ML15118A198

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Insp Repts 50-269/97-01,50-270/97-01 & 50-287/97-01 on 970209-0322.Violations Noted.Major Areas Inspected: Operations,Engineering,Maint & Plant Support
ML15118A198
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 04/21/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A196 List:
References
50-269-97-01, 50-269-97-1, 50-270-97-01, 50-270-97-1, 50-287-97-01, 50-287-97-1, NUDOCS 9705080200
Download: ML15118A198 (30)


See also: IR 05000269/1997001

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270, 50-287, 72-04

License Nos:

DPR-38, DPR-47, DPR-55, SNM-2503

Report No:

50-269/97-01, 50-270/97-01, 50-287/97-01

Licensee:

Duke Power Company

Facility:

Oconee Nuclear Station, Units 1, 2 & 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

February 9 - March 22, 1997

Inspectors:

M. Scott, Senior Resident Inspector

G. Humphrey, Resident Inspector

N. Salgado, Resident Inspector

D. Billings, Resident Inspector

C. Rapp, Reactor Inspector (Section E3.1)

Approved by:

C. Casto, Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9705080200 970421

PDR ADOCK 05000269

G

.PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station. Units 1, 2 & 3

NRC Inspection Report 50-269/97-01,

50-270/97-01. 50-287/97-01

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a six-week

period of resident inspection: in addition, it includes the results of an

announced inspection by one regional inspector.

Operations

On February 12. Unit 1 returned to power operation with an

elevated vibration level on the 1A1 Reactor Coolant Pump (RCP)

that was analyzed to be acceptable for an interim period.

Management and controls for the startup were adequate. Problems

during the startup and power escalation were appropriately

addressed by the licensee. (Section 01.2)

On February 26, while in refueling conditions, Unit 3 experienced

a loss of Reactor Coolant System (RCS) inventory to the Letdown

Storage Tank (LDST). Core cooling was not jeopardized. The loss

was due to a valve mispositioning that is identified as a third

example of a previous violation (VIO 269,270.287/96-17-06) for

which corrective action had yet to be completed. (Section 01.3)

On March 6, Unit 3 achieved criticality after a 160 day refueling

outage. No problems were identified during the observation of the

criticality evolution or during low power physics testing.

Performance by Operations personnel was thorough and professional,

and Reactor Engineering provided appropriate guidance. (Section

01.4)

On March 21. the Unit 3 reactor tripped from approximately 70%

power. The unit trip recovery was well controlled by the reactor

operators. The post trip report was thorough and accurately

reflected the root cause of the trip. A procedural weakness was

identified in that Procedure IP/0/A/0305/014-1 did not include any

steps for ensuring that fuses were not open in the reactor trip

confirm circuitry. An Inspector Followup Item (IFI) was

identified to followup on the licensee's inspection of the Unit 1

and Unit 2 Reactor Trip Confirm Circuits to ensure proper fuse

installation/sizing. (Section 01.5)

Although .some water/steam hammers were noted during the Unit 3

startup, the licensees efforts were effective in minimizing this

problem. The automated control system performed well and

eliminated the need for manual operation of the valves with the

unit operating at power; and thereby eliminating the personnel

hazards involved with the manual operation. (Section 01.6)

Enclosure 2

2

Maintenance

The inspectors concluded that the general Maintenance and

Surveillance activities observed were completed thoroughly and

professionally. (Section M1.1)

The licensee adequately identified and corrected an incorrectly

assembled emergency feedwater pump turbine steam admission valve.

Post modification testing was pending due to the unit status.

(Section M8.3)

A violation was identified in which Maintenance personnel did not

comply with the requirements of a valve repair procedure while

working on multiple Appendix "R" valves.

(Section M8.1)

Engineering

As part of the licensee's Generic Letter 96-06 activities, a

special Low Pressure Service Water (LPSW) test was adequately

performed with good engineering cooperation and support. The

results were acceptable and provided the licensee a better

understanding of plant response in Loss of Offsite Power

.(LOOP)/Loss of Coolant Accident (LOCA) conditions.

(Section E1.1)

The inspectors concluded that Unit 3 Integrated Control System

(ICS) testing (two sections of TT/3/B/0326/001 and all of

TT/3/B/0326/002) was satisfactorily performed in accordance with

the licensee's test procedures, and that deficiencies identified

during the testing were resolved appropriately. Control of all

test activities was considered good. Positive observations were

made.relating to test briefings, control room briefings, and

communication and coordination of the test evolutions.

(Section

E1.2)

Post validation and verification changes to Unit 3 ICS software

resulted in an error being introduced. This occurrence resulted

in a minor plant perturbation but was discovered in the system

testing phase. The occurrence was considered a substantial

weakness in the overall ICS modification process. An IFI was

initiated to.follow the corrective actions associated with this

occurrence, which will take place during planned ICS modifications

on the other two units.

(Section E3)

As a fallout from the licensee's Generic Letter 96-06 evaluation

efforts, two 10 CFR 50.72 reports were made this period. One

concerned the water hammer susceptibility of LPSW piping to the

Reactor Building Cooling Units. The other involved the potential

for thermal pressurization making the active boron dilution flow

path valves inoperable. The inspectors assessed the compensatory

Enclosure 2

3

actions taken and identified two Unresolved Items with respect to

each issue. (Section E8.2)

Plant Support

An unresolved item was identified in which the licensee did not

meet the requirements of 10 CFR 70.24, Criticality Accident

Requirements. (Section R2.1)

Enclosure 2

Report Details

Summary of Plant Status

Unit 1, which had been shutdown in early October 1996 for secondary piping

of inspections and water hammer.modifications, was tied to the grid on

February 12, 1997. It subsequently operated at or near full power throughout

the rest of the reporting period.

Unit 2 operated at or near full power throughout the reporting period.

During this inspection period the licensee completed the Unit 3 End of Cycle

16 refueling outage. The outage length was 160 days. The principal causes

for the extension of the outage were secondary piping inspections and water

hammer reducing modifications. Unit 3 achieved criticality on March 6. 1997,

and increased power to specified power levels for Integrated Control System

(ICS) testing. While holding at 70%.power for ICS testing on March 20, 1997,

the unit tripped. It was subsequently restarted on March 21, 1997.

Review of UFSAR Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the Updated Final Safety Analysis Report (UFSAR)

that related to the areas inspected. The inspectors verified that the UFSAR

wording was consistent with the observed plant practices, procedures, and/or

parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general, the conduct of

operations was professional and safety-conscious. Specific events and

noteworthy observations are detailed in the sections below.

01.2 Unit 1 Startup

a. Inspection Scope (93702, 71707).

The inspectors observed various phases of the Unit 1 return to power

operations and attended associated pre-job briefs for each major

evolution.

b. Observations and Findings

Unit 1 was connected to the electrical grid on February 12, without any

major problems. The secondary experienced a few minor water hammers

Enclosure 2

2

that were observed, in part, by the inspectors. These minor water

hammers were similar to those previously experienced by Unit 2. which

had recently also returned from outage conditions with a modified

secondary. The licensee captured the occurrences within their

corrective action program. As with Unit 2 (see Inspection Report 96

20), the licensee's engineering staff observed and evaluated the plant

secondary as it went through power transition. Procedure changes

associated with equipment changes, equipment and piping changes

themselves, and operator training had occurred prior to the restart.

