|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr 05000250/LER-1998-006-02, :on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With1998-10-27027 October 1998
- on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With
ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. 05000250/LER-1998-005-02, :on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With1998-10-16016 October 1998
- on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With
ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr 1999-09-30
[Table view] |
Text
m PR.IC)R.IT V (ACCELERATED RIDS PROCESSIN REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9504180061 DOC.DATE: 95/04/07 NOTARIZED: NO DOCKET N FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH. NAME AUTHOR AFFILIATION KNORR,J.E. Florida Power & Light Co. P PLUNKETT,T.F. Florida Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION R
SUBJECT:
LER 95-003-00:on 950309,intake cooling water flow rate through CCW heat exchangers fell below assumed design basis.
Caused by an influx of aquatic grass & algae onto basket strainers.Strainers cleaned.W/950407 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Inciden Rpt, etc.
NOTES RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 PD 1 1 CROTEAU, R .
1 1.
INTERNAL: D SPD B 2 2 AEOD/SPD/RRAB 1 1 I
NRR D C TE EEL 1
1 1
1 NRR/DE/ECGB NRR/DE/EMEB 1
1 1
1 NRR/DISP/PIPB 1 1 NRR/DOPS/OECB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 0
NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 u
N NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE O'ASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOK! P!-37 (EXT. 504-2083 ) TO ELIAtINATEYOUR iAME FROM DISTRIBUTION LISTS I'OR DOCI.'NIEiTS YOU DON"I'EED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 27 ENCL 27
NpL APR 0'7 1995 L-95-105 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:
Re: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Reportable Event: 95-003-00 Intake Cooling Water System Flow Rate Found Less Than The attached Licensee Event Report, 250/95-003-00, is being provided in accordance with 10 CFR 50.73 (a) (2) (ii) (B) .
If there are any questions, please contact us.
V ruly yours, T. F. P un et Vice President Turkey Point Plant JEK Attachment cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Thomas P. Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant rwpr~ ~ I
~vcU J <
9'504i8006i 950407 PDR ADOCK 05000250 S PDR an FPL Group company
LICENSEE EVENT REPORT LER DOCKET NUMBER 2 PAGE 3 FACILITY NAME (1)
TURKEY POINT UNIT 3 05000250 1 '" ll TITLE (4) Intake Cooling Water System Flow Rate Found Less Than Required by Desi n Basis EVENT DATE 5 LER NUMBER 6 RPT DATE 7 OTHER FACILITIES INV. 8 MON DAY YR SE 4 Rf MON DAY YR FACILITY NAMES DOCKET 4 S 03 09 95 95 003 00 04 07 95 Tutkoy Point Unit 4 05000251 OPERATING MODE 9
1/5 POWER, LEVEL (10) 60/0 LICENSEE CONTACT FOR THIS LER 12 TELEPHONE NUMBER J. E. Knorr, Regulation Compliance Specialist 305-246"6757 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 COMPNT MANUFACTURER NPRDST CAUSE SYSTEM COMP NT MANUFACTU NPRDS7 CAUSE RER EXPECTED MONTH DAY SUPPLEMENTAL REPORT EXPECTED (14) NO YES 0 SUBMISSION DATE (15)
(if yoni ccoploto EXPECTED SUBMISSION DATE)
ABSTRACT (16)
At approximately 0435 (EST), on March 9, 1995, the Intake Cooling Water (ICW) flow rate through the Component Cooling Water (CCW) heat exchangers fell below that assumed in the Turkey Point design basis.
