ML15118A189

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Insp Repts 50-269/96-20,50-270/96-20 & 50-287/96-20 on 961229-970208.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML15118A189
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 03/10/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A185 List:
References
50-269-96-20, 50-270-96-20, 50-287-96-20, NUDOCS 9703280016
Download: ML15118A189 (44)


See also: IR 05000269/1996020

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270, 50-287, 72-04

License Nos:

DPR-38, DPR-47, DPR-55, SNM-2503

Report No:

50-269/96-20. 50-270/96-20, 50-287/96-20

Licensee:

Duke Power Company

Facility:

Oconee Nuclear Station, Units 1, .2

& 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

December 29, 1996 - February 8. 1997

Inspectors:

M. Scott. Senior Resident Inspector

G. Humphrey, Resident Inspector

N. Salgado, Resident Inspector

D. Billings, Resident Inspector

W. Holland, Reactor Inspector (Section E1.1)

P. Fillion, Reactor Inspector (Section El. 1)

N. Merriweather, Reactor Inspector (Section E2.4)

C. Rapp, Reactor Inspector (Section E2.5)

Approved by:

C. Casto, Chief, Projects Branch 1

Division of Reactor Projects

9703280016 970310

PDR ADOCK- 05000269

Enclosure 2

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2 & 3

NRC Inspection Report 50-269/96-20,

50-270/96-20. 50-287/96-20

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a six-week

period of resident inspection; in addition, it includes the results of

announced inspections by four-regional reactor inspectors.

Operations.

The Unit 2 return to power was well controlled and planned, with

very few problems encountered. (Section 01.2)

With Unit 3 in cold shutdown, a short duration diversion of water

occurred from the Reactor Coolant System (RCS) to the Borated

Water Storage tank (BWST) due to Valve 3LP-40, a Low Pressure

Injection (LPI) pump test line valve, being in the wrong position.

Operations personnel acted promptly to stop the event. An

Unresolved Item (URI) was identified to further evaluate this loss

.of RCS inventory. A post event review resulted in re

hydrostatically testing the subject valve-and associated piping at

a higher value. This was considered an engineering weakness

involving modification review and approval.

(Sections 01.3 and

E1.3)

0

With Unit 2 at power, LPI Valve 2LP-18 became potentially

hydraulically locked, causing the licensee to enter a Technical

Specification (TS) Limiting Condition for Operation (LCO) on the

2B LPI train.. The valve was subsequently tested and found

operable. Integration of corrective actions was considered a

weakness for this event. (Sections 01.3 and E2.2)

A URI was identified regarding a potential past operability issue

on the Standby Shutdown Facility (SSF) pressurizer heater level

control. (Section 02.2)

Unit 3 refueling activities were adequately performed with care

and attention to detail. (Section 04.1)

The Emergency Power and Engineered Safeguards Functional Test

classroom and simulator training provided to the B-Shift operators

was thorough, presented clearly, and professionally. The

operators participated in the training with a focused and

questioning attitude. (Section 05.1)

A violation was identified regarding an Operations Procedure not

being placed on Administrative Hold to prevent its use prior to

being changed. This was a major factor in the September 24, .1996,

Unit 2 water hammer event. Unrelated secondary piping code

Enclosure 2

2.

deficiencies identified and corrected by the licensee after -the

Unit 2 water hammer event were identified as a Non-Cited Violation

with respect to 10 CFR 50.59. (Section 08.1)

Maintenance

0

Maintenance and Surveillance activities such as the Unit 1 heater

drain work, complex Unit 3 Emergency Core Cooling System (ECCS)

flow test, complex Unit 3 Low Pressure Service Water (LPSW) pump

surveillance, and Unit 2 rod drop test, were thoroughly and

professionally completed. (Section M1.1)

The i-nspectors reviewed a recent nonsafety-related motor failure.

Questions regarding possible broader implications on safety

related equipment are being tracked by an Inspector Followup Ithm.

(Section M2.1)

Engineering

0 .Integrated

testing of the Oconee emergency power system was

satisfactorily accomplished in accordance with the approved test

procedure. Deficiencies identified during testing were, or will

be resolved in-accordance with the licensee's problem

investigation process. Control of all test activities was good.

Positive obse'rvations were made relating to test briefings,

control room briefings, and communication/coordination of test

evolutions. (Section E1.1)

Based on a review of the nonsafety-related and safety-related fuse

programs, the licensee had adequately addressed the resolution of

fuse failures. (Section E1.2)

A violation was identified because the licensee did not have a

programmatic material condition Reactor Building (RB) closeout

procedure. The lack of a procedure (organized program) resulted

in a poor understanding of RB material condition. Accordingly, a

URI was identified concerning past operability of the RB

recirculation flow path. (Section E1.4)

0

The licensee made a.concerted effort in addressing the issues of

Generic Letter (GL) 96-06 as it relates to the Oconee design

basis. Their long-term GL response .concerning RB penetration over

pressurization and water hammer is scheduled for issue by April 15

and August 1, 1997, .respectively. (Section E2.1)

Although some water/steam hammers were noted during the Unit 2

startup, the licensee's efforts were effective in minimizing this

problem. The modified moisture separator reheater.drain system

automated controls performed well and eliminated the need for

manual operation of the associated valves .with the unit operating

Enclosure 2

3

at power. This -reduced the potential personnel hazards involved

with secondary plant operation. (Section E2.3)

Design controls for the Operator Aid Computer (0AC) and Main Steam

Line Break (MSLB) modifications on.Unit 3.were adequate. Overall

engineering performance on these modifications-was considered good

even though a significant number of Variation Notices (VNs) had

been issued against the OAC modification. (Section E2.4)

The 10 CFR 50.59 Unit 3 Integrated Control System (ICS)

modification installation procedures were considered to be

adequate. In response to.traceability concerns with respect to

translation of ICS functional requirements into software

specifications, the licensee implemented independent contractor

assessments and took appropriate corrective action. Initial

concerns regarding formal software configuration management

controls were adequately addressed by the licensee through the

inclusion of ICS software in the engineering calculation control

program. Also adequately addressed were initial concerns over the

ICS Unreviewed Safety Question (USQ) evaluation; software

development, and verification and validating (V&V) process.

Further followup inspection of the ICS test plan and plant testi-ng

will be conducted under an IFI.

Enclosure 2

Report Details

Summary of Plant Status

Unit 1, which had been shutdown in early October 1996 for secondary piping

inspections and water hammer modifications, remained shutdown for the entire

reporting period.

Unit 2 returned to power operations on February 3. 1997, after an extended

shutdown that resulted from a heater drain line rupture that occurred on

September 24, 1996. The unit continued to operate at power throughout the

remainder of the reporting period.

Unit 3. which had been shutdown in early October 1996 for secondary piping

inspections and water hammer modifications, remained in refueling mode

throughout the entire reporting period.

Review of UFSAR Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the Updated Final Safety Analysis Report (UFSAR)

that related to the areas inspected. The inspectors verified that the UFSAR

wording was consistent with the observed plant practices, procedures, and/or

parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments- (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant Operations. In general, the conduct of

operations was professional and safety-conscious; specific events and

noteworthy observations are detailed in the sections below.

01.2

Unit 2 Startup

.a. Inspection Scope (93702, 71707)

The inspectors observed major portions of the Unit 2 startup and power

ascension activities. Unit 2 returnedto power operation on February 3,

1997.

b. Observations and Findings

The inspectors were present in Unit 2 for major critical evolutions,

including system lineups, main turbine generator (MTG) latching, and

reactor power ascension. Observed plant system lineups were found to be

adequate. Effective pre-job briefs were presented to the Operations and

support staff prior to each major plant status change. Satisfactory rod

Enclosure 2

2

drop testing was observed as discussed in Section M1.1. Observation of

the approach to criticality was found to be adequate. MTG

synchronization was delayed slightly: the synchronizing breaker PCB 23

did not immediately latch the MTG to the grid.on the first several

tries, but after some minor tuning of switchyard to MTG voltage, it

subsequently latched. The Number 4 intercept valve was slow to respond

to an open signal requiring the replacement of an electronic card.in its

control circuits. The licensee's engineering department had

instrumented the secondary heater drains and was present to monitor the

startup of the .secondary plant (discussed in Section E2.3).

After the MTG had been latched, the inspectors observed the operators

valve-in extraction steam to the "B"

heaters. The valving caused no

waterhammers. Extraction steam Valve HPE-36 did not immediately work

and required repair by Instrument and Electrical (I&E) personnel.

Additionally, several heater water level gages on Panels 2SA 10 and 11

did not work well and were also identified by Operations for repai.r.

c.

Conclusions

The Unit 2 return to-power was controlled and very few'problems were

encountered. The inspectors found the level of control and planning

during the complex startup to be appropriate.

02

Operational Status-of Facilities and Equipment

02.1 Engineered Safety Feature System Walkdowns (71707,71750)

The inspectors used Inspection Procedure 71707 to walkdown accessible

portions of the following safety-related systems:

Keowee Hydro Station

Units 1, 2, and 3 Reactor Building's (RBs)

0

Units 1 and 2 Emergen cy Core Cooling System (ECCS) pump areas

0

Unit 2 High Pressure Injection (HPI) System

Emergency Feedwater Systems

  • Unit 3 Spent Fuel Pool Area

Units 1 and 2 Pipe Penetration Rooms

Equipment operability, material condition, and housekeeping were

acceptable in most cases.

During normal daily tours, the inspector

identified some poor housekeeping conditions in the Unit 3 spent fuel

pool area. The inspector informed Maintenance management of the poor

housekeeping conditions-and the potential for foreign material entering.

the pool.

The licensee's Management sensitivity to foreign material,

exclusion (FME) is high, and the poor housekeeping conditions were

appropriately addressed in a prompt manner.

During this period, the inspectors toured Units 1, 2, and 3 RBs. As.

discussed in Section E1.4. several significant conditions related to

Enclosure 2

3

tape, RTV, paint, and-insulation were identified during the inspectors'

tour of the Unit 2 RB.-

Aside from these significant conditions, the

inspectors found and reported to the licensee 112 additional items that

were minor in nature. Overall, aside from the several significant

conditions that the licensee had to evaluate, the inspectors found -the

three RBs in good mechanical condition. Unit 3 RB material condition

was preliminarily reviewed by the residents while the other two RBs were

inspected after the licensee had performed their maintenance closeout

inspections prior to unit startup.

02.2 Standby Shutdown Facility (SSF) Pressurizer Heaters

a. Inspection Scope

On January 20, 1997, the licensee identified a problem which indicated

that the pressurizer heaters controlled from the SSF could be uncovered

prior to actuation of the low pressurizer level cutoff. The inspector

reviewed the licensee's Problem Investigation Problem (PIP) report 0

097-0273 which described the problem and associated corrective actions.

b. Observations and Findings

A revision of SSF Pressurizer level instrument uncertainty Calculation

OSC-2746. SSF Pressurizer Level Loop Instrument Accuracy Calculations

LT-72,. indicated that the SSF pressurizer heaters could be uncovered

before the low level cutoff was actuated. The low level cutoff is

provided to remove power from the.heaters before they are uncovered to

prevent possible burnout of the heaters. The current setpoint for the

low level cutoff is 105 inches of Water decreasing. The licensee's

immediate corrective actions required the recalibration of SSF

pressurizer level instrument loops for SSF operating conditions.

