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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M3801999-10-21021 October 1999 Forwards Insp Rept 50-263/99-06 on 990813-0923.Four Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217G0711999-10-13013 October 1999 Forwards Insp Rept 50-263/99-12 on 990913-17.No Violations Noted ML20217B1421999-09-30030 September 1999 Informs That on 990902,NRC Staff Completed mid-cicle Plant Performance Review of Monticello Nuclear Generating Station. Staff Conducted Reviews for All Operating NPPs to Integrate Performance Information & to Plan for Insp Activities ML20212K9131999-09-30030 September 1999 Refers to 990920 Meeting Conducted at Monticello Nuclear Generating Station to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA ML20216J2491999-09-30030 September 1999 Ack Receipt of 980804,990626 & 0720 Ltrs in Response to GL 98-01,suppl 1, Year 2000 Readiness of Computer Sys at Npps. Staff Review Has Concluded That All Requested Info Has Been Provided ML20216G4341999-09-24024 September 1999 Forwards Exam Rept 50-263/99-301 on 990823-26.Violation Occurred & Being Treated as Ncv,Consistent with App C of Enforcement Policy.Test Was Administered to Two Applicants. Both Applicants Passed All Sections of Exam ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20216J8091999-09-24024 September 1999 Informs That New Diaphragm Matl Has Corrected Sticking Problem Associated with Increased Control Rod Drive Scram Times.Augmented Testing of Valves at Monticello Has Been Discontinued ML20212G9801999-09-23023 September 1999 Refers to Resolution of Unresolved Items Identified Re Security Alarm Station Operations at Both Monitcello & Prairie Island ML20212F0901999-09-21021 September 1999 Confirms Discussion Between M Hammer & Rd Lanksbury to Have Routine Mgt Meeting on 991005 in Lisle,Il.Purpose of Meeting to Discuss Improvement Initiatives in Areas of Operations & Equipment Reliability ML20212A9761999-09-0909 September 1999 Submits 1999 Annual Rept of Any Changes or Errors Identified in ECCS Analytical Models or Applications ML20217A5751999-09-0909 September 1999 Forwards Individual Exam Results for Licensee Applicants Who Took Aug 1999 Initial License Exam.Without Encls ML20211Q6981999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Monticello Operator License Applicants During Wks of 010604 & 11.Validation of Exam Will Occur at Station During Wk of 010514 ML20211L1981999-09-0101 September 1999 Forwards Insp Rept 50-263/99-05 on 990702-0812.No Violations Noted ML20211K7971999-09-0101 September 1999 Informs That Util Reviewed Rvid as Requested in NRC .Recommended Corrections Are Listed ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211F9961999-08-26026 August 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 990101-990630, Revised Effluent & Waste Disposal Semi-Annual Rept for 980701-981231 & Revs to ODCM for Monitcello Nuclear Generating Plant ML20211C9501999-08-23023 August 1999 Forwards Rev 17 to Monticello Nuclear Generating Plant USAR, Updating Info in USAR to Reflect Implementation of Increase in Licensed Core Thermal Power from 1,670 Mwt to 1,775 Mwt.Rept of Changes,Tests & Experiments Not Included ML20210T9601999-08-12012 August 1999 Provides Rept on Status of Util RPV Feedwater Nozzle Insps Performed in Response to USI A-10 Re BWR Nozzle Cracking ML20210U1831999-08-12012 August 1999 Revises 980202 Commitment Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design- Basis Accident Conditions ML20210Q0341999-08-0404 August 1999 Forwards SE Granting Licensee 980724 Relief Request 10 Re Third 10-year Interval ISI Program Plan,Entitled, Limited Exam ML20210H0861999-07-28028 July 1999 Forwards Insp Rept 50-263/99-04 on 990521-0701.No Violations Noted.Licensee Conduct at Monticello Facility Characterized by safety-conscious Operations,Sound Engineering & Maint Practices & Appropriate Radiological Controls ML18107A7051999-07-20020 July 1999 Provides Suppl Info Which Supersedes Info in 990625 Ltr in Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML20212H3191999-07-16016 July 1999 Forwards Aug 1999 Monticello RO Exam Package,Including Revised Outlines.All Changes Are in Blue Font ML20209G5621999-07-14014 July 