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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20212J1891999-10-0101 October 1999 Safety Evaluation Supporting Exemption from 10CFR54.17(c)re Schedule to Apply for Renewed Operating Licenses ML20212G1211999-09-22022 September 1999 Safety Evaluation Supporting Amends 188 & 169 to Licenses NPF-9 & NPF-17,respectively ML20212G2671999-09-22022 September 1999 Safety Evaluation Supporting Amends 187 & 168 to Licenses NPF-9 & NPF-17,respectively ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20211P1371999-09-0808 September 1999 Safety Evaluation Supporting Amend 186 to License NPF-9 ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20154B7991998-09-28028 September 1998 Safety Evaluation Supporting Amends 183 & 165 to Licenses NPF-09 & NPF-17,respectively ML20236X3611998-07-30030 July 1998 Safety Evaluation Supporting Amends 179 & 161 to Licenses NPF-9 & NPF-17,respectively ML20249B6281998-06-12012 June 1998 Safety Evaluation Accepting 980303 Request to Review & Approve Proposed Change to Plant,Units 1 & 2 TS Re Relocation of Meteorological Tower ML20248B0441998-05-27027 May 1998 Safety Evaluation Authorizing Proposed Alternative Use of Current TS Section 3/4.7.8 Requirements for Snubber Visual Exam & Functional Testing,Based on Finding That Proposed Alternative Proposes Acceptable Level of Quality & Safety ML20217P7261998-04-0808 April 1998 Safety Evaluation Supporting Amends 178 & 160 to Licenses NPF-09 & NPF-17,respectively ML20197A6551998-03-0202 March 1998 Safety Evaluation Supporting Licensee Proposed Action to Set Gwl Alarm at Higher Elevation than Current Level of El 731 Feet ML20203B1071998-02-0404 February 1998 Safety Evaluation Approving Proposed Alternative to Reactor Vessel Augmented Exam Requirement of Reactor Vessel Shell Welds,Per 10CFR50.55a(g)(6)(ii)(A)(5) ML20199F3361998-01-28028 January 1998 Safety Evaluation Supporting 951227 Request for NRC Approval of Proposed EALs to McGuire Nuclear Station,Units 1 & 2 ML20202C0001997-11-25025 November 1997 Safety Evaluation Supporting Amends 177 & 159 to Licenses NPF-9 & NPF-17,respectively ML20198J7651997-10-15015 October 1997 Safety Evaluation Accepting 10-yr Interval Insp Program Plan Alternatives for Listed Plants Units ML20211E6871997-09-22022 September 1997 SER Accepting DPC Responses to GL-95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20210Q9421997-08-26026 August 1997 Safety Evaluation Supporting Amends 176 & 158 to Licenses NPF-9 & NPF-17,respectively ML20141H9821997-07-31031 July 1997 Safety Evaluation Supporting Exemption Re Criticality Accident Requirements ML20148S2231997-07-0202 July 1997 Safety Evaluation Accepting Supplemental Test Program for Relief Request 1.4.2 for Units 1 & 2 ML20148H2501997-06-0505 June 1997 Safety Evaluation Accepting Proposed Restructuring of Util Through Acquisition Of,& Merger W/Panenergy Corp ML20138B5521997-04-24024 April 1997 Safety Evaluation Supporting Amends 174 & 156 to Licenses NPF-9 & NPF-17,respectively ML20134P2421997-02-20020 February 1997 Safety Evaluation Accepting TR BAW-10199P for Ref in Plants Licensing Documentation & Use in Licensing Applications ML20134G5551996-11-0707 November 1996 Safety Evaluation Accepting Proposed Application of BWU-Z CHF Correlation for Plants Mark-BW 17x17 Type Fuel ML20116D6401996-07-30030 July 1996 Safety Evaluation Supporting Amends 169 & 151 to Licenses NPF-9 & NPF-17,respectively ML20117A2841996-07-29029 July 1996 Safety Evaluation Supporting Amends 168 & 150 to Licenses NPF-9 & NPF-17,respectively ML20113F1551996-07-0202 July 1996 Safety Evaluation Supporting Amends 167 & 149 to Licenses NPF-9 & NPF-17 ML20097G8311996-02-15015 February 1996 Safety Evaluation Supporting Amends 165 & 147 to Licenses NPF-9 & NPF-17,respectively ML20096E0951996-01-11011 January 1996 Safety Evaluation Supporting Amends 162 & 144 to Licenses NPF-9 & NPF-17,respectively ML20087C4431995-08-0202 August 1995 Safety Evaluation Supporting Amends 157 & 139 to Licenses NPF-9 & NPF-17,respectively ML20087B2401995-08-0202 August 1995 Safety Evaluation Supporting Amends 158 & 140 to Licenses NPF-9 & NPF-17,respectively ML20087B6071995-08-0202 