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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-10-04
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-10-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J1891999-10-0101 October 1999 Safety Evaluation Supporting Exemption from 10CFR54.17(c)re Schedule to Apply for Renewed Operating Licenses ML20212A6271999-09-30030 September 1999 Rev 0 to WCAP-15243, Anaylsis of Capsule V & Capsule Y Dosimeters from Duke Energy Catawba Unit 2 Reactor Vessel Radiation Surveillance Program ML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 05000413/LER-1999-015, :on 990616,discovered That Auxiliary Bldg Filtered Ventilation Exhaust Sys Was Inoperable.Caused by Improperly Positioned Vortex Damper.Damper Was Repositioned Correctly & Sys Was Retested Successfully1999-09-27027 September 1999
- on 990616,discovered That Auxiliary Bldg Filtered Ventilation Exhaust Sys Was Inoperable.Caused by Improperly Positioned Vortex Damper.Damper Was Repositioned Correctly & Sys Was Retested Successfully
05000414/LER-1999-004-01, :on 980906,error During Tagout Caused de-energization of Vital Bus & Actuation of Ltop.Caused by Inadequate Work Practices.Individuals Involved Were Counseled1999-09-27027 September 1999
- on 980906,error During Tagout Caused de-energization of Vital Bus & Actuation of Ltop.Caused by Inadequate Work Practices.Individuals Involved Were Counseled
ML20212G2511999-09-22022 September 1999 Safety Evaluation Supporting Amends 180 & 172 to Licenses NPF-35 & NPF-52,respectively 05000413/LER-1999-008, :on 990610,operations Prohibited by TS 3.5.2, Was Violated.Caused by Inoperable Centrifugal Charging Pump. Operators Swapped to CCP 1A & Sys Parameters Were Returned to Normal.With1999-09-21021 September 1999
- on 990610,operations Prohibited by TS 3.5.2, Was Violated.Caused by Inoperable Centrifugal Charging Pump. Operators Swapped to CCP 1A & Sys Parameters Were Returned to Normal.With
05000414/LER-1999-005-02, :on 990727,missed Emergency DG TS Surveillance Concerning Verification of Availability of Offsite Power Sources,Was Declared.Caused by Defective Procedure.Revised Affected Procedure1999-09-20020 September 1999
- on 990727,missed Emergency DG TS Surveillance Concerning Verification of Availability of Offsite Power Sources,Was Declared.Caused by Defective Procedure.Revised Affected Procedure
05000413/LER-1999-009, :on 990518,inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits Was Noted. Caused by Inadequate Retest Following Surveillance Test Failure.Valve Was Retested & Returned to Service1999-09-15015 September 1999
- on 990518,inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits Was Noted. Caused by Inadequate Retest Following Surveillance Test Failure.Valve Was Retested & Returned to Service
ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 05000414/LER-1999-004, :on 990616,CIV 2NM-221A Was Returned to Svc Without Testing,As Required by TS 3.6.3.Caused by Programmatic Deficiency.Test Procedure Has Been Revised & Subject Valve Was Successfully Tested & Returned to Svc1999-09-0101 September 1999
- on 990616,CIV 2NM-221A Was Returned to Svc Without Testing,As Required by TS 3.6.3.Caused by Programmatic Deficiency.Test Procedure Has Been Revised & Subject Valve Was Successfully Tested & Returned to Svc
05000413/LER-1999-014, :on 990816,missed Surveillances & Operation Prohibited by TS Was Noted.Caused by Defective Procedures or Programs Inappropriate TS Requirements.Affected Procedures/ Programs Were Revised & Testing Was Performed1999-09-0101 September 1999
- on 990816,missed Surveillances & Operation Prohibited by TS Was Noted.Caused by Defective Procedures or Programs Inappropriate TS Requirements.Affected Procedures/ Programs Were Revised & Testing Was Performed
ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 05000414/LER-1999-003, :on 990612,unplanned Actuation of ESFAS Occurred Due to a SG High Level.Caused by Inadequate Procedural Guidance.Msiv 2SM-7 Was Closed & SG 2A Level Was Returned to Normal1999-08-31031 August 1999
- on 990612,unplanned Actuation of ESFAS Occurred Due to a SG High Level.Caused by Inadequate Procedural Guidance.Msiv 2SM-7 Was Closed & SG 2A Level Was Returned to Normal
