ML15118A154

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AIT Reps 50-269/96-15,50-270/96-15 & 50-287/96-15 on 960924-1008.No Violations Noted.Major Areas Inspected: Licensee Response to 960924 Event Re Balance of Plant Heater Drain Line Rupture
ML15118A154
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 11/04/1996
From: Jaudon J, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A153 List:
References
50-269-96-15, 50-270-96-15, 50-287-96-15, NUDOCS 9612030116
Download: ML15118A154 (50)


See also: IR 05000269/1996015

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

AUGMENTED INSPECTION TEAM (AIT) INSPECTION

Docket Nos:

50-269, 50-270, 50-287

License Nos:

DPR-38, DPR-47, DPR-55

Report No:

50-269/96-15, 50-270/96-15, 50-287/96-15

Licensee:

Duke Power Company

Facility:

Oconee Nuclear Station Units 1, 2 and 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

September 24 - October 8, 1996

Team Leader:

Thomas A Peebles, Chief

Date Signed

Operator Licensing and Human Performance Branch

Division of Reactor Safety

Inspectors:

P. Harmon, Senior Reactor Inspector, DRS

N. Economos, Reactor Inspector, DRS

D. Forbes, Inspector, DRS

E. Brown, AEOD

G. Hornseth, NRR

W. Scott, Inspector, DRCH/HQMB

R. Correia, DRCH/HQMB

G. Humphrey, Oconee Re 50ent Ins ector

Approved by:

.LZLAL

J ns P. Jaudon

Date Signed

puty DirectorI

ivision of Reactor Safety

Enclosure

9612030116 961104

PDR ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station Units 1, 2, and 3

NRC Inspection Report 50-269/96-15, 50-270/96-15, 50-287/96-15

The objectives of the inspection established for the NRC Augmented Inspection Team were

to: (1) determine the facts surrounding the specific event, (2) assess licensee response to

the event, (3) assess generic aspects of operations/inspections that may have had broad

applicability to other facilities, (4) oversee licensee activity during their event review, and

(5) interface with other on-site entities such as Occupational Safety and Health

Administration.

On September 24, 1996, at 4:45 p.m., during the restart of Oconee Unit 2, facility personnel

were manually realigning the moisture separator reheater drains at approximately 50 percent

power, when an 18 inch heater drain line ruptured. The water and steam, at approximately

400 degrees F., 250 psig, severely burned seven plant workers in the Turbine Building. The

personnel burned were involved in the manual realignment to feed-forward the heater drains.

Control room operators immediately tripped the Unit 2 reactor and turbine. The 18 inch pipe

between the 2A and 2B second stage reheaters and the 2A1 and 2A2 feedwater heaters had

ruptured at the point where a 45 degree 10 inch stub pipe was attached.

The NRC team reviewed the procedures for the quarantine of the failed piping and

determined that they were appropriate. The team also reviewed the proposal for the

laboratory analysis of the Unit 2 failed piping and found that it was appropriate. The team

monitored the on-going laboratory analyses and agreed with the preliminary finding that the

rupture was due to a one time over-pressure event that was large enough to have ruptured a

new piece of pipe. The 12 inch branch similarly failed due to internal overpressure.

The

piping configuration near the rupture included the 18 to 12 inch reducer, the 45 degree dead

leg, and the 12 inch tee, all of which reflected and intensified the impact force. Thus, the

pipe location with the geometric stress concentrators contributing was the point of the pipe

rupture.

The NRC team monitored both the licensee's Event Investigation Team and their Failure

Investigation Process Team's progress. The NRC team's conclusions agree with those of the

Failure Investigation Process Team. The Event Investigation Team's report was not available

for review in this report.

The team monitored the licensee's progress on precursor event reviews and reached

conclusions on: the root cause of the event; and the adequacy of corrective actions for prior

water hammer events.

The team's review of the most significant event precursors found that:

A water nammer event in the Unit 2 second stage reheater drain system occurred in

May of 1996 which caused a support to fail in the area of the current pipe rupture.

The cause of this water hammer, on the same pipe that later ruptured, was due to the

opening of the high level divert valve, 2HD-26, and resultant reverse flow. The design

modification process evaluated the damaged pipe support but did not rigorously

pursue the root cause of the water hammer event.

During the July 1996 startup of Unit 2, the facility system engineers spent

considerable time working with operations to find a better way of realigning flow from

the second stage reheater drain tank from the condenser to the feedwater heaters.

The general procedure for feed-forward of the drains was used, and it was decided to

close two manual valves prior to startup in an attempt to eliminate possible water

hammers.

The criteria for opening the valves included: a) assuring the pressures in

the system would cause the flow to be in the forward direction, to the feedwater

heaters; and b) that the valves were to be opened very slowly, to allow time for the

lines to warmup. This startup of the second stage reheater drain system was

accomplished with no problems noted.

During the September 24, 1996, startup of Unit 2, the same procedure was used;

however, the procedure had not been modified to include the specific guidance about

system pressures and valve opening timing. The operators began to open the valves

earlier in the startup than in July. Also, they opened the valves over a period of

minutes instead of the one and one half hour evolution that was used during the July

startup.

The team concluded that beginning the realignment evolution, when one of the second stage

reheater drain tanks was at a lower pressure than the A feedwater heaters along with the

relatively quick opening of the isolation valves, caused a backflow and subsequent water

hammer. The operators' actions were conducted with an inadequate procedure, which had

not been changed or put "on-hold" per the site's administrative procedures.

The team's root cause analysis found that the root cause was that the Oconee staff and

management, both operations and engineering, had not appreciated the potential of past

water hammer events. This led to each water hammer event's root cause analysis being less

than complete. During the past several years, the site staff proposed several design

modifications to minimize water hammer events in the second stage reheater drain system.

None of these modifications had been installed at the time of the event.

The team found that neither safety equipment availability nor operability was directly affected,

but that access to the area, if needed, to get to the safety-related equipment or support

equipment in the basement was severely hampered, during and immediately after the event.

The team found that numerous water hammer events had previously occurred on the second

stage reheater drain systems of all three Oconee units.

The team assessed the Erosion/Corrosion program as it pertained to this piping system and

found that it was covered and that thickness measurements were periodically taken on

portions of this piping system. As a result of past inspections, some piping components had

been replaced. The team did not find any evidence that this piping failure was the result of

erosion or corrosion.

The team found that the Maintenance Rule applied to this line and that the licensee staff

agreed it applied, and they have been implementing the Maintenance Rule appropriately with

respect to this line and components.

The team found the startup procedures were general and did not benefit from lessons

learned from previous events. The scheduled revision date for the procedure in question was

October 14, 1996; and the administrative procedure, which required that this procedure be

put "on hold," was not done. Corrective action modifications completed prior to the event

were the repair of specific components damaged during past water hammer events. Planned

future corrective actions included investigation of better operating techniques and preparing

modification packages to minimize water hammers.

The team found that there was no detectable radioactive contamination released as a result

of this event.

The team found that the performance related to emergency response was appropriate. The

notification calls were made to the NRC and courtesy calls to the state and county. Their

corporate staff informed the State Occupational Safety and Health Administration.

TABLE OF CONTENTS

0

Paq e

1.0

INTRODUCTION - AUGUMENTED INSPECTION TEAM FORMATION AND

IN IT IA T IO N . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1.1

B ackg ro und . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1.2

Augmented Inspection Team Formation ............................

1

2.0

EVENT DESCRIPTION

............................................

1

2.1

System Description ...........................................

1

2.2

Description of Event .........................................

2

3.0

EQUIPMENT FAILURES/PERFORMANCE ..............................

3

3.1

Determination of the operational history of this piping system

and whether or not it had been subject to water hammer events

in the past ................................................

3

3.1.1

Augmented Inspection Team Findings and Conclusions . . . . 4

3.2

Assessment of past inspections applicable to the piping systems

in question and the applicability and effectiveness of the

Erosion/Corrosion program at the Oconee Nuclear Station ..............

4

3.2.1

Augmented Inspection Team Findings and Conclusions . . . . 8

3.3

Determination of the status of the components of this system

in relation to the new maintenance rule 10 CFR 50.65 ................

8

3.3.1

Scope of Structures and Components Included within the Rule

. . . . 8

3.3.1.1

Augmented Inspection Team Findings and

Conclusions .....................

9

3.3.2 Goals, Monitoring, and Effective Preventative Maintenance ........ 9

3.3.2.1

Augmented Inspection Team Findings and

Conclusions ...............................

9

3.3.3

Engineering Knowledge of the Maintenance Rule .............

10

3.3.3.1

Augmented Inspection Team Findings and

Conclusions ..............................

10

3.4

Review of the corrective actions taken previously to minimize

water hammer or other operational events related to the system ........

10

3.4.1

Augmented Inspection Team Findings and Conclusions ...

10

4.0

HUMAN FACTOR/PROCEDURAL DEFICIENCIES

.......................

11

4.1

Assessment of the startup (i.e., warm-up and heat-up) and

power ascension procedures and techniques with regard to the

secondary systems in question ................................

11

4.1.1

Augmented Inspection Team Findings and Conclusions ......... 12

5.0

RADIOLOGICAL CONSEQUENCES ..................................

13

5.1

Independent verification of the status of radioactive

contamination associated with this pipe and determine if there

was a release of contaminated material ..........................

13

5.1.1

Augmented Inspection Team Findings and Conclusions .........

13

6.0

EMERGENCY RESPONSE ........................................

14

6.1

Assessment of the licensee's performance related to emergency

response, i.e., classifying this event, offsite notifications,

onsite response and interface with offsite emergency agencies ......... .14

6.1.1

Augmented Inspection Team Findings and Conclusions ......... 14

7.0

ASSESSMENT OF THE LICENSEE'S INVESTIGATION OF THESE EVENTS ...

15

7.1

Monitoring and review of the licensee activities related to

event investigation such as quarantine procedures, laboratory

analyses of failed piping materials, root cause analysis and

precursor event reviews .....................................

15

7.1.1

Quarantine Procedures .............

..

15

7.1.2

Laboratory analyses of failed piping materials ................

15

7.1.2.1

Augmented Inspection Team Findings and

Conclusions ..............................

18

7.1.3 Augumented Inspection Team root cause analysis and review

of precursor events ...................................

18

7.2

Assessment of the licensee's overall technical response and

activities to this event .......................................

19

7.2.1

Augmented Inspection Team review of the licensee's

Failure Investigation Process Team Assessment .............. 19

7.2.1.1

Augmented Inspection Team Findings and

Conclusions ..............................

21

7.2.2

Augmented Inspection Team Review of the Licensee's

Event Investigation Team Assessment .....................

21

7.2.2.1

Augmented Inspection Team Findings and

Conclusions ..............................

22

7.3

Team leader shall interface with onsite regulatory entities/

authorities, such as Occupational Safety and Health

Administration .............................................

22

8.0

EXIT MEETING .................................................

22

APPENDIX A - Augmented Inspection Team Charter

APPENDIX B - SEQUENCE OF EVENTS

The sequence of events associated with the Moisture Separator/Reheater pipe rupture

of September 24, 1996, at the Oconee Nuclear Station.

APPENDIX C SPECIFIC ACTIVITY SEQUENCE IMMEDIATELY BEFORE AND AFTER

UNIT 2 HEATER DRAIN LINE RUPTURE

APPENDIX D WATER HAMMER -PROCEDURE AND SYSTEM HISTORY -MOISTURE

SEPARATER REHEATER DRAIN LINES

APPENDIX E - THE LICENSEE REVIEW TEAMS

APPENDIX F - EXIT ATTENDANCE

FIGURE 1 -Unit 2 Heater Drain Piping Elevational Drawing

FIGURE 2 -Unit 2 Piping Layout in Area of Pipe Rupture

FIGURE 3 -Unit 2 Heater Drain Line Rupture Mechanism in Progress

REPORT DETAILS

1.0

INTRODUCTION

1.1

Background

On September 24, 1996, at approximately 4:45 p.m., during the restart of Oconee Unit 2,

non-licensed operators and instrument technicians were manually realigning the Moisture

Separator Reheater Drains at approximately 50 percent power on Unit 2, when an 18 inch

heater drain line ruptured. The contents of the line (hot water and steam at approximately

400 degrees F., 250 psig) severely burned seven plant workers in the Turbine Building.