1999 Forwards Insp Rept 50-263/99-11 on 990621-24.No Violations Noted.Objective of Insp,To Determine Whether Monticello Nuclear Generating Station Emergency Plan Adequate & If Station Personnel Properly Implemented Emergency Plan ML20196J5351999-07-0202 July 1999 Discusses GL 92-01,Rev 1,Supp 1, Rv Integrity, Issued by NRC on 950515 & NSP Responses & 980917 for Monticello Npp.Informs That Staff Revised Info in Rvid & Released Info as Rvid Version 2 ML20196J9681999-07-0101 July 1999 Informs That in Sept 1998,Region III Received Rev 20 to Portions of Util Emergency Plan Under 10CFR50.54(q).Based on Determination That Changes Do Not Decrease Effectiveness of Licensee Emergency Plan,No NRC Approval Required ML20209B6151999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Y2K Readiness Disclosure Attached ML20196H2291999-06-24024 June 1999 Responds to Administrative Ltr 99-02,dtd 990603,requesting Licensee to Provide Estimate of Licensing Action Submittals Anticipated.Four New Submittals Per Year Are Anticipated IR 05000263/19990031999-06-18018 June 1999 Forwards Insp Rept 50-263/99-03 on 990409-0520.Four Violations Noted & Being Treated as non-cited Violations, Consistent with App C of Enforcement Policy ML20207D5851999-05-25025 May 1999 Submits Info Re Partial Fulfillment of License Conditions Placed on Amend 101,which Approved Use of Ten Exceptions for 24 Months Subject to Listed App C Conditions.Util Will Submit Second Rept to Obtain Approval for Continued Use ML20206S0911999-05-17017 May 1999 Forwards Response to NRC 990324 RAI Re Proposed Amend to pressure-temp Limits & Surveillance Capsule Withdrawal Schedule, .Supporting Calculations Also Encl ML20206N5601999-05-13013 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Cm Craig Will Be Section Chief for Monticello Npp.Organization Chart Encl ML20206G2181999-05-0505 May 1999 Discusses Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, Dtd 960110,for Plant ML20206G4901999-05-0404 May 1999 Forwards Staff Review of Licensee 960508 Response to NRC Bulletin 96-002, Movement of Heavy Loads Over Sf,Over Fuel in Rc or Over Safety-Related Equipment, .Overall, Responses Acceptable.Tac M95610 Closed ML20206G7741999-05-0303 May 1999 Forwards Insp Rept 50-263/99-02 on 990223-0408.One Violation Occurred & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20206D1651999-04-27027 April 1999 Forwards Radiation Environ Monitoring Program for MNGP for Jan-Dec 1998, Per Plant TS 6.7.C.1.Ltr Contains No New NRC Commitments or Modifies Any Prior Commitments ML20205N0821999-04-12012 April 1999 Forwards SE of NSP Response to NRC GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves. Licensee Adequately Addressed Actions Requested in GL ML20205N4811999-04-0909 April 1999 Forwards Licensing Requalification Insp Rept 50-263/99-10 on 990308-12.No Violations Noted.However,Inspectors Through Observation of Simulator Scenario Exams Noted Difficulties in Ability of SM to Simultaneously Implement Duties of SM ML20205N5301999-04-0909 April 1999 Discusses Arrangements Made on 990406 for Administration of Licensing Exams at Monticello Nuclear Generating Station During Wk of 990823.Requests That Exam Outlines Be Submitted by 990128 & Supporting Ref Matls by 990719 ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20205C4851999-03-26026 March 1999 Informs That on 990203,NRC Staff Completed PPR of Nuclear Plant.Staff Conducts Reviews for All Operating NPPs to Develop an Integrated Understanding of Safety Performance ML20205A5881999-03-24024 March 1999 Forwards Request for Addl Info Re Submittal Requesting Rev of pressure-temperature Limits & Surveillance Capsule Withdrawal Schedule ML20204H4711999-03-18018 March 1999 Forwards SER Concluding That Util Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello & Adequately Addressed Actions Requested in GL 96-05 ML20207H5161999-03-11011 March 1999 Forwards Insp Rept 50-263/99-01 on 990112-0222.No Violations Noted ML20207F4091999-02-28028 February 1999 Forwards Fitness for Duty Program Performance Data for Six Month Period from 980701-981231,IAW 10CFR26.71 ML20207F6741999-02-24024 February 1999 Forwards Summary of Nuclear Property Insurance Maintained at Monticello & Prairie Island Nuclear