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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
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March 12', 1990 t
E m- Document Control Desk U. S. Nuclear Regulatory Commission (
Washington, D. C. 20555 3--
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Subject:
Catawba Nuclear Station
. Gentlemen:
Attached is Licensee Event Report 413/90-12, concerning TECHNICAL SPECIFICATION 3.0.3 ENTERED FOR BOTH TRAINS OF ANNULUS VENTILATION '
SYSTEM INOPERABLE DUE TO A CONTROLLED ACCESS DOOR FOUND OPEN AS A RESULT OF- AN INAPPROPRIATE ACTION. '
2 This event-was considered to be of no. significance with respect to tho ;
l health and: safety of-the public.
Very truly yours,
[ b
' Tony B.-Owen Station Manager keb\LER-NRC.TBO xc: Mr. S. D. Ebneter American Nuclear Insurers Regional Administrator, Region Il c/o Dottie Sherman, ANI Library
'U. S. Nuclear Regulator Commission The Exchange, Suite 245 101. Marietta Street, NW, Suite 2900 270 Farmington Avenue Atlanta, GA 30323 Farmington, CT 06032 M & M Nuclear Consultants Mr. K. Jabbour 1221 Avenues of the Americas U. S. Nuclear Regulatory Commission r New York, NY- 20020 office of Nuclear Reactor Regulation Washington, D. C. 20555 INPO Records Center Suite 1500 Mr. W. T. Orders 1100 Circle 75 Parkway NRC Resident Inspector
' Atlanta, GA 30339 Catawba Nuclear Station
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Catawba' Nuclear Station, Unit 1 0 l510 t o l 014 l 113 1 loFl0 l 8 tit* Technical Spe::ification 3.0.3 Entered For Both Trains Of Annulus Ventilation System Inoperable Duc To Inappropriate Action !
EVENT DATE 151 LER IdWMcE R ($1 REPORT DATE (71 OTHER F actITIES INVOLVED 191 MONTH II U '"4 F ACILITV NAMES DOCAET NUMBERtSi DAY YEAR YEAR , fu e MONTH DAV YEAR N/A 0l5l0l0l0; ; ;
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NIME TELEPHONE NUMBER ARE A CODE j R.M. Glover, Compliance Manager 8 1 01 3 813 11 l- 1 3121316 COMPLETE ONE LINE FOR E ACH COMPONENT F AILURE DESCRIBED IN THIS REPORT H31 CAUSE SYSTEM COMPON E NT MA AC- RE' CAV$E Sv 8T E V COMPON%T "" "U "I' " '
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~} vts uo r na. intereo sunwssion od rei ~) NO l l l Aes,R ACT ev-., ra um a . i. . m.-.w, r.<, ,. .o-a no. awi s > os, On January 27, 1990, at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />, Unit I was in Mode 3, Hot Standby.
Controlled. Access Door'(CAD) 311, Lower Containment Personnel Air Lock, had been ,.
placed on a continuous fire watch. At approximately 2205 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.390025e-4 months <br />, the Central Alarm Station (CAS) Operator noted that CAD 311 was not closed. The Security Lieutenant directed the Operator to immediately notify the Security Officer at the hatch area. An Operations (OPS) Control Room Operator (CRO) was notified and Technical Specification 3.0.3 was entered due to the inoperability of the Annulus Ventilation (VE) System. The door was closed at 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br />, and the OPS CR0 exited Technical Specification 3.0.3 at that time. Several individuals were interviewed regarding the status of the door during their transits, and Security door alarm typers were reviewed.
It was concluded that the door had been tied i
to the adjacent railing with a rope from approximately 2110 to 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />, and again from approximately 2150 to 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br />. The cause cf this incident is attributed to inappropriate action taken which was unauthorized. Personnel
)- entering Containment were instructed not to leave the door open. A review of l
CAD doors critical to Ventilation System operability will be completed, as well l
L as distribution of information to all station personnel emphasizing the importance of ventilation system operability.