Control room operators immediately tripped the Unit 2 reactor and turbine.

1.2

Augmented Inspection Team Formation

On the evening of September 24, 1996, a special NRC inspection team arrived on the site to

review the pipe rupture event. On September 26, 1996, senior NRC managers concluded

that events surrounding the pipe rupture warranted further independent evaluation; an

Augmented Inspection Team was formed. A detailed charter was developed to guide the

team (the Augmented Inspection Team Charter is Appendix A).

2.0

EVENT DESCRIPTION

2.1

System Description

The four Moisture Separator/Reheaters for each Oconee unit had two separate stages of

reheat bundles for reheating the High Pressure turbine exhaust steam prior to the exhaust

steam entering the Low Pressure Turbines. The Moisture Separator/Reheaters first stage

reheater was supplied by the bleed or extraction steam from the High Pressure turbine and

was drained through a Moisture Separator/Reheaters drain tank. The Moisture

Separator/Reheaters second stage reheater heating steam was supplied directly from the

main steam system via 8 inch, main steam control Valves (2MS 112 and 2MS 173). Valve

2MS 112 supplied reheating steam to the second stage reheaters of Moisture

Separator/Reheaters 2A1 and 2A2, while 2MS 173 supplied steam to Moisture

Separator/Reheaters 2B1 and 2B2.

After the High Pressure turbine exhaust steam was reheated, the second stage reheater

steam (actually hot water at approximately 460 degrees F., 530 psig.) was returned to the

condensate/feedwater system via two second stage reheater drain tanks. The second stage

reheater drain tanks collected the pressurized hot water and directed it to either the main

condenser (at power less than 60 percent), or to the High Pressure feedwater heaters (at

power greater than 60 percent). The valves to the main condenser were four inch high level

divert Valves (2HD 26 for second stage reheater Drain Tank B and 2HD 25 for second stage

reheater drain tank A). The level range for these level control valves to operate was 31 inch

(Shut) to 45 inch (Full Open).

The second stage reheater drain tanks are approximately 66

inches high. The high level divert was used until approximately 60 percent power to control

tank level. At that time, the system was realigned to the "Feed Forward" mode. The drain

tank's contents were then routed through three inch level control valves, 2HD 95 for drain

tank 2B and 2HD 92 for drain tank 2A. The level control range for these valves to operate

2

was 12 inch (Shut) to 36 inch (Full Open). The outlet of the control valves was directed into

an 18 inch common header. From that point the drain tank contents were sent to the A

(highest pressure) feedwater heaters, 2A1 and 2A2, to provide additional feedwater heating.

The changeover to the feed forward mode was accomplished by opening manual isolation

Valves (2HD 91 and 2HD 94), upstream of the level control valves. The outlet of the isolation

valves then combined at an 18 inch common header, before splitting into two parallel 12 inch

headers to the A feedwater heaters. Since there were no check valves in the lines, the two

second stage reheater drain tanks were cross-connected at the 18 inch common header. A

potential existed for "sluicing" to occur between the two tanks, due to uneven heating from

the two separate Moisture Separator/Reheaters control systems.

2.2

Description of Event

This event involved piping between the 2A and 2B second stage reheaters and the 2A1 and

2A2 feedwater heaters (see Figure 1). The physical configuration had two second stage

reheater drain tanks, each with a 12 inch drain line which went to a 12 inch gate isolation

Valve (2HD 91 for the A tank and 2HD 94 for the B tank), then to a 3 inch level control valve

(2HD 92 and 2HD 95) and finally through a 12 inch butterfly valve (2HD 93 and 2HD 96).

These were parallel lines that eventually joined in a 18 inch common header. Each tank also

had a high level divert line with a 4 inch level control Valve, (2HD 25 and 2 HD 26) that

returned flow to the condenser. This was used to maintain tank level when the unit was at

less than approximately 60 percent power. The 18 inch common line divided into individual

12 inch pipes, with each running to an A Feedwater heater.

The second stage reheater drain lines exit from the drain tanks and generally stay at an

elevation within five feet of the bottom of the tank. The 12 inch line from the 2A second

stage reheater drain tank runs approximately 40 feet horizontally, with a 90 degree elbow,

before an expander to an 18 inch common line where the 2B second stage reheater drain

line joins via a tee. The rupture occurred approximately one foot from where the 2B second

stage reheater drain line joined the 18 inch line at 90 degrees, where a capped, 16 inch long,

10 inch diameter pipe joined at 45 degrees. The 45 degree pipe was an abandoned

connection from a previous modification (see Figure 2). The 18 inch pipe continued at the

same elevation for approximately 41 feet, with a 90 degree horizontal elbow, and then a 90

degree vertical elbow. The pipe rises 26.5 feet vertically, and all of this upstream piping was

sloped to drain back toward the second stage reheater drain tanks. The 18 inch pipe then

turns horizontal via a 90 degree elbow for approximately 56 feet and begins to slope toward

the feedwater heaters. The pipe then vertically drops about seven feet via a 90 degree

elbowwhich is followed by a 90 degree elbow that turns the pipe horizontal for 42 feet, then

upward for two feet, and finally runs 43 feet before dropping vertically about nine feet to the

elevation of the 2A1 and 2A2 feedwater heaters, where it splits into the two 12 inch pipes.

This configuration introduces high points in the 18 inch diameter pipe that were 56 feet long

and 43 feet long and a low point volume, loop seal, that was 42 feet long. This portion of

the piping was sloped to drain toward the feedwater heaters. There were no check valves to

either prevent flow between the second stage reheater drain tanks or back flow from the

feedwater heaters.

3

Steam pressurizing and heating the 56 foot long high point (Figure 3) was the most likely

mechanism to intensify the water hammer, resulting in pipe rupture. The 2HD-91 and 2HD

94 valves were closed while the unit was shutdown, allowing an accumulation of low

temperature water in the entire section of piping that drained toward the second stage

reheater drain tanks. Figure 3 illustrates this situation with the piping being heated and

pressurized with steam from the A feedwater heaters. The steam percolated through the low

point, 42 foot, water filled leg, (refer to Figure 3(a)), and the 56 foot long high point was

pressurized and heated with steam. At this stage in the event sequence, the 2B second

stage reheater drain tank pressure was lower than that in the down stream piping, while the

2A second stage reheater drain tank pressure was approximately equal in pressure to the

down stream piping and the A feedwater heaters.

When the two isolation valves were manually opened, reverse flow in the piping initiated

through the 2HD-94 valve toward the 2B drain tank. The fluid in the vertical pipe and all

piping upstream from there was filled with sub-cooled condensate, which began flow toward

the drain tank. Figure 3(b) illustrates motion of the 56 foot long steam void, -99 cubic feet,

followed by the 42 foot water slug toward the drain tank. The 42 foot water slug only partially

filled the 56 foot long high point pipe such that pockets of steam bubbles formed along the

length. These bubbles then collapsed, due to the liquid acting like a surface condenser.

This flow continued, as depicted in Figure 3(c), until the steam void was in the 26 foot vertical

section and the water slug started to cascade downward in the vertical pipe section. This

caused the steam void to rapidly collapse, to -1 cubic foot, while the water slug accelerated

to fill the void and collided with the water in the upstream piping.

An impact pressure wave was caused by the acceleration impact of the two water slugs

colliding which rapidly propagated through the fluid in the pipe, toward the second stage

reheater drain tanks. This pressure wave was additive to the pipe internal pressure and

effectively increased the pipe hoop stress in the immediately affected area. The piping

configuration near the rupture included the 18 to 12 inch reducer, the 45 degree dead leg,

and the 12 inch tee, all of which reflected and intensified the impact force. Thus, the pipe

location with geometric stress concentrators contributing was the point of the pipe rupture.

3.0

EQUIPMENT FAILURES/PERFORMANCE

3.1

Determination of the operational history of this piping system and whether or not it

had been subject to water hammer events in the past.

Oconee had experienced severe and frequent water hammers in the second stage reheater

drain system since initial operation. Design studies driven by the Corrective Action Program

and the problem reports from those water hammer events revealed several design and

operating flaws. A proposed Nuclear Station Modification 2941, developed in 1991 and 1993

described the Moisture Separator/Reheaters controls as inadequate and recommended

substantial changes to the valves, piping and controls of the two related systems. Another

modification, Nuclear Station Modification 2901, focused on the design of the second stage

reheater drain system and components. Principal recommendations of Nuclear Station

Modification 2901 included installing check valves to prevent backflow from the A feedwater

heaters to the second stage reheater drain tanks and to prevent tank-to-tank sluicing.

4

Control valve design and control changes were also recommended. Both Nuclear Station

Modification scoping documents refer to problems with water hammer and inadequate system

controls that existed since the early days of plant operation. Several Station Problem

Reports and Problem Identification Reports documented water hammers, rapid, uncontrolled

heatups of the systems and support and hanger damage.

3.1.1, Augmented Inspection Team Findings and Conclusions

The Moisture Separator/Reheaters, first stage reheater and second stage reheater drain

systems all had separate steam sources and controls for heating and separate cooling or

condensing points for water cooling/steam condensing on both the Moisture

Separator/Reheaters and feedwater heaters. Each train met at critical points that included

loop seals, drain tanks, drain tank level control valves, and the common 18 inch header

between the drain tanks and the feedwater heaters. Lack of adequate controls and system

temperature excursions in combination with the system layout had contributed to the past

problems.

3.2

Assessment of past inspection applicable to the piping systems in question and the

applicability and effectiveness of the Erosion/Corrosion program at the Oconee

Nuclear Station.

The team inspected the pipe's exterior weld surface and the interior surface through the

fracture opening. Areas of specific interest included the weld's root surface and crack

surfaces.

The team observed no apparent evidence of erosion/corrosion in the pipe sections where the

failure occurred. Also, the balance of the weld that joined the 10 inch angled dead leg

branch to the 18 inch drain line had no evidence of cracking. There was no evidence of

rejectable fabrication defects in this area. A total of three fractures or cracks were observed

during the initial field inspection. One of the three fractures was at the edge of the weld

joining the 12 inch branch that connected valve 2HD-96 to the 18 inch heater drain line, just

upstream from the dead leg branch. This crack was approximately six inches long. The

fracture surface of this crack could not be observed due the tightness of the crack. A second

fracture was observed in the 18 inch drain line. This fracture could be described as a "fish

mouthed" tear which ran parallel with and was connected to the short 10 inch diameter dead

leg branch connection that was attached to the drain line at a 45 degree angle. This pipe

section (18 inch diameter) appeared to have experienced some bulging over a distance of

several feet. The fracture surface had a relatively smooth matte appearance with evidence of

shear lipping and appeared to have the characteristics of a single fast crack type failure.

Evidence of a chevron pattern was discernable on the fracture surface with a direction that

suggested the fracture initiated at the intersection between the 18 inch pipe and the 10 inch

dead leg branch connection. The fracture progressed down the branch connection for a

distance of approximately 18 inches in length. Chevrons were also observed on the fracture

surface of this crack, and these were oriented toward the direction of the weld joint between

the drain line and the branch connection.

6

tank discharge areas, where the inspections were concentrated. Five of the components with

single inspection data were replaced with stainless steel piping, and four of the areas on this

line were scheduled for reinspection during the upcoming EOC-17 refueling outage.

The expanders, elbows, and piping immediately downstream of the control valves on both

trains were replaced with stainless steel during outage EOC-9. Also, at EOC-9, the reducers

and pipe downstream of Valve 1 HD-91 were replaced with stainless steel piping. The elbow

downstream of butterfly Valve 1 HD-93 (B-Train) had been inspected during four previous

outages and was scheduled to be replaced during EOC-17 with stainless steel piping. The

discharge elbow for Valve 1HD-96 (A-train) was replaced with stainless steel during EOC-13.

Unit 3

There were 20 Erosion/Corrosion program inspection locations included in this run of piping.

