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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
Text
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Duke her Company . (803) 831 4 000 C &n
?+ . PO Box 2M '
[ : Civm. S C 29710.
f DUKEPOWER March 14:, .1990
& Document Control.DeskJ ~
J~ 1U. .
S. Nuclear Regulatory Commission
. Washington,..D. C. .
20555-Subj ect:-: ' Catawba Nuclear-St'ation Docket'No. 50-413
'LER 413/90-05, Rev. 1 ,
Gentlemen:
Attached is Licensee Event Report-413/90-05, Revision 1,'concerning '
TECHNICAL SPECIFICATION 3.0.3 ENTERED FOR INOPERABLE POWER RANGE !
NUCLEAR INSTRUMENTATION DURING UNIT SHUTDOWN DUE TO A MANAGEMENT DEFICIENCY .-
This.cVent'was considered to be of no significance with respect'to' the health and. safety of the public.
c.
t lVery truly yours,
[ b '
' Tony B. Owen- '
' Station Manager keb\LER-NRC.TBO
. 30 ' '
xc: .Mr..S. D. Ebneter American Nuclear Insurers
$@ Rsgional Administrator, Region II c/o Dottie Sherman, ANI Library Ao U. S. Nuclear Regulator Commission The Exchange, Suite 245 )
70bh 101 Marietta Street, NW, Suite 2900 270 Farmington Avenue 90 ' Atlanta, GA 30323 Farmington, CT 06032
' bg M & M Nuclear Consultants Mr. K. Jabbour ioo g' _1221 Avenues of the Americas U. S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation
.N< New' York, NY 10020
$x . Washington, D. C. 20555
~@@g INPO Records Center
- <) . Suite 1500 Mr. W. T. Orders 1100 Circle 75 Parkway NRC Resident Inspector Atlanta, GA 30339 Catawba Nuclear Station
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U.S. NUCLE 12 RE;ULOT AY COMMitBION '
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. Catawba Nuclear Station, Unit 1 o l5 l o 10 l 0 l4 l 1l 3 1 lOFl 0l 9
"'" Technical Specification 3.0.3 Entered For Inoperable Power Range Nuclear Instrumer ration Durinn Unit Shutdown Due To A Manacement Deficiency EVENT DATE tll LER NUMcER tel REPORT DATE (71 OTHER F ACILITl!$ INVOLVED les MONTH DAY TEAR YEAN 860v f AL tv , MONTH DAY Y[AR f ACILIT V NAMES DOCK!T NUM8ERI51 N/A 0l5l0l0l0l l l
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20 4064eH1Het 60.7 3te H2%) 60.731sH2Hal LICENSEE CONT ACT FOR THis LER till NIME TELEPHONE NUMBER ARE A CODE R.M. Glover, Compliance Manager 803 g 83i i 1l i3 ;2l3l6 COMPLETE ONE LINE FOR E ACH COMPONENT F AILURE DESCRIBED IN THl$ REPORT (136 M REPORTA Lt
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On January 26, 1990, at 1830 hours0.0212 days <br />0.508 hours <br />0.00303 weeks <br />6.96315e-4 months <br />, Catawba Unit 1 began to decrease power to start its end-of-cycle 4 refueling outage. At 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />, Technical Specification 3.0.3 was entered due to more than one power range nuclear
-instrumentation (PRNI) channel exceeding 5% deviation (non-conservative) between rated thermal power (RTP) and indicated excore detector power. Standing Work Request 4099 SWR was in progress at the time to calibrate the PRNI. Technical Specification 3.0.3 was exited at 2327 hours0.0269 days <br />0.646 hours <br />0.00385 weeks <br />8.854235e-4 months <br />, when calibration was completed on 3 of 4 channels. Deviations between RTP and PRNI indicated power are an expected occurrence during power changes; the operating procedure cautions Operators to initiate calibration as needed to prevent the deviation from exceeding 5%. This incident is attributed to a Management Deficiency in scheduling by not starting the calibration in time to avoid exceeding the limit.
Corrective actions will be developed to better anticipate and carry out PRNI calibration so as to avoid exceeding the deviation limit.
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- The purpose of the Excore Nuclear Instrumentation [EIIS:JG] (ENB) System is to monitor Reactor [EIIS:VSL] Core leakage neutron flux and generate appropriate i trips and alarms for various phases of Reactor operations. The three separate
/ overlapping ranges of Source Range, Intermediate Range, and Power Range also provide control functions and indicate Reactor status during Mode 2, Startup and Mode 1, Power Operation. Technical Specification 4.3.1.1 requires that channel calibration be performed' daily on the Power Range Neutron Flux High Setpoint.