05000413/LER-1999-012, :on 990727,adverse Sys Interaction Between Annulus Ventilation Sys & Auxiliary Building Ventilation Sys Was Discovered.Caused by Inadequate Design.Compensatory Actions Developed & Implemented.With1999-08-26026 August 1999
- on 990727,adverse Sys Interaction Between Annulus Ventilation Sys & Auxiliary Building Ventilation Sys Was Discovered.Caused by Inadequate Design.Compensatory Actions Developed & Implemented.With
ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210U8341999-08-13013 August 1999 Safety Evaluation Supporting Amends 179 & 171 to Licenses NPF-35 & NPF-52,respectively ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 05000413/LER-1999-009, :on 990518,inoperability of Containment Valve Injection Water Sys Valve Was Noted in Excess of TS Limits. Caused by Inadequate Testing Following Surveillance Test Failure.Valve Was Retested & Restored to Service1999-07-19019 July 1999
- on 990518,inoperability of Containment Valve Injection Water Sys Valve Was Noted in Excess of TS Limits. Caused by Inadequate Testing Following Surveillance Test Failure.Valve Was Retested & Restored to Service
05000414/LER-1999-004-02, :on 990610,violation of TS 3.6.3 Was Noted Due to CIV 2NM-221A Being Returned to Service Without Testing. Caused by Procedure Deficiency.Civ 2NM-221A Was Tested & Returned to Operable Status1999-07-15015 July 1999
- on 990610,violation of TS 3.6.3 Was Noted Due to CIV 2NM-221A Being Returned to Service Without Testing. Caused by Procedure Deficiency.Civ 2NM-221A Was Tested & Returned to Operable Status
ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation 05000414/LER-1999-003-02, :on 990612,unplanned Actuation of Esfa Sys Due to a SG High Level Was Noted.Caused by Inadequate Procedural Guidance.Long Term Corrective Actions to Prevent Recurrence of Event Are Being Developed1999-07-0808 July 1999
- on 990612,unplanned Actuation of Esfa Sys Due to a SG High Level Was Noted.Caused by Inadequate Procedural Guidance.Long Term Corrective Actions to Prevent Recurrence of Event Are Being Developed
ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 05000414/LER-1999-002-03, :on 990504,plant Was Forced to Shutdown as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Affected Piping Was Cleaned & Flow Tested1999-06-0303 June 1999
- on 990504,plant Was Forced to Shutdown as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Affected Piping Was Cleaned & Flow Tested
ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions 05000413/LER-1999-004, :on 990310,operation Prohibited by TSs Was Noted.Caused by Incorrect TS Requirements for Cravs & Auxiliary Bldg Filtered Ventilation Exhaust Sys Actuation Instrumentation.Submitted Lar.With1999-04-12012 April 1999
- on 990310,operation Prohibited by TSs Was Noted.Caused by Incorrect TS Requirements for Cravs & Auxiliary Bldg Filtered Ventilation Exhaust Sys Actuation Instrumentation.Submitted Lar.With
ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205N2381999-04-0909 April 1999 Safety Evaluation Supporting Amends 178 & 170 to Licenses NPF-35 & NPF-52,respectively ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205B3101999-03-26026 March 1999 Safety Evaluation Supporting Amends 176 & 168 to Licenses NPF-35 & NPF-52,respectively 05000413/LER-1999-001-01, :on 990215,inoperable Refueling Water Storage Tank Level Channels Resulted in Operation Outside Design Basis.Caused by Inadequate Program Design.Reviewed Procedure & Communication Improvements Between Groups1999-03-17017 March 1999
- on 990215,inoperable Refueling Water Storage Tank Level Channels Resulted in Operation Outside Design Basis.Caused by Inadequate Program Design.Reviewed Procedure & Communication Improvements Between Groups
1999-09-07
[Table view] |
Text
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- October 19, 1989 ,
4 s - Document Control Desk U. S. Nuc1 car Regulatory Commission ,
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-' Washington, D. C. 20555
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Catawba Nuclear Station
Subject:
l- Docket No. 50-413 I
i LER 413/89-25
}
Gentlemen: ;
Attached isl Licensee Event Report 413/89-25, concerning Technical Specification 3.0.3'being entered on both units due to inoperable
- power range nuclear instrumentation resulting from a power reduction caused by the loss of cooling tower f ans during Hurricane.Hugo.