The reduced flow rate was due to an influx of aquatic grass and algae onto the basket strainers of the ICW flow path upstream of the CCW heat exchangers. The strainers were cleaned and flow returned to required levels at 0521. The plant was operating at 60 percent reactor influx power as of a conservative measure due to the potential for an increasing aquatic grass and algae into the ICW and circulating water systems.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 95-003"00 20F 11 Z. DESCRIPTION OF THE EVENT During the evening of March 8, 1995, an influx of aquatic grass mixed with algae occurred at the cooling water intake [NN] from the closed cooling canal [BS:RVR] system at Turkey Point. The cooling water intake is common to the Intake Cooling Water (ICW) system [BS] and the circulating water system [NN]. The ICW system supplies water to the safety related component cooling water (CCW) system and the non-safety related Turbine Plant Cooling Water (TPCW) [TF] system. The ICW, system has three pumps
[BS:P] and two headers [BS] leading to thr'ee CCW heat exchangers
[BS:HX], and two headers leading to two TPCW heat exchangers
[TF:HX], with an in-line basket strainer [BS:STR] for each header. The TPCW headers are automatically isolated upon receipt of a safety injection signal. The circulating water system supplies water to the main condensers [NN:HX]. Early in the evening on March 8, reactor power for Unit 3 was conservatively reduced to 60% to provide operating margin influx were to increase. Unit 4 was in mode 5.
if the grass and algae The outlet of the ICW headers with basket strainers feeds a common header at the inlet of the tube side of three CCW heat exchangers. For a basket strainer to be mechanically cleaned, the strainer must be isolated. The ICW header containing that strainer is thus declared inoperable. The remaining header (basket strainer) must pass the minimum design flow to maintain operability of the remaining header.
Early in the morning of March 9, the accumulation of aquatic grass and algae on the strainers caused the differential pressure across one ICW strainer to increase, indicating the need for mechanical cleaning. That ICW header was declared inoperable. As a result of the increasing fouling on the opposite ICW header's basket strainer, at approximately 0435 EST, Florida Power & Light Company (FPL) determined that Unit 3 was in a condition that was outside the design basis for ICW flow.
Technical Specification 3.7.3 reads as follows:
"The Intake Cooling Water System (ICW) shall be OPERABLE with:
- a. Three ICW pumps, and
- b. Two ICW headers.
MODES 1, 2, 3, and 4.
ZZ'KQH:
a ~ ~ ~ ~
b ~ ~ ~ ~
- c. With only one ICW header OPERABLE, restore two headers to OPERABLE status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
FACILITY NAME t
LICENSEE EVENT REPORT DOCKET NUMBER t
(LER) TEXT CONTINUATXON LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 95-003-00 3 OF 11 Operating Procedure 3/4-0P-019, "Intake Cooling Water System,"
provides guidance on the minimum flow criteria for operability of an ICW header. The criteria are based on fouling factors and canal temperatures. In this case, the minimum flow rate for the conditions at the time was approximately 9500 gpm. The flow rate of 9500 gpm ensures that the CCW heat exchangers, with the canal temperature of 75.5 F, are capable of removing the design basis post-accident heat load.
With one of the strainers out of service for mechanical cleaning,
-~- flow through the opposite strainer declined to below the required 9500 gpm as a result of clogging of that strainer. As the aquatic grass and algae continued to flow into the remaining strainer, the ICW flow to the CCW heat exchangers continued to drop to approximately 2500 gpm. At 0435, the second header of ICW was declared inoperable. The action statement in Technical Specification 3.7.3 does not apply to the condition of two inoperable headers. Therefore, the plant entered Technical Specification 3.0.3 which required, within one hour, action to place the unit in Mode 3 within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. At 0521, one basket strainer was cleaned and returned to service, restoring the overall ICW flow rate to greater than 9500 gpm. Therefore, no plant shutdown was required.
II. CAUSE OF THE EVENT In February and early March 1995, south Florida had little rain.
As a result, the Turkey Point closed cooling canal water level was reduced. When heavy rain and wind occurred gust prior to the event, the canal levels increased allowing clumps of canal aquatic grass (ruppia mari tima) mixed with algae (batophora) to break loose and flow toward the ICW/circulating water system intake. Under normal grass and algae loading conditions, the aquatic grass and algae are captured by traveling screens at the plant's cooling water intake structure, and washed off of the screens by a screen wash system. In this event, the large amount of suspended grass and algae was enough to cause some of the aquatic material to carry over the traveling screens and into the intake bays for the ICW and circulating water systems. The ICW pumps picked up the carry over material. The ICW basket strainers, as designed, removed the majority of the grassTheand algae from the flow stream to the CCW heat exchangers.