Calibration procedure IP/O/A/0370/002C. Standby Shutdown Facility RCS

Pressurizer Level and Pressurizer Pressure, was revised to incorporate

the correct calibration range for SSF Pressurizer Level Loops 1,2,3 . .

RCLTOO72.

The Unit 1, Unit 2, and Unit .3

recalibrations were completed

via Work Orders (WO) 97006889. 97006874, and 97006868, respectively.

The licensee was performing a past operability review. This issue will

be identified as Unresolved Item (URI) 50-269,270,287/96-20-01. $SF Past

Operability, pending completion and review of the licensee's evaluation.

c. Conclusion

The licensee identified that the pressurizer heaters could be uncovered

on a low level if operated from the SSF. Recalibration of instrument

loops corrected.this deficiency. There were no present operability

concerns based on the Units' status. The licensee was performing a past

operability evaluation at the close of the inspection.

.

Enclosure 2

4

04

Operator Knowledge and Performance

04.1 Unit 3 Refueling Activities (60710)

a. Inspection Scope

The inspectors observed, in part, all phases of the Unit 3 refueling.

b. Observations and Findings

The inspectors observed fuel movement in the RB, fuel movement tracking

efforts, refueling cavity and Spent Fuel Pool (SFP) FME practices.

These efforts were found to be adequate and in accordance with

Maintenance Procedure MP/0/A/1500/009, Defueling - Refueling Procedure.

The operators and maintenance personnel performing the evolutions were

attentive to detail and methodical in their actions. The refueling

cavity and SFP water had good clarity, thus facilitating an effective

work effort.

c. Conclusions

Observed Unit 3 refueling activities were adequately performed with.care

and attention to detail.

05

Operator Training and Qualification

05.1 Emergency Power and Engineered Safeguards Functional Test Training

a. Inspection Scope (61701)

The inspectors attended the licensed operator classroom and simulator

training for TT/O/A/0610/025, Emergency Power and Engineered Safeguards

Functional Test. (Section E1.1 addresses actual test performance.)

b. Observations and Findings

The- licensee provided "just in time training," for the B-shift licensed

operators. The terminal objective of the training was to enable the B

Shift to perform Test TT/0/A/0610/025. On December 29, 1996, the

licensee provided the classroom training which encompassed the overall

purpose of the testing, described the six individual tests associated

with Test TT/0/A/0610/025, and contingencies. On December 30, 1996, B

shift was provided simulator training on Test TT/0/A/0610/025. The

training was separated into three separate sections, Unit 1, Unit 2, and

Unit 3. Each section went through Test TT/0/A/0610/025 step-by-step on

the simulator as it applied to their respective unit. The operators

identified a few procedural discrepancies, and procedure changes were

initiated appropriately.

.

.Enclosure

2

5

c. Conclusions

The inspectors concluded that the classroom and simulator training

provided to the B-Shift operators was thorough, presented clearly.,and

professionally. The operators participated in the training with a

focused and questioning attitude.

08

Miscellaneous Operations Issues (92901)

08.1 (Closed) Apparent Violation (EEI) 50-270/96-17-08:

Failure To Use

Procedure Administrative Hold

(Closed) EEI 50-269,270.287/96-17-01: Failure To Complete A Written

Safety Evaluation Of Secondary Plant Piping Not In Accordance With The

Piping Code Referenced In The FSAR

Inspection Report 50-269.270.287/96-17 (dated January 27. 1997)

identified two apparent violations which were being considered for

escalated enforcement action in accordance with the "General Statement

of Policy and Procedures for NRC Enforcement Actions" (Enforcement

Policy), NUREG-1600. Having concluded that a predecisional enforcement

conference was not necessary to assist NRC in its deliberations, the

apparent violations are administratively closed and the disposition of

the associated violations is addressed below.

The first apparent violation (EEI 50-270/96-17-08) involved a Moisture

Separator Reheater Operations Procedure (OP/2/A/1106/14) that.was not

placed on "Administrative Hold" to prevent its use prior to being

changed.

This was a major factor in the September 24, 1996. Unit 2

water hammer event.

The failure to follow Nuclear Station Directive

(NSD)

703.12, Revision 14, Administrative Hold Of Procedures, is a

violation of Technical Specification 6.4.1 and is identified as

Violation 50-270/96-20-06, Failure To Use Procedure Administrative .Hold.

The circumstances surrounding this violation are described in.detail in

Inspection Report 50-269,270,287/96-17.

Also addressed in detail in Inspection Report 50-269,270,287/96-17. the

second apparent violation (EEI 50-269,270.287/96-17-01) concerned a

number of examples where secondary plant piping did not-meet the piping

code referenced in the Final Safety Analysis Report (FSAR) and the

failure to provide a written safety evaluation for this condition.

Viewed as original construction errors with minimal nuclear safety

related significance, this past programmatic failure to meet 10 CFR

50.59 does not involve a current performance issue nor does it have a

current impact. Accordingly, the NRC concluded that this failure to.

comply with 10 CFR 50.59 represents a licensee-identified and corrected

violation. In accordance with-Section VII.B.1 of the NRC Enforcement

Policy, this violation is dispositioned as a non-cited violation (NCV)

50-269,270,287/96-20-07. Failure To Complete A Written Safety Evaluation

Of Secondary Plant Piping Not In Accordance With The Piping Code

0

Referenced In

The FSAR.

Enclosure 2

  • .

6

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707,61726,60710)

The inspectors .observed all or portions of the following maintenance.

activities:

PT/2/A/0600/14

Emergency Feedwater Pump Suction From Hotwell

Test

OP/2/A/1106/02

Enclosure 3.4, Feedwater Cleanup Valve

Checklist; Enclosure 3.3, Condensate

Recirculation Valve Checklist

TT/3/A/0610/25B

Hydraulic Flow.Functional Test

PT/0/A/0750/011

Defueling/Refueling Activities

MP/0/A/1500/009

Defueling/Refueli.ng Procedure

WO 96082817

Reset./Verify Setpoint of Timers LC 1X5

WO 96082818

Reset/Verify El-LK-1X6 Setpoint Timer

WO 96030239

Install Minor Modification ONOE-9067, Pressure

Locking Relief for 3LP-2

OP/2/A/1104/01 .

Verifying Operability of Core Flood Check-Valves

PT/2/A/0152/07

Core Flood Valves Stroke at Hot Shutdown

.PT/2/A/0150/15D

Intersystem Loss of Coolant Accident (LOCA) Leak

Test

MP/O/A/1720/010

System/Component Hydrostatic Test Controlling

Procedure

WO 96089958

1C LPI Pump Motor, MP/0/A/3009/017, Visual PM

Inspection and Electrical Motor Tests

WO 96103558

IC Low Pressure Service Water (LPSW) Pump Motor,

MP/0/A/3009/017. Visual PM Inspection and

Electrical Motor'Tests

  • .Enclosure

2

7

WO 97001658

2A Component Cooling (CC) Pump Motor.

MP/0/A/3009/017, Visual PM Inspection and

Electrical Motor Tests

WR 97009672

LPSW Lines for the 2B2 RCP Coolers

and 97009878

PT/0/A/0300/01

Control Rod Drive Trip Time Test

WO 96079756

Modify Heater Drain system

WO 96070942

PM Relays in Compartment 1TD-9 (HPI-C)

IP/1/A/4980/051A Westinghouse Type CO-5. CO-6, CO-7, and CO-11

Relay Test

0

WO 96103549

Replace Branch Connection Heater Drain (HD)

System

IP/0/B/0275/011B. Heater Drain Moisture Separator Drain Tank Level

Calibration

PT/2/A/0204/07

Reactor Building Spray Pump Test

WO 96072924

Unit-1 Reactor Protection System (RPS) Channel A

and Functional Test

0

WO 97010587

Troubleshooting and/or Corrective Maintenance,

1FDW-380 - 1B FWP

b. Observations and Findings

On January 7. the inspectors observed satisfactory performance of

TT/3/A/0610/25B, Hydraulic Flow Functional Test. Unit 3 was defueled

and in a refueling outage. The purpose of the test was to determine

ECCS borated source flow characteristic response during close to actual,

but simulated. LOCA conditions. Using the BWST and Let Down Storage

Tank (LDST) as the suction source, the ECCS pumps flowed to the

refueling cvity. The tank levels, LDST pressure, and flows were

closely monitored. The pumps were stopped prior to any problems being

encountered (BWST reached approximately 30 feet, LDST reached 20 inches,

and LDST pressure was 6.5 psig). At the time of the inspection, the

licensee had yet to complete test data analysis, which should provide

more accurate plant operation information. The test was well controlled

and properly documented.

On January 19, the licensee satisfactorily completed a Unit 3 complex

surveillance test in accordance'with PT/3/A/0251/23, Low Pressure

Service Water System Flow Test. During the test, two condenser

circulating water pumps were run to establish circulation flow and then

Enclosure 2

8

secured. Siphon circulation maintained flow for the rest of the test.

The LPSW pumps on Unit 3 took suction from the siphon circulation flow

as required to complete the test. During test performance, operations

and engineering demonstrated good command and control over the test.

The inspectors observed the satisfactory Unit 2 rod drop test that was

conducted in accordance with PT/0/A/0300/01, Control Rod Drive Trip Time

Test. The slowest rod drop time was 1.387 seconds which was below the

administrative limit of 1.4 seconds. The TS time limit was 1.66

seconds.

c. Conclusion

In general, the inspectors-found the work and testing performed during

observed maintenance activities to be professional and thorough. All

work observed was performed with the work package present and in active

use. Technicians were experienced and knowledgeable of their assigned

tasks. The inspectors frequently observed-supervisors and system

engineers monitoring job progress. Quality control personnel were

present when required by procedure. When applicable, appropriate

radiation control measures .were in place.

M2

Maintenance and Material condition-of Facility and Equipment

M2.1 Inspection Scope 1B RCW Motor (62707)

a. Inspection Scope

The inspectors investigated information regarding the safety-felated

pump motor program and recent occurrences at the site.including the

failure of the 1B Raw Coolant Water (RCW) motor.

b: Observations and Findings

On January 5. during preparations for the fifth Emergency Safeguards

(ES) test discussed in Section E1.1, the nonsafety-related lB RCW pump

motor tripped prior to test initiation. The motor was not a load for

the test and was evaluated later. The motor was determined to have a.

short to ground, indicating winding failure. The inspector observed the

failed windings of the disassembled motor, noting both the burned

windings at the six o'clock location on one end of the stator and heavy

dirt buildup in the general interior of the motor, particularly on the

lower winding coils. The motor had no cooling port entry filter. Per

discussions with the licensee,. one of the other RCW motors had recently

failed. At the request of the inspector and in conjunction with the

system engineer's efforts, PIP 5-97-0205 was generated on the motor

failure.

A motor repair vendor provided a Written report evaluating the motor's

"as-found" condition. In part, the report read as follows:

Enclosure 2

"There was extensive dust and debris concentrated on the stator

windings as a result of cooling air flow through the motor....

There was no sign of single phasing or a low voltage situation....