Multiple data sets were available for 11 of the 20 test areas (one inspection on nine

components, two inspections on two components, three or more inspections on nine

components). The only areas that showed signs of appreciable wear were the valve and

tank discharge areas, where the inspections had been concentrated. Four of the

components with single inspection data were replaced with stainless steel and five of the

areas in this line were scheduled for reinspection during the upcoming EOC-16 refueling

outage.

The first elbow off the B drain tank was replaced with stainless steel piping during EOC-1 1.

The A drain tank discharge elbow had been inspected three times previously and was

scheduled for reinspection at the next outage. The expanders, elbows, and piping

immediately downstream of the control valves on both trains were replaced with stainless

steel piping during EOC-9. The elbows immediately downstream of butterfly valves 3HD-93

and 3HD-96 have been inspected two and three times respectively and were scheduled for.

reinspection during upcoming outages EOC-16 and 17.

These lines were originally installed per USAS B31.1.0-1967. The following table includes

pertinent information for the material in the area of the failure:

Description

Material Size Schedule

Nom. Wall

HoopStressMin

Main Header

A106B 18"

Standard

.375"

.293"

Capped Lateral Branch

A106B 10"

Standard

.365"

.175"

Branch from B Tank

A106B 12"

Standard

.375"

.210"

Visual and Maqnetic Particle Examinations

As a followup to the inspection of the fracture surfaces and pipe condition in the immediate

vicinity of the pipe failure, the licensee performed visual and magnetic particle examinations

of pipe welds and hanger lug attachment welds on either side of the effected components to

determine weld integrity. Results of these inspections were as follows:

5

'

The pipe saddle welded for reinforcement around the 10 inch branch connection, was also

fractured but its fracture surface was not evaluated at this time. The dead leg branch to the

pipe saddle weld had a circumferential fracture, about eight inches long. This crack ran

along the toe of the saddle weld on the dead leg branch side of the joints. The fracture

surface of this crack had a rusty rough woody appearance without discernable fracture

characteristics. Therefore, judging from its appearance, it was difficult to make an

assessment on the evolution of the crack, although this could have been the result of a single

event, e.g., water hammer.

Erosion/Corrosion Test Proqram

Through discussions with cognizant personnel and by document review, the team ascertained

that the subject line was in the Erosion/Corrosion program and in the CHECKWORKS

computer model. As such, several upstream and downstream components were inspected

during previous outages. The area associated with the failure had not been included in the

program as a result of the relatively low velocity and flow rates, the ranking in the computer

model and the lack of flow in the 10 inch dead leg branch pipe. In general, it appeared that

the Erosion/Corrosion inspections had focused on the heater drain tank discharge piping,

isolation and control valve arrangements, expansion loops and heater inlet areas.

Within this area, the team noted that there were 24 Erosion/Corrosion program inspection

locations in this run of piping. Test results showed that the only areas showing signs of

appreciable wear were the valve and tank discharge areas where inspections had been

O

concentrated. The most recent inspection data had been included in the Checkworks model

for Pass 2 Analysis.

Pipe Repairs and Replacement Unit 2

The first fittings off the A and B drain tanks were replaced with stainless steel during outages

EOC-10 and EOC-11 respectively. The expanders, elbows, and piping immediately

downstream of the control valves on both trains were replaced with stainless steel during

outage EOC-7. The elbow downstream of butterfly Valve 2HD-93 (B-train) was replaced

during outage EOC-9 with stainless steel. The discharge elbow for Valve 2HD-96 (A-train)

was inspected during outages EOC-8, 11, 13, and was scheduled for reinspection during the

upcoming outage EOC-16.

In Unit 2, a limited number of preliminary ultrasonic thickness measurements indicated the

material thickness around the affected area was within the manufacturing tolerance.

Additional ultrasonic thickness measurements were planned during the continuing failure

investigation process.

Unit 1

There are 22 Erosion/Corrosion program inspection locations included in this run of piping.

Multiple data sets were available for 14 of the 22 test areas (one inspection on seven

components, two inspections on five components, three or more inspections on nine

components). The only areas which showed signs of appreciable wear were the valve and

7

'9

Unit 3

Weld No.

Size

Description

3-05B-58-2

10"x0.365"

Lateral dead leg to 18" diameter drain line. Rejectable

undercut indication.

3-05B-60-1,2,3

12"xO.375"

Elbow welds from valve 3HD-92 to 18" diameter drain

line. No rejectable indications.

3-05B-64-1

12"xO.375"

Pipe weld between valve 3HD-95 and 18" drain line. No

rejectable indication observed.

Unit 2

2-05B-16-11,12,13

18"xO.375"

18" drain line welds. Linear indications on either side of

weld #12.

2-05B-16-15

10"xO.365"

Lateral dead leg to 18" diameter drain line. No rejectable

indications.

2-05B-16-15A

10"xO.365"

Dead leg cap weld. No rejectable indications.

2-05B-19-1thru5

12"xO.375"

A:2" linear indication on elbow extrados between welds

  1. 1 and

B:Several indications on elbow, between welds #2 and #3

- some removed by light buffing.

2-05B-19-8,9,10

3"xO.216"

Stainless steel pipe installed under erosion/corrosion

program. No rejectable indications observed.

2-05B-18-5thrul0

3"xO.216"

Same as above.

Unit 1

1-05B-4-109CA

10"x0.365"

Welded cap no rejectable indications.

1-05B-4-147C

10"xO.365"

Lateral dead leg to 18" drain line weld. Rejectable

undercut approximately 1/4" long, 3/32" deep.

1-05B-07-63,64,65

10"xO.375"

Linear indication from toe of weld #65 into pipe, axial.

Linear indication from toe of weld #64 into elbow, axial.

Arc gouge in elbow grinding gouge near weld #63.

The team witnessed visual and magnetic particle examinations on all carbon steel welds

listed above; i.e., 10, 12, and 18 inch diameter welds. The team concurred with the above

described findings. The inspections were performed using a code acceptable, magnetic

8

particle procedure. The technique used followed code prescribed practices. Inspectors who

performed these examinations were adequately trained and qualified to perform this assign,ed

task.

Inspection of as Built Piping Configuration

Following the removal of insulation, the team, along with members of the licensee's Quality

Control staff, inspected as built piping for visible anomalies. Piping sections inspected

included those around the 10 inch diameter, capped lateral, the 12 inch diameter T

connections from drain tanks A and B and the 18 inch drain line header.

Within these areas, the combined inspection team noted that not all of the 10 and 12 inch

branch connections to the 18 inch header had a reinforcing ring welded on the header

around the branch connection. The controlling code for these lines, as referenced in Section

3.2.2.2 of the Oconee Final Safety Analysis Report is the Power Piping Code USAS B31.1,

1967 edition, (code). Paragraph 104.3 of the code states in part, that when a pipe is

penetrated by a branch connection, the size of which weakens the pipe, additional

reinforcement must be provided. The amount of reinforcement provided must meet

Paragraph 104.3.1, D and E requirements.

At the close of this inspection, the licensee was making arrangement to inspect all high

energy, balance of plant lines to verify that as built conditions met code requirements. Their

inspection will include associated supports and hangers in these systems.

3.2.1

Augmented Inspection Team Findings and Conclusions

The team concluded that the pipe rupture was the result of a single water hammer

event. The area in the vicinity of the rupture showed no evidence of significant

erosion/corrosion, and the team did not believe that erosion/corrosion was associated

with the pipe rupture.

The licensee's erosion/corrosion program was consistent with industry guidelines and

was implemented in a conservative manner.

As-built heater drain lines did not appear to be consistent with the piping code of

record, B31.1, requirements as many of the locations where branch connections

penetrate main headers lacked reinforcement collars.

3.3

Determine status of the components of this system in relation to the new maintenance

rule 10 CFR 50.65.

3.3.1

Scope of Structures, Systems, and Components Included Within the Rule

During the onsite inspection, the inspectors reviewed certain of the licensee's maintenance

rule records and program documents to determine if the Heater Drain System (which had

experienced the pipe rupture) was in the scope of the Maintenance Rule. The licensee had

determined that the system is in the scope of the Maintenance Rule as required by

9

10 CFR 50.65(b)(iii), nonsafety-related structures, systems, and components whose failure

could cause a reactor scram or an actuation of a safety-related system. The licensee's

decision was based on system analysis and actual system performance.

3.3.1.1

Augmented Inspection Team Findings and Conclusions

The inspectors concluded that the licensee had correctly scoped the Heater Drain System as

being covered by the maintenance rule.

3.3.2

Goals, Monitoring and Effective Preventive Maintenance

The licensee's Maintenance Rule program generally followed the guidance of NUMARC 93

01 (May 1993), "Industry Guideline for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants." NUMARC 93-01 was endorsed through Regulatory Guide 1.160

(June 1993), "Monitoring the Effectiveness of Maintenance at Nuclear Power Plants."

In accordance with NUMARC 93-01, the licensee categorized the Heater Drain System as

normally operating and non-risk (low-safety) significant. Plant level performance criteria of <2

reactor scrams/fuel cycle and <8 percent forced outage rate were established for monitoring

Heater Drain System performance and demonstrating effective preventive maintenance, as

required by 10 CFR 50.65(a)(2).

Part of the licensee's initial implementation phase of the rule included a historical review of

.

each unit's Heater Drain System performance against the performance criteria. This was

done to place structures, systems, and components into the 10 CFR 50.65(a)(1) and (a)(2)

categories. The licensee determined that a Unit 3 system failure that resulted in reactor

scram would require the system to be placed in the (a)(1) category. The Heater Drain

Systems for Units 1 and 2 had met their performance criteria and were placed in the (a)(2)

category.

The licensee's goals, monitoring, and corrective actions under Section (a)(1) of the

Maintenance Rule included the addition of two moisture/separator reheater level detectors

and appropriate new controls. Even though the Heater Drain Systems for Units 1 and 2 had

not experienced a failure that resulted in a reactor scram, the licensee decided to make the

same system changes as for Unit 3. This change was made to Unit 1, with Units 2 and 3

scheduled to receive the change during future refueling outages.

3.3.2.1

Augmented Inspection Team Findings and Conclusions

Based on a review of system and plant performance data and discussions with the licensee

site Maintenance Rule Coordinator, the inspectors determined that the licensee's

maintenance rule categorizations, performance criteria, monitoring and corrective actions for

the Heater Drain System for all three units satisfied the requirements of 10 CFR 50.65 (a)(1)

and (a)(2).

10

3.3.3 Engineering Knowledge of the Maintenance Rule

The inspectors interviewed the licensee's site Maintenance Rule Coordinator to assess

understanding of the maintenance rule and associated responsibilities.

3.3.3.1

Augmented Inspection Team Findings and Conclusions

The licensee's site Maintenance Rule Coordinator was very knowledgeable of the

requirements of the maintenance rule, industry guidelines, and plant systems. The

information established by the coordinator that was provided to the inspectors reflected a

clear understanding of site specific systems' performance as they related to the rule. The

inspectors also noted that the site coordinator understood the responsibilities of the position

in overseeing that the requirements were correctly, consistently and timely implemented.

3.4

Review corrective actions taken previously to minimize water hammer or other

operational events related to the system.

The corrective actions in the past have been primarily limited to upgrading the hangers and

supports that have been damaged during the water hammer events. In most cases, the

hanger designers had been unable to predict accurately the loading of the water hammers.

The descriptions of the system limitations and the proposed corrective actions described

below were contained in the two Nuclear Station Modifications referenced in Paragraph 2.1

above.

Second stage reheater tube bundle, and Moisture Separator/Reheater tube bundle

heatup rates were exceeded when Valves MS-112 and 173 were allowed to control

tube bundle heatup in AUTO. (The 30 degree F /30 minute heatup limit was

exceeded, it actually was approximately 260 degrees F in 30 minutes). SOLUTION:

(a) Replace MS-1 12 and MS-1 73 valve internals with Class IV valves, having better

control characteristics, and (b) Replace MS-1 12 and MS-1 73 control system with

digital valve controllers.

