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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
Text
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DUKEPOWER January 12, 1990-Document Control Desk U. S.-Nuc1 car Regulatory Commission, Washington, D. C. 20555
Subject:
Catawba Nuclear Station-Docket ~No. 50-413 LER 413/89-29 Gentlemen:
. Attached'is Licensee Event-Report 413/89-29. submitted as a Courtesy.? ,
Report'concerning POTENTIAL INOPERABILITY OF COMPONENT COOLING-ISOLATION VALVES DUE-TO AGE-HARDENED ELASTOMERIC SEAT MATERIAL.z This event was. considered to be of no significance with respect to the-health and safety of'the public.
cry trul yours,
'ITony B. Owen Station Manager keb: COURTESY LER xc: Mr. S. D. Ebneter American Nuclear Insurers _ ,
Regional Administrator, Region II c/o Dottie'Sherman, ANI. Library i U. S. Nuclear Regulator Commission The Exchange,: Suite 245 101 Marietta Street, NW, Suite 2900 270 Farmington Avenue Atlanta, GA 30323 Farmington, CT 06032 M & M Nuclear Consultants Mr. K; Jabbour 1221 Avenues of the Americas U. S. Nuclear Regulatory. Commission' How York, NY 10020 6ffice of Nuclear Reactor-Regulation-Washington, D. C. 20555 INPO Records Center Suite 1500 Mr. W. T. Orders 1100 Circle 75 Parkway NRC Resident Inspector' R Atlanta, GA 303.39 Catawba Nuclear Station j j
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... LICENSEE EVENT REPORT (LER) l . ACiuTv AME m ooCxET NousER m Paar a Catawba Nuclear Station, Unit 1 01510l0l0l41113 1 lOFl Ol 7 n T ' Potential Inoperability of Component Cooling-Isolation Valves 7 Due To Age-Hardened Elastomeric Seat Material EVENT DATE Ili LER NUMeER (s) REPORT OATE 171 OTHER F ACILITIES INVOLVID (8)
MONTH DAY YEAR YEAR stov as as isp MONTM DAY YEAR F ACILITv mavts DOCKE T NuvetR!$1 CNS, Unit 2 0 15101ol0l411 14
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ARIA;OQt R.M. Glover, Compliance Manager 81013 81311 l- l 3121316 COMPLETE ONE LINE 70R E ACM COMPONENT F AILURE DESCRISED IN THIS REPORT t131 CAUSE SYSTEM COMPONENT MA A? A OmTA MA C. m " t g g qpq CAUSE SY ST E M COMPONENT 0 NPR B CI C VI I i B 12 1 5 l 0 Y I i i i l I l I l i I I I I I I I I I I I SUPfLEMENTAL REPORT EXPECTED 114: MONTM DAY YEAR
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~} YEs ur ,.n.,.M ex ucruo svowssioN oara, 9 No , , 1 A.m A Cuo.4 ,. , . ..; . . . ,. ...,,, ,.,, .,,- . .,,.. ,,,,, n . , 4 On December 13, 1989, at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />, with Units 1 and 2 in Mode 1, Power ,
1 Operation, Compliance issued a Technical Specification Operability Notification identifying valves IKC-81B, KC to ND Hx 1B Supply Isolation, and 2KC-56A, KC to ND Hx 2A Supply Isolation, as inoperable. At that time, both Units 1 and 2 entered the Technical Specification Action Statement for one inoperable train of the Emergency Core Cooling System. A potential inoperability was' identified by Design Engineering after determining that the maximum actuator torque switch setting may not be sufficient to overcome the friction force that may exist due to age hardening of the elastomeric seat material. These KC System valves have never failed to open when called upon during performance tests, thus it was a conservative approach to determine them " inoperable" and make the necessary torque switch adjustments. The actuator's open torque switch was bypassed for I fifty percent of the valve stroke. The actuator is sufficiently rated to produce the required opening torque with the torque switch bypassed. Units 1 and 2 exited their action statements on December 14, 1989, at 0244 hours0.00282 days <br />0.0678 hours <br />4.034392e-4 weeks <br />9.2842e-5 months <br /> and 1 0325 hours0.00376 days <br />0.0903 hours <br />5.373677e-4 weeks <br />1.236625e-4 months <br />, respectively. This incident is classified as a manufacturer's ,
functional design deficiency due to an inadequate estimate of the degree of age '
hardening in the elastomeric seat material. This report is being submitted as a l Courtesy LER and is reportable pursuant to 10CFR21. I 1
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F BACKGROUND L
i The Residual Heat Removal [EIIS:BP] (ND) System functions as part of the. i y Emergency Core Cooling System (ECCS). The'ECCS1is actuated by a Safety j Injection. Signal with' the flow alignment changing over time after initiation, j The ND System can be used to deliver cooling water directly to the Reactor j
, Coolant [EIIS:AB] (NC) System provided that NC~ pressure has dropped bel.ow:the ND "
pump's discharge pressure. The ND System-can also provide water to the suction -
of other ECCS pumps capable of injecting into the NC. System at higher pressures.