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M i BACKGROUND 4
The Annulus Ventilation [EIIS:VD] (VE) System is designed to achieve a negative pressure of at least 0.5 inches water gauge (inwg) in the annulus, following a loss-of-coolant accident (LOCA). Following a LOCA event, the VE System i minimizes the release of radioisotopes by filtering and recirculating a large y amount of air relative to the volume discharged. It consists of two j independent, 100 percent capacity trains. Upon receipt of a safety signal, recirculating and discharge dampers are automatically aligned to the Unit vent a until negative pressure is greater than or equal to 0.5 inwg. These dampe: 4
} then modulate to maintain the annulus at a negative pressure of 0.5 inwg.
? In the initial design of the VE System and evaluation of various annulus j conditions, Duke Power developed the CANVENT computer model. CANVENT was used to establish and evaluate various design parameters for the VE System. This i program takes several factors into account, such as pre-LOCA temperature-distributions, post-LOCA temperature distributions, post-LOCA annulus temperature and pressure, and the capability of the VE fans [EIIS:BLO] to achieve and maintain a vacuum in the annulus following a LOCA. Other factors
, included in this program are heat transfer from upper and lower Containment e [EIIS:NH] into the annulus, effects of swelling of Containment, and changes in j annulus air density during a LOCA.
i
) Technical Specification 3.0.3 is required to be entered when the Unit is
- operating in a condition prohibited by Technical Specifications. This condition 2
exists when a Limiting Condition for Operation is not met except as provided in the associated Action Requirements. It requires that within one hour action 1 shall be initiated to place the Unit in a Mode in which the specification does i not apply by placing it, as applicable, in; a.-At least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,
- b. At least HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and
- c. At least COLD SHlfTDOWN within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Technical Specification 3.6.1.8 requires both trains of VE to be operable in ,
-Mode 1, Power Operation, Mode 2, Startup, Mode 3, Hot' Standby, and Mode 4, Hot Shutdown. The Action Requirement is that with one train of VE inoperable,-the train must be restored to operability or the Unit must be in at least Mode 3 within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and in Mode 5, Cold Shutdown, within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. Surveillance Requirement 4.6.1.8.d.4 states that at least once per 18 months, it must be.shown that each train of VE can produce a negative pressure of at least 0.5-inwg in the annulus within one minute after the start signal.
This requirement is periodically met by the Annulus Ventilation System Performance Test, PT/1,2/A/4450/03C.
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f Technical Specification 3.6.1.3 requires that each Containment air lock be q, operable in Modes 1 through 4. Surveillance Requirement 4.6.1.3b requires an overall air lock leakage test at least once per 6 months. This test is 7 performed in PT/1,2/A/4200/01F, Lower Containment Personnel Air Lock Leak Rate Test.
Technical Specification 3.7.11 states that all fire barrier penetrations
[EIIS: PEN] separating safety related areas shall be operable at all-times. With any of the required fire barrier penetrations or sealing devices inoperable, r
within one hour either establish a continuous fire watch on at least one side of the affected penetration, or verify the operability of fire detectors [EIIS:XT]
on at least one side of the inoperable penetration and establish an hourly fire watch patrol.
The Fire Detection [EIIS:IC] (EFA) System monitors unattended areas of the plant e for smoke or fire, and alerts personnel of the existence and laation of-a fire. ,
, The EFA System is equipped with a Central Fire Detection Panel that alerts Operators, via an alarm, for specific zones within the plant.
Station Directive 2.12.7, Fire Detection and Protection establishes the requirements and responsibilities to ensure that the fire protection standards comply with applicable Technical Specifications. Operations (OPS) assigns the responsibility of Fire Protection Console Operator (FPCO) the duties of maintenance of the Fire Watch Log and all other assignment of continuous and hourly fire watches by station personnel.
Station Directive 3.1.2, Access to Containment, requires that during periods of Reactor shutdown when frequent access to Containment is necessary, Security personnel shall be posted at the personnel air lock area to collect Security badges and to grant access. Also, when the Unit is in Mode 5, Cold Shutdown, or Mode 6, Refueling, the CADS may be propped open and remote card readers utilized to maintain Security documentation.