Frequent and severe water hammers in the second stage reheater drain systems

occur due to uncontrolled heating of the system as a result of Moisture

Separator/Reheaters controls, backflow between drain tanks and from the feedwater

heaters, interactions between the drain tank level controllers. SOLUTION: (a) add

check valves between the tanks and between the tanks and feedwater heaters, and

(b) replace level control circuit and level control valves to reduce valve failures and

leakage.

3.4.1

Augmented Inspection Team Findings and Conclusions

None of the proposed solutions had been incorporated, although the general

recommendations had been approved for implementation prior to the steam break event.

The schedule for implementing the Nuclear Station Modifications was set for beginning with

the Unit 2 outage beginning October 1997, and continuing with the other units in outage

11

sequence. However, a modification meeting September 23, two days before the steam break

event, reset the implementation schedule to start with the Unit 3 outage beginning March

1998. The licensee has decided to implement the modifications during the current outages.

4.0

HUMAN FACTOR/PROCEDURAL DEFICIENCIES

4.1

Assess the startup (i.e., warm-up and heat-up) and power ascension procedures and

techniques with regard to the secondary systems in question.

Water hammer was noted as being a long standing problem on this system in that problems

were referenced in Nuclear Station Modification-1,2,3 2901 scoping document, which

identified operational procedure changes that were made in 1981 to OP/1,2,3/A/1106/14,

Moisture Separator Reheater, to lessen the severity of water hammers experienced when

valving in and out the Moisture Separator/Reheaters and Drain Tanks. The procedure

changes were reported to have greatly alleviated the pipe wear due to corrosion, but water

hammers continued which were severe enough to cause valve seat damage and breakage

of tank and pipe supports. These problems were documented in, but not limited to Problem

Identification Reports 1-094-1001, 1-095-0115, 1-95-0513, 2-96-0984, 3-96-1860, and earlier

Station Problem Reports.

In order for the operation of the system to have better control, design changes and system

modifications were planned. The team evaluated the Design Scoping Documents for Nuclear

Station Modification, Nuclear Station Modification-1,2,3 2901, and Nuclear Station

Modification-1,2,3 2941 which were initiated in 1991 and 1993 respectively. These proposed

modifications were for valve replacements associated with the Moisture Separator Reheaters,

first and second stage heater drains and for piping configuration changes to eliminate water

or steam perturbations that have been experienced in that system during previous years.

Nuclear Station Modification scoping document, Nuclear Station Modification-1,2,3 2941,

further documented problems associated with automatic control of the startup and operating

relationship with the reheat steam system. This inadequate control had resulted in heatup

rate limits that were exceeded and also suggested that these problems had been

experienced since the beginning of plant operation. This scoping document recommended

that the pipe layout and supports be evaluated and that valves be added to better control the

startup of the system.

An earlier design modification in the time frame of June 1980, Scoping Document Nuclear

Station Modification 844, Revision 0, Moisture Separator/Reheater First Stage Piping

Revision, involved the removal of two 10" lines to separate the first and second stage

Moisture Separator/Reheaters drains and to reroute the first stage drains to the "B" feedwater

heaters and the second stage to the "A" feedwater heater. This was done to increase

Moisture Separator/Reheaters scavaging steam flow from 0.5 percent to 10 percent in order

to improve plant efficiency and Moisture Separator/Reheaters stability operation by reducing

condensate flooding of reheater tubes. In lieu of cutting the 18 inch line for the branch

removal, the method of removal was to cut and cap the 10" lines and leaving a short length

of piping connected at a 45 degree angle to the bottom of the 18 inch header. The 18 inch

header at the 10 inch intersection was the area that ruptured during the steam break event.

12

This configuration provided a trap for water collection during plant startup and shutdowns.

An acceptable design could have been to cut the 18 inch line on both sides of the stub/s and

replace the existing section with an 18 inch straight piece of piping, eliminating the high

stress areas and collection point for water.

During recent and previous water hammer events, extensive pipe hanger damage had been

noted. The team reviewed Problem Identification Report 1-095-0513 which documented that

the second stage reheater Drain Tank and associated piping and supports were not designed

for steam/water hammer transients such as those experienced during plant startups.

A review of the licensee's Evaluation of Pipe Support 2-05B-2-0-1410N-H98 revealed it was

reworked in May 1996 after one of the two support legs pulled out of the concrete during an

apparent water hammer event. The arrangement supported the 18 inch pipe that ruptured

during the most recent water hammer event. The modification included moving the West leg

that was attached to the floor by a baseplate with anchors installed in the concrete to the

East side of the main support. During the event in May 1996, the anchors pulled out of the

concrete on the support leg on the East side of the main support member. It was noted that

concrete in the area where the anchors pulled out did not contain rebar. The licensee

advised that the floor of the Turbine Building contained rebar, but after the original floor was

completed an additional 12 inches of concrete without rebar was placed on top to cover drain

lines and other piping routed on the floor. It is in this top 12 inches of concrete cover that the

anchor bolts were installed.

O

Although the design engineering effort for Design Scoping Documents, Nuclear Station

Modification-1, 2, 3 2901, and Nuclear Station Modification-1,2,3 2941, was in progress at

the time of this inspection, it had not progressed sufficiently for the team to evaluate it's final

adequacy. The team's review included field inspections of the existing piping configuration,

review of relevant Problem Identification Reports, drawings, and various discussions with

engineering personnel. The team discussed several of the as-found installation

configurations with the licensee such as loads on embed plates attached to the ceiling,

anchor bolt installation in concrete in conjunction with baseplate to embed plate welding,

vacant holes adjacent to installed anchor bolts and the practice of supporting one support

from another support using an L beam. The team concluded, based on these discussions,

that the licensee was performing field inspections of these various type installations and the

engineers were performing evaluations to determine the installations' adequacy.

4.1.1

Augmented Inspection Team Findings and Conclusions

Onsite documentation showed that water hammers occurred since initial plant startup. The

licensee's design review did not identify that water hammers were a problem in the 18 inch

lines when the 10 inch lines were removed and capped. This earlier engineering design

modification did not eliminate these high stress areas and collection points for condensed

water. The team concluded that leaving the stub pieces protruding from the bottom of the 18

inch header did not cause the water hammer event. However, due to the stress risers

created by the piping geometry in the area and to the trapped water, it did cause the water

hammer to concentrate more in this area. Combining this with inherently high stresses that

occur at pipe junctures increased the potential for pipe rupture due to water hammer events.

13

S

When water hammer occurred in the 18 inch piping with the stub piece that projects from the

bottom of the 18 inch pipe full of water, excessive reaction forces occurred. The water in the

stub piece reacted like a piston with downward and outward forces occurring. Stresses at the

stub piece juncture were significantly higher than stresses in a straight piece of pipe. The

piping configuration in the area, including the 12 inch branch connection and the 12 inch to

18 inch expander, were also stress concentrator contributors.

5.0

RADIOLOGICAL CONSEQUENCES

5.1

Independently verify the status of radioactive contamination associated with this pipe

and determine if there was a release of contaminated material.

Following the event, the inspectors interviewed Radiation Protection personnel involved with

event recovery and discussed boundary controls, surveys performed, instruments used, and

survey documentation.

Records reviewed for the Unit 2 Turbine Building sump monitor and unit ventilation monitors

determined the event did not result in any discharge of radioactivity to the environment above

background levels. Also, surveys- reviewed independently verified no radioactive

contamination above background was detected in the Turbine Building, change area,

O

canteen, in asbestos insulation debris, on injured personnel, ambulances, and other

miscellaneous equipment associated with the event. Some discrepancies in survey

documentation were noted by the team. These discrepancies did not alter survey results.

However, this issue was discussed with Radiation Protection supervision, and survey

corrections were subsequently performed.

During tours of the facility, the team observed radiological monitoring equipment in use to

include: portal monitors, contamination instruments, radiation instruments, The Turbine

Building sump monitors and unit ventilation monitors. Calibration records reviewed verified

equipment in use at the time of the event was currently calibrated.

5.1.1

Augmented Inspection Team Findings and Conclusions

The team found that radioactive contamination associated with this event was not detectable

and that no release of radioactive material occurred.

--. o

14

6.0

EMERGENCY RESPONSE

6.1

Assessment of the licensee's performance related to emergency response, i.e.,

classifying this event, offsite notifications, on-site response and interface with offsite

emergency agencies.

The team reviewed the declaration and termination actions taken by the licensee for the

licensee's Notice of an Unusual Event associated with this event to verify the licensee

complied with their Emergency Coordinator procedures.

The inspectors verified the event was classified in accordance with licensee Procedure

RP/O/B/1000/01, Emergency Classification, Change 3, dated July 16, 1996. The licensee

classified this event as an Unusual Event based on emergency action levels identified in the

procedure.

The Event Notification form was reviewed and verified that the event was declared and

terminated at 2040 hours0.0236 days <br />0.567 hours <br />0.00337 weeks <br />7.7622e-4 months <br /> on September 24, 1996, from the Technical Support Center.

During the event debrief, the licensee identified that the Emergency Coordinator procedure

did not contain adequate guidance for event declarations and termination. Specifically, an

event checklist used in the Control Room and Emergency Operating Facility for terminating

an event was not available in the Technical Support Center Emergency Coordinator

procedure. The licensee initiated a Problem Identification Report to evaluate the problem

and completed a draft procedural revision for the Emergency Coordinator Technical Support

Center procedure prior to the end of the onsite inspection.

A review of the Event Notification form, control room logs, and interviews with personnel

determined that the offsite notifications to the required agencies were accomplished in a

timely manner and met licensee requirements for conducting the notifications. Throughout

the event, the NRC, State of South Carolina, Oconee County, and Pickens County

emergency agencies were continuously updated on plant status and conditions resulting from

the event. The inspectors noted during event debriefs that site assembly to account for

personnel in the Turbine Building was also conducted in a timely manner. In addition, a

debrief for personnel involved in the medical evacuation of injured personnel to hospitals was

conducted. The Medical Emergency Response Team personnel commented during the

debrief that coordination and communications between site personnel and medical

responders was good.

The licensee notified the State of South Carolina office of Occupational Safety and Health

Administration of this event which resulted in seven personnel injuries and Occupational

Safety and Health Administration responded to the site with an inspection team.

6.1.1

Augmented Inspection Team Findings and Conclusions

The team found that the performance related to emergency response was appropriate. They

made the notification call to the NRC and courtesy calls to the state and county. Their

corporate staff informed the State Occupational Safety and Health Administration.

15

7.0

ASSESSMENT OF THE LICENSEE'S INVESTIGATION OF THESE EVENTS

7.1

Monitor and review licensee activities related to event investigation such as quarantine

procedures, laboratory analyses of failed piping materials, root cause analysis and

precursor event reviews.

7.1.1

Quarantine Procedures

The team reviewed the procedures for the quarantine of the failed piping and determined that

these were appropriate. The team reviewed the proposal for the laboratory analyses of the

Unit 2 failed piping and found that it was appropriate.

7.1.2

Laboratory analyses of failed piping materials

On October 2 and 3, 1996, an inspection was conducted at the Duke Power Company

corporate metallurgy lab located at the McGuire plant site. A metallurgist from the Materials

and Chemical Engineering Branch of the Office of Nuclear Reactor Regulation, conducted the

inspection. The purpose of the visit was to monitor and evaluate the licensee's metallurgical

investigation of a catastrophic rupture of an 18 inch diameter heater drain line from Oconee

Unit 2. A licensee metallurgist performed the metallurgical investigations and was

interviewed during this inspection.

The licensee's proposed investigation plan was reviewed prior to the inspector's arrival at the

.

metallurgical lab. The plan of the investigation was detailed in a two page outline of the

documentation, metallurgical examinations and mechanical tests that would be performed to

determine the root cause of the pipe failure. Listed steps of the outline included:

documenting the "as received" condition of the pipe, a plan showing locations for removing

sections from various portions of the pipe, metallurgical evaluations, and chemistry and

mechanical tests to determine the material properties. The plan was found to be

comprehensive and complete. No significant revisions were necessary. The investigation

plan was fully adequate to support the root cause determination.