Heat is removed from the ND System via two ND Heat Exchangers [EIIS:HX] (Hx). ,
The Component-Cooling [EIIS:CC) (KC) System essential header provides cooling water to the ND Hxs.
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The KC Supply Isolation Valves [EIIS:V] to the ND Mxs are.normally closed and: i opened on Low-Low Refueling Water Storage Tank (FWST) level in conjunction with '
a Safety Injection Signal or on a Hi-Hi Containment Pressure (Phase B) <
Containment Isolation Signal. The supply isolation valves- are 16 inch butterfly ,
valves, model number 0652, manufactured by BIF/ General Signal- Corporation (B250),.with Limitorque SMB-000 motor operators and H1BC gearboxes. Flow is controlled by a control valve on the discharge of the ND'Hx; Technical Specification 3.5.2 requires that two independent ECCS subsystems be operable in Mode 1, Power Operation, Mode 2, Startup, and Mode 3, Hot Standby.
~
An ECCS subsystem is comprised of one centrifugal charging pump, one safety-injection pump, one ND pump, one ND Hx, and a flow path capable of taking suction from the FWST on an actuation signal.and automatically transferring suction to the~ Containment sump on Low-Low FWST level ^. With one ECCS subsystem ;
inoperable, an operable status is to be restored within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, or cooldown to 1 at least Mode 3 within the next six hours, and to Mode 4, Hot Shutdown, within -i the following six hours.
EVENT DESCRIPTION On October 21, 1988, PIR 0-C88-0314 was issued on valves 1(2)RN-148A, NS Heat i Exchanger 1(2)A Outlet Isolation Valves, for failure-to open under high-differential pressure during alignment for the Nuclear Service Water [EIIS:BI]
(RN) System Train A flow balance. Design Engineering (DE) used the results from Design Study CNDS-0078 (initiated in April 1988, to evaluate-seat leakage problems of BIF valves) to conclude that age hardening of seat material to a ,
mean durometer measurement of 80 Shore A is being experienced at Catawba. The manufacturer's (BIF) original specification used a 65-70 Shore A measurement in their sizing calculations. DE recommended that the actuator's open torque switch be reset to the maximum allowable position for all BIF Butterfly valves that are required to open to satisfy their safety function. There were-56 '
valves involved in this recommendation which included both the KC System, RN-System, and various ventilation systems of Units 1 andL2. By July 26, 1989, all open torque switches had been adjusted and the as-left torque switch settings for each valve was sent to DE for a final-review. j 1
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.- EXPtMES: t/31/0B FACOTY 4Amt til DOCKET esuassen (2) LER NUMSER 16) Pact tal vsAa o @,', ' .> "*48,3 hp Catawba Nuclear Station, Unit 1 itXT (# mom spese 4 #ecurest see ashesons/ ##C 7ene JgMw (17) o l5 l0 l 0 l 0 l 4l 1l3 8l9 -
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An evaluation of the final torque switch settings was documented by DE in 3 Certification of Engineering Calculations CNC-1205.02-00-0006. This evaluation-1 found that three of the actuators still may not produce the opening torque 4 required for the maximum seat hardening condition. . Valve 1KC-81B, KC to ND Hx.
7 IB Supply Isolation, and 2KC-56A, KC to ND Hx 2A Supply Isolation. were H considered to be potentially inoperable due to age hardening of the elastomeric
? seat material. The seat had been replaced in valve 2KC-81B, KC to ND Hx 2B
@ Supply Isolation, in May 1989,'under repair Work Request 42714 0PS and
- significant age hardening of the seat material is not expected to have occurred l within this time. Therefore, 2KC-81B was considered to be conditionally operable. The actuator on valve 1KC-56A,'KC to ND Hx 1A supply Isolation, has a j greater output torque for its maximum torque switch setting and would not be
. restricted from opening by the age hardened seat condition. On December 13, ;
1989, DE issued PIR 0-C89-0376 with recommendations to install a torque switch i
^
bypass in the open direction on all three valves. The bypass will allow-full i
- motor stall capability during unseating which will be sufficient 10 open the- !
