inquiry Into Leak Rate Data Falsifications at TMI-2.Recipient Interviews & Statement Encl.W/O Encls. Served on 860902 ML20203L6971986-08-27027 August 1986 Forwards Subpoena Requiring Appearance at Sept 1986 Hearing Re TMI-2 Leak Rate Falsification.Served on 860828 ML20205C5931986-08-0808 August 1986 Requests Return of Page 3 of Encl 2 to NRC Rept, Results of NRR Investigation & Evaluation of 10 Licensed Operators Involved in TMI-2 Preaccident Leak Rate Testing Irregularities. Served on 860811 ML20205C6281986-08-0808 August 1986 Requests Return of Page 3 of Encl 2 to NRC Rept, Results of NRR Investigation & Evaluation of 10 Licensed Operators Involved in TMI-2 Preaccident Leak Rate Testing Irregularities. Served on 860811 ML20205C6471986-08-0808 August 1986 Requests Return of Page 3 of Encl 2 to NRC Rept, Results of NRR Investigation & Evaluation of 10 Licensed Operators Involved in TMI-2 Preaccident Leak Rate Testing Irregularities. Served in Aug 1986 ML20205C6321986-08-0707 August 1986 Forwards Subpoena Requiring Appearance as Witness at Hearings in Sept 1986 Re Leak Rate Test Data Falsifications During 1978 & 1979.W/o Encl.Served on 860811 ML20205C4371986-08-0707 August 1986 Forwards Subpoena Requiring Appearance as Witness at Sept 1986 Hearing Re Responsibility for Leak Rate Test Data Falsifications at Facility in 1978-79.Estimated Date of Testimony Is 860930.W/o Encl.Served on 860811 ML20205C5511986-08-0707 August 1986 Forwards Subpoena Requiring Appearance as Witness at Hearings in Sept 1986 Re Leak Rate Test Data Falsifications During 1978 & 1979.W/o Encl.Served on 860811 1990-07-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days ML20196J5631999-07-0101 July 1999 Informs That Util 981203 Joint Application with Amergen Energy Co Marked Proprietary Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20196J5741999-06-30030 June 1999 Informs That as Result of Staff Review of Util Response to GL 92-01,rev 1,suppl 1,info Provided in Support of PT Limits License Amend & B&W Topical Rept,Staff Revised Info for Plant,Unit 1,in Reactor Vessel Integrity Database ML20196H6811999-06-29029 June 1999 Forwards Insp Rept 50-289/99-03 on 990425-0605.No Violations Noted.However,Adequacy of Assessment of Reactor Bldg Emergency Cooler Operability Prior to Conducting Maintenance on One Reactor Bldg Spray Sys,Questionable ML20212H8711999-06-21021 June 1999 Discusses Updated Schedule Commitment Submitted by Gpu on 990602 for Implementing Thermo-Lag 330-1 Fire Barrier C/As & Completion of Thermo-Lag Effort at TMI-1.Informs NRC Will Incorporate Commitment Into Co Modifying License ML20195K2821999-06-17017 June 1999 Forwards Request for Addl Info Re Kinetic Expansion Region Inspection Acceptance Criteria ML20212H6621999-06-0404 June 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Ss Bajwa Will Be Section Chief for Three Mile Island Nuclear Station ML20207E7201999-05-27027 May 1999 Discusses Reorganization of Nrr,Effective 990328. Organization Chart Encl ML20207B6541999-05-27027 May 1999 Forwards SER Accepting Util Program to Periodically Verify design-basis Capability of safety-related MOV at TMI-1 & That Util Adequately Addressed Actions Requested in GL 96-05 ML20207C0321999-05-18018 May 1999 Forwards Fifth Rept Which Covers Month of Apr 1999. Commission Approved Transfer of TMI-1 Operating License from Gpu to Amergen & Transfer of Operating License for Pilgrim Station from Beco to Entergy Nuclear Generating Co ML20206S3411999-05-14014 May 1999 Forwards Insp Rept 50-289/99-02 on 990314-0424.Violations Occurred & Being Treated as non-cited Violations.Security Program Was Inspected During Period & Found to Be Effective ML20206N5831999-05-13013 May 1999 Requests Description of Proposed Corrective Actions for Fire Zones AB-FZ-3,AB-FZ-5,AB-FZ-7,FH-FZ-2,CB-FA-1 & FH-FZ-6. Confirmation That Corrective Actions & Commitments Made Will Be Completed by 991231,requested IR 05000298/19980091999-05-12012 May 1999 Refers to Insp Rept 50-298/98-09 Conducted Between 981227-990130.During Insp,Apparent Violation of 10CFR50.50 Identified & Being Treated as non-cited ML20206H3571999-05-0606 May 1999 Forwards RAI Re 981203 Application & Suppls & 0416,requesting Review & Approval