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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
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J DUKEPOWER April 30, 1990 l Document Control Desk U. S. Nuc1 car Regulatory Consnission [
Washington, D. C. 20555 ,
Subject:
Catawba Nuclear Station Docket No. 50-413 LER 414/90-06 Gentlement i f
Attached is Licensec Event Report 414/90-06 concerning TECHNICAL SPECIFICATION VIOLATION DUE TO LOSS OF ASSURED MAKEUP TO CONTAINMENT VALVE INJECTION WATER SYSTEM DUE A DEFECTIVE PROCEDURE. ,
Thin event was considered to be of no significance with respect to the hculth and safety of the public.
Very truly yours, ;
7 a o -/7e To B. Owen .
Station Manager kob\LER-NRC.TBO xc: Mr. S. D. Ebnoter American Nuclear Insurers Regional Administrator, Rogion 11 c/o Dottio Sherman, ANI Library U. S. Nuclear Regulato? Commission Tho Exchange, Suito 245 101 Marietta Stroot,. N4, Suite 2900 270 Farinington Avenue Atlanta, GA 30323 Farmington, cT 06032 i
M f. M Nuclent Consultants Mr. K. Jabbour 1221 Avenucc of the Americas U. S. Nuclear Regubtory iCommission New York, NY 10020 Office of Nuclear Reactor Regulation Washington, D. C. 20555 INPO Records Conteir Suite 1500 Mr. W. T. Orders 1300 Circle 75 P.urkway NRC Resident Inspector Atlarita, GA 303T3 Catawba Nuclear Station 9005080369 900503 ~
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On March 21, 1990, at approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, with Unit 2 in Mode 1, Power Operation, it was discovered while performing PT/2/A/4200/62, RN to NW Piping Flush, that the Nuclear Service Water (RN) System assured makeup source to the Containment Valve Injection Water (NW) System Surge Chamber 2A would not provide adequate flow. Previous test results indicate this condition occurred between the June 26, 1989 and September 23, 1989 tests. Subsequent investigation revealed that RN to NW piping was clogged with sediment thereby reducing flow.
System piping and components have been cleaned, tested and returned to service.
) This incident is attributed to a Defective Procedure due to inadequate acceptance criteria. Acceptance criteria established for minimum flow will be incorporated into Unit 1 and 2 test procedures, and testi ig frequency will be increased. In addition, an evaluation will be performed on similar tests to determine the need for acceptance criteria or trending programs.
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0l0 0l 2 or 0 l7 BACKGROUND The Containment Valve [EIIS:V] Injection Water [EIIS:JM] (NW) System is designed to inject water between the two seating surfaces of selected gate valves used for Containment Isolation. The injection pressure is higher than Containment design peak pressure during a Loss of Coolant Accident (LOCA). This will provent leakage of the Containment atmosphere through the gate valves, thereby reducing potential offsite dose following a postulated accident.
The NW System consists of two independent, redundant trains; one supplying A train valves and the other supplying 8 train valves. This separation of trains peuvents the possibility of Containment isolation valves not sealing due to a single failure. Each train contains a surge chamber which is filled with water and pressurized with nitrogen. Makeup water is provided from the Demineralized Water [EIIS KJ) (YM) Storage Tank for testing and adding water to the surge chambers during normal plant operation. Assured makeup is prcvided from the essential header of the Nuclear Service Water [EIIS:BI] (RN) System. An automatic swap to RN occurs after an ST (Containment Isolation) Signal when the aurge chamber water level drops below the low-low level setpoint or when nitrogen pressure drops below the low-low pressure setpoint. )
F The RN System serves as the ultimate heat sfnk for heat loads in the Auxiliary
[EIIS:NF] and Reactor [EIIS:NH] Buildings other than the secondary (steam) side of the station. The RN System also serves as the assured source of makeup water for several safety related systems, including NW. RN is a raw water system which uses Lak6 Wylie or the Standby Nuclear Service Water Pond (SNSWP) as the supply.