EVENT DESCRIPTION On January 27, 1990, Unit I was in Mode 3, Hot Standby. Controlled Access Door (CAD) 311, Lower Containment Personnel Air Lock, had been placed in a continuous fire watch status at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />, due to the mechanical lock on the door being taped to facilitate entry into Containment. This action to the lock was taken by direction of Radiation Protection (RP) due to CAD 311 being a High Radiation Area Door. In addition to Security personnel being present at the hatch area, an RP Technician was also present maintaining the Controlled Area Access Log.
Also, due to the increased flow of personnel through the door, Security had located a CAD key beside the CAD access box and the personnel entering were instructed to use the key for entry. At 0750 hours0.00868 days <br />0.208 hours <br />0.00124 weeks <br />2.85375e-4 months <br />, the OPS FPC0 had logged CAD 311 as being in " access" status due to the high personnel traffic flow and the
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register on the typer printout in the CAS, but will not alarm at the CAS panel, All entries and exits are maintained on the alarm typer. An assigned Security Officer was stationed outside the door with a Vital Area' Access Log. Each individual who was authorized access to Unit 1 Lower Containment was " badged into" Containment and " logged out" by surrendering their Security badge to the Security Officer. At 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br />, the Contral Alarm Station (CAS) Operator noted that CAD 311 was opened (not completely closed) and was instructed by the Security Lieutenant to notify the Security Officer at the hatch area, outside CAD 311. OPS was notified by Security at 2210 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.40905e-4 months <br /> that the door was found open.
Technical Specification 3.0.3 was entered due to both trains of VE being declared inoperable. The door was closed at 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br />. Following this event, the door's mechanical lock was re-enabled. The OPS CR0 exited Technical c Specification 3.0.3 at 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br />.
Following the incident, interviews were held with seven workers who entered and exited via CAD 311. During the period from 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> to 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br /> on January 27, 1990, five workers had noted that the door was tied to the adjacent railing with a 1/4 inch nylon rope. Also, from approximately 2150 hours0.0249 days <br />0.597 hours <br />0.00355 weeks <br />8.18075e-4 months <br /> until 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br />, two workers interviewed stated that the door was tied open. One individual interviewed who entered Containment at 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />, clearly recalled having difficulty opening the door.and stated that CAD 311 was closed. It is concluded that CAD 311 was closed correctly prior to 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br />. A review of Security alarm typer door records indicated that CAD 311 was not fully closed from 1818 hours0.021 days <br />0.505 hours <br />0.00301 weeks <br />6.91749e-4 months <br /> to 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br />, i.e. the electromagnetic pickup was not engaged.
The review also indicated that no one transiting CAD 311 between 1825 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.944125e-4 months <br /> and
?225 hours0.0026 days <br />0.0625 hours <br />3.720238e-4 weeks <br />8.56125e-5 months <br /> used the CAD key posted at the door in gaining entry, and no computer '
indications of CAD key use were recorded during this time.
CONCLUSION The continuous fire watch on CAD 311 was initiated at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />, on January 27, 1990. The reason given for establishment of the fire watch was that the mechanical lock on CAD 311 was " taped back" to facilitate passage through the High Radiation Area Door. Therefore, personnel entrances and exits for Lower Containment were logged onto a Vital Area Access Log by the Security Officer on duty. At 0750 hours0.00868 days <br />0.208 hours <br />0.00124 weeks <br />2.85375e-4 months <br />, the FPC0 initiated the entry into the Fire Watch Log and noted that CAD 311 was in " access" per the Fire Watch Sign Out Sheet. Station Directive 3.1.2, Section 5.4.4 allows CAD doors to Containment to be propped open only in Modes 5 or 6. During the time period that CAD 311 was tied open, Unit 1 was in Mode 3. At the instruction of the Security Lieutenant, CAD 311 was closed and the mechanical lock was re-enabled to ensure that the door latched.
j In addition, the Security Officer at the hatch was instructed by the Security Lieutenant to ensure that the door was not left open. All required fire watch entries were completed by Security personnel. Following the inter' views of personnel who entered and exited CAD 311 on January 27, 1990, no indication or identification was given as to the placement of the rope on the
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Also, during the period of this fire watch and of this incident, the :
Security Officers on duty were not able to see CAD 311 completely from their station. They were unable to see the point that the rope was tied, due to the 4 material placed at the platform for contamination / housekeeping control.
