ML15118A096

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Insp Repts 50-269/96-03,50-270/96-03 & 50-287/96-03 on 960128-0309.Violation Noted.Major Areas Inspected:Plant Operations;Maint & Surveillance Testing Including Keowee Hydro Maint Program,Engineering & Plant Support
ML15118A096
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 04/04/1996
From: Crlenjak R, Harmon P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A094 List:
References
50-269-96-03, 50-269-96-3, 50-270-96-03, 50-270-96-3, 50-287-96-03, 50-287-96-3, NUDOCS 9604240158
Download: ML15118A096 (33)


See also: IR 05000269/1996003

Text

VRE 1UNITED

STATES

0

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.: 50-269/96-03, 50-270/96-03 and 50-287/96-03

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.:

50-269, 50-270 and 50-287

License Nos.: DPR-38, DPR-47 and DPR-55

Facility Name: Oconee Units 1, 2, and 3

Inspection Conducted: January 28 - March 9, 1996

Inspectors:

  • < /'/

P.E Hron,Tenior Residen 0speoor

Date Sign d

P. G. Humphrey, Resident Inspector

L. A. Keller, Resident Inspector

N. L. Salgado, Resident Inspector

P. J. Fillion, Reactor Inspector (paragraphs 3.3 and 3.4)

G. A. Walton, Reactor Inspector (paragraphs 3.3 and 3.4)

R. L. M e, Reactor Inspector (paragraphs 4.4, 4.7 and 6.0)

L. K g Re ctor Inspector (paragraphs 4.4, 4.7 and 6.0)

Approved by:

/

AV

R .Cre4k

ranch

ief

Dite Signed

Division of Reactor Projects

SUMMARY

Scope:

Inspections were conducted by the resident and regional inspectors in the

areas of plant operations; maintenance and surveillance testing, which

included a review of the Keowee Hydro Maintenance Program; engineering, which

included an inspection of the spent fuel and associated equipment; and plant

support.

Results:

Plant Operations

Unit 1 tripped from full power on February 28, 1996, due to a failed circuit

card in the Integrated Control System. The unit was restarted and achieved

full power on March 1, 1996. Management made a conservative decision to have

the operators responsible for the restart perform a startup on the simulator

ENCLOSURE

9604240158 960404

PDR

ADOCK 05000269

PDR

(1

2

prior to restarting the unit. The restart of the unit was accomplished

without incident (paragraph 2.2).

The periodic rotation of control room personnel to prevent complacency towards

malfunctioning alarms was considered a good practice (paragraph 3.1.2).

Maintenance

Activities reviewed within the maintenance area were performed to acceptable

standards. During a Keowee Hydro Station modification test, the licensee's

actions to exit the test when problems were encountered and enter a

contingency to back out of the modification was considered to be conservative

(paragraph 3.1.3).

A review of the Keowee Maintenance Program indicated it met regulatory

requirements, being enhanced by the Keowee Upgrade Project (paragraph 3.3).

Engineering

Addressed as Unresolved Item (URI) 96-03-01, errors were identified by the

licensee in calculation OSC-2280 involving low pressure service water net

positive suction head absolute and minimum required lake level (paragraph

4.1).

Apparent Violation 96-03-02 was identified that involved an

inoperability issue associated with the Containment Hydrogen Control Systems

that had existed since the system was originally installed (paragraph 4.2).

Plant practices, procedures, calculations, and parameters associated with the

Spent Fuel Pool (SFP) were determined to be consistent with the licensee's

engineering analysis. However, URI 96/03-03 was identified that addressed the

adequacy of the information provided by Duke to the NRC when designing the

interface taps for the supply lines from the SFP to the Standby Shutdown

Facility (paragraph 4.4.2).

The licensee continues to have difficulties in the area of NRC reporting

requirements (paragraph 4.6).

Plant Support

Two spills/leaks of low activity liquid waste resulted from the use of a wrong

size hose clamp on a transfer line and an incorrectly installed gasket in the

manway on the 'D' demineralizer (paragraph 5.1).

ENCLOSURE

REPORT DETAILS

Acronyms used in this report are defined in paragraph 8.

1.0

PERSONS CONTACTED

Licensee Employees

  • M. Bailey, Regulatory Compliance
  • E. Burchfield, Regulatory Compliance Manager

S. Burton, Keowee, Operations

T. Coutu, Operations Support Manager

D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

  • W. Foster, Safety Assurance Manager
  • J. Hampton, Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

T. Ledford, Supervisor, Electrical Systems

C. Little, Electrical Systems/Equipment Manager

  • B. Milisaps, Manager, Mechanical/Civil Equipment
  • B. Peele, Station Manager

R. Severance, Mechanical Systems Engineer

J. Smith, Regulatory Compliance

J. Stevens, Electrical Systems Engineer

R. Sweigart, Work Control Superintendent

S. Townsend, Keowee, Operations

L. Underwood, Electrical Systems Engineer

J. Weir, Maintenance Engineer

  • Attended Exit Interview

Other licensee employees contacted during this inspection included

engineers and technicians.

2.0

PLANT OPERATIONS (71707)

The inspectors reviewed plant operations throughout the reporting period

to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls.

Control room logs,

shift turnover records, temporary modification log, and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted on day and night shifts, during

weekdays and on weekends. Inspectors attended some shift changes to

evaluate shift turnover performance.

Actions observed were conducted as

required by the licensee's Administrative Procedures. The complement of

licensed personnel on each shift inspected met or exceeded the

ENCLOSURE

2

requirements of TS. Operators were responsive to plant annunciator

alarms and were cognizant of plant conditions.

Plant tours were taken throughout the reporting period on a routine

basis. During the plant tours, ongoing activities, housekeeping,

security, equipment status, and radiation control practices were

observed.

2.1

Plant Status

Unit 1 operated at or near full power until February 28, 1996, when the

unit tripped because of problems that developed from a failed circuit in

the Integrated Control System (ICS).

The unit was restarted on March 1,

1996, and achieved full power at 3:20 a.m., on March 2, 1996.

Unit 2 operated at or near full power throughout the reporting period.

Unit 3 operated at or near full power throughout the reporting period.

2.2

Unit 1 Trip

Unit 1 tripped from full power on February 28, 1996, at 9:03 p.m. The

trip was evaluated and determined to have been initiated by a faulty

feedwater temperature compensator circuit in the ICS. This circuit

failure caused a disturbance in the feedwater system. During the

resultant transient, the condensate cooler bypass valve (1C-61) closed

as designed to control the booster pump suction pressure, but did not

re-open when required. This caused the condensate booster pumps to lose

suction and trip on low suction pressure. The loss of the booster pumps

in turn caused the main feed pumps to trip on low suction pressure,

which provided the signal that initiated the reactor trip.

Main Steam Valve 1MS-77 (Second Stage Reheater Supply Valve) failed to

close as required in response to the trip. This valve failure was

detected by the OATC and upstream steam header supply valves 1MS-76 and

79 were closed to isolate the main steamline and prevent a pressure

blowdown. Steam and feedwater systems were "walked down" by civil

engineering to ensure there was no damage to the equipment, piping, or

hangers.

Shutdown margins were maintained during the trip and operator actions

were determined to be have been adequate.

