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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr 05000250/LER-1998-006-02, :on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With1998-10-27027 October 1998
- on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With
ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. 05000250/LER-1998-005-02, :on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With1998-10-16016 October 1998
- on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With
ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr 1999-09-30
[Table view] |
Text
CATEGORY 1 ~
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9603250229 DOC.DATE: 96/03/18 NOTARIZED: NO DOCKET FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH. NAME AUTHOR AFFILIATION HANEK,O. ,Florida Power & Light Co.
HOVEY,R.J. Florida Power & Iight Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 96-004-00:on 960220,surveillance testing of AFW actuation circuitry was inadequate. Caused by inadequate surveillance procedures. Tested untested portions of actuation logic for AFW automatic start signal.W/960318 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR I ENCI ~ SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 PD 1 1 CROTEAU,R 1 1 INTERNAL: 8 2 2 AEOD/SPD/RRAB 1 1 FILE CENTE 1 1 NRR/DE/ECGB 1 1 D EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCEPJ H 2 2 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDSN RECIPIENTS:
CONTROL DESKS PLEASE HELP US TO REDUCE WASTE) CONTACT THE DOCUMENT ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
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MAR 18 t996 L-96-068 10 CFR 50.73 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:
Re: Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 96-004-00 Inadequate Surveillance Testing of the Auxiliar Feedwater Actuation Circuitr The attached Licensee Event Report, 250/96-004-00, is being provided in accordance with 10 CFR 50.73(a) (2) (i) (B) .
Should there be any questions, please contact us.
Very truly yours, 40tb Robert J. Hovey Vice President Turkey Point Plant OIH attachment cc: S. D. Ebneter, Regional Administrator, Region II, USNRC T. P. Johnson, Senior Resident Inspector, USNRCg Turkey Point Plant
'7603250229 9603%8 PDR S
ADOCK 05000250 PDR pg f7f" an FPL Group company
LICENSEE EVENT REPORT LER DOCXET NUHBER 2 PACE 3 FACILITY NAHE (1)
TURKEY POINT UNIT 3 05000250 1 Of' TITLE (4) INADEQUATE SURVEILLANCE TESTING OF THE AUXILIARY FEEDWATER ACTUATION CIRCUITRY EVENT DATE 5 LER NUHBER 6 RPT DATE I OTHER FACILITIFS INV 8 HON DAY YR Rf HON DAY YR FACILITY NAHES DOCXET 4 S 02 20 96 96 004 00 03 18 96 Turkey Paint Unit 4 05000251 OPERATING NODE (5)
PURER LEVEL (10) 100 LICENSEE CONTACT FOR THIS LER 12 Tele hone Number Olga Hanek, Licensing Engineer 305 246-6607 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 CAUSF. SYSTDI COHPONFNT HANUFACTURFR NPRDS? CAUSE SYSTEH COHPONENT HANUFACTURFR NPRDS?
EXPECTED HONTH DAY SUPPLEHENTAL REPORT EXPECTED (14) NO YESO SUBHISS ION DATE (15)
(lf yee, canylete EXPECTED SUBHISSION DATE)
ABSTRACT (16)
On February 20, 1996, while performing a review of Plant Procedures 3(4)-OSP-075.4, Florida Power & Light Company (FPL) identified that not all three combinations of the two out of three logic for the Steam Generator (SG) Low-Low Water Level Auxiliary Feedwater (AFW) start signal were verified as required by Technical Specification Table 4.3.2, Item 6.a.
Turkey Point has determined the root cause to be inadequate surveillance procedures.
Corrective actions included testing of the untested portions of the actuation logic for the AFW automatic start signal on SG low-low water level. Plant Procedures 3(4)-OSP-075.4 will be revised to include all three combinations of the two out of three logic for the SG low-low water level AFW start signal prior to the next performance of this surveillance.
This inadequate surveillance testing is being reported in accordance with 10 CFR 50.73 a 2 i B
t LICENSEE ERG'NT REPORT (LER) TEQVZ t
CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 96-004-00 2OF7 Z. DESCRZPTZON OF THE EVENT On February 20, 1996, during the performance of scoping and scheduling the effort required to respond to NRC Generic Letter 96-01,"Testing of Safety-Related Logic Circuits," Florida Power & Light Company (FPL) identified a potential Technical Specification non-compliance associated with surveillance testing of the AFW [AB] actuation circuitry on steam generator (SG) low-low water level. After review and evaluation of this issue, FPL concluded that the Technical Specification required testing for this circuitry was insufficient and the system was declared inoperable. The evaluation supporting this conclusion was completed at approximately 9:00 am on February 22, 1996.
