|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M3801999-10-21021 October 1999 Forwards Insp Rept 50-263/99-06 on 990813-0923.Four Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217G0711999-10-13013 October 1999 Forwards Insp Rept 50-263/99-12 on 990913-17.No Violations Noted ML20217B1421999-09-30030 September 1999 Informs That on 990902,NRC Staff Completed mid-cicle Plant Performance Review of Monticello Nuclear Generating Station. Staff Conducted Reviews for All Operating NPPs to Integrate Performance Information & to Plan for Insp Activities ML20212K9131999-09-30030 September 1999 Refers to 990920 Meeting Conducted at Monticello Nuclear Generating Station to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA ML20216J2491999-09-30030 September 1999 Ack Receipt of 980804,990626 & 0720 Ltrs in Response to GL 98-01,suppl 1, Year 2000 Readiness of Computer Sys at Npps. Staff Review Has Concluded That All Requested Info Has Been Provided ML20216G4341999-09-24024 September 1999 Forwards Exam Rept 50-263/99-301 on 990823-26.Violation Occurred & Being Treated as Ncv,Consistent with App C of Enforcement Policy.Test Was Administered to Two Applicants. Both Applicants Passed All Sections of Exam ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20216J8091999-09-24024 September 1999 Informs That New Diaphragm Matl Has Corrected Sticking Problem Associated with Increased Control Rod Drive Scram Times.Augmented Testing of Valves at Monticello Has Been Discontinued ML20212G9801999-09-23023 September 1999 Refers to Resolution of Unresolved Items Identified Re Security Alarm Station Operations at Both Monitcello & Prairie Island ML20212F0901999-09-21021 September 1999 Confirms Discussion Between M Hammer & Rd Lanksbury to Have Routine Mgt Meeting on 991005 in Lisle,Il.Purpose of Meeting to Discuss Improvement Initiatives in Areas of Operations & Equipment Reliability ML20212A9761999-09-0909 September 1999 Submits 1999 Annual Rept of Any Changes or Errors Identified in ECCS Analytical Models or Applications ML20217A5751999-09-0909 September 1999 Forwards Individual Exam Results for Licensee Applicants Who Took Aug 1999 Initial License Exam.Without Encls ML20211Q6981999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Monticello Operator License Applicants During Wks of 010604 & 11.Validation of Exam Will Occur at Station During Wk of 010514 ML20211L1981999-09-0101 September 1999 Forwards Insp Rept 50-263/99-05 on 990702-0812.No Violations Noted ML20211K7971999-09-0101 September 1999 Informs That Util Reviewed Rvid as Requested in NRC .Recommended Corrections Are Listed ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211F9961999-08-26026 August 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 990101-990630, Revised Effluent & Waste Disposal Semi-Annual Rept for 980701-981231 & Revs to ODCM for Monitcello Nuclear Generating Plant ML20211C9501999-08-23023 August 1999 Forwards Rev 17 to Monticello Nuclear Generating Plant USAR, Updating Info in USAR to Reflect Implementation of Increase in Licensed Core Thermal Power from 1,670 Mwt to 1,775 Mwt.Rept of Changes,Tests & Experiments Not Included ML20210T9601999-08-12012 August 1999 Provides Rept on Status of Util RPV Feedwater Nozzle Insps Performed in Response to USI A-10 Re BWR Nozzle Cracking ML20210U1831999-08-12012 August 1999 Revises 980202 Commitment Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design- Basis Accident Conditions ML20210Q0341999-08-0404 August 1999 Forwards SE Granting Licensee 980724 Relief Request 10 Re Third 10-year Interval ISI Program Plan,Entitled, Limited Exam ML20210H0861999-07-28028 July 1999 Forwards Insp Rept 50-263/99-04 on 990521-0701.No Violations Noted.Licensee Conduct at Monticello Facility Characterized by safety-conscious Operations,Sound