Other coils in the winding had good color and did not show any

evidence of thermal breakdown.....Cause of failure: it appears the

dust and debris accumulated in the 6:00 position, abrasives in the

debris (sand, grit, etc) eroded away the varnish which protected

and supported the copper conductors. The bare copper wires either

shorted to each other or arced to ground once sufficient debris

and/or moisture collected at the damaged.area. Other coil's showed

signs of damaged varnish coating; however, no failure had yet

occurred at these spots (also at the 6:00 position but.at other

side of iron) [opposite end of stator iron winding support ring].

Preventive action: this is a an open construction motor.... This

open construction allowEs] for dust and moisture to enter the

motor freely. The motor should be, at a minimum, blown out with

dry compressed air whenever a significant amount of debris

collects on the winding. Keep abrasive dust from entering the.air

intakes if possible. Use internal motor heaters to keep

winding[s] warm during periods of non-use. This-will prevent

condensation from collecting on the windings."

All the 4160 volt safety-related (S-R) motors are also without

ventilation filters. These motors are generally located in confined

rooms-with their own ventilation systems. Over the 30 year life of the

plant there has been cleaning, painting, insulation removal, and other,

activities that have generated debris around all of the S-R motors. The

exception were the LPSW pump motors which were not in confined spaces.

  • The LPSW motors are located on the turbine building basement floor in a

generally well maintained large industrial area that is subject .to

routine cleaning and debris producing work. -The

RCW motors are located

in areas adjacent to the LPSW pump motors.

- During mid-December 1996, the residents identified that.debris generated

by welding, grinding, and general construction activity of the three

unit outages was present in the area around the operating Unit 1 and

.-

Unit 2 LPSW pumps. The motor intake grills were observed.to have some

debris encrusted upon them. There was debris around the Unit 3 pumps,

but they were not operating (fuel was removed from the reactor vessel at

the time). The licensee responded to the immediate concern by cleaning

areas around the pumps and changing the Operations round sheets to have

the non-licensed operators not only walkdown the area but also inspect

the motor intake grills. The licensee also generated PIP 0-96-2478.

The inspector asked for and received loaded motor stator and bearing

temperature data that indicated that the motors were not under heat

duress during the recent ES testing. At the time, the turbine building

temperatures were cooler than when at power. However, as indicated

above, the dirt seen in'the RCW motor was primarily concentrated at the

Enclosure 2

.

10

six o'clock position and probably would not contribute to motor over

heating.

The residents reviewed the licensee's motor Preventive Maintenance (PM)

program. The program did not routinely clean the ventilation ducting or

windings of the unfiltered motors. The licensee recently initiated a

motor PM to perform testing of selected safety-related motors in

accordance with MP/0/A/3009/017, Visual PM Inspection and Electrical

Motor Tests, dated January 9, 1997. The procedure includes a visual

check of the exterior of the assembled motors. Previously, the licensee

only performed voltage to ground checks on motors. The licensee's

current program, which ascribes to the guidance provided by an Electric

Power Research Institute (EPRI) document (Electric Motor Predictive and

Preventive Maintenance Guide), is more comprehensive. The electrical

checks, such as the Insulation Resistance and Polarization Index (PI)'

tests performed by the above procedure, are indicated to be trendable

information in Table 4-1 of the document. However, these tests are

stated to provide basic information if the insulation is clean and dry

(page 5-3 of the guidance document). Page 4-2 of the guidance did not

reflect the above information in that it stated that the PI test is a

good test for determining the overall condition of the insulation.

Again, these new electrical tests have just been recently initiated and

iterative information is not available. The inspectors had observed

some recent testing and understood that for the first test performance,

the motors appeared'to have acceptable initial test values.

The EPRI document gives further guidance on visual inspections. The

document indicates "that the decision to dismantle a motor for

inspection was expensive and-disruptive. The decision should be

evaluated based on the analysis of trendable.tests [the inspectors

assumed a number of iterative tests], any abnormal noise or odor,

unexplained operation of protective relays, and industry experience with

similar motors.... However, in certain cases, visual inspection

[disassembled] is an accepted means of evaluating physical condition of

stator windings, rotor windings, and magnetic cores."

In the case of

the LPSW pump motors, the argument could be made that the RCW motor was

a similar motor in that it was in the same environment, about the same

inservice time, and in similar continuous service.

Given the implication this failure has on safety-related equipment,. the

inspector will continue to pursue the issue with the licensee. .This

issue shall be tracked as Inspector Followup Item (IFI) 50

269.270.287/96-20-02, Unfiltered Motors.

c. Conclusions

Receht failure of the 1B RCW motor was due to its in service

environment. The licensee did a thorough evaluation of the specific

failure. However, the inspector will continue to pursue implications of

this failure with the licensee.

Enclosure 2

III. Engineering

El

Conduct of Engineering

E1.1

Integrated Emergency Power Supply Electrical Testing

a. Inspection Scope (61701)

a.1 Background.

On September 19, 1996, NRC met with Duke Power Company (DPC) to discuss

proposed integrated testing of the Oconee emergency electrical

distribution system. DPC's described tests that were to be conducted .in

late 1998 or early 1999. These tests were .conceptually described in a

DPC submittal dated October 31, 1996.

On September 24. 1996, a drain line rupture event on a Unit 2 reheater

drain line resulted in DPC's decision to shutdown all three Oconee

units. NRC sent a letter to DPC on October 18, 1996, requesting that

the licensee review the possibility of performing electrical system

tests during the three unit outage. On November 21, 1996. DPC stated in

a letter to the NRC their intentions to perform.a one-time, integrated

emergency power engineered safeguards functional test as described in

the October 31, 1996, letter.

On December 3, 1996, the NRC sent a letter to .DPC requesting information

about special considerations wi.th respect to shutdown risks during the

performance of the functional tests. Information on DPC considerations

relating to control of reactor pressure, reactor coolant temperature,

reactor vessel water level, shutdown margin, and contingencies was

requested. On December 11, 1996, (with supplements dated December 17,

19. and 26) DPC requested amendments to the Oconee Technical

Specifications (TS) to address their determination that an unreviewed

safety question existed in that the testing exceeded that which was

described in the Final Safety Analysis Report (FSAR).

On January 2, 1997, the NRC issued Amendment Nos. 220, 220, and 217 to

the TS of Oconee Units 1, 2, and 3, respectively. The amendments

concluded the FSAR change which referenced the submittal describing the.

electrical system functional tests was acceptable. Testing of the

Oconee emergency electrical distribution system in accordance with test

Procedure TT/O/A/0610/025, Emergency Power and Engineered Safeguards

Functional Test, commenced after receipt of the TS amendments.

a.2 Test Inspection

The inspectors observed licensee test activities for the six tests which

were conducted in accordance with test Procedure TT/O/A/0610/025.

Inspectors monitored test activities from both control rooms, the Keowee

Hydro Station, Lee Turbine Units, and other selected locations in the

Enclosure 2

12

plant. Licensee pre- and post-test briefings were also monitored.

Licensee personnel provided daily debriefs to the inspectors regarding

disposition of deficiencies identified during testing.

Tests were designed to demonstrate a critical or worst case scenario

related to performance of the electrical systems. Monitoring and

recording instrumentation was installed at points throughout the

electrical and mechanical systems to allow sufficient verification of

correct system performance.. Each test involved the simulation of a loss

of offsite power with specific acceptance criteria defined in the

procedure.

b. Observations and Findings

b.1 Test Objectives

Major test objectives were to demonstrate the ability of the Oconee

emergency power system to accept loads in six different loss of coolant

accident/loss of offsite power (LOCA/LOOP) or LOOP scenarios; to

accumulate data for post-test engineering analysis of the emergency

-power.system performance; and to demonstrate the ability of the

Engineering Safeguards equipment to operate in four different LOCA/LOOP

scenarios. The six test scenarios involved:

Block loading of three unit LOOP loads-onto the Keowee underground

power supply from Keowee standby condition (Test 1)

Block loading of three unit LOOP loads onto the Keowee~overhead

power supply after Keowee load rejection and switchyard isolation

(Test 2)

Block loading one unit LOCA and one unit LOOP loads onto-the

Keowee underground power supply from Keowee standby condition

(Test 3)

Block loading one unit LOCA and one unit LOOP loads onto the

Keowee underground power supply simultaneously after.a Keowee load

rejection (Test 4)

Block loading single unit LOCA followed by two unit LOOP loads

onto the Keowee underground power supply after a Keowee load

rejection (Test 5)

Block loading single unit LOCA followed by two unit LOOP loads

onto a Lee combustion turbine power supply (Test 6)

For each of the tests, inspectors walked down.the 4.16 KV safety-related

switchgear and selected 600V switchgear immediately before the test to

verify circuit breaker positions, protective relay status, and power

monitoring instrumentation. During the tests, the inspectors observed

Enclosure 2

  • II13

breaker operations and voltmeters. The inspectors determined that-the

testing described above.was conducted in accordance with the licensee's

test procedure.

b.2 Conduct of Testing

Test Preparation Activities

Refer to Section 05.1.

Pre/Post-Test Briefings

Prior to ea-ch test, the licensee conducted pre-test briefings for all

personnel involved in testing. Pre-test briefings were conducted by a

manager specifically assigned oversight of testing and the test

coordinator for each test. The manager emphasized nuclear safety as the

primary focal point of his portion of the brief. The test coordinator

emphasized test evolution control and communications: The coordinator

exhibited a questioning attitude to assure all present understood the

test, their responsibilities, and duties. The inspectors considered the

pre-briefs conducted prior to each test to be thorough and they

appropriately emphasized nuclear safety.

After completion of each test, a post-test brief was conducted by the

test coordinator with all personnel involved in the test. These briefs.

focused on data acquisition results, test acceptance criteria, lessons

learned, necessity for procedure changes prior to continuing, equipment

repairs, and other concerns. Again, a questioning attitude was

.

demonstrated by the test coordinator to assure that all who participated

in the test identified any concerns so that appropriate resolution of

issues would be accomplished prior to test-resumption. The inspectors

considered the test post-briefs to be thorough and they appropriately

addressed issues requiring resolution prior to continuation of testing.

Control Room Activities

The inspectors monitored testing activities from the Unit .1/2 control

room and the Unit 3 control room.' The test coordinator was located in

the Unit 1/2 control room for all testing. The inspectors noted during

the first test, that the Unit 1/2 control room activity and response to

annunciation after test initiation could have been improved. Unit 1/2

control room activity and response to annunciation for subsequent

testing was improved. Command and control in both control rooms during

all testing was good. Control room briefi-ngs for the Operations crew

were conducted by the Operations Shift Manager prior to each test'

initiation. These briefings were good and focused on Nuclear Safety and

the appropriate response by operators in the .event of equipment

problems. Operators were observed while performing-test.steps. Good,

communication/coordination/verification techniques were noted. The test

coordinator maintained good control of all test evolutions. The

Enclosure 2

14

inspectors concluded testing activities conducted in the Unit 1/2 and

Unit 3 control rooms were good and operators maintained appropriate

focus on nuclear safety at all times.

Keowee Hydro/Lee Combustion Turbine (CT) Units' Activities

The inspectors observed activities in the Keowee Hydro Units (KHU)

control room (CR) during the performance-of TT/O/A/0610/025. The KHUs

met the acceptance criteria for all six tests. The inspector did not

identify any abnormal operation or annunciation in the KHU CR during the

performance of TT/0/A/0610/025. Activities in the CR were adequately

controlled by the Keowee operat.ors. Continuous communications with the.