This is to be performed by comparison of calorimetric (reactor thermal power best estimate, based on actual plant temperatures) to excore power (based upon nuclear power levels from excore instrumentation) when the Unit is above 15%
d Rated Thermal Power (RTP). Excore channel gains are to be adjusted to make
- indicated excore power consistent with indicated calorimetric power whenever this comparison reveals an absoluto difference of more than 2% between the two.
I Technical Specification 3.3.1, Table 3.3-1, requires that three out of four channels of Power Range Nuclear Instrumentation (PRNI) must be operable during i Modes 1 and 2.
During Mode 1, a power range channel must be considered INOPERABLE whenever a mismatch exists between calorimetric power and excore power indication that is greater than 5.0% in the non-conservative direction (calorimetric power greater than excore power). If the mismatch is between 2.0% and 5.0% in the non-conservative direction, the channel is OPERABLE as long as the calibration process has been initiated. When the Unit is engaged in a power maneuver which ,
results in a mismatch between calorimetric and excore power in excess of 2%, !
excore adjustment may be delayed until the Unit reaches a steady-state power level, provided the mismatch does not exceed 5.0% in the non-conservative direction, as specified by the Technical Specification Interpretation, dated ,
August 25, 1989.
Technical Specification 3.0.3 is required to be entered when the Unit is operating in a condition prohibited by Technical Specifications. This condition exists when a Limiting Condition for Operation is not met except as provided in the associated Action Requirements. It requires that within one hour action shall be initiated to place the Unit in a Mode in which the specification does i l not apply by placing it, as applicable, in: l
[' a. At least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,
- b. At least HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and
- c. At least COLD SHUTDOWN within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
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UCENSEE EVENT REPORT (LER) TEXT CONTINUATION Amovio oMe nomso-oio. !
9 , , EX?tRES. 8/31/88 9 ACIL617 feAM4 Of DOCKET NUMetR (2) LER NUMBER 16) PA04 (31 YEAM .
Catawba Nuclear Station, Unit 1 TEXT (# snore asem a segww, use espoonsi NRC Fe,m Js5NsH1M o l5 l0 lo lo l 4l113 910 -
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Ol 1 0l 3 OF O !9 EVENT DESCRIPTION i On' January 26, 1990, Catawba Unit 1 was in Mode 1, Power Operation, and initiated a controlled shutdown to begin its end-of-cycle 4 refueling outage.
~
Power decrease from 300% began at 1830 hours0.0212 days <br />0.508 hours <br />0.00303 weeks <br />6.96315e-4 months <br />, at a rate of 10% per hour. 1 Standing work request 4099 SWR was given to Instrumentation and Electrical (IAE)
Crew Supervisor A during the Shift Manager's meeting at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, to calibrate the Power Range Nuclear-Instrumentation (PRNI) to Rated Thermal Power (RTP).
This work activity was not on the IAE crew's schedule for the shift. At 2300 ,
1: bours, with the calibration in progress, two or more PRNI channels deviated from !
RTP by more than 5% in the non-conservative direction, placing Unit 1 into Technical Specification-3.0.3. The calibration continued and at 2327 hours0.0269 days <br />0.646 hours <br />0.00385 weeks <br />8.854235e-4 months <br />, 3 I channels of PRNI had been calibrated to agree with RTP; Unit 1 exited Technical ,
Specification 3.0.3 at that time. (
l Unit shutdown continued; IAE performed a second calibration before the 5% ;
deviation limit was exceeded. Unit 1 entered Mode 2, Startup, at 0414 hours0.00479 days <br />0.115 hours <br />6.845238e-4 weeks <br />1.57527e-4 months <br />, !
and Mode 3, Hot Standby, at 0440 hours0.00509 days <br />0.122 hours <br />7.275132e-4 weeks <br />1.6742e-4 months <br />, on January 27, 1990.
CONCLUSION l- Deviations between PRNI indicated power and RTP are an expected phenomenon i i during power changes. Control rod [EIIS:R00] insertion causes the PRNI excore l l detectors [EIIS:XT] to experience a greater decrease in neutron flux relative to the corresponding decrease in thermal power (i.e. " rod shadowing"). Recent !
analysis and interpretation of Technical Specification limits has determined that PRNI channels must be declared inoperable if they deviate (non-conservatively) from RTP by more than 5%. Deviations between 2% and 5% are )
permitted provided that the calibration process has been initiated. The i' relevant safety analyses assume a 2% deviation as an initial condition.