Engineering & Maint Practices & Appropriate Radiological Controls ML18107A7051999-07-20020 July 1999 Provides Suppl Info Which Supersedes Info in 990625 Ltr in Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML20212H3191999-07-16016 July 1999 Forwards Aug 1999 Monticello RO Exam Package,Including Revised Outlines.All Changes Are in Blue Font ML20209G5621999-07-14014 July 1999 Forwards Insp Rept 50-263/99-11 on 990621-24.No Violations Noted.Objective of Insp,To Determine Whether Monticello Nuclear Generating Station Emergency Plan Adequate & If Station Personnel Properly Implemented Emergency Plan ML20196J5351999-07-0202 July 1999 Discusses GL 92-01,Rev 1,Supp 1, Rv Integrity, Issued by NRC on 950515 & NSP Responses & 980917 for Monticello Npp.Informs That Staff Revised Info in Rvid & Released Info as Rvid Version 2 ML20196J9681999-07-0101 July 1999 Informs That in Sept 1998,Region III Received Rev 20 to Portions of Util Emergency Plan Under 10CFR50.54(q).Based on Determination That Changes Do Not Decrease Effectiveness of Licensee Emergency Plan,No NRC Approval Required ML20209B6151999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Y2K Readiness Disclosure Attached ML20196H2291999-06-24024 June 1999 Responds to Administrative Ltr 99-02,dtd 990603,requesting Licensee to Provide Estimate of Licensing Action Submittals Anticipated.Four New Submittals Per Year Are Anticipated IR 05000263/19990031999-06-18018 June 1999 Forwards Insp Rept 50-263/99-03 on 990409-0520.Four Violations Noted & Being Treated as non-cited Violations, Consistent with App C of Enforcement Policy ML20207D5851999-05-25025 May 1999 Submits Info Re Partial Fulfillment of License Conditions Placed on Amend 101,which Approved Use of Ten Exceptions for 24 Months Subject to Listed App C Conditions.Util Will Submit Second Rept to Obtain Approval for Continued Use ML20206S0911999-05-17017 May 1999 Forwards Response to NRC 990324 RAI Re Proposed Amend to pressure-temp Limits & Surveillance Capsule Withdrawal Schedule, .Supporting Calculations Also Encl ML20206N5601999-05-13013 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Cm Craig Will Be Section Chief for Monticello Npp.Organization Chart Encl ML20206G2181999-05-0505 May 1999 Discusses Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, Dtd 960110,for Plant ML20206G4901999-05-0404 May 1999 Forwards Staff Review of Licensee 960508 Response to NRC Bulletin 96-002, Movement of Heavy Loads Over Sf,Over Fuel in Rc or Over Safety-Related Equipment, .Overall, Responses Acceptable.Tac M95610 Closed ML20206G7741999-05-0303 May 1999 Forwards Insp Rept 50-263/99-02 on 990223-0408.One Violation Occurred & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20206D1651999-04-27027 April 1999 Forwards Radiation Environ Monitoring Program for MNGP for Jan-Dec 1998, Per Plant TS 6.7.C.1.Ltr Contains No New NRC Commitments or Modifies Any Prior Commitments ML20205N0821999-04-12012 April 1999 Forwards SE of NSP Response to NRC GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves. Licensee Adequately Addressed Actions Requested in GL ML20205N4811999-04-0909 April 1999 Forwards Licensing Requalification Insp Rept 50-263/99-10 on 990308-12.No Violations Noted.However,Inspectors Through Observation of Simulator Scenario Exams Noted Difficulties in Ability of SM to Simultaneously Implement Duties of SM ML20205N5301999-04-0909 April 1999 Discusses Arrangements Made on 990406 for Administration of Licensing Exams at Monticello Nuclear Generating Station During Wk of 990823.Requests That Exam Outlines Be Submitted by 990128 & Supporting Ref Matls by 990719 ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20205C4851999-03-26026 March 1999 Informs That on 990203,NRC Staff Completed PPR of Nuclear Plant.Staff Conducts Reviews for