It is concluded from interviews and material reviewed that CAD 311 was tied open from approximately 2110 to 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />, and again from approximately 2150 to 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br />. The person (s) responsible for tying the door open could not be determined. This incident is attributed to inappropriate action due to unauthorized actions taken.
Recent analyses by Design Engineering indicated that the VE System would not operate as described in FSAR or Technical Specifications if the " main door to
- the annulus or the CAD door to the upper or lower air locks is left open". Per the Intrastation Letter from T.B. Owen, dated July 5, 1989, all Station Supervisors were instructed to complete a Compensatory Action sheet, (Enclosure 3 of Station Directive 3.1.14, Operability Determination) which would result in the maintenance of the capabilities of the VE System with one or more of the described doors open. The form requires that a person be at the door (s) with communications established with the Control Room. This action would then allow the person to be told immediately to close the door (s) in the event of a LOCA.
' The individuals completing the Compensatory Action sheet must initial the sheet upon completion of the form and that they understand their responsibilities for
^ the actions. Prior to this incident there was no Compensatory Action sheet completed. There were no specific communications capabilities arranged prior to the opening of the CAD 311, although a Security Officer was continually'present.
As a result'of this event, an Intrastation Letter will be issued to emphasize to all employees the importance of CAD position to ventilation system performance and the action to be taken when doors are repositioned. Alternative courses of action will be evaluated to achieve tighter control of CADS critical to ventilation system performance.
A review of the Operating Experience Program (OEP) Database for the previous 24 months identified one incident that involved VE System operability (see PIR 0-C88-0266). This incident resulted in both trains of VE being unable to meet FSAR conditions due to removal of a bypass leakage enclosure plate. The root cause of this incident was attributed to a defective procedure. The tests performed as part of the investigation established the VE System operability limits noted above. These events are similar in nature, although they involve different causes. This reported incident is not considered to be a Recurring
- Event per the Nuclear Safety Assurance guidelines. Ventilation system performance and operability issues are receiving close scrutiny. A Task Force has been established to provide closer review of testing requirements; a thorough and systematic review of ventilation system design requirements is underway.
NT.C FORM 366A "U.6, CP9 ' L P8 6 - S h* S H
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< .awma ec ra. smru on t i In addition to.the OEP Database review for past VE System inoperability, a '
search was performed to identify fire watch or Technical Specification
' violations pertaining to fire watches and fire barrier integrity. A total of seven reports were identified. Five reports (see IIR C88-003-0, IIR C88-045-1, IIR C88-071-1, PIR 1-C89-0288, and PIR 2-C89-0184) resulted from missed hourly fire watches and two reports (see LER 413/89-02, and LER 413/89-024) resulted in Technical Specification violations- for inoperability of a fire barrier. There were no violations of Technical Specifications pertaining to fire doors or fire barriers during this incident.
CORRECTIVE ACTION IMMEDIATE
- 1) CAD 311 was closed following direction from the Security Lieutenant.
SUBSEQUENT
- 1) The mechanical lock on CAD 311 was re-enabled.
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- 2) The Security Officer at the hatch was instructed by the Security LieuteAant to ensure that CAD 311 was not left open.
, PLANNED
- 1) Distribute Intrastation Letter to all station personnel emphasizing
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the following:
- a. The requirements that shall be performed when a component such as CAD 311 and other doors critical to ventilation systems' operability are to be left open,
- b. Specific references to Station Directive 3.1.14, Operability Determination, as it pertains to completion of Enclosure 3 and specific requirements as mentioned in "a".
