|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:RO)
MONTHYEARML20024J2601994-10-0404 October 1994 LER 94-006-00:on 940913,automatic Reactor/Turbine Trip Occurred on Over Power Differential Temperature.Caused by Equipment Failure.Replaced Relay & Evaluated Failure Rate of Types of relays.W/941004 Ltr ML20029D1011994-04-20020 April 1994 LER 93-003-01:on 930925,reactor Tripped Due to Inadvertent Closure of Msiv.Caused by Inadequate Checking.Corrective Actions:Cros Throttled CA Flow & Entered Procedure EP/2/A/5000/01.W/940420 Ltr ML20046D5871993-08-17017 August 1993 LER 93-008-00:on 930718,reactor Tripped & Auxiliary Feedwater Sys Automatic Start Due to low-low-level in SG 1A. Developed General Troubleshooting procedure.W/930817 Ltr ML20045H2421993-07-12012 July 1993 LER 93-006-00:on 930612,automatic Reactor Trip Initiated by intermediate-range Channel N35 Hi Flux Reactor Trip Bistable.Caused by Blown Fuse in Channel.Entire Drawer Replaced & Channel Placed Back in svc.W/930712 Ltr ML20024G9751991-05-0909 May 1991 LER 91-004-00:on 910410,tech Spec Violation Occurred Re Containment Valve Injection Water Sys Being Inoperable. Caused by Inapropriate Action.Maint Staff Instructed Supervisors & Technicians of Correcting cause.W/910509 Ltr ML20024G7371991-04-18018 April 1991 LER 91-006-00:on 910323,nuclear Svc Water Valves Left W/O Emergency Power Supply.Caused by Inappropriate Action Due to Misreading of Operator Aid Computer (Oac) Graphics.Oac Graphics Training Will Be provided.W/910418 Ltr ML20029A3311991-02-12012 February 1991 LER 91-002-00:on 910113,reactor Exceeded 5% Power Level W/ RHR Sys Pump 1A Inoperable Due to Closed Suction Valve. Caused by Inappropriate Action & Procedural Deficiency. Incident Discussed W/Involved personnel.W/910212 Ltr ML20044B1761990-07-10010 July 1990 LER 90-013-00:on 900611,approx 5,000 Gallons of RCS Water Inadvertently Transferred to Refueling Water Storage Tank. Caused by Inappropriate Action.Proper Sys Parameters Restored & Analysis of Event performed.W/900709 Ltr ML20043G6441990-06-14014 June 1990 LER 90-008-00:on 900430,high Pressure CO2 Discharge Occurred on Auxiliary Feedwater Fire Protection Sys.Caused by Const/ Installation Deficiency in Solenoids.Solenoids Orientation Verified to Be Installed correctly.W/900614 Ltr ML20043C8951990-05-29029 May 1990 LER 89-010-01:on 880314,auxiliary Feedwater Pump 2A Discharge to Steam Generator 2A Isolation Failed to Completely Close.Caused by Design Deficiency.Mods to Actuator Torque Switch Setting increased.W/900524 Ltr ML20042G6301990-05-0909 May 1990 LER 90-025-00:on 900409,unexpected ESFs Actuation Occurred During Performance of Incore Thermocouple Testing.Caused by Deficient Procedure.Procedure Revised & Reviewed W/Personnel Lessons Learned from event.W/900503 Ltr ML20043A9271990-05-0303 May 1990 LER 89-030-01:on 890726,Tech Spec Violation Occurred Due to Shipment of Two Liners of Secondary Bead & Powdex Resin Mixture.On 891215,same Tech Spec Violation Occurred.Caused by Mgt Deficiency.Shipments suspended.W/900503 Ltr ML20042F4721990-05-0303 May 1990 LER 90-015-00:on 900402,Tech Spec 3.0.3 Entered When Both Trains of Containment Valve Injection Water Sys Rendered Inoperable.Caused by Supervisor Incorrectly Denoting Valve Position.Valves 1RN-493 & 494 closed.W/900430 Ltr ML20042F4741990-05-0303 May 1990 LER 90-006-00:on 900321,discovered That Nuclear Svc Water Sys Assured Makeup Source to Containment Valve Injection Water Sys Surge Chamber 2A Would Not Provide Adequate Flow. Caused by Clogged pipe.W/900430 Ltr ML20042E3141990-04-0303 April 1990 LER 90-002-01:on 900103,containment Air Return Fan Failed to Start During Test & Breaker FO1A in Motor Control Ctr Opened.Caused by Inappropriate Action.Measures Taken to Ensure Positions of Breakers verified.W/900409 Ltr ML20012C6881990-03-15015 March 1990 LER 90-011-00:on 900215,discovered That Control Room Doors Were More Difficult to Open than Normal.Ventilation Sys Found to Be Incapable of Maintaining Positive