Operators that were scheduled to restart the unit performed a startup on

the simulator. This had not been a practice at ONS and was implemented

by the plant manager as a result of NSRB recommendations. The operators

felt this near-term training was very beneficial, and plan to continue

the practice in the future.

ENCLOSURE

1

3

The inspectors responded on-site to the trip and monitored the recovery

operations. In addition, the inspectors attended PORC meetings,

reviewed the trip report, and monitored the restart activities.

Within the areas reviewed, the units were operated in accordance with

procedures. An enhancement was noted prior the restart of Unit 1 by

first having the operators responsible for the restart to perform a

plant startup on the simulator.

3.0

MAINTENANCE (62703, 61726, 62700, 40500 and 92902)

3.1

Maintenance Activities

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work that

was not within the skill of the craft. Activities, procedures and work

orders were examined to verify that proper authorization and clearance

to begin work was given, cleanliness was maintained, exposure was

controlled, equipment was properly returned to service, and limiting

conditions for operation were met. Maintenance activities observed or

reviewed in whole or in part are addressed in the sub-paragraphs of 3.1

below:

3.1.1 NSM-22922 Install Y-Strainer Upstream Of 2MS-93, W095023925

On February 8, 1996, the inspector observed the installation of a

differential pressure gauge to monitor the pressure drop across a

Y-strainer that was scheduled to be installed in the main steam

line to the Unit 2 Turbine Driven Emergency Feedwater Pump during

the refueling outage scheduled to begin on March 28, 1996. The

pressure gauge and associated instrument tubing was installed to

QA safety class standards and was in accordance with applicable

procedure IP/0/A/3010/003A, Procedure for Mounting Field Run

Instrument Tubing And Cable Support Systems.

All work was performed to acceptable standards and with proper

documentation.

3.1.2 Spurious Alarms, WO 96013595-01

On February 14, 1996, multiple statalarms on panels 1SA

5,6,8,9,14,and 15 were received in the Unit 1 CR. The statalarms

were annunciating approximately every two minutes. The licensee

initiated PIP 1-096-0290 to address this recurring problem. The

inspector observed portions of the licensee's troubleshooting of

this problem. After extensive troubleshooting, the licensee

determined that the -problem was a short in the 1A FWPT oil cooler

outlet temperature gauge 1TH-141A from the alarm circuit to the

ENCLOSURE

0

4

center of the gauge needle. The licensee repaired the

malfunctioning gauge by removing the needle and reaming the

mounting hole to a larger size so that the indicator needle would

seat further on the shaft to allow for an air gap to prevent arcs.

The licensee successfully calibrated the gauge using

IP/O/B/0270/005B-1, FWPT Instrumentation Rearing Temperature and

Oil System, and returned it to service. The Shift Operations

Supervisor rotated control room personnel periodically during the

time the malfunction was occurring to prevent complacency toward

the alarms. The inspector considered this rotation to be a good

practice and concluded that the licensee's actions were

appropriate in addressing this issue.

This was the same problem identified on February 3, 1996, as

documented in PIP 1-096-0213, which was thought to be corrected by

WO 96010253. The WO 96010253 addressed a loose intermittent

connection.

3.1.3 Installation Of Keowee Unit 1 Overspeed/Overfrequency Logic,

TN/5/A/2966/BL1/08

The licensee was proceeding with TN/5/A/2966/BL1/08, Installation

of Keowee Unit 1 Overspeed/Overfrequency Logic. The purpose of

the procedure was to install overspeed/overfrequency logic in

various circuits for Keowee Unit 1. It was also to remove the

underground breaker permissive from the 94 GB circuit. On

February 23, 1996, during the post modification testing of

TN/5/A/2966/BL1/08 which involved initiating an ES signal

coincident with a governor failure signal, ACB-1 cycled

approximately twelve times. The testing was being performed

during a 72-hour LCO due to both Keowee units being out of

service. Troubleshooting procedure MP/0/A/2000/13 was initiated

to determine the problem with the breaker. The licensee tested

the anti-pump circuitry of ACB-1 and found it to be operable. The

inspector attended a PORC meeting which was convened on February

23, 1996, at 7:30 p.m. to evaluate the problem and it's effect on

the modification. The PORC recommended that the modification team

execute the preplanned contingency and back out of the

modification. The contingency plan was performed, both paths were

declared operable, and the LCO was exited. The licensee

determined that the problem with ACB-1 cycling was due to a

transformer undervoltage relay dropping out the anti-pump

circuitry. During the test of the governor failure logic, the

breakers partially closed and induced some voltage on the step-up

side of the breaker. This voltage caused the close permissive to

be removed and allowed the breaker to close. Upon closure of the

breaker, the breaker tripped due to the governor failure logic.

While developing the modification the licensee had evaluated the

possibility of ACB-1 cycling during the test. A Caution statement

documented in TN/5/A/2966/BL1/08 prior to Step 4.14.50, states

ENCLOSURE

5

"Should ACB-1 cycle continuously, Keowee Operations should HOLD

GENERATOR ACB NO. 1 control switch in the CLOSE position until

cycling stops."

However, this note did not address that the

Master Select switch needed to be in the manual position for the

cycling to terminate. The licensee had to remove control power

from ACB-1 to terminate the cycling. The licensee performed

normal maintenance checks on ACB-1 to ensure that the repeated

cycling had not adversely affected its operability. The inspector

concluded that the licensee's actions to execute the

TN/5/A/2966/BL1/08 contingency to back out of the modification was

conservative.

3.2

Surveillance Activities

The inspectors observed surveillance activities to ensure they were

conducted with approved procedures and in accordance with site

directives. The inspectors reviewed surveillance performance, as well

as system alignments and restorations. The inspectors assessed the

licensee's disposition of any discrepancies which were identified during

the surveillance. Surveillance activities observed or reviewed in whole

or in part are addressed in the sub-paragraph of 3.2 below:

3.2.1 Unit 2 RPS Channel B Calibration And Functional Test, WO 96012180

The inspector observed activities in progress during the

calibration of the Unit 2 RPS Channel B. The effort was performed

in accordance with applicable procedures, IP/0-2/A/0305/003,

Nuclear Instrument and Reactor Protective System and IP/0

2/A/0305/003B, Instrument Procedure Data Package for RPS Channel

B, and IP/0-O/A/0305/015, Nuclear Instrumentation RPS Removal and

Return to Service.

Documentation was current and work observed was performed to

acceptable standards.

3.2.2 Unit 2 RPS A,B,C,D CRD Breaker Test, WO 96005963

The inspector observed performance of procedure, IP/O/A/0305/14,

RPS Control Rod Drive Breaker Trip and Timing Test on February 1,

1996. The effort included performance of operations procedure

OP/0/A/0330/009, Power Supply Check of Control Rod Drive, and

IP/0/A/0305/15, Nuclear Instrumentation RPS Removal and Return to

Service.

The equipment was found to be within acceptable tolerances and the

activity was performed in accordance with the procedures.

ENCLOSURE

6

3.2.3 Unit 3 Control Rod Movement, PT/3/A/0600/15

On February 15, 1996, the inspector observed the performance of

PT/3/A/0600/15 which tests control rod drive operation under

actual operating conditions. The procedure met the monthly

surveillance requirements as specified in TS 4.1.2.