Generating Plants ML20207F6901999-02-23023 February 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 980701-981231, Off-Site Radiation Dose Assessment for 980101-981231 & Revised Effluent & Waste Disposal Semi- Annual Rept for 980101-980630, for Monticello 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20216J8091999-09-24024 September 1999 Informs That New Diaphragm Matl Has Corrected Sticking Problem Associated with Increased Control Rod Drive Scram Times.Augmented Testing of Valves at Monticello Has Been Discontinued ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212A9761999-09-0909 September 1999 Submits 1999 Annual Rept of Any Changes or Errors Identified in ECCS Analytical Models or Applications ML20211K7971999-09-0101 September 1999 Informs That Util Reviewed Rvid as Requested in NRC .Recommended Corrections Are Listed ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211F9961999-08-26026 August 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 990101-990630, Revised Effluent & Waste Disposal Semi-Annual Rept for 980701-981231 & Revs to ODCM for Monitcello Nuclear Generating Plant ML20211C9501999-08-23023 August 1999 Forwards Rev 17 to Monticello Nuclear Generating Plant USAR, Updating Info in USAR to Reflect Implementation of Increase in Licensed Core Thermal Power from 1,670 Mwt to 1,775 Mwt.Rept of Changes,Tests & Experiments Not Included ML20210T9601999-08-12012 August 1999 Provides Rept on Status of Util RPV Feedwater Nozzle Insps Performed in Response to USI A-10 Re BWR Nozzle Cracking ML20210U1831999-08-12012 August 1999 Revises 980202 Commitment Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design- Basis Accident Conditions ML18107A7051999-07-20020 July 1999 Provides Suppl Info Which Supersedes Info in 990625 Ltr in Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML20212H3191999-07-16016 July 1999 Forwards Aug 1999 Monticello RO Exam Package,Including Revised Outlines.All Changes Are in Blue Font ML20209B6151999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Y2K Readiness Disclosure Attached ML20196H2291999-06-24024 June 1999 Responds to Administrative Ltr 99-02,dtd 990603,requesting Licensee to Provide Estimate of Licensing Action Submittals Anticipated.Four New Submittals Per Year Are Anticipated ML20207D5851999-05-25025 May 1999 Submits Info Re Partial Fulfillment of License Conditions Placed on Amend 101,which Approved Use of Ten Exceptions for 24 Months Subject to Listed App C Conditions.Util Will Submit Second Rept to Obtain Approval for Continued Use ML20206S0911999-05-17017 May 1999 Forwards Response to NRC 990324 RAI Re Proposed Amend to pressure-temp Limits & Surveillance Capsule Withdrawal Schedule, .Supporting Calculations Also Encl ML20206D1651999-04-27027 April 1999 Forwards Radiation Environ Monitoring Program for MNGP for Jan-Dec 1998, Per Plant TS 6.7.C.1.Ltr Contains No New NRC Commitments or Modifies Any Prior Commitments ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20207F4091999-02-28028 February 1999 Forwards Fitness for Duty Program Performance Data for Six Month Period from 980701-981231,IAW 10CFR26.71 ML20207F6741999-02-24024 February 1999 Forwards Summary of Nuclear Property Insurance Maintained at Monticello & Prairie Island Nuclear Generating Plants ML20207F6901999-02-23023 February 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 980701-981231, Off-Site Radiation Dose Assessment for 980101-981231 & Revised Effluent & Waste Disposal Semi- Annual Rept for 980101-980630, for Monticello ML20203A3081999-01-28028 January 1999 Forwards TS Page 60d,as Supplement 3 to 971125 LAR Re CST Low Level Hpci/Rcic Suction Transfer.Page Includes NRC Approved Amend 103 Changes for Use by NRC in Issuing SER ML20202F7821999-01-27027 January 1999 Forwards 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility, Per 10CFR55.45(b)(5)(ii) & 10CFR55.45(b)(5)(vi).Ltr Contains No New Commitments or Modifies Any Prior Commitments ML20206S0331999-01-20020 January 1999 Submits Annual Rept of Safety & Relief Valves Failure & Challenges ML20206P1221998-12-31031 December 1998 Forwards LAR for License DPR-22,revising TS pressure-temp Curves Contained in Figures 3.6.1,3.6.2,3.6.3 & 3.6.4, Deleting