August 1995 Safety Evaluation Supporting Amends 156 & 138 to Licenses NPF-9 & NPF-17,respectively ML20082C3171995-04-0303 April 1995 Safety Evaluation Supporting Amends 154 & 136 to Licenses NPF-9 & NPF-17,respectively ML20073G2871994-09-22022 September 1994 Safety Evaluation Supporting Amends 148 & 130 to Licenses NPF-9 & NPF-17,respectively ML20029E7081994-05-11011 May 1994 Safety Evaluation Supporting Amends 142 & 124 to Licenses NPF-9 & NPF-17,respectively ML20064N5531994-03-22022 March 1994 Safety Evaluation Supporting Amends 141 & 123 to Licenses NPF-9 & NPF-17,respectively ML20067A5041994-02-10010 February 1994 Safety Evaluation Supporting Amends 140 & 122 to Licenses NPF-9 & NPF-17,respectively ML20063E4671994-01-31031 January 1994 Safety Evaluation Supporting Amends 139 & 121 to Licenses NPF-9 & NPF-17,respectively ML20059G8601993-10-29029 October 1993 SE Granting 921130 Request for Relief from Requirements of 1986 Edition of ASME Boiler & Pressure Vessel Code,Section XI Re Inservice Insp of safety-related Snubbers During Second 10-yr Interval ML20057F4121993-10-12012 October 1993 Safety Evaluation Re Inservice Testing Program Requests for Relief.Alternatives Authorized Per 10CFR50.55a(a)(3) or Relief Granted Per 10CFR50.55a(f)(6)(i) ML20057A0361993-08-26026 August 1993 Safety Evaluation Supporting Amends 138 & 120 to Licenses NPF-9 & NPF-17,respectively ML20056H3191993-08-24024 August 1993 SER Accepting Proposed TS Changes Re RWST & Cla Boron Concentrations ML20046C8471993-07-20020 July 1993 Safety Evaluation Granting Licensee 930429 Request to Use Alternative Matls in Fabrication & Installation of SGs at Plant ML20046A5241993-07-19019 July 1993 Safety Evaluation Supporting Amends 137 & 119 to Licenses NPF-9 & NPF-17 ML20044H3901993-06-0303 June 1993 Safety Evaluation Granting Relief from ASME Section XI Inservice Insp Hydrostatic Testing of Class B Piping within Mechanical Penetrators M372 & M373 During First ten-yr Interval ML20127E4781993-01-0606 January 1993 Safety Evaluation Supporting Amends 134 & 116 to Licenses NPF-09 & NPF-17,respectively 1999-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J1891999-10-0101 October 1999 Safety Evaluation Supporting Exemption from 10CFR54.17(c)re Schedule to Apply for Renewed Operating Licenses ML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20212G1211999-09-22022 September 1999 Safety Evaluation Supporting Amends 188 & 169 to Licenses NPF-9 & NPF-17,respectively ML20212G2671999-09-22022 September 1999 Safety Evaluation Supporting Amends 187 & 168 to Licenses NPF-9 & NPF-17,respectively ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20211P1371999-09-0808 September 1999 Safety Evaluation Supporting Amend 186 to License NPF-9 ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 05000369/LER-1999-001-04, :on 990306,TS SR for Ice Condenser Lower Inlet Doors Was Not Met.Caused by Failure to Recognize That Recorded Valve Was Outside Acceptance Criteria.Mgt Reinforced Expectations for Procedure Performance & Review1999-03-31031 March 1999
- on 990306,TS SR for Ice Condenser Lower Inlet Doors Was Not Met.Caused by Failure to Recognize That Recorded Valve Was Outside Acceptance Criteria.Mgt Reinforced Expectations for Procedure Performance & Review
ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B7991998-09-28028 September 1998 Safety Evaluation Supporting Amends 183 & 165 to Licenses NPF-09 & NPF-17,respectively ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage 05000369/LER-1998-006-02, :on 980812,noncompliance with Ice Condenser TS SR 4.6.5.1b.3 Noted.Caused by Lack of Clear Documentation Re Interpretation of TS SR 4.6.5.1b.3.Submitted TS Amend to Clearly Establish SR & Will Review Ice Condenser TSs1998-09-11011 September 1998
- on 980812,noncompliance with Ice Condenser TS SR 4.6.5.1b.3 Noted.Caused by Lack of Clear Documentation Re Interpretation of TS SR 4.6.5.1b.3.Submitted TS Amend to Clearly Establish SR & Will Review Ice Condenser TSs
1999-09-08
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$1 UNITED STATES p
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NUCLEAR REGULAT^9Y COMMISSION o
WASHINGTON, D.C. 20066 0001 kg I
SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO.183 TO FACILITY OPERATING LICENSE NPF-9 AND AMENDMENT NO.165 TO FACILITY OPERATING LICENSE NPF-17 DUKE ENERGY CORPORATION MCGUIRE NUCLEAR STATION. UNITS 1 AND 2 DOCKET NOS. 50-369 AND 50-370
1.0 INTRODUCTION
By l( tier dated October 22,1996, as supplemented by letters dated March 19, July 6, and September 15,1998, Duke Energy Corporation (DEC/the licensee), submitted a request for changes to the McGuire Nuclear Station (McGuire), Units 1 and 2, Technical Specifications (TSs). The requested changes would allow continued plant operation at elevated containment lower compartment temperatures between 125 *F and 135'F for a period not to exceed 72 cumulative hours per calendar year. The March 19, July 6, and September 15,1998, submittals provided clarifying information and did not change the no significant hazards determination, or expand the scope of the original Federal Register notice.
2.0 EVALUATION Current TS 3.6.1.5, allows McGuire to operate at a containment lower compartment temperature between 100 *F and 120 *F with the stipulation that the lower compartment temperature may be between 120 *F and 125 *F for up to 90 cumulative days per calendar year provided the lower compartment temperature average over the previous 365 days is less than 120 *F. The proposed amendment would add the following:
Within this 90 cumulative day period, containment lower compartment temperature may be between 125* and 135"F for 72 cumulative hours.
The licensee states that the inclusion of this provision will permit additional time for minor repairs should the unit experience an air handling unit failure involving the containment lower compartment ventilation (VL) system. The licensee adds that performing these repairs while the unit is on-line will avoid an unnecessary forced shutdown and the resulting transient.
The containment lower compartment is cooled by the containment lower compartment VL system during normal operation and shutdown. The VL system is cooled by water from Lake Norman. During late summer and early fall, the lake water experiences steadily increasing temperature along with increasing fouling conditions. During this period the TS limit of 120 *F 9810060015 980928 DR ADOCK 050003 9
l l
2-is typically exceeded for a period less than 10 days. If one of the VL system air handling units were to fail, the containment lower compartment temperature would increase approximately 10 'F, resulting in a weighted average temperature between 130 'F and 135 'F. This currently would result in exceeding the stated TS temperature limit, theteby forcing the units to cold shutdown.
The licensee already has a footnote statement in its TSs that allows operation at 125 'F for up to 90 cumulative days per calendar year. The licensee is proposing to insert an addition to that footnote allowing operation at a lower compartment temperature between 125 'F and 135 'F for 72 cumulative hours within this 90-day period to avoid a unit shutdown caused by the Lake Norman heatup of late summer and early fall.
The licensee evaluated all the transients in Section 6.2 of the Updated Final Safety Analysis Report (UFSAR) to determine the effect of raising the initial containment lower compartment temperature from 120 'F to 135 'F. It was concluded that the relative ranking of the various breaks would remain unaffected. As a result, the limiting peak containment temperature transient for McGuire remains as the steam line break accident. However, due to the complex interactions, the specific effects of a steam line break can only be determined through a
- reanalysis using complex computer programs.
The need for reanalyses is due to a number of factors. An increase in the initial containment lower compartment temperature will impact the peak containment temperature following a steam line break due to the reduced energy transfer to the passive heat structures in the lower containment. A lower differential temperature between these structures and the containment atmosphere results in reduced condensation of steam on the surfaces of these structures, resulting in increasing pressures and temperatures in the lower containment.