The operators performed the control rod movements according to the

procedure, and were cognizant of plant operating status during the

test. During the portion of the test which involved Group 5 rods,

the absolute position indication for rod one of that group dropped

to approximately 40 percent. The operator initiated WO 96007256

to address this discrepancy. The problem was determined to be a

position indicator card, which was replaced. The procedure

acceptance criteria was met. The inspector concluded that the

operations staff actions were appropriate during the performance

of this procedure.

3.2.4 Keowee Hydro Operation, PT/0/A/620/09

On February 21, 1996, the inspector observed the performance of

PT/0/A/620/09 from the Oconee CR. The test satisfied the monthly

requirement of TS 4.6.1. While performing the test, Keowee Unit 1

was aligned to the underground feeder and Keowee Unit 2 was

aligned to the overhead feeder. Keowee Unit 1 was started and

voltage was required by Step 12.16 documented and verified to be

within the allowable band of 13.8 - 14.49 KV. The voltage was

13.6 KV as indicated in the Oconee CR and 13.5 KV as read in the

Keowee CR. As required by the test, System Engineering was

notified to discuss the operability of the Keowee Unit 1.

Concurrently, the licensee generated PIP 0-096-0364. The licensee

determined that 13.5 KV was an adequate voltage and

PT/0/A/0620/009 does not account for expected synchronizer

response when the grid voltage decreases to a point that 13.8 KV

system bus voltage was below generator output voltage. The

computer point for bus voltage was reading approximately 13.6 KV.

In this condition, the generator bus voltage would be expected to

increase to 13.8 KV and then decrease as the synchronizer matched

generator and bus voltage. The licensee determined that this was

consistent with observed unit response during the performance of

the PT. The screening remarks of PIP 0-096-0364 indicated that

the PT should be written to verify operability with the

synchronizer in manual, which will make the unit respond

consistent with an emergency start where the synchronizer is

defeated by emergency start relay contacts. The licensee

continued with the remaining portions of the test and no other

problems were encountered. The inspector concluded that the

operators had adhered to the procedure, and that all the

acceptance criteria was met except for acceptance criteria 11.5,

"Each Keowee Unit OUTPUT VOLTAGE is within the allowable band.

ENCLOSURE

7

The allowable voltage band is 13.8 to 14.49 KV," for which the

licensee performed a required operability evaluation.

3.2.5 Reactor Protective System Channel "D" RC Temperature Instrument

Calibration, IP/O/A/0305/001H

On February 27, 1996, the inspector observed portions of

IP/O/A/0305/OO1H, Reactor Protective System Channel "D" RC

Temperature Instrument Calibration. The calibration satisfied TS section 3.5.1.1 Table 3.5.1-1 #5 and #6, and section 4.1.1 Table

4.1.1 #7 and #11.

The inspector verified that proper test

equipment was used, and that the licensee was adhering to the

respective procedure. The inspector concluded that all activities

observed were satisfactory.

Within the areas reviewed, no violations or deviations were identified.

3.3

Maintenance Program for Keowee

As addressed in the sub-paragraphs of 3.3 below, Regional based

inspectors reviewed and evaluated an issue identified during the

Electrical Distribution System Functional Inspection (EDSFI), NRC

Inspection Report 50-269,270,287/93-02. EDSFI Finding 6.b stated that

testing had not been performed on safety-related mechanical components

(i.e., coolers and pumps).

As a result of this finding, the licensee

has significantly upgraded the test program for mechanical components at

Keowee. In addition, at a meeting between licensee and NRC management,

the licensee committed to significantly upgrade the maintenance

procedures related to equipment at Keowee. NRC followup of this issue

was tracked under Inspector Followup Item 50-269,270, 287/95-26-02,

Review Test Program for Mechanical Components at Keowee to Resolve EDSFI

Finding 6.b.

The criteria applied by the inspectors in reviewing this issue was that

periodic testing demonstrated that the design basis requirements of the

equipment being tested was maintained, and the maintenance activities

met the requirements of 10 CFR 50, Appendix B, and FSAR Section

13.5.2.2.1, Maintenance Procedures. The licensee was in the process of

enhancing their Inservice Test program with regard to Keowee, and they

planned to submit the revised program to NRC. Since the enhanced

program had not been submitted to NRC, the enhanced Inservice Test

program was not within the scope of the inspection.

3.3.1 Site Walkdowns

The inspectors toured the Keowee facility in order to evaluate the

workmanship, cleanliness and overall operation controls being

implemented in order to maintain the facility in an emergency

operational ready condition. The facility was noted to be well

maintained, the personnel were knowledgeable of the equipment, and

ENCLOSURE

1

8

the equipment appeared to be maintained in an acceptable quality

condition. The inspector observed one generator operating and

noted oil and water leakage was maintained at a minimum level.

On February 15, 1996, at about 10:00 p.m., while craftsmen were

functional testing an electrical modification at the Keowee

station (NSM-5-2966-BL1), a short-circuit occurred in a 125 VDC

circuit. As a result of the short-circuit, arcing occurred when a

terminal block link in a termination cabinet was being closed.

Since the affected equipment was already out of service for

testing, operational consequences were minimal.

The NRC

inspectors examined the damaged terminal block and reviewed the

plan for repairing the damage and assessing the extent of damage.

The inspector agreed that the planned repairs would restore the

terminal block and wiring to good condition. This event is

described in further detail in paragraph 4.3 of this report.

3.3.2 Duke Power Self-Initiated Technical Audit (SITA) SA-95-39

A licensee audit was conducted November 13 through December 12,

1995, of the Keowee operational controls, maintenance,

surveillance and other testing, and personnel training to ensure

Keowee is operated and maintained to perform its safety-related

function. The audit identified 13 findings. However, the audit

noted that none of the findings impact the operability or

reliability of the emergency power system. All findings were

identified on PIPs to ensure comprehensive corrective actions

would be implemented.

From the list of PIPs, the inspector selected PIP 4-0-95-1720 for

review. The PIP was open at the time of this inspection and

identified that "Several Keowee maintenance and testing procedures

were reviewed and found to contain considerably less detail than

approved Oconee maintenance and testing procedures." An example

given in the audit finding was that procedure MP/1/A/2200/017,

Unit 1 Turbine, Governor, and Generator Weekly Preventative

Maintenance, does not contain instructions for the proper amount

of torque to be applied to strainer bolting. For corrective

actions, the licensee determined the deficiency identified was not

significant, but planned to enhance the procedure by incorporating

this procedure into a site procedure entitled PT/1/A/2200/001 KHU

1 Weekly Surveillance. Although this procedure had not been final

approved at the time of this inspection, the inspector reviewed it

to determine if the corrective actions addressed the audit finding

concern. The inspector noted that PT/1/A/2200/001 contained

significantly more details for the inspection of the strainer,

including the installation of the bolting material.

The licensee's overall plan to enhance the Keowee procedures and

make them comparable to the Oconee maintenance procedures

ENCLOSURE

9

consisted of: (1) delete several Keowee specific procedures that

had duplicate Oconee procedures or (2) change the procedure(s) to

PTs, as discussed above. The new or revised procedures will

incorporate changes that enhance and address the SITA findings.

3.3.3 Review of Keowee Maintenance Procedures

The inspectors reviewed eight maintenance procedures to ascertain

compliance with FSAR and 10 CFR requirements. The procedures

reviewed are listed below. Those listed with an asterisk were

also reviewed by the SITA team inspection.