The 1A1 Reactor Coolant Pump (RCP) vibrations, that were elevated during

preparations for startup, persisted into normal power operations.

Vibration levels were evaluated by the licensee and reviewed by the

inspectors prior to any power escalation. The mis-alignment vibration

which was due to transitional change in pump parametric performance was

understood and appropriately documented in a 50.59 evaluation and

Problem Identification Process (PIP) Report 1-97-568. The evaluation

recognized that the running of the pump would be limited and Unit 1

would be shutdown for repair of the RCP after Unit 3 was at power, which

was initially scheduled for March 14, and then rescheduled for March 28.

1997.

Control rod drop times prior to returning to power operations were

observed and found to be acceptable with three control rod drop times

slightly exceeding the licensee's refueling outage restart

administrative limit. The licensee evaluated the condition and, in

light of the remaining core life fuel/operational time, the licensee

considered them acceptable.

c. Conclusions

Management and controls for the Unit 1 startup were adequate. Problems

encountered during startup and power escalation were appropriately

handled.

01.3 Valve 3HP-5 Mispositioning

a: Inspection Scope (93702)

During the inspection period, Unit 3 had a loss of Reactor Coolant

System (RCS) inventory event. The inspectors were alerted to its

occurrence by the licensee and followed the details of the

investigation.

b. Observations and Findings

While returning from Unit 3 outage conditions on February 20, Operations

performed Enclosure 3.7, Procedure for Establishing Low Pressure

Injection (LPI) Purification, of OP/3/A/1104/04, Low Pressure Injection

Enclosure 2

System. Step 2.2 of the Enclosure. Purification Lineup, verified that

Valve 3HP-5 (first letdown isolation valve off the RCS) was closed.

On February 26. the RCS was at 40 psig on a pressurizer nitrogen bubble

with RCS temperature at 108 degrees F. Further into the preparation for

return to power operations, the High Pressure Injection (HPI) system was

being aligned for return to service in accordance with OP/3/A/1104/02,

High Pressure Injection System, Enclosure 5.1, HPI System Startup. Step

2.3 of that enclosure opened 3HP-78, Letdown Storage Tank (LDST) Inlet

Stop Check. When this valve was opened, approximately 720 gallons of

water from the RCS (as indicated by pressurizer level drop)

inadvertently flowed into the LDST before being identified and isolated

by Operations personnel. The flow persisted from 3:19 to 4:30 a.m. when

Valve 3HP-5, had been discovered opened and was closed. Venting of the

HPI pumps was also in progress at the time. Pressurizer level went from

105 inches to 76 inches.

The amount of water removed from the RCS did

not challenge Decay Heat Removal (DHR) capability. Within approximately

20 minutes Operations made up to the RCS to partially refill the

pressurizer to a level greater than existed before to the event (120

inches)..

The LDST level went up from 83 inches to 100 inches (the maximum tank

level). LDST pressure reached a maximum of approximately 50 psig which

was well below the setpoint of LDST relief Valve 3HP-79. It was also

noted that the volume in the Bleed Holdup Tank (relief valve discharge

point) did not change.

On February 26, prior to opening 3HP-78, an operator had performed step

2.1 of Enclosure 5.1 (OP/3/A/1104/02) that directed the operator to

"Complete the following check lists".

Enclosure 5.15 of Procedure

OP/3/A/1104/02, which was contained in/listed under step 2.1, checked

Valve 3HP-5 closed. Enclosure 5.15 was last completed in the December

10 - 20, 1996, time frame. No procedural guidance had been provided to

the operators regarding valve checklist performance frequency. Normal

Operations' practice was that if the list had been performed the same

post outage time period, no repetition of list performance need occur

since the licensee's system removal and restoration tagout process would

be used to maintain system configuration control. The operator

performing Enclosure 5.1 knew that Enclosure 5.15 had been performed in

December and he believed that was sufficient information to proceed with

the system startup lineup.

After the Unit 3 RCS inventory loss to the LDST, Operations re-performed

a number of Emergency Core Cooling System (ECCS) valve checklists. None

of the re-checks identified any of the valves out of position. A

computer historical data base on plant valve position indicated that

3HP-5 was opened in lieu of being closed as required during performance

of Procedure OP/3/A/1104/04, Enclosure 3.7 on February 20.

Enclosure 2

4

The above misposition event, in conjunction with those previously

identified in Violation 50-270/96-17-06 and Non-Cited Violation 50

269/96-13-01, indicates .a

potential negative trend in valve

mispositioning problems. The licensee, who had reached the same

conclusion regarding the negative trend, had yet to complete the

corrective'actions indicated in their response to Violation 50-270/96

17-06 (dated February 26, 1997).

Paragraph 3 of the response indicated

that actions would be continuing under a licensee's Continuous

Improvement Team. The licensee recently formed a Continuous Improvement

Team to evaluate the problem and the inspectors have been tracking the.

actions of Operations and the team. The licensee has elicited response

from the operators and is drafting additional procedural guidance on

configuration control.

Continuing future actions for valve

configuration during Maintenance is also addressed in the violation

response. Accordingly, as these 'corrective actions are still underway,

this most recent mispositioning event will be dispositioned as another

example of a cited violation 50-270/96-17-06, Failure to Maintain

Configuration Control.

c. Conclusions

The licensee had a recent significant mispositioning event that

persisted for some period of time prior to the control room staff

discovering it. This situation was mollified by plant conditions (low

RCS pressure) and LDST status (intact with its relief valve functioning

as required). The event follows on the heels of a previous event

similar in nature and corrective action. The licensee has responded to

these configuration control issues and was taking actions to address a

potential negative trend.

01.4 Unit 3 Startup Activities

a. Inspection Scope (71707)

The inspectors observed the Unit 3 startup evolution to assess control

room operations and operator decorum.

b. Observations and Findings

On March 6, at 1:30 p.m., the inspector attended the pre-job briefing on

the startup evolution conducted by the Operations Shift Manager (OSM)

and the lead reactor engineer. Procedure OP/3/A/1102/01, Controlling

Procedure For Unit Startup, provided the guidance for the unit startup.

The inspector concluded that the briefing was conducted thoroughly with

appropriate emphasis on safety.

On March 6, 1997, Unit 3 achieved criticality. It was noted that a

trainee withdrew the control rods under appropriate supervision.

Reactor engineers, performing 1/M plots after the withdrawal of the

first four banks of control rods, interfaced with operations during the

0

Enclosure 2

5

control rod withdrawal evolution. The frequency of the 1/M plots

increased as the unit was approaching criticality. Reactor Engineers

then performed 0% power physics testing, which did not identify any

problems.

Due to several Integrated Control System (ICS) questions that were

raised during the low power ICS tuning, the licensee decided to evaluate

the need to make a design change to the new ICS modification (see

Section E3.1).