At the time of the inspection, sample removal and preparation were under way. Most of the

"as received" documentation was complete. Since the inspection was conducted prior to the

end of the metallurgical examinations and mechanical property tests, the results noted herein

are preliminary.

The sample consisted of a section of 18 inch nominal pipe size, standard schedule (0.375

inch wall), carbon steel pipe with two branch connections. One branch connection was 10

inch nominal pipe size and the other 12 inch nominal pipe size. The 10 inch branch was a

45 degree lateral with an external reinforcing saddle, constructed in accordance with usual

practice for moderate energy lines. This branch was capped off roughly 1 foot down the line.

The 12 inch branch was a 90 degree "tee" and lacked the normally expected external

reinforcing saddle or ring. The absence of the external reinforcing saddle was determined to

be a construction deficiency.

16

Typically, construction material used for this class of service was seamless carbon steel pipe,

ASTM A-106 grade B. Laboratory analysis results reviewed by the team verified that a

typical carbon steel, such as A-106 grade B, was the material of construction.

The primary failure was at the 10 inch branch connection. It had the attributes of a classic

hoop stress driven rupture. (Hoop stress is the principal pipe stress that arises from internal

pressure. When the hoop stress exceeds the structural capabilities of a pipe, a longitudinal

rupture occurs.) The rupture consisted of a throuigh-wall longitudinal split originating at the

inside corner of the 45 degree 10 inch lateral. A fracture would be expected to originate in

the 45 degree corner at the branch connection (because of the stress concentration that

arises from the geometry) and then propagate as observed. The rupture ran roughly 1 foot

along each line. It ran through both the reinforcing saddle, connecting welds and underlying

pipe of the 18 inch line. It continued some distance past the edge of the reinforcing saddle

before arresting in the pipe base material. In the 10 inch pipe, the fracture ran from the

same origin, along the entire length of the branch, and arrested in the pipe cap. A secondary

fracture ran about 900 around the edge of the reinforcing saddle of the 18 inch line. As a

result of the size of the rupture opening displacement, considerable bending distortion existed

in the 18 inch line all around the 10 inch lateral. There was a sufficient fracture opening

displacement to allow visual observation of the fracture faces over nearly its entire length.

The 12 inch tee showed much less damage. Two cracks were evident. They were located at

the tee to main branch weld, in the 18 inch line, and ran four to six inches circumferentially

around the connecting weld for the 12 inch line. The crack opening displacement was

O

negligible. These cracks were situated such that both were primarily longitudinal to the 18

inch line but on opposite sides of the 12 inch connection from each other. Because of the

lesser degree of damage, it was concluded that the internal pressure that caused these

cracks was substantially less at the location of the 12 inch branch compared to the 10 inch

branch. Additionally, the location of the cracks at the 12 inch branch suggested other

differences in the failure mechanism.

All the fracture faces exhibited classic ductile tensile overload features: 45 degree shear lips

were readily apparent on all the fracture surfaces through the base and weld materials. This

type of failure mode is normal for a ductile material such as carbon steel. After these initial

observations, the investigation concentrated upon examining the details of the fractures,

looking for pre-existing damage, if any, or other contributing conditions.

A number of sections were removed from the welds and base material along the fracture

path. Micro hardness traverses of these different weld, heat affected zone and base material

sections were performed. The hardness of the base material was normal for carbon steel

pipe. The welds showed normal hardness values for welds in the as-welded condition.

Carbon steel of this thickness (nominal wall 0.375 inch) did not require heat treatment after

welding. These welds exhibited this normal construction code practice. Additional testing

was planned to characterize more fully the mechanical properties of the base and weld

materials. However, this work had not been started at the time of the inspection (it was to be

performed by a commercial laboratory with additional testing facilities). It is expected that,

based upon the general observations of the fractures and the hardness test results, that no

material deficiencies will be found.

17

Microstructural examination of the various sections removed for fracture surface

characterization and micro hardness tests revealed a normal grain structure. Several fracture

faces were examined with a scanning electron microscope to verify the failure mode. Classic

ductile failure artifacts were noted. This again demonstrated the failure was the result of a

tensile overload of the material rather than a material deficiency or progressive failure mode

such as fatigue.

During examination of the primary fracture origin, it was noted that several small (1/4 inch

deep), heavily oxidized cracks were on the edge of the cut opening in the 18 inch pipe at the

10 inch connection. Several such cracks were adjacent to either side of the main fracture.

One such crack served as the initiation site for the main fracture. Several of these cracks

were opened for surface fractography. All showed heavy oxidation with consequent

broadening of the crack opening and blunting of the crack tip. From this crack morphology it

was obvious that these small cracks were quite old. Additionally, since there was no sharp

crack front and no indication of recent propagation, these cracks were inactive. The one that

served as the origin for the main fracture was similarly well oxidized. Due to its small size

and lack of ongoing propagation evidence, it was judged that it had not been a significant

contributing cause to the main fracture. Instead, it simply served as a local stress

concentrator at the point in the pipe where the highest tensile overload stress had occurred.

A larger, similarly well oxidized crack also existed roughly 1/2 inch away (also in the edge of

the 10 inch hole) but it did not propagate or play any role in the formation of the main

fracture. Consequently, it was concluded that these small flaws were insignificant to the

structural integrity, were not precursors to a progressive failure, and were not a cause of the

O

failure.

At the time of the inspection, the bulk of the investigative effort was concentrated upon the

large rupture at the 10 inch branch, since it was the location of the greatest damage. Late in

the inspection it was noted that the 2 cracks at the 12 inch branch may have had precursors.

Some part-through-wall cracks, showing oxidized surfaces, were noted at portions of the

fracture surfaces. The oxides did not appear, upon preliminary examination, to be as heavy

as in the case of the small heavily oxidized cracks associated with the 10 inch branch

connection. This suggests these small cracks were more recent and possibly active. Since

this branch lacked a code required reinforcement, the existence of possibly active precursor

cracks is plausible. It was noted that the fresh fracture surfaces resulting from the failure

event exhibited ductile features, supporting the previous conclusion that the material

properties were nominal. At the end of the inspection, the licensee's metallurgical evaluation

of this component was ongoing.

An in-depth review was conducted to determine the possible role of erosion/corrosion wall

thinning as a contributing factor or causative factor in the failure. Some minor wall thinning

was noted in a limited area of the 18 inch line. However, the slightly thinned area was

remote from the fractures and was of no consequence to the failure.

S

18

7.1.2.1

Augmented Inspection Team Findings and Conclusions

The team concluded that the licensee's investigation plan was comprehensive. The

licensee's metallurgist demonstrated excellent knowledge and capabilities. The ongoing

examinations were thorough, and the preliminary conclusions were congruent with the

available evidence. The preliminary results indicated the 10 inch branch failure resulted from

a one time internal pressure overload that exceeded the design and ultimate strength

capabilities of the pipe. No material property deficiencies, significant prior degradation,

progressive failure mechanisms, or construction deficiencies contributed to the failure that

occurred at the 10 inch branch.

The 12 inch branch similarly failed due to internal overpressure. However, preliminary

observations suggest there may have been a construction deficiency (lack of branch

reinforcement) at the 12 inch branch. Some small oxidized cracks were noted along parts of

the 12 inch branch fracture faces. These precursor cracks may have been active and may

have contributed to the through-wall cracking of the 12 inch branch connection.

7.1.3 Augmented Inspection Team root cause analysis and review of precursor events.

The team's review of the most significant event precursors found that a water hammer event

in the Unit 2 second stage reheater drain system occurred in May of 1996 that caused a

support to fail in the area of the current pipe rupture. The design modification process

evaluated the damaged pipe support. However, the cause of this water hammer, on the

same pipe that later ruptured, was due to the opening of the high level divert valve, 2HD-26,

and resultant reverse flow. The cause of these contributors was not rigorously pursued.

During the July 1996 startup of Unit 2, the facility system engineers spent considerable time

working with operations to find a better way of realigning flow from the second stage reheater

drain tank from the condenser to the feedwater heaters. The general procedure for feed

forward of the drains was used, and it was decided to close two manual valves prior to

startup in an attempt to eliminate possible water hammers.

The criteria for opening the

valves included: (a) assuring the pressures in the system would cause the flow to be in the

forward direction, to the feedwater heaters; and (b) that the valves were opened very slowly,

to allow time for the lines to warmup. This startup of the second stage reheater drain system

was accomplished with no problems noted.

During the September 24, 1996, startup of Unit 2, the same procedure was used; however,

the procedure had not been modified to include the guidance about system pressures and

valve opening timing. The operators began to open the valves earlier in the startup than in

July. Also, they opened the valves over a period of minutes instead of the one and one half

hour evolution that was used during the July startup.

The team concluded that beginning the realignment evolution when one of the second stage

reheater drain tanks was at a lower pressure than the A feedwater heaters, along with the

relatively quick opening of the isolation valves, caused a backflow and subsequent water

hammer. The operators' actions were conducted with an inadequate procedure, which had

not been changed or put "on-hold" per the site's administrative procedures until the revisions

reflecting the July experience were made.

19

The team's root cause analysis found that the root cause was that the Oconee staff and

management, both operations and engineering, had not appreciated the potential of past

water hammer events. This led to each water hammer event's root cause analysis being less

than complete. During recent years, the site staff began several design modifications to

minimize water hammer events in the second stage reheater drain system.

None of these

modifications had been installed at the time of the event.

7.2

Assess the licensee's overall technical response and activities to this event.

The team developed their independent evaluation of the events and root causes and

reviewed their results against the licensee's teams findings. The Augmented Inspection

Team concluded that the licensee completed a thorough job of review and that their root

cause determinations were reasonable. The licensee's level of management involvement in

their investigations and in their internal critiques of their investigations was in-depth and

involved the highest levels of their respective organizations. The Augmented Inspection

Team findings basically agree with that of the licensee as noted below and in specific places

in the report.

7.2.1

Augmented Inspection Team Review of the licensee's Failure Investigation Process

Team Assessment

The Failure Investigation Process Team determined that the failure mechanism was believed

to be the cumulative effect of water slug induced water hammer and steam void collapse

O

induced (pressure pulse) water hammer. The initiation point of the rupture was at a pre

existing, minor defect noted at the junction of the branched "Y" connection.

The Failure Investigation Process Team found it important to differentiate this event from

water hammers which have occurred in the Heater Drain System in the past. The differences

included:

-

The approach to operating the Heater Drain System.

-

The condition of system components, particularly the second stage reheater drain tank

dump valves.

-

The Heater Drain System ambient conditions, including pressures and temperatures,

prior to alignment for feed forward operation.

-

The Feedwater heater steam admission rates.

Contributing Factors:

1)

System Design Inadequacies:

-

Mechanical - The historical review revealed that the Heater Drain Systems on

all units have a noteworthy history of maintenance and operational concerns.

Review of site documentation revealed that these concerns resulted in several

design studies and proposed modifications.

20

-

Control - The control of the second stage reheater steam admission valves,

S

2MS- 112 and 173 as well as the second stage reheater drain tank dump

valves, 2HD-25 and 26, appeared to have made system control difficult.

These valves are critical to controlling system pressures and temperatures

such that back flow was prevented.

2)

Communications Concerns:

Interviews with personnel involved revealed that system concerns were well

acknowledged; however, personnel were focusing on unit power as the criteria to use

in establishing drain tank forward flow. The appropriate plant data to consider to

lessen the potential for backflow was the differential pressures between the second

stage reheater drain tanks and the A Feedwater Heaters.

Recommended Corrective Actions:

-

Provide a method to drain stagnant fluid from the high point pocket (loop seal)

in the 18 inch drain line and a method to drain the stagnant water from the

piping between the new check valves and the vertical riser, upstream of the

high points.

-

Decrease the Heater Drain System piping stresses by: eliminating unnecessary

discontinuities; and minimizing multiple discontinuities in close proximity to one

another.

-

Modify the Heater Drain System operation to avoid sudden changes in the fluid

flow direction and/or thermodynamic state.

-

Improve the Heater Drain System piping strength by incorporating forged

fittings.

-

Improve the plant control systems relating to Feedwater steam admission and

Heater Drain tank level control.