-

  • MP/1/A/2200/008, Unit 1 Hydraulic Turbine Inspection

-

  • MP/1/A/2200/017, Unit 1 Turbine, Governor, and Generator

Weekly Preventive Maintenance

-

  • MP/1/A/2200/001, Governor Number 1 Oil Pump Assemblies

Inspection and Maintenance

-

MP/2/2000/018, Unit 2 Turbine and Governor Monthly

Preventive Maintenance

-

TT/O/A/0620/012, Keowee Unit 2 Governor Oil System Test

-

OP/O/A/2000/027, Unit 1 Governor Actuator Pumping Units

-

MP/2/A/2200/001, Unit 2 Turbine, Governor, and Generator

Weekly Preventive Maintenance

-

MP/A/3019/004, Hangers, Pipe - Removal, Installation, or

Modification

-

MP/0/A/2005/001, Keowee Hydro Generator Inspection and

Maintenance

The inspector also reviewed vendor manual KM-200-0158-001, Allis

Chalmers Instruction Book and compared the vendor requirements

against the procedure requirements. The inspector found the

procedures reviewed contained sufficient guidance to permit the

maintenance/tests to be performed correctly. No significant

errors were noted.

3.3.4 Review of Maintenance and Preventive Maintenance Data

The inspectors reviewed the completed maintenance and preventive

maintenance (PM) data for ten activities performed within the last

year at Keowee. The components selected for the PM reviews were

safety related and included the Governor Oil System and Turbine

ENCLOSURE

10

Guide Bearing Oil System. The maintenance activity was for the

installation of a pipe support. The activities reviewed were:

-

Units 1 & 2, monthly test performed January 31, 1996, on the

Turbine Guide Bearing Oil System.

-

Units 1 & 2, annual test performed January 24, 1996, on Unit

1 and January 11, 1996, on Unit 2. This PM was implemented

on the Governor Oil System.

-

Unit 1, test performed February 22, 1995, for removal from

service and restoration to service of the Keowee Governor

Actuator Pumping System.

-

Unit 1, annual tests performed February 22 and October 23,

1995, for inspection and maintenance of governor number 1

oil pump assembly.

-,

Unit 2, annual tests performed February 14 and October 12,

1995, for the governor actuator oil pump.

-

Unit 2, installation of U-bolt was performed on April 25,

1995, using WO 95030111.

The inspector's evaluation found the maintenance activities were

implemented in accordance with the applicable procedure

requirements.

3.3.5 Quality Assurance Program for Repair of Copper Materials

Item 55 in the Keowee Upgrade Project consisted of creating a

safety-related procedure for the repair of copper instrumentation

lines at the Keowee Hydro Station. The licensee implemented a

soldering procedure for connecting or repairing copper lines.

This procedure (MP/0/A/1810/020, Soldering - Copper/Copper Alloys

- Tubing, Fitting, Valves) was issued November 4, 1995, and

provided instructions for repair and installation of soldered

socket type joints using the manual torch heating process.

The inspector reviewed this procedure and determined it describes

an adequate process for control of material and provides

acceptable instructions to achieve an adequate soldered joint on

copper materials. The inspector had no questions on the adequacy

of this procedure.

3.3.6 Heat Exchanger Testing Program

The inspector reviewed the licensee's heat exchanger testing

program for the Keowee Hydro Station. The licensee's original

response to Generic Letter 89-13 did not include the Keowee Hydro

ENCLOSURE

11

Station. To address the Keowee station, a procedure to obtain

trending data was generated and requires collecting data on a

monthly basis through continuous monitoring utilizing a data

acquisition program, regardless of Keowee unit operation. The

procedure (TT/O/A/0620/022, Keowee Heat Exchanger Performance Data

Test) was in the development stage and had not been reviewed or

approved by licensee management. However, the licensee performed

an evaluation to determine the adequacy of the cooling water

systems and documented that normal operating conditions bound

worst case design basis accident conditions. The configurations

of the systems were the same during normal and accident conditions

and flow indications were available and were procedurally

monitored on a periodic basis during unit operation.

3.3.7 Replacement of 13.8 kV Circuit Breakers

Keowee Upgrade Project, Item 21, involved the need for replacement

or refurbishment of the 13.8 kV, indoor, air-operated, generator

output breakers. The inspector interviewed the cognizant engineer

concerning the status of this item. He stated that the decision

was made to replace these circuit breakers with new breakers of

the same design. The reason for replacement was the age of the

breakers and number of operations as compared to the "Schedule of

Operating Endurance Capability for Circuit Breakers" in ANSI

C37.06-1987. Homewood Company, a subsidiary of Westinghouse

Electric Corporation, has the capability to manufacture the

breakers. The licensee's plan was to have Westinghouse, or

others, prepare the dedication/qualification package. The

schedule was to issue a request for bids by March 1, 1996. There

was a 40-week lead time for this equipment. The inspector agreed

that the replacement project should resolve the breaker wear out

issue for the long-term.

The above review of the maintenance/test program for the Keowee Hydro

Units indicated that the program met the regulatory requirements. The

licensee has met commitments to enhance the program as described in the

Keowee Upgrade Project.

In addition, the inspectors concluded that the SITA on the Keowee

maintenance program was comprehensive. The program was found to meet

the regulatory requirements and some good enhancements were identified.

The inspectors' review of the program had essentially the same finding

as the SITA. The licensee was committed to submitting to the NRC a

revised Inservice Test program, significantly enhanced with regard to

the Keowee Hydro Units. Therefore, Inspector Follow-up Item

269,270,287/95-26-02 is considered closed.

ENCLOSURE

  • I12

3.4

Maintenance Followup Items

3.4.1 (Closed) Inspector Follow-up Item, 95-26-03, Purpose and

Limitations of the List of SSCs in the Quality Standards Manual

During a previous inspection an inspector identified the fact that

four safety-related valves were not listed in the Quality

Standards Manual. The licensee initiated PIP 0-095-1687 in

response to this finding inorder to resolve the confusion among

the affected organizational groups concerning the purpose and

limitations of the list of structures, systems and components

provided in Appendix B of the Quality Standards Manual.

During this inspection, through interviews with engineering

personnel, the inspector determined that the list of SSCs in

Appendix B of the Quality Standards Manual was not intended to be

a complete list. The fact that a particular type of item appears

on the list does not imply that the list was intended to be

complete for safety-related items of the same type. Users of the

Quality Standards Manual determine safety classifications by use

of flow chart type instructions (referred to as a "road map").

The list provided supplementary information to the flow chart. To

address concerns that may arise from users of the manual

incorrectly assuming that the list of safety-related SSCs was

complete, the licensee issued a memorandum to all managers

clarifying the purpose and limitations of the list. The inspector

interviewed two managers who confirmed that the memorandum

accurately describes how the Quality Standards manual should be

used. In response to questions by the inspector, the corrective

actions in the PIP were modified to require an instructive

memorandum be issued to all users of the Quality Standards Manual

cautioning that the list of safety-related SSCs is not complete.

The licensee was working toward generating a comprehensive

Equipment Data Base, which will indicate the quality assurance

classification of all equipment having a unique identification

number. When the Equipment Data Base is approved for use, it will

become the preferred tool for determining quality assurance

classifications of equipment, and will effectively supersede the

list in the Quality Standards Manual.