Provisions are made for IAE to perform the calibration via a preplanned, standing work request (SWR) to be issued by Operations; the need for calibration ,
is widely recognized. Operating procedure OP/1(2)/A/6100/03, Controlling Procedure for Unit Operation, contains a caution to initiate calibration as needed and states that Control Rod Bank D insertion will lead to PRNI-RTP deviation.
A significant amount of time is needed to prepare for this activity. Prior to beginning work, IAE Technician availability and qualification for the task must be verified, the work assigned, and the procedure reviewed. The calibration is begun by verifying a working copy of IP/1/A/3240/11, Calibration Procedure NIS Power Range Calibration At Power. Each channel is calibrated in turn using a separate enclosure to the procedure: the time required to complete the calibration can vary from one to two hours. In this event, the SWR was issued at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, the working copy was signed off as verified at 2205 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.390025e-4 months <br />, Technical Specification 3.0.3 was entered at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />, and calibration was completed at 2335 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.884675e-4 months <br /> (2 1/2 hours after initiation of the work activity).
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,j LICENSEE EVENT REPORT (LER) TEXT CONTINUATION - Arnovio on no me .
EXPlRES: 8'3 UNI -
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E A distinction can be drawn between planned power changes (i.e. shutdowns) and I: unplanned or rapid power changes (i.e. runbacks) with respect to the amount of time available to calibrate the PRNI prior to exceeding the 5% deviation limit.
I In the latter situation, a Unit may be decreasing power rapidly in order to '
avoid a more'significant event, e.g. a Unit trip ' In such circumstances s: PRNI-RTP deviations of greater than 5% could be unavoidable. But in the former
- b. case of planned power changes it should be possible to initiate and complete PRNI calibration without exceeding the limit.
This incident is attributed to a Management Deficiency, in that scheduling of j this work activity did not ensure that the limit would not be exceeded. A !
contributing Management Deficiency is also identified because, although the need i for PRNI calibration was identified, due to poor group interface action was not l initiated in time to avoid exceeding the limit. ;
l
- As previously planned (LER 413/89-025), an Operations procedure has been l developed and is being evaluated on the simulator to give Control Room Operators !
the recourse of adjusting PRNI channels (using gain adjustment) during power changes. .
1 Planning, scheduling, and conduct of PRNI calibration during power changes were !
discussed by Station Management at an " Abnormal Plant Event" meeting on February 28, 1990. Representatives-from affected station groups, Design Engineering, and other Duke stations participated. Crew expertise, time constraints, work priority and safety significance were discussed, as were alternative measures that can be taken to avoid exceeding the deviation limit. As a result of these !
discussions, the following corrective actions will be taken.
- Operations procedure OP/1(2)/A/6100/03-and its enclosure will be i revised to issue the SWR to IAE for PRNI calibration when a planned l power decrease begins (if a decrease of more than approximately 20% 1 l power is planned). l i
- IAE crews will receive training to emphasize the urgency of PRNI ;
calibration and the need for prompt completion of this activity.
l
- Possible ways to streamline the preparation for PRNI calibration will l be evaluated, including faster confirmation to Shift Managers and/or Shift Supervisors of the validity of current thermal power calculations.
- Emphasis will be placed on including the PRNI calibration activity in work schedules for planned power decreases. To facilitate this, PRNI calibration SWRs will be added to the Unit Trip and Forced Outage lists.
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- Discussion with cognizant Design Engineering personnel indicates that no-additional margin.is' available to relax the limitation further. Also, lower -l
' power accidents pose as significant a concern as higher power accidents and t,
hence relaxation at lower power levels is not viable. 1 I
( There have been three previous Technical Specification 3.0.3 events involving
.. inoperable PRNI' channels (LERs 413/89-025, 413/89-016, and 414/88-030).. LER A 413/89-025 involved.a rapid manual power reduction to prevent a Turbine (
[EIIS:TRB] and Reacto'r trip, which did not allow enough time for PRNI calibration before exceeding the 5% deviation limit. LER 413/89-016 involved a Turbine runback which did not allow enough time for PRNI calibr.ation. -LER
, 414/88-030 involved a planned power reduction where prompt action was not taken l' to calibrate the PRNI and was attributed to'a procedure deficiency. The
? procedure changes prompted by this event, to caution the Operators to anticipate R the need for PRNI calibration during power reduction, had been incorporated at
- the time of the current event..This is considered a recurring event. An
" Abnormal Plant Event" meeting will be held to discuss these events and determine any additional corrective action needed-to minimize recurrence.