This event.was considered to be of no significance with respect to the .
health and safety of the public.
Very truly yours, .,
hh.. r Ton . Owen y Station Manager l keb\LER-NRC.TBO xc: Mr. S. D. Ebneter American Nuclear Insurers c/o Dettie Shermen, ANI Library Regional Administrator, Region II U. S. Nuclear Regulator Commission The Exchange, Suite 245 101 Marietta Street, NW, Suite 2900 270 Farmington Avenue l Atlanta, GA 30323 Farmington, CT 06032 1 M & M Nuclear Consultants Mr. K. Jabbour 1221 Avenues of the Americas U. S. Nuclear Regulatory Commission
(. New York, NY 10020 Office of Nuclear Reactor Regulation Washington, D. C. 20555 INPO Records Center Suite 1500 Mr. W. T. Orders 1100 Circle 75 Parkway NRC Resident Inspector Atlanta, GA 30339 Catawba Nuclear Station 8911060235 891020 PDR ADOCK 05000413e
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- Catawba Nuclear Station, Unit 1 015 l 010 l 0 l 411 13 1 l0Fl01 8 T'T'ta' Technical Specification 3.0.3 Entered On Both Units For Inoperable Power Range Nucle.ar Instrumentation Due To Power Reduction During llurricane Hugo EVf NT DAf t lli LER NUMBER (St REPORT DATE (71 OTHth ACILITits BWVOLVtD tel vtAR " $. Q ',* 6 "*j$ DAY vtAR S Aciuf v haMas DocntT hvMetRtli Mos 'T M Dav vtAR . MON 1H Catawba, Unit 2 0 1510l0]ol 411l4,
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- ness 06 On September 22, 1989, Units 1 and 2 were in Mode 1, Power Operati,on, at 100%
and 98% power, respectively. At 0547 hours0.00633 days <br />0.152 hours <br />9.044312e-4 weeks <br />2.081335e-4 months <br />, 1HTA, 13.8 KV Auxiliary Switchgear, deenergized resulting in the loss of power to the Condenser Circulating Water Cooling Tower Fans. This required the Operators to reduce Reactor power in order to maintain condenser vacuum. During the power reductions, Units 1 and 2 entered Technical Specification 3.0.3 at 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> and 0632 hours0.00731 days <br />0.176 hours <br />0.00104 weeks <br />2.40476e-4 months <br />, respectively, due to greater than 5 percent mismatch between Thermal Power Best Estimate and the Power Range Nuclear Instrumentation (PRNI). Following recalibration of the PRNIs, Units 1 and 2 exited Technical Specification 3.0.3 at 0655 hours0.00758 days <br />0.182 hours <br />0.00108 weeks <br />2.492275e-4 months <br /> and 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />, respectively. The PRNI mismatch is considered to be an expected phenomenon during a power reduction. The power reduction is attributed to unusual weather conditions caused by the high winds and rainfall delivered by Hurricane Hugo which caused water from the Service Building roof to leak on the 1HTA switchgear, thus tripping the switchgear. Although a subsequent inspection of the roof did not identify any defects, the roof is l I
scheduled to be reworked in the near future.
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- xt u, . - w w = nn BACKGROUND The purpose of the Excore Nuclear Instrumentation [EIIS:JG] (ENB) System is to monitor Reactor [EIIS:VSL] Core leakage neutron flux and generate appropriate trips and alarms for various phases of Reactor operations. The three separate overlapping ranges of Source Range, Intermediate Range, and Power Range also provide control functions and indicate Reactor status during Mode 2, Startup and Mode 1, Power Operation. Technical Specification 4.3.1.1 requires that channel calibration be performed daily on the Power Range Neutron Flux High Setpoint.