The inspector reviewed the status of the licensee's Equipment Data

Base in order to determine the projected completion of this

project. Currently, the licensee has a two-year funded project to

make the Equipment Data Base match the Quality Standards Manual.

Once this is achieved, the list in the QSM will be removed. The

effort includes field inspection of equipment and a determination

regarding whether the equipment is safety-related. The Keowee

equipment was the first equipment scheduled to be entered into the

new data base. The data base will require validation with three

ENCLOSURE

(113

levels of signatures. Most of the Keowee equipment was entered on

the data base at the time of this inspection. However, it had not

received the required validation. The target for completing the

Keowee Station was in approximately one year. The inspector had

no further questions on this activity. Based on the above facts,

Inspector Followup Item 269,270,287/95-26-03 is closed.

3.4.2 (Closed) Inspector Followup Item 269,270,287/95-26-02, Replacement

of 13.8 kv Circuit Breakers

Closure of this item is addressed in paragraph 3.3.

3.4.3 (Closed) NRC Information Notice 92-51

The inspectors reviewed the licensee's actions to address the

concerns expressed in NRC Information Notice 92-51, Supplement 1,

Misapplication and Inadequate Testing of Molded-Case Circuit

Breakers. This notice was concerned with the setpoint for the

instantaneous trip element in molded-case circuit breakers. It

alerted addressees to the possible need for checking that breakers

would not trip as a result of motor starting transient current.

These checks may involve engineering evaluation and field testing.

In general, the licensee utilized thermal magnetic circuit

breakers in combination starters for motor circuits. In a limited

number of cases magnetic-only breakers were utilized. The

inspector reviewed the licensee's Engineering Criteria Manual,

Section RE-3.03, with regard to the setting of MCC breakers and

found that the criteria were adequate. To ensure that replacement

breakers actually performed close to published time/current

characteristics, the licensee performed time-delay (thermal) and

instantaneous (magnetic) overcurrent trip test on breakers upon

receipt at the warehouse. The test procedure was specified in

CGPA-3000.00-00-0013, General Electric Molded-Case Circuit

Breakers, Procurement and Acceptance Requirements. The inspector

observed that the test ensured breakers would be within the

specified range (i.e., upper and lower limit). In addition,

periodic testing not exceeding five years was being performed to

demonstrate continued correct performance. The periodic testing

was specified in:

-

Nuclear Station Directive: 401, Maintenance and Testing of

Class 1E AC and DC Molded-Case Circuit Breakers

-

Procedure IP/0/A/3011/013, Molded-Case Circuit Breaker Test

and Inspection

The inspector reviewed the breaker sizing and setting for 150/75

hp reactor building cooling fan motor and a 15 hp valve motor (PR

1) at the Keowee plant. The breaker for the fan motor was thermal

ENCLOSURE

(

14

magnetic type with adjustable magnetic setting, and the breaker

for the valve was fixed thermal magnetic type. The inspector

concluded that the settings would allow the motor to fulfill its

safety function considering minimum voltage running and maximum

voltage starting transient. The inspector concluded that the

concerns expressed in the information notice had been addressed by

the licensee.

3.4.4 (Closed) Apparent Violation (EEI) 269,270,287/96-02-01, Inadequate

Control Over Fuel Assembly Movement

On March 5, 1996, this Apparent Violation was cited under

Enforcement Action (EA)96-019 as a Severity Level III Violation

with proposed imposition of a $50,000 Civil Penalty. Accordingly,

EEI 269,270,287/96-02-01 is administratively closed and Violation

EA 96-019-01013, Inadequate Procedural Control Over Movement of

Fuel Assemblies in the Spent Fuel Pool, is being opened.

4.0

ENGINEERING (37550, 37551, 40500, 92700 and 92903)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

4.1

Low Pressure Service Water Pump Suction Requirements

The licensee discovered deficiencies in the calculated suction pressure

for the LPSW pumps when revising OSC-2280, LPSW NPSHA and Minimum

Required Lake Level.

The error in the calculation was that a minimum

flow rate of 10,000 gpm through the LPSW system was used as the basis

with an allowed pressure drop of 1.3 psid across the pump suction

strainer. The review of the calculation and operating parameters

revealed that the normal flow rate through the LPSW system could be as

low as 7,000 gpm during cold weather with the 1.3 psid across the

suction strainer and accident flow rates could reach approximately

15,000 gpm. An accident scenario where the CCW pumps would be

eliminated and at a time when the LPSW flow rates were at 7,000 gpm and

a strainer pressure drop of 1.3 psid, the pressure drop across the

strainer would increase significantly due to an increased LPSW flow of

approximately 8,000 gpm. At that point, there would be an inadequate

suction pressure for the LPSW Pumps to operate.

The licensee has revised their SLC, section 16.9.7, to maintain the

Keowee Lake level at 793 feet above sea level or to enter the action

statement when the level drops below that elevation. In addition, the

NLO surveillance requirements were changed to require the LPSW Pump

suction strainers to be backflushed when the pressure drop increases to

0.6 psid. The licensee has not completed past operability

ENCLOSURE

15

determinations. As a result, this item will be identified as URI

269,270,287/96-03-01, LPSW Suction Pressure Discrepancies.

4.2

Containment Hydrogen Control Systems (CHCS)

The Oconee CHCS as defined in TS 3.16.1 consists of a portable hydrogen

recombiner unit and a reactor building hydrogen purge system. Over the

years, the reactor building hydrogen purge system has not been

maintained in an operable status since TS 3.16.1 specifically states it

is not required to be operable when the hydrogen recombiner unit is

operable.

On February 1, 1996, at 1:30 p.m., Oconee entered a Limiting Condition

For Operability (LCO) per TS 3.16.3b due to the discovery that a

potential existed for condensate to collect in the common lines

associated with the hydrogen purge system and the hydrogen recombiner

for each Oconee unit. The condensate would inhibit flow to the

recombiner (as well as the already inoperable purge system), rendering

the CHCS inoperable. This condition existed on all three units since

initial construction of the system.

An accident scenario involving hydrogen gas buildup in the reactor

building would require processing by the Hydrogen Recombiner to avoid

reaching explosive limits. This condition would not occur until

approximately 15 days following the Design Basis LOCA. If the

containment atmosphere is not purged or the hydrogen is not removed, a

potentially explosive level of hydrogen could accumulate. An explosion

could breach containment. The inspectors agree with the licensee's

assessment that sufficient time would have been available to recognize

the problem with the hydrogen recombiner unit and take appropriate

actions to maintain containment integrity.

The deficiency was identified by the licensee's engineering personnel

during a review of the Hydrogen Control Systems to evaluate power

supplies to the areas designated for the portable hydrogen recombiner

unit. As a result, corrective actions were immediately started to

install a drain system in each unit to drain the loop seals in the

affected lines and return the condensation to the reactor building.

On February 6, 1996, the licensee requested an emergency TS amendment to

allow a one-time extension of the 7-day LCO for an additional 7 days.

The extension was granted on February 8, 1996, and allowed ample time to

complete the modification without shutting down all three Oconee units.

The modification was completed and LCOs were exited on February 10,

1996.

The system deficiency will be identified as an Apparent Violation, VIO

50-269,270,287/96-03-02, Inoperability of Containment Hydrogen Control

Systems.