of Revised Core Protection SL & Bases for TMI-1 to Reflect Average of 20% of Tubes Plugged Per Sg.Response Requested within 10 Days of Receipt ML20207A5401999-04-29029 April 1999 Informs That Licensee 980930 Response to GL 96-06,appears to Be Reasonable & Appropriate for Specific Design & Configuration of RB Emergency Cooling at Plant,Unit 1 & That Staff Satisfied with Licensee Resolution of Waterhammer ML20206D4001999-04-20020 April 1999 Informs of Completion of Review of Gpu Request for Exemption Submitted on 961231,970908,971230,980521,981014,981125 & 981223 from Requirements of 10CFR50,App R,Section III.G.2 for TMI Unit 1.Forwards Exemption & Safety Evaluation ML20205S6791999-04-16016 April 1999 Forwards Insp Rept 50-289/99-01 on 990131-0313.No Violations Noted.Identification by Licensee Staff of Elevated Tritium Activity in Monitoring Well Led to Investigation & Identification of Leak from Buried Radwaste Path ML20205P3391999-04-0909 April 1999 Discusses Results of Plant Performance Review for Three Mile Island Completed on 990225.Historical Listing of Plant Issues That Were Considered During PPR Encl IR 05000289/19980061999-03-26026 March 1999 Ack Receipt of 981112 & s Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-289/98-06 .Action Does Not Change NRC Determination That Change to Hpis Valve Configuration Involved URI ML20204E3911999-03-17017 March 1999 Informs That Region I Plans to Conduct Open Predecisional Enforcement Conference to Discuss Apparent Violations Re Efs Issues as Described in Insp Rept 50-289/98-09,per ML20204B6771999-03-15015 March 1999 Submits Withdrawal of Amend Request for Operating License DPR-46.Proposed Change Would Have Modified Facility TSs Pertaining to Neutron Monitoring Neutron Detectors ML20207H7391999-03-0505 March 1999 Forwards Insp Rept 50-289/98-09 on 981227-990130.Two Apparent Violations Being Considered for Enforcement Action.First Violation Deals with Failure to Follow Procedures for Control of Emergency Boration Source ML20203F4911999-02-0505 February 1999 Forwards Request for Addl Info Re Licensee 981125 Amend Application Re TS Change Request 277 for OTSG Inservice Insp During 13R for Three Mile Island,Unit 1 ML20202H6771999-02-0303 February 1999 Documents Basis for NRC Staff Generic Approval of Requests to Relocate TS Requirements from Tss.Staff Generic SER Finding Relative to Relocated TS Requirements Encl ML20196K3511999-01-22022 January 1999 Refers to Gpu Responses to Second NRC RAI Re GL 92-08 & Review of Gpu Analytical Approach for Ampacity Derating Determinations.Forwards SE & SNL Technical Ltr Rept Concluding That No Outstanding Safety Concerns Identified ML20199H6471999-01-20020 January 1999 Forwards RAI Re Gpu TS Change Request 277 OTSG Cycle 13 for Plant Unit 1.NRC Has Determined That Addl Info Needed to Complete Review ML20199G7401999-01-12012 January 1999 Forwards Insp Rept 50-289/98-08 on 981101-1226.No Violations Noted.Operator Workaround Program Found to Be Acceptable ML20206S0221999-01-0808 January 1999 Responds to Re Changes to Physical Security Plan Identified as Rev 38,submitted Under Provisions of 10CFR50.54(p).Based on NRC Determination,Changes Do Not Decrease Overall Effectiveness of Security Plan 1999-09-30
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7 AUG 9 BBS Ms. Ellyn R. Weiss and Mr. Robert D. Pollard '
Union of Concerned Scientists 1346 Connecticut Avenue, N.W. Suite 1101 Washington, DC 20036
Dear Ms. Weiss and Mr. Pollard:
I have been asked to respond to your letter to the Commissioners dated April 12, 1985 regarding Three Mile Island, Unit 1 (TMI-1). Your letter was I basically concerned about staff positions on the boiler-condenser decay heat removal process. In the following responses, we do not respond directly to the six specific questions asked in your letter because a major portion of the requested information is already contained in the staff's testimony and the hearing record. We do address, however, what we understand to be your underlying concern, namely the apparent discrepancy between the previous staff testimony on TMI-1 restart and more recent statements made by the Office of Nuclear Regulatory Research (RES) in response to Congressional inquiries.
