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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
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Dukihunt Company *
' (M3MI'3M Y
. 'Catauha NuclearStati n'-
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' Clover, S C 29710 DUKEPOWER
' January' 17, 1990
'D'ocument' Control Desk-
.U. S. Nuclear Regulatory Commission Washington, D.-C.c -20555-
Subject:
> CatawbaLNuclear.Stati'on Docket No. 50-4131 .
.LER'413/89-16, Rev. 1 Gentlemen:
Attached is-Licensee Event Report 413/8D-16,' Revision?1,- concerning TECHNICAL SPECIFICATION.3'O.3 ENTERED DUE'.TO FOUR~ CHANNELS OF POWER.
RANGE' INSTRUMENTATION BEING DECLARED INOPERABLE:FOLLOWING UNIT' RUNBACK.
AS.A RESULT 0F FAILURE.OF,A GENERATOR' BREAKER AIR PRESSURE GAUGE..
This event was considered to beTof no significance lwith respect'to the, health and' safety of the,public.
Very truly.yours,
[
Tony ." Owen.
Station Manager 1 keb\LER-NRC.TBO xc: Mr.-S.'D. Ebneter American^ Nuclear. Insurers Regional Administrator,-Region II' _c/o Dottie.Sherman,'ANI. Library l U. S.1 Nuclear Regulator Commission The Exchange, Suite ~245 101LMarietta Street, NW, Suite 2900- -270 Farmington~Avenuel Atlanta. GA -30323 Farmington, OT 06032 M &'M Nuclear. Consultants Mr. K. Jabbour 1221 Avenues of tho' Americas U'. S. Nuclear' Regulatory Commission-Nek York, NY 10020 Office of Nuclear Reactor'. Regulation .J Washingtoni D. C. L205S5 .; i
- INPO Records Center
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~1100 circle 75 Parkway NRC Resident Inspector.
Atlanta, GA 30339 Catawba Nuclear! Station <
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- ' ' ' * ' Four Channels of Power Range Instrumentation' Inoperable Following Unit-Runback As A Result of Failure of a Cencrator Breaker Air Pressure Gauge EVENT OATI 161 LER NUMeER 18) REPORT DATE (7) OTHER F ACitfTIES INVOLVED fel MONT'ef%AY YEAR YEAR -
, MONT H OAV YEAR F ACIL4TY N AMts DOCKET NUMBERis) 7 N/A ol5lo10lo] l l
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On September 13, 1989, at 0541' hours Unit i was in Mode 1, 100% Power Operation. Generator 1B Power Circuit Breaker (PCB) opened causing Unit runback to 54% Power. Four out of four channels of Power Range Nuclear Instrumentation !'
(PRNI) displayed greater than the 5% allowable mismatch between Rated Thermal l l
Power (RTP) and Nuclear Power, in the non-conservative direction. At 0550-hours, l Technical Specification 3.0.3 was entered and Work Request 4099 SWR was issued-l to complete calibration of the PRNIs. The Unit was stable at 54% Power at 0630 '
hours and the calibrations were performed. Following the required calibrations of the PRNIs, the Unit exited Technical Specification 3.0.3. The pneumatic gauge was subsequently replaced, and Generator PCB 1B was restored.to service.
Unit Power increases commenced at 1003 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.816415e-4 months <br />'on September 13, 1939. All required PRNI calibrations were completed to within 2% of RTP by 1525 hours0.0177 days <br />0.424 hours <br />0.00252 weeks <br />5.802625e-4 months <br />.
Unit Power reached 97% Power at 1815 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.906075e-4 months <br />. At 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, Unit Reactor Power reached 100%. The Power Range mismatch was considered to be an expected phenomenon following e Unit runback. This incident has been attributed to Equipment Failure due to the failure of the pressure gauge on the PCB which caused the Unit runback.