Power escalation was held at approximately 70% power for

ICS tuning on March 20, at which time Unit 3 experienced a reactor trip

during Reactor Protection System (RPS) Testing (see Section 01.5).

c. Conclusion

The inspector concluded that the restart of Unit 3 was conducted

thoroughly and professionally by Operations personnel. Reactor

engineering personnel provided appropriate guidance as necessary.

01.5 Unit 3 Reactor Trio

a. Inspection Scope (93702)

The Unit 3 reactor tripped from approximately 70% power on March 20,

1997, at 9:12 a.m..

The inspector was in the control room immediately

following the reactor trip and observed operator responses. The

inspector also reviewed the post trip report, procedures, and applicable

PIPs.

b. Observations and Findings

Prior to the unit tripping, the licensee was performing Procedure

IP/0/A/0305/014-1., RPS Control Rod Dri*ve Breaker Trip and Events

Recorder Timing Test. The licensee had completed testing Control Rod

Drive (CRD) breaker 10, and had returned RPS Channel A to its normal

state. When RPS Channel B was placed in manual bypass for testing. CRD

breaker Number 11 was tripped and the reactor trip subsequently

occurred. The licensee's post investigation determined that the cause

of the trip was due to an electrical short to ground which occurred in

the circuit associated with Relay K3 in the Reactor Trip Confirm A

logic. The licensee discovered the short at electrical connector J2 of

the Electronic Trip Enclosure in the CRD Group 5 regulating power-supply

cabinet. Threads on a screw which secured a clamp at the back of the

electrical connector had cut into the insulation of one of the wires

entering the connector. This was original Oconee installed equipment.

When the electrical short to ground occurred (measured later at 0.6 ohms

to ground), sufficient fault current existed to open Fuse F3. This

nonsafety-related fuse provides branch circuit protection for the K3

relay circuit and isolates a fault in this circuit.

When the fault

occurred, the fuse performed its intended function by opening to isolate

this fault.

The result was that Relay K3 de-energized, which provided a

Enclosure 2

6

trip signal to the reactor trip confirm A logic circuit.

Channel A trip

confirm generated a generator backup lockout which opened the generator

breakers PCBs 58 and 59. This caused a turbine trip due to power/load

unbalance which caused a reactor trip.

Post trip response was normal with the exception of the loss of 3X1 and

3X3 nonsafety-related switchgear. Following the trip, load center 3X1

and 3X3 feeder breakers opened. The licensee's investigation found that

the reactor trip confirm signal tripped the generator breakers, but not

the generator. The generator was tripped 0.75 seconds later after a

backup timer timed out and energized the shutdown lockout relay. This

caused a power transfer which allowed the undervoltage relays for 3X1

and 3X3 to operate and trip the load centers. All equipment operated as

designed. The licensee generated PIP 3-097-1013 to evaluate the time

setting for the backup timer.

The licensee discovered that the F3 fuse opening and the K3 relay de

energization were not alarmed to any type of remote indication. The

only indication of this is a "blown-fuse" indicator on the F3

fuseholder. 'This indicator would normally illuminate if the fuse was

blown. These fuses are located inside a cubicle located above the AC

Reactor Trip Breaker cabinets which were not normally observable. The

blown-fuse indicator, a light, associated with fuse F3 was also non

functional and in the same cubicle. These conditions could have existed

since the completion of the last performance of Procedure

IP/0/A/0305/014-1 on February 20, 1997.

The procedure for performing the testing did not include any steps for

ensuring that no fuses were open in the reactor trip confirm circuitry.

This was identified as a procedural weakness. Steps will be added to

the procedures (Units 1, 2, and 3) for reactor trip breaker testing to

ensure that visual inspections for blown fuses in the reactor trip

confirm circuitry will be made prior to initiating any testing-related

breaker trips.

An additional item observed during the investigation involved

discrepancies with the fuses installed in the redundant trip confirm

circuitry. The licensee initiated PIP 0-097-1014 to resolve these

discrepancies. It was noted that two vendor drawings which show these

nonsafety-related (but important to safety) fuses are in disagreement as

to the proper fuse size for fuses F1-F4. One drawing showed them to be

0.5 Amp(A) fuses and the other drawing showed them as 0.25A slow blow

fuses. It was determined that the 0.25A fuses were the correct size.

The licensee will revise the vendor drawings to show the correct fuse

sizes in the near future. It was also noted that the fuses installed in

the field were not the correct size. Of the eight fuses installed, six

of them were 1.OA fuses and two were 0.5A fuses. The licensee

determined that the larger size fuses would have adequately protected

the circuitry. The licensee will conduct an inspection of Unit 1 and 2

Reactor Trip Confirm circuit fuses to ensure that the correct fuses are

Enclosure 2

7

installed at the next available opportunity. Inspector Followup Item

(IFI) 50-269,270/97-01-01, Reactor Trip Confirm Circuit Fuse Inspection,

will be used to follow this issue.

The unit trip recovery was well controlled by the reactor operators. A

four-hour non-emergency 10 CFR 50.72 notification was made in a timely

manner by the licensee. Unit 3 remained at hot shutdown during the

investigation process. The inspector reviewed the licensee's trip

report and attended the Plant Operating Review Committee meeting for

evaluating the trip and authorization for restart.

The unit was restarted on March 21. 1997, with no noted problems.

c. Conclusions

The Unit 3 trip'recovery.was well controlled by the control room

operators. The post trip report was thorough and accurately reflected

the root cause of the trip. A procedural weakness was identified in

that Procedure IP/0/A/0305/014-1 did not include any steps for ensuring

that fuses were not open in the reactor trip confirm circuitry. Because

of the incorrect sized fuses found in Unit 3, an IFI was identified to

followup on the licensee's inspection of the Unit 1 and 2 Reactor Trip

Confirm Circuits.

01.6 Unit 3 Heater Drain System Modifications

a. Inspection Scope

Review of the Unit 3 modified heater drain system and operating

procedure revisions for plant startup and operation.

b. Observations and Findings

The inspector reviewed the implementation of the Unit 3 modified heater

drain system and associated equipment that was modified per NSM ON

32941. The modification was a result of a water/steam hammer incident

that caused a steam drain pipe rupture in Unit 2 on September 24, 1996.

All three of the Oconee units were modified as a result, in an attempt

the eliminate water/steam hammers in the system. Post modification

testing was performed during unit restart. A problem report. PIP 0-096

2420, was generated to document and track recommendations based on the

investigation and analysis of the steam line break and track the issues

until corrective actions were completed. The modifications and

procedure upgrades have been completed on all three units and Units 1

and 2 were returned to service at earlier dates.

Approximately 25 procedures were revised for each unit. The inspectors

performed a random sampling of the procedures that were initiated or

revised due to the modifications. This review was performed for each

unit prior to restart and included administrative controls for procedure

Enclosure 2

8

changes such as administrative hold instructions. It also involved

verifying that the latest procedure/revision had been placed in.the

control room for operator use.

