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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-10-04
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-10-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J1891999-10-0101 October 1999 Safety Evaluation Supporting Exemption from 10CFR54.17(c)re Schedule to Apply for Renewed Operating Licenses ML20212A6271999-09-30030 September 1999 Rev 0 to WCAP-15243, Anaylsis of Capsule V & Capsule Y Dosimeters from Duke Energy Catawba Unit 2 Reactor Vessel Radiation Surveillance Program ML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 05000413/LER-1999-015, :on 990616,discovered That Auxiliary Bldg Filtered Ventilation Exhaust Sys Was Inoperable.Caused by Improperly Positioned Vortex Damper.Damper Was Repositioned Correctly & Sys Was Retested Successfully1999-09-27027 September 1999
- on 990616,discovered That Auxiliary Bldg Filtered Ventilation Exhaust Sys Was Inoperable.Caused by Improperly Positioned Vortex Damper.Damper Was Repositioned Correctly & Sys Was Retested Successfully
05000414/LER-1999-004-01, :on 980906,error During Tagout Caused de-energization of Vital Bus & Actuation of Ltop.Caused by Inadequate Work Practices.Individuals Involved Were Counseled1999-09-27027 September 1999
- on 980906,error During Tagout Caused de-energization of Vital Bus & Actuation of Ltop.Caused by Inadequate Work Practices.Individuals Involved Were Counseled
ML20212G2511999-09-22022 September 1999 Safety Evaluation Supporting Amends 180 & 172 to Licenses NPF-35 & NPF-52,respectively 05000413/LER-1999-008, :on 990610,operations Prohibited by TS 3.5.2, Was Violated.Caused by Inoperable Centrifugal Charging Pump. Operators Swapped to CCP 1A & Sys Parameters Were Returned to Normal.With1999-09-21021 September 1999
- on 990610,operations Prohibited by TS 3.5.2, Was Violated.Caused by Inoperable Centrifugal Charging Pump. Operators Swapped to CCP 1A & Sys Parameters Were Returned to Normal.With
05000414/LER-1999-005-02, :on 990727,missed Emergency DG TS Surveillance Concerning Verification of Availability of Offsite Power Sources,Was Declared.Caused by Defective Procedure.Revised Affected Procedure1999-09-20020 September 1999
- on 990727,missed Emergency DG TS Surveillance Concerning Verification of Availability of Offsite Power Sources,Was Declared.Caused by Defective Procedure.Revised Affected Procedure
05000413/LER-1999-009, :on 990518,inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits Was Noted. Caused by Inadequate Retest Following Surveillance Test Failure.Valve Was Retested & Returned to Service1999-09-15015 September 1999
- on 990518,inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits Was Noted. Caused by Inadequate Retest Following Surveillance Test Failure.Valve Was Retested & Returned to Service
ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 05000414/LER-1999-004, :on 990616,CIV 2NM-221A Was Returned to Svc Without Testing,As Required by TS 3.6.3.Caused by Programmatic Deficiency.Test Procedure Has Been Revised & Subject Valve Was Successfully Tested & Returned to Svc1999-09-0101 September 1999
- on 990616,CIV 2NM-221A Was Returned to Svc Without Testing,As Required by TS 3.6.3.Caused by Programmatic Deficiency.Test Procedure Has Been Revised & Subject Valve Was Successfully Tested & Returned to Svc
05000413/LER-1999-014, :on 990816,missed Surveillances & Operation Prohibited by TS Was Noted.Caused by Defective Procedures or Programs Inappropriate TS Requirements.Affected Procedures/ Programs Were Revised & Testing Was Performed1999-09-0101 September 1999
- on 990816,missed Surveillances & Operation Prohibited by TS Was Noted.Caused by Defective Procedures or Programs Inappropriate TS Requirements.Affected Procedures/ Programs Were Revised & Testing Was Performed
ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 05000414/LER-1999-003, :on 990612,unplanned Actuation of ESFAS Occurred Due to a SG High Level.Caused by Inadequate Procedural Guidance.Msiv 2SM-7 Was Closed & SG 2A Level Was Returned to Normal1999-08-31031 August 1999
- on 990612,unplanned Actuation of ESFAS Occurred Due to a SG High Level.Caused by Inadequate Procedural Guidance.Msiv 2SM-7 Was Closed & SG 2A Level Was Returned to Normal