Completed RPV Sample SRs & Requirement to Withdraw Specimen at Next Refueling Outage & Removing Redundant SR ML20198M3271998-12-28028 December 1998 Submits Change to Commitment for Submittal of ITS Application.Util Plans to Provide ITS Conversion Package Submittal to NRC in Dec of 2000 ML20198J7511998-12-22022 December 1998 Informs of Completion of Listed Commitment Made in Re Severe Accident Mgt. Severe Accident Mgt Guidelines Have Been Assessed,Plant Procedures Have Been Modified & Training of Affected Plant Staff Has Been Completed ML20198J4311998-12-21021 December 1998 Forwards Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv. Under Separate Cover,Licensee Is Providing LAR to Revise Curves ML20198J7711998-12-14014 December 1998 Documents 981214 Discussion with NRC Staff Re Deviation from Emergency Procedure Guidelines ML20195C9631998-11-11011 November 1998 Forwards 120-day Response to NRC GL 98-04, Potential for Degradation of ECCS & CSS After LOCA Because of Construction & Protective Coating Deficiencies & Foreign Matl in Containment ML20195C8781998-11-11011 November 1998 Forwards Supplement to 971125 License Amend Request Re Condensate Storage Tank Low Level Suction Transfer Setpoints for HPCI Sys & Reactor Core Isolation Cooling Sys ML20195E2261998-11-10010 November 1998 Submits Suppl 1 to Util Response to NRC Request for Addl Info Re 981118 Request for Deviation from Emergency Procedure Guidelines ML20155H6591998-11-0404 November 1998 Forwards Response to 980910 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20155F9091998-10-27027 October 1998 Forwards Master Table of Contents to Rev 16 of Usar.Info Was Inadvertantly Omitted at Time of 981023 Submittal ML20155A2661998-10-23023 October 1998 Forwards Rev 16 to USAR for Monticello Nuclear Generating Plant. Summary of Changes,Tests & Experiments Made Under Provisions of 10CFR50.59(b)(2) Also Encl.Rev Updates Info in USAR for Period Up to 980801 05000263/LER-1998-005, Forwards LER 98-005-00,re HPCI Being Removed from Service to Repair Steam Leak in Drain Trap Bypass.Commitments Made by Util Are Listed1998-10-21021 October 1998 Forwards LER 98-005-00,re HPCI Being Removed from Service to Repair Steam Leak in Drain Trap Bypass.Commitments Made by Util Are Listed ML20154L9321998-10-12012 October 1998 Forwards Suppl 2 to LAR & Suppl 980319,which Proposed Changes to Ts,App a of Operating License DPR-22 for Mngp.Number of Addl Typos & One Title Change on Pages Associated with Amend Request Have Been Identified 05000263/LER-1998-004, Forwards LER 98-004-00 Re Manual Scram Inserted Following Pressure Transient Closes Air Ejector Suction Isolation Valves & Trips Offgas Recombiners.Ler Contains Listed Commitment1998-10-0909 October 1998 Forwards LER 98-004-00 Re Manual Scram Inserted Following Pressure Transient Closes Air Ejector Suction Isolation Valves & Trips Offgas Recombiners.Ler Contains Listed Commitment ML20154L8671998-10-0909 October 1998 Forwards Suppl 1 to LAR for License DPR-22, Replacing Exhibits B & C of Original Submittal to Reflect Item 2 & Subsequent Changes.Request for APRM Flow Converter Calibr Interval Extension,Withdrawn ML20154J6201998-10-0505 October 1998 Forwards Rev 49 to Monticello Security Plan.Encl Withheld, Per 10CFR73.21 ML20154D7921998-10-0101 October 1998 Forwards Response to NRC RAI Re Licensee 971118 Request for Deviation from Emergency Procedures Guidelines.Proprietary Flow Charts,Including Rev 5 to C.5-110 RPV Control & Rev 6 to C.5-110 RPV Control, Encl.Proprietary Info Withheld ML20154D8031998-09-25025 September 1998 Submits Annual Rept of Any Change or Error Identified in ECCS Analytical Models or Application ML20153F0051998-09-25025 September 1998 Forwards Suppl 1 to 971031 Application for Amend to License DPR-22,replacing Exhibit C Which Contains TS Pages Incorporating Proposed Changes Described in Original 971031 Request ML20153F5351998-09-25025 September 1998 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Improved TS ML20153E0331998-09-17017 September 1998 Forwards Response to NRC 980629 RAI Re RPV Weld Chemistry Values Previously Submitted as Part of Plant Licensing Basis.Next Monticello RPV Sample Capsule Scheduled to Be Removed During 1999/2000 Refueling Outage