This is to be performed by comparison of calorimetric (reactor thermal power best estimate, based on actual plant indicator temperatures) to excore power (based upon nuclear power levels from detector instrumentation) when the Unit is above 15% Rated Thermal Power (RTp). Excore channel gains are to be adjusted to make indicated excore power consistent with indicated calorimetric power whenever this comparison reveals an absolute difference '
of more than 2% between the two.
Technical Specification 3.3.1, Table 3.3-1, requires that three out of four channels of Power Range Nuclear Instrumentation (PRNI) must be operable during Modes 1 and 2.
During Mode 1, a power range channel must be considered INOPERABLE whenever a mismatch exists between calorimetric power and excore power indication that is greater than 5.0% in the non-conservative direction (calorimetric power greater than excore power). If the mismatch is between 2.0% and 5.0% in the non-conservative direction, the channel is OPERABLE as long as the calibration process has been initiated. When the. Unit is engaged in a power maneuver which results in a mismatch between calorimetric and excore power in excess of 2%,
excore adjustment may be delayed until the Unit reaches a steady-state power level, provided the mismatch does not exceed 5.0% in the non-conservative direction, as specified by the Technical Specification Interpretation, dated June 2, 1989.
Technical Specification 3.0.3 is required to be entered when the Unit is .
operating in a condition prchibited by Technical Specifications. This condition exists when a Limiting Condition for Operation is not met except as provided in the associated Action Requirements. It requires that within one hour action shall be initiated to place the Unit in a Mode in which the specification does not apply by placing it, as applicable, in:
- a. At least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, l h. At least HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and
- c. At least COLD SHUTDOWN within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The Condenser Circulating Water [EIIS:SG] (RC) System is a closed loop system that removes rejected heat from the secondary steam cycle to maintain a vacuum l
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010 013 0F 0 18 nur w ~ . ~.,- ne r-, aw,nm on the main condenser [EIIS:SQ]. This rejected heat is transferred to the atmosphere through three mechanical draft cooling towers on each Unit. The cooling tower fans [EIIS:BLO] air powered from motor [EIIS:M0] control centers that are fed from 13.8 KV Auxiliary Switchgear [EIIS:EA] 1HTA and 2HTA. The 13.8 KV Auxiliary Switchgear is housed in the Service Building [EIIS:MF]. '
EVENT DESCRIPTION On September 22, 1989, Unit 1 and Unit 2 were in Mode 1, Power Operation, at 100% and 98% power, respectively. During this time, sustained winds of 42 miles per hour and heavy rainfall were experienced in the vicinity of the plant as a result of Hurricane Hugo. At 0426 hours0.00493 days <br />0.118 hours <br />7.043651e-4 weeks <br />1.62093e-4 months <br />, the Unit 1 Control Room Operators (CR0s) received a Main Condenser Low Vacuum Alarm and began to reduce power by 10% to maintain condenser vacuum. The low vacuum condition on Unit 1 was apparently caused by the warm moist air from the Unit 2 cooling towers being blown into the Unit I cooling towers by the high winds, thus reducing the efficiency of the Unit I cooling towers. At 0440 hours0.00509 days <br />0.122 hours <br />7.275132e-4 weeks <br />1.6742e-4 months <br />, the CR0s began securing the Auxiliary Building [EIIS:VF] and Fuel Building [EIIS:VG] ventilation systems and secured Containment Purge [EIIS:VA] on both Units as a precautionary measure for the adverse weather conditions per RP/0/A/5000/07, Natural Disaster and Earthquake.
At 0547 hours0.00633 days <br />0.152 hours <br />9.044312e-4 weeks <br />2.081335e-4 months <br />, the protective relaying [EIIS:RLY] on the 13.8 KV Auxiliary Switchgear deenergized the switchgear due to grounding of the primary disconnects in compartment 1HTA-2, Feeder to Auxiliary Boiler A. The grounding of the primary disconnect was caused by rain water leaking from the Service Building, roof into the switchgear compartment. The loss of power to the 1HTA buss resulted in the loss of power to the fans on Cooling Towers 1A and 2A.
Therefore, the CR0s commenced power reduction at 0547 hours0.00633 days <br />0.152 hours <br />9.044312e-4 weeks <br />2.081335e-4 months <br /> on Unit 1 and 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> on Unit 2 in order to maintain condenser vacuum.