circulating water pumps also pumped some of the material into the inlet side of the main condenser waterboxes affecting condenser cooling efficiency.
t LICENSEE EVENT REPORT t
(LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 95-003-00 4 OF 11 IXI . ANALXSES OF THE EVENT The analysis of this event includes a safety assessment of the following seven areas:
ICW system functionality CCW system functionality Containment integrity Equipment qualification Loss of coolant accident (LOCA) Emergency Containment Cooling (ECC) system analysis Main steamline break Radiological consequences Following is a list of some of the key parameters used in the event safety assessment. They reflect the actual conditions found or design basis assumptions at Turkey Point on the morning of March 9, 1995.
Containment air temperature = 105 F Outside ambient temperature = 68.5 F Refueling Water Storage Tank (RWST) fluid temperature = 75 F (assumed)
ICW canal (inlet) temperature = 75.5'F Offsite power available 3 Emergency Containment Coolers (ECCs) available 2 Containment Spray pumps available 2 ICW pumps in service 2 CCW pumps in service 2 Residual Heat Removal (RHR) pumps and heat exchangers available Average CCN heat exchanger total fouling level at the original design level (0.00159 hr-ft F/BTU)
All three CCN heat exchangers in service Containment pressure = 0.3 psig (assumed)
TPCW isolation upon a safety injection signal {by design)
The overall function of the ICW system during post-accident conditions is to provide continuous cooling to the CCW heat exchangers. The ICW system design basis for post-accident operation is a minimum of ICN flow to CCN heat exchangers. A network of closed cooling canals is used as the ultimate heat sink for Turkey Point and provides a continuous supply of cooling water. The limiting safety related ICW flow requirement is based upon the heat load during the mitigation of a design basis large break loss of coolant accident (LBLOCA) .
The configuration of the ICW system at the time of the event was two ICW pumps directing flow to three CCW heat exchangers via one header. The second header was out of service for strainer cleaning, as discussed above. The ICW system was also delivering
1 LICENSEE EVENT REPORT t
(LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 95-003-00 5 OF 11 flow to the TPCW heat exchangers. The TPCW system is automatically 'solated on a safety injection signal. As a conservatism, for the purposes of this evaluation, credit was not taken for the increased ICW flow through the CCW heat exchangers due to the TPCW isolation.
The controlling parameter on the functionality of the CCW heat exchangers during post-accident conditions at reduced ICW flows is the ICW temperature at the outlet of the CCW heat exchangers.
The reduction in ICW flow through the CCW heat exchanger, given a constant heat removal duty, results in an increase in the ICW outlet temperature of the CCW heat exchanger. The relatively low ICW system inlet temperature (approximately 75 F compared to 95 F design basis canal temperature) at the time of the event, reduced the potential maximum for the post accident ICW temperature at the outlet of the CCW heat exchangers.
As discussed below, a detailed thermal analysis of the design basis LBLOCA event was analyzed assuming that the event occurred concurrent with the ICW low flow event. To support the LBLOCA thermal analysis, a time averaged ICW flow to the CCW heat exchangers was established for the ICW low flow event. The following flow profile was used, representative of the plant conditions observed:
0-10 minutes, 9000 gpm 11 minutes, step change to 5000 gpm 11-40 minutes, gradual reduction to 2500 gpm 40-56 minutes, 2500 gpm 57 minutes, step change to 9500 gpm 57-60 minutes, 9500 gpm Using the above profile a time averaged ICW flow of approximately 4675 gpm (1560 gpm per CCW heat exchanger) was used in the analysis for the first hour and 9500 gpm thereafter. This is a conservative assumption since the ICW flow rates returned to levels greater than 9500 gpm after the a basket strainer was mechanically cleaned. This time averaged ICW flow was used to provide a more realistic set of input parameters for the LBLOCA thermal analysis. The analysis model used conservative assumptions for overall heat transfer.