ML20153D1441998-09-17017 September 1998 Informs NRC That Listed Commitments 1 & 3 Were Completed by End of 1998 Refueling Outage.Commitments Involved Final Disposition of Remaining Outlier Components Re All Known Outstanding Work Associated with GL 87-02,Suppl 1,USI A-46 ML20153D8561998-09-17017 September 1998 Forwards Rev 17 to EPIP A.2-414, Large Vol Liquid Sample &/ or Dissolved Gas Sample Obtained at Post Accident Sampling Sys. Superseded Procedures Should Be Destroyed.Ltr Contains No New NRC Commitments,Nor Does It Modify Prior Commitments ML20153E9011998-09-0909 September 1998 Forwards Rev 1 to MNGP Colr,Cycle 19, Incorporating Changes to power-flow Maps in Figures 6 & 7.Changes Made to Correct Errors in Stability Exclusion Region & Stability Buffer Region Shown on Rev 0 ML20151S7401998-08-28028 August 1998 Responds to NRC Re Violations Noted in Insp Rept 50-263/98-09.Corrective Actions:Procedure 4 AWI-04.04.03 Will Be Revised to Eliminate Term Urgent from Section 4.3.1.D 1999-09-09
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Northern states Power Company Monticello Nuclear Generating Plant 2807 West County Road 75 Monticello, MN 55362 October 1,1998 US Nuclear Regulatory Commission NUREG-0737 Attn: Document Control Desk Supplement 1 Washington, DC 20555 MONTICELLO NUCLEAR GENERATING PLAN Docket No. 50-263 License No. DPR-22 Proprietary Information Related to NSP Response to NRC Request for Additional Information Regarding November 18,1997 Request for Deviation from Emergency Procedure Guidelines Ref.
Letter from Michael F. Hammer, NSP, to USNRC Document Control Desk,
" Request for Deviation From Emergency Procedure Guidelines, Revision 4, NEDO-31331, March 1987," November 18,1997.
By letter dated November 18,1997 (Reference 1) NSP requested a deviation from the Boiling Water Reactor (BWR) Owners' Group Emergency Procedures Guidelines (EPGs), Revision 4, NEDO-31331, March 1987. The deviation was requested to recognize 2/3 core height as adequate core cooling following a large break loss of coolant accident.
The NRC Staff subsequently asked five specific questions which were discussed between NSP and NRC representatives in a conference call on September 28,1998.
At the conclusion of that discussion the Staff requested that responses be submitted in writing. These questions and answers are being provided as requested in the attachments to this letter.
Northem States Power Company (NSP), a Minnesota corporation, hereby requests that certain information (Attachments 3 and 4) hereby provided to the Nuclear Regulatory Commission (NRC), be withheld from public disclosure due to its proprietary nature.
The details of this request are provided in the attached affidavit.
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USNRC NORTHERN STATES POWER COMPANY October 1,1998 Page 2 l
This submittal contains no new NRC commitments, nor does it modify any prior commitments. Please contact Marcus H. Voth, Project Manager of Licensing, at 612-271-5116 if you require additional information related to this request.
N h44tM1/A)
Michael F. Hammer Plant Manager Monticello Nuclear Generating Plant c: Regional Administrator-111, NRC i
NRR Project Manager, NRC Sr. Resident Inspector, NRC State of Minnesota, Attn: Kris Sanda J Silberg Attachments:
- 1. NSP Response to NRC Request for Additional Information Regarding November 18, 1997 Request for Deviation from Emergency Procedure Guidelines
- 2. Affidavit of Michael F. Hammer, Northern States Power
- 3. Monticello Flowchart,"C.5-1100 RPV Control," Revision 5
- 4. Monticello Flowchart, "C.5-1100 RPV Control," Revision 6 1
I 3
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l UNITED STATES NUCLEAR REGULATORY COMMISSION NORTHERN STATES POWER COMPANY MONTICELLO NUCLEAR GENERATING PLANT DOCKET NO. 50-263 Request to Withhold Proprietary Information from Public Disclosure AFFIDAVIT I, Michael F. Hammer, being duly sworn, depose and state as follows:
(1)
I am Plant Manager, Monticello Nuclear Generating Plant, Northern States Power Company
("NSP") and have been delegated the function of reviewing the information described in paragraph (2) which is sought to be withheld, and have been authorized to apply for its withholding.