For the reanalyses, the licensee used a previously approved methodology used originally to compute the containment responses for the McGuire Nuclear Station. They also used the same nodalization for GOTHIC as those approved by the staffin 1995. The mass and energy releases were not recalculated, since a singular change to the initial lower containment would not affect the blowdown profile. The ice condensar containment response was modeled using the GOTHIC 4.0/ DUKE computer code. Therefore, the reanalyses used the exact same nodalization, computer code, and blowdown profile as was used in the original analyses which were accepted by the staff in 1995. The only difference was the initial lower containment temperature, which was set at 135 'F rather than the previous value of 120 *F.
The licensee ran several steam line break cases. Examples of conservative assumptions that were used in both the original as well the most recent analyses included Technical Specifications limits for containment pressure of 0.3 psig; upper containment pressure of 100 'F; and ice condenser initial temperature of 30 'F. The assumed relative humidity level was kept the same for both sets of analyses at 100%. The only difference between the previously approved analysis and the current one is the lower containment initial temperature l
which was assumed to be 135 'F instead of 120 *F. The results showed that when the initial l
lower compartment temperature is increased to 135 *F, the maximum break compartment l
temperature increased to 317' F as compared to the previous peak value of 316 'F. The average containment lower compartment temperature is virtually urichanged, at 302 'F. Thus, I
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. it is apparent that a 15 'F increase in the initial containment lower compartment temperature eakes very little difference in1he peak temperature.
The licensee has evaluated the potential impact on the environmental qualification (EQ) of safety-related electrical equipment located in the lower containment when the containment lower compartment temperature is increased. The licensee documented that its ane!yses show l
that the highest containment temperature and lower containment average temperatures result-l from a 2.4 ft* main steamline break (MSLB). The compartment temperature following an MSLB of this size is 316 'F with an initial temperature of 120 'F. The peak lower containment average temperature for this case is 302 'F. Both of these values are below the qualification of 340 'F for McGuire. When the initial containment lower compartment temperature is increased to 135.*F, the maximum break containment temperature increases to 317 *F. The average containment lower compartment temperature is virtually unchanged at 302 'F.
The staff noted that the licensee's evaluation only addressed the bounding condition for the peak temperature conditions and did not address the conditions for the duration of a postulated loss-of-coolant accident (LOCA) and MSLB. The staff requested the licensee to provide the qualification temperature test profiles for a representative set of safety-related electrical components located in the containment lower compartment area and to demonstrate that these EQ test profiles still bound the new containment response profiles resulting from the proposed increase of initial containment lower compartment temperature.
By letter dated July 6,1998, the licensee responded to the staff's request, and provided test profile curves for several safety-related electrical components located in the containment lower compartments. The licensee also provided the long-term containment response (lower containment temperature) for both the 120 'F and 135 *F initial condiiions. The more severe initial temperature profile results from the MSLB during blowdown of the faulted generator.
Following the blowdown period, the containment temperature drops rapidly and the long-term l
containment temperature is less than the LOCA profile. A comparison of these curves indicates that a 10 'F increase in the initial containment lower compartment temperature does not make significant differences in containment lower compartment accident and post-accident responses. The EQ test profiles bound the accident profiles, including the peak conditions, with l
an adequate margin. In addition, the allowable window of 72 cumulative hours at the maximum temperature of 135 'F is small.
Since the licensee has performed all the transients in Section 6.2 of the UFSAR to determine the effect of raising the initial containment lower compartment temperature from 120 'F to 135 'F, and has evaluated the potential impact on the EQ of the safety-related electrical equipment located in the lower containment for the noted temperature increase, the staff finds that allowing the containment lower compartment temperature increase to 135 *F for a period of l
72 cumulative hours will not have a significant impact on the safety-related electrical equipment i
and the qualification of other equipment located in the lower compartment of the containment.
Therefore, the staff concludes that the proposed amendments will not have an adverse impact j
on the health and safety of the public, and finds the proposed change acceptable.
l l
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3.0 STATE CONSULTATION
in accordance with the Commission's regulations, the North Carolina State official was notified of the proposed issuance of the amendments. The State official had no comments.
4.0 ENVIRONMENTAL CONSIDERATION
The amendments change requirements with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20 and change surveillance requirements. The NRC staff has determined that the amendments involve no significant increase in the amounts, and no significant change in the types, of any effluents that may-be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendments involve no significant hazards consideration, and there has been no public comment on such finding (62 FR 6574 dated February 12,1997). Accordingly, the amendments meet the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendments.
5.0 CONCLUSION
The Commission has concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amendments will not be inimical to the common defense and security or to the health and safety of the public.
PrincipalContributors: A. Gill D. Nguyen Date: September 28, 1998
,