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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
[Table view] |
Text
REGULATORY I RMATION DISTRIBUTION SYS (RIDS)
ACCESSION NBR: 8707020316 DOC. DATE: 87/06/2'7 NOTARIZED: NO DOCKET FACIL 50 250 Turkey Point Planti Unit 3i Florida Power and Light C 05000250 AUTH. NAME AUTHOR AFFILIATION HARTi R. D. Florida Paver 8. Light Co.
WOODY'. O. Florida Poeer 8. Light Co.
REC IP. NAME RECIPIENT AFFILIATION
SUBJECT:
LER 87-017-00: on 8705287 5 0603 normal h emergency boration floe paths were lost. Caused bg damaged inboard mechanical seal on 4B boric acid transfer pumps. Mechanical seal repaired. W/870626 ltr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR TITLE: 50. 73 Licensee Event Repor t (LER) Incident Rpti
+ ENCL / SIZE:
etc.
NOTES:
I REC IP IENT COP IES REC IP IENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 PD2-2 PD 1 1 McDONALDi D 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TP*B 1 1 DEDRO 1 NRR/DEST/*DE 0 NRR/DEST/ADS 1 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1 NRR/DEST/ I CSB 1 1 NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 1 NRR/DEST/PSB 1 1 NRR/DEST/RSB 1 1 NRR/DEST/SGB 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 NRR/DOEA/EAB 1 1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 2 N AS./ LRB 1 NRR/PMAS/PTSB 1 EQ L 02 1 1 RES DEPY QI 1 1 RES TELFORDi J 1 1 RES/DE/EIB 1 1 RQN2 - FILE 01 1 1 EXTERNAL: EGhG GROHi M 5 5 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 NSIC HARRIS' 1 1 NSIC MAYST Q 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 44 ENCL 42
~ v NRC Form 366 .o. NUCLEAR AEGULATOAYCOMMISSION (9.43)
APPROVED OMB NO,3150410(
LICENSEE EVENT REPORT {LER) EXPIAES: 4/31/44 FACILITY NAME (I) DOCKET NUMBER (2) PAGE 3I Turkey Point Unit 3 2 5 0 0 5 0 0 0 1 OF 0 5 Loss of Boric Aci owpat ue to a2. e ec an2.ca ea S.c owe 2. rogen to Enter and Bind Up the Pumps FVENT DATE IS) LEA NUMBER (6) REPORT DATE LTI OTHER FACILITIES INVOLVED (4)
SEQVENTIAL REVISION OAY YEAR FACILITY NAMES OOCKFT NUMBER(S)
MONTH OAY YEAR YEAR NUMBER NUMBER MONTH Turke Point Unit 4 0 5 0 0 0 2 5 I 5 8 8 7 8 7 017 0 0 6 2 9 8 7 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUANT T 0 THE REGUIREMENTS OF 10 CFR (): IChrce onr or morr of thr fotrowrnpt (11 OPERATING MODE (1) 6 20.402(III 20A05(cl 50.73(e)(2)Bvl 73.71IIII POWER 20A05( ~ l(1)(il 50.36(cl I I I 50.73( ~ )(2)(v) 73.71(cl LEvEL 0 0 0 20A05(e) ill(ii) 50.36(c) (2) 50.73(el(2)(mi) DTHER Isprcify in Aottrrct Orrow rnd in Test, Ht)C Form 20A06( ~ ) (1)(i51 50.73( ~ ) (2) lil 50.73(el(21(viii) (A) 366A1 20A05(e) (1)(iv) 50.73( ~ ) LT I Iii) 50.73(el(2l(viiil(BI 20.C05(e) Ill(v) E0.73(e) (21(i(I) 50.73( ~ l(2)lel LICENSEE CON'TACT FOR THIS LEA (12)
NAME TELEPHONE NUMBER 305 246 -6559 AREA CODE Randall D. Hart, Licensing Engineer COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCAIBEO IN THIS REPORT (131 MANVFAC. REPORTABLE COMPONENT MANVFAC. EPORTABLE CAUSE SYSTEM COMPONEtvT TO NPAOS CAVSE SYSTEM TVREA TURER TO NPRDS BSEAL D272N SUPPLEMENTAL REPORT FXPECTED Ilel MONTI~ OAY YEAR EXPECTED SUBMISSION DATE (15(
YES Iif vrL comPirrr FXPECTFO SUShttSSIOH OATFI NO ABSTRACT ILimit to tr00 tpecrt. i.r., rpprovimerHy fifteen tinpie toter tyorwnttrn lirnl (Id)
On May 28, 1987, the normal and emergency boration flow paths were lost on Unit 4 which exceeded the requirements of Technical Specification (TS) 3.6.a. An alternate flow path was established later and trouble-shooting was commenced on the initial problem. On May 29, 1987, thethis normal and emergency boration flow paths for Unit 3 were lost. At time CORE ALTERATIONS were halted on Unit 3 until a boration flow path was re-established within 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Trouble shooting of the problem was begun and additional attempts were made on June 1 and 2 to establish a
boric acid flow path from the Unit 4 BATPs which were unsuccessful.