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U.S. NUCLEA3 ECEIULATORY COMMEW40N
" 4' 1 1 UCENSEE EVENT REPORT (LER) TEXT CONTINUATION ' Aaenovto ous No. mo-oiot [
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j ~ The purpose of the Out of Core Instrumentation [EIIS:JG] (ENB) System is to 4 s monitor. Reactor-[EIIS:VSL] Core leakage neutron flux and generate appropriate t
< trips and alarms for various phases of. Reactor [EIIS:VSL], operations. The three i 2 ' separate overlappi.ng ranges' of Source Range, Intermediate Range, and Power Range
, also provide control functions and indicate Reactor status during Mode 2,
- Startup and Mode 1, Power Operation _ Technical Specification;4.3.1.1 requires . S that channel calibration ~be performed daily on;the Power Range Neutron Flux High Setpoint. This is to be. performed by-comparison-of. calorimetric (reactor . .
, thermal power best estimate, based on; actual plant indicator temperatures). to ,
) excore' power (based upon nuclear'powernlevels from detector instrumentation) i indication when the Unit is above 15% Rated Thermal Power.(RTP). Excore channel !
- ' gains are to be adjusted to make indicated.excore power consistent with
? indicated calorimetric power whenever- this comparison . reveals an absolute !'
j difference of more than 2% between the two..
l' Technical Specification 3.3.1, Table 3.3-1, requires-that three out of 1our-channels of PRNI must be operable during. Modes 1 and 2. ;
During power operation, a power.. range channel must be considered INOPERABLE i 1 whenever a mismatch exists-between calorimetric; power and~excore power- >i indication that is-greater than 5.0% in the non-conservative direction '
'(calorimetric power greater'than:excore power). If the mismatch is between 2.0%
L and'5.0% in the'non-conservative direction, the channel is OPERABLE as long as i
. the calibration process has been ' initiated. ;When the Unit is engaged in a= power maneuver which results in a mismatch between . calorimetric and excore power in 1 excess of 2%, 'excore adjustment may be delayed.until the Unit reaches a steady state power level, provided the mismatch does not exceed 5.0% in the non-conservative direction, as specified by the Technical; Specification
' Interpretation, dated June 2,'1989.
Technical Specification 3.0.3 is required to be entered when the Unit.is -
operating in a condition prohibited by Technical Specifications. This condition .
exists when a Limiting Condition for Operation-is not met except as provided in the associated Action Requirements. It requires'that within one hour-action- -
shall be initiated to place the Unit in a Mode-in which the' specification d m s {
not apply by placing:it, as applicable, in:
- a. At least HOT STANDBY within'the next 6_ hours,
- b. At least HOT SHUTDOWN-within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and
- c. At least COLD SHUTDOWN within'the subsequent 24' hours.
The Unit Main Power [EIIS:EA]-(EPA)' System's primary function is to generate and transmit power '.o Duke's Transmission. System while-simultaneously supplying the -
6.9KV Normal' Auxiliary Power-[EIIS:EA]-(EPB) System. 'If the generator NK Om 366A - .g.s. cro, 19tg.90439 00010 W__-. - . . _ --_ - . . - . . . . . - ..
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. U1 NUCLEA3 REGULATORY -~
, LICENSEE EVENT REPORT (LER) TEXT CENTINUATION
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[EIIS: GEN]-is out of service, the EPA System is used to supply power from the
~
e Transmission System to the Unit Auxiliary Power System. The EPA ~ System is 5 divided into non-safety trains, connected to the 230KV switchyard through a ;
h step-up transformer [EIIS:XFMR] and two power circuit breakers [EIIS:BRK] (PCBs) 1 K located in the switchyard. A generator breaker is provided on each train. The l- generator breaker and step-up transformer combination on each train is capable of carrying approximately fifty percent (750MVA) of the rated generator output.
EVENT DESCRIPTION On September 13, 1989, at 0541 hours0.00626 days <br />0.15 hours <br />8.945106e-4 weeks <br />2.058505e-4 months <br />,'with Unit 1 at 100% Power Operation, i Generator PCB 1B tripped open, causing an unexpected Unit runback. Operations Q entered AP/0/A/5500/03, Load Rejection. At 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, the PRNI:versus Thermal' f Power (TP) was observed to be greater than 5% non-conservative on all four
(- channels. Technical Specification 3.0.3 was entered'at 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, and Work . 'i Request 4009 SWR was issued to direct the Instrumentaion and Electrical (IAE) section to calibrate the PRNI. The-determination was made at 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br />,'that Generator PCB 1B tripped on low air pressure as a result of a failed pressure gauge at the PCB, Phase X. The Unit was stablized'at 54% Power at'0630' hours.