Pressure. Caused by Design Deficiency.Walls sealed.W/900315 Ltr ML20012C6901990-03-15015 March 1990 LER 90-005-01:on 900126,Tech Spec 3.0,3 Entered Due to More than One Power Range Nuclear Instrumentation Channel Exceeding 5% Deviation.Caused by Mgt Deficiency.Operations Procedure revised.W/900314 Ltr ML20012C3741990-03-13013 March 1990 LER 90-012-00:on 900127,central Alarm Station Operator Noted That Controlled Access Door Not Closed.Caused by Inappropriate Action Taken Which Was Unauthorized.Personnel Counseled on Importance of Sys operability.W/900313 Ltr ML20012C5091990-03-13013 March 1990 LER 90-009-00:on 900212,containment Purge Sys Heaters Not Being Verified to Be Running During Monthly Surveillance as Required by Tech Specs.Caused by Defective Procedures,Due to Incomplete Info.Procedures revised.W/900313 Ltr ML20012C5111990-03-12012 March 1990 LER 90-007-01:on 891108,discovered That Transmission Procedures Used to Perform Undervoltage Relay Tests Revealed That Test Acceptance Criteria Did Not Agree W/Tech Specs & Relays Not Being Adjusted as required.W/900316 Ltr ML20012B8121990-03-0909 March 1990 LER 90-008-00:on 900203,discovered That Insulation Removed from Main Steam Auxiliary Equipment Piping to Auxiliary Feedwater Pump Turbine.Caused by Design Oversight Due to Unanticipated Interaction of sys.W/900309 Ltr ML20012C4961990-03-0707 March 1990 LER 90-010-00:on 900205,discovered That Standby Shutdown Facility Wide Range RCS Temp Indications Had Not Been Subj to Monthly Channel Check as Required by Tech Spec 4.7.13.6. Caused by Defective procedure.W/900307 Ltr ML20012A1781990-02-27027 February 1990 LER 90-005-00:on 900126,Tech Spec 3.0.3 Entered Due to Inoperable Power Range Nuclear Instrumentation (Prni) During Unit Shutdown.Caused by Mgt Deficiency.Action Developed to Better Anticipate & Carry Out Prni calibr.W/900227 Ltr ML20006E8231990-02-14014 February 1990 LER 90-004-00:on 900104,contact Carrier Screws in nonsafety- Related Breaker Found Loose & in Bottom of Motor Control Ctr Cubicle.Caused by Mfg Deficiency.Loose Screws Secured. Part 21 related.W/900215 Ltr ML20006D4861990-02-0707 February 1990 LER 90-001-00:on 900105,unexpected Auxiliary Feedwater Automatic Startup Occurred During Periodic Cabinet Test. Caused by Procedure Deficiency.Procedures to Be Revised to Prevent recurrence.W/900207 Ltr ML20011E2281990-02-0202 February 1990 LER 90-002-00:on 900103,containment Air Return Fan 1B Failed to Start During Quarterly Test & Breaker F01A in Motor Control Ctr Discovered Open.Caused by Inappropriate Operator Action.Lockout Breakers closed.W/900202 Ltr ML20011E3951990-02-0202 February 1990 LER 90-001-00:on 891116,potential Concern Identified W/ Pressurizer Safety Valve Blowdown Being Greater than Assumed in Safety Analyses.Caused by Functional Design Deficiency. Also Reportable Per Part 21.W/900202 Ltr ML19354E0191990-01-19019 January 1990 LER 89-020-01:on 891118,Tech Spec 3.0.3 Entered & 5-month Auxiliary Bldg Ventilation Sys Inoperability Occurred as Result of Low Filter Exhaust Flow Condition on 891111.Caused by Design Oversight.Duct Will Be cleaned.W/900119 Ltr ML19354E0931990-01-18018 January 1990 LER 89-025-01:on 890922,power Lost to Condenser Circulating Water Cooling Tower Fans Due to Deenergization of 13.8 Kv Auxiliary Switchgear.Caused by Weather Conditions.Reactor Power Reduced to Maintain Condenser vacuum.W/900119 Ltr ML19354E0201990-01-18018 January 1990 LER 89-016-01:on 890913,generator 1B Power Circuit Breaker Opened,Causing Unit Runback to 54% Power & Failure of Generator Breaker Air Pressure Gauge.Caused by Equipment Failure.Pneumatic Gauge replaced.W/900117 Ltr ML19354D8261990-01-15015 January 1990 LER 89-029-00:on 891213,determined That Max Actuator Torque Switch Setting Insufficient to Overcome Friction Force Due to Age Hardening of Elastomeric Seat Matl on Bif/General Signal Corp Valve.Also Reported Per Part 21.W/900112 Ltr ML20005G4261990-01-12012 January 1990 LER 89-013-00:on 890726,two Carbon Steel Liners,Containing