All Operating NPPs to Develop an Integrated Understanding of Safety Performance ML20205A5881999-03-24024 March 1999 Forwards Request for Addl Info Re Submittal Requesting Rev of pressure-temperature Limits & Surveillance Capsule Withdrawal Schedule ML20204H4711999-03-18018 March 1999 Forwards SER Concluding That Util Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello & Adequately Addressed Actions Requested in GL 96-05 ML20207H5161999-03-11011 March 1999 Forwards Insp Rept 50-263/99-01 on 990112-0222.No Violations Noted ML20207F4091999-02-28028 February 1999 Forwards Fitness for Duty Program Performance Data for Six Month Period from 980701-981231,IAW 10CFR26.71 ML20207F6741999-02-24024 February 1999 Forwards Summary of Nuclear Property Insurance Maintained at Monticello & Prairie Island Nuclear Generating Plants ML20207F6901999-02-23023 February 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 980701-981231, Off-Site Radiation Dose Assessment for 980101-981231 & Revised Effluent & Waste Disposal Semi- Annual Rept for 980101-980630, for Monticello 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20216J8091999-09-24024 September 1999 Informs That New Diaphragm Matl Has Corrected Sticking Problem Associated with Increased Control Rod Drive Scram Times.Augmented Testing of Valves at Monticello Has Been Discontinued ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212A9761999-09-0909 September 1999 Submits 1999 Annual Rept of Any Changes or Errors Identified in ECCS Analytical Models or Applications ML20211K7971999-09-0101 September 1999 Informs That Util Reviewed Rvid as Requested in NRC .Recommended Corrections Are Listed ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211F9961999-08-26026 August 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 990101-990630, Revised Effluent & Waste Disposal Semi-Annual Rept for 980701-981231 & Revs to ODCM for Monitcello Nuclear Generating Plant ML20211C9501999-08-23023 August 1999 Forwards Rev 17 to Monticello Nuclear Generating Plant USAR, Updating Info in USAR to Reflect Implementation of Increase in Licensed Core Thermal Power from 1,670 Mwt to 1,775 Mwt.Rept of Changes,Tests & Experiments Not Included ML20210T9601999-08-12012 August 1999 Provides Rept on Status of Util RPV Feedwater Nozzle Insps Performed in Response to USI A-10 Re BWR Nozzle Cracking ML20210U1831999-08-12012 August 1999 Revises 980202 Commitment Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design- Basis Accident Conditions ML18107A7051999-07-20020 July 1999 Provides Suppl Info Which Supersedes Info in 990625 Ltr in Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML20212H3191999-07-16016 July 1999 Forwards Aug 1999 Monticello RO Exam Package,Including Revised Outlines.All Changes Are in Blue Font ML20209B6151999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Y2K Readiness Disclosure Attached ML20196H2291999-06-24024 June 1999 Responds to Administrative Ltr 99-02,dtd 990603,requesting Licensee to Provide Estimate of Licensing Action Submittals Anticipated.Four New Submittals Per Year Are Anticipated ML20207D5851999-05-25025 May 1999 Submits Info Re Partial Fulfillment of License Conditions Placed on Amend 101,which Approved Use of Ten Exceptions for 24 Months Subject to Listed App C Conditions.Util Will Submit Second Rept to Obtain Approval for Continued Use ML20206S0911999-05-17017 May 1999 Forwards Response to NRC 990324 RAI Re Proposed Amend to pressure-temp Limits & Surveillance Capsule Withdrawal Schedule, .Supporting Calculations Also Encl ML20206D1651999-04-27027 April 1999 Forwards Radiation Environ Monitoring Program for MNGP for Jan-Dec 1998, Per Plant TS 6.7.C.1.Ltr Contains No New NRC Commitments or Modifies Any Prior Commitments ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20207F4091999-02-28028 