At 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br />, Unit 1 entered Technical Specification 3.0.3 due to a greater than 5% mismatch between the Thermal Power Best Estimate and the PRNI on all four channels. Unit I was reduced to approximately 85% RTP at that time. At 0632 hours0.00731 days <br />0.176 hours <br />0.00104 weeks <br />2.40476e-4 months <br />, Unit 2 entered Technical Specification 3.0.3 due to 4 PRNI channels l
being inoperable while at approximately 85% RTP, At 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />, Unit 2 exited Technical Specification 3.0.3 after Instrumentatbn and Electrical (IAE) personnel recalibrated the PRNI channels per Stanting Work Request 5969 SWR. At 0655 hours0.00758 days <br />0.182 hours <br />0.00108 weeks <br />2.492275e-4 months <br />, the Unit 1 power reduction wa:, suspended at 30% RTP and Unit i exited Tecnnical Specification 3.0.3 after three of the PRNI channels were returned to operable status per Standing Work Request 4099 SWR. Unit 2 l.. continued power reduction and suspended power reduction at 30% RTP at 0746 hours0.00863 days <br />0.207 hours <br />0.00123 weeks <br />2.83853e-4 months <br />.
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010 0h 0F 013 After the discovery of the tripped 1HTA switchgear at 0547 hours0.00633 days <br />0.152 hours <br />9.044312e-4 weeks <br />2.081335e-4 months <br />, the Operators checked 2HTA and found water leaking onto the 2HTA switchgear. The decision was then made to reduce power to 30% RTP to allow fans to be removed from service on Unit 1 and Unit 2 Cooling Towers B and C. 2HTA was to be deenergized to install a temporary protective covering to redirect the leaking water away from the switchgear. A temporary protective covering was also installed on 1HTA. ,
At 0905 and 0915 hours0.0106 days <br />0.254 hours <br />0.00151 weeks <br />3.481575e-4 months <br />, respectively, Unit 1 and Unit 2 began power increase after 2HTA was energized and the B and C Cooling Tower fans were returned to service on each Unit. At 1020 hours0.0118 days <br />0.283 hours <br />0.00169 weeks <br />3.8811e-4 months <br />, Work Request 50047 OPS was written to '
repair 1HTA. By 1627 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.190735e-4 months <br />, faulted breaker 1HTA-2 had been removed and 1HTA was reenergied for checkout by the Transmission Department. By 1642 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.24781e-4 months <br />, the !
fans on Cooling Tower 1A had been restarted and Unit i recommenced power increase to 100% RTP. Unit 2 remained at 68% RTP until 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br />, on September 23, 1989 in order to remove storm related debris from the Condenser Circulating Water System before resuming power escalation to 98% RTP. . 1 i
CONCLUSION The entry into Technical Specification 3.0.3 followed the decrease in Reactor power that was necessitated by the need to maintain condenser vacuum after the loss of Cooling Tower Fans 1A and 2A. The mismatches on the PRNI channels are i an expected phenomenon during power changes and are normally recalibrated during load changes, or after the load increase or decrease is suspended.
The rapid load reduction on Unit 1 and Unit 2 was due to the trip of the 1HTA switchgear which was caused by rainwater leaking into compartment 1HTA-2 and .
grounding the primary disconnect. The rainwater leaked through the Service Building roof and was reported to be dripping off the ductwork above the 1MTA-2 breaker compartment. The exact location of the leak in the rooms housing 1HTA l and 2HTA has not been determined. Rainwater leaks have not previously been :
I reported in these rooms although they are normally locked and are not routinely surveyed by plant personnel. Faint streaking marks were observed on the west ;
i walls of the IHTA and 2HTA switchgear rooms and rainwater may have possibly leaked down the west wall onto the ductwork that penetrates the west wall. 'The l' i
west wall of the 1HTA and 2HTA switchgear rooms protrudes above the Service Building roof to provide a wall for the adjacent stairwell. The flashing on the l
stairwell wall appears to be intact with no obvious defects. The water may have been blown under the flashing by the abnormally high winds and high rainfall produced by Hurricane Hugo. It was also noted that a downspout for the stairwell roof directs drainage to the Service Building roof within one foot of the flashing. Water splashing from the downspout may have also contributed to this problem. The Service Building roof is currently scheduled to be replaced per Nuclear Station Modification CN50350 before the end of the year due to previous leaks that have occurred in other areas of the Service Building.