Oconee test coordinator were established without any problems. The

Keowee operator and several other key KHU personnel attended the pre-job

briefings and.post job briefings. There were no issues raised by KHU

operators.during the post job briefings.

The inspectors witnessed the startup and operation of the 6C Gas Turbine

at the Lee Steam Station for the block loading of an Oconee single unit

LOCA followed by two unit LOOP loads during the sixth part of

TT/O/A/0610/025.. The activity was accomplished in accordance with the

Lee Steam Station Procedure. Emergency Power or Backup.Power to Oconee.

and no deficiencies were noted.

Other Plant Testing Activities

At the switchgear locations, inspectors observed that the pre-test

alignments were according to the procedure. Inspectors also observed

that.monitoring and recording instruments were installed per-the

procedure. This instrumehtation recorded current, voltage and power.

The inspectors observed that buses were re-energized at times consistent

with the expected system performance, and there'were no unexpected

voltage excursions that could be seen from observing the voltmeters.

The inspector noted that the licensee had test engineers and technicians

stationed at the switchgear locations. The inspectors noted that these

engineers and technicians were experienced in performing testing. The

inspectors concluded that observed test activities were conducted in a

good manner.

b.3 Test Results

Test Procedure TT/O/A/0610/025, Emergency Power And Engineered

Safeguards Functional-Test, provided acceptance criteria for each test

as follows:

Test 1 - Both Keowee Units.emergency start from simulated LOOP

actuation. The Keowee underground power supply unit obtains rated

speed and voltage less than or equal to 23 seconds after emergency

start actuation. Each Oconee unit automatically transfers-to

receive power from the Keowee underground power suppl.y.

The

  • ..

Enclosure 2

15

connected 4 KV motors and. 600V component cooling pump LOOP loads

start, accelerate, and continue to.operate until secured.

Test 2 - Both Keowee Units emergency start from simulated LOOP

actuation. The Keowee overhead power supply unit separates from

the system grid on emergency start actuation. The switchyard

isolation logic properly isolates the Yellow bus from the system

grid. The connected 4 KV motors and 600V component cooling pump

LOOP loads start, accelerate, and-continue to operate until

secured.

Test 3 - Both Keowee Units emergency start on engineered

safeguards actuation. Oconee Units 1 and 3 automatically load

shed and transfer to receive power from the standby bus. The

Keowee underground power supply unit accepts load at reduced

voltage and frequency. Connected Unit 3 4KV motor and 600V LOCA

loads start, accelerate, and continue to operate until secured.

The connected non-load shed loads are-energized following the

transfer to the standby bus. All ES 'actuated Motor Operated

Valves (MOVs) operate to their ES position. LPI flow is greater

than or equal to 2800 GPM per pump in less than or equal to 48

seconds. The licensee revised their test-procedure to start the

underground Keowee unit without pre-lube on its lower bearing;

this provided a more realistic start configuration for the unit.

The start time for the affected unit was not affected.

Test 4 - Both Keowee Units emergency start on engineered

safeguards actuation. Oconee Units 1 and 3 automatically transfer

to receive power from the standby bus. The Keowee Unit

underground power supply Air Circuit Breakers (ACBs) open on

emergency start actuation. Connected Unit 3 4KV motor and 600V

LOCA loads start, accelerate, and continue to operate until

secured. The connected non-load shed loads are energized.

following the transfer to the standby bus. All ES actuated MOVs*

operate to their ES position. LPI flow is greater than or equal

to 2800 GPM per pump in less than or equal to 48 seconds.

Test 5 - Both Keowee Units emergency start on engineered.

safeguards actuation. The Keowee Unit underground power supply

ACBs open on emergency start actuation. Each Oconee unit

automatically transfers to receive power from the standby bus.

Connected Unit 3 KV motor.and 600V LOCA loads start, accelerate,

and continue to operate until secured. The connected hon-load

shed loads are energized following the transfer to the standby

bus. All ES actuated MOVs operate to their ES position. LPI flow

is greater than-or equal to 2800 GPM per pump in less than or

equal to 48 seconds.

Test 6 - Each Oconee Unit automatically transfers to receive power

from-the standby bus energized by a Lee CT. Connected Unit 3 4KV'

Enclosure 2

16

motor and 600V LOCA loads start, accelerate, and continue to

operate until secured. The connected non-load shed loads are

energized following the transfer to the standby bus. All ES

actuated MOVs operate to their ES position. LPI flow is greater

than or equal to 2800 GPM per pump in less than or equal to 48

seconds.

The inspectors monitoring the test were able to observe that the

generators, control circuits, key valves, large motors, and pumps met

the specific acceptance criteria during the tests. The licensee, during

each test, verified and. recorded whether any overcurrent devices had

actuated. Status of the overcurrent devices was an indicator that

adequate voltage was provided throughout the system, and factored into

the decisions to proceed with the next test segment. The licensee .

reviewed test results after each test was conducted and concluded that

test acceptance criteria was met. The inspectors reviewed available

data after each test and independently determined acceptance criteria

was met. The licensee will be providing a test report to the NRC after

all data is reviewed and validated.

b.4 Deficiencies Identified During Testing Requiring Further Disposition

Blown fuse in control circuit for 3A CC pump

During performance of Test 1, the licensee recorded that nonsafety

related Component Cooling pump 3A was not running. This was a test

anomaly in the sense that this pump was not.load shed, and should have

run after re-energization of the bus. This pump was powered by a 60-hp

motor fed from a motor control center. Trouble-shooting identified that

the fuse on the secondary side of the control power transformer had

blown. The fuse that had blown was rated 3-amp, and was.a Gould Shawmut

style OT. Persons doing the trouble-shooting noted that the Control

Fuse Replacement List indicated a 4-amp Bussman style FRN fuse for .this

particular model and size of motor controller, and therefore they

replaced. the.blown OT-3 with an FRN-4.

PIP 3-097-0040 was written to evaluate this potential fuse control

problem. As part of the PIP evaluation, the control circuit fuses for

the six Component Cooling pumps were -inspected. Each control circuit

had two primary fuses and one secondary fuse. A total of seventeen

fuses were inspected, twelve primary and five secondary. The PIP stated

that one secondary fuse was a 3-amp NON style fuse by Bussmann Co. and

four secondary fuses were 6-amp NON fuses. The Control Fuse Replacement

List recommended Bussmann Co. time-delay, dual-element fuses. The OT

and NON fuses were non-time-delay fuses, and therefore, were suspected

of being incorrect for the application. After review of the time

current characteristics of the'OT-3 and NON-3 fuses (which were very

similar) as compared to the inrush current of the contactors in the CC

pump circuits, the inspectors noted that these fuses may have been too

fast acting for the application. A review of work requests for the CC

Enclosure 2

17

pumps indicated that-the OT-3 fuse in the 3A Component Cooling pump

circuit blew, and had been replaced in July 1994. The primary side

fuses in the CC pump control circuits were acceptable for the

application.

The licensee was continuing to evaluate the above information and

ramifications with regard to the overall fuse control program for

nonsafety-related circuits and system loading in relation to test

results. The licensee stated that control over safety-related fuses was

not in question, because they had just completed a program of field and

design verification for all the safety-related fuses. The determination

by the licensee was that total system loading remained sufficient to

meet test objectives. Section E1.2 further addresses this issue.

Overload relays trip reactor building cooling units

The safety-related reactor building cooling units (RBCUs) are driven by

two-speed motors. When the control switch is placed in high speed mode,

the motor starts in low speed, runs for about 25 seconds-(timer set

point) then transitions to high speed. A three second time delay is

inserted between de-energizing the low speed contactor.and energizing

the high speed contactor. An Engineered Safeguards (ES) signal

overrides th.is control sequence. Upon an ES signal, the RBCUs run in

slow speed with the thermal overload relays bypassed.

Pre-test alignment required two RBCUs per unit to be running in high

speed. During.Tests.1 through 5, one RBCU tripped on overload, and

during Test 6, two RBCUs tripped on overload. The 1B RBCU tripped

during Test 5. The IC RBCU tripped during Tests 3, 4 and 6. The 2A

RBCU tripped .during Tests 1 and 2. PIP 2-097-0044 was written to

evaluate this situation as a test anomaly.

Trouble-shooting; monitoring instrumentation data, observation., and

evaluation led the licensee to the following cause for these trips.

Following a LOOP, when power was restored to a previously running RBCU,

the cooldown period for the high speed thermal overload relays was about

61 seconds maximum (28 seconds due to the control timers plus the LOOP

time of not more than 33 seconds). When the still hot high speed

thermal overload relays were subjected to starting inrush current.into

the high speed winding, they were very close to tripping. Thermal

overshoot phenomenon caused tripping a few seconds after current had

returned to normal running current.

The inspectors reviewed the relevant elementary diagrams to confirm

operation of the control circuit. -The inspectors concluded that the

safety significance of the high speed overloads tripping on the RBCUs

during the test did .not affect test results. This was based on the fact

that the safety-related function of the RBCUs was to run in low speed

with the. overloads bypassed. In other modes of operation, the motor

windings should be protected by the combination Of control'timers and.

Enclosure 2

18

thermal overload relays.

Since the RBCUs did start and run for a brief

period, their load was present during critical times from an electrical

systems performance perspective.

c. Conclusions

The inspectors concluded that integrated testing of the Oconee emergency

power system was satisfactorily accomplished in accordance with the

licensee's test procedure and that deficiencies identified during

testing were, or'will be.resolved in accordance with the licensee's

problem investigation process. Control of all test activities was good.

Positive observations were made relating to test briefings, control room

briefings, and communication/coordination of test evolutions.

E1.2 Fuse Control Program (37551)

Inspection Scope

The inspector reviewed the method which the licensee utilizes to address

fuse failures. The inspection effort incTuded reviewing the licensee's

Maintenance Directive 4.4.12, Preliminary Engineering Support Program on

Fuses. PIPs, and WOs.

Observations *and Findings

Maintenance Directive 4.4.12 establishes guidelines for the replacement

of fuses once a failure occurs. A root cause evaluation is to be

conducted by engineering once a failed fuse is identified unless the

fuse failed because of a true overcurrent condition. The licensee will

be revising Maintenance Directive 4.4.12 to include Drawing OEE-36A,

Control Fuse Replacement List, which identifies.fuses which should be

used in Motor Control Centers, and to make reference to generating PIPs

as necessary. The licensee is developing an engineering support program

on fuses which should be completed in the near future.

The licensee recently completed-a configuration control inspection,

which has been going on since 1991, on all safety-related electrical

cabinets. In part, the inspection included removing fuses and verifying

that the fuses were the correct size and manufacturer. The inspector

accompanied the licensee on their final inspection of the last two

electrical cabinets. No discrepancies were identified during this stage

of the inspection. At this time, the licensee does not anticipate

performing inspections of nonsafety-related electrical cabinets.

Nonsafety-related fuse problems are to be resolved via Maintenance

Directive 4.4.12.