A walkdown of the plant steam reheat and drain system was performed by

the licensee's engineers and the inspectors during the Unit 3 restart.

Some water hammers were noted during startup of the main turbine, which

was similar to those noted during the restart of Units 1 and 2. PIP 3

097-0922, was generated to document the issue and specify corrective

actions. The corrective actions require some minor modifications and

procedure revisions to further refine the secondary system operation on

all three units.

c. Conclusions

Although some water/steam hammers were noted during the plant startup,

the licensees efforts were effective in minimizing this problem. The

automated control system performed well and eliminated the need for

manual operation of the valves with the unit operating at power: and

thereby eliminating the personnel hazards involved with the manual

operation.

02

Operational Status of Facilities and Equipment

02.1 Engineered Safety Feature System Walkdowns

a. Inspection Scope (71707)

The inspectors used Inspection Procedure 71707 to walkdown accessible

portions of the following safety-related systems:

Keowee Hydro Station

Unit 3 HPI System.

Unit 1 and 3 Low Pressure Service Water (LPSW) System

Unit 1, 2 and 3 Penetration Rooms

Unit 1, 2 and 3 Condenser Circulating Water (CCW) Pump and Intake

Structure

Unit 1, 2 and 3 Electrical Equipment Rooms

b. Observations and Findings

Equipment operability, material condition, and housekeeping were

acceptable in all cases. Several minor discrepancies were brought to

the licensee's attention and were corrected. The inspectors identified

no substantive concerns as a result of these walkdowns.

On February 25, 1997, the inspectors conducted a safety inspection of

the Unit 3 Reactor Building (RB) prior to the Unit startup. The

inspectors performed an inspection of the Unit 3 RB after Quality

Assurance (QA) had performed their final walkdown. Several minor

Enclosure 2

9

discrepancies were identified to the licensee for resolution. The items

were evaluated prior to the Unit 3 startup and resolved as necessary.

05

Operator Training and Qualification

05.1 Unit 3 Integrated Control System (ICS) Training

a. Inspection Scope (71707)

On February 15, 1997, the inspector attended the classroom portion of

the operator training provided on TT/3/B/0326/001, ICS/NNI Transient

Testing at Power: ICS/NNI System Upgrade, NSM ON-32989/AL1 and

TT/3/B/0326/002, ICS Loss of Power Testing at 25% Reactor Power: ICS/NNI

System Upgrade, NSM ON-32989/AL1.

b. Observations and Findings

The training. was provided to one reactor operator and one senior reactor

operator from each shift, with all shifts being represented. The

terminal objective of the "just in time" training was to demonstrate the

ability to perform TT/3/B/0326/001, and TT/3/B/0326/002 in accordance

with the applicable guidelines of each of these procedures. The

operators questioning attitude led to numerous changes to both draft

procedures. The training included performing the procedures on the

simulator, including taking actions as necessary per contingency plans.

c. Conclusions

The inspector concluded that the "just in time" training was conducted

thoroughly and professionally. The operators' questioning attitude led

to numerous changes to both draft procedures.

08

Miscellaneous Operations Issues (92901)

08.1

(Closed) Licensee Event Report (LER) 50-269/95-001-00:

Potential

Unanalyzed Main Steam Line Break Scenario

The circumstances described in this voluntary LER were documented in

Inspection Report 50-269,270,287/95-01 and were to be tracked by

Deviation 269,270,287/93-31-01. The subject deviation was closed in IR

50-269,270,287/95-09; therefore, this LER is closed.

Enclosure 2

  • 10

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726, 62707, 92902)

The inspectors observed all or portions of the following maintenance and

surveillance activities:

OP/1/A/1106/02

Enclosure 3.17 Taking 1B Feedwater Pump Turbine

(FWPT) Off Hand Jack

PT/1/A/600/12

Turbine Driven Emergency Feedwater Test

PT/O/A/0300/01

Control Rod Drive Trip Time Testing

WR # 97007993:

I/R U-1 Bias Control on 1B FDW Pump

TT/2/B/027/012

Controlling Procedure for NSM 22941 for Testing

& Tuning Controllers Associated With 2MS-112,

2MS-173, 2HD-92, 2HD-95, 2HD-37, 2HD-52.

TT/3/A/025/63

LPSW Flow Test

0II)OP/0/A/1105/09

Recovery of a Dropped/Misaligned*Safety Control

Rod, Enclosure 14.9

TT/3/A/160/19

Start 3A Reactor Building Cooling Unit (RBCU) in

Fast Speed

IP/.0/A/0100/001

Attachment 1. Trouble Shooting Plan, ICS Testing

Procedure

0

TT/3/B/0326/001

ICS/NNI Transient Test at Power

0

OP/3/A/1106/06

Enclosure 3.2, Emergency Feedwater Pump Turbine

Overspeed Test

0

IP/0/A/4980/027G ITE 27N Relay Test

0

WO 96060767

PM Yellow Bus Degraded Grid UV Relay 27YBDGX

WO 96036418

Perform the #3 Main Steam Relief Valve (MSRV)

Setpoint Pop Test

OP/0/A/1106/19

Keowee Hydro At Oconee, Enclosure 3.6,

Operabili.ty Verification

Enclosure 2

11

WO 96103330

Perform Mulsifyre System Annual "Wet" Test

WO 97018361

Unit 2., RPS A. B, C. D CRD Breaker Test

IP/0/A/2005/003

Keowee Hydro Station - Westinghouse WTA Voltage

Regulator Test

OP/3/A/1006/01

Enclosure 3.18, Turbine Overspeed Testing During

Startup

WO 96072589

Unit 1. Reset RPS HI Flux Trip Set Point To

104.75%

WO 97010420

Unit 2, RPS A, B, C. D CRD Breaker Test

WR 97007698

Unit 2, Assist In Tuning HD/MSRH Drain Tank

Levels

WO 96083444

Unit 3, RPS A, B. C, D CRD Breaker Test

WO 97003881

Unit 3. Replace Pressure Transmitter, 3PT 41B

b. Observations and Findings

The inspectors found the work performed under these activities to be

professional and thorough. All work observed was performed with the

work package present and in active use. Technicians were experienced

and knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

c. Conclusion

The inspectors concluded that the Maintenance and Surveillance

activities listed above were completed thoroughly and professionally.

M1.2

Unit 3 Emergency Feedwater Pumo Turbine Overspeed Test

a. Inspection Scope (62707)

The inspector observed the licensee's first attempt to perform procedure

OP/3/A/1106/06. Emergency Feedwater Procedure, Enclosure 3.2 Emergency

Feedwater Pump Turbine (EFWPT) Overspeed Test, and associated PIPs.

b. Observations and Findings

On February 18, 1997, during the performance of Procedure

OP/3/A/1106/06, Enclosure 3.2, at step 2.18, Operations halted the test,

and identified that a procedure change was required to reset the trip on

Enclosure 2

12

Valve 3MS-94 (EFWPT Stop Valve) in order for the system to operate.