05000413/LER-1999-012, :on 990727,adverse Sys Interaction Between Annulus Ventilation Sys & Auxiliary Building Ventilation Sys Was Discovered.Caused by Inadequate Design.Compensatory Actions Developed & Implemented.With1999-08-26026 August 1999
- on 990727,adverse Sys Interaction Between Annulus Ventilation Sys & Auxiliary Building Ventilation Sys Was Discovered.Caused by Inadequate Design.Compensatory Actions Developed & Implemented.With
ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210U8341999-08-13013 August 1999 Safety Evaluation Supporting Amends 179 & 171 to Licenses NPF-35 & NPF-52,respectively ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 05000413/LER-1999-009, :on 990518,inoperability of Containment Valve Injection Water Sys Valve Was Noted in Excess of TS Limits. Caused by Inadequate Testing Following Surveillance Test Failure.Valve Was Retested & Restored to Service1999-07-19019 July 1999
- on 990518,inoperability of Containment Valve Injection Water Sys Valve Was Noted in Excess of TS Limits. Caused by Inadequate Testing Following Surveillance Test Failure.Valve Was Retested & Restored to Service
05000414/LER-1999-004-02, :on 990610,violation of TS 3.6.3 Was Noted Due to CIV 2NM-221A Being Returned to Service Without Testing. Caused by Procedure Deficiency.Civ 2NM-221A Was Tested & Returned to Operable Status1999-07-15015 July 1999
- on 990610,violation of TS 3.6.3 Was Noted Due to CIV 2NM-221A Being Returned to Service Without Testing. Caused by Procedure Deficiency.Civ 2NM-221A Was Tested & Returned to Operable Status
ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation 05000414/LER-1999-003-02, :on 990612,unplanned Actuation of Esfa Sys Due to a SG High Level Was Noted.Caused by Inadequate Procedural Guidance.Long Term Corrective Actions to Prevent Recurrence of Event Are Being Developed1999-07-0808 July 1999
- on 990612,unplanned Actuation of Esfa Sys Due to a SG High Level Was Noted.Caused by Inadequate Procedural Guidance.Long Term Corrective Actions to Prevent Recurrence of Event Are Being Developed
ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 05000414/LER-1999-002-03, :on 990504,plant Was Forced to Shutdown as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Affected Piping Was Cleaned & Flow Tested1999-06-0303 June 1999
- on 990504,plant Was Forced to Shutdown as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Affected Piping Was Cleaned & Flow Tested
ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions 05000413/LER-1999-004, :on 990310,operation Prohibited by TSs Was Noted.Caused by Incorrect TS Requirements for Cravs & Auxiliary Bldg Filtered Ventilation Exhaust Sys Actuation Instrumentation.Submitted Lar.With1999-04-12012 April 1999
- on 990310,operation Prohibited by TSs Was Noted.Caused by Incorrect TS Requirements for Cravs & Auxiliary Bldg Filtered Ventilation Exhaust Sys Actuation Instrumentation.Submitted Lar.With
ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205N2381999-04-0909 April 1999 Safety Evaluation Supporting Amends 178 & 170 to Licenses NPF-35 & NPF-52,respectively ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205B3101999-03-26026 March 1999 Safety Evaluation Supporting Amends 176 & 168 to Licenses NPF-35 & NPF-52,respectively 05000413/LER-1999-001-01, :on 990215,inoperable Refueling Water Storage Tank Level Channels Resulted in Operation Outside Design Basis.Caused by Inadequate Program Design.Reviewed Procedure & Communication Improvements Between Groups1999-03-17017 March 1999
- on 990215,inoperable Refueling Water Storage Tank Level Channels Resulted in Operation Outside Design Basis.Caused by Inadequate Program Design.Reviewed Procedure & Communication Improvements Between Groups
1999-09-07
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'D'ocument: Control Desk; f ,
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Subject:
?. Catawba 7 Nuclear-Station f
[' l Docket No'. 50-4141
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< , .LER'414/89-192 AGentiemen:l m
LAttachedEisiLicensee Event R nort 414/89-19,. concerning three
' iauxiliaryffeedwater pumpsfinoperable due to defective procedure and
' Linappropriate: actions.