On June 3, 1987, the normal and emergency boration flow paths were again lost on Unit 3. An investigation into the cause of these events discovered that a mechnical seal was damaged on the 4B boric acid transfer pump which allowed a nitrogen cover gas on the cooling water for the seal to enter the pump causing it to be gas bound. The Unit 3 and Unit 4 boric acid systems were cross-tied during these events which allowed theiso-nitrogen from Unit 4 to enter the Unit 3 pumps. The 4B pump controls was lated and the mechanical seal was repaired. Administrative were established to isolate the nitrogen supply and regulate its use.
A training brief has been issued describing this event and the procedure changes that have resulted.
yg.
87070 (BIDOCI{, 0316 8 70629 PDR 05 000~50 pDR NRC Form 3d6 r983r S
NRC Form 3ddA U.S. NUCLEAR REGULATORY COMMISSION (943 I LICENSEE EVENT REPORT (LER) TEXT CONTINuATION APPROV EO 0MB NO. 3150W104 EXPIRES: 9/31/88 o FACILITY NAME I'l OOCKET NUMBER (2(
LER NUMBER (dl PAGE (3I YEAR pRB< sdGUENTrAL Nii'rsvrsro4 oo?. 4UMSSR .. 3 4UMddrr Turkey Point Unit 3 0 s o 0 0 2 5 0 8 7 017 0 0 0 2 OF 0 5 TEXT /lfmoro o/rooo io for/rrdod. o>> odd ir/rrro/iVRC Form 3dr/O'/ ((7)
EVENT:
On May 28, 1987, while unit 4 was in mode 5 (cold shutdown), the normal and emergency boric acid flow path required by Technical Specification (TS) 3.6.a were lost. At 2100, an attempt was made to add water to the Unit 4 volume control tank (VCT) from the 4A and 4B boric acid transfer pumps (BATPs) through the normal and emergency flow paths. The operators did not obtain any flow indication and attempted to obtain flow from the refueling water storage tank (RWST), but this was not successful either. At this time the 3B BATP was operable and aligned to Unit 3. The boric acid system is designed such that both unit s BATPs can be aligned to either unit. At 2208, the 3B BATP was also aligned to Unit 4 and a flow path for boron injection was verified to unit 4.
A charging pump was vented and a flow path from the RWST was verified. The 4A and 4B BATPs were declared out of service and plant work orders were written to have them repaired.
At 0145 on May 29, 1987, Operations attempted to add borated water to the reactor coolant system (RCS), but they were unable to obtain any flow. At this time the 38 BATP had been aligned to the C boric acid storage tank (BAST). This had been done during trouble shooting of the earlier problems on the 4A and 4B BATPs. These pumps had been aligned to the C BAST when they had developed flow problems. The 3B BATP was realigned to the B BAST, however, no indication of flow could be obtained. At 0230, CORE ALTERATIONS were halted on Unit 3. At 0535, a boration flow path was established for unit 3 from the 3B BATP. At this time, it was thought that a loss of suction occurred to the 3B BATP because it was aligned to the C BAST. PWO s were written to the mechanical and electrical maintenance departments to check heat tracing circuits and possible flow path blockage on the C BAST outlet line.
At 0330 on June 1, 1987, Operations attempted to establish boric acid flow to Unit 4 from the 4A and 4B BATPs but was unsuccessful. A boration flow path from the Unit 4 RWST was verified via control valve (CV) CV-4-115B. A boric acid flow path for Unit 3 was verified from the B BAST via the 3B BATP.
Trouble shooting of heat tracing circuits continued. As a result of this trouble shooting, at 0130 on June 2, 1987, the 4A BATP suction was aligned to the batch tank and the pump discharge to the C BAST but the Operators were not able to obtain any flow. Then the 4B BATP suction was aligned to the batch tank and the pump discharge to the C BAST but again not flow was obtained.
Trouble shooting was continued.