During the re-performance of the overspeed test it appeared that Valve

3MS-93 (EFWPT Steam.Admission Valve) operated backwards. The licensee

initiated PIP 3-97-639 to investigate the problem. Upon further

investigation the licensee determined that 3MS-93 was set up to fail

closed rather than fail open.

Valve 3MS-93 was disassembled and reassembled during the Unit 3 outage

under Work Orders 96036488 and 95093317. Maintenance personnel failed

to follow Procedure MP/0/A/1200/33, Valve - Fisher - "U" Design - 300

Pound and 16 Inch 150 Pound Vee-Ball - Disassembly, Repair and Assembly,

on step 11.4.17 and 11.4.24. If steps 11.4.17 and 11.4.24 of

MP/0/A/1200/33 had been performed correctly, 3MS93 would have operated

as designed. The licensee had not retested the valve to that point

because of the plant status. The retest, which scheduled via WO 95093317 to be performed after the overspeed test, would have identified

the problem. The licensee's corrective action to disassemble and

reassemble the valve was completed under WO 97007963.

Conclusion

The inspector concluded that the licensee adequately identified and

corrected the incorrectly'assembled 3MS-93 EFWPT Steam Admission Valve.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed) Unresolved Item (URI) 270.287/96-17-07: Incorrect Electrical

Connection of 2LP-1, 2LP-2, 3LP-1, and 3LP-2

This item concerned the discovery of incorrect wiring to the motor

operators on four Low Pressure Injection Loop (LPI) Suction Valves on

Unit 2 and Unit 3. The wiring leads were rolled at the Motor Control

Center (MCC) and at the valve. The licensee determined that this

allowed the valve to operate correctly from the Control Room, but would

have operated in the reverse direction if an intervening temporary

Appendix R panel had been installed and used during a hypothetical

event. The licensee postulated that if the motor operated in reverse

during an Appendix R event, the motor would have driven the valve into

the seat, tripped the breaker, and damaged the motors such that the

valves would not have opened electrically. This would have rendered the

valves, and therefore, the LPI system inoperable for decay heat removal.

Since these valves are located in the containment, they would have been

inaccessible until a Reactor Building entry could have been made. Decay

heat removal under these postulated conditions would have been

accomplished using the Safe Shutdown Facility, Auxiliary Feedwater Pump,

and the Steam Generators. The additional time could have prevented the

unit from being in cold shutdown within the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> per the Appendix R

requirements.

Enclosure 2

13

Technical Specification (TS) 6.4.1 requires that the station be

maintained in accordance with approved procedures. To the contrary,

the station was not maintained in accordance with Instrumentation

Procedure IP/O/A/3001/010, Maintenance of Limitorque Valve Operators.

Specifically, for an indeterminate time since the compliance audit with

Appendix "R" in 1987, the phases at the MCC and the valve operator for

LP-1 and LP-2 on Units 2 and 3 were reversed at the MCC. Accordingly,

the URI will be closed and this violation (VIO) of valve electrical

configuration control will be identified as VIO 50-270,287/97-01-03,

Failure to Follow Procedure.

M8.2 (Closed) VIO 50-270/96-13-10: Failure To Perform An Adequate 10 CFR

50.59 Evaluation

This violation was identified during a review of the completed

modification ONS-22975, Replace HPI Check Valves 2HP-126. 2HP-127. 2HP

152, and 2HP-153. The review of the modification identified the lack of

a fatigue analysis. This had generic implications for all three units.

The violation was discussed in IR 50-269,270,287/96-20 for Unit 2.

During this inspection period, the inspector reviewed the corrective

actions for identification and evaluation of the modifications for Units

1 and 3. The evaluations for Units 1 and 3 were completed prior to unit

startup. The inspector did not identify any weaknesses or deficiencies.

This item is considered closed.

M8.3 Institute of Nuclear Power Operations (INPO) Report Review

During the inspection period, the inspectors reviewed the most recently

completed INPO report that had been performed this period by

representatives from the World Association of Nuclear Operators. The

findings of the report, which spanned the dates of inspection from

September 30 to October 11, 1996. were consistent with NRC findings of

the last 18 months. The last INPO visit/inspection had been in January

1995.

III. Engineering

El

Conduct of Engineering

E1.1 LPSW Containment Piping Tests

a. Inspection Scope (37551, 61726)

Generic Letter (GL) 96-06 water hammer issues which were discussed in

Inspection Report 96-20 were further investigated by the licensee during

this inspection period (PIP 97-311). The licensee performed tests on

the outage unit similar to their normal LPSW ES tests with new

additional instrumentation. The tests were collecting data for input

Enclosure 2

14

into the LPSW piping model.

The inspector observed all of the test/data

collection.

b. Observations and Findings

On February 22, an adequate pre-job brief was held regarding details of

Test Procedure TT/3/A/025/63, LPSW Flow Test, and personnel involvement

during the evolution. Prerequisites for this Unit 3 test had been

established prior to the test. Operations clearly understood their part

in the test. With appropriate communication established, engineering

personnel were located in the RB, by the LPSW pumps, and in the piping

penetration room for the data collection and observation of potential

LPSW piping movement. The inspectors observed all three data collection

runs from the control room and then from the piping penetration room.

As part of the prerequisites, instrumentation had been hooked up to LPSW

piping test points. The instrumentation was to collect hydraulic

pressure pulse data on the piping leading into the RB (to the RBCUs) and

the associated return piping. A vendor, who was an expert in water

hammer evaluation, had hooked up computers to the instrumentation to

monitor and analyze the hydraulic data.

Test performance and data collection went smoothly. The single running

LPSW pump was shut off for 33 seconds and then restarted.on three

separate data runs. Data collection began before the pump was shut down

and ended two minutes after the restart. The actual water column

rejoining pressure pulses were well below the licensee's computer RELAP

5 Model bounding values with short duration pressure spikes of

approximately 125 to 135 psig. Very little piping movement was observed

(on the order of less than !12 inch side to side). The collected

information will be evaluated for inclusion into or in the tuning of the

RELAP-5 Model predictions.

c. Conclusions

The overall LPSW test was performed professionally with good engineering

cooperation and support. The results were acceptable and provided the

licensee a clearer understanding of plant response in Loss of Offsite

Power(LOOP)/Loss of Coolant Accident (LOCA) conditions.

0

Enclosure 2

15

E1.2 ICS Testing

a. Inspection Scope (61726, 62707, 61701)

The inspectors observed complex post modification testing of the new

Unit 3 ICS.

b. Observations and Findings

Testing Objectives

The testing was being controlled by two separate temporary tests,

TT/3/B/0326/001, ICS/NNI Transient-Testing at Power: ICS/NNI System

Upgrade, NSM ON-32989/AL1 and TT/3/B/0326/002, ICS Loss of Power Testing

at 25% Reactor Power: ICS/NNI System Upgrade, NSM ON-32989/AL1.

Procedure TT/3/B/0326/001 was written to test the functional

requirements of various features of the ICS. The scope of the test

included functional verification of the design basis ICS response to a

turbine trip at 15% power, a loss of electrical lOaD at 25% power, a

feedwater pump trip at 70%, a maximum runback transient from 65% to 50%

power, and a reactor coolant pump trip from 50% power. Procedure

TT/3/B/0326/002 was written to test the functional requirements of the

ICS/NNI system to cope with loss of ICS HAND and loss of ICS AUTO power.