Mixture of Powdex & Bead Resins,Shipped to Barnwell,Sc,In Violation of Process Control Program.Caused by Mgt Deficiency.Shipment suspended.W/900112 Ltr ML20005G3061990-01-0909 January 1990 LER 89-020-00:on 890921,abnormal Degradation of Steel Containment Vessels Observed.Caused by Corrosion by Standing Water in Annulus Areas.Steel Containment Vessels Will Be Recoated During Next Refueling outage.W/900109 Ltr ML20005E4021989-12-29029 December 1989 LER 89-028-00:on 891204,steam Generator 1D Power Operated Relief Valve Did Not Close on Train a Main Steam Isolation Signal During Valve Inservice Test.Caused by Failed Fuse. Fuse replaced.W/891229 Ltr ML20011D3321989-12-20020 December 1989 LER 89-021-00:on 890821,hydrogen Skimmer Fan 2A Declared Inoperable in Order to Replace Breaker,In Response to NRC Bulletin 88-010.On 890825,breaker Tripped & Power Reduction Resumed.Caused by Inappropriate action.W/891222 Ltr ML20011D3351989-12-20020 December 1989 LER 89-027-00:on 891120,chemical & Vol Control Sys Centrifugal Charging Pump 1B Declared Inoperable Due to Inability to Maintain Sufficient Charging Flow.Cause Not determined.Power-range Detector replaced.W/891222 Ltr ML20011D2321989-12-18018 December 1989 LER 89-020-00:on 891111,low Filtered Exhaust Flow Discovered by Control Room Operators During Observation of Indications. Caused by Design Oversight Re Interaction of Sys/Components. Clothes Dryer Filters to Be modified.W/891218 Ltr ML19332E7201989-12-0606 December 1989 LER 89-023-01:on 890915,Tech Spec 3.0.3 Entered as Result of Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Equipment Malfunctions.Control Room & Area Pressurization Flow Rates revised.W/891120 Ltr ML19324B1141989-10-20020 October 1989 LER 89-024-00:on 890920,safety Review Group Staff Member Identified Committed Fire Door S102A as Possibly Inadequate. Caused by Design Deficiency.Fire Watch Established & Door repaired.W/891019 Ltr ML19324B4091989-10-20020 October 1989 LER 89-025-00:on 890922,13.8 Kv Auxiliary Switchgear Deenergized Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Power Reduction Due to Hurricane Hugo.W/891019 Ltr ML19325C6381989-10-11011 October 1989 LER 89-023-00:on 890915,Tech Spec 3.0.3 Entered Due to Both Trains of Control Room Area Ventilation Sys Being Inoperable.Caused by Defective pre-operational Testing Procedure.Train a Control Room Damper adjusted.W/891011 Ltr ML19325C6401989-10-11011 October 1989 LER 89-016-00:on 890913,four Channels of Power Range Instrumentation Showed Greater than 5% Allowable Mismatch Between Rated Thermal Power & Nuclear Power.Caused by Equipment Failure.Pneumatic Gauge replaced.W/891011 Ltr ML19325C6441989-10-11011 October 1989 LER 89-019-00:on 890912,capability of Switches 2CA-15A & 2CA-18B Disabled Rendering Feedwater Pumps 2A & 2B Inoperable.Caused by Defective Procedure & Inappropriate Actions.Procedure Revised & Update issued.W/891011 Ltr ML19325C1961989-10-0404 October 1989 LER 89-026-00:on 890823,tested Breaker Replaced W/Traceable Breaker in Response to Bulletin 88-010.Breaker Tripped. Caused by Mfg Deficiency.Work Request Written.Item Reportable Per Part 21.W/891003 Ltr ML19327B6071989-09-20020 September 1989 LER 89-025-00:on 890922,auxiliary Switchgear Deenergized, Resulting in Loss of Power to Condenser Circulating Water Cooling Tower Fans.Caused by Inoperable power-range Instrumentation Due to Hurricane Hugo.W/890920 Ltr ML17303B1821986-12-30030 December 1986 LER 86-058-01:on 861111 & 18,overtemp Delta T Reactor Trip Occurred on Increasing Reactor Coolant Temp Rate.Caused by Spike on Potentiometer.Valve Realigned & Unit Returned to Previous status.W/861230 Ltr 1994-04-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
Text
is
.a f\[l) ,. '\ [ '..
'I ;
b$' i
- h. p h ,
l:
g .
7'T; O , Duke hwir Cony <eny #'O###
- qh;p, v p .?
- f
,.w i Catiuba Nudear Station :-
_-f>0 Baryjg ;
- a. N % , * ,
Cimxr. S C.]9710 L iM- -
j ' 3
- DUKE POWER L
.y t
c, ! OctolserL11,c 198'9 W
&[
U."S.6 Nuclear Regulatory. Commission.