At 0158 on June 3, 1987, Operations attempted to establish a boric acid flow path with the 4B BATP from the C BAST but were unable to obtain flow. At 0215, an attempt was made to obtain boric acid flow with the 4A BATP from the B BAST but again no flow was obtained. This flow path was attempted again at 0315 but again no flow was obtained. At 0505, Operations attempted to verify the boric acid flow path for Unit 3 and again could not establish flow. At 0600, the primary water source was isolated on a clearance to the plant super-visor nuclear (PSN). An event response team (ERT) was formed to evaluate the root cause and provide for corrective actions.
NRC FORM SddA (943(
NRC Form 3ddA V.S, NUCLEAR REOULATORY COMMISSION (9.83(
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVEO OMB NO. 3150&(04 EXPIRES: 8/31/88 FACrLITY NAME (ll OOCKET NUMBER (3) LER NUMBER Idl PAOP. (3)
YEAR SSOVSNTIAL REVISION
@Pi NVMSC II +O?A NVMIISII Turkey Point Unit 3 0 5 0 0 0 7 1 7 0 3 OF TEXT /// moro opoco /F ror/rr/rorL Irw or/I/ro'ono/H/IC Asm 388A'F/ (ll(
The ERT determined that the mechanical .,seal on the 4B BATP could be damaged.
This would drain the water from the seal tank and allow the nitrogen cover gas to enter into the system and bind the pumps. Based on this the cross-tie valve was closed, the 3B BATP was vented and a boric acid flow path was established for Unit 3 at 0940 on June 3, 1987. The 4B BATP was isolated, the 4A BATP was vented and the normal boric acid flow path was established for Unit 4 at 1030 on June 3, 1987.
CAUSE OF EVENT:
The BATPs mechanical seal design utilizes a tank of primary water that is pressurized for cooling requirements. A 40 psig supply of nitrogen is constantly applied to the tank. The level of cooling water can be checked by a "bullet" type sight glass. The investigation by the ERT determined that a damaged inboard mechanical seal on the 4B BATP resulted in a loss of seal water in the tank. As the water drained into the pump, the pressurized nitrogen supply entered the 4B BATP casing and into the boric acid system. This resulted in gas binding the Unit 4 BATPs. Also when the Unit 3 BATPs suction line was cross-connected to the Unit 4 BATPs through a normally closed cross-tie valve, the nitrogen entered the Unit 3 BATPs and gas bound these pumps.
ANALYSIS OF EVENT:
During this event, Unit 3 was in mode 6 and Unit 4 was in mode 5. A review of the Final Safety Analysis Report (FSAR) indicates that the accidents analyzed for in these conditions do not take credit for boron injection. The analysis for the boron dilution event during refueling assumes that the minimum boron concentration is 1950 ppm. The analysis assumes that the operator has prompt and definite indication of any boron dilution from the audible count rate instrumentation. Assuming the 1950 ppm concentration and a maximum dilution rate, it would take approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to reach the boron concentration that is required to make the reactor critical. This is ample time for the operator to recognize the high count rate signal and isolate the primary water makeup source by closing valves.
During this time period, the RCS boron concentration for Unit 3 was maintained greater than or equal to 2250 ppm which satisfied the requirements of TS 3.10.8 of maintaining the reactor at least 10% shutdown. The boron concentra-tion for Unit 4 was maintained greater than or equal to 1550 ppm which satis-tied the requirements for a unit in cold shutdown of maintaining the reactor 1% shutdown as specified in TS Table 1.1, Operational Modes. In addition, the control rod drive system for both units was not capable of rod movement, so the accidents analyzed for this system were not applicable. Based on the above, the health and safety of the public were not affected.
CORRECTIVE ACTIONS:
- 1) The mechanical seal for the 4B BATP was inspected and repaired as necessary.
NRC FORM SddA (983)
NAC Form 3ddA U.S. NUCLEAR RECULATOAY COMMISSION (943)
LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROVEO OM8 NO. 3150M)Cd EXPIRES: 8/31/88 F jECILITY NAME II) COCKET NUMEER (3) LER NUMEER ld) PACE (3)
YEAR g~v.'SCVENTIAI. .'Ig REVISION oroSI NVMSE4 I NVM SR Turkey Point Unit 3 0 5 0 0 0 2 5 017 OF 0 5 TEXT ///moro opodo /I rOI)o/IOI/ IIW OIA//I/ono/ H/IC Form 3//843/ (IT)
- 7) An event response team was formed to review the sequence of events to assist in identifying the root cause and propose appropriate corrective actions. The following are some of the corrective actions identified:
a) A request for engineering assistance will be generated to review the existing seal design to identify possible alternative seal designs or enhancements to the existing design.
b) The Training Department will be requested to review this event for appropriate training requirements and methods.
c) The Procedure Upgrade Group is developing guidance for a loss of boric acid flow and defining additional boric acid flow path valve alignments. This guidance will be incorporated into apropriate procedural requirements.
d) Additional guidance for Operations is being developed to clarify the requirements to be met during off normal conditions.