(2)
The information sought to be withheld consists of Monticello Nuclear Generating Plant, Emergency Operating Procedure (EOP) Flow Charts, "C.5-1100 RPV Control," Revision 5, and "C.5-1100 RPV Control," Revision 6. This information describes key technical details of NSP's plans for responding to beyond design basis events. The proprietary information is identified by the words "NSP PROPRIETARY INFORMATION" on each page.
(3)
The information sought to be withheld is being submitted to the NRC in confidence. The original EOP flow charts were BWR Owners Group proprietary. The attached revisions are NSP proprietary. This information is of a sort customarily held in confidence by NSP, and is in fact so held. The information sought to be withheld has, to the best of my knowledge and belief, consistently been held in confidence by NSP, no public disclosure has been made, and it is not available in public sources. All disclosures to third parties including any required transmittals to NRC, have been made, or must be made, pursuant to regulatory provisions or proprietary agreements which provide for maintenance of the information in confidence.
(4)
Public disclosure of the information sought to be withheld is likely to cause harm to NSP's competitive position and reduce the availablity of profit-making opportunities. The research,
{
development, engineering, and analytical costs comprise a substantial investment of time and money by NSP. The value of this information to NSP would be lost if the information were disclosed to the public. Making such information available to competitors without their having i
been required to undertake a similar expenditure of resources would unfairly provide competitors I
with a windfall, and deprive NSP of the opportunity to exercise its competitive advantage to seek an adequate return on its investment in developing this information.
This letter contains no restricted or other defene,e information.
b dA44/144/4>
By Michael F. Hammer Plant Manager l
Monticello Nuclear Generating Plant On this k day of OcT8b e C, M8 before n'e a notary public in and for said County, personally appeared Michael F Hammer, Plant Manager, Monticallo Nuclear Generating Plant, and being first duly sworn acknowledged that he is authorized to execute this document on behalf of Northem States Power Company, that he knows the contents thereof, and that to the best of his knowledge, information, and belief the statements made in it are true and that it is not interposed for delay.
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SAMUEL l. SHIREY l
Notary Public - Minnesota NOW
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My Commission Expires January 31,2000
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NSP Response to NRC Request for AdditionalInformation Regarding November 18,1997 Request for Deviation from Emergency Procedure Guidelines 1.
Explain why the MSCR WL (calctdated in accordance with the B WROG methodologyfor EPG Rev 4) is greater than 2B core height, given that NEDO-20566A (Section lH.A.5) shows thepeak clad temperature to be well below 1500Ffor the most limiting break.
l NEDO-20566A (Reference 1)is the basis for the detailed SAFER evaluation of the design basis loss of coolant accident (DBA-LOCA). The Boiling Water Reactor Owners' l
Group (BWROG) methodology is a simplified calculation, independent of plant-specific systems or characteristics. As such, the BWROG methodology is very conservative.
General Electric states that the BWROG methodology is based on a simplified, steady state calculation using a single rod model. The BWROG methodology also uses a very conservative axial power shape that has an axial power peak of 2.0 in node 19 of 24 (node 1 is the bottom of the core). A sensitivity study performed by GE determined the axial power shape is the dominant factor in determining the elevation of the minimum
]
steam cooling RPV water level (MSCRWL). Furthermore, the BWROG methodology assumes steam cooling is the only mechanism for bundle cooling above the MSCRWL.
j References 4 and 5 state the MSCRWL is calculated assuming the reactor has been shutdown from rated power for ten minutes. The assumptions used to calculate the MSCRWL approximate the conditions experienced by the hottest pin in the hottest bundle when the reactor has been reflooded (including level swell) to only the j
MSCRWL. Using these conservative conditions, peak clad temperatures on the order of 1500 *F are calculated.