The inspector reviewed past and present PIPs involving fuses. The

licensee has identified several fuse issues and has appropriately

addressed them. The only significant issue is'already addressed as

Unresolved Item (URI) 269,270,287/96-17-03, RBCU Operability Concerns

  • .Enclosure

2

19

Due to Wrong Type Fuse In Control Circuit. Regarding unit restart, the

correct fuses were subsequently installed in Units 1, 2, and 3 under WOs

97008569. 96006532, and 96101374, respectively. As there is no present

RBCU fuse operability concern, the URI will be addressed by an NRC

Regional inspector at a later date.

Conclusions

The inspector concluded that the licensee's fuse control programs

adequately address the resolution of.fuse failures.

E1.3 Inadvertent Draindown of the Unit 3 RCS (37551).

a. Inspection Scope

The inspector reviewed the actions taken by the licensee with respect to

the February 1.'1997, inadvertent diversion of water from the Unit 3 RCS

to the Borated Water Storage Tank (BWST). The inspector reviewed the

recovery actions, control board indications, operator logs, and computer

trends. At the time, Unit 3 had completed refueling, the reactor head

was installed, the RCS was at atmospheric pressure (primary hand holds

were open on the Once Though Steam Generators (OTSG)

-and three CRD' vents

were open), and there was very little decay heat '(outage length greater

than 120 days).

b. Observations and Findings

The Unit 3 LPI system is a dual train system used to remove decay'heat

from the reactor fuel. It takes a suction from the bottom of one of the

two RCS hot legs and discharges through two separate heat exchangers,

where the RCS fluid is cooled, and then returned to the RCS via two

separate discharge paths. There is a branch off-each injection train

for pump testing that leads to a common line to the BWST. These branch

test lines, which contain isolation Valves 3LP-40 (3A LPI Header Test

Line Valve) and 3LP-41 (3B LPI Header Test Line Valve), discharge to the

BWST via a common line through isolation Valve 3LP-42 (Return to the

BWST).

On February 1..1997, at approximately-7:00 p.m., a primary Non-Licensed

Operator (NLO) was dispatched to open Valve 3LP-42 for a visual leakage

inspection (VT-2) of the welds downstream of 3LP-40.This line had

recently been.modified per Minor Modifications ONOE-8857, ONOE-8859,

ONOE-8860. and ONOE-8953. Valves 3LP-40 and 3LP-42 had been replaced

and the associated piping reconfigured as described above.

At 7:55 p.m., on February 1, 1997, a control room operator observed RCS

level at approximately 22 inches on reactor vessel level indicator LT-5,

and decreasing. (Just prior to Valve 3LP-42 being opened, reactor

vessel level was stable at 80 inches on LT-5.)

The operators

immediately started makeup to the RCS and closed 3LP-14.("B" Injection

Enclosure 2

20

Train LPI Cooler Discharge Valve). From the time that level was.

observed to be dropping until the operators closed 3LP-14, approximately

three minutes past. The operators reviewed the actions in Abnormal

Procedure AP/3/A/1700/26 Case "C", Loss of Decay Heat Removal.

During

the event, RCS level decreased to 18 inches (as indicated by LT-5) with

make-up to the RCS in progress. Later, the licensee calculated that

actual RCS level never decreased to less than 50 inches (the LT-5 level

indication was incorrect due to the rapid RCS pressure decrease caused

by the loss of inventory). -Approximately 4000 gallons in five minutes

were added by the operators to the RCS. to return level to normal (80

inches on LT-5).

Decay heat removal was not lost during the event. The

licensee notified the NRC resident inspector at approximately 10:45 p.m

as.a courtesy and the inspector promptly responded to the site (11:15

p.m.).

The control room subsequently contacted the NLO to close 3LP-42.

Investigation identified that Valve 3LP-40 was open. Operations

personnel attempted to close the valve, turning the valve operator in

the clockwise direction. Investigation further revealed the.valve

operated in the reverse.direction (clockwise to open, counterclockwise

to close). Although Valves 3LP-40 and 42 were bought at the same time,

under the same purchase order and specification, Valve 3LP-42 was

clockwise to close. The licensee initiated PIP 3-097-0439 and initiated

. an Event Investigation Team to evaluate the event.

The licensee is investigating the procurement, installation, and test

requirements of Valve 3LP-40, as well as attendant modification details.

The NRC will review: the results of the licensee's team; valve

  • modification functional test requirements; modification piping pressure

requirements: valve receipt inspection requirements: valve vendor

  • requirements: and other germane aspects. The issues associated .with

this event will be tracked as URI 50-287/96-20-03. Loss of RCS

  • Inventory.

Following the draining event, the licensee realized that the piping

pressure rating and drawings had not been updated. This resulted in

requiring a hydrostatic test of the modified piping at.approximately 650

psig in lieu of the original test pressure (i.e., head pressure of the

BWST). Licensee review and approval of the modification failed to

identify the preferred.change in piping class and pressure rating.prior

to implementing the modification. This is recognized as an engineering

  • weakness.

c. Conclusions

Shift personnel acted promptly and conservatively to stop the event and

identify the cause of the loss of RCS inventory. An engineering

weakness involving modification review and approval was identified.

Pending further review,'this event is being addressed as an URI.

Enclosure 2

21

E1.4 Unit 2 Reactor Building Material Condition

a. Inspection Scope (37551, 92903, 92902. 92901. 71707)

The inspectors reviewed reactor building (RB) closeout issues during the

inspection period. Several material condition items were identified.

b. Observations and Findings

During this period, the inspectors evaluated the licensee's close-out of

the RBs, particularly the Unit 2 RB as it was prepared.to return to

power .operation.

Reflective of the fact that the licensee had no proceduralized RB

closeout, a number of conditions were encountered by the residents that

required technical evaluation by the licensee. Tape, loose paint, and

insulation without supporting documentation were found in significant

quantities in various locations in the Unit 2 RB. These were of concern

due to the requirements of 10 CFR 50.46 to ensure long-term cooling.

Until canceled on April 16, 1996, the licensee had a Quality Assurance

walkdown procedure (Procedure QAD-1 Nuclear Inspection Program.

Housekeeping Inspection) that included the RB, but it was limited in

nature and was only performed after a refueling outage. It was not

scheduled to be performed after this protracted Unit 2 forced outage.

After the inspectors had identified a number of discrepant items in the

Unit 2 RB, QA and maintenance did perform a more complete material

condition closeout inspection.. Much tape, paint. and insulation were

removed from the Unit 2 RB, and later in the Unit .1

RB (Unit 3 exhibited

similar conditions, but was still in its refueling .outage and not ready

for closeout). Operations had a section.in their startup procedure

(OP/2/A/1102/01 Enclosure 4.8. Reactor Building Checklist at Hot

Shutdown) that required them to walkdown the RB. There was not a pre

startup material condition inspection requirement in that procedure.

Licensee RB closeout had been performed on an on-the-job performance

basis by the RB maintenance coordinator with no clear implementing

procedure guidance. Standard licensee RB material policy was to replace

like for like on an as needed basis. The material condition instruction

for the site (NSD 104. Housekeeping.Material Condition, and Foreign

Material Exclusion) did not specifically address the RB. Power

Chemistry Materials Guide Program, SDQA Plan "D", did not address

insulations and tape used in the RBs. There were specific coatings

identified for use in the RB,.but the licensee had yet to schedule

maintenance of the deteriorating liner coating conditions found in the

Unit 2 RB prior to the December 1996 NRC tours.

As required by 10 CFR 50 Appendix B, Criterion V. quality related

activities must be prescribed by procedure.. The licensee did not have.a

procedure to ensure the RBs were returned to proper material

configuration prior to power operation. This is identified as Violation

Enclosure 2

22

(VIO) 50-269,270,287/96-20-04, Failure to Have RB Material Condition

Closeout Procedure.

During the inspection period, the licensee removed material from the

Unit 2 RB to ensure a recirculation flow path during emergency

conditions and due to the fact that for certain fibrous insulation and

tape present in the RB there was no clear specification for its use.

The inspectors questioned the acceptability of the licensee's evaluation

for past RB recirculation operability (OSC-6827, Rev 0, Oconee Nuclear

Station Units 1, 2. and 3 Emergency Sump Operability Evaluation, dated

January 24, 1997). At the end of the inspection period, the licensee

was re-evaluating past operability conditions for the RBs.

Until this

re-evaluation can -be completed by the licensee and it can be

appropriately reviewed by the NRC, this item is identified as URI 50

269,270.287/96-20-05, Past Operability of RB Recirculation Flow Path.

c. Conclusions

A violation was identified because the licensee did not have a

programmatic material condition RB closeout procedure.

The lack of a

procedure (organized program) resulted in a poor understanding of RB

material condition and past operability RB recirculation flow path ,

concerns. Pending further inspection, this issue is being addressed as

an URI.

E2

Engineering Support of Facilities and Equipment (71707, 37550, 37551,

92903, 40500)

E2.1 Generic Letter (GL) 96-06, Assurance of Equipment Operability and

Containment Integrity During Design Basis Conditions

a. Inspection Scope

The resident inspectors were involved with review of GL 96-06 related

site activities, observed operational and plant changes that emerged,

and attended Plant Operational Review Committee meetings on the subject

prior to restart.

b. Observations and Findings

Based on their review of the plant design basis and equipment history

with regard to the GL issues,'the licensee took actions to ensure the

units met the intent of the GL prior to restart. The licensee's-actions

were as follows:

-

performed a safety-related systems water hammer modeling study to

the extent necessary to comply with the GL and provide short-term

actions for re-start

Enclosure 2

23

made a 10 CFR 50.72 report on January 24 regarding a technical

issue discovered during the above modelling

-

made plant configurational changes to mitigate possible

operational problems for issues discussed in the GL

-

issued a response to the GL by the date specified (January 28)

The licensee had made two configurational changes to Unit 2 prior to its

restart. Similar changes are expected for the other units prior to

their restart. The changes were as follows:

The auxiliary fan coolers in the RB were drained and isolated.

This prevented any potential water hammer in the LPSW system

during certain accident conditions discovered in the above

modelling. Although the computer model identified potential water

hammer in this piping, historically, the licensee had no visual

evidence of water hammer nor was it observed during the recent ES

testing (an engineer.had been stationed by the potentially'

affected piping during tests on January 2 - 6).

-

Several pipe runs between-valves in the RB could be susceptible to

overpressurization during certain accident conditions. These

piping runs were partially drained to allow for water expansion

during heating in postulated accidents.

c. Conclusions

  • The licensee made a concerted effort in addressing the issues of GL'96

06 as it relates to the Oconee design basis. Their long-term GL

response concerning RB penetration over pressurization and water hammer

is scheduled for issue by April 15 and August 1, 1997, respectively.

E2.2 2LP-18 Pressure Locking Issue

a. Inspection Scope

.

  • The

inspectors reviewed the licensee's actions in relation to an

operability issue associated with Unit 2 containment isolation Valve

  • 2LP-18. The inspectors reviewed the facts concerning PIPs 2-097-0487 and

95-1440 that had been generated by the licensee regarding this issue,

and then observed the licensee's activities to resolve the operability

concern.

b. Observations and Findings

The licensee was performing PT/2/A/0150/15B, Intersystem LOCA Leak Test,

on January 31, 1997, on the LPI piping. This test.verified that the RCS.

check valves properly seated. At the beginning of the test for check

Valve 2CF-13, the system pressure was indicated to be 830 psig on

Enclosure 2

24

pressure indicator 2LPIPG1043. This meant that the RCS side check valve

had not fully seated and that the section of piping between the RCS

check valve and LPI isolation Valve 2LP-18 was pressurized to existing

RCS pressure. In accordance with the test procedure, the pressure was

then bled off to approximately 300 psig. The RCS check valve

subsequently seated. At-the time the technician read the 830 psig, his

procedure did not address higher pressures in the line and he did not

recognize that system pressure could have pressurized the valve bonnet

and the area between the valve's double disc; thereby hydraulically

locking the valve and making it unable to open.