- 8) The safety injection pumps, the containment spray pumps, and the BATPs for both units will be tested for operability prior to the start up of either unit ~
- 9) The results of this event response team will be provided to a team investigating charging pump and volume control tank problems to determine the nitrogen in-leakage from the BATPs contributed to these problems.
if ADDITIONAL DETAILS:
The BATPs are manfuctured by Goulds, Inc., model number 3196-ST-8. The mechanical seals are manufactured by Durametallic. The mechanical seal cooling design was done by our Power Plant Engineering Department in con)uction with Durametallic.
Similar occurrences: LER 251-79-011 NAC FOAM SddA (983)
NRC Form 3SSA UA. NUCLEAR REGULATORY COMMISSION (9431 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3150M)04 EXPIR ESI B/31/88 FACILITY NAME (I ) OOCKET NUMBER (3) LER NUMBER IS) PAGE (3) yEAR oW 5SOUSNTIAL Pr(+ RFVISION NUMSSR <)r/r/ NUMSSR Turkey Point Unit 3 o s o o o 017 4 OF 0 5 TEXT //f more specs/s reqII/red, use edd/o'ooe/FVRC Form 36SA's/ l)T)
- 2) The following procedures were revised to isolate the constant nitrogen supply and provide instructions for maintaining the proper nitrogen pressure based on the new configuration.
a) Operating- surveillance procedure (OSP) O-OSP-201.2, SNPO Daily Logs, was revised to direct the operators to off normal operating procedure (ONOP) 2608.2, CVCS-Malfunction Of Boron Concentration Control System, if the nitrogen pressure drops below 35 psig.
b) Administrative procedure (ADM) O-ADM-205, Administrative Control of Valves, Locks and Switches, was revised to require the BATP seal tank nitrogen supply valves to be locked closed .
c) Operating procedure (OP) O-OP-065.3, Nitrogen Gas Supply. System, was revised to require the outlet isolation valves of the BATPs seal tank nitrogen regulator to be normally closed and the inlet isolation valves to be locked closed.
d) ONOP 2608.2 was revised to de'fine the action to be taken if the acceptance criteria stated in O-OSP-201.2 is not met.
- 3) Training brief 201 was issued to describe to the operators the sequence of events, the significance of what happened and the procedure changes described in corrective action 2 above .
- 4) The Safety Engineering Group has reviewed 'IE Information Notice 82-19, Loss of High Head Safety Injection Emergency Boration and Reactor Coolant Makeup Capability, for applicability at Turkey Point. Their review has indicated that gas intrusion into the charging system can only come from the BATP seal pot. Since the nitrogen supply is being administratively controlled to avoid unmonitored supply to the seal pot and a training brief on the concern has been issued, this item can be closed from review at Turkey Point. This response is currently under closure review per site administrative procedures')
A non-conformance report (NCR), NCR 87-157, has been issued to request Power Plant Engineering to evaluate and disposition the drawing changes necessary as a result of the procedure changes described in corrective action 2 above.
- 6) An inspection was conducted to determine if any of the nitrogen could have made its way into the safety injection and containment spray pumps for both units. The results indicated that the samples tested were similar to a test sample of air and that there was only a small amount of air present in the pumps.
NRC FORM SSSA (94)3)
P, 0, BOX 0r JUNO BEACH, FL 33408 FLORIDA POWER & LIGHT COMPANY see 86 >987 L-87-27 I IO CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gent 1emen:
Re: Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 87-I 7 Date of Event: May 28, I 987 Loss of Boric Acid Flowpath Due to Failed Mechanical Seal Which Allowed Nitro en to Enter and Bind U the Pum s The attached Licensee Event Report is being submitted pursuant to the requirements of IO CFR 50.73 to provide notification of the subject event.
Very truly yours,
).%.Q( ~Q" Group Vice President Nuc I ear Energy COW/SDF/gp Attachment cc: Dr. J. Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant PEOPLE... SERVING PEOPLE SDF I /035/I