In contrast, the clad temperatures reported in Reference 1 are calculated using a single channel, time domain computer model assuming an axial peak of 1.4 near the core mid-plane (as is typical for licensing bases calculations). Figure 6 of Reference 1 shows the l
peak cladding temperature as a function of time following the design basis accident.
l The initial temperature transient is terminated when the core is flooded by the accumulation of emergency core cooling system (ECCS) water and decay heat causes l
the two phase water boundary to swell above the top of the fuel. As bundle decay heat decreases, level swell in that bundle also decreases. A bundle will remain covered as long as the energy stored in that bundle can produce sufficient level swell. When the bundle finally does uncover, the uncovered portion is cooled by the steam generated in l
the covered portion of the bundle. This results in an increase in the peak cladding l
temperature. This can occur as early as 10 minutes for the lowest power bundles, but will take several hours for the highest power bundles. Thus the decay heat in the hottest bundle when the upper portion of the bundle is cooled only by steam cooling is significantly less in Reference 1 (two hours) than in the BWROG methodology (ten l
minutes).
For the reasons given above, the peak clad temperatures calculated in Reference 1 are less than those calculated using the BWROG methodology, even though the MSCRWL used in the BWROG methodology is higher than the 2/3 core height used in the Reference 1 calculation.
1 i
l l
2.
' Discuss thc consequences ofmaintaining reactor level at 2B core height without core sprayfor an ex,tendedperiod (e.g., while waitingfor the TSC to derclop recommendations regarding containmentflooding). Provide an estimate ofthepeak cladding temperature and the extent of cladding oxidation under best estimate assumptions.
Figure 5 of Reference 1 shows the maximum c! adding temperature as a function of time using low pressure coolant injection (LPCI) only. This figure shows the peak cladding temperature for long term cooling to be on the order of 950*F. Figure 7 of Reference 1 shows the peak cladding temperature response to a loss of coolant accident with a break area that is in the limiting spectrum of breaks. This figure shows the long-term peak cladding temperature decays below 900 *F within hours of bundle uncovery.
Assuming the cladding temperature in the upper three feet of the fuel remained at 900*F l
for 11 days, and that all rods are at the same temperature as the hottest rod, the l
amount of metal-water reaction in the total active cladding in the core is calculated to be 0.09% in Reference 1.
4 3.
The B WROG decided toflood at TAF (or MSCR WL)for several reasons identified in the Monticello submittal dated November 18,1997 (page 5). Explain why reasons #2 and #3 do not apply to Monticello.
Reason #2 Flooding ofcontainment and the reactor vessel to above TAFplaces the reactor into a stable conditionfor long-term cooling. Reliance on pumps and other active equipment to maintain this l
condition is minimi:cd. Conditions are stable and required operator action times are long.
J Reason #3 l
Following a LOCA, level will be quickly restored above TAF, and the core will remain covered for long term cooling exceptfor the largest breaks in the recirculation piping. A break ofthis si:e will require containment to beflooded anywayfor accident recovery.
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Reason #2 is concemed with potential additional failures beyond the design basis of the l
plant and implies early containment flooding is the best method to minimize these l
hypothetical failures. Requiring containment flooding early in a DBA-LOCA to minimize the consequences of potential additional equipment failure may not provide the best I
total plant response. For example, requiring containment flooding per the EPG Rev. 4 instructions will require primary containment venting to maintain pressure below the containment design pressure. Venting, however, is not expected to occur until after the hard pipe vent is submerged. Venting would have to be through the standby gas treatment (SBGT) system. At the containment pressures at which venting would occur, damage to the SBGT suction ductwork would probably occur. This could impact the ability of the plant to utilize a filtered, elevated release pathway. The Monticello l
containment pressure response to the DBA-LOCA (Reference 3, Figure 5.2-15) shows the pressure would be less than 5 psig within 6 days. Deferring containment flooding, l
and thus deferring the need to vent, greatly reduces the potential for damage to the SBGT ductwork.
As stated on page 6 of the Monticello submittal (Reference 2), Monticello would flood 2
primary containment if 2/3 core height could not be restored and reliably maintained. If i
fewer than two ECCS pumps were available for RPV injection (the minimum number expected to be available following the DBA-LOCA), Monticello would flood primary containment if RPV water level could not be restored and maintained above the minimum steam cooling RPV water level.