ENCLOSURE

16

4.3

Electrical Fire in Logic Cabinet 1LC3 in Keowee Control Room,

IP/0/A/400/10

On February 16, 1996, While implementing IP/0/A/400/10, Controlling

Procedure for Troubleshooting and Corrective Maintenance at Keowee, an

electrical fire occurred in logic cabinet 1LC3 in the Keowee CR. The

licensee was troubleshooting why a DC power supply breaker tripped

unexpectedly while implementing NSM 52966 using TN/5/A/52966/BL1-07,

Modification of SK Breaker and Underground Control Circuit Logic. While

performing step fourteen of the IP, which was to close sliding link TB

18-29 in 1LC3, an electrical flash and fire began immediately. The fire

lasted approximately one minute. The licensee's immediate corrective

action was to extinguish the fire using a CO2 fire extinguisher and work

was stopped. The Unit 2 CR was notified and fire brigade members were

dispatched to the KHU where they confirmed that the fire was

extinguished. The licensee initiated PIP 0-096-0310 to resolve this

issue.

The licensee used the same IP for troubleshooting the cause of the fire.

The licensee determined that a Cutler-Hammer switch (light) Model number

10250T/91000T/E34 associated with ACB-3 indication had been incorrectly

wired on August 16, 1995, as part of TN/5/2966/BL1/01, Modification Of

Keowee Unit 1 & 2 Overspeed Protective Circuitry. The modification had

installed two switches to provide information as to which unit (ACB-3 or

ACB-4) was selected as the underground unit per TN/5/2966/BL1/01. The

licensee determined that both switches had been wired incorrectly in

August 1995. The two switches remained isolated since their

installation, due to the licensee backing out of the modification on

August 31, 1995. The incorrectly connected switch caused a short

circuit while the licensee was conducting the troubleshooting discussed

in the previous paragraph. The switch was connected according to the

drawing supplied in TN/5/2966/BL1/01. It was noted that a QC inspector

verified that the proper connections had been made. The connection

diagram for the new switch was not verified by the design engineer when

developing the modification. The engineer assumed that the vendor had

not made any changes, while in fact the vendor had upgraded the switch

and incorporated changes to the respective connection diagram. The

licensee is conducting a root cause evaluation as part of PIP 0-096-031

to ensure that appropriate corrective actions are put in place to

prevent this from recurring.

The licensee replaced the damaged terminal block in logic cabinet 1LC3.

On February 22, the licensee completed the replacement of the pretest

lights per TN/5/A/2966/BL1/10, Replacement of L141 Pretest Lights for

ACB-3 and ACB-4 Plant Support. The inspector observed portions of

TN/5/A/2966/BL1/10. No problems were identified.

ENCLOSURE

17

4.4

Spent Fuel Pool

An engineering inspection was performed on the spent fuel pool from

February 26 - March 1, 1996. The inspectors reviewed the plant

practices, procedures, calculations, and parameters associated with the

Spent Fuel Pool (SFP) and support systems to determine if these were

consistent with the description in the licensing basis as described in

the Final Safety Analysis Report (FSAR) and related Safety Evaluation

Report (SER).

Sections 9.1.2, 9.1.3, and 3.8.4 of the FSAR described

the SFP systems and structures. Amendments dated December 24, 1980, and

September 29, 1983, to the FSAR addressed SFP rerack modifications. The

interface of the SFP and the Safe Shutdown System (SSS) was addressed in

numerous NRC/Duke Power company correspondence between 1978 and 1983.

FSAR section 9.6.3.2 described the SFP incorporation as an SSS Reactor

Coolant Pump seal makeup source. Additionally, the inspectors reviewed

the potential for SFP draw down and applicability to Oconee Nuclear

station of the Millstone SFP issue.

4.4.1 SFP Licensing Basis Review

The SFP and support system configuration described in the FSAR was

verified by review of system drawings and field verification.

Licensee procedures, logs, and Technical Specifications were

reviewed to determine if FSAR referenced parameters and operating

conditions were consistent with the FSAR description. Critical

parameters reviewed included predicted decay heat loads, SFP bulk

water temperature, and SFP level.

In particular, the calculations

were reviewed to verify that the SFP decay heat loads specified in

the FSAR for various SFP loading configurations were evaluated and

the cooling system was adequately sized to maintain SFP

temperatures within the values specified for the corresponding

loading conditions. Licensee controls to assure the SFP loading

configurations did not exceed the evaluated conditions are

addressed below in sub-paragraph 4.4.3.

There are two SFPs at Oconee; a combined Unit 1 and 2 SFP and a

Unit 3 SFP. There are three trains of spent fuel cooling for each

SFP. There have been several rerack amendments approved for the

Oconee SFPs. The inspectors reviewed the amendments and

concentrated on the last of three rerack amendments to determine

the present heat loads in the SFPs. For the Unit 1 & 2 SFP

Cooling System, the design basis normal heat load assumes that

Units 1 and 2 are refueled consecutively and the rack positions

are filled with previous discharges, except for 118 spaces

reserved for a full core discharge. The design basis abnormal

heat load assumes that Unit 1 and 2 are refueled consecutively,

followed by a full core discharge after a short period of

operation. Similar normal and abnormal decay heat load

configurations were described for the Unit 3 SFP.

ENCLOSURE

18

The predicted maximum normal and abnormal heat loads for the Unit

1/2 SFP were 21.9 E6 BTU/hr and 34 E6 BTU/hr, respectively. For

the Unit 3 SFP, the respective heat loads were 12.6 E6 BTU/hr and

30.8 E6 BTU/hr. Calculation OSC-610,"Expanded Oconee 1 & 2 Heat

Load on the Spent Fuel Pool," Revision 1, analyzed the decay heat

loads for the normal and abnormal conditions and supported the

values specified in the FSAR. Calculation OSC-1765, Unit 3 Spent

Fuel Pool Heat Load, revision 0, analyzed the loading conditions

in the Unit 3 SFP. The following calculations analyzed the

cooling system capacity for each SFP and verified that the FSAR

Section 9.1.3.1.2 and FSAR Section 9.1.3.1.1 specified bulk water

temperature limits on the pools would be maintained:

OSC-616, Spent Fuel Temperature vs. Heat Load Calculation,

Revision 0

OSC-1835, Oconee Unit 3 Spent Fuel Cooling System Analysis,

Revision 0

The calculations indicated that the SFP cooling systems were

adequately designed to remove the decay heat generated from the

analyzed fuel loading and maintain pool bulk temperatures below

the design criteria referenced in the FSAR.

The inspectors reviewed graphs of the Recirculating Cooling Water

(RCW) temperatures from January 1, 1993, to December 31, 1995, for

all three units and determined that the temperatures had not

exceeded 90 F. RCW provided the heat sink for the SFP cooling

system. This is the design temperature for the RCW to the SFP

coolers. There were no tubes plugged on the coolers. The

inspectors reviewed the data sheets for the original spent fuel

coolers and the newer plate type coolers. The manufacturer's most

conservative mean temperature differences were used to calculate

heat load. The inspectors concluded that the normal and abnormal

heat load conditions for the Oconee SFPs had been analyzed and

that adequate cooling system capacity was available to maintain

the temperature limits specified in the licensing basis.