2.
This e' vent was considered to be'of no significance with respect to the I- Jhealth and safetyLof,the public.
ry ;truly:. yours ,-
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-StationiManager;
- KEB\LER-NRC.TBO" xc
- *Mr. S. D. Ebneter- American Nuclear Insurers Regional Administrator, Region II c/o Dottie Sherman, ANI Library U -.S. Nuclear Regulator Commission The Exchange, Suite 245
' 2
.101 Marietta Streets NW, Suite 2900 270 Farmington Avenue Farmington, CT 06032
-Atlanta, GA 30323 t &'M Nuclear Consultants Mr. K. Jabbour U. S. Nuclear Regulatory Commission 1221' Avenues of the Americas Office of Nuclear Reactor Regulation
-New' York, NY 10020 Washington. D. C. 20555
[ LINPO Records ranter Suite 1500. Mr. W. T. Orders
-1100 circle 75 Parkway NRC Resident Inspector
. Atlanta, GA 30339 Catawba Nuclear Station ,
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SACILtTV teat #8 Hi DOCkti NUMet R 63. FAGEi3 Catawba Nucler.r Station , Unit 2 o l51010 l 0141114 1 loFl 015
"' Three Auxiliary Feedwater Pumps inoperable Due to Def ective Procedure and Inappropriate Actions -
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On September 12, 1989, at 1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br />, a control Room Operator (CRO) turned the Close-Auto Open switches for 2CA-15A (CA Pump 2A Suct From RN Isol Valve) and 2CA-18B (CA Pump 2B Suct frc-n RN Isol Valve) f rom the Auto position to the Close position. This action disabled the automatic opening capability of 2CA-15A and 2CA-18B, rendering Auxiliary Feedwater (CA) Pumps 2A and 2B inoperable. The CA Turbine Driven Pump was already inoperable, due to modification work in progress. The audible alarm for the 1.47 Bypass Panel was not heard when the switches were turned. The CRO subsequently noticed that the lights for "CA Train A Bypassed" and "CA Train B Bypassed" on the 1,47 Bypass Panel were lit.
'At 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br />, after reviewing the appropriate logic diagrams, the CR0 returned PT/2/A/4200/59, RN to CA suction Piping the switches to the Auto position.
Flush, has a step to " Ensure the following valves are closed", and lists 2CA-15A and 2CA-18B. Th.1- incident is attributable to a defective procedure, due to the intent of the st 9 ceing unclear, and to inappropriate actions, for placing both 2CA-15A and 2CA-186 in the Close position, and for turning down the volume level on the 1.47 Bypass Panel audible alarm. PT/2/A/4200/59 has been revised, and an Operator Update has been issued. Unit 2 was in Mode 1. Power Operation, at the time of this incident.
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BACKGROUND l
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The Auxiliary Feedwater [EIIStBA) (CA) System supplies feedwater flow to the .