February 1999 Forwards Fitness for Duty Program Performance Data for Six Month Period from 980701-981231,IAW 10CFR26.71 ML20207F6741999-02-24024 February 1999 Forwards Summary of Nuclear Property Insurance Maintained at Monticello & Prairie Island Nuclear Generating Plants ML20207F6901999-02-23023 February 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 980701-981231, Off-Site Radiation Dose Assessment for 980101-981231 & Revised Effluent & Waste Disposal Semi- Annual Rept for 980101-980630, for Monticello ML20203A3081999-01-28028 January 1999 Forwards TS Page 60d,as Supplement 3 to 971125 LAR Re CST Low Level Hpci/Rcic Suction Transfer.Page Includes NRC Approved Amend 103 Changes for Use by NRC in Issuing SER ML20202F7821999-01-27027 January 1999 Forwards 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility, Per 10CFR55.45(b)(5)(ii) & 10CFR55.45(b)(5)(vi).Ltr Contains No New Commitments or Modifies Any Prior Commitments ML20206S0331999-01-20020 January 1999 Submits Annual Rept of Safety & Relief Valves Failure & Challenges ML20206P1221998-12-31031 December 1998 Forwards LAR for License DPR-22,revising TS pressure-temp Curves Contained in Figures 3.6.1,3.6.2,3.6.3 & 3.6.4, Deleting Completed RPV Sample SRs & Requirement to Withdraw Specimen at Next Refueling Outage & Removing Redundant SR ML20198M3271998-12-28028 December 1998 Submits Change to Commitment for Submittal of ITS Application.Util Plans to Provide ITS Conversion Package Submittal to NRC in Dec of 2000 ML20198J7511998-12-22022 December 1998 Informs of Completion of Listed Commitment Made in Re Severe Accident Mgt. Severe Accident Mgt Guidelines Have Been Assessed,Plant Procedures Have Been Modified & Training of Affected Plant Staff Has Been Completed ML20198J4311998-12-21021 December 1998 Forwards Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv. Under Separate Cover,Licensee Is Providing LAR to Revise Curves ML20198J7711998-12-14014 December 1998 Documents 981214 Discussion with NRC Staff Re Deviation from Emergency Procedure Guidelines ML20195C9631998-11-11011 November 1998 Forwards 120-day Response to NRC GL 98-04, Potential for Degradation of ECCS & CSS After LOCA Because of Construction & Protective Coating Deficiencies & Foreign Matl in Containment ML20195C8781998-11-11011 November 1998 Forwards Supplement to 971125 License Amend Request Re Condensate Storage Tank Low Level Suction Transfer Setpoints for HPCI Sys & Reactor Core Isolation Cooling Sys ML20195E2261998-11-10010 November 1998 Submits Suppl 1 to Util Response to NRC Request for Addl Info Re 981118 Request for Deviation from Emergency Procedure Guidelines ML20155H6591998-11-0404 November 1998 Forwards Response to 980910 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20155F9091998-10-27027 October 1998 Forwards Master Table of Contents to Rev 16 of Usar.Info Was Inadvertantly Omitted at Time of 981023 Submittal ML20155A2661998-10-23023 October 1998 Forwards Rev 16 to USAR for Monticello Nuclear Generating Plant. Summary of Changes,Tests & Experiments Made Under Provisions of 10CFR50.59(b)(2) Also Encl.Rev Updates Info in USAR for Period Up to 980801 05000263/LER-1998-005, Forwards LER 98-005-00,re HPCI Being Removed from Service to Repair Steam Leak in Drain Trap Bypass.Commitments Made by Util Are Listed1998-10-21021 October 1998 Forwards LER 98-005-00,re HPCI Being Removed from Service to Repair Steam Leak in Drain Trap Bypass.Commitments Made by Util Are Listed ML20154L9321998-10-12012 October 1998 Forwards Suppl 2 to LAR & Suppl 980319,which Proposed Changes to Ts,App a of Operating License DPR-22 for Mngp.Number of Addl Typos & One Title Change on Pages Associated with Amend Request Have Been Identified 05000263/LER-1998-004, Forwards LER 98-004-00 Re Manual Scram