-

Improve the Heater Drain System instrumentation by providing actual pressure

indication in the first and second stage heater drain tanks; providing

temperature indication in the Heater Drain System riser and high point; and

providing a dynamic pressure transmitter at the base of the Heater Drain

System riser.

3)

Insufficient Procedural Guidance:

The Operations Procedure used provided insufficient guidance for initiating second

stage reheater drain flow without introducing the potential for Heater Drain System

backflow.

21

SUMMARY

The Failure Investigation Process Team concluded that the root cause of the event was the

cumulative effect of water slug water hammer and steam void collapse (pressure pulse) water

hammer. Significant contributing factors were poor design, poor procedural guidance and

ineffective communication.

7.2.1.1

Augmented Inspection Team Findings and Conclusions

The Augmented Inspection Team independently evaluated the failure mechanism, root cause

of the event, the contributing factors and potential corrective actions and, as delineated in the

first paragraphs of this report, agreed with the Failure Investigation Process Team findings

with the following exception:

-

An additional Contributing Factor was the speed of valve opening. During the July

1996 startup, the Heater Drain manual valves were cracked open and then left for the

piping to warm. The team believes that this technique vwuld minimize the magnitude

of any potential water hammer.

7.2.2

Augmented Inspection Team Review of the licensee's Event Investigation Team

Assessment

The licensee's Event Investigation Team Charter included:

O Identification of any strengths or good practices worthy of sharing with other sites.

Development and validation of a sequence of events associated with this event.

Evaluation of the significance of the event with regard to radiological consequences,

safety system performance and proximity to safety limits as defined in the technical

specifications.

Identification of procedures in use during and leading up to the event and used to

recover from the event.

Evaluation of the adequacy of administrative controls and implementation of those

controls.

Identification of any human factors, training or procedural deficiencies.

Evaluation of any necessary event classification and other pertinent emergency

planning issues.

Evaluate as necessary, the impact of plant material condition, maintenance,

modification/implementation group and engineering on the event.

22

For any pertinent equipment malfunctions, the following determinations will be made:

Root Cause

Any known deficiencies prior to the event

Equipment history

Pre-event status of surveillances, testing, preventative maintenance,

modifications

Any previous corrective actions associated with the equipment

Similar Duke and industry events shall be identified and the application of corrective

actions from those events shall be evaluated.

The root cause and any contributing factors for the event.

An evaluation of applicable management actions prior to, during and following the

event

An evaluation of the response to the medical attention of injured personnel.

7.2.2.1

Augmented Inspection Team Findings and Conclusions

The team followed the licensee's Event Investigation Team Assessment while in progress at

the site. The team listened to their on-site debrief on October 3, 1996. The licensee's team

covered the response to the injured by the Medical Emergency Response Team, the

operation of the heater drain system by the facility and a summary of their sequence of

events. The NRC team's conclusions agreed with the licensee's team's comments and

conclusions.

The licensee's Event Investigation Team Assessment report was released to be reviewed and

evaluated when this inspection was concluded.

7.3

Team leader shall interface with onsite regulatory entities/authorities, such as

Occupational Safety and Health Administration.

The team leader attended discussions concerning the event between the State of South

Carolina Occupational Safety and Health Administration and the facility.

8.0

EXIT MEETING

A public exit meeting was held on October 8, 1996, at 11:00 a.m. on the Oconee site.

Several members of the public attended.

No dissenting comments were received from the

licensee.

Unit 2 Heater Drain Piping

Elevational Drawing

2A

SSRH

Drain

Tank

@ ---

784'-3"

52785'-9

To Condenser

787'-3"

--

784'-3-

2HD-25

784*-3"

2B

SSRH

2HD-91

2HD-92 2HD-93

Drain

Tank

785-9"

7859

To Condenser

TE

-

784*-3"

2HD-26

787'-3"

-56

@ 813'-9"

784'-3"

782'-3"7

2HD-94

2HD-95

-43 @ 808'

~42' @ 806-6

2HD-105

2A1

FDWV

799'-6'

HTR

z

E

2HD-106

2A2

FOW

/787'-3"

HTR

FIGURE 1

Ie ,.12!.

MCK

gEoucck

lo"~ S-1-b 13.W

CA-P

N rT

C

FIGURE 2

UN~IT 2 PIPING IN AREA OF PIPE RUPTURE

UNIT 2 HEATER DRAIN LINE RUPTURE

r

MECHANISM IN PROGRESS

Ag'060

4026

S INITI AL

e

1

CONDI TIONSc

s

00INCRASEDCONDNSIN

94

~~ONDRENSE

OwNDNS

8 STEAM

AF TEi

/VOID7

DR

IN

0c

BEO INS

Hof

ep

1795

,

P067

SLUG ACCELERATING RAPIDLY

CONDENSATE

BEING SWEPT

INTO RISER

RAPID CONDENSATION OCCURRING

STEAM CAVITY COLLAPSE

IN PROGRESS

NOTE= PIPE LENGTHE' ARE APPROY1t-1-TE

9A

FIGURE. 3

UNITED STATES

00

NUCLEAR REGULATORY COMMISSION

REGION II

o!P

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

September 26, 1996

MEMORANDUM TO:

Thomas A. Peebles

Team Leader

Augmented Inspection Team

FROM:

Stewart D. Ebneter

-2

Regional Administrator

SUBJECT:

AUGMENTED INSPECTION TEAM CHARTER

An Augmented Inspection Team (AIT) has been established to inspect and assess

the moisture Separator/Reheater pipe rupture of September 24, 1996 at the

Oconee Nuclear Station. The team composition is as follows:

Team Leader:

T. Peebles

P. Harmon (Operator)

D. Forbes (Emergency Preparedness and

Radiological aspects)

N. Economos (Materials Application)

E. Brown (Water Hammer Events)

Others (To be determined on an as needed basis.)

The objectives of the inspectioh are to (1) determine the facts surrounding

the specific event, (2) assess licensee response to the event, (3)

assess

generic aspects of operations/inspections that may have broad applicability to

other facilities, (4) oversee licensee activity during their event review and,

(5) interface with other on-site entities such as Occupational Safety and

Health Administration (OSHA).

For the period during which you are leading this inspection and documenting

the results, you shall report directly to me. The guidance of Inspection

Manual Chapters 0325 and 0610 apply to your inspection and the report.

If you

have any questions regarding the objectives or the attached charter, contact

me.

Attachment: AIT Charter

cc w/att:

J. Milhoan. EDO

F. Miraglia, NRR

E. Jordan, AEOD

A. Thadani, NRR

S. Varga. NRR

H.

Berkow, NRR

APPENDIX A

AUGMENTED INSPECTION TEAM CHARTER

OCONEE NUCLEAR STATION

STEAM LINE RUPTURE EVENT

The objectives of the inspection are to (1) determine the facts surrounding

the specific event (2)

assess licensee response to the event (3)

assess

generic aspects of operations/inspections that may have broad applicability to

other facilities (4) oversee licensee activity during their event review and

(5) interface with other on-site entities such as Occupational Safety and

Health Administration (OSHA).

Monitor and review licensee activities related to event investigation

such as quarantine procedures, laboratory analyses of failed piping

materials, root cause analysis and precursor event reviews.

Develop a sequence of events associated with the Moisture

Separator/Reheater pipe rupture of September 24, 1996, at the Oconee

Nuclear Station.

Determine whether the pipe rupture event adversely affected safety

equipment availability or operability.

Determine the operational history of this piping system and whether or

not it had been subject to water hammer events in the past.

Assess past inspection applicable to the piping systems in question and

the applicability and effectiveness of the Erosion/Corrosion program at

the Oconee Nuclear Station. Determine status of the components of this

system in relation to the new maintenance rule 10 CFR 50.65.

Assess the startup (i.e., warm-up and heat-up) and power ascension

procedures and techniques with regard to the secondary systems in

question. Review corrective actions taken previously to minimize water

hammer or other operational events related to the system.

-Independently verify the status of radioactive contamination associated

with this pipe and determine of there was a release of contaminated

material.

Assess the licensee's performance related to emergency response, i.e.,

classifying this event. offsite notifications. on-site response and

interface with offsite emergency agencies.

Assess the licensee's overall technical response and activities to this

event.

Team leader shall interface with on-site regulatory entities/

authorities, such as Occupational Safety and Health Administration.

Offsite activities with regard to these entities shall be referred to

Region II.

Document the inspection findings and conclusion in an inspection report

within 30 days of the inspection completion.

ATTACHMENT

OVERALL

SEQUENCE OF EVENTS SEPTEMBER 24, 1996

UNIT 2 HEATER DRAIN LINE RUPTURE

September 23, 1996

Procedure OP/2/A/1106/14 (Moisture Separator/Reheaters), Enclosure 3.6 (Abnormal

Operating Conditions (1st Stage and 2nd Stage Reheater Drain Operation With 1st and 2nd

Stage Reheaters In Service)) has 2HD-91 and 2Hd-94 closed as an initial condition.

Use of this procedure enclosure was the result of an agreement between Operations and

Systems Engineering to prevent water hammers from occurring. This system evolution was

first performed July 22, 1996 on Unit 2 under Systems Engineering direction.

September 24, 1996

1130

Plant conditions prior to placinq Unit 2 Generator On-Line

Generator Load = 0 Mwe

2A1/2A2 Feedwater Heater Shell pressure = 0 psig

2A1/2A2 second stage reheater Tube Supply pressure = 0 psig

2B1/2B2 second stage reheater Tube Supply pressure = 0 psig

2A second stage reheater Drain Tank temp. = 136 degrees F

2B second stage reheater Drain Tank temp. = 155 degrees F

second stage reheater Feed Forward temperature to 2A Feedwater Heaters =

112 degrees F

1135

Unit 2 Generator placed On-Line, automatically picks up 5 percent load.

1140

Plant conditions after Unit 2 Generator On-Line

Generator Load = 42 Mwe

2A1/2A2 Feedwater Heater Shell pressure = 0 psig

2A1/2A2 second stage reheater Tube Supply pressure = 0 psig

2B1/2B2 second stage reheater Tube Supply pressure = 0 psig

2A second stage reheater Drain Tank temperature = 136 degrees F

2B second stage reheater Drain Tank temperature = 156 degrees F

second stage reheater Feed Forward temperature to 2A Feedwater Heaters =

114 degrees F

1147 Second stage reheater Drain Tank 2B high level alarms/clears.

1216 Second stage reheater Drain Tank 2A and 2B low level alarms.

1248

2A1 Feedwater Heater Inlet, (2HPE-6) open. Begins heating, pressurizing the 2A1

Feedwater Heater.

APPENDIX B

2

1310

Second stage reheater Drain Tank 2A level low level alarm clears.

1317 2HPE-10 (2A2 Feedwater Heater Inlet) open. Begins pressurizing the 2A2 Feedwater

Heater. Second stage reheater Drain Tank 2B low level alarm clears.

1336

Feedwater Heater 2A1 and 2A2 low level alarms cleared (level established in the 2A1

and 2A2 Feedwater Heaters).

1411

2MS-76 (TO 2A second stage reheater) and 2MS-79 (TO 2B second stage reheater)

not fully closed. (Throttled open by operators because 2MS-112 and 2MS-173 not

operating properly.)

1422

2HD-25 cycles not closed to closed.

1423

2HD-25 not closed.

1435

2HD-25 closed.

1441

Second stage reheater 2A Drain Tank low level alarm clears.

1448

Power escalation stopped to investigate 2B second stage reheater drain tank level

problems. This was due to high tank level alarm and 2HD-26 indication closed.

1500 Power escalation resumed. Work order written for 2HD-26.

1509:59

2HD-25 not closed.

1510:30

2HD-25 closed.

1512:46

2HD-25 not closed. NOTE: With 2A second stage reheater Drain Tank

operating off High Level Control, 2HD-92 will be open, but with the manual

isolation valve 2HD-91 still shut, feed-forward level control has no effect on

tank level.

1513:17

2HD-25 closed.

1610:53

2HD-26 not closed. NOTE: With 2B second stage reheater Drain Tank

operating off High Level Control, 2HD-95 will be full open.