The concern identified was that not all three (3) combinations of the 2/3 logic for the Low-Low Level SG Level Auxiliary Feedwater (AFW) start signal are verified in Plant Procedure 3/4-0SP-075.4, "Auxiliary Feedwater Auto-Start Test". In accordance with Table 4.3-2, Item 6.a and Section 1.2 of the Technical Specifications, "each possible interlock logic state" shall be tested when performing the "Actuation Logic Test". A review of other applicable Operations and Maintenance Plant Procedures determined that the required testing was not performed. Therefore, the subject surveillance requirement was not satisfied and Section 4.0.3 of the Technical Specifications was applicable. Technical Specification 4.0.3 allows 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for completion of a missed surveillance. The test was completed successfully at approximately 10:15 pm on February 22, 1996, for both units.
Although AFW has four other auto-start signals [JE:RLY] (Loss of offsite power (LOOP), safety injection (SI), ATWS Mitigating System Actuation circuitry (AMSAC), SG Feedwatez Pump Trip), credit is taken for Low-Low SG Level as the primary auto-start signal for several plant accident analyses.
ZZ. CAUSE OF THE EVENT The root cause of the event was inadequate surveillance procedures.
ZZZ. ANALYSIS OF THE EVENT The Turkey Point AFW System is a shared system between Units 3 and 4.
uses secondary steam to drive three AFW pump turbines which supply feedwater It to the steam generators during transients when the normal feedwater source is not available. The system consists of two independent trains each capable of providing required flows to both units. Control and motive power to the AFW valves is provided by either Vital AC or DC. The required AFW flow of approximately 125 gpm/unit must be delivered within three minutes of the generation of an RPS/ESFAS signal for LOOP or Small Break LOCA. This time is an assumption for the analyses used to establish the minimum flow requirement.
The control logic governing AFW operation is such that a variation in specific plant parameters, beyond the setpoint limits, results in a signal to open the steam supply valves on the affected units(s). As configured, the AFW system automatically initiates as a result of any one of the following:
- 1) SI actuation
t t LICENSEE EVENT REPORT (LZR) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 96-004-00 3OF7
- 2) 2 out of 3 Low-Low water level in any one of the three SGs
- 3) Loss of both steam generator feedwater pumps (SGFP)
- 4) Bus Stripping (Bus stripping from one bus opens two out of three AFW steam motor operated valves (MOVs))
- 5) ATWS Mitigating System Actuation circuitry Surveillance requirements of the AFW System that apply to auxiliary feedwater actuation are provided in Technical Specification Section 4.7.1.2.1. as stated below:
"The required independent auxiliary feedwater trains shall be demonstrated OPERABLE:
a ~
- b. At least once pez 18 months by:
- 1) Verifying that each automatic valve in the flow path actuates to its correct position upon receipt of each Auxiliary Feedwater Actuation test signal, and
- 2) Verifying that each auxiliary feedwater pump receives a start signal as designed automatically upon receipt of each auxiliary Feedwater Actuation test signal."
Surveillance requirements for Engineered Safety Features Actuation System (ESFAS) Instrumentation that apply to auxiliary feedwater actuation are provided in Technical Specification Section 4.3.2.1 as stated below:
"Each ESFAS instrumentation channel and interlock and the automatic actuation logic and relays shall be demonstrated OPERABLE by performance of the ESFAS Instrumentation Surveillance Requirements specified in Table 4.3-2".
Item 6a of Technical Specification Table 4.3-2, requires that the automatic actuation logic and actuation relays of the auxiliary feedwater system have an ACTUATION LOGIC TEST performed each refueling outage.
The definition of an ACTUATION LOGIC TEST is provided in Technical Specification Section 1.2 as stated below:
"An ACTUATION LOGIC TEST shall be the application of various simulated input combinations in conjunction with each possible interlock logic state and verification of the required logic output. The ACTUATION LOGIC TEST shall include a continuity check, as a minimum, of the output device".
If a Technical Specification Surveillance Requirement is not performed, Surveillance Requirement 4.0.3 must be met. It states the following:
"Failure to perform a Surveillance Requirement within the allowed surveillance interval, defined by Specification 4 '.2, shall
FACILITY NAHE DOCKET NUHBER LER NUHBER PAGE NO.
TURKEY POINT UNIT 3 05000250 96-004-00 4 OF 7 constitute noncompliance with the OPERABILITY requirements foz a Limiting Condition for Operation. The time limits of the ACTION requirements are applicable at the time it is identified that a surveillance requirement has not been performed. The ACTION requirements may be delayed for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit the completion of the surveillance when the allowable outage time limits of the ACTION requirements are less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Surveillance requirements do not have to be performed on inoperable equipment".
Surveillance Requirement 4.0.2 that is referred to above states:
"Each Surveillance Requirement shall be performed within the specified time interval with a maximum allowable extension not to exceed 25% of the surveillance interval".