Inserted Following Pressure Transient Closes Air Ejector Suction Isolation Valves & Trips Offgas Recombiners.Ler Contains Listed Commitment1998-10-0909 October 1998 Forwards LER 98-004-00 Re Manual Scram Inserted Following Pressure Transient Closes Air Ejector Suction Isolation Valves & Trips Offgas Recombiners.Ler Contains Listed Commitment ML20154L8671998-10-0909 October 1998 Forwards Suppl 1 to LAR for License DPR-22, Replacing Exhibits B & C of Original Submittal to Reflect Item 2 & Subsequent Changes.Request for APRM Flow Converter Calibr Interval Extension,Withdrawn ML20154J6201998-10-0505 October 1998 Forwards Rev 49 to Monticello Security Plan.Encl Withheld, Per 10CFR73.21 ML20154D7921998-10-0101 October 1998 Forwards Response to NRC RAI Re Licensee 971118 Request for Deviation from Emergency Procedures Guidelines.Proprietary Flow Charts,Including Rev 5 to C.5-110 RPV Control & Rev 6 to C.5-110 RPV Control, Encl.Proprietary Info Withheld ML20154D8031998-09-25025 September 1998 Submits Annual Rept of Any Change or Error Identified in ECCS Analytical Models or Application ML20153F0051998-09-25025 September 1998 Forwards Suppl 1 to 971031 Application for Amend to License DPR-22,replacing Exhibit C Which Contains TS Pages Incorporating Proposed Changes Described in Original 971031 Request ML20153F5351998-09-25025 September 1998 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Improved TS ML20153E0331998-09-17017 September 1998 Forwards Response to NRC 980629 RAI Re RPV Weld Chemistry Values Previously Submitted as Part of Plant Licensing Basis.Next Monticello RPV Sample Capsule Scheduled to Be Removed During 1999/2000 Refueling Outage ML20153D1441998-09-17017 September 1998 Informs NRC That Listed Commitments 1 & 3 Were Completed by End of 1998 Refueling Outage.Commitments Involved Final Disposition of Remaining Outlier Components Re All Known Outstanding Work Associated with GL 87-02,Suppl 1,USI A-46 ML20153D8561998-09-17017 September 1998 Forwards Rev 17 to EPIP A.2-414, Large Vol Liquid Sample &/ or Dissolved Gas Sample Obtained at Post Accident Sampling Sys. Superseded Procedures Should Be Destroyed.Ltr Contains No New NRC Commitments,Nor Does It Modify Prior Commitments ML20153E9011998-09-0909 September 1998 Forwards Rev 1 to MNGP Colr,Cycle 19, Incorporating Changes to power-flow Maps in Figures 6 & 7.Changes Made to Correct Errors in Stability Exclusion Region & Stability Buffer Region Shown on Rev 0 ML20151S7401998-08-28028 August 1998 Responds to NRC Re Violations Noted in Insp Rept 50-263/98-09.Corrective Actions:Procedure 4 AWI-04.04.03 Will Be Revised to Eliminate Term Urgent from Section 4.3.1.D 1999-09-09
[Table view] |
Text
..
t Begubtmy Dodet Rie-ygy f
NORTHERN STATE 5 POWER COMPANY MIN N E A POL 6 9 M 4NN E sb7A B D 4 01
/nm.fNj %
,/f -
N October 26, 1973
,/
'j 4 39
' 7 / D/d h
Mr. J F O' Leary, Director
'cf.}y[pj b\\
W Directorate of Licensit.g
'6' g -
1p Office of Regulation
% Q)Q,}, g:
",/s s
U S Atomic Energy Commit,sion Wa shington, D C 20545
'&ge
Dear Mr. O'Learv :
MOSTICELLO NUCLEAR GESERATING P1 ANT Docket No. 50-263 License No. DPR-22 change Request Dated October 26, 1973 Attached are three signed originals and 37 conformed copics of a request for change of Technical Specifications, Appendix A, of the Provisional Operating hLicense DPR-22, for the Monticello Nuclear t,cnerating Plant.
This change request has bee.n reviewed by the Monticello Operations Committci. and the Safety Audit Committee.
On August 20, 1071, we submitted a document entitled " Change Request No. 3" which included a compilation of errors and inadequacies of the initial print-ing of the ' icd dr.,
acifications. As pages have since been revised for other reasont. t
'2s from Change Request No. 3 have been incorporated into the revisi "s.