1611:46

2HD-26 closed.

1612:02

2B second stage reheater Drain Tank level not high. NOTE: probable

adjustment of 2HD-26 setpoint occurred around this time. I&E called the

Unit 2 control room and reported they found 2HD-91 and 2HD-94 closed. I&E

suggested that this was the cause of the high level. The Unit 2 Shift

APPENDIX B

3

Supervisor and the Units 1 and 2 CR SRO decided to open 2HD-91 and 2HD

94 now at 500 Mwe rather than waiting for 600 Mwe as specified on the

Septemver 23, 1996, 1800 Worklist (night orders). There was no day shift

Worklist.

(NOTE: .Engineers had previously specified 600 paig in second stage reheater

to ensure no backflow from Feed Water heaters.)

1625:19

2HD-26 not closed.

1625:21

2HD-26 closed..

1630:00

After a pre-job briefing, Operators were dispatched to open 2HD-91 and 2HD

94 per OP/2/A/1 106/14 (MSRH), Enclosure 3.6 (Abnormal Operating

Conditions (1st Stage & 2nd Stage Reheater Drain Operation With 1st and 2nd

Stage Reheaters In Service)). It was stressed to the Operators to slowly open

these valves.

Current plant conditions:

Generator Load = 500 Mwe

2A1/2A2 Feedwater Heater Shell pressure = 251 psig

2A1/2A2 second stage reheater Tube Supply pressure = 254 psig/266 psig

2B1/2B2 second stage reheater Tube Supply pressure = 250 psig/240 psig

2A second stage reheater Drain Tank temperature = 400 degrees F

2B second stage reheater Drain Tank temperature = 357 degrees F

second stage reheater Feed Forward temperature to 2A Feedwater Heaters =

237 degrees F

1640:30

Probable opening time of 2HD-91 and 2HD-94. Back flow from 2A Feedwater

Heaters can be observed from Operator Aid Computer, alarm typewriter data.

Interviews indicated that both 2HD-91 and 2HD-94 were throttled 1/4 open

simultaneously. Post accident, this was found to be 12-13 turns open. 1/4

open on this gate valve would allow for essentially full flow, depending on d/p

across the valve. Interviews indicate it took 3-4 minutes to open these valves

to 1/4 open. At that time then the line lunged to the East, a steam leak was

heard and then the line ruptured.

NOTE: during the 3-4 minute period required to open the valves to the 1/4

open point, no line movement or noise was heard.

1640:34

2HD-26 not closed. Level in 2B second stage reheater Drain Tank is

increasing, probably from backflow.

APPENDIX B

4

Current plant conditions:

Generator Load = 498 Mwe

2A1/2A2 Feedwater Heater Shell pressure = 250 psig

2A1/2A2 second stage reheater Tube Supply pressure = 254/265 psig

2B1/2B2 second stage reheater Tube Supply pressure = 250 psig/240 psig

2A second stage reheater Drain Tank temperature = 403 degrees F

2B second stage reheater Drain Tank temperature = 372 degrees F (dec)

second stage reheater Feed Forward temperature to 2A Feedwater Heaters =

237 degrees F (inc)

1640:42

2HD-26 closed (Increased frequency of 2B second stage reheater Drain Tank

dump valve cycling indicates increased backflow into Tank from 2A Feedwater

Heaters.

1640 to 1641 2HD-26 cycled seven times. This further substantiates that additional water

volume was coming into the 2B second stage reheater Drain Tank.

1642

2A2 Feedwater Heater Level Low.

Current plant conditions:

Generator Load = 495 Mwe

2A1/2A2 Feedwater Heater Shell Pressure = 238 psig

2A1/2A2 second stage reheater Tube Supply Pressure = 252 psig/263 psig

2B1/2B2 second stage reheater Tube Supply Pressure = 247 psig/237 psig

2A second stage reheater Drain Tank temperature = 403 degrees F

2B second stage reheater Drain Tank temperature = 338 degrees F (dec)

second stage reheater Feed Forward Temperature to 2A Feedwater Heaters =

290 degrees F (inc)

Simultaneous high and low level alarms on both the 2A and 2B second stage reheater

Drain Tank. The alarms cleared and the 2A second stage reheater Drain Tank high

and low level alarms returned within approximately 20 seconds. The alarms cleared

and the 2A second stage reheater Drain Tank high and low level alarms returned with

approximately 20 seconds. (utility typer)

1642:16

Lube Oil Purifier 2A tripped. NOTE: Steam cloud is theorized as actuating

sprinkler which trips the 2A and 2B lube oil purifiers. 2B second stage

reheater Drain Tank temperature reached its minimum and started increasing.

APPENDIX B

5

Current plant conditions:

Generator Load = 495 Mwe

2A1/2A2 Feedwater Heater Shell pressure = 234 psig

2A1/2A2 second stage reheater Tube Supply pressure = 251 psig/262 psig

2B1/2B2 second stage reheater Tube Supply pressure = 246 psig/236 psig

2A second stage reheater Drain Tank temperature = 403 degrees F

2B second stage reheater Drain Tank temperature = 333 degrees F (inc)

second stage reheater Feed Forward temperature to 2A Feedwater Heaters =

297 degrees F (inc)

1642:53

2A second stage reheater Drain Tank Level Low. 2B second stage reheater

Drain Tank Level High.

Current plant conditions:

Generator Load = 486 Mwe

2A1/2A2 Feedwater Heater Shell pressure = 224 psig

2A1/2A2 second stage reheater Tube Supply pressure = 243 psig/254 psig

2B1/2B2 second stage reheater Tube Supply pressure = 238 psig/228 psig

2A second stage reheater Drain Tank temperature = 403 degrees F

2B second stage reheater Drain Tank temperature = 355 degrees F (inc)

second stage reheater Feed Forward temperature to 2A Feedwater Heaters =

320 degrees F (inc)

1642:55

Second stage reheater Drain Tank Level alarms clear.

1643

The Unit 2 Shift Supervisor exited the Units 1 and 2 control room. When he

(heard/saw) the steam in the Turbine Building 5th floor, he returned to the

control room. He then directed the Unit 2 Reactor Operators to trip the

Reactor manually and to isolate steam to the 1st and 2nd Stage Moisture

Separator/Reheaters.

1643:18

2MS-76 and 2MS-79 closed. This isolates steam to the Moisture

Separator/Reheaters, second stage reheaters.

1643:25

Reactor manually tripped.

1643:35

2B second stage reheater Drain Tank level low. 2HD-95 failed open due to

loss of its instrument air lines. This allowed the 2B second stage reheater

Drain Tank to blow down.

1704

Attempted to isolate break from 2A Feedwater Heaters. 2HD-106 closed but

2HD-105 did not.

APPENDIX B

6

1705

Exited Emergency Operating Procedure.

2040

Notification of Unusual Event declared, terminated, based on "explosion within plant

resulting in visible damage to permanent structures/equipment." Terminated after

deciding that the damaged equipment had no effect on ability to reach/maintain safe

shutdown.

0

9

APPENDIX B

SPECIFIC ACTIVITY SEQUENCE

IMMEDIATELY BEFORE AND AFTER

UNIT 2 HEATER DRAIN LINE RUPTURE

1.

Non-licensed Operators OPEN 2HD-91

Nothing happens because the 2A second stage reheater Drain Tank

temperature was 403 degrees F (Psat approximately 242 psig).

2A Feedwater Heater was 250 psig which was close enough to 2A second

stage reheater Drain Tank Psat so there was no D/P across 2HD-91.

(Interviews stated 2HD-91 was easy to operate).

There were no water hammers because there was not enough D/P to force

flow through the lines in either direction.

2.

Non-licensed Operators start opening 2HD-94

They had to "tug" on the valve chain to operate the valve which indicates a

D/P across 2HD-94.

2B second stage reheater Drain Tank temperatures was 372 degrees F (Psat

163 psig).

2A Feedwater Heaters 250 psig resulting in a 90 psig reverse D/P.

With 2B second stage reheater Drain Tank pressure less than 2A feedwater

heaters' shell pressure and adequate D/P to force flow, there was reverse flow

from the 2A Feedwater Heaters to the 2B second stage reheater Drain Tank.

This corresponds to a decrease in 2B second stage reheater Drain Tank

temperature.

After approximately 2 minutes of back flow into 2B second stage reheater

Drain Tank, the line ruptured.

3.

When the line ruptured:

2HD-95 failed open on a loss of control air pressure (Instrument air line blown

off).

With 2HD-95 failed open, there was a blow down path from both the 2A1 and

2A2 Feedwater Heaters, the 2A and 2B second stage reheater Drain Tanks,

and the second stage reheater Tube bundles for all four Moisture

Separator/Reheaters.

APPENDIX C

2

4.

When 2MS-76 and 2MS-79 were closed at 1643:18, this isolated steam to the second

stage reheater Tube bundles. As 2A second stage reheater Drain Tank level

decreased, 2HD-92 closed isolating the 2A second stage reheater Drain Tank from

the break. 2B second stage reheater Drain Tank continued to blow down until it was

completely empty at 1643:35.

5.

When the reactor was tripped, it manually isolated extraction steam to the 2A

feedwater heaters and they continued to blow down.

APPENDIX C

WATER HAMMER

PROCEDURE AND SYSTEM HISTORY

MOISTURE SEPARATER REHEATER DRAIN LINES

NOTE: Water hammer history and events were documented in-depth for only one year.

Other numerous water hammers were routine from beginning of plant operation.

Moisture Separator/Reheaters Procedure and System History

1.

October 2, 1973 - Original Procedure OP/2/A/1106/14 issued. No specific guidance

for feeding forward second stage reheater and first stage reheater drains.

2.

August 21, 1975 - Change #1 to procedure. General Electric recommendation.

Heater drains (first stage reheater and second stage reheater) routed forward to the

'A' (Highest pressure) feedwater heaters to provide part of final heating of Main

feedwater.

3.

December 28, 1977 - Reissued procedure requirement added for turbine to be above

300 MWe prior to aligning second stage reheater drains to 'A' Feedwater heaters

(feed forward).

4.

= 1980- First stage reheater drain, 10 inch pipe, into 18" header cut off and rerouted

to flash tanks.

5.

November 3, 1992 - Revision 23, Guidance in procedure (Enclosure 3.8 Abnormal

Operating Conditions, Startup of first stage reheaters and second stage reheater at

Power) to require Moisture Separator/Reheaters Tube Supply Steam Pressures above

the A/B feedwater heater extraction steam pressure. (Prior to this, the entire system

was brought on-line with the drain aligned to the "feed forward" mode. Guidance also

included to slowly open HD-91, 94 valves when aligning to "feed forward". This same

guidance is not in Enclosure 3.6, Reheater Drain Operation, used to align first stage

reheater, second stage reheater drains to feed forward/dump back to condenser.

6.

July 24, 1994 - Problem Identification Report 94-1001 - Evidence of water hammer on

Unit 1 second stage reheater Drain Tank during transition of feed forward mode.

(Lines shook, lagging shaken loose) Dump back to condenser periodically opened,

causing control interaction with feed forward level controls. "B" side lines continued to

swing two feet side to side.

7.

May 9, 1995 - Problem Identification Report-1 -95-513 - Water Hammer on 1B second

stage reheater drain system broke drain tank supports. Problem Identification Report

evaluation revealed excessive heatup rates, thermal transients on all three units'

second stage reheaters, first stage reheaters, and Moisture Separator/Reheaters.

(=260 degrees F/30 minutes versus 50 degrees F/30 minute limit) Problem

Identification Report corrective actions included reevaluation of second stage reheater

Tank and Line Supports, replacing level control/dump valves and control systems,

APPENDIX D

2

6

development of Nuclear Station Modification 2941 for replacing MS-112, 173 valves

and control systems, changes to Procedure OP/1106/14 to implement restrictive

heatup rates (30 degrees/30 minutes) per vendor.

8.

April 27, 1995 - Problem Identification Report-95-0457 - During Unit 1 Startup, wrong

Enclosure to Procedure OP/A/1106/14 used for securing "feed forward" mode,

resulted in Moisture Separator/Reheaters relief actuation.