On-February 3, 1997. the engineers associated with the test realized the

potential significance of the high pressure during the test relative to

the subject double-disc valve. Based on the evaluation in PIP 97-0487

on February 5, 1997, Operations declared the affected train of LPI

inoperable and entered a 72-hour Limiting Condition for Operation (LCO)

per TS 4.5.1.2.1.

Procedure TT/2/A/0150/046, Functional Verification Procedure for 2LP-18,

was generated and approved to stroke the valve and eliminate any

possibility of a pressure binding issue and to assureoperability of the

valve. The valve was successfully stroked on February 6, 1997, per the

approved procedure and the valve/system was declared operable before the

LCO expired. The inspectors were present for the stroke test.

Generic Letter (GL) 95-07, Pressure Locking And Thermal Binding Of

Safety-Related Power-Operated Gate Valves, was issued in 1995 by the NRC

to address the issue of valve pressure locking and to alert the licensee

of the potential thermal hydraulic locking of certain double disc .

valves.

This problem was captured in PIP 95-1440 by the licensee. The

corrective .action for the PIP had already modified the Unit 3 LP-17 and

18 valves and had the Unit 1 and 2 valves scheduled for modification

during their next refueling -outage.

The licensee initiated intersystem LOCA surveillance PT/2/A/150/15B on

January 31, 1997. When PIP 95-1440 was evaluated to have the subject

valves (2LP-17 and 2LP-18) modified to prevent pressure locking, the

surveillance was not modified to recognize the potential impact when the

RCS check valves failed to reseat above a critical pressure for the

subject valves.

c. Conclusions

Once the licensee identified the pressure-locking potential associated

with 2LP-'18, their efforts were appropriate. However, the intersystem

LOCA surveillance had not been modified to recognize the potential

impact when the RCS check valves failed to reseat above a critical

pressure for Valves 2LP-17 and 2LP-18. This indicated a.weakness in

-the

operating experience and PIP-data base integration into the testing

program.

Enclosure 2

25

E.2.3 Testing of Unit 2 Moisture Separator Reheater (MSR) Drain System

Modifications

a. Inspection Scope

The Unit 2 MSR drain system experienced a pipe rupture on September 24,

1996. Prior to the Unit 2 restart, the inspectors reviewed the test

procedures and activities related to testing the MSR drain system (NS.M

ON-22941 discussed in Inspection Report 96-17). Also, during power

escalation and steam admission to the secondary piping, the residents

were oh hand to observe the licensee's test efforts,.as well as the

modification's impact on secondary plant piping and its operation.

b. Observations and Findings

The inspectors reviewed the MSR drain system modification test

procedures prior to Unit 2 restart and found them to be adequate.

Implemented during startup of the Unit 2 modified MSR drain system,

these procedures were utilized to evaluate the automated MSR drain

system controls during main turbine generator (MTG) warmup, startup, and

power ascension to 30 percent of plant rated ca-pacity, as well as to

monitor the drain system for water hammers or other affects that could

be damaging to plant equipment or personnel.

During the period between reactor startup and power ascension, no

personnel were required to enter the potentially hazardous secondary

areas for valving operations. The modifications had eliminated the need

for general personnel entry. Additionally, until-new welds.and the

modification performance could be evaluated, licensee management had

clear controls to prevent inadvertent.entry into the potentially

hazardous areas.

For observation purposes, engineers were posted at safe locations around

the potentially hazardous areas. The licensee's engineers were

positioned throughout the plant during the startup to monitor plant

performance and document any disturbances identified. Additionally,

,remote cameras were placed in three locations for monitoring.

The test procedures utilized were as follows:

  • TT/2/B/0271/011, Controlling Procedure for NSM ON-22941, 2MS-112

and 2MS-173 Controls and.,Heater Drain Upgrade Post Modification

Testing. The purpose of this procedure was to monitor and.

document the performance of the secondary testing activities, to

provide engineering oversight, and to provide a means of

evaluating performance of the modified equipment.

  • TT/2/B/0271/012, Controlling Procedure For NSM ON-22941 for

Testing and Tuning the Moore Controllers Associated With 2MS-112,

Enclosure 2

26

2MS-173, 2HD-92, 2HD-95, 2HD-37, and 2HD-52. This procedure

tracked changes in the input/output signals of the new automated

Moore secondary valve controllers, provided instructions for data

collection, and ensured proper controller tuning during plant

startup and operation.

The MTG was taken off its turning gear with. the reactor at 15 percent

power and was brought to the operating speed of 1800 rpm on February 3,

1997. When the MTG was connected to the electrical grid at 10:06 p.m.,

somewater/steam hammers were noted at the first and second stage heater

drain tanks and associated piping. Approximately 5 to 6 water/steam

hammers with associated side to side pipe movement of about 3 to 5

inches in one plane (6 to 10 inches total swing) were observed over

approximately a five minute period.

There was no damage to piping or

hangers identified as a result of the water/steam hammers. The hangers

for the second stage heater drain tanks and associated piping had been

modified during the plant outage to eliminate rigid mounted hangers and

to support the heater string piping with a more floating type of support

system that allowed more flexibility and energy dissipation: This new

flexibility appeared to minimize the impact of steam/Water hammers to

the system.

c. Conclusions

Although some water/steam hammers were noted.during plant startup, the

licensee's efforts were effective in minimizing this problem. The

modified MSR drain system automated controls performed well and

eliminated the need for manual operation of the associated valves with

the unit operating at power: This reduced the potential personnel

hazards involved with secondary plant operation.

E.2.4 Design Changes and Plant Modifications

a. Scope

The inspector reviewed engineering activities associated with the design

and implementation of two Unit 3 electrical Nuclear Station

Modifications (NSMs) to determine if the.design controls and

installation practices were consistent with the 'guidance of the

licensee's implementing procedure NSD-301, Nuclear Station,

Modifications, Revision 10: licensee c'ommitments; and NRC regulatory

requirements.

b. Observations and Findings

The NSMs reviewed are as follows:

NSM-32962, "Replace Operator Aid Computer"

NSM-32873; "Modify MFDW Control on MSLB"

Enclosure 2

27

The inspector reviewed the theory and assumptions for the nuclear

station modifications and 10 CFR 50.59 Safety Evaluation for the changes

and determined that they were adequately reviewed/evaluated and that no

unreviewed safety questions were identified.

Nuclear Station Modification NSM-32962

This NSM provided for replacing the existing nonsafety-related Honeywell

Operator Aid Computer (OAC) on Unit 3 with an open architecture, data

acquisition system that can utilize commercially available components.

The field installation work on Unit 3 OAC replacement-was over 90

percent complete. The new OAC installation involved rewiring

approximately 1200 analog inputs and 2000 digital inputs from the

existing OAC. The inspector found that the new OAC equipment was

installed in existing analog and digital input cabinets utilizing

terminal strip racks and swing arm devices that were fabricated to

accommodate installation of the new equipment. Some of the cabinets had

been removed because they were no longer needed with -the new equipment.

The terminal strip racks and connectors were pre-assembled, wired and

tested in special trailers that had been setup specifically to. support

the 0AC modifications. This reduced the required installation time in

the field.

The inspector observed that the field routed cables were

labeled, neatly bundled and terminated on the terminal blocks.

The

licensee had approximately 200 data points that had been temporarily

wired to the Honeywell 45000 0AC to support the outage. These 200

points still remained to be rewired to the new 0AC. The licensee

indicated that a significant amount of testing remained to be completed,

including startup testing. Although the OAC is a nonsafety-related

system, it interfaces with safety-related systems such as the Inadequate

Core Cooling Monitor (ICCM).

The inspector examined some of the details

associated with these interfaces and found them to be acceptable.

The licensee had initiated 26 Variation Notices (VNs) for'this

modification. The inspector reviewed the first 24 VNs issued and

confirmed that they had been properly reviewed and approved. The

inspector found that one PIP had been issued because of a design wiring

error which resulted in a breaker tripping.in the plant when the circuit

was energized. A VN was issued to correct the wiring problem. This was

one of the 24 VNs reviewed by the inspector.

The inspector expressed a concern to the lead engineer that 24 VNs

appeared to be a significant number of VNs against one NSM. The lead

engineer indicated that the number of VNs was not excessive considering

the fact that the modificafion involved over 3200 separate data inputs

and several hundred drawings. The inspector considered the licensoees

explanation to have some merit. The inspector found that the licensee

routinely critiques engineering and craft performance on modifications.

The number of VNs is one area that is normally assessed to judge quality

of design. Based on this information the inspector had no further

Enclosure 2

28

concerns regarding the-number of VNs issued. The inspector concluded

that design controls for the GAC modification were adequate.

Nuclear Station Modification NSM 32873

This NSM provided for the addition of safety-related -circuitry to detect

and mitigate a Main Steam Line Break (MSLB) on Unit 3. Similar

modifications had been implemented on Units 1 and 2. This modification

was .implemented,to resolve a safety issue involving the potential of

over pressurizing the containment during a MSLB inside containment

without operator action. This safety issue resulted from the licensee's

reanalysis .of the FSAR Chapter 15 MSLB transi.ent.

By letter dated June 14, 1995, the licensee provided NRC a supplemental

response to IE Bulletin 80.-04 in which they outlined the design basis

for the MSLB modifications. This submittal states that the associated

pressure transmitters, logic, and control circuitry installed by this

modification for mitigation of a MSLB will be safety-related, redundant

and single failure proof. It further states that the ma-in-feedwater

(MFW) equipment.being controlled by the new circuitry is nonsafety

related and is not single failure proof. This modification is being

implemented as an enhancement to the plant's mitigation.strategy for

MSLB. The inspector reviewed the Engineering Completion Notice (ECN)

and 50.59 Safety Evaluation for the changes and determined that they

were adequately reviewed and evaluated. No unreviewed safety questions

were identified. The inspector examined the redundant solenoid valves

that were installed in the control.air supply line for the Main and

Startup FDW Control valves. The inspector also examined the termination

cabinets 'housing the signal isolators, current switches, time.delay

relays, and power supplies. In the control room the inspector examined

the control room MSLB Train A and B Enable/Disable switch and manual

initiate pushbutton. The inspector concluded that the.modification was

being implemented on Unit 3 in accordance with the above licensee

commitments.

The inspector reviewed the two post modification critiques that had been

performed by the project manager after completion of the Units 1 and 2

MSLB modifications. The critiques evaluated the quality of the NSM by

examining scope changes,.major procedure changes,..variation notices, and

PIPs. The inspector found that the lessons learned from the Unit 1

modification had been factored in the planning for the Unit 2

modification and that this resulted in a reduction of craft hours, major

procedure changes, variation notices, and PIPs. However, a wiring error

occurred during the Unit 2 Modification that was not detected until

after post modification testing was completed. This resulted from an

inadequate post modification test procedure. This problem was

documented on a PIP .and corrective action was taken to address this

concern in the Unit 3 modification test plan.