In addition to SFP decay heat load and temperature, SFP level was

a critical parameter referenced in the FSAR. FSAR Section

9.1.4.2.3 specified a minimum of 23.5 feet of water above the

spent fuel stored in the spent fuel racks. There was no minimum

SFP level referenced in the TS; however, administrative controls

allowed a level of two feet below the nominal SFP level at a site

elevation of 838 feet. The top of the racked fuel assemblies was

at the 816.5 foot elevation. This would result in a water

coverage of 21.5 feet which was not consistent with the FSAR

value. This discrepancy between the licensing basis and plant

procedures was previously identified as Deviation 50-269,270,

287/95-30-03 and corrective actions had been implemented.

ENCLOSURE

19

Licensee analysis determined that the level discrepancy would not

result in increased radiation levels in the SFP area.

The inspectors reviewed the operator logs to verify the monitored

parameters were consistent with FSAR referenced values. The

inspectors reviewed the non-licensed operator logs (NLO) for

February 18, 1996. OP/2/A/1102/20, Unit 2 Primary NLO Primary

Round Sheet, Enclosure 5.8, NLO Turnover Sheet; Enclosure 5.10,

Basement Round; and Enclosure 5.11, Round Sheet, were reviewed.

The round sheets specified a range for each parameter and the

operator verified the value was within the indicated range. An

explanation was required if the parameter was not within the

range. Enclosure 5.11 verified the spent fuel pumps on or off for

each individual pump. It also checked cooler flows within range.

The check sheet additionally addressed motor and pump bearing

temperatures and pump bearing oil level.

No actual temperature or

levels were recorded. The licensee indicated that important

parameters were trended by computer. Enclosure 5.11 checked the

SFP gas monitor operation and SFP water level at the skimmer

trough, which approximately corresponds to a level of 23.5 feet

above the fuel.

Additionally, SFP area cleanliness was checked.

SFP level and temperature indicators were in the control room.

Enclosure 13.1, Periodic Checks Schedule Sheet when RCS is Greater

than 200 degrees F., verified that the SFP water temperature is

less than 143 degrees F. The inspectors concluded that the logs

indicated that SFP parameters were maintained consistent with the

values specified in the FSAR.

The inspectors reviewed the parameters associated with the SFP

ventilation system. TS 3.8.12 requires the SFP ventilation system

to be operable whenever fuel movement is in progress. Section

9.4.2.1 of the FSAR states, "The ventilation system is designed to

maintain the SFP area at a maximum inside temperature of 104

degrees F and a minimum temperature of 60 degrees F."

The 104

degrees F temperature may have been exceeded during full core off

loads in the summer or autumn, but area temperature was not

monitored. However, the SFP water temperature had reached 110

degrees F on some occasions. Although unverified, this large heat

source could result in air temperatures greater than 104 degrees

F. The licensee initiated PIP 0-095-0389 to review this problem

and determined that the higher temperatures would not impact

safety-related equipment in the SFP area. The inspectors were

concerned that the higher temperature might have affected the

efficiency of the charcoal filters in the fuel handling building

ventilation system. The inspectors determined that no credit was

taken for the ventilation filter system in the spent fuel pool in

calculating releases during an accident.

ENCLOSURE

20

4.4.2 Potential SFP Draw Down

The Oconee SFP design provides two mechanisms for SFP draw down.

The High Pressure Injection (HPI) Pumps could provide Reactor

Coolant Pump (RCP) seal make up during a Tornado event and the

reactor make up pumps could provide RCP make up during a SSS

event. The SFP level decrease due to a Tornado event via the HPI

was physically limited to approximately 18.5 feet above the top of

the racked fuel assemblies due to a siphon break on the supply

line. The SSS interface could permit a draw down to approximately

six feet below the top of the fuel assembly if not limited by

administrative controls.

The SSS interface is located on the fuel transfer tube centerline

in the reactor building at approximately the 810 foot elevation.

This interface was provided by three-inch diameter seismically

qualified piping. The top of the racked fuel assembly was at the

816.5 foot elevation. The fuel transfer tube is a large diameter

tube which connects the SFP to the reactor building through which

the fuel assemblies are transported between these locations.

Although the transfer tube can be isolated, it is normally open to

the SFP to ensure availability of the SSS make up to the RCP

seals.

The inspectors noted that the SSS modification to the SFP deviated

from the Standard Review Plan (SRP) description of the SFPs.

Section 9.1.3 of the SRP stated that the SFP should be designed

such that the failure of inlets, outlets, piping or drains will

not result in inadvertent drainage below a point approximately ten

feet above the top of the active fuel in the SFP. The NRC

approved the SSS modification which included the interface.

However, it is not clear in the documented correspondence that the

NRC would have had the opportunity to identify this deviation from

the SRP design. The available Duke/NRC correspondence does not

include any specifics about the location of the interface tap or

relative elevations between the tap and the SFP fuel assemblies.

It is not clear whether the licensee provided adequate information

in their submittal for the NRC to identify this deviation from the

SRP design or that the SFP section of the SRP was addressed during

the SSS evaluation. Pending further NRC review, this matter is

identified as URI 269,270,287/96-03-03, Adequacy of Information

for SFP/SSF Interface.

The following references included pertinent information regarding

the process for acceptance of the Oconee SSS design which included

the RCP seal supply interface with the SFP:

a.

NRC letter to Duke Power, Mr. H. B. Tucker, dated April 28,

1983

b.

Duke letter to NRC, Mr. E. G. Case, dated, June 19, 1978

ENCLOSURE

21

c.

Duke letter to NRC, Mr. H. R. Denton, dated September 20,

1982

d.

Duke letter to NRC, Mr. H. R. Denton, dated March 28, 1980

In references (b) and (c) the licensee stated that the design of

the SSS would not specifically apply all sections of the SRP.

Reference (d) stated that the SSS provided for SFP draw down to

one foot above the fuel racks. Reference (a) included the NRC

approval of the licensee's SSS submittal and program.

The inspectors reviewed barriers which would reduce the potential

for SFP draw down. The licensee's submittal (reference d. above)

indicated that the analyzed 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> SSS event duration would

result in a SFP level of one foot above the racked fuel

assemblies, assuming no operator actions. The subsequent SFP area

radiation levels and refill capability were not addressed and this

was the issue of URI 269,270,287/94-31-06, which is discussed in

sub-paragraph 4.7.1 of this report. Barriers were provided by

administrative controls, level monitoring, alarms, and seismic

qualification of the system. The emergency procedures which

activate the SSS facility required the SFP level be monitored

after the RCP seal supply was initiated. The refill procedure was

referenced and actions to align the refill source initiated early

)

in the SSS activation procedure. A mechanism for level monitoring

via the RCM pump suction pressure parameter is provided in the

procedure if operator access to the SFP is restricted. Level

alarms near the normal operating levels would alert operators to

an unplanned level decrease. The RCM supply piping from the

SFP/fuel transfer tube was seismically qualified for the Safe

Shutdown Earthquake.

A manual isolation valve was provided for

isolation of the fuel transfer tube. Two motor operated isolation

valves were provided downstream of the RCM pump suction. These

were normally closed. The inspectors concluded that multiple

barriers were now available to prevent inadvertent draw down of

the SFP via the SSS interface.