The scope of the test involved tripping the ICS HAND circuit breaker.

verifying the response, then restoring ICS HAND power. Then the test

involved tripping the.AUTO circuit breaker, verifying the response, then

restoring AUTO power.

Conduct Of Testing

Test Preparation Activities

Refer to Section 05.1.

Pre/Post-Test Briefing

Prior to each test section (for both tests), the licensee conducted pre

test briefings for all personnel involved in the testing.

Pre-test

briefings were conducted by the manager (or his designee), who was

assigned oversight of the test, and a test coordinator. The manager

emphasized safety and.control room decorum during his briefs. The test

coordinator focused on the test evolution control and communications.

The inspector considered the pre-briefs to be thorough and with the

appropriate focus on nuclear safety.

After .completion of each test, a post-test brief was conducted by the

test coordinator with all personnel involved in the test. The briefs

focused on data acquisition results, test acceptance criteria, lessons

learned, necessity for procedure changes prior to.continuing, and other

Enclosure 2

16

concerns. The inspectors considered the test post-briefs to be

thorough, and they appropriately addressed issues requiring resolution

prior to continuation of testing.

Control Room Activities

The inspectors monitored testing activities from the Unit 3 control

room. The test coordinator and management designee was located in the

Unit 3 control room for all testing. Command and control in the control

room during all testing was good. Control room briefings for the

Operations crew were conducted by the Unit 3 shift management team prior

to initiation of each test section for both tests. Good communication

and coordination were noted. The test coordinator maintained good

control of all test evolutions. The inspectors concluded that testing

activities conducted.in the Unit 3 control room were good and operators

maintained appropriate focus on nuclear safety at all times.

TT/3/B/0326/001 Test Results

The licensee performed the first two test sections of this procedure

during this inspection period:

Turbine Trip At 15% Power

The licensee conducted the turbine trip at 15% power on March 14,

1997. All acceptance criteria was met for this test. Minor

discrepancies were noted, and resolved appropriately.

Load Reject Test

During the test, the Operations Senior Reactor Operators (SROs)

and test coordinator maintained good control of the overall

evolution. Operations personnel were well focused and understood

the test details, as well as their roll in test performance. At

the time of the test, the plant was stable with all prerequisites

met. At the point of the Main Turbine Generator (MTG) load

rejection, the inspector was in position at the MTG front standard

to observe the I&E rotating element speed instrumentation and Non

Licensed Operator (NLO) performance in case the .MTG over-sped with

the loss of load. Upon the loss-of load, the turbine control

valves closed and element speed approached within 4 RPM of the MTG

mechanical trip point, leaving the MTG running in an unloaded

condition. This was acceptable. Speed subsequently returned to

its normal setpoint value of 1800 RPM. The inspector proceeded

down the side of the turbine observing that the intercept valves

had closed as required and that bypassed steam that was no longer

entering the control valves had been appropriately diverted to the

condenser via the steam bypass valves. The MTG-ran very smoothly

through out this test.

Enclosure 2

17

Satisfied that the MTG and its associated equipment had performed

well and had responded to the ICS and Electro-Hydraulic Control

(EHC) system (on a loss of load EHC took over for many MTG control

functions), the inspector entered the control room to observe how

the ICS and reactor had responded to the perturbation. The

control room annunciator boards exhibited only three minor and

expected statalarms that resulted from the test parametric

changes. As anticipated by the test procedure, feedwater, Once

Through Steam Generator (OSTG) level controls, and reactor

controls were still in automatic and controlled in an expected

manner. RCS Tavg had risen one degree Fahrenheit, which was well

within expectations. The operators electrically reloaded the MTG

and resumed power escalation to 25% power.

The inspectors observed that the load rejection test met all

acceptance criteria. The Operations personnel, who were well

supported by other plant staff., performed the test in a controlled

manner.

TT/3/B/0326/002 Test Results

On March 15, 1997, the inspector observed the performance of Procedure

TT/3/B/0326/002 in the control room. Unit 3 was at 25% power for this

test which was within the required band described in the procedure. All

acceptance criteria was met for the Loss of HAND Power Test and for the

Loss of AUTO Power Test. Minor discrepancies were identified, and

evaluated by Engineering and Operations.

c. Conclusions

The inspectors concluded that the ICS testing (two sections of

TT/3/B/0326/001 and TT/3/B/0326/002) was satisfactorily accomplished in

accordance with the licensee's test procedures, and that deficiencies

identified during the testing were resolved appropriately. Control of

all test activities was good. Positive observations were made relating

to test briefings, control room briefings, and communication and

coordination of test evolutions.

E3

Engineering Procedures and Documentation

E3.1 Unit 3 ICS Tuning - Post Modification

a. Inspection Scope (37550, 37551)

The inspectors observed operational tuning and testing of the ICS

modification installed in Unit 3. During the performance adjusting or

tuning phase of the ICS modification prior to the testing addressed in

Section E1.2 above, the Engineering staff induced a problem in the

evolution. The inspectors followed up on the investigation and

identified problem resolution.

Enclosure 2

18

b. Observations and Findings

During the period of tuning, with the Unit 3 ICS at low reactor power

prior to actual testing, site engineering held meetings to discuss

information and problems that had been encountered. Meetings were

primarily held on March 9 and 12, to discuss problems found in the

control of feedwater and rod control. During these meetings, problems

were explored and teams were formed to bound the problem areas and

provide resolution. The meetings were chaired by ICS project engineers

and well attended by management.

On March 9, software changes were determined to be needed to reduce main

feedwater valve control oscillations and manage other ICS control

problems. These software changes were made through the Duke engineering

software change process. The approved changes were installed on

computers.

ICS was designed to automatically switch between Low Level Limits (LLL)

and Feedwater Flow control of steam generator level when certain plant

conditions were met. During a power increase to 15% Reactor Thermal

Power (RTP), those plant conditions were met. However, when the ICS

attempted to automatically switch to Feedwater FLow control of steam

generator levels, the ICS generated feedwater crosslimits due to

excessive mismatch between feedwater flow and reactor power. In

response. ICS automatically reduced reactor power to clear the feedwater

crosslimits as designed. When reactor power was reduced below the power

limit for Feedwater Flow control, ICS automatically switched back to

LLL; thereby, effectively removing the feedwater crosslimits. Reactor

power stabilized at about 8% RTP. Several minutes later, the Reactor

Master and Steam Generator Master controllers transferred to manual.

The licensee determined that the software which provided total feedwater

flow 'value to the ICS control modules was inadvertently deleted during a

routine software update of ICS response constants (PIP 3-97-910). This

inadvertent deletion was identified after the above problem occurred

when the previous copy and the updated copy of the software were

compared. It was not detected on the initial review because the

licensee only reviewed that portion of the software that was modified.