The AFW automatic start logic consists of 5 actuation signals: Bus Stripping, SI, Trip of SGFPs, AMSAC, and Low-Low Level on any SG. In order to determine if Technical Specification surveillance requirements of the AFW actuation logic was being satisfied, schematic and logic diagrams of the logic circuitry were compared against the associated test procedures to ensure all logic and parallel signal paths were being tested properly. The following summarizes the results of this design versus testing review.
The logic associated with Bus Stripping and SI is verified by simulating the actual process signals (i.e. Loss of 4KV Voltage, Hi-Hi Containment Pressure) during Integrated Safeguards Testing procedures 3/4-0SP-203.1,2.
The Trip of SGFPs logic is satisfied when both pump breakers are open and either pump control switch has been placed in the start position and returned to mid position. Therefore, this logic actuated AFW when either/both SGFPs have tripped oz one has tripped while the other has been manually stopped. The various combinations of switch positions are tested properly as well as independent actuation of each train of AFW circuitry by procedure 3/4-0SP-075.4.
The AMSAC auto start logic is not required to be tested by Technical Specifications. However, the AMSAC logic is tested via procedure 3/4-OSP-093.1 as directed by Operations or following design modifications or maintenance activities.
The Low-Low S/G Level logic for AFW start is derived from the same logic relays used in the Reactor Protection System (RPS) to initiate reactor trip.
Operation of these logic relays'oils and contacts which generate a reactor trip are tested on a monthly basis by procedure 3/4-0SP-049.1. However, the relay contacts used for the AFW start logic are not verified since its test relay contacts are wired in series to block AFW actuation. As a result, the AFW start logic is tested separately (on an 18 month basis) by procedure 3/4-0SP-075.4 by placing the Low-Low Level instrument loop bistable switches in test in order to actuate the logic relays. However, only channels 1 & 2 bistables are actuated on each S/G to simulate the Low-Low S/G Level signal.
In order to properly verify the 2/3 relay logic matrix, channels 1 & 3 and 2 3 bistables should also be actuated.
FACILITY NAME DOCKET NUNBER LER NUNBER PAGE NO.
TURKEY POINT UNIT 3 05000250 96-004-00 5OF7 ANALYSIS The Updated Final Safety Analysis Report (UFSAR) Chapter 14 accident analysis credits AFW for mitigation of several events. The following AFW related transients were reviewed: 1) Loss of Normal Feedwater Flow, 2) Loss of Non Emergency AC to Plant Auxiliaries, 3) Steam Generator Tube Rupture (SGTR), 4) Main Steam Line Break, and 5) Small Break LOCA. None of these transients rely on AFW initiation from bus stripping. The analyses assume AFW System actuation on SI or Low-Low SG Water Level.
The Loss of Normal Feedwater Flow transient is analyzed in Section 14.1.11 of the UFSAR. A loss of normal feedwater results in a reduction in capacity of the secondary system to remove the heat generated in the reactor core.
The analysis of the transient described in this section demonstrates that the AFW system is capable of removing the stored and residual heat, thus preventing either overpressurization of the Reactor Coolant System or loss of water from the reactor core, and returning the plant to safe condition.
The UFSAR analysis assumes that AFW flow is initiated three (3) minutes following a start signal on Low-Low SG level. This event specifically credits AFW initiation on Low-Low SG level. As a backup, the operator would also be expected to manually initiate AFW on a reactor trip at Step 7 of 3/4-EOP-E-O, which is one of the memorized immediate operator steps.
The Loss of Non-emergency A-C Power to Plant Auxiliaries is analyzed in Section 14.1.12 of the UFSAR The accident of record assumes that AFW is
~
initiated on Low-Low SG level. However, because this event also assumes a LOOP, both main feedwater pumps will trip on undervoltage and cause an AFW initiation on the main feed pump breakers opening. AFW will also be initiated on bus stripping for this event. Accordingly, the AFW Actuation System (AFAS) testing inadequacies did not affect plant response to this event.
The SGTR transient is analyzed in Section 14.2 4 of the UFSAR. AFW is initiated for the SGTR on a SI signal. Accordingly, the AFAS testing inadequacies did not affect plant response to this event.
The Main Steam Line Break transient is analyzed in Section 14.2.5 of the UFSAR. AFW is initiated for the steam line break on a SI signal.
Accordingly, the AFAS testing inadequacies did not affect plant response to this event.
The Small Break LOCA is analyzed in Section 14.3.2.2 of the UFSAR. AFW is initiated for the small break LOCA on a SI signal. Accordingly, the AFAS testing inadequacies did not affect plant response to this event.
Based on the preceding, the only event where AFW automatic initiation is not demonstrated by the conduct of the surveillance testing is the Loss of Normal Feedwater event resulting in initiation on Low-Low SG level.
Additionally, a normal reactor trip is expected to result in AFW initiation on Low-Low SG level.