Tecnnical Specification 3.6.6 states that both trains of the Containment Valve Injection Water System shall be OPERABLE in Mode 1, Power Operation, Mode 2, Startup, Mode 3, Hot Standby, and Mode 4, Hot Shutdown. With one train of NW inoperable, required action is to restore the inoperable system to OPERABLE status within 7 days or be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Periodic test PT/1,2/A/4200/62, RN to NW Piping Plush, is performed quarterly to remove clams from the RN to NW Surge Chambers supply line. This line contains normally closed valve 2NW8A (NW Surge Chamber 2A RN Supply Isolation) with vent valve 2NW118 (NW Surge Chamber 2A RN Supply Vent) downstream. The test method consists of isolating the surge chamber, opening 2NW8A and 2NW118, and establishing flow throtch the vent valve. The length of time needed to flush one gallon of water int:, a container is measured and recorded. The piping
[EIIS: PSP] is then flushed for 15 minutes before returning the system to its ;
original condition. This process is repeated for the resp e.lw B train components.
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[ EVENT DESCRIPTION On March 21, 1990, while Unit 2 was in Mode 1, power Operation, Periodic Test PT/2/A/4200/62, RN to NW Piping Flush, was performed. After completing the test, Operations noted, at approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, that A train flow was significantly less than B train flow. The time necessary to obtain one gallon of flow from A train was 103 seconds while the time for B train was only 6 seconds. Subsequent investigation by Operations revealed that the two previous tests indicated similar results (performed on September 23, 1989 and December j 21, 1989). Work requests had been initiated by operations after each test to I investigate and repair vent valve 2NW118 for flow blockage. Equipment history I records for 2NW118 and the Train B vent valve (2NW117) indicated to operations i that clogging and/or valve internals problems created low flow during prev bus tests. The work request written following the December 21, 1989 test was assigned a low priority and had not been worked as of March 21, 1990. The Operations Unit Managers group was contacted and agreed to have this work request completed the next week during other scheduled A Train work activities.
Due to equipment history records. vent valve 2NW118 was considered by operations as the source of flow blockage.
On P.a c h 23, 1990, Operations originated several work requests to break cu.nections in the RN to NW supply line to investigate for possible blockage.
On March 29, vent valve 2NW118 was removed from the system and cleaned. The valve was found to be clogged with mud and debris. Also on March 29, W RN to NW supply line was disconnected and cleaned at several locations. A w atantial amount of mud and debris was also found in this section of piping.
On March 30, operations initiated Problem Investigation Report (pIR) 2-C90-0110 due to the clogged RN to NW supply line.
On April 2, after reviewing test results, Design Engineering concluded that RN could not have supplied adequate makeup flow to the NW Traia A Surge Chamber at the indicated flow rate and that Unit 2 was probably in violation of T/S 3.6.6.
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l This condition was resolved by cleaning the RN to NW supply lines on March 29, 1990.
l CONCLUSION l
The Operations periodic Test Procedure, pT/1,2/A/4200/62, does not contain acceptance criteria to irdicate if adequate flow exists during the flushing process. Therefore, this incident is attributed to a Defective Procedure due to incomplete information. As a result of this event, Design Engineering developed-acceptance criteria to indicate minimum RN to NW flow based on RN essential i header pressure for use during future tests. pT/1,2/A/4200/62 will be revised j to incorporate thia data, j i
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0l0 0l4 or 0l7 Following system cleaning, Operations determined that the flow blockage existed due to sediment buildup at the inlet to valve 2NW8A (NW Surgo Chamber 2A RN Supply Isolation), which is normally closed. The piping upstream of this valve is filled with stagnant RN water which is susceptible to sediment buildup. The
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blockage that existed at vent valve 2NW118 compounded the low flow measurements recorded while completing PT/2/A/4200/62. Thus, the procedure is also deficient due to the specified test method of measuring flow at the vent valve. Actual RN to NW Surge Chamber flow was not measured and cannot be determined.
PT/1,2/A/4200/62 will be revised to require flow to be measured between the last in-line valve and the surge chamber. This will indicate actual RN to NW flow during future tests.