- c. In regards to the Units 1&2 Lower Containment Personnel Air Lock Doors, the Security officer on duty at the hatch would provide the required responsibility for communication to the Control Room when the door (s) are opened for personnel traffic, as during the initial stages of a Refueling outage, Modes 1-4,
- 2) Review CADS and ventilation system operation to identify those doors that can impair system performance. Evaluate alternatives for tighter control of these doors during plant modes when ventilation systems operabilities are required.
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SAFETY ANALYSIS 5
.. The incident described by this LER affects operation of the VE System. -The purpose of the VE System is to control the release of fission products that leak r from Containment following a LOCA. During a LOCA, the VE System withdraws air from the annulus, filters it, and then exhausts it to the environment or recirculates it back into the annulus. Exhausting a portion of this air creates a negative pressure in the annulus. The negative pressure assures that fission products leaking from Containment will be collected and filtered before being released to the environment. Control Room and offsite doses are affected by the~
exhaust air flow rate. CAD 311 is part of the annulus pressure boundary.
During a LOCA, having a pressure boundary door open will increase exhaust flow rate and, therefore, increase Control Room and offsite doses.
For the periods when the CAD was open, if the VE System had been required to operate, Control Room and offsite doses would have increased. However, according to Design Engineering, there are two possible mechanisms that may have ,
closed the door in the event of an accident. Closing the door would decrease-the dose consequences associated with this incident. One means of closing the j door was a Security Officer stationed nearby and another means was by the individuals in the area. The Officer was stationed nearby to log persons entering and exiting this area. The Officer was given instructions to close the CAD in the event of a fire, but no specific guidance was given regarding other types of accidents. However, it is reasonable to assume that, if an accident K had occurred and the Officer was notified, he would have checked the door and l-closed it before leaving the area. Another possible means of closing the door P
was by the individuals in the annulus that would exit through this door. If an c accident had occurred and they were exiting the annulus, it is reasonable to
). assume that they would'have closed the door as they were leaving. However, even
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if the door had been closed, it would not have sealed as designed because the latch was taped. A small increase in annulus inleakage would result from not properly latching the door. This amount of additional inleakage would not have significantly increased Control Room or offsite doses.
Even if the door was left completely open there is a possibility that it would have been closed in a timely manner. Emergency procedures (EPs) direct the Operators to check annulus pressure. With the CAD open, the annulus pressure may-not reach its setpoint. The EPs would direct the Operators to check VE damper alignment, and if correct, to investigate further. It is reasonable to assume that station personnel would then have discovered the open CAD and closed it.
Because of the uncertainties associated with the above scenarios and the lack of specific directives regarding the closing of CAD 311, no credit can be taken for personnel actions during this incident. Therefore, Design Engineering has determined that the VE System was inoperable during the periods when CAD 311 was opened.
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It should be noted though that the safety significance of the event in the
((. specific time frame involved was low. When the door was discovered open at 2210-hours, Technical Specification 3.0.3 was entered and the door was closed in five i minutes. During the two periods when the door was open (2110-2130 hours and t' 2150-2215 hours) people were working in the area and returned the door to a O
' closed position in a relatively-short time. The significance of the event is further minimized by the fact that the Unit was in a cooldown for the end of cycle 4 refueling outage and was close to the point of entering Mode 4 (350 '
, degrees F) at these times. Because of the reduced temperature and pressure in the primary system the mass and energy release in a LOCA event would have been less than a full power event.
No fires occurred in the areas surrounding the Unit 1 Lower Containment air lock i-
' or in any nearby zones during the period of this Fire Watch. All required hourly Fire Watch documentation was complete for the period. Had any fires-occurred, operable fire detection instrumentation on both sides of the CAD 311 penetration would have alerted OPS personnel in the Control Room. The alarm would have been investigated and the fire extinguished.
The health and safety of the public were not affected by this incident.
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