The Control Room Operator (CRO) exited Technical Specification 3.0.3 at 0640 ;
g hours, due to the acceptable power mismatch on three of the four channels. '
Operations determined-that the failed pressure gauge would be replaced by 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, by the Transmission Department; therefore, adjustment of the remaining.
power range channel per Technical Specifications was unnecessary as power escalation was expected to correct the mismatch problem. ,
' Generator PCB 1B was restored to service at 0952 hours0.011 days <br />0.264 hours <br />0.00157 weeks <br />3.62236e-4 months <br />, following the -
i replacement of the pneumatic pressure gauge. No problems were encountered following this action.
At 1003 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.816415e-4 months <br /> on September 13, 1989, Unit 1 Power increase began to establish '
100% Power Operation. Power was increased from 54% at a rate.of 10% per hour.
At 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br />, Reactor power was at 90% and holding to perform Main Steam
[EIIS:SB] (SM) System control valve _[EIIS:V] movement tests and to complete final PRNI calibrations. All four channels of the PRNI registered Quadrant ,
Power Tilt Ratios of less than 1.02%. The control valve movement test and PRNI 1 calibrations were complete at 1525 hours0.0177 days <br />0.424 hours <br />0.00252 weeks <br />5.802625e-4 months <br />. Power _ increases continued to 100% at '
3% per hour. Unit power reached 97% thermal power at 1815 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.906075e-4 months <br /> and by 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, the Unit reached 100% Power Operation.
CONCLUSION This incident has'been attributed to Equipment Failure. The pneumatic gauge, manufactured by Protais (France), normally displays _a pressure of 500 lbf/sq.in. !
on Phase X, Y, and Z of the Generator B PCB. The failure of the gauge occurred '
at the connection of the bourdon tube and the linkage of the meter. The pneumatic pressure that resulted from the break of the soldered connection caused the gauge to be separated from its housing on the breaker. The immediate l
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.' x UCENSEE EVENT REPORT (LER) TEXT CONTINUATION . Ae*Roveo ous wo. smoo.
. EXPtRit; 8/31/m ,
FACILITY esAast it) , 00 cutt NUaWER 82) Litt Ni4ISER (G) . PA06 (3) vs.. .pgg,a' ery,;; ;
Catawba Ndelear Station, Unit 1 o l5 l0 lo lo l @ 1l3 _8l 9 0l1j6 -
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TEXT ta mese guess e segueset use estseenaf WC Fen m W 117l drop in pressure caused the Generator 1B PCB to tr'ip open. During the fourteen !
year use history of the Protais. gauges, there have.been no failures reported.
The mismatches reported.on the PRNI channels after Unit power reduction were considered to be-an expected phenonmenon. Within the past twelve months, one previous Problem Investigation Report (PIR)-2-C88-0335 was-initiated as a. result
' of entering Tech Spec 3.0.3 due to all four channels of PRNI being declared
-inoperable. This occurred during a power manuever of Unit 2 from 96% to 51%
' power. All channels were' inoperable due to the allowable non-conservative mismatch between calorimetric power and excore power. The cause of that incident was attributed,to Defective Procedures. The procedure OP/2/A/6100/03,. -
Controlling Procedure'For Power Operation,.did not contain a Caution or other L information concerning the Power Range mismatch that normally occurs on a power
( decrease. The procedures-for both Units were revised. A Technical .
F Specification Interpretation revision was issued June 9, 1989. Since this previous incident was not. caused by Equipment Failure,- the current incident is not considered to be a recurring event. ;
The Protais' gauge is not NPRDS reportable.
CORRECTIVE ACTION l
l SUBSEQUENT t
l 1) Work Request 4099 SWR was issued to recalibrate the PRNI.
l l 2) The Protais pneumatic gauge was replaced for? Generator IB PCB. !
! 3) Recalibration of PRNI was completed, per IP/1/A/3240/11.
- 4) Safety Analysis was revised based upon review.