W l Washington,-D. C.. 20555' m
Subject:
Catawba' Nuclear Station Docket No. 50-413-
~
LER 413/89-16:
o : Gentlemen:-
4:- ' Attached-is Licensee Event Report 413/89-16, concerning Technical il . Specification.3.0.31being entered-due-to'four= channels of power-range-
[# -instrumentation being declared inoperable following unit runback as a>
' result of: failure:of a generator breaker air pressure gauge.
- u. ,
.}^'
This eveht was considered to be of no significance with respect to the
,- health!andTsafntyloffthe3public.
$ h ~~-
VeryWruly yours,:
'i l- .
Tony )Ouen' iStation' Manager
~ '
'KEB\LER-NRC.TBO., t American Nuclear Insurers b
'xc: :Mr. S. D. Ebheter c/o Dottie Sherman, ANI Library 1
Regional Administrator, Region II rU.'S. Nuclear' Regulator Commission The Exchange, Suite 245
-101~Marietta Street,-NW, Suite 2900 '270 Farmington Avenue y*
' ~
DAtlanta, GA 30323 Farmington, CT 06032 1 Y-M'& M Nuclear Consultants Mr. K. Jabbour 1 1 -
U. S. Nuclear Regulatory Commission
"'@ 1221' Avenues of the Americas New York, NY 10020 office of Nuclear Renctor Regulation '
Washington, D. C. 20555
=INPO Records Center Suite 1500'- Mr. W. T. orders 1100, Circle 75 Parkway NRC Resident Inspector Atlanta, GA 30339 Catawba Nuclear Station a
- t: .e G .8910170127 891011 T d W ,
fDRA ADOCK 05000413 PDC f
r f-
,., s f 'W
, , pena. 33s . U.S. LUCL11M E ElutATWY COMutsalose s.PPRO'/ED OMS NO 31E00104 5"3 8 8"O J.: .
LICENSEE EVENT REPORT (LER) e~ ~f i FACILlTY NAME 111 - DOCKET Nuh0St R 42) FAL*L G* ,
Ca'tawba' Nuclear' Station. Unit l- 0 l5 l 0 l0 l 0 l 4l 1 l3 1 lOFl Ol 7
"'Four Channels of- Power Raage Instrumentation Inoperable Following Unit Runback As A - ,
Reeult ~o f Failure of a Generator Breaker Air Pressure Gauge i i
SVENT DAff t$l Lim NunsetR ts: REPORT Daf t (71 - OTHER F ACitittt$ INVOLVED 101 -
DOCKE1 NUMetaisi (li MONTH DAY YEAR YEAR biU L ['5*$ MONTH DAY VtAR f aC3LsYv h4MES
~4 N/A 015 j 010 l 0 l ; j H
- Oj9 ; j '3 89 8l9 0l1y -
0j 0 1 l0 1l1 8l 9 o ,3 to,o,ni ,. ,
THis REPORT is susMIT150 PUR8uaNT 70 THE REoutREMENTs OF 10 CFR l- IC*eck eae or mere er rae ferie.. ass (11)
. OPE R ATING MOOT tel 20 402tti - 20 405tel to 73teH2Hevi 73.71the !
. 1 20 406taH1Hd 60 36teHit .- 50.731aH2Hvl 73.71tel no, . is o iO 20 0.i.inHo
= =, nti w n .H2H..
_ g3g,;.g74 20 4061eH1HeiH y 60.73tell2HJ $0.73teH2Hvadl Al J66AA
[ 20 406 tan 1H4vi 60.73taH2HW 90.73taH2HvehM56 to 406teH1H,6 ' 50.73teH2HWB 50.73tsH2 Hat LICENSEE CONTACT FOR TMtb $ER ttil NIME TELEPMONE NUMBER ARL A CQQi
- R.M. Glover. Compliance Manager 810 13 81 311 l- 131213 16
... COMPLETE ONE LINE FOR (ACM COMPONENT F AILuRE OrsCRISED IN TMil R$ PORT 1131 R ORfA E CAV58 SYSTEM COMPONENT "'NN'g AC- #0RfasLt '
C1U38 SYSTEM CovPCNENT MANy8 g g AC. pp pp 5 i X E lA - X l Il l- X1919 9' N I I I I I I I I 'l l- 1 I I I I I I I I I I SUPeLEMENT AL REPORT E MPECTED 114l MONTH DAY YEAR SU8 MISSION
'~] Yts n,,. c.y. excretic suewssioN od tri ] No 111 1 15 81 9 Aesn.ACT rum,e M mo an < e neo. -ere, surm one ma tvm-re osmo us, On September 13, 1989, at 0541 hours0.00626 days <br />0.15 hours <br />8.945106e-4 weeks <br />2.058505e-4 months <br />, Unit I was in Mode 1, 100% Power Operation. ' Generator 1B Power Circuit Breaker (PCB) opened causing Unit runback to 55% Power. Four out of four channels of Power Range Nuclear Instrumentation (PRNI) displayed greater than the 5% allowable mismatch between Rated Thermal Power (RTP) and Nuclear Power, in the non-conservative direction. At 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, Technical Specification 3.0.3 was entered and Work Request 4099 SWR was issued to complete calibration of the PRNIs. The Unit was stable at 55% Power at 0630 i
hours and the calibrations were performed. Following the required calibrations of'the PRNI, the Unit exited Technical Specification 3.0.3. The pneumatic gauge
- .