The licensee replaced the missing software and reprogrammed the affected

ICS control module. The licensee also reviewed all other recent

software changes and did not identify any additional undetected software

errors.

The licensee discussed the potential causes for the Reactor Master and

Steam Generator Master controllers transferring to manual, but was

unable to identify any ICS control condition that would cause this

transfer. During this discussion, it was noted that these controllers

transferred to manual when an ICS cabinet door was closed. The licensee

wrote a special troubleshooting procedure to determine if a loose

connector or wire could have been the cause.

Using a high-speed data

Enclosure 2

19

logger, the licensee identified that the transfer relay was susceptible

to contact "bounce." As a precaution, the licensee had manually

transferred the Reactor Master and Steam Generator Master controLlers to

manual. Therefore, there was no positive indication that contact

"bounce" was the root cause. The licensee did replace the relay before

resuming power ascension.

After the licensee had resumed power ascension, significant feedwater

oscillations were observed during the transfer from the startupflow

control valve to the main feedwater regulating valve.

The licensee

reduced power below 10% RTP and conducted troubleshooting. The licensee

determined that the feedwater integral gain factor for feedwater flow

control was set too high, resulting in the ICS responding too quickly to

minor feedwater flow/steam generator level errors. The licensee

reviewed the feedwater integral gain factor setting for the Unit 1 ICS

and found that it was set at 4.5 repeats per minute. The licensee also

stated that the value for the original Unit 3 ICS was about 4.0 repeats

per minute. The feedwater integral gain factor for the Unit 3 ICS was

set at 25 repeats per minute based on V&V simulator testing results.

The licensee adjusted the Unit 3 feedwater integral gain factor setting

to 4.5 and again increased power. Feedwater oscillations were observed:

however, these oscillations were much smaller in magnitude than

previously observed. The licensee also adjusted the proportional gain

constant resulting in a longer period for the feedwater oscillations

than previously observed. The 'B'

loop did transfer from the startup

flow control valve to the main feedwater regulating valve at about 13%

RTP: however, the 'A'

loop did not transfer even after power was

stabilized at about 15% RTP. The licensee attributed this to

differences in flow characteristics between the two loops. The licensee

stated .that they would adjust ICS to allow the 'A'

and 'B'

loops to

transfer at the same time.

c. Conclusions

The inspectors observed the troubleshooting and determined that it was

conducted in a methodical and controlled manner. Appropriate

precautions were taken to guard against unintended reactivity changes.

The failure of the licensee to detect an unintended software change

prior to placing modified.software in service was a substantial concern.

As documented in Inspection Report 96-20, inspector concerns were

expressed that unintended software error could be introduced due to

weaknesses in the V&V program. In response, the licensee had placed the

finalized version of the ICS control module software in the licensee's

Quality Assurance (QA) control program for engineering calculations.

Changes to engineering calculations were independently reviewed to

ensure accuracy. However, the independent review failed to detect the

software error, indicating that a simple independent review may not be

sufficient.

Enclosure 2

20

The large feedwater integral gain factor was another area for concern.

This factor was derived based on V&V simulator testing which was

supposed to accurately reflect Unit 3 dynamic response. As stated in

Inspection Report 96-20. the V&V simulator was not validated for Unit 3

dynamic response. Furthermore, the difference between the initial value

of integral gain (25 repeats per minute) and the original Unit 3 ICS

value (about 4 repeats per minute) indicated that the licensee did not

compare response constants to ensure reasonable and stable ICS

operation. This would also be of concern because, as documented in

Inspection Report 96-20, the V&V tests to be conducted during power

ascension did not test the full range of ICS response. Other large

response constants may be present in the ICS software, which would only

be evident at specific plant conditions, and may result in unstable ICS

operation.

The licensee was aware of the inspectors' concerns and was developing

corrective actions.

The licensee was to determine root cause on this loss of computer code

event under their corrective action program. This condition was

discovered during tuning of the ICS after the software validation had

occurred. The licensee i.ntends to .install this same ICS modification on

Units 1 and 2 during future refueling outages. Accordingly, review of

ICS software implementation during those outages will be tracked under

IFI 50-269,270/97-01-04, Adequacy of Review Software Change,

Additionally, IFI 50-270/96-20-08, ICS Post Modification Testing, will

be evaluated upon the completion of the Unit 3 testing that is to be

completed during the next inspection period.

Post validation and verification changes to Unit 3 ICS software resulted

in an error being introduced. This occurrence resulted in a minor plant

perturbation but was discovered in the system testing phase. The

occurrence was considered a substantial weakness in the overall ICS

modification process.

E8

Miscellaneous Engineering Issues (40500, 90712, 92903)

E8.1 (Closed) LER 50-269/95-002-00: Vendor Analysis Deficiency Results InA

Condition Outside Design Basis Of The Plant

This LER was issued because B&W had discovered an error in the non

conservative direction which resulted in an error of greater than 50

degrees F in the final peak clad temperature. As described in

Inspection Report 50-269,270,287/95-01, the licensee addressed this

issue by restricting the allowable axial imbalance which could be

present at the beginning of the event. The new, restrictive limits for

axial imbalance were imposed after review by the Plant Operations Review

Committee (PORC). and implemented by a conditional operability

evaluation. The new limits were considered temporary until B&W

Enclosure 2

21

completes their analysis for Oconee, and provides a new initial

condition limit for axial imbalance. Duke re-evaluated the Core

Operating Limits Report (COLR) based on.the information provided by B&W.

and the COLRs for all three units were revised restoring the operating

limits to their previous values before identification of the B&W error.

All three units' COLRs and associated procedures and alarm limits were

revised on March 9, 1995. Therefore, this item is closed.

E8.2 Generic Letter (GL) 96-06 Followup

IR 96-20, Section E2.1, discussed the licensee's efforts to review and

respond to GL 96-06. Assurance of Equipment Operability and Containment

Integrity During Design Basis Conditions. During this inspection

period. the licensee has made two.10 CFR 50.72 reports as followup to

these efforts. The associated issues are as follows:

" LER 97-02. dated February 20. addressed a potential "Reactor

Building Cooling Unit [RBCU] Technically Inoperable Due to Design

Deficiency" problem. As part of the GL 96-06 evaluation, Duke

engineering has been performing detailed thermal-hydraulic

analyses to determine if any portion of the Low Pressure Service

Water (LPSW) piping which served the RBCUs were susceptible to

water hammer. .On January 24. 1997. the analyses determined that

during certain design basis scenarios condensation induced water

hammers associated with the nonsafety-related auxiliary cooling

units could result in safety-related RBCUs being unable to perform

their intended function. This resulted in the first 10 CFR 50.72

report. The root cause of this potential problem will be

addressed in a supplement to the LER. The licensee had taken

compensatory actions (discussed in the IR 96-20) to eliminate the

problem by making valve lineup/position changes. Until this issue

is resolved, this shall be identified as URI 50-269.270.287/97-01

05. LPSW Piping .to the RB Cooling Inoperability.

" On March 17, the licensee made the second 10 CFR 50.72 report as

followup on inoperable boron dilution flow paths (BDFP). There

are three redundant BDFPs provided in the Oconee design. Two of

these paths are available by positioning certain valves to

establish the flowpath (active paths), and one is available

internal to the reactor vessel via a passive path. The active

flowpaths can be established by open valves LP-1 and LP-2 or the

other path by opening LP-103 and LP-104. The UFSAR required that

two of the three flowpaths be available in the event of a LOCA.