- 5) The' failed Protais pneumatic gauge was sent to the Duke Power i Standards Laboratory for' failure analysis and testing.
L SAFETY ANALYSIS l
The excore power range neutron detectors [EIIS:XT]'are arranged and located such that one detector measures core leakage neutron flux for one quadrant. Each l
detector and its associated circuitry comprise one channel, for a total of four PRNI channels. The Power Range High Neutron Flux Trip (High Setpoint) function utilizes a 2-out-of-4 trip logic. l Nn po7su sse.
'U.S. CPCs 1968 320 5894000M
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, LICENSEE EVENT REPORT (LER) TEXT C2NTINUATION -
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DOCKET NuestR (2) HR NumetR m Pm m p vtan - agg,a6 q=,7; 1
f Catawba Nuclear Station, Unit 1 o l5 l0 jo l0 l 11 1l 3 8l 9 0l1l6 0 l1 0l 5 OF 0 l8 7
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', 1 Catawba Technical Specification 4.3.1.1 requires that channel calibration be-performed daily on the Power Range Neutron Flux High Setpoint. This is to be performed by comparison of calorimetric (thermal.best estimate) to excore. power
..1 indication when the Unit is above 15% rated thermal power-(RTP). Excore. channel
[; gains are to be adjusted to make' indicated excore (NIS) power consistent with .
' indicated calorimetric power whenever this comparison reveals an absolute difference of more than 2% between the two.
During power operation, a power range channel must be considered IN0PERABLE
~
whenever a mismatch exists between calorimetric power and excore power -
. indication that is greater than 5.0% in the non-conservative direction i (calorimetric power greater than excore power). If_the mismatch is between 2.0%
f.I '
and 5.0% in the non-conservative direction, the channel is OPERABLE as long as the calibration process has been initiated. When the-Unit is engaged inLa power-maneuver which results in a mismatch between calorimetric and excore power in excess of 2%, excore adjustment may be delayed until-the Unit reaches,a steady: l state power level, provided the mismatch does not exceed 5.0% in- the non- i' conservative direction, as specified by the Technical Specification Interpretation, dated June 2, 1989. The justification for the increased allowable mismatch is based upon the existing margins in the Steam Generator
,, [EIIS:HX] (S/G) low-low level and power range high flux (high and low) setpoint !
i calculations, power range response during specific transient analyses, and the- i conservatisms inherent in the Catawba FSAR analyses.
Bank D Rod Cluster Control Assemblies (RCCAs) are located in the core such that- j one RCCA is inserted in the middle of the core along.the vertical axis, with one '
- 'RCCA inserted in each of the four quadrants (for a total of 5 RCCAs in Control Bank D). -The RCCAs in control Bank D are positioned more closely to the excore neutron flux seen by these detectors to a greater degres than the other control banks. This phenomenon commonly _ occurs during power reductions in which Control Bank D is partially inserted.
~
Core quadrant 1 (channel N43) mismatch exceeded 5% from 0555 hours0.00642 days <br />0.154 hours <br />9.176587e-4 weeks <br />2.111775e-4 months <br /> to.0643 hours0.00744 days <br />0.179 hours <br />0.00106 weeks <br />2.446615e-4 months <br />; core quadrant 2 (channel N42) mismatch exceeded 5%'from 0555 hours0.00642 days <br />0.154 hours <br />9.176587e-4 weeks <br />2.111775e-4 months <br /> to 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br />; core quadrant 3 (channel N44) mismatch exceeded 5% from 0555 hours0.00642 days <br />0.154 hours <br />9.176587e-4 weeks <br />2.111775e-4 months <br /> s to 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />; core quadrant 4-(channel N41) mismatch exceeded 5% from 0552 hours0.00639 days <br />0.153 hours <br />9.126984e-4 weeks <br />2.10036e-4 months <br /> to 0623 hours0.00721 days <br />0.173 hours <br />0.00103 weeks <br />2.370515e-4 months <br />. Therefore, all four NIS channels were technically inoperable from 0555 hours0.00642 days <br />0.154 hours <br />9.176587e-4 weeks <br />2.111775e-4 months <br /> to 0623 hours0.00721 days <br />0.173 hours <br />0.00103 weeks <br />2.370515e-4 months <br />, a total of 28 minutes. The maximum mismatch errors were 8.1%, 7.8%, 6.95%, and 8.2% for quadrants 1, 2, 3, and 4, respectively. During this short period of multiple channel inoperability, the channels were not functionally inoperable, as they would have still_provided input to the SSPS Reactor trip function. The NIS channels were only 3.1%, 2.8%, j 1.95%, and 3.2% non-conservative beyond.the allowable mismatch, for quadrants 1 !