- Steam Generators [EIIStHX] (S/Gs) in the event that Main Feedwater [EIISISJ) l (CF) flow is unavailable, and during Unit startup or shutdown. Upon loss of the i normal suction supplies to the CA Pumps [EIIStP), the suction automatically l aligns to the Nuclear Service Water [EIIS BI} (RN) System. A part of this i automatic alignment is the opening of CA-15A, CA Pump A Suct from RN Isol Valve, l and CA-18B, CA Pump B Suct from RN Isol Valve, which are normally closed in the L Auto position. This automatic opening capability can be defeated by placing the Control Room Close-Auto Open switches in the Close position.
i Technical Specification 3.7.1.2, Auxiliary Feedwater System, specifies that with thrae CA pumps inoperable, immediate corrective action must be taken to restore at least one CA pump to operable status ss soon as possible. The Technical l Specification Bases for the CA S;' stem state that it is to be capable of :
delivering at least 492 gpm at 1210 psig to at least two S/Gs.
The ESF Lypass Indication (EIIS:JE] (EMA) Syntem provides indication, on the 1.47 Bypass Panel, to Control Room Operators (CRos) when a train of any Safety Related System in inope.able. The EMA System provides operator awareness, to ,
ensure that equipment required to be operabic by Technical Specifications is not ,
inoperable. OP/2/B/6100/07E, Annunciator Response for 1.47 Bypass Panel, is provided to guide the Operators in consulting the appropriate Electrical Elementary diagrams to determine the cause of an alarm.
Operations Management Procedure (OMP) 1-4, Use of Procedures, Section 8.12, Constrained Language, states that " Terms which are commonly used in operating procedures generally have inherent meanings". The definition of " Ensure",
according to the Constrained Language List (OMP 4-1, Procedure Writing Guide, Enclosure 10.6) is to "Take necessary/ appropriate actions to guarantee component, reading, etc., is as specified". The definition of " Verify" on this '
list is to " Determine if in proper condition / status".
PT/2/A/4200/59 RN to CA Suction Piping Flush, is performed periodically to rer:ove Asiatic clams from the RN to CA suction piping. RN flow is established through the RN to CA pump suction piping to the Condenser Circulating Water
[EIIS SG) (RC) System. The Turbine Driven CA Pump (CAPT) is the only CA pump
, rendered inoperable by the performance of this procedure.
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EVENT DESCRIPTION On September 12, 1989, at 0740 hours0.00856 days <br />0.206 hours <br />0.00122 weeks <br />2.8157e-4 months <br />, with Unit 2 in Mode 1, Power Operation, the CAPT was declared inoperable for modification work on the steam inlet piping and turbine control valve [EIIS V) (see LEE 414/89-017). At 1255 hours0.0145 days <br />0.349 hours <br />0.00208 weeks <br />4.775275e-4 months <br />, Operations personnel began performing PT/2/A/4200/59, RN to CA System Piping Flush. Step 12.2.6 of this procedure states to " Ensure the following valves are s-
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ssx, - em . a.< , ,an.- w , mu y on closed" ar.d lists 2CA-15A and 2CA-18B. Both valves were indicating closed, and their Main Control Board switches were in the Auto position. To ensure that these valves _ remained in the closed position, at 1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br />, the CR0 turned their Close-Auto-Open switches from the Auto position to the Close position.
This action defeated the automatic opening capability of the valves, rendering CA Pumps 2A and 2B inoperable, and provided actuation inputs to the 1.47 Bypass Panel logic. 'The audible alarm for the panel did not sound during the incident.
'At approximately 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br />, the CR0 noticed that the Unit 2, 1,47 Bypass Panel lights for "CA Train A Bypassed" and "CA Train B Bypassed" were lit. Due to other ongoing activities in the Control Room, and the belief that other CA valve manipulations performed in the procedure may have caused these indications, the CR0 did not immediately investigate the cause of the panel lights. At approximately 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />, an NRC Resident Inspector also noticed the 1.47 Bypass '
Panel indications and consulted the CRO. The CR0 then reviewed the appropriate Electrical Elementary diagrams and found that placing the selector switches for 2CA-15A and 2CA-18B in the Close position would actuate the lights. The CR0 then returned the switches to the Auto position, at approximately 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br />, on September 13, at 0347 hours0.00402 days <br />0.0964 hours <br />5.737434e-4 weeks <br />1.320335e-4 months <br /> PT/2/A/4200/59 was completed. The modificat' work on the CAPT was compleced and the CAPT was restored to operable status by
- 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br />.