- was subsequently replaced, and Generator PCB 1B was restored to service. Unit
[ Power increases commenced at 1003 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.816415e-4 months <br /> on September 13, 1989. All required L PRNI calibrations were completed to within 2% of RTP by 1525 hours0.0177 days <br />0.424 hours <br />0.00252 weeks <br />5.802625e-4 months <br />. Unit Power reached 97% Power at'1815 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.906075e-4 months <br />. At 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, Unit Reactor Power reached 100%. The Power Range mismatch was considered to be an expected phenomenon following a Unit runback. This incident has been attributed to Equipment Failure due to the failure of the pressure gauge on the PCB which caused the
! Unit runback.
l k"aV'""'" _
Y H - '
I GP4C Poesn ageA
" ' ' U S. NUCLEIA E EIULATORY COMntlS$10N fa LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPxovEc ove No me-em
, EXPIRES. S/31/IB '
FACIUTY NAASE (Il . DOCKET I,UR*94R tal LER NUMSER 16) PAGE m vE*I " d?,u" -
S*.W
, C3ttwba Nuclear Station, Unit 1 ,
ftXT F mesa, ausse er escuset use adsuneast NRC ponn JEWas 117) 0 l5 l0 l0 l0 l4 l1 l 3 49 -
0l 1 l6 -
0l0 0l 2 OF 0l7
-BACKGROUND F
The purpose of the Out of Core Instrumentation [EIIS:JG} (ENB) System is to monitor Reactor [EIIS:VSL) Core leakage neutron flux and generate appropriate trips and alarms for various phases of Reactor [EIIS:VSL] operations. The three separate overlapping ranges of Source Range, Intermediate Range, and Power Range also provide control functions and indicate Reactor status during Mode 2, Startup and Mcde 1. Power Operation. Technical Specification 4.3.1.1 requires
-that channel calibration be performed daily on the Power Eange Neutron Flux High Setpoint. This is to be performed by comparison of calorimetric (reactor-thermal power best estimate, based on actual plant indicatar temperatures) to excore power (based upon nuclear power levels from detector instrumentation) indication when the Unit is above 15% Pated Thermal Power (RTP). Excore channel gains are to be adjusted to make indicated excore power consistent with indicated calorimetric power whenever this comparison reveals an absolute difference of more than 2% betueen the two.
Technical Specification ~3.3.1, Table 3.3-1, requires that three out of four channels of PRNI must be operable during Modes 1 and 2.
During-power operation, a power range channel must be considered INOPERABLE whenever a mismatch exists between calorimetric power and excore power indication that is greater than 5.0% in the non-conservative direction (calorimetric power greater than excore power). If the mismatch is between 2.0%
and 5.0% in the non-conservative direction, the channel is OPERABLE as long as the calibration process has been initiated. When the Unit is. engaged in a power maneuver which results in a mismatch between calorimetric and excore power in excess of 2%, excore adjustment may be delayed until the Unit reaches a steady state power level, provided the mismatch does not exceed 5.0% in the non-conservative direction, as specified by the Technical Specification
~ Interpretation, dated June 2, 1989.
Technical Specification 3.0.3 is required to be entered when the Unit is operating in a condition prohibited by Technical Specifications. This condition exists when a Limiting Condition for Operation is not met except as provided in the associated Action Requirements. It requires that within one hour action shall be initiated to place the Unit in a Mode in which the specification does not apply by placing it, as applicable, in:
- a. At least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,
- b. At least HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and
- c. At least COLD SHUTDOWN within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The Unit Main Power [EIIS:EA] (EPA) dystem's primary fanction is to generate and transmit power to Duke's Transmission System while simultaneously supplying the 6.9KV Normal Auxiliary Power [EIIS:EA] (EPB) System. If the generator I
. a n n.usv w, g- =~ .
, .- ^ - ~ ,
gggIC Poem 3Bea . .
U.S. NUCLEIN CElvt1 TONY COMMitSION fI UCENSEE EVENT REPORT (LER) TEXT CONTINUATION arraOvs0 OM8 NO 3150 0104 hf expints. sisic ,
h emoiuty name m Oocaat Numosa us ten Numeen tai Paos tai "aa -
" W W.'.' "n*.J CatwbaNuclbarStation, Unit 1 ^
5 0 l5 lo lo l0 l4 l1 l 3 49 -
0l1l6 ,0 l0 0l3 OF 0l7 TEXT M susse apsee is roommt, asas easesamt MC Form JEEd W tih
[EIIS: GEN] is out of service,.the EPA System is used to supply power from the ;
- Transmission System to the Unit Auxiliary Power System. The EPA System is divided into non-safety trains, connected to the 230KV switchyard through a step-up transformer [EIIS XFMR] and two power circuit' breakers [EIIStBRK] (PCBs) located in the switchyard. A generator breaker is provided on each train. The generator breaker r.nd step-up transformer combination on each train is capable -
- of carrying approximately fli'ty percent (750MVA) of the rated generator output.