through-4, respectively, i
-The following'is a list of Catawba FSAR Chapter 15 transients in which credit is assumed for the Power Range High Neutron Flux Trip (High Setpoint):
i l
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[
t j 1)- Startup of an-Inacti.ve Reactor Coolant Pump [E!IS:P] at an Incorrect !
1 Temperature (discussed in Section 15.4.4).
S- .
1
- 2) Feedwater System Malfunctions that Result in a Reduction in Feedwater b Temperature (discussed in Section 15.1.1).
b L 3) . Excessive Increase in Secondary Steam Flow (discussed in Section. <
[.. -15.1.3).
- 4) Inadvertent Opening of a Steam _ Generator Relief or Safety Valve '
(discussed in Section'15.1.4).
- f I
j 5) Steam System. Piping Failure (discussed in Sectionf15.1.5). .
ls ll 6) Uncontrolled Rod [EIIS: ROD] Cluster Control Assembly Bank Withdrawal
[; From a Suberitical or Low Power Startup. Condition (discussed in L Section 15.4.1), r
( .
[ 7) Uncontroll'ed Rod Cluster Control Assembly Bank Withdrawal.at Power p (discussed in Section'15.4.2).
h
- 8) . Spectrum of Rod Cluster Control Assembly Ejection- Accidents (discussed in Section 15.4.8).
The following discussion outlines the protective features'which existed for the above scenarios other than the Power Range High Neutron Flux Trip Function (High Setpoint): -
- 1) The "Startup of an Inactive Reactor' Coolant Pump at an Incorrect Temperature" scenario.is not applicable. All.four Reactor Coolant loops were in operation during this incident. However .if the Unit-had been operating in'a three loop configuration, any. postulated power excursion would have been terminated.at the P-8 setpoint (2-out-of-4 '
power range indications > 49% full. power).
L 2) The Unit would be protected against a "Feedwater System Malfunctions that Result in a Reduction in Feedwater Temperatures "' scenario by the Overtemperature and Overpower Delta-T trip functions.
- 3) The Unit would be protected against the " Excessive Increase-in Secondary Steam Flow" scenario by the Overtemperature and Overpower-Delta-T trip functions. -;
L
' 4) The Unit would be protected against the " Inadvertent Opening of a- ,
Steam Generator Relief or Safety Valve" scenario.by initiation of a Safety Injection signal (due to steamline pressure) which initiates a' .
Reactor Trip signal. The~0vertemperature and Overpower Delta-T trip functions also provide Reactor protection in this scenario. j g,o= x.. . ..... cro i,.. 3m s., m m .
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d 5) The Unit would be protected against a " Steam System Piping Failure"-
J' scenario by initiation of a Safety Injection signal (due to steamline>
e' pressure) which initiates a Reactor Trip signal. The Overtemperature
[ and Overpower Delta-T trip functions also provide Reactor' protection =
D' in this scenario.
? 6) The " Uncontrolled Rod Cluster Control Assembly. Bank Withdrawal From a i Subcritical-~or. Low Power.Startup Condition" scenario,is not 2 applicable, as this. incident involved a load: follow power reduction:
~
(Unit runback). ,
1 7) The " Uncontrolled. Rod: Cluster: Control- Assembly Withdrawal at Power"~
i scenario is. assumed to be terminated by the following trip functions r^
in addition to the Power Range High Neutron Flux Trip Function (High:
- Setpoint): . 0vertemperature and'0verpower Delta-T, pressurizer
. pressure, and pressurizer level. In, addition to these trip functions, .
there are the following RCCA withdrawal blocks: '
[ a) high-neutron flux, b) Overtemperature Delta-T, and F c) Overpower Delta-T. For slow RCCA withdrawal accidents, i thermal-time constraints on the heatup do not become'al factor; the Unit is tripped and DNBR-is maintained above the limit.value. ' <
E
- 8) The " Spectrum of Rod Cluster Control Assembly Ejection Accidents" b scenario assumes credit for the High Neutron: Flux Rate. Trip Function.