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.There have been two previous Technical Specificati on 3.0.3 events involving inoperable PRNI channels. However, these events did not involve the 1HTA or 2HTA switchgear, or roof leaks, therefore this is not a recurring event.
CORRECTIVE ACTION ,
IMMEDIATE
- 1) The CR0s began reducing Reactor power to maintain Main condenser vacuum.
SUBSEQUENT
- 1) Work Requests 4099 SWR and 59695WR were issued and the PRNI on Unit 1 '
and Unit 2 were recalibrated. ,
- 2) Temporary protective coverings were placed on 1HTA and 2HTA to.
redirect leakage.from the switchgear.
- 3) The Transmission Department removed the burned breaker from the 1HTA-2 compartment per Work Request 50047 OPS and 1HTA was raturned to ,
service.
- 4) Flashing on the Service Building roof was inspected.
PLANNED 1)' Breaker 1HTA-2 will be repaired per Work Request 50047 OPS. 7
- 2) The Service Building roof is scheduled for modification and replacement per NSM CN50350.
- 3) An Operations procedure is currently being developed and evaluated to possibly allow the Control Room Operators to adjust the PRNI channels while load changes are in progress. ,
- 4) The Safety Analysis will be revised if necessary after further review.
l SAFETY ANALYSIS The excore power range neutron detectors are arranged and located such that one detector measures core leakage neutron flux for one quadrant. Each detector and l its associated circuitry comprise one channel, for a total of four PRNI l channels. The Power Range High Neutron Flux Trip (High Setpoint) function utilizes a 2-out-of-4 logic. i 1
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010 0l 6 OF 0 l8 text c - . ., e ci = . m m Catawba Technical Specification 4.3.1.1 requires that channel calibration be performed daily on the Power Range Neutron Flux High Setpoint. This is to be performed by comparison of calorimetric (thermal best estimate) to excore power indication when the Unit is above 15%'RTP. Excore channel gains are to be ,
adjusted to make indicated excore power consistent with indicated calorimetric power whenever this comparison reveals an absolute difference of more than 2%
between the two.
Operability requirements of the PRNI channels are met provided the process of adjusting the excore channel (s) has been initiated and the mismatch does not exceed 5.0% in the non-conservative direction.
The basis for an allowable non-conservative mismatch of up to 5.0% is the application of Technical Specification 2.2.1. Operation with setpoints less conservative than the trip setpoint but within the allowable value is acceptable '
since an allowance has been made in the safety analysis to accommodate this error. An optional provision has been included for determining the operability of a channel when its trip setpoint is found to exceed the allowable value. The methodolgy of this option utilizes the as-measured deviation from the specified calibration point for rack and sensor [EIIS:XI] components in conjunction with a statistical combination of the other uncertainties of the instrumentation to measure the process variable and the uncertainties in calibrating the ,
instrumentation. ;
In Technical Specification Equation 2.2.1, Z + R + S $ TA, the interactive i effects of the errors in the rack and the sensor and the as-measured values are 1 considered. Z, as specified in Table 2.2-1 in percent span, is the statistical summation of errors assumed in the analysis excluding those associated' with the sensor and rack drift and the accuracy of their measurement. TA or Total Allowance is the difference in percent span, and R or Rack Error is the as-measured deviation, in percent span, for the affected channel from the specified trip setpoint. S or Sensor Error is either the as-measured deviation cf the sensor from its calibration point or the value specified in Table 2.2-1 in percent span, from the analysis assumptions. Use of Equation 2.2.1 allows j for a sensor drift factor, an increased rack drift factor, and provides a threshold value for reportable events, as described in the Bases of Technical i Specifications.
1 l The following is a list of Catawba FSAR Chapter 15 transients in which credit is assumed for the Power Range High Neutron Flux Trip (High Setpoint):
- 1) Startup of an Inactive Reactor Coolant Pump [EIIS:P] at an Incorrect Temperature (discussed in Section 15.4.4).