Reason #3 states that Monticello would need to flood primary containment to recover from a DBA-LOCA. Containment flooding performed during the recovery phase of the DBA-LOCA would be a more controlled evolution than flooding initiated as soon as RPV water level could not be restored and maintained above TAF (or MSCRWL).
4.
Explain the specille benefits oftheproposed approach (waiting toflood until directed by the TSC) relative to the BlVROG approach oftaking these actions inunediately. Does theproposed approach reduce the irnpact on public health andsafety when compared to the BIVROG approach? IVould safety be adversely impacted ifthe BlVROG approach is retained?
As stated in the Monticello submittal (Reference 2, Page 5), adhering to the EPG Revision 4 (and EPG/ SAG) approach of immediately flooding primary containment creates the following conflicts with the licensing basis plant response described in the Monticello Updated Safety Analysis Report (USAR)(Reference 3):
RHR and RHR service water pumps would not be aligned for long-term suppression pool cooling.
USAR environmental qualification, shielding, and radiological analyses may no longer be applicable because conditions are different than those originally assumed.
RPV venting to the condenser (and ultimately to the environment) is required to flood the reactor vessel. This creates a vent path not pieviously considered in the USAR radiological analysis.
In addition, flooding early in the accident may result in damage to the SBGT system if it l
used for containment venting. This could result in additional vent paths not previously considered in the USAR radiological analysis and may render vital areas of the plant I
inaccessible.
l The proposed approach is preferred over the BWROG approach since it would enable l
'he Monticello plant to respond to a DBA-LOCA event while remaining within the design basis capabilities of the plant as described in USAR. The proposed approach would also minimize the potential for damage to systems that could be used to recover from the event by deferring venting until primary containment pressure is reduced.
5.
Explain how the transitionfrom the EOPs to the severe accident guidelines wordd occur if the proposed approach is adopted, since the operators would stay in the EOPs and notflood containment until additionalfailures resulting in levelfalling below 2B core height. Describe l
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l the expectedprogression ofeventsfollowing loss ofinjection (e.g., timing ofcore heatup, core relocation, and vesselfailure) ifactions toflood containment are not initiated until levelfalls below 2B core height.
1 Monticello ECCS systems are designed to restore and maintain reactor pressure vessel (RPV) water level at 2/3 core height following a DBA-LOCA. No analysis has been performed to determine the timing of core heatup, core damage, or vessel failure if RPV water level falls below 2/3 core height since this would require additional failures beyond the design basis of the plant.
As stated in the response to question 3 above, if fewer than two ECCS pumps are l
available, Monticello would flood primary containment if RPV water level could not be restored and maintained above the minimum steam cooling RPV water level. When primary containment flooding is initiated the severe accident management guidelines would be entered and decision making responsibility would be transferred to personnel in the Technical Support Center (TSC). The two ECCS pump criteria was chosen because this is the minimum number of ECCS pumps expected to be available for RPV injection following a DBA-LOCA.
If only one ECCS pump were available for injection into the RPV following a DBA-LOCA event, the plant would be in a condition that is beyond the design basis of the facility.
Transferring to the severe accident management guidelines under these conditions is the prudent action to be taken, and would occur once the TSC is staffed and i
operational.
l The EPG guidance for RPV level control and alternate RPV level control is provided to the Monticello Operators in flowchart C.5-1100. Revision 5 of this flowchart shows this guidance prior to implementing 2/3 core height as adequate core cooling. Revision 6 (in draft form) shows the proposed changes to implement 2/3 core height as adequate core cooling. Copies of these flowcharts are provided to show how Monticello tvould transition from the EOPs to the Severe Accident Management Guidelines if the l
proposed approach is adopted.
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REFERENCES-l i
1.
NEDO-20566A, General Electric Company Analytical Model for Loss-of-Coolant i
Analysis in Accordance with 10CFR50 Appendix K, Volume 11, Section Ill 2.
Letter form NSP to NRC, " Request for Deviation from Emergency Procedure l
Guidelines, Revision 4, NEDO-31331, March 1987," November 18,1997.
3.
Monticello Updated Safety Analysis Report.
4.
EPG Revision 4 Appendix C Calculations Workshop Notebook, May 1993.
5.
BWROG Emergency Procedure and Severe Accident Guidelines, Revision 1, Appendix C, July 1997.
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