! Furthermore, in any postulated rod withdrawal accident, the out-of-calibration L condition would have corrected itself during the transient-due to the absence of 1 the cause of the deviation, i.e., insertion of Control Bank D.~ Also, the I conservative effects of moderator and doppler feedback would tend to limit any
~
postulated power excursion.
The calibration problem was one of gain setting, or overall absolute value power indication. The ability of the NIS to detect axial flux difference (AFD) and- i high flux rate was unaffected. The Overtemperature Delta-T and the Overpower Delta-T Trip Function receives AFD as an input _to the setpoint equation, and the Overpower Delta-T Tr.ip Function is unaffected by neutron flux, .Therefore, the-high flux rate, Overtemperature Delta-T, and Overpower Delta-T Trip Functions ' - ;
remained intact and functional ~throughout this event. -The Overtempe'rature ,
Delta-T Trip function protects against DNB conditions, and the Overpower Delta-T I Trip Function ensures that allowable heat generation rate-(kw/ft)=is not
. exceeded.
The Unit 1 0-3 S/Gs utilize a ramped operating level based on NIS indication input to the feedwater control valve position. ~Hence, during this transient, it -1 is likely that the control system was " searching", causing oscillations in-ge *om un .u. . era, n,... w .,. m w a m .
^
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$ vsaa "n?.I'. #Jf.O 2 !
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0j 1 l6 0 l1 0l8 or 0 l8 1 itxt w- . = wme w asuu nn j feedwater flow and S/G level. For example, at the minimum achieved power level )
of 54% RTP (thermal best estimate), the feedwater control valves would have been-L throttling to maintain approximately 48% power based on NIS input. However, these oscillations were apparently minor, as S/G low-low level Reactor trip and. j 7
high-high level signals-did not occur.-
l .
\ .
F Addition' ally, power mismatch signal, based on the difference between Turbine I impulse pressure (correlative thermal power level) and NIS indication, is a control input to the Rod Control System program. However, this program does not utilize absolute power mismatch, but rather, rate of change of power. mismatch ;
(i.e., it is an anticipatory function). Therefore, the out-of-calibration-
- i condition of the NIS did not affect automatic rod control. j After recovery of the NIS from the out-of-calibration condition, core quadrant 2 1 Quadrant Power Tilt Ratio (QPTR) exceeded the value (1.02) allowed by Technical_
l Specifications (from 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> to 1150 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.37575e-4 months <br />). Because of fuel loading i patterns and other factors, one quadrant may see a higher burnup rate as '
compared to other quadrants. Upon RCCA insertion, the Xenon transient induced is in part related to burnup; it may also be driven by secondary side phenomena.
The indicated QPTR was perhaps slightly exacerbated _by the out-of-calibration
. condition of the NIS. However, for the most-part, the indicated quadrant power tilt was real and not merely indicate'd,-being driven by Xenon production /burnup ;
and other factors.
The QPTR Limiting Condition for Operation (LCO) states that thermal power must ,
be decreased at least 3% from RTP for each 1% of indicated QPTR in excess of 1 and that the Power Range Neutron Flux-High Trip Setpoints-must.be decreased i
!- similarly within the next four hours. This LC0 ensures that peaking factors j l (heat flux hot channel- factor and enthalpy rise hot channel factor) remain l l within permissible limits. The maximum value of QPTR measured was 1.0266, j
.approximately 3% in excess of 1 (one). Thus, the maximum permissible RTP during l l this period was 91%. Due to the Unit runback, power did not exceed j
, approximately 74% (thermal best estimate) during this period of time. Also,_
l since the QPTR was only in excess of 1.02 for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 50 minutes, the NIS adjustments were not required to be performed. Catawba Unit 1 was in compliance with the LCO. I The health and safety of the public were unaffected by this incident. 1 i
Neh4 ,CFOs 1980*520 589-60070 l