CONCLUSION This incident has been attributed to a defective procedure, due to the intent of step 12.2.6 not being clearly stated. The wording of this step was not in compliance with the Constrained Language List of OMP 4-1. The intent of this step was to verify that 2CA-15A and 2CA-18B were closed, using plant indications, not to place their selector switches in the Close position.
Changes have been incorporated into PT/1,2/A/4200/59, changing step 12.2.6 from
" Ensure the following valves" to "Vorify the following valves", and inserting a note before the step, stating that if CA is aligned for standby readiness, these switches are to remain in the Auto position. Operationa procedures will be reviewed to ensure compliance with OMP 4-1 with respect to switch manipulations.
This incident has also been attributed to an inappropriate action, for placing the selector switches for both 2CA-15A and 2CA18B in the Close position at the same time. This incident has been discussed with the CR0 involved, and an Operator Update has been issued, emphasizing the importance of considering the consequences of actions to be taken when performing a procedure. This update
, also emphasizes the importance of taking prompt action when lights are lit on the 1.47 Bypass Panel. Operator training will be enhanced to emphasize that placing these switches in the Close position defeats the RN to CA automatic swap capability, and renders the respective trains of CA inoperable.
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This incident has also been attributed to an inappropirate action, due to the audible alarm for the 1.47 Bypass Panel not sounding at the time of the incident. If an audible alarm had sounded when the switches were turned to the Close poaition, the CR0 voeld have known that this action was providing inputs to the panel. The audible alarm was checked under Work Request 2020 MES, and it was found that the volume had been turned down to a level which could not be heard by the CR0s. The time at which the volume was altered, and the activity responsible for it, have not been identified.
A review of the Operating Experience Program database showed no previous similar events within the past twelve months, in which both trains of CA were rendered inoperable due to a defective procedure.
CORRECTIVE ACTION SUBSEQUENT
- 1) The CR0 returned the Close-Auto open switches for 2CA-15A and 2CA-18B to Auto.
- 2) PT/1,2/A/4200/59 were revised to clarify their intent and to include a caution on positioning of the CA 15A and CA-18B switches.
- 3) The incident was discussed with the CR0 involved.
- 4) An Operator Update was issued, emphasizing the purpose of the Auto positioa of these switches, the importance of prior to performing a step in a procedure to consider the consequences of taking the l specified actions, and the importance of taking prompt action to l
determine the cause and take actions to correct the situation when 1.47 Bypass Panel lights are lit.
1
( 5) The volume for the Unit 2, 1.47 Bypass Panel audible alarm was I increased under Work Request 2020 MES, PLANNED
- 1) Operations procedures will be reviewed to determine if procedure changes are required to prevent an operator from rendering equipment inoperable in steps involving switches. ,
- 2) Operator training will be provided to emphasize that placing the Close-Auto-Open switches for CA-15A and CA-18B renders the respective trains of CA inoperable. ,
- 3) A review will be performed on the use of the 1.47 Bypass Panel to determine if additional training and system modification are required to make it more effectivo and usable for the Operator.
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rsus c a ,a, . m . - - n ce w n m SAFETY ANALYSIS The normal CA suction sources (CA Condensate Storage Tai. , Upper Curge Tanks and Hotwell) were available during this incident. In the event that an accident described in Chapter 15 of the FSAR occurred during the thirty-five minutes that I the switches were in the Close position, the motor driven CA pumps would have supplied the required flow to two S/Gs. The CR0 was fully aware that the switches were in the Close position, and would have had approximately thirty minutes to return them to Auto, if an accident occurred, before the normal suction sources were depleted. The probability of a seismic event of sufficient magnitude to render the normal CA suction sources inoperable, during the thirty-five minutes that the switches were in the Close position is low (on the order of 1.0E-08). Therefore, the health and safety of the public were not affected by this incident.
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