'.e more significant: changes remaining in Change Request No. 3, which war. ant present consideration, are compiled in the attached change request.
The re:naining portions of Change Request No. 3 will be incorporated into later requested changes as in the past.
In this uay Change Request No. 3 will in ef fect be deleted.
0.. September 22, 1973, supplement No. I to Change Request No. 3 was submitted the AEC request to it.chde control rod drop accident considerations and atother topics. We understand that this, supplement is presently under review and should not be considered deleted.
[v,, \\ 'II1/./
\\
Yours very truly, SEP
/
A L 0 M2yer, PE s'
OCT S11973 t-11 Director of Nuclear Support Services g,g
~
/
1n s;: w; l
WCpCLM [
LOMhMV/br cc:
J G Kcppler l
G Charnof f l
Minnesota Pollution Control Agency 7gy a
,,n_...,
91043DC426 731026 PDR ADOCK 050C0263 P
PbR l.
C Regulatory Docket File 3
cWN
" ' ",. g gn EXH1B1T A
~~
MONTICELLO NUCLEAR GENERATING PLANT DOCKET No. 50-263 CHANGE REQUEST DATED OCTOBER 26, 1973 PROPOSED CHANGES TO THE TECHNICAL SPECIFICATIONS APPENDIX A 0F PROVISIONAL OPERATING LICENSE NO. DPR-22 Pursuant te 10CFR50.59, the holders of the abovc-mentioned license hereby propese the following changes to Appendix A, Technical Specifications.
1.
PR0 POSED CilANGE on page 7, TS 2.1.B, change ".... less than 25% of design.... " to read ".... less than 5% of design....
On page 10, Figure 2.1.1, extend the two curves linearly from the pres-ent termination at 25% flow to 5% flow at 187. thermal power (300 MW).
i on page 15, Bases: 2.1, change the first two sentences of the last paragraph to read "The renge in pressure and flow usud fot Specifi-cation 2.1.A was 600 psig to 1250 psig and 5% to 100% flow respec-tively.
Specification 2.1.B requires a restriction on power level when operating below 500 psig or 5% flow."
REASON FOR CRANCE The basis given for fuel cladding integrity safety limits applies to the lower core flow limit of 5% but with less margin than the current lowcr limit of 25% flow.
Following the recirculation pump trip test at Monticello, the operating point was found to be close to the 25%
flow limit lire.
These changes will decrease the chance of a "techni-cal" violation of the Specification and will make the safety limit curve consistent with curves presently in use at other facilities.
2.
PROPOSED CHANGE on page 30 Table 3.1.1, opposite Item 4.c, add ":E[3/125 of full scale" under the column of Limiting Trip Settings.
RFASDA FOR CHANGE This was an omission in previous submittals.
v
/~
EXHIBIT A s 3.
PROPOSED C11ANCE On page 51, Tabic 3.2.1, chat.ge the Item 4 entry to read as follows:
Min No of Opera-Total No of ble or Operating Trip Inst Ch per Inrt Ch per Trip Required Function Settings Trip System System (1,2)
Conditions 1
4.
IIPCI Steam Lines a.
IIPCI liigh 51150,000 2 (4) 2 F
Steam Flow lb/hr with 1
j
$;60 second time delcy b.
HPCI 111gh 6;300,000 2 (4) 2 F
Steam Flow lb/hr j
c.
HPCI Steam
- 55 2000F 16(4) 16 F
Lipe Area High Temp REASON FOR CHANGC On HPCI initiation, initial steam flow surges cause instrumentation indica-tions in excess of the current trip setting of 150,000 lb/hr.
Testing of this system has shown that normal steam flow indications are reached within 60 seconds after initially exceeding the 150,000 lb/hr trip setting.
The trip setting of 300,000 lb/hr will provide steam line break protection during the time delay period on the 150,000 lb/hr trip.