EVENT DESCRIPTION On September 13, 1989, at 0541 hours0.00626 days <br />0.15 hours <br />8.945106e-4 weeks <br />2.058505e-4 months <br />, with Unit 1 at 100% Power Operation,
- Generator PCB 1B tripped open, causing an unexpected Unit runback. Operations entered AP/0/A/5500/03, Load Rejection. At 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, the PRNI versus Thermal Power (TP) was observed to be greater than 5% non-conservative on all four channels. Technical Specification 3.0.3 was entered at 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, and Work Request 4099 SWR was issued to direct the Instrumentaion and Electrical (IAE) section to calibrate the PRNI. The determination was made at 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br />, that Generator PCB 1B tripped on low air pressure as a result of a failed pressure gauge at the PCB, Phase X. Tha Unit was stablized at 55% Power at 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br />.
The Control Room Operator (CRO) exited Technical Specification 3.0.3 at 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />, due to the acceptable power mismatch on three of the four channels.
Operations determined that the failed pressure gauge would bn replaced by 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, by the Transmission Department; therefore, adjustament of the remaining power range channel per Technical Specifications was unnecessary as power escalation was expected to correct the mismatch problem.
Generator PCB IB was restored to service at 0952 hours0.011 days <br />0.264 hours <br />0.00157 weeks <br />3.62236e-4 months <br />, follcwing the replacement of the pneumatic pressure gauge. No problems were encountered following this action.
At 1003 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.816415e-4 months <br /> on September 13, 1989, Unit 1 Power increase began to establish
!. 100% Power Operation. . Power was increased from 55% at a rate of 10% per hour.
At 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br />,-Reactor power was at 90% and holding to perform Main Steam
[EIIS:SB]'(SM) System control valve [EIIS:V) movement tests and to complete final PRNI calibrations. All four channels of the PRNI registered Quadrant Power Tilt Ratios of less than 2%. The control valve movement test and PRNI calibrations were complete at 1525 hours0.0177 days <br />0.424 hours <br />0.00252 weeks <br />5.802625e-4 months <br />. Power increases continued to 100% at 3% per hour. Unit' power reached 97% thermal power at 1815 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.906075e-4 months <br /> and by 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />,:the Unit reached 100% Power Operation.
CONCLUSION l
This incident has been attributed to Equipment Failure. The pneumatic gauge, manufactured by Protais (France), normally displays a pressure of 500 lbf/sq.in, i
on Phase X, Y, and Z of the Generator B PCB. The failure of the gauge occurred l
at the connection of the bourdon tube and the linkage of the meter. The pneumatic pressure that resulted from the break of the soldered connection caused the gauge to be separated from its housing on the breaker. The immediate L
NTC FOKM 356A .8. CP0 198 3 - i D '8*
19 83;
GIRC Poem asea +
U.S. NUCLEM KliULATORY COMMIS&lON g' ,
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Aerrovio ous wrt aiso.oio4 execes sinic
- AC1Laty esaast tip DOCAET NUMB 4R 621 - atR NUMeth461 PAGE(31 vsaa "d?,P. -
'A*.,#
Cittwba Nuc1 car Station, Unit 1 o l5 lo lo lo l4 l1 l 3 49 -
0l1l6 -
0l0 0l4 OF 0 l7 TEXT M mese seco e amounod, var adelocaal MC hwm 30Ws/1171 s
drop in pressure caused the Generator 1B PCB to trip open. During the fourteen year use history of the Protais gauges, there have been no failures reported.
The mismatches reported on the PRNI channels after Unit power reduction were considered to be an expected phenonmenon. Within the past twelve months, one previous Problem Investigation Report (PIR) 2-C88-0335 was initiated as a result of entering Tech Spec 3.0.3 due to all four channels of PRNI being declared inoperable. This occurred during a power manuever of Unit 2 from 96% to 51% '
power._ All channels were inoperable due to the allowable non-conservative mismatch between calorimetric power and excore power. The cause of that incident was attributed to Defective Procedures. The procedure OP/2/A/6100/03, Controlling Procedure For Power Operation, did not contain a Caution or other
.information concerning the Power Range mismatch that normally occurs on a power decraase.__ The procedures for both Units were revised. A Technical Specification Interpretation revision was issued June 9, 1989. Since thin previous incident was not caused by Equipment Failure, the current incident is not- considered to be a recurring event.
The Protals gauge is not NPRDS reportable.