A contributing cause of this event is attributed to the less than adequato understanding by Operations of previous test results which indicated a substantial difference in flow rate between the trains of NW. The System Expert was not consulted nor involved in the review of these data. This time difference between trains was noted by Operations and attributed to clogging of 2NW118. Each time 2NW118 was taken apart it was found to be significe.ntly clogged. An inappropriate action occurred when it was assumed that the total reason for the low flow was clogging of 2NW118 and that sufficient flow did exist from RN to the NW surge chamber. Because of this assumption, low priority was assigned to the work requests for cleaning 2NW118. The System Expert was not consulted in the assignment of work request priority. As corrective action, Operations staff personnel will be reminded of the importance of involving the assigned System Expert in reviewing problems.
Another contributing cause of this event is less than adequate implementation of the recommendations made by the Asiatic Clam Tack Force to ensure acceptable performance of raw water systems. Review and trending of the results of the NW flush test were not performed. As corrective action, a review will be performed to evaluate the remainder of the raw water system flush program to ensure adequate implementation of the Task Force's recommendations.
An extensive review of RN and NW piping configurat.v was conducted to determine if A train is more susceptible to flow blockage th.. 3 train. There were no differences identified that would indicate this condition.
A review of the OEp database for the previous 24 months revealed no other incidents where raw water system interaction with safety systems caused a 4 Technical Specification (T/S) violation. Therefore, this is not considered to f be a recurring event. However, 25 months ago, LER 413/88-15 was written due to the degraded performance of the Unit 1 Auxiliary Feedwater [EIIS:BA) (CA) System )
and required Hot Shutdown of both Units due to Asiatic clam infestation in the RN System. Corrective actions initiated as a result of this incident were {
1 extensive, and no related T/S violations had occurred up to this incident.
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l Catawba Nuclear Station, Unit 2 o l6 lo jo jo l q 1l4 0l0 l6 0l0 0l $ or 0[7 91 0 rixt u -. . =w. w ,w we i ,asumm CORRECTIVE ACTION SUBSEQUENT
- 1) The Unit 2 Train A RN to NW Supply Line and valve 2NWil8 were cleaned and flushed to meet acceptance criteria provided by Design Engineering.
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- 2) The Unit 2 Train B and both Unit 1 trains of RN to NW were flushed to check for flow blockage. No problems were noted during this process.
, 3) Design Engineering developed acceptance criteria for minimum RN to NW flow based on RN essential header pressure for use during future
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tests.
- PTANNED
- 1) Operations test procedures will be revised.to incorporate data from Design Engineering for use as acceptance criteria for minimum flow.
The test method will also be changed to require flow measurement to be
, taken between the last in-line valve and the surge chamber. In addition, the test frequency for the RN to NW Piping Flush will be ;
increased from quarterly to monthly as an interim measure, until l results are further evaluated. i
- 2) A review will be performed to evaluate the raw water system flush and flow monitoring program relative to the' recommendations of the Asiatic Clam Task Force. ,
- 3) Operations will communicato with Operations staff the need to involve the assigned System Expert in reviewing problens. Lessons learned <)
from this event will be provided to operations staff to emphasize this point.
SAFETY ANALYSIS The NW surge chambers are normally maintained with a pressurized volume corresponding to 72% level, or approximately 67 gallons. Upon receipt of a phase A Containment Isolation signal, the chamber outlet isolation valve would open to inject water into the cavity between the seating surfaces of certain 4 gate valves used tor containment isolation. One noted difference'between a !