Your April 12, 1985 letter identifies an apparent discrepancy between testi-mony filed by the staff with the TMI-1 Appeal Board and a statement made in response to Congressional inquiries concerning NRC's research budget.
Specifically, the NRC staff, in 1983 testimony filed with the TMI-1 appeal board, stated that experimental testing was not needed prior to restart in order to confirm the effectiveness of boiler-condenser decay heat removal in the TMI-1 plant during small break loss of coolant accidents (LOCAs). More recently however, in responding to Congressional inquiries regarding the research budget, RES stated that testing to assess the effectiveness of the boiler-condenser process to remove heat from the reactor coolant and maintain natural circulation was research needed in response to TMI-1 regulatory concerns. These were set forth in ALAB 729 which recommended continuation of research on decay heat removal capability. The RES statement was made on March 14, 1985 prior to the NRC decision on TMI-1 restart which was reached on May 29, 1985.
We reaffirm our position that experimental testing is not needed to confirm the effectiveness of boiler-condenser decay heat removal for TMI-1. Since we recognize that the statement provided to Congressman Udall implies a con-tradiction with this position, the following discussion is provided to clarify this issue and show that no discrepancy or contradiction actually exists.
During certain small break LOCA's, a possible steam formation at the top of the hot leg U-bends was predicted to interrupt natural circulation. Under these accident conditions, the reactor coolant pumps are not running and natural circulation causes the flow of cooling water through the core. In the absence of natural circulation, decay heat removal capability would be lost and the primary system would repressurize as the primary system temperature increased. This would have a twofold effect of increasing the rate of coolant N
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-7 loss out of the break and reducing the flow of safety injection water into the primary system. If decay heat removal was not restored, the system would continue to lose more water than was being made up, and eventually core uncovery and core damage would occur. In order to stabilize the system, it would be necessary to reestablish decay heat removal. This would lower the primary system pressure, reduce the break flow, and increase the safety injection flow sufficient to prevent core uncovery and to refill the primary system. Under these circumstances, it may be necessary to rely on the boiler-condenser mode of decay heat removal. The effectiveness of the boiler- I condenser mode of decay heat removal was in question.
Because of the primary system configuration at TMI-1 (and all other lowered loop B&W-designed reactors), the staff concluded that before the coolant level in the primary system could drop below the top of the core in the accident
, sequence described in the proceeding paragraph, a condensing surface would be exposed in the once through steam generators (OTSG) that would be sufficient to remove decay heat and depressurize the primary system. This process is what is referred to as the boiler-condenser mode of decay heat removal.
Safety injection flow would then be sufficient so that core uncovery would be avoided. The efficacy of the thermal hydraulic and heat transfer processes involved were not deemed to require experimental data since (a) all B&W reactor licensees had modified their emergency procedures to instruct the operators to raise the secondary side water level to 95 percent of the operating range when cooling by nai. ural circulation, thus ensuring an ample condensing surface in the OTSG at an elevation above the top of the core should the boiler-condenser cooling mode be necessary, (b) the heat transfer correlations associated with condensation heat transfer were well established, (c) systems calculations of this process had been performed by independently I developed computer codes, including RELAP4, RELAP5, and CRAFT, and despite
! differences in the predicted detailed thermal hydraulic behavior associated l with the boiler-condenser mode of decay heat removal, all of the codes l predicted the ultimate establishment of decay heat removal and no core uncovery, (d) decay heat removal by condensation beat transfer had been experimentally confirmed in test facilities with inverted U-tube steam generators, which, while not exactly the same, exhibit many of the thermal
, hydraulic characteristics of the B&W OTSG design, and (e) sufficient margin I existed such that uncertainties in the analytical results would not have influenced our conclusions. Rased on the above considerations, we determined that experimental information demonstrating the efficacy of boiler-condenser decay heat removal was not needed to ensure safe operation of TMI-1.
f No new information has been ectablished in the intervening period since we made this determination that would cause us to change our conclusions today.
Rather, data recently obtained from the GERDA and OTIS facilities (B&W raised loop simulations) and recent TRAC and REBL analyses on the MIST facility have served to confirm our conclusions.