Based upon the time averaged flow conditions, the peak ICW temperature was calculated to occur shortly after the beginning of an assumed LBLOCA following the start of the emergency containment coolers (ECCs) . The maximum calculated CCW heat exchanger ICW outlet temperature is approximately 134 F. The temperature steadily declines to less than 100 F after about 45 minutes. Following switchover to cold leg recirculation (after placing the RHR heat exchangers in service), the ICW temperature increases to approximately 124 F, again decreasing steadily after reaching that temperature.
, FPL performed an assessment of the temperature affects on the structural integrity of the ICW system and has concluded that'he ICW system would remain functional. Therefore, the ICW system
t LICENSEE EVENT REPORT t
(LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 95-003-00 6 OF 11 would have continued to perform its safety function of continuing to cool the CCW heat exch~ngers.
The overall function of the CCW system during post-accident conditions is to provide a continuous cooling of safety related components. This requires that the CCW return header temperature remain within the design basis of the system and that the supply temperature remain within equipment operating limits.
At Turkey Point, essential components served by the CCW system are the RHR pumps, Safety Injection (SI) pumps, Containment Spray (CS) pumps, ECCs and RHR heat exchangers. In addition a Chemical and Volume Control System (CVCS) positive displacement (charging) pump is used post-accident to adjust containment sump pH and is also served by CCW.
The following are the CCW system temperatures of interest:
CCW shell side outlet (" supply" ) temperature ECC CCW outlet temperature RHR heat exchanger CCW outlet temperature CCW shell side inlet ("return") temperature The post accident operability limit for CCW "supply" is 150 F.
The temperature has been modeled to remain at 150 F for four hours and then to decrease at a minimum of 1 F/hr for the next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> to 120 F, remaining at that level for the remainder of the LBLOCA. The SI pump oil cooler is controlling for this temperature profile. The analysis shows that the SI pump remains operable.
For the ECCs and RHR heat exchangers, the analysis verified that the CCW "supply" temperature remained below the system design temperature for those systems. The limit on the "supply" temperature is required to ensure maintenance of single phase flow through the systems.
For the CCW heat exchanger "return, " the limiting temperature is dictated by the net positive suction head of the CCW pump. A temperature as high as 172.7 F has been evaluated as acceptable for the CCW pump suction. This calculation ensured single phase flow at the suction of the CCW pumps.
An assessment of the overall CCW heat removal capability was made based upon the operating conditions at the time of the ICW low flow event. The design basis post-accident CCW heat exchanger heat load used to verify the thermal performance of the CCW heat exchangers is approximately 60 million BTU/hr per heat exchanger.
With two heat exchangers (design basis) available the total heat removal capability of the CCW system is 120 million BTU/hr.
t LICENSEE EVENT REPORT t
(LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 95-003-00 7 OF 11 At the lower ICW flow and lower ICW inlet temperature present on March 9, with an allowance for the CCW "supply" temperature to rise to 150 F and three CCW heat exchangers available, the total heat removal capability of the CCW system is estimated to be approximately 123 million BTU/hr. This assessment indicates that the reduced ICW flow to the CCW heat exchangers would not have caused the CCW system "supply" temperature to be significantly higher than the limit of 150 F. If CCW system thermal inertia and heat up times were considered, the actual CCW "supply" temperature rise would have been less than calculated above.
A detailed analysis of the ICW low flow event limiting system flows and maximum heat loads (e.g., three ECCs) was also completed. The analysis assumed two CCW pumps and three CCW heat exchangers with the fouling factors experienced when the ICW low flow event occurred. As mentioned before, the time averaged ICW flow rate of approximately 4675 gpm was used for the first 60 minutes and 9500 gpm for the remainder of the analysis. Credit was taken for operation of all essential safeguards equipment and actual plant operating conditions at the time of the ICW low flow. In general, the actual plant operating conditions at the time of the event were much less limiting that those assumed in the safety analysis. The conditions present at the time of the event provided a benefit that compensated for the lower than normal ICW flow. However the assumption of 3 ECCs in service is more limiting from a CCW system heat removal perspective.
The peak CCW "return" temperature was calculated to reach approximately 170 F, decreasing to about 105 F within 45 minutes.