CORRECTIVE ACTION ,
SUBSEQUENT-
- 1) Work Request 4099 SWR was issued to recalibrate the PRNI.
- 2) The Protais pneumatic gauge was replaced for Generator 1B PCB.
- 3) Recalibration of PRNI was completed, per IP/1/A/3240/11.
PLANNED
- 1) The Protais pneumatic gauge will be sent to the Duke Power Standards Laboratory for failure analysis and testing.
- 2) Further review of the Safety Analysis of this Report will be performed and this report will be revised if necessary, following completion of Planned Item #1.
SAFETY ANALYSIS The excore power range neutron detectors are arranged and located such that one detector measures core leakage neutron flux for one quandrant. Each detector and its associated circuitry comprise one channel, for a total of four PRNI channels. The Power Range High Neutron Flux Trip (High Setpoint) function utilizes a 2-out-of-4 logic.
NIC 70AM 366A *1.$. Cror 19Aa-520- W W '-
, . . _ _ . _ _ _ _m.
A U.S. NUCLE A2 8.LIULATORY CoueAtO510N 01 00 pennEsta-'
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION trenovso ove No siso-oio.
p ,
DOCKET sevesBER (21 gen ,,yenggn (si txeimes. swa paog g3i I P406LITV seams its
" N vtAR "k%N,", ' -,E aP Cstiwba-Nuc1' ear-Station. Unit 1 Op 0F 0 l6 l0 l0 l0 l4 l1 l 3 49 -
Olll6 -
01 5 0 17 TONT W mese ansee a eseusev, use edessener 44C Fenn Jundw (1M -
Catawba Technical Specification 4.3.1.1 requires that-channel calibration be
. performed' daily on the Power Range Neutron Flux High Setpoint. This is to be.
, performed by comparison of calorimetric (thermal best estimate) to excore power indication when the Unit is above 15% kTP. Excore channel gains are to be adjusted to make indicated excore power consistent with indicated calorimetric power whenever-this comparison reveals an absoluto difference of more than 2%
between the two.
' Operability requirements'of the PRNI channels are met provided the process of-
-adjusting the excore channel (s) has been initiated and the mismatch does not exceed 5.0% in the non-conservative direction.
The basis for an allowable non-conservative mismatch of up to 5.0% is the application of Technical Specification 2.2.1. Operation with setpoints less conservative than the trip setpoint but within the allowable value sinceAnan allowance has been made in the safety analysis accomodate this error.
-optional provision has been included for determining the operability of aThe channel when its trip setpoint is found to exceed the allowable value.-
methododolgy of this option utilizes the as-measured deviation from the specified calibration point for rack and sensor [EIIS:XI] components in conjunction with a statistical combination of the other uncertainties of the instrumentation to measure the process variable and the uncertainties in calibrating the instrumentation.
In Technical Specification Equation 2.2.1, Z + R + S 1 TA, the interactive effects of the errors in the rack and the sensor and the as-measured values are considered. Z, as specified in Table 2.2-1 in percent span, is the statistical
. summation of errors assumed in the analysis excluding those associated with the sensor and rack drift and the accuracy of their measurement. TA or Total Allowance is the difference in percent span, and R or Rack Error is the
. as-measured deviation, in percent span, for the affected channel from the specified trip setpoint. S or Sensor Error is either the as-measured deviation of the sensor from its calibration point or the value specified in Table 2.2-1 in percent span, from the analysis assumptions. Use of Equation 2.2.1 allows for a sensor drift factor, an increased rack drift factor, and provides a threshold-value for reportable events, as described in the Bases of Technical Specifications.
The following is a list of Catawba FSAR Chapter 15 transients in which credit is assumed for the Power Range High Neutron Flux Trip (High Setpoint):
- 1) Startup c; an Inactive Reactor Coolant Pump [EIIS:P] at an Incorrect Temperati..e (discussed in Section 15.4.4),
. u cre, m . m e. - ,
a,ic 'oa" =^
~
"'~
4 guRCPere 308A .
- U.S. NUCLEM K60VLATORY CouMegei0et
~,
LICENSEE EVENT REPORT (LER) TEXT CONTINUATl3N '
s/
4 4 APP 70VE0 0Me No. 3150 4104 exPints: eraires
.j-PACtLITy asaast tu Dockii NUMSER 623 tta NUmstR tt) PA06 (31 4
ma "Mf.T -
"'a*.O E C:t:wba Nuclear Station ' Unit 1 ~
-i
% 0 l5 l0 l0 l0 l4 l1 l 3 ' fi 9 0l1l6 OF 0 l0' 0l6 0 l7 sexi wm ou.a aus am um.ww ec v. n anexanm F L2) Feedwater System Malfunctions that Result in a Reduction in Feedwater Temperature (discussed in Section'15.1.1). ;
~
-3)- Excessive Increase in Secondary Steam Flow (discussed in Section 15.1.3).
x -4) Inadvertant Opening'of a Steam Generator Relief of Safety Valve ,
(discussed in Section-15.1.4). ]4
, 5)- Steam System Piping Failure (discussed in Section 15.1.5).