As stated above, we fully rvognized that uncertainties existed in the analysis methods available at the time of the appeal board hearing, and we actively supported the need for a thermal hydraulic experimental facility geometrically similar to the B&W nuclear steam supply system (NSSS) design in
Mb Ub order to study and quantify the uncertainties in the small break LOCA analyses for B&W designed NSSSs ar set forth in ALAB 729 which recomended that confirmatory research into decay heat removal be continued in order to
... increase the current knowledge of thermal-hydraulic behavior during small break loss of coolant accidents".
The need for this information was to provide confirmatory data for the purpose of (1) quantifying the ability of themal hydraulic codes, such as RELAp5 and TRAC, to calculate the best-estimate, or realistically expected thermal hydraulic response of a B&W NSSS to small LOCAs, (2) providing a data base from which code improvements, if needed, could be based and assessed, and (3) using these codes as an audit tool for confirming selected emergency operator guidelines for B&W NSSSs.
The need for and use of this data, and its relationship to the licensing process, is considered identical to our need for and use of data from other thennal hydraulic facilities, notably LOFT and Semiscale for pWRs and TLTA and FIST for BWRs. Data from these facilities has been used primarily to confirm and quantify safety margins in licensing requirements, to provide a basis for reducing excessive margins, and to provide a data base against which best estimate codes can be assessed and improved.
Therefore, our response to Congressman Udall's staff does not mean that experimental data is needed to conclude that TPI-1 meets the Commission's regulations and can safely remove decay heat and prevent unacceptable core uncovery during small break LOCAs. Rather, it is intended to mean that a generic effort is needed to obtain additional experimental data to be used by the Regulatory staff for the purposes of quantifying thermal hydraulic performance uncertainties in codes used for evaluating small break LOCAs in all B&W-designed NSSSs.
With respect to the use of these codes to confirn emergency operating procedures, you point out statements made in a 1981 NRR Research User Need Letter that implies incorrect operator actions could result as a consequence of unpredicted phenomena producing false symptoms of other events. Since the -
User Need Letter was written in 1981, we have completed an in-depth review of the 88W Abnormal Transient Operator Guidelines (ATOGs), from which the TMI-1 plant emergency procedures were developed. The AT0G guidelines are designed to treat symptoms of accident conditions such as steam generator heat transfer and core cooling problems and are not dependent on operator event diagnosis for safe shutdown. We approved these guidelines and concluded that since any operator error of significance will manifest itself as an abnormal symptom or plant
! rnponse and would be treated accordingly, operator error is adequately covered.
Sincerely, 8gGM $MDNO Harold R. Denton, Director -
Office of Nuclear Reactor Regulation
- See previous white for concurrences.
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The need for and use of this data, and its relationship to the licensing process, is considered identical to our need for and use of data from other thermal hydraulic facilities, notably LOFT and Semiscale for PWRs and TLTA and FIST for BWRs. Data from these facilities has been used primarily to confirm and quantify safety margins in licensing requirements, to provide a basis for reducing excessive margins, and to provide a data base against which best estimate codes can be assessed and improved.
Therefore, our response to Congressman Udall's staff does not mean that experimental data is needed to conclude that TMI-1 meets the Connission's '
regulations and can safely remove decay heat and prevent unacceptable core uncovery during small break LOCAs. Rather, it is intended to mean that a generic effort is needed to obtain additional experimental data to be used by the Regulatory staff for the purposes of quantifying thennal hydraulic performance uncertainties in codes used for evaluatii.g small break LOCAs in all B&W-designed NSSSs.
With respect to the use of these codes to confirm emergency operating procedures, you point out statements made in a 1981 NRR Research User Need Letter that implies incorrect operator actions could result as a consequence of unpredicted phenomena producing false symptoms of other events. Since the User Need Letter was written in 1981, we have completed an in-depth review of the B&W Abnormal Transient Operator Guidelines (AT0Gs), from which the TMI-1 plant emergency procedures were developed. The AT0G guidelines are designed to treat symptoms of accident conditions such as steam generator heat transfer and core cooling problems and are not dependent on operator event diagnosis for safe shutdown. We approved these guidelines and concluded that since any operator error of significance will manifest itself as an abnormal symptom or plant response and would be treated accordingly, operator error is adequately covered.
Sincerely, Original signed by l
\3 Darrell G. Eisenhut Ng Harold R. Denton, Director l
d Office of fluclear Reactor Regulation k
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DISTRIBUTION FOR GREEN TICKET # 790 Docket File or Central File w/ orig. incoming ltr.
NRC PDR w/inc.
L POR w/inc.
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