- valves in the hardened seat condition. Valves IKC-81B and 2KC-56A required that ,
7 the bypass be installed to eliminate operability concerns. Valve 2KC-81B would !
require the. bypass to be installed prior to the end of the Unit 2 E003 refueling. l outage to maintain its operability. )
On December 13, 1989, at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />, with Units 1 and 2 in Mode 1, Compliance L issued a Technical Specification Operability Notification identifying valves I L 1KC-81B and 2KC-56A as inoperable taking the most conservative approach for L
plant status. At that time, both Unit 1 and 2 entered the Technical' !
Specification Action Statement for one inoperable train of ECCS due to a
? potentially inoperable ND Hx. Variation Notice CE-2698 (Work Request 3436 NSM)
- r. and Variation Notice CE-2699 (Work Request 3437 NSM) were issued for valves j l 1KC-81B and 2KC-56A, respectively, to install the torque switch bypass. The ,
l bypasses were installed, a functional stroke-test was-performed, and Units 1 and ;
2 exited their action statements on December 14, 1989, at 0244 hours0.00282 days <br />0.0678 hours <br />4.034392e-4 weeks <br />9.2842e-5 months <br /> and 0325 i hours, respectively.
CONCLUSION ;
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This event has been classified as a manufacturer's functional design deficiency !
due to an inadequate estimate of the degree of age hardening in the elastomeric seat material. The elastomeric seat material used in BIF butterfly valves is !
subject to age-induced hardening. This tends to increase the friction force to i be overcome in unseating the valve. The increased friction was not properly '
accounted for in the manufacturer's actuator sizing calculations. ,
Review of the performance history for valve 1KC-81B revealed no occurrences (since startup) of failure to open due to mechanical binding. The performance history for valve 2KC-56A indicated that a bad wire in the motor control center resulted in a failure to open in Decmeber 1985, and that a limit switch repair was required after a stroke time test failure in October 1988. These repairs were performed under Work Request 4518 PRF and 6620 PRF, respectively. ,
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! The stroke response time for valves 1KC-818 and 2KC-56A have been trended since
$ 1987 within the ASME Section XI Valve Performance Testing Program. Both va1ves j have consistently met the 60 second response time requirement with most responses within 56-57 seconds. The trend gives no indication that the valves response time has increased with age. However. review of this data with Design Engineering concluded that thir , formation was not conclusive for determining the valves operability in rela m t to the age-hardened seat condition.
For a butterfly valve, an age-hardened seat condition would have the greatest affect on disc movement during the first few degrees of disc rotation. After the first few degrees, the age-hardened seat would have little to no affect on disc movement. A butterfly valve's performance would continue as expected _until l- the point where an age-hardened seat condition would restrict disc movement-
- completely. At best, there may be only a slight increase in the response trend E over time.
From the performance history and the response time trend, it can be concluded that valve 1KC-81B and 2KC-56A were in good working condition prior to their operability determination on December 13, 1989, and that there is a high probability that the valves would have opened in response to a safety signal.
This conclusion is supported by the performance history in that no failures of o i the valves have occurred due to binding, and by the resp.nse' time trend in that a total of 10 and 11 response tests (1KC-81B and 2KC-56A, respectively) have been performed since 1987 without a failure related to seat binding. The +
issuance of the inoperability notification was a conservative approach in identifying and correcting a potentially inoperable component, albeit one proven i to be reliable by cast performance and testing.
A review of the Nuclear Maintenance Database for the past 24 months identified five BIF butterfly valves that have failed to open on-demand. Of these, only valves 1 and 2 RN-148A previously identified by PIR 0-C88-0314' failed to open due to seat binding within the seat material. A review of the NPRDS Database -
did not reveal any failures to open of BIF butterfly valves due to disc binding within the elastomeric seat material. The Operating Experience Program Database does not identify any similar occurrences within the past 24 months.
This incident is similar to other events, at Duke Power and other plants, involving valve operability under maximum design consideration conditions. This concern is the subject of NRC IE Bulletin 85-03 and Generic Letter 89-10.
Catawba Nuclear Station has established a comprehensive, on going program to ensure valves will function properly under all anticipated conditions. The thoroughness with which valve operability concerns are addressed, including DE's review of the as-left torque switch settings, contributed to the identification and prompt resolution of the current event.
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A'similar event occurred on March 14, 1988, when valve 2CA-62A, CA Pump 2A 1 Discharge to S/G 2A Isolation Valve, failed to close under high pressure drop
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conditions uni.il the valve actuator was adjusted to the maximum torque switch setting allowable. This failure was contributed to a valve factor greater than that used by the valve manufacturer in sizing the valve actuator. .The failure b of valves'to respond due to inappropriate actuator sizing by the manufacturer is L. determined to be a recurring event.
1:
b This event is considered to be 10CFR21 reportable. These valve failures are L
reportable to NPRDS. These valves are 16 inch butterfly valves manufactured by BIF/ General Signal Corporation (B250), model number 0652.