Prior to the recent return to power operations by the three units,

past operability questions were postulated with the active

flowpaths on all three units. The postulated problem was that

thermally induced overpressurization of the water volume between

the two pairs of valves could make opening of the valve pairs not

possible. Thus, the active flow paths may not have been

available., IR 96-20 addressed compensatory actions taken prior to

Enclosure 2

22

the returh to power operations while the licensee continued their

evaluation. On March 17, with their analysis now complete, the

licensee determined that the active paths were past inoperable,

resulting in the above report with a LER to follow. Until this

issue is resolved, this shall be identified as URI 50

269.270.287/97-01-06, BDFP Inoperability.

IV.

Plant Support Areas

R2

Status of RP&C Facilities and Equipment

R2.1 10 CFR 70.24 Criticality Accident Requirements

a. Inspection Scope (71750)

The inspector reviewed the licensee's compliance with 10 CFR 70.24,

Criticality Accident Requirements. The review became necessary

following the identification at other nuclear sites that were not in

compliance with the regulation.

b. Observations and Findings

The inspector reviewed the Oconee Nuclear Station license, emergency

procedures, Technical Specifications, and interviews with site

personnel.

Based on this review, it was identified that Oconee Nuclear

Station, Units 1. 2. and 3. neither satisfies nor is exempted from the

requirements of 10 CFR 70.24 (a)1 or (a)2. This issue is being

identified as Unresolved Item (URI) 50-269,270,287/97-01-02, Failure to

Meet Requirements of 10 CFR 70.24.

c. Conclusions

The licensee did not meet the .requirements of 10 CFR 70.24, Criticality

Accident Requirements. A URI was opened pending further NRC evaluation

of the enforcement action.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on March.20. 1997. The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

Enclosure 2

23

Partial ,List of Persons Contacted

Licensee

E. Burchfield,. Regulatory Compliance Manager

T. Coutu, Operations Support Manager

D. Coyle, Systems Engineering Manager

T. Curtis, Operations Superintendent

J. Davis, Engineering Manager

B. Dobson, Systems Engineering Manager

W. Foster, Safety Assurance Manager

J. Hampton. Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

B. Peele, Station Manager

J. Smith, Regulatory Compliance

NRC

D. LaBarge, Project Manager

J. Ganiere, Electrical Engineer

Enclosure 2

24

Inspection Procedures Used

IP90712:

In-Office Review of Written Event Reports

IP71750:

Plant Support Activities

IP71707:

Plant Operations

IP61726:

Surveillance Observations

IP62707:

Maintenance Observations

IP40500:

Self-Assessment

IP37551:

Onsite Engineering

IP92901:

Followup - Operations

IP92902:

Followup - Maintenance

IP92903:

Followup - Engineering

IP93702:

Prompt Onsite Response to Events

IP61701:

Complex Surveillance

Items Opened, Closed, and Discussed

Opened

50-269,270/97-01-01

IF.1

Reactor Trip Confirm Circu'it Fuse

Inspection (Section 01.5)

50-269,270287/97-01-02

URI

Failure to Meet Requirements of 10 CFR

70.24 (Section R2.1)

50-270,287/97-01-03

VIO

Failure to Follow Valve Procedure (Section

M8.1).

50-269,270/97-01-04

IFI

Adequacy of Review Software Change

(Section E3.1)

50-269F270,287/97-01-05

URI

LPSW Piping to the RB Cooling

Inoperability (Section E8.2)

50-269,270,287/97-01-06'

URI

BDFP Inoperability (Section E8.2)

Closed

50-269/95-001-00

[ER

Potential Unanalyzed Main Steam Line Break

Scenario (Section 08.1)

270,287/96-17-07

URI

Incorrect Electrical Connection of 2LP-1,

2LP-2, 3LP-1, and 3LP-2 (Section M8.1)

50-270/96-13-10

VIO

Failure to Perform Adequate 10 CFR 50.59

Evaluation (Section M8.2)

sEnclosure2

25

50-269/95-002-00

LER

Vendor Analysis Deficiency Results In A

Condition Outside Design Basis Of The

Plant (Section E8.1)

Discussed

50-270,287/96-20-08

IFI

ICS Post Modification Testing (Section

E3.1)

List of Acronyms

ACB

Air Circuit Breaker

amp

ampere

BDFP

Boron Dilution Flow Path

B&W

Babcock and Wilcox

CF

Core Flood

CFR

Code of Federal Regulations

CCW

Condenser Circulating Water

COLR

Core Operating Limits Report

CR

Control Room

CRD

Control Rod Drive

CF

Core Flood

DHR

Decay Heat Removal

EFW

Emergency Feedwater

EHC

Electro-Hydraulic Control

EOC

End Of Cycle

EPRI

Electrical Power Research Institute

ES

Engineered Safeguards

FDW

Feedwater

FWPT

Feedwater Pump Turbine

GL

Generic Letter

HD

Heater Drain

HP

High Pressure

HPI

Hig.h Pressure Injection

IAW

In accordance with

ICS

Integrated Control System

I&E

Instrument & Electrical

INPO

Institute of Nuclear Power Operations

IR

Inspection Report

IP

Inspection Plan

IFI

Inspector Followup Item

KHU

Keowee Hydro Unit

LDST

Letdown Storage Tank

LER

Licensee Event Report

LCO

Limiting Condition for Operation

LLL

Low Level Limits

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

.

LP

Low Pressure

Enclosure 2

26

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

MP

Maintenance Procedure

MS

Main Steam

MSRH

Main Steam Re-heater

MTG

Main Turbine Generator

NCV

Non-Cited Violation

NLO

Non-Licensed Operator

NNI

Non-Nuclear Instrumentation

NRC

Nuclear Regulatory Commission

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

ONS

Oconee Nuclear Station

OP

Operations Procedure

OSM

Operations Shift Manager

OTSG

Once Through Steam Generator

PCB

Power Circuit Breaker

PDR

Public Document Room

PIP

Problem Investigation Process

PM

Preventive Maintenance

PORC

Plant Operations Review Committee

PT

Performance Test (surveillance)

QA

Quality Assurance

RB

Reactor Building

RBCU

Reactor Building Cooling Unit

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RP&C

Radiation Protection and Chemistry

RPS

Reactor Protection System

RPM

Revolutions Per Minute

SRO

Senior Reactor Operator

RTP

ReactorThermal Power

Tavg

Temperature Average of the RCS

TS

Technical Specifications

TT

Temporary Test

URI

Unresolved Item

UFSAR

Updated Final Safety Analysis Report

VIO

Violation

V&V

Validation and Verification

WO

Work Order

WR

Work Request

Enclosure 2