system test and actual system operation is that the cavities of the majority of the valves served would already be filled with water at a pressure higher than i Containment design pressure, thereby minimizing depletion of the surge chamber. i Based on the maximum allowable valve seal injection flow rate of 1.21 g:n (Unit ;
2-Train A), it can be expected that with no chamber makeup provided, the '
available surge chamber volume of 67 gallons would be depleted in approximately
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EXPIRES: l'31/gs
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LtR NUMttR 461 PACE (3) vtan S$4y(A4 .Q848,Q Catawba Nuclear Station, Unit 2 rsx, tu ma. eu. e ea.o .m w ec r.~ au ei on 0l5l0l0l0l q 1l4 S0 --
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0l0 0[6 or ol7 55 minutes. The most recent actual leakage test results have indicated an injection flow rate to be approximately .23 gpm, which would yield a chamber depletion time of approximately 291 minutes following an actuation of the NW System. It is therefore reasonable to assume that adequate sealing of the affected containment isolation valves would have been provided for at least 291 minutes. Symptoms indicating isolation of assured NW makeup would not be evident at least until low-low chamber level was reached, set to occur at 25%
level and approximately 152 minutes into an accident. '
At the low los chamber level setpoint with the Containment Isolation signal present, automatic makeup from RN would normally occur. With that source unavailable, the contents of the surge chamber would in fact be depleted, but j not before control room computer alarms would be received for surge chamber low ;
level and pressure. position status of the RN supply isolation valve (2NW-BA or l 2NW-61B) would indicate OpEN cn the computer at the low-low level signal. ;
Analog computer indication of chamber level, as well as control board gauges of pressure and level are also available to the Operator. Indication of low surge ;
chamber level and pressure, open status for the RN supply isolation valve, and normal RN essential header pressure would be evidence of either a closed valve or blockage in the supply line to the surge chamber. These symptoms could j
, reasonably be expected to be evident on both trains and at different times due to a difference in train leakage rates.
With the situation recognized, manual makeup of a limited volume from the Makeup !
Domineralized Water [EIIS:KJ) (YM) System, coordinated with the proper nitrogen '
overpressure from the available nitrogen supply, would have remained as a viable but limited option. The limitation of resorting to YM in an accident situation it in view of the 30-day capacity and minimum pressure requirement placed on the NW surge tank assured makeup.
A review of previous test results indicate the RN to NW supply line was clear of obstruction on March 24, 1989. The time required to obtain the one gallon sample was 7 seconds on this date.
l The data from the test performed June 26, 1989 (27 seconds) indicates that some amount of blockage existed at that time. Due to the test method of measuring flow at the vent valve, the location of this blockage cannot be determined. It is reasonable to assume that blockage existed in the vent valve and in the supply line. Therefore, to assure conservatism, the Unit 2 Train A RN to NW supply line will be assumed inoperable starting June 26, 1989. At the next tust i date, September 23, 1989, the data (130 seconds) further indicates system ;
inoperability. The supply line was cleaned, tested, and returned to service on March 29, 1990, therefore the time frame addressed in this safety Analysis is June 26, 1989 to March 29, 1990. !
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Technical Specification 3.6.6 requires that both NW trains are operable during Modes 1, 2, 3, and 4. Catawba Unit 2 operated in these Modes almost exclusively during the time period in question, with A Train potentially inoperable. Due to redundancy provided by IN Train B, 2njection water would have been available to
, ensure Containment isolation. However, IN Train B was also inoperchle at intermittent times during this period due to train related testing or work activities (D/G 2B RN Train B, IN Train 2B). During these short, intermittent periods of time, both trains of NW were inoperable, periods of Train B IN inoperability were limited by the Tech Spec Action Statement time limits applicable to the system causing inoperability. The longest period permitted is 7 days (for the NW system). The maximum single duration of inoperability of both trains of NW is assumed to be 7 days.
The postulated event in concern is a LOCA at a time between June 26, 1989 and March 29, 1990 when NW Train B was inoperable. The low probability of a large break LOCA (7E-4) is further reduced during the approximate 9 month period in questisn. The probability of this postulated event is significantly reduced by the short periods of time that NW Train B was inoperable. Due to the cumulative effect of these conditions, the overall probability of the postulated event is reduced to approximately 7.5E-5.
If the postulated event were to occurr (a LOCA with both NW trains inoperable),
seal injection flow would have been available until depletion of the surge chamber. After this tine, with no makeup assumed, offsite dose limits specified in 10CFR100 could have been exceeded due to increased leakage outside j Containrent.
During the period of time in which Train A NW is considered to have been potentially inoperable, an accident requiring operation of the NW did not occur.
Thus, there were no radiological consequences as a result of this incident and the health and safety of the public were not affected.
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