9.

September 21, 1995 - Change #24 changed ambiguous enclosure titles to prevent

use of wrong enclosure addressed in Problem Identification Report-95-0457.

10.

October 1995 - Nuclear Station Modification 2941 Scoping document issued.

11.

December 1995 - Unit 1 Startup using revised OP/A/1106/14 using Manual loading of

MS-112, 173. No water hammer, but heatup rates close to 100 degrees F/hour.

Operator burden (local air-loading MS-112, 173 while Control room operator in contact

with info on temperature change) deemed too great. Recommended Nuclear Station

Modification implementation to revise valve/control design change.

12.

May 1996 - Temporary modification TT/2/B/0271/009 setup and control of Moore

Controller for 2MS-1 73 developed to test capability of manual loading of MS-1 12, 173

using new, digital controller. Attempt to see if controller change out alone could

provide acceptable steam admission rates to Moisture Separator/Reheaters.

13.

May 4, 1996 - Revision #26 to OP/2/A/1106/14, Changes to:

a.

Allow manual loading of 2MS-1 12, 173 up to a point (350 degree F second

stage reheater Tube Temperature) at which time the Auto Controller will

control adequately by its control program to prevent exceeding second stage

reheater Heatup Rate Limits.

b.

Remove Loading Curve from procedure because of conflict with second stage

reheater Heatup Limits for normal power escalation rates and initially valve-in

Main Steam to second stage reheater with second stage reheater Tube

Temperature 50 degrees F> LP Turbine Inlet Temperature as discussed and

recommended by Engineering.

c.

Initiate MS to second stage reheater later (after T-G on-line at approximately

200 Mwe) to reduce Operator burden of placing second stage reheater in

service in Manual during T-G Startup and at advice of Engineering (Main

Steam to second stage reheater's not needed at low loads and there is an

increased potential for introducing unnecessary thermal stress to the second

stage reheater tube bundles).

APPENDIX D

3

14.

May 7, 1996 - OP/2/A/1106/14 Moisture Separator/Reheaters Operation, in

conjunction with TT/2/B/0271/009, performed for Unit 2 Post Refueling outage Startup

of second stage reheater's. Results were acceptable for controlling second stage

reheater Heatup Rate and showed that replacement of the MS-112, 173 Control

System with minor valve trim replacement for improved seat leakage was acceptable.

However, a severe water hammer was introduced in the second stage reheater Heater

Drain System during the second stage reheater startup sequence that broke a support

at the junction of the two second stage reheater Drain Tank feed forward pipes. This

water hammer was later found to be caused by 2HD-26 failing open while the normal

level control valve 2HD-95 to FEED WATER Heater 2A also OPEN. (Reverse flow

from heaters to condenser.) (Problem Identification Report-2-96-0984)

15.

July 1996 - The data analysis for the Unit 2 5-96 second stage reheater Startup was

complete and it was concluded that the water hammer was initiated by backflow from

the 2A High Pressure Feedwater Heaters through the failed-open 2A second stage

reheater Drain Tank Dump Valve. The second stage reheater Drain Tank Pressure

could not be maintained greater than the 2A High Pressure Feedwater Heater. This

confirmed the argument for placing Check Valves in these Drain Lines, and the

Nuclear Station Modification-2941 scope was changed accordingly.

16.

July 16, 1996 - A meeting was held between Engineering and Operations

representatives to discuss the water hammer phenomenon in the second stage

reheater Drain Pipes and to reach consensus on recommendations for short-term and

long-term Corrective Action (later addressed in Problem Identification Report-2-96

0984). This meeting was prompted by the Unit 2 upcoming Startup and the fact that

procedural changes (not yet identified in the incomplete Problem Identification Report)

may be required in support of the Unit 2 Startup. The following is a summary of the

discussions and outcome resulting from that meeting:

a.

Described the May 7, 1996, Unit 2 Water Hammer event that was caused by

backflow in the second stage reheater Heater Drain feed forward pipe when

second stage reheater Drain Pressure was less than High Pressure Feedwater

Heater Shell Pressure.

b.

Described how second stage reheater Drain Pressure may be less than High

Pressure Feedwater Heater Shell Pressure; dependent on MS-1 12, 173

operation and second stage reheater Dump Valve operation (it was stated that

a second stage reheater Dump Valve open failure can lead to depressurization

of second stage reheater Drain and initiation of backflow from the High

Pressure Feedwater Heaters).

c.

Described that the most significant water hammers can be eliminated by

preventing backflow in the second stage reheater Heater Drain System by

maintaining second stage reheater Pressure greater than "A" High Pressure

Feedwater Shell Pressure (with additional consideration of static head in the

second stage reheater Drain Pipe).

APPENDIX D

4

d.

Described further that initial slow admission of Main Steam to second stage

reheater's via MS-1 12, 173 should help to minimize water hammer as

evidenced in the previous Unit 1 Startup.

e.

Described the Long-Term Solutions proposed for Nuclear Station Modification

2941: Proposed addition of Check Valves in the second stage reheater Drain

Pipes to prevent backflow conditions. Change-out of MS-1 12, 173 trim for

positive seating and finer control. Change-out of MS-112, 173 Control System

for allowing finer control and with possible new control logic for minimizing

excessive heat-up rates.

f.

Opened discussions of a Short-Term Solution for second stage reheater

Startup to prevent backflow. The following options were discussed and

evaluated:

(1)

Manually Close HD-91 and HD-94 prior to any second stage reheater

Startup (following Shutdown). Then Manually and slowly throttle HD-91

and HD-94 open during the Startup Sequence while maintaining second

stage reheater Pressure greater than 'A' Heater Shell Pressure (with

margin) with MS-112, 173.

(2)

Manually Close isolation valves downstream of level control valves HD

92, HD-95, HD-105 and HD-106, prior to any second stage reheater

Startup (following Shutdown). Then Manually and slowly throttle HD

105 and HD-106 open during the Startup Sequence while maintaining

second stage reheater Pressure greater than 'A' Heater Shell Pressure

(with margin) with MS-112, 173.

(3)

Maintain second stage reheater Pressure greater than 'A' Heater Shell

Pressure (with margin) by slowly throttling MS-112, 173 open and

communicating with the Control Room prior to and during Main Turbine

roll and throughout the startup sequence using a similar procedure to

the current Unit 1 OP/1106/14 Moisture Separator/Reheaters.

g.

Option 3 was ruled out as not having enough positive control to prevent

backflow (i.e., not having the closed manual isolation valves in the second

stage reheater Heater Drain System and due to the Operator burden and the

extreme attention required while using a Main Steam Admission and Drain

Tank level control system known for inaccuracy and potential failures).

h.

Option 1 was modified when it was concluded that there would be optimum

control if the throttling of HD-91, 94 began at a second stage reheater

Pressure greater than the Design Pressure of the 'A' Heater Shell Pressure

APPENDIX D

5

which was shown to be 500 psig. A second stage reheater Pressure of

600 psiq was chosen for conservatism as the starting point for throttling open

HD-91, 94 to ensure a positive second stage reheater drain flow from any

operating condition.

Option 2 was discussed with personnel safety, compared to Option 1, initially

considered as one of its benefits. It was later ruled out based upon the

thought that these valves would be difficult (or impossible) to open manually

with a differential pressure across the valves and because of their potentially

confining location that might have been less safe than that presented in

Option 1.

j.

Consensus was reached in utilizing the Modified Option 1, requiring 600 psiq

second stage reheater Pressure, prior to slowly throttling HD-91, 94 open to

valve in second stage reheater Drains to the 'A' High Pressure Feedwater

Heaters.

k.

A discussion followed on how best to initiate this change. It was discussed

that a procedure change to the existing Procedure OP/2/A/1106/14 would be

necessary to include the requirements of item (j). It was brought to the table

that there already existed an Enclosure in the procedure that directed manual

operation of the second stage reheater feed forward drains and that it could be

utilized with additional instruction to perform the desired steps for manually

valving in second stage reheater drains to 'A' Feedwater Heaters. It was also

stated that the OP/1106/14 Procedures for all three units were undergoing re

write. Because of these circumstances, consensus was reached to utilize the

Unit Operations Daily Worklist until such time that the procedure rewrites were

completed for the additional directions necessary to ensure that HD-91, 94

were isolated prior to startup and that after reaching 600 psig second stage

reheater Pressure, HD-91, 94 would be slowly throttled open per the existing

OP/1106/14 Enclosure and procedure to introduce second stage reheater

Drain feed to 'A' Feedwater Heaters.

NOTE: Administrative Procedure OMP 1-9 prescribes the method to be used

to place a procedure on Administrative Hold to prevent its use prior to

incorporating the necessary changes. The decision to rely on non-controlled

processes (verbal precautions, Daily Worklist) resulted in use of a procedure

that was not adequate. Those items were covered adequately during the

July 22, 1996 system startup when system engineers accompanied the

operators, but not for the September 24, 1996 event.

I.

It was agreed that Engineering would be present to observe the Unit 2 second

stage reheater Startup sequence, including the manual feed forward of second

stage reheater drains to the 'A' Feedwater Heaters.

9

APPENDIX D

6

17.

July 22, 1996 - Unit 2 startup accomplished with no problems during transition to feed

forward mode. Engineering accompanied operators, drain tank d/t, d/p maintained

closely. Also, operators cracked open 2HD-91, 94 much less than 1/4 open, then

waited approximately 40 minutes before opening further. (Operators left area for

"coffee break" to allow slow, thorough heatup and equalization.)

18.

Operators charged with revising OP/A/1106/14 to incorporate precautions used during

July 21, 1996 startup and July 5, 1996 meeting between OPERATIONS/Engineering.

The revision due date was October 14, 1996. No effective communication to shift

crew on September 24, 1996 startup. Only reference is "slow" opening of 2HD-91,

94, erroneous reference to "600 Mwe" vs agreed upon value of 600 psig.

5

APPENDIX D

THE LICENSEE REVIEW TEAMS

Event Investigation Team

G. Gilbert - NSRB staff - Team Leader

C. Curry - Operational Assessment, NGO - Assistant Team Leader

M. Pyne - Mechanical Equipment Engineering, NGO

A. Buzhardt - Safety and Industrial Hygiene, NGO

M. Langel - Mechanical/Civil Equipment Engineering, MNS

S. Shillinglaw - Security (MERT), CNS

J. Bryant - Safety Review Group, ONS

C. Goslow - INPO, Event Analysis

F. Krauss - Operating Experience Assessment, NGO

K. Wilmer - Corporate Safety and Industrial Hygiene

Failure Investiqation Process Team

D. Coyle - Investigation and Recovery Coordinator

B. Millsaps - Management Oversight

B. Dobson - Management Oversight

T. Royal - Supervisory Direction

B. Heineck - Supervisory Direction

P. Fisk - Investigation Lead

N. Watson - Investigation Lead

G. Lareau - MSE

.

A.

Park - MSE

H. Harling - SME

V. Bowman - Pressure Transient

M. Haynes - Operations

D. Smith - Operations

R. Bowman - Operations

B. Jones - Operations

M. Miller - I&C

D. Phelps - I&C

B. Davis - Documentation

K. Alter - Documentation

C. Arnold - Outage Team Liaison

D. Kelley - Recovery Team Engineering Supervisor

S. Anderson - Metal Analysis

T. Brown - Stress Analysis

M. Kelly - Vibration

APPENDIX E

5

EXIT ATTENDANCE

Licensee

J. Hampton, Vice President, Oconee Site

B. Peele, Station Manager

D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

W. Foster, Safety Assurance Manager

B. Millsaps, Engineering Manager

D. Hubbard, Maintenance Superintendent

E. Burchfield, Regulatory Compliance

C. Little, Electrical Systems/Equipment Manager

J. Smith, Regulatory Compliance

G. Ridgeway, Acting Operations Superintendent

NRC

J. Jaudon, Deputy Director, DRS

M. Scott, Senior Resident Inspector, Oconee

O

N.

Economos, Reactor Inspector, DRS

T. Peebles, Augmented Inspection Team leader

APPENDIX F