This event is reportable under the requirements of 10 CFR 50.73(a)(2)(i)(B).
t t LICENSEE EVENT REPORT (LER) TEXT CONT INUATION FACILITY NAHE DOCKET NUHBER LER NUHBER PAGE NO.
TURKEY POINT UNIT 3 05000250 96-004-00 6 OF 7 As defined by 10 CFR 50.36, Limiting Conditions for Operation (LCO) are "the lowest functional capability oz performance levels of equipment required for safe operation of the facility. When an LCO of a nuclear reactor is not met, the licensee shall shut down the reactor or follow any remedial action permitted by the Technical Specifications until the condition can be met."
Implicit in this definition is that the lowest functional capability or performance levels of equipment be maintained assuming any credible single failure. As such, the principle purpose of LCOs is to ensure the preservation of single failure criteria by requiring all redundant components of safety systems be operable. When the required redundancy is not maintained, either due to equipment failure, maintenance, or surveillance testing, action is required within a specified time to shutdown the plant and/or perform actions to ensure a safe condition. This LCO action time is a temporary short term relaxation of the single failure criteria which is consistent with the overall system reliability, probability of the equipment function being required (i.e. LOOP Design Basis Accident occurring) during the specified time, and the safety significance of the inoperable equipment/system.
I Also, as defined by 10 CFR 50.36, "Surveillance Requirements aze requirements relating to test, calibration, or inspection to assure that the necessary quality of systems and components is maintained, that the facility operation will be within safety limits, and that the limiting conditions of operation will be met". This states that Surveillance Requirements support meeting LCOs.
GL 91-18 provides guidance on actions to be taken when a Technical Specification Surveillance is missed. The GL refers to the Standard Technical Specifications version of Surveillance Requirement 4.0.3 and which forms the basis for Surveillance Requirement 4.0.3 contained in the Turkey Point Technical Specifications. The GL version of 4.0.3 states in part that:
"Failure to perform a Surveillance Requirement within the specified time interval shall constitute a failure to meet the OPERABILITY requirements for a Limiting Condition of Operation...".
Surveillance Requirements and the "Action Logic Test" definition imply or intend that all signal/actuation paths be tested. The review of 3/4-OSP-075.4 showed that the signal/actuation paths for the steam generator low-low level AFW initiation signal was only tested foz one of three paths on each steam generator. This is inconsistent with the Turkey Point Plant testing that is performed on similar logic for both the RPS and ESFAS. Based on this difference, the existing testing performed was not considered sufficient to meet the intent of the Technical Specification surveillance, and Technical Specification 4.0.3 was entered and the required actions met ~
Additional testing that insured compliance with the Technical Specification surveillance requirements was implemented without a plant shutdown.
LICENSEE E'OlENT REPORT (LER) TEXT CONTZNUATXON FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 96-004-00 7OF7 While GL 91-18 and the Technical Specifications provide specific criteria to be followed when a surveillance is not met, there is a strong case that demonstrates that operability of the AFW system and its actuation logic was maintained even though surveillance testing had some inadequacies. All active components (e.g., relays, bistables) have been shown by existing testing to remain operable and capable of changing state. By testing of the RPS, the subject relays and contacts for the RPS have been shown to be operable. The primary aspect of testing that had not been met was showing those contact points foz AFW actuation for the remaining two out of three logic points are made up when required. These relays and their associated contacts are located in the Cable Spreading Room, which is a controlled environment. The contacts are open during normal operation, and are not subject to welding or other phenomenon that would result in their degradation. It is considered highly improbable that one set of relay contacts would remain functional and another set would fail to function.
Accordingly, on this basis, there was a high level of confidence that the untested portions of the steam generator low-low level AFW actuation circuitry were functional and capable of performing their design functions.
An analysis was performed to determine the change in Coze Damage Frequency (CDF) for failure of the AFW system to actuate in the event of a low-low level in the steam generators. The analysis increased the AFW pump common cause failure to start by a factor of one hundred to account for the actuation failure and assumed the probability of the operator's failure to turn on the AFW pumps while carrying out the Emergency Operating Procedure as 1.50E-02. The calculated CDF is 7.00E-07 which is below 1.00E-06, the screening criteria of the Electric Power Research Institute Pzobabilistic Safety Assessment Application Guide.
ZV. CORRECTIVE ACTIONS The untested portion of the Low-Low S/G Level AFW start logic was tested successfully on February 22, 1996.
- 2. Plant Procedures 3-0SP-075.4 and 4-0SP-075.4 will be revised to include all combinations of the 2/3 low-low steam generator level logic prior to the next performance of this surveillance.
V. ADDITIONAL INFORMATION A. Similar Events: None B. Additional Information: None EIIS Codes are shown in the format [EIIS SYSTEM: IEEE component function identifier, second component function identifiez (if appropriate)].