- 6) . Uncontrolled Rod [EIIS: ROD) Cluster Control Assembly Bank Withdrawal- -
' From a Subcritical or Low Power Startup Condition (discussed in Section 15.4.1).
7)- Uncontrolled Rod Cluster Control Assembly Bank Withdrawal at Power
~
(discussed in Section 15.4.2).
- 8) Spectrum of Rod Cluster Control Assembly Ejection Accidents (discussed in Section 15.4.8).
The following discussion outlines the protective features which existed for the above scenarios other than the Power Range High Neutron Flux Trip Function (High Setpoint): ,
.' -1) The "Startup of an Inactive Reactor Coolant Pump at an Incorrect Temperature" scenario is not applicable and the 55% Power level was above the P-8 interlock. All four Reactor Coolant loops were in operation during this incident.
2)~ The Unit would be protected against a "Feedwater System Malfunctions that Result in a Reduction in Feedwater Temperatures " scenario by the Overtemperature and Overpower Delta-T trip functions.
,o 3)' The Unit would be protected against the " Excessive Increase in i Secondary Steam Flow" scenario by the Overtemperature and Overpower Delta-T trip functions.
- 4) The Unit would be protected against the " Inadvertent Opening of a Steam Generator Relief or Safety Valve" scenario by initiation of a Safety Injection signal (due to steamline pressure) which initiates a Reactor Trip signal. The Overtempcrature and Overpower Delta-T trip functions also provide Reactor protection in this scenario.
=xc roau m .u... ,, im.m.m m
m ,
p e a sec fenn any , . . . v.s. NOCLEJ.R f.tOULf. Tony Co.eMISSloN T! ' B ' LICENSEE EVENT REPORT (LER) TEXT CONTINUATION s.erzovso ove wo siso.oio4 i@* .
_ , ;s expiacs; e/ sic D mm n, oocm.nv .. ., t , ,,v . , ,,r ,,,, ,,
viaa "Et.W '
an".?:
b C tcwba' Nuclear Station,' Unit 1 '
0 l5 l0 l0 l0 l4 l1 l 3 49 -
0l1l6 -
0l0 g7 or 0 l7 ;
T33tT M mese anses 4 auguted, see esweens/ Nec #enn 334 W 07)
- 5) 'The Unit would'be protected against a " Steam System Piping Failure" b scenario by initiation of a Safety Injection signal (due to steamline pressure) which initiates a Reactor Trip signal.. The Overtemperature
[ ',
and Overpower Delta-T trip functions'also provide Reactor protection L in this scenario, p
l6) The " Uncontrolled Rod Cluster Control Assembly Bank Withdrawal From a l Suberitical or Low Power Startup Condition" scenario is not applicable i
.as this incident involved a load follow power reduction. ;
l i,
7)- .The " Uncontrolled Rod Cluster Control Assembly Withdrawal at Power" I scenario is assumed to be terminated by the following trip. functions - '
' -in addition to the Power Range High Neutron Flux Trip Function (High
- .Setpoint): Overtemperature.and Overpower Delta-T, pressurizer pressure, and pressurizer level. In addition to these trip functions, ;
there are the following RCCA withdrawal blocks: i l
a) high neutron flux, b) Overtemperature Delta-T,'and c) Overpower Delta-T. For slow RCCA withdrawal accidents, thermal' time constraints on the heatup do not become a factor; the l
' plant is tripped and DNBR is maintained above the limit value.
8)~ The " Spectrum of Rod Cluster Control Assembly Ejection Accidents" scenario' assumes credit for the High Neutron Flux Rate Trip Function.
'The calibration problem was one of gain setting, or overall absolute value power .1
-indication. The ability of the'PRNI to detect-axial flux difference (AFD) and 1 ihigh flux rate was unaffected. The Overtemperature Delta-T Trip Function
- -receives AFD as an-input to the setpoint equation, and the Overpower Delta-T Trip Function is unaffected-by neutron flux. Therefore, the high flux rate, Overtemperature Delta-T,.and Overpower Delta-T Trip Functions remained intact and' functional throughout the incident. The Overtemperature Delta-T Trip function protects against DNB conditions, and the Overpower Delta-T Trip L ' Function ensures that allowable heat generation rate (kw/ft) is not exceeded.
Based on the above analysis,.it can be concluded that the Reactor was protected
.at all' times, and that no postulated scenario could have occurred which would
.have challenged the Power Range High Neutron Flux Trip Function.
B 1
Further' review of this Safety Analysis will be performed.
i; l- The health and safety of the public were unaffected by this incident.
NRC POAM 366a .,j,y y 9, , y , ,,s.
- 49 SL