Wording in the current Technical Specifications is actually inconsistent with the trip system agreed upon with AEC-DL and installed in the plant. This change corrects the wording to be consistent with the existing trip system.
l 4
PROPOSED CHANGE On page 70, Table 3.2.5, opposite entry " Instrumentation That Initiates Rod Block - Table 3.2.3" add "APRM Downscale" and "RBM Downscale" under the Trip Function column and add "- 2/125 of Scale" for each new entry i
under the Deviation column.
I RFAFON FOR CHANGE I
j AEC Change No. 5 to the Technical Specifications included a change in the l
APRM and REM downecale trip settings.
The bases (page 70) lack
=~- -.- - - ~ -
~ _.
/~
(
4 EXHIBIT A j :
l an allowable deviation for the ApRM and RBM downscale trip settings.
Ad-dition of these allowable deviations in the bases are desirable to avoid
)
inadvertent scrams during startup or shutdown due to the current need to set the actual tripc at 5%, to assure that the 3% limit is always main-tained, and thereby creating a narrow interlock overlap between IRM's and APRM's.
i 5.
PROPOSED CHANGE I
on page 92, Figure 3.4.1, con'tinue the lower portion of the curve to terminate at 10.8% at 2895 gallons.
Remove the limit of 11.4%
atit 2700 gallone.
i REASON FOR CllANGE In one of the early draf t ver; ions of the Technical Specifications, the bottom portion of the curve was removed to assure that the required amount of boron would be injected within 100 minutes at a minimum flow of 27 gpm.
Subsequently, the requirements were changed.
The present Specification and bases require a minimum flow of 24 gpm and a pumping time not to exceed 125 minutes.
Restoration of the lower portion of the curve is consistent with the present bases and will allow lower concentrations, thereby reducing minimum temperature requirements and reducing the possibility of crystallization.
6.
PROPOSED CitANGE On page 92, figure 3.4.1, add the following parenthetical statement to the ordinate label:
(as w/o Na2B10016 ' 10110).
2 2
On page 93, Figure 3.4.2, add the following parenthetice' statement to the cissa label:
(as w/o Na2 10 16
B 0 REASON FOR CilANGE The proper chemical form of sodium pentaborate for the standby liquid control system was not precisely identified in the Technical Specifica-tions. Addition of the formula for the decahydrate form to Figure 3.4.1 and 3.4.2 is appropriate for clarification.
7.
PROPOSED CllANCE on page 134, Basis 4.6.D, Coolant Leakage, delete the third paragraph and substitute the following paragraph:
"An annual report will be prepared and submitted to the AEC summarizing the primary coolant to drywell leakage measure-n-
r 1
s.
EXHIBIT A
, ments.
Other techniques for detecting leaks and the applicability of these techniques to the Monticello Plant will be the subject of continued study."
REASON FOR CRANCE This basis and the original Technical Specification required a one-thne report after 18 months of plant operation which was to include an eval-untion of the performance of the reactor coolant leakage detection sys-tem.
This reporting requirement Gas fulfilled by a Ictter from L 0 Mayer (NSP) to A Giambusso (AEC) dated December 28, 1972. This report described a systen for bmprovement of the speed of leak detection which was undergoing technical evaluation.
Equipment for this system is on order and will be installed at the firat outage of suf ficient duration to permit its installation.
AEC Change No. 6 to the Monticello Technical Specifications dated April 3,1973 included certain modifications to the reporting requirements under TS 6.7 C, Special Reports.
One of these modifications was to require an annual report on primary coolant leakage to the drywell.
This proposed change is to make the basis consistent with the new reporting requirement.
8.
PR0p0 SED CRANCE on page 150, TS 4.7.C.1.a-c, delete paragraph a; delete paragraph b; reletter paragraph c as paragraph a and insert it in place of paragraph a; and in new paragraph a, change ".... rate oi 4,000 sefm.... " to read ".... rate of dE 4,000 sc fm.... " Add a acntence at the end of new paragraph a to read, "This surveillance testing should be reported in the semiannual operating reports.
REASON FOR CHANCE The preoperational tests required by existing paragraph a have been conducted.