CORRECTIVE ACTION SUBSEQUENT
+
- 1) Design Engineering issued PIR 0-C89-0376 identifying the effect of age-induced hardening of the seat material on the operability of o valves 1KC-81B, 2KC-56A, and 2KC-818.
- 2) Design Engineering issued an operability notification identifying-valves 1KC-81B and 2KC-56A as inoperable.
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- 3) 10CFR 50.59 Evaluation for PIR 0-C89-0376 identified 2KC-81B as conditionally operable through the end of the Unit 2 E003 refueling outage.
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- l. 4) Valves 1KC-81B and 2KC-56A were modified with an open torque switch I' bypass under Variation Notice CE-2698 (3436 NSM) and CE-2699 (3437.
NSM),respectively.
! PLANNED
- 1) Valve 2KC-81B will be modified with an open torque switch bypass.
SAFETY ANALYSIS Two independent ECCS subsystems ensure that sufficient emergency core cooling f capability will be available assuming the loss of one subsystem through any l single failure consideration. Either subsystem operating in conjunction with l the accumulators is capable of supplying sufficient core cooling to limit the i peak cladding temperature within acceptable limits in the event of a design
!. basis loss of coolant accident (LOCA). In addition, each ECCS subsystem l- provides long term core cooling capability in the recirculation mode during the accident recovery period.
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EXPIRES: 8/31/W FACIMfYNAMf H) DOCKET NUISER 12) LER NUIASER (6) PAGE131 k vaan -
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L,[ The initial response of the ECCS to a LOCA is to provide makeup water to the NC
% System. Makeup water is provided from the FWST to the NC System via the
? charging pumps, safety injection pumps, and the ND pumps. The actual flow path p changes over time and is dependent on NC System pressure. The ND makeup flow i would not be restricted by the KC to ND Hx supply. isolation valve's failure to open. Heat removal by the ND Hxs is not required during the initial response of the ECCS to a Safety Injection Signal. Therefore, the initial response of the p ECCS to a LOCA was not impaired.
1 After the FWST is depleted, the ECCS recirculates c wling water from the
? Containment Sumps to the NC System. During recirculation, the ND Hxs and the KC System provide a heat sink for removal of decay heat from the NC System makeup.
- . The opposite train of ND would have been capable of providing adequate decay heat removal if valve 1KC-81B or 2KC-56A failed to open to supply KC flow to i
their associated ND Hx.
i Control Room Operators have multiple indications of the status of the KC valves u and KC flow through the ND Hxs. Open/ Closed position of 1KC-81B and 2KC-56A is
+ indicated on-the main control board. The Engineered. Safeguards (ESF) Monitor
[! Panels 1(2) MD-4 in the Control Room include indication of the position of. these L. valves ard serve to quickly indicate abnormal alignment of equipment receiving h an ESF signal. Also, an annunciator, "ND 'Hx A(B) KC Outlet Low Flow" actuates L. if low flow exists and the respective ND pump is running. The second step of EP/1(2)/A/5000/1C3, " Transfer to Cold Leg Recirculation", directs the Operators -
to " Ensure KC flow to at least one ND heat exchanger". Operator action to'open L either 1KC-81B or 2KC-56A, if needed, could be taken locally at the valves which i are located on elevation 577 feet in the Auxiliary Building just outside the '
rooms containing the ND Hxs (as is 2KC-81B; IKC-56A.is located just inside the entrance of the Unit 1 Mechanical Penetration Room on elevation 577 feet.) It i is estimated that an Operator could locally open these valves, if needed, within 15 minutes after they were recognized as closed.
During extended operation in recirculation, the ND System has.the capability of supplying residual spray for Containment cooling to support Containment spray.
The NS System consists of two separate, equal capacity trains with each train capable of limiting Containment pressure below design restrictions during a LOCA. The ND System residual spray headers are provided to supplement NS System cooling; credit is taken for ND System spray AFTER ice bed depletion IF one train of NS spray is unavailable. Failure.of a KC to ND Hx Supply Isolation valve to open would have prevented the associated ND train from supplying cooled residual spray. One ND train has the capacity to provide sufficient residual spray as well as adequate core cooling flow via one centrifugal charging and one safety injection pump (ND injection into the NC System is manually isolated prior to swapping ND train to residual spray).
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i These valves, had consistently passed their stroke time test with no indication of an adverse trend resulting from the age-hardening process. However, c
calculations indicated that the potential' existed for age-hardening to affect l: the valves ability to open under the maximum differential pressure condtion. ,
f; Therefore, the valve was adjusted for maximum torque to further assure l l: operability. It is concluded that the health and safety of'the public were not )
l:- adversely affected.
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'U.S. GPCs 1998-120-569 u0071) g