.

Enclosure 2

29

On January 17, 1997, the licensee issued a Selected Licensee Commitment

(SLC) which requires operable MSLB detection, feedwater isolation

circuitry and main feedwater control valves to protect against

containment over pressurization during a MSLB inside containment. -The

licensee indicated that a TS Change request would be submitted later to

address the MSLB circuitry.

c. Conclusion

The inspector concluded that the design controls for the OAC and MSLB

modifications on Unit 3 were adequate. Overall engineering performance

on these modifications was considered good even though a significant

number of VNs had been issued against the OAC NSM.

E2.5 Unit 3 Integrated Control System (ICS) Modification (37550)

Background

The inspectors reviewed the licensee's quality.assurance measures

related to the ICS modification that was implemented on-Unit 3 during

the present refueling outage. The inspectors reviewed the modification

status, installation procedures, post-modificati-on test plan,

translation of system functional requirements into software, software

configuration management; software validation and verification (V&V),

and the 50.59 safety evaluation. The ICS system was classified as

important to safety, but not safety-related. Applicable regulatory

requirements were provided by 10 CFR 50.59. Specific inspection scope,

observations, findings, and conclusions are addressed in Sections

E2.5i-v.

i. ICS Installation Procedures and Post Modification Test Plan

a. Inspection Scope

The inspectors reviewed the installation procedures to determine if the

installation impacted unit safe shutdown conditions. The post

modification test plan was reviewed to assess the extent of system

function verification.

b. Observations and Findings

The procedures for installation of the modification were completed and

approved. Procedure 50.59 evaluations were adequate. The new ICS

control modules and wiring were available for installation. The

completion of the modification 50.59 evaluation was the primary obstacle

delaying modification installation. The unit was defueled during the

outage; therefore, *no potential impact on safe shutdown conditions

existed.

Enclosure 2

30

The post modification test plan was comprehensive: however, the test

plan relied mainly on testing conducted on the verification and

validation (V&V) simulator. Only a limited subset of these transients

were planned for actual plant testing at reduced plant conditions.. One

limitation of the V&V simulator was the inability to test the Stator

Coolant Runback function. The post modification test plan did not

include this function for actual plant testing.

Several ICS functions were not appropriate for actual plant testing,

including Asymmetric Rod Runback and.Loss of Four RCP's. The licensee

stated that the V&V simulator would demonstrate these functions and

point-to-point wiring checks during installation would be sufficient to

assure operability. However, t-he V&V simulator used software modeled

for Unit 1 configuration modified with Unit 3 response characteristi.cs

and was not validated for Unit 3 actual configuration. The licensee

indicated that V&V simulator testing: in conjunction with post

modification testing, provided adequate assurance that the ICS would

function as designed.

c. Conclusion

ICS modification installation procedures were completed and the

procedure 50.59 evaluations -were adequate. The post-modification test

plan did not test all design system equipmentfunctions, but was

considered adequate by the inspectors. Further followup inspection of

the test plan and post modification testing will be conducted under IFI

50-287/96-20-O8, ICS Post Modification Testing.

ii. Translation of ICS Functional Requirements into Software Specifications

a. Inspection Scope

The inspectors reviewed the -software requirements specification to

verify that software functional and performance characteristics were

correctly translated from the ICS design basisspecification. The

translation consisted of conversion of system functional requirements

into logic diagrams-that were then translated into computer codes for

the ICS control. modules.

b. Observations and Findings

The licensee developed Scientific Apparatus Manufacturers Association

(SAMA) logic block flow diagrams from the ICS design basis

specification. The SAMA logic diagrams defined the ICS functional

requirements and served as the software requirements specification and

software design description for the software used in the ICS control

modules. The SAMA diagrams were adequate for these purposes.

However, the inspectors initially noted that the SAMA logic diagrams did

not thoroughly specify the functional and performance characteristics of

Enclosure 2

31

the software. The inspectors also noted that there did not appear to be

traceability between the software functions depicted in the SAMA logic

diagrams and the ICS design basis document. In addition, the software

V&V plan did not clearly identify which tests were to be used to

validate each software requirement. As a result, the lack of

traceability to software requirements could contribute to incomplete

validation of the software functional and performance requirements.

In response to these comments, the licensee had an independent

assessment of the ICS design basis specification performed by an outside

contractor. During January 29 and 30, 1997, the inspectors reviewed the

contractor's report and found that similar concerns were identified.

The inspectors also reviewed the completed independent assessment of the

ICS control module software. The inspectors reviewed the licensee's

corrective actions for both of these independent assessments and found

the concerns were adequately addressed.

c. Conclusion

The inspectors determined that the software requirements

specification/software design description was initially incomplete and

that there was poor traceability to the ICS specification or to software

validation d.ocumentation. This limited the capability to independently

verify the translation of system functional requirements into software

coding which implemented the ICS functions. The capability to

independently verify the coding and.logic would provide assurance that

the system would function correctly. Based on the additional review,

the inspectors concluded that the licensee's corrective actions to the

independent assessments ha.d adequately addressed these concerns.

ii.i. Software Configuration Management

,a.

Inspection Scope

The inspectors reviewed the licensee's software configuration management

program as described in the Software and Data Quality Assurance (SDQA)

Plan to verify that software changes were properly controlled. The

inspector also reviewed an ICS control module program verification

procedure and calibration procedure to verify that controls existed to

ensure that the proper revision of the software was downloaded.into the

ICS control modules and that the downloaded software was the same as the

controlled copy.

b. Observations and Findings

The inspectors noted that the licensee's SDQA Plan contained a short

description of the software configuration management process, but that

it did not specify formal controls or procedures for managing the.

software change process during the software development. In reviewing

the licensee's software configuration management process,*the inspectors

Enclosure 2

32

noted that the licensee maintained an appropriate level of access

control to the controlled version of the software and maintained a

complete history of. software revisions. Each software revision was

assigned a revision number and the date of the revision was recorded.

The software revision list also includes a brief description of the

changes associated with each revision. The inspectors noted that each

software program header contained a-complete list of revisions and a

description of the changes -associated with each revision. The inspector

did not identify any deficiencies in the software revision lists or

program headers.

To address the concern of a lack of formal controls, the licensee had

placed the finalized revision of the ICS control module software in the

same control program used for engineering calculations. This provided

for a more formal method to control software revisions and.also resulted

in a more detailed explanation of software changes. Also, the licensee

stated that additional procedural controls required the verification of

ICS control module software against the controlled copy after any

maintenance actiVities.

c. Conclusion

The inspectors concluded that the licensee did not implement-a good

software engineering practice of establishing a software configuration

management plan or procedural controls.for managing software changes

made during the software development process. However, inclusion of the

ICS software in the engineering calculation control program provided

adequate configuration management controls.

iv. Software Verification and Validation

a. Inspection Scope

The inspectors reviewed the licensee's V&V program and preliminary V&V

results to verify that the ICS control modules software met the function

and performance requirements contained in the ICS design basis

specification and the SAMA logic diagrams. The V&V in conjunction with

post-modification testing were the major elements for assurance that the

ICS would pe.rform as designed.

b. Observations and Findings

At the time of the inspection, the final validation results were still

being documented. As previously discussed, there was poor traceability

.maintained during the software development: therefore, a thread audit

could not be performed. The licensee performed a verification of the

ICS control module software prior to integrating the hardware with the

software. In addition, a contractor performed an independent

verification of the source code and a comparison to the functional

requirements contained in the SAMA logic diagrams. The inspectors noted

Enclosure 2

33

that the licensee did not appear to have performed unit testing of the

software prior to integrating the software and hardware.

Although the source code Verification identified that there were errors

in the SAMA logic diagrams, no independent verification of the logic was

performed. The potential.for SAMA logic diagram errors and the poor

traceability between the V&V and software development indicated that the

licensee did not perform a rigorous verification of the software

requirements specification prior to writing the ICS control module

software.

After integrating the hardware and software, validation testing was

performed by the contractor using a V&V simulator that simulated inputs

to the ICS control modules. The validation was accomplished by

operating .the V&V simulator through various evolutions expected during

plant operations. Although the design simulator provided assurance that

the ICS would perform as designed.for the simulated conditions, there

were aspects of the simulator which challenged its validation as a

design verification tool.

As previously noted, the V&V simulator used

software modeled for Unit 1 and was not validated for Unit 3 actual

configuration. Additionally, the V&V simulator response was based on

anticipated plant conditions and only verified the associated software

and hardware performance. SAMA logic diagram and software errors

related to unanticipated plant conditions would not be identified. The

licensee stated that they would use their standard testing and

troubleshooting methods during post modification testing to identify and

correct ICS control module software errors.

The inspectors rev-iewed the contractor's final V&V report and noted that

the licensee had addressed all of the problems identified during the

software verification. However, the actual resolution of the problem

was difficult to determine because the resolution comments in the V&V

report only stated that the code was revised. In addition, the

inspectors noted that there was no description of the potential impact

of the software change resolution on the overall software program.

There was no requirement for a verification or regression testing of the

revised code. As discussed previously, to .address these concerns, the

licensee placed the finalized revision of the ICS software.in the same.

control program used for engineering calculations. Coding changes were

screened for potential effects on ICS operations: however, the inspector

did note that the effect on other plant procedures, particularly ICS

calibration procedures, was.not included in the screening. The licensee

stated they would consider adding such a review for future software

revisions.

c. Conclusion

The inspectors noted weaknesses in the licensee's software V&V related

to poor traceability between V&V and software development and no

independent verification of the SAMA logic diagram after indications

Enclosure 2

34

that errors existed. Following discussion with the licensee on these

issues, the licensee performed an independent verification of .the ICS

design. Based on the inspectors' review of the licensee's corrective

actions to the concerns identified in the independent review, the

inspectors concluded that the software development and V&V concerns

initially identified were .adequately addressed. The i.nspectors

identified no examples where operation or fault of the ICS would impact

the capability to safely shutdown the plant during any operating mode

condition.

v. 10 CFR 50.59 Unresolved Safety Question Evaluation

a. Inspection Scope

The inspectors reviewed the licensee's 10 CFR 50.59 evaluation to

determine if the licensee addressed digital equipment failures,

including software common mode failure considerations, as described'in

NRC Generic Letter (GL) 95-02, in addition to determining if an

unreviewed safety question (USQ) was' involved with this modification.

Although the ICS is categorized as a nonsafety-related system, it

provides inputs for various primary system setpoints and indications for

primary system parameters. The system is identified in the UFSAR and is

referenced in accident mitigation descriptions.

b. Observations and Findings

The inspectors noted that the responses to the standard USQ

determination questions in the 50.59 evaluation had incomplete

explanations. For example, on page 12 the statement "The instruments

being installed are at least equivalent to those currently installed."

did not include any explanations as to why the ICS control modules were

equivalent. On page 14,. when discussing the self-checking feature.