Following switchover to cold leg recirculation, a second peak of approximately 155 F was calculated to occur.
For the CCW "supply" temperature, a peak of 156 F was calculated decreasing to'150'F within about a minute. Over the next 45 minutes the temperature would drop to about 100 F. After switchover to cold leg recirculation, the temperature would again increase to about 141 F. Although the maximum calculated temperature slightly exceeded the previously established limit (156'F versus 150 F), the duration of the higher temperature condition (less than a minute) was much less than previously considered. Over the short time frame, the thermal lag of the system combined with thermal inertia would have limited the temperature rise to less than 150'F. In all cases the temperatures steadily decline as ICW flow is restored after a basket strainer is cleaned.
Although the specific detailed thermal analysis results are clearly conservative in nature to the use of steady-state instantaneous heat transfer assumptions, the results are consistent with the overall heat removal assessment noted earlier. Considering the dynamic nature of the CCW heat removal process, the analyses show that the CCW temperature would have remained within the component allowable temperatures and the CCW system would not have been adversely affected by the ICW low flow event.
t LICENSEE EVENT REPORT t
(LER) TEXT CONTINUATION PAGE NO.
FACILITY NAME DOCKET NUMBER LER NUMBER TURKEY. POINT UNIT 3 05000250 95-003-00 8 OF 11 In addition, FPL performed a preliminary assessment of temperature conditions which bound the above analyses and concludes, considering thermal stress effects, the CCW system would remain functional. Therefore, the overall functionality of the CCW system with respect to its primary safety function would not have been affected by this event.
The impact of this ICW low flow condition was evaluated for containment pressure response with respect to LBLOCA and Main Steamline Break (MSLB) inside containment. The plant conditions and configuration at the time of the ICW low flow event are less limiting than the current design basis LOCA containment transient. The current limiting transient is the containment response to the double-ended pump suction (DEPS) break with a concurrent loss of off-site power and the failure of an emergency diesel generator. The current peak containment initial pressure for this transient is 49.9 psig which occurs during the blowdown is 55 period. The containment design pressure for Turkey Point psig. Recently revised calculations of mass and energy releases provided additional conservatism in the initial core stored energy, decay heat level, initial internal RCS energy, and safety injection enthalpy over the current plant conditions.
In the analysis, the containment response to the DEPS break was terminated at 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Modeling the low ICW flow transient for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> after regaining the required ICW flow of 9500 gpm ensured the data recovery for containment response from the blowdown period through cold leg recirculation. This analysis showed a peak containment pressure of 45.2 psig at approximately 19.4 seconds after initiation of the DEPS. Although not part of the design basis for Turkey Point, NRC Standard Review Plan criteria for pressure reduction after an event isavailable 50% of the peak pressure within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Due to the amount of heat removal equipment, the containment pressure met the criteria within approximately 30 minutes and is near 25% of peak pressure within 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
Using recently revised calculations, the limiting MSLB containment peak pressure is 42.8 psig. This is based upon a transient beginning at zero power with a failure ft'. of a main steam all check valve (MSCV) and a break area of 1.4 With secondary safety systems assumed operable and no single active failures, the mass and energy releases from the broken steam line would be significantly less when compared to the limiting transient. Peak containment pressures which result from a MSLB transient with no system failures typically are less than 30 psigo Based upon the above results, the current design basis DEPS break containment response with the failure of a diesel generator and concurrent loss of offsite power, and the 1.4 ft MSLB at flow zero power with a MSCV failure, remain bounding. The low ICW event would not have caused a more limiting condition than that which is already analyzed for containment integrity.
TURKEY POINT UNIT 3 t
LICENSEE EVENT REPORT FACILITY NAME DOCKET NUMBER 05000250 l
(LER) TEXT CONTINUATION LER NUMBER 95-003-00 PAGE NO.