CORRECTIVE ACTION l'
5UBSEQUENT
- 1) IAE calibrated all four PRNI channels within acceptable deviation.
PLANNED
- 1) A procedure has been developed and will be tested on the simulator to evaluate the feasibility of allowing Operations Control Room pe'rsonnel to adjust PRNI readings,-at the discretion of the Shift Supervisor, to agree with Rated Thermal Power.
- 2) Revise OP/1(2)/A/6100/03 and enclosure to issue SWR to IAE for PRNI i
calibration when power decrease begins (if a decrease of more than l
approximately 20% is planned).
L 3) IAE crews will receive training to emphasize the urgency of PRNI
[ calibration and need for prompt completion of this activity.
i ,
L 4) Evaluate possible ways to streamline the preparation for PRNI l calibration, including faster confirmation to Shift Managers and/or l Shift Supervisors of the validity of thermal power calculations.
[
l 5) To facilitate prior scheduling of PRNI calibration during planned shutdowns, Unit Trip and Forced Outage lists will be revised to include this work activity.
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@ . SAFETY ANALYSIS
[ 1 l- The excore power range neutron detectors are arranged and located such that one o detector measures core leakage neutron flux for one quadrant. Each detector and its associated circuitry comprise one channel, for a total of four PRNI
- channels. The Power Range High Neutron Flux Trip (High Setnoint) function utilizes a 2-out-of-4 logic.
Catawba Technical Specification 4.3.1.1 requires that channel calibration be performed daily on the Power Range Neutron Flux High Setpoint. This is to be performed by comparison of calorimetric (thermal best estimate) to excore power indication when the Unit is above 15% RTP. Excore channel gains are to be E adjusted to make indicated excore power consistent with indicated calorimetric power whenever this comparison reveals an absolute difference of more than 2%
between the two.
Based upon a Technical Specification Interpretation, during power maneuvers the operability requirements for the Nuclear Instrumentation System (NIS) channels are met provided.that the process of calibration has been initiated, and the total thermal best estimate and NIS mismatch does not exceed 5% in the non-conservative direction (i.e., thermal best estimate > NIS). The justification'for the increased allowable mismatch is based upon the existing margins-in the Steam Generator [EIIS:HX] (S/G) low-low level and power range high flux (high and low) setpoint calculations, power range response during specific transient analyses, and the conservatisms inherent in the Catawba FSAR analyses.
Bank D Rod Cluster Control Assemblies (RCCAs) are located in the core such that one RCCA is inserted in the middle of the core along the vertical axis, with one RCCA inserted in each.of the four quadrants (for a total of 5 RCCAs in Control Bank D). The RCCAs in Control Bank D are positioned more closely to the excore neutron detectors than other Control Bank RCCAs, and therefore affect the leakage neutron flux seen by these detectors to a greater degree than the other control banks. This phenomenon commonly occurs during power reductions in which Control Bank D is partially inserted.
The following is a list of Catawba FSAR Chapter 15 transients in which credit is assumed for the Power Range High Neutron Flux Trip (High Setpoint):
- 1) Startup of an Inactive Reactor Coolant Pump [EIIS:P] at an Incorrect Temperature (discussed in Section 15.4.4).
- 2) Feedwater System Malfunctions that Result in a Reduction in Feedwater Temperature (discussed in Section 15.1.1),
i
- 3) Excessive Increase in Secondary Steam Flow (discussed in Section l
15.1.3).
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< Taxi <n, - . o mcr.,. m m mi I 4) Inadvertent Opening of a Steam Generator Relief or Safety Valve Y
[EIIS:V] (discussed in Section 15.1.4).
k 5) Steam System Piping [EIIS: PSP] Failure,(discussed in Section 15.1.5).
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- 6) Uncontrolled Rod Cluster Control Assembly Bank Withdrawal From a Subcritical or Low Power Startup Condition (discussed in Section l 15.4.1).