The additional tests required by existing paragraph b during the first operating cycle have been performed and reported as required in TS 6.7.C.2 in a letter from L 0 Mayer (NSF) to J F O' Leary (AEC) dated July 23, 1973.
The addition of the "2E" sign ahead of 4,000 scfm allows more flexibility in operation and test-ing but still requires demonstration of the specified integrity.
9.
PROPOSED CRANCE en page 164, Basic 4.7, econd paragraph, delete last two sentences, "In addition,.... to the AEC."
Substitute the following sentence:
l 1
r EXHIBIT A
, "A sunnary report of the results of main steam line isolation valve Icakage tests and closure time measurements will be pre-pared and submitted to the AEC following completion of periodic main steam isolation valve Icakage tests."
REASG4 FOR CHANCE This basis and the original Technical Specification required a one-time report after 18 months of plant operation to report on main stema iso-lation valve performance and to include an evaluation of programs at other plants to reduce Icakage.
This reporting requirement was fulfilled by a letter from L 0 Mayer (NSP) to A Giambusso (AEC) dated December 28, 1972 and supplemented by a letter from L 0 Mayer (NSP) to J F O' Leary (AEC) dated June 28, 1973.
AEC Change No. 6 to the Monticello Technical Specifications dated April 3, 1973 included certain modifications to the reporting requirements under TS 6.7.C, Special Reports.
One of these modifications was to require a report of the results of main steam isolation valve leakage tests and closure time measurements with a submittal date of 90 days af ter completion of the periodic main steam isolation valve Icak rate tests.
This proposed change is to make the basis consistent with the new reporting requirement.
10.
PROPOSED CHANGE On page 216, TS 6.7. A.2.1, under Occupational Personnel Radiation Exposure, delete the whole paragraph and substitute the following paragraphs:
" Tabulate the number of personnel exposures for plant per-sonnel (permanent and temporary) in the following exposure increments for the reporting period:
less than 100 mrem, 100 - 500 aren, 500 - 1250 mrem, 1250 - 2500 mrem, above 2500 mrem.
Tabulate the number of personnel receiving more than 500 mrem exposure in the reporting period according to duty
- function, i.e.,
routine plant surveillance and inspection (regular duty), routine plant maintenance, special plant maintenance (describe maintenance), routine refueling operations, special refueling operation (describe opera-l tion) and other job related exposures. Annually tabulate 1
the number of personnel receiving more than 2500 mrca and report major cause(s)."
Move TS 6.7. B, Non-Routine Reports, to a new page 216A.
7 l
l l
l i
J r'
s
.)
EXil1 BIT A j
6-REASON FOR CilANCE 1
1 The proposed wording reficcts the current desires of the AEC and is identical to that which has been included in the NSP Prairic Island j
Plant Technical Specifications.
It is highly desirable that TS 6.0, 1
Administrative Ccatrols, be as consistent as possible for each nuc-lear plant operated by a given licensee, i
11.
PROPOSED CHANCE f
on page 62. Tabic 4.2.1 change the calibration frequency entry for the of f Gas Isolation Monitors from "onc.e/3 months" to.
" Note 6."
a REASON FOR CHANGE The proposed wording more precisely defines the method used for the
]
three-month and refueling outage calibrations.
]
12.
PROPOSED CHANGE on page 70, Table 3.2.5, under Trip Function, change " Reactor Low Pressure Permissive" to " Reactor Low Pressure (Pump Start)
Permissive" and change " Low Reactor Pressure Valve Permissive" to " Low Reactor Pressure (Valve Permissive)."
'i REASON FOR CHANGE 4
The proposed wording more precisely defines the trip function and is consistent with the functions listed in Table 3.2.2.
a l
i
)
b i
l 5
r A
(.1 D3tIBIT B 1his exhibit consists of the following pages revised to incorporate the proposed changes:
I Page 7 l
Page 10 Page 15 Page 30 Page 51 Page 62 Page 70 Page 92 Page 93 j
Page 134 Page 150 i
Page 164 Page 216 I
Page 216A i
l l
u i
f i
l i
I l
\\
i i
l i