.

there was no discussion of whether a failure of this feature could-cause

an ICS control module to stop functioning needlessly and the impact on

margin of safety or malfunction of a different kind. On page.29, Loss

of Coolant Flow, was the statement that a LOCA is managed by the

Emergency Core Cooling System and the ICS does not play a major part in

.its mitigation. This did not discuss the response of the ICS nor did it

discuss the difference in possible response from the previous ICS. On

page 42, the first question states, "The failure modes of the new.ICS

are not more severe or more likely'than those currently analyzed or

submitted-in response to NUREG-0737." There was no documentation to

support this conclusion.

There was no mention of failure modes or how those failure modes would

be detected. The licensee stated that read back of the ICS control.

module output would be sufficient to detect internal failures. The

licensee was also in the process of performing a Failure Modes and

Effects Analysis (FMEA) for the .ICS control module. A failure of an

analog memory module, used to retain ICS statepoint data when an.ICS

Enclosure 2

35

control module fails, was annunciated in the control room. This

annunciation provided early warning to the operator to prevent unstable

ICS operation in the event of an ICS module failure after an analog

memory module failure. The inspector noted'that ICS reliability and

availability requirements were not specified in the ICS design

documents. The licensee stated these values would be determined through

their Maintenance Rule program.

An additional weakness of the 50.59 evaluation was the licensee's

analysis of the effect of the new ICS on accidents analyzed in Chapter

15 of the UFSAR. This review was limited to a review of the discussions

of ICS response in Chapter 15 of the UFSAR and did not include review -of.

the accident analysis assumptions or the basis for those assumptions..

Because of the summary nature of Chapter 15, insufficient detail existed

to determine if the ICS modification would have affected an underlying

accident analysis assumption or basis. For example, there was no

discussion of the response of ICS to a Steam Generator Tube Rupture in

Chapter 15. However, the licensee determined that because the ICS does

not directly affect steam generator tube integrity, there was no adverse

effect on this accident sequence due to the ICS modification. Further,

the licensee used vague language in describing the effect of ICS on

accidents analyzed in Chapter 15. For example, the discussion on

Startup Accident and Rod Withdrawal at Rated Power did not conclude .the

ICS responses would be similar. The fact.that the ICS modification

could cause a different ICS response from that assumed in the accident

analysis could result in an USQ determination. As a result of the

inspectors concern in this area, the licensee stated that available

accident analysis information would be reviewed.to ensure completeness

of the 50.59 evaluation. The licensee stated that they would document

this review in a revision to the approved 50.59 evaluation.

By internal memorandum dated February 171997, the licensee stated that

the original design information available and the original FSAR and

associated supplements had been reviewed. Based on this review, the

licensee had concluded that the ICS modification did not impact any

accident analysis assumptions. The inspectors reviewed this internal

memorandum and found the licensee had adequately addressed the

inspectors' concern.

c. Conclusion

The inspectors concluded the 50.59 evaluation USQ determination question

  • explanations were weak. However, the additional review conducted by

licensee had adequately addressed the inspectors' concerns.

Enclosure 2

36'

E8

Miscellaneous Engineering Issues (92903)

E8.1 (Open) VIO 50-270/96-13-10:

Failure to Perform Adequate 10 CFR 50.59

Evaluation

This violation was identified during a review of the completed

modification ONS-22975, Replace HPI Check Valves 2HP-126, 2HP-127, 2HP

152. and 2HP-153.. The review of the modification identified the lack of

a fatigue analysis. During this inspection period, the inspector

reviewed the corrective actions for identification and evaluation of the

modifications for Unit 2. The evaluations for Unit 2 were completed

prior to unit startup. The inspector did not identify any weaknesses or

deficiencies. This item is closed for Unit 2 but remains open for Unit

1 and Unit 3. Unit 1 and Unit 3 evaluations are to be completed prior

to startup of each unit.

E8.2

(Closed)fURI 50-270/96-13-09:

RCS Piping Socket Weld Failure

This URI involved a failure of a downstream socket weld on Valve 2HP

491. The weld was removed and transferred offsite for evaluation. The

evaluation has been completed and reviewed by the inspector. The

failure mechanism was identified as being fatigue related. Accordingly,

the licensee has committed to a fatigue analysis program. Based on the

implementation of a fatigue analysis program, this URI is closed.

E8.3 (Open) VIO 50-269/96-17-09: LPSW Modification Did Not Meet ASME Code

NDE Requirements

This violation concerned 8 welds on Unit 1/2 LPSW piping that did not

have proper NDE performed. Prior to the Unit 2 start-up from a recent

forced outage, the inspectors verified-that the affected piping welds

were satisfactorily hydrostatically tested per Procedure

TN/0/A/9749/MM/01M. Procedure to Install MM ONOE-9749 and Hydro Test a

Portion of LPSW Piping. This violation remains open pending review.of

associated root cause corrective actions.

E8.4 (Closed) EEI 50-270,287/96-16-05: Failure to Properly Install MSSV

Spindle Nut Cotter Pins

This issue involved several missing and incorrectly installed main steam

safety valve (MSSV) spindle nut cotter pins which could have resulted in

the affected MSSVs failing to -reseat and complicate recovery actions

from some plant transients. Following the associated predecisional

enforcement conference, this issue was dispositioned (by NRC letter

dated December 23, 1996) as Severity Level.IV Violation EA 96-478-01014:

Failure to Follow Procedure and Properly Install MSSV Spindle Nut Cotter

Pins. Accordingly, EEI 50-270,287/96-16-05 is administratively closed.

With respect to unit restart, the inspector verified that modifications

were made to remove MSSV fork levers, spindle nuts, and cotter pins on

all three units.

Enclosure 2.

37

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of.the inspection on February 12. 1997. The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

Partial List of Persons Contacted

Licensee

E.

  • Burchfield, Regulatory Compliance Manager

D. Coyle, Systems Engineering Manager

T. Coutu, Operations Support Manager

C. Curry, Test Coordinator

T. Curtis. Operations Superintendent

J. Davis. Engineering Manager

R. Dobson, Oconee Nuclear Station Engineering

W. Foster, Safety Assurance Manager

.J.

Hampton, Vice President, Oconee Site

S. Hollinsworth, Operations ShiftManager, Oconee Nuclear Station

D. Hubbard, Maintenance Superintendent

R. Lingle, Oconee Nuclear Station Operations

C. Little, Electrical Systems/Equipment Manager

B. Peele, Station Manager

J. Smith, Regulatory Compliance

NRC

D. LaBarge, Senior ProjectManager, NRR

J. Lazevnick, Senior'Electrical Engineer,NRR

D. Thatcher, Section Chief, Electrical Engineering Branch, NRR

Inspection Procedures Used

IP 71750:

Plant Support Activities

IP 71707:

Plant Operations

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 37551:

Onsite Engineering

IP 60710:

Refueling Activities

IP 61701:

Complex Surveillance

IP 37550:

Engineering

IP 93702:

Onsite Response to Events

IP 92901:

Followup-Plant Operations

  • aEnclosure 2

IP

9902:38.

I P 92902:

Followup-Maintenance

3

IP 92903:

Followup-Engineering

IP 40500:

Effectiveness of Controls for Problem Identification and Resolution

Items Opened, Closed, and Discussed

Oened

50-269,270,287/96-20-01

URI

SSF Past Operability (Section 02.2)

50-269.270.287/96-20-02

IFI

Unfiltered Motors (Section M2.1)

50-287/96-20-03

URI

Loss of.RCS Inventory (Section E13)

50-269,270,287/96-20-04

.

VIO

Failure to Have RB Material Condition

Closeout Procedure (E1.4)

50-269.270,287/96-20-05

URI

Past Operability of RB Recirculation Flow

Path (Section E1.4)

50-27.0/96-20-06

VIO

Failure To Use Procedure Administrative

Hold (Section 08.1)

50-269,270,287/96-20-07

NCV

Failure to Complete a Written Safety

Evaluation of Secondary Plant Piping Not

in Accordance With the Piping Code

Referenced in the FSAR (Section 08.1)

50-287/96-20-08

IFI

ICS Post Modification Testing (Section

E2.5i)

EA 96-478-01014

VIO

Failure to Follow Procedure and Properly

Install MSSV Spindle Nut Cotter.Pins

(Section E8.4)

Closed

50-270/96-13-09

URI

RCS Piping Socket Weld Failure (Section

E8.2)

50-270/96-17-08

E

Failure to Use Procedure Administrative

Hold (Section 08.1)

50-269,270,287/96-17-01

EEl

Failure to Complete a Written Safety

Evaluation of Secondary Plant Piping'Not

in Accordance With the Piping Code

Referenced in the FSAR (Section 08.1)

50-270,287/96-16-0.5

EEI

Failure to Properly Install MSSV Spindle

Nut Cotter Pins (Section E8.4)

Enclosure 2

39

Discussed

50-270/96-13-10

VIO

Failure to Perform Adequate 10 CFR 50.59

Evaluation (Section E8.1)

50-269/96-17-09

VIO

LPSW Modification Did Not.Meet ASME Code

NDE Requirements (Section E8.3)

List o.f Acronyms

ACB

Air Circuit Breaker

BWST

Borated Water Storage Tank

CFR

Code of Federal Regulations

CC

Component Cooling

CR

Control Room

CRD

Control Rod Drive

CT

Combustion Turbine

DPC

Duke Power Company

DRS

Division of Reactor Safety

ECCS

Emergency Core Cooling System

ECN

Engineering Completion Notice

EEI

Escalated Enforcement Item

EFW

Emergency Feedwater

EPRI

Electric Power Research Institute

ES

Engineered Safeguards

F

F

FDW

Feedwater

FME

Foreign Material Exclusion

FSAR

.

Final Safety Analysis Report

FWP

Feedwater Pump

GL

Generic Letter

GPM

Gallons Per Minute

hp

Horsepower

HD

Heater Drain

HPI

High Pressure Injection

IAW

In Accordance With

ICCM

Inadequate Core Cooling Monitor

I&E

Instrument & Electrical

IFI

Inspection'Followup Item

IE

Inspection and Enforcement

IR

Inspection Report

IP

Inspection Procedure

KHU

Keowee Hydro Unit

KV

Kilovolt

LDST

Letdown Storage Tank

LCO

Limiting Condition for Operation

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LPI

.

Low Pressure Injection

LPSW

Low Pressure Service Water

Enclosure 2

40

MFDW

Main Feedwater

MOV

Motor Operated Valve

MP

Maintenance Procedure

MS

Main Steam

MSLB

Main Steam Line Break

MTG

Main Turbine Generator

MVA

Mega Volts-Amps

MW

Megawatts

NCV

Non-Cited Violation

NLO,

Non-Licensed Operator

NRC

Nuclear Regulatory Commission

NRR

Nuclear Regulation and Research

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

0AC

Operator Aid Computer

ONS

Oconee Nuclear Station

OTSG

One Through Steam Generator

PCB

Power Circuit Breaker

PM

Preventive Maintenance

PIP

Problem InvestigationProcess

QA -

Quality Assurance

RB

Reactor Building

RBCU

Reactor Building Cooling Unit

RC.

Reactor Cool'ant

RCW

Raw Coolant Water

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RPS

Reactor Protection System

SLC

Selected Licensee Commitment

SFP

Spent Fuel-Pool

S-R

Safety Related

SSF

Safe Shutdown Facility

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

V

Volts

VIO

Violation

VN

Variation Notice

WO

Work Order

WR

Work Request

Enclosure 2