- 2) Feedwater System Malfunctions that Result in a Reduction in Feedwater Temperature (discussed in Section 15.1.1).
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- 3) Excessive Increase in Secondary Steam Flow (discussed in Section 15.1.3).
- 4) Inadvertent Opening of a Steam Generator. Relief of Safety Valve (discussed in Section 15.1.4).
- 5) Steam System Piping Failure (discussed in Section 15.1.5).
- 6) Uncontrolled Rod [EIIS:R003 Cluster Control Assembly Bank Withdrawal From a Suberitical or Low Power Startup Condition (discussed in Section 15.4.1).
- 7) Uncontrolled Rod Cluster Control Assembly Bank Withdrawal at Power (discussed in Section 15.4.2). !
- 8) Spectrum of Rod Cluster Control Assembly Ejection Accidents (discussed in Section 15.4.8).
The following discussion outlines the protective features which existed for the ;
above scenarios other than the Power Range High Neutron Flux Trip Function (High ,
Setpoint):
- 1) The "Startup of an Inactive Reactor Coolant Pump at an Incorrect Temperature" scenario is not applicable and the Abnormal Procedures do l not permit the Operators to start an inactive Reactor Ccolant Pump above 25% RTP.
2)' The Unit would be protected aga' inst a' "Feedwater System Malfunctions that Result in a Reduction in Feedwater Temperatures " scenario by the Overtemperature and Overpower Delta-T trip functions.
, 3) The Unit would be protected against the " Excessive Increase in '
Secondary Steam Flow" scenario by the Overtemperature and Overpower Delta-T trip functions.
- 4) The Unit would be protected against the " Inadvertent Opening of a ',
Steam Generator Relief or Safety Valve" scenario by initiation of a Safety Injectinn signal (due to steamline pressure) which initiates a Reactor Trip signal. The Overtemperature and Overpower Delta-T trip functions also provide Reactor protection in this scenario.
- 5) The Unit would be protected against a " Steam System Piping Failure" scenario by initiation of a Safety Injection signal (due to steamline pressure) which initiates a Reactor Trip signal. The Overtemperature and Overpower Delta-T trip functions also provide Reactor protection in this scenario.
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- 6) The " Uncontrolled Rod Cluster Control Assembly Bank Withdrawal From a Suberitical or Low Power Startup Condition" scenario is not applicable as this incident involved a load follow power reduction.
- 7) The " Uncontrolled Rod Cluster Control Assembly Withdrawal at Power" scenario is assumed to be terminated by the following trip functions in addition to the Power Range High Neutron Flux Trip Function (High Setpoint): Overtemperature and Overpower Delta-T, pressurizer pressure, and pressurizer level. In addition to these trip functions, there are the following RCCA withdrawal blocks:
a) high neutron flux, b) Overtemperature Delta-T, and c) Overpower Delta-T. For slow RCCA withdrawal accidents, thermal time constraints on the heatup do not become a factor; the plant is tr,ipped and DNBR is maintained above the limit value.
- 8) The " Spectrum of Rod Cluster Control Asse'nbly Ejection Accidents" scenario assumes credit for the High Neutron Flux Rate Trip Function.
The calibration problem was one of gain setting, or overall absolute value power indication. The ability of the PRNI to detect axial flux difference (AFD) and
.high flux rate was unaffected. The Overtemperature Delta-T Trip Function receives AFD as an input to the setpoint equation, and the Overpower Delta-T Trip Function is unaffected by neutron flux. Therefore, the high flux rate, Overtemperature Delta-T, and Overpower Delta-T Trip Functions remained intact and functiona' throughout the incident. The Overtemperature Delta-T Trip function protects against DNB conditions, and the Overpower Delta-T Trip Function ensures that allowable heat generation rate (kw/ft) is not exceeded.
1 i Based on the above analysis, it can be concluded that the Reactor was protected l at all times, and that no postulated :cenario could have occurred which would have challenged the Power Range High Neutron Flux Trip Function.
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Further review of the Safety Analysis will be performed.
l The health and safety of the public were unaffected by this incident.
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