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- 7) Uncontrolled Rod Cluster Control Assembly Bant Withdrawal at Power i (discussed in Section.15.4.2). j
' 8). Spectrum of' Rod Cluster Control Assembly Ejection Accidents (discussed-
. in Section 15.4.8).
4 i' The following discussion outlines the protective features which existed for the ;
above scenarios other than the Power Range High Neutron Flux Trip Function (High l Setpoint): ,
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- 1) The "Startup of an Inactive Reactor Coolant Pump at an Incorrect !
Temperature" scenario is not applicable and'the Abnormal Procedures do l not permit the Operators to start an inactive Reactor Coolant Pump i above 25% RTP.
n 2) The Unit would be protected against a "Feedwater System Malfunctions 1 that Result in a Reduction in Feedwater Temperatures " scenario by the- l Overtemperature and Overpower Delta-T trip functions. j
- 3) The Unit would be protected against the " Excessive Increase in Secondary Steam Flow" scenario by the Overtemperature and Overpower Delta-T trip functions.
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- 4) The Unit would be protected against the " Inadvertent Opening of a Steam Generator Relief or Safety Valve" scenario by initiation of a Safety Injection signal (due to steamline pressure) which initiates a Reactor Trip signal. The Overtemperature and Overpower Delta-T trip ,
functions also provide Reactor protection in this scenario. ;
- 5) The Unit would be protected against a " Steam System Piping Failure" scenario by initiation of a Safety Injection signal (due to steamline pressure) which. initiates a Reactor Trip signal. The Overtemperature and Overpower Delta-T trip functions also provide Reactor protection in this scenario.
- 6) The " Uncontrolled Rod Cluster Control Assembly Bank Withdrawal From a Subcritical or Low Power Startup Condition" scenario is not applicable as this incident involved a power reduction.
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% scenario.is-assumed to be terminated by the following trip functions )
in addition to the Power Range High Neutron' Flux' Trip Function (High l
?" Setpoint): Overtemperature and Overpower Delta-T, pressurizer i i pressure, and pressurizer level. In addition to these trip functions, y there are the following-RCCA withdrawal blocks:
h a) high neutron flux, b) Overtemperature Delta-T, and c);0verpower Delta-T. For slow RCCA withdrawal accidents, o thermal time constraints on the heatup do not become a factor; the plant'is. tripped and DNBR is maintained above the limit value.
f; 8) 'The_" Spectrum of Rod Cluster Control Assembly Ejection Accidents" scenario assumes credit for the High Neutron Flux Rate Trip Function.
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? Therefore,-in addition to the NIS being functionally able to provide input to 1
'. the SSPS, protection was provided against exceeding Reactor-related and other l NSSS Safety Limits by the above stated operable limiting safety system settings.
Furthermore, in 'any postulated rod withdrawal accidents, the out-of-calibration j condition would correct itself during the transient due to the absence of the w cause, i.e., insertion of Control Bank D. Also, the conservative effects of f moderator and doppler feedback would tend to omit any postulated power
, excursions.
The calibration problem was one of gain setting, or overall absolute value power L: indication. - The ability of the PRNI to detect axial flux difference (AFD) and high flux rate was unaffected. The Overtemperature Delta-T Trip Function
' receives AFD as an input to the setpoint equation, and the Overpower Delta-T Trip Function'is unaffected by neutron flux. Therefore, the high flux rate, Overtemperature Delta-T, and Overpower Delta-T Trip Functions remained intact and functional throughout the incident. The Overtemperature Delta-T Trip function protects against DNB conditions, and the Overpower Delta-T Trip Function ensures that allowable heat generation rate (kw/ft) is not exceeded.
The Unit 1 D-3 S/Gs utilize a ramped operating level based on NIS indication input to the Feedwater control valve position. Hence, during this transient, it is likely that the control system was " searching" causing oscillations in feedwater flow and S/G level (the control valves would attempt to control based on NIS indicated power, while actual' power is given by thermal best estimate).
However, these oscillations were apparently minor, as S/G Low-Low Level Reactor Trip, Signal and S/G High-High Level Reactor Trip Signal did not' occur.
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Additionally, Power Mismatch Signal, based on the difference between Turbine 7 impulse pressure (correlative _ thermal power level) and NIS indication, is a control input to the Rod Control System program. However, this program does not utilize absolute power mismatch, but rather rate of change of power mismatch l" (i.e., it is an anticipatory function). Therefore, the out-of-calibration condition of the NIS did not affect automatic rod control.
The health and safety of.the public were unaffected by this incident.
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