9 OF 11 From the containment integrity analyses above, the calculated limiting peak containment temperature ~as determined to be 268.4 F at 19.4 seconds into the event. The analyses indicate that, assuming a low ICW flow event, containment temperatures are maintained well below the envi.ronmental qualification (EQ) envelope at all times. At 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> aftex a LOCA event, the containment temperature will be approximately 197 F. Also, from the containment integxity analyses, the peak containment pressure reached was 45.2 psig at 19.4 seconds and fell to 13.5 psig within 5.hours. Therefore, the calculated containment temperatures and pressure levels due to the low ICW flow event did not exceed the EQ allowables.
This analysis is not affected by the low ICW flow event in a non-conservative manner. Elevated CCW system "supply" temperatures to the ECCs are a benefit to the 'containment pressure affects on the LOCA peak clad temperature (PCT) calculations. The minimum backpressures assumed in PCT calculations are conservative since the elevated CCW temperatures to the ECCs would reduce the ECCs performance and therefore increase backpressures.
See above for a discussion of the affect of the event on containment integrity.
The MSLB analysis is not affected by the ICW low flow event as long as the SI pumps and all other safety systems remain operable.
The design basis doses are not affected by the ICW low flow event. As stated earlier, the design basis containment integrity analyses remain bounding, the LOCA PCT analyses are not affected, the MSLB analyses are not affected and the safety system components remain operable and intact. Therefore, doses to plant personnel and the general public are not affected.
The overall conclusions of the above safety assessments are that all critical areas of plant accident analyses remain bounded.
This conclusion is possible because of the short duration of the low flow transient and actual plant operating conditions at the time of the event are well below limiting analyses conditions.
The inherent margin provided by the plant configuration and the lower operating conditions countered the adverse affects associated with the temporary low ICW flow.
t LICENSEE EVENT REPORT t
(LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE No.
TURKEY, POINT UNIT 3 05000250 95-003-00 10 OF 11 Additionally, FPL performed a probablistic safety assessment for this event. The low ICW flow was conservatively modeled as a complete loss of CCW flow for one hour. The assessment concluded that the calculated core damage frequency did not increase above the base line of 6.63x10 '/year.
ZV. CORRECTIVE ACTIONS The basket strainers were mechanically cleaned to restore ICW flow to greater than the minimum flow required for the canal temperature and CCW heat exchanger fouling factors found at the time of the event.
- 2. Two floating booms are installed in the canal system. The first, installed prior to the event, is at the extreme southern end of the canal system to catch floating aquatic grass and algae material prior to the flow release point into the return canals. This first boom was only partially effective in controlling the grass and algae influx. The second was installed in the final return canal within a quarter mile of the intakes to catch any floating material which was not caught by the first floating boom. These booms are used on an as needed basis.
- 3. A pump has been installed to remove the grass and algae from the canal at the location of the first boom installed at the southern end of the canal system. This pump is used on an as needed basis.
4 ~ An Off Normal Operating Procedure, 3/4 ONOP-011, "Screen Wash System/Intake Malfunction," has been developed (March 28, 1995) to provide guidance on actions to be taken in the event of a major influx of grass/debris into the intake structure. This procedure also references 3/4-0NOP-019, "Intake Cooling Water Malfunction."
- 5. Training brief g544, which clarifies the need to run ICW pumps in bays without circulating pumps operating to reduce the level of basket strainer fouling, has been issued.
- 6. A traveling screen performance program will be developed to monitor and improve the performance of the screen system.
Areas to be considered, and included if appropriate, are screen wash nozzle performance, screen wash pump performance, screen wash strainer performance, and traveling screen hole size. The program will be evaluated and implemented by July 15, 1995.
- 7. The ICW/CCW basket strainer performance can be improved. A method for determining flow through each basket strainer will be evaluated and implemented as appropriate. The evaluation and recommendation of corrective actions will be completed by July 1, 1995. Any recommended system modifications will be scheduled for refueling outages starting after 1996.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 95-003"00 11 OF 11 V. ADDITIONAL INFORMATION EIIS Codes are shown in the format [EIIS SYSTEM: IEEE component function identifier, second component function identifier (if appropriate)].
No similar Licensee Event Reports have been submitted concerning low ICN flow.