4.4.3 Millstone Issue - SFP Loading Condition Not Evaluated

The inspectors reviewed the SFP loading conditions evaluated by

the predicted decay heat load analyses referenced in paragraph

4.4.1 of this report. SFP loading considerations included heat

loads and criticality. The heat load analyses assumed a minimum

of 168 hours0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br /> cool down prior to transfer of fuel assemblies from

the reactor to the SFP. FSAR sections 9.1.3.1.1 and 9.1.3.1.2

assume minimum cool down of 168 hours0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br /> and 6 days (144 hours0.00167 days <br />0.04 hours <br />2.380952e-4 weeks <br />5.4792e-5 months <br />) cool

down, respectively. Section 3.8.11 of the TS restricts fuel

movement from the core to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> after the reactor is

subcritical. Procedure OP/0/A/1502/07, Operations Defueling/

Refueling Responsibilities, dated November 11, 1995, specified

ENCLOSURE

22

that irradiated fuel shall not be removed from the reactor core to

the SFP until the reactor has been subcritical seven days (168

hours). This administrative control assures that the 168-hour

assumption in the heat load analyses was valid.

Nuclear Engineering's routine outage task list required Nuclear

Engineering to review planned SFP loading for refueling and verify

that the calculated decay heat loads were bounded by the FSAR

specified heat loads and the following heat load calculations:

OSC-4776, Unit 3 SFP, Revision 1

OSC-4998, Units 1&2 SFP Heat-up Rate, Revision 5

OSC-5928, SFP Decay Heat Load Projections for Future

Equilibrium Core Designs, Revision 0

Decay heat loads for fuel assemblies were calculated in accordance

with NRC Branch Technical Position ASB 9-2, Residual Decay Energy

for Light Water Reactors for Long Term Cooling. PIP 0-096-0362,

dated February 20, 1996, included a corrective action to include

the routine SFP heat load review practice as an operations

procedure requirement.

Normal and abnormal decay heat loads define specific loading

conditions for evaluation that supported sizing of cooling systems

and SFP bulk water temperature criteria. The significant

difference being that the abnormal heat load included a full core

off load rather a one third core off load. Oconee has routinely

performed a full core off load during refueling outages since

1982. This condition is not prohibited by the licensing basis.

SFP loading configuration based on criticality analysis was

specified by TS 3.8.16 and implemented by procedure

PT/0/A/0750/12, Development of Fuel Movement Instructions, dated

February 22, 1996. Procedure OP/0/A/1503/09, Documentation of

Fuel Assemblies and/or Component Shuffle Within a SFP, dated

February 22, 1996 also implemented SFP configuration controls.

4.4.4 Self-Assessment

The inspectors reviewed the licensee's self-assessment in this

area. A team of engineering and licensing personnel were

assembled in the week prior to the inspection to review the SFP

design and licensing basis compliance. The team concluded that

Oconee was in compliance with the SFP design and licensing basis.

Several PIPs were initiated to address areas for improvement

identified by the self-assessment team. PIP 0-096-0362 dated

February 20, 1996, identified discrepancies with the SFP heat load

calculations. Included in these were that the FSAR heat load

ENCLOSURE

ll

23

values will be exceeded when the higher enrichment fuel is

transferred to the SFP in future off loads. Although the normal

and abnormal predicted heat loads will be higher, they will still

be within the capacity of the cooling system. PIP 0-096-0389

dated February 26, 1996, identified that ventilation system design

documentation did not support the area design temperature range of

60 - 104 degrees F referenced in the FSAR and that the temperature

may have been exceeded. The NRC is in the process of reviewing

the consistency between the FSAR descriptions and the licensee's

policy, procedures, and practices.

4.5

Keowee Voltage Regulator Problem

On February 27, 1996, the licensee made a 10 CFR 50.72 notification to

the NRC concerning a postulated failure which could drive the Keowee

voltage regulator to its lower limit and result in inadequate voltage

being supplied to some low voltage (208V) motor operated valves during a

LOOP/LOCA scenario. The licensee's current analysis does not support

operability of the underground path with this failure. The licensee

entered an LCO for the underground path. The licensee determined that

this failure does not relate to the overhead path, since existing

undervoltage relays on the 27E breaker will detect these degraded

voltages, and transfer loads to the underground.

On February 27, 1996, the licensee performed TT/0/A/620/24, Keowee

Voltage Regulator Voltage Adjust Low Setpoint, on Keowee Unit 1 to

check and adjust the Keowee regulator voltage adjust low setpoint value.

The Keowee Unit 1 low setpoint value was determined to be 11.9 KV, but

was then adjusted to 13.5 KV. The licensee's calculation OSC-5952,

Oconee-Keowee Underground Path Analysis Using CYME, documents the

operability of the underground path with a Keowee generator voltage of

13.5 KV. The licensee then exited the LCO for the Keowee underground

path. The licensee determined that Keowee Unit 2 which was lined-up to

the overhead was in an operable, but degraded condition until the low

voltage setpoint on its voltage regulator was checked and set. On March

1, 1996, the licensee performed TT/0/A/620/25, Keowee Unit 2 Voltage

Regulator Voltage Adjust Lower Setpoint, to check and adjust the Unit 2

Keowee regulator voltage lower setpoint value. The Keowee Unit 2

voltage regulator low setpoint value was 12.7 KV, but was subsequently

adjusted to 13.5 KV. The licensee continues to determine the past

operability of the low voltage motor operated valves. The inspector

will continue to follow this issue.

4.6

Failure of 1HP-276

The licensee reported to the NRC on February 19, 1996, that an Appendix

"R" fire could cause the spurious opening of valve 1HP-276 (RCP Seal

Leakoff), resulting in the Unit 1 RCS leakage rate being greater than

what was assumed in previous calculations. Since the Unit 1 SSF makeup

pump supply to the RCS through the RCP seals is marginal, the excess

ENCLOSURE

24

leakage could result in exceeding the available pump capacity. An

inadequate flow to the RCP seals could prevent RCS natural circulation,

thereby preventing decay heat removal during an Appendix "R" accident

scenario.

As indicated above, this normally closed valve is a leakoff for the

number 1 seal on the Unit 1 RCPs. When opened, it allows makeup flow to

by-pass the number 2 and 3 seals, reducing backpressure and resulting in

an increased flow that would exceed the capacity of the makeup pumps.

Corrective actions to eliminate a spurious opening of this valve

involved ensuring that the valve was closed and then opening the power

supply breaker to the valve motor.

Although engineering personnel identified the deficiency on February 2,

1996, it was not reported until February 19, 1996. The failure to meet

the 4-hour reporting requirement of 10 CFR 50.72 resulted in additional

training for the engineers. The licensee is taking actions to ensure

that reporting is accomplished in the required timeframes. This issue

of reporting requirements will be examined further during the corrective

action followup of related Violation 50-269,270,287/95-27-01.

Further

evaluations and long-term corrective actions will also be reviewed

during a closure of the licensee's LER.

4.7

Engineering Followup Items

4.7.1 (Closed) URI 50-269,270,287/94-31-06, High SFP Radiation Levels

This issue addressed the potential high radiation levels in the

SFP area resulting from the draw down of the SFP during an SSS

event.

The licensee had not evaluated the SFP radiation levels

due to loss of shielding if the level was reduced to one foot

above the racked fuel assemblies as assumed in the SSS analysis.

Additionally, the mechanism for refill of the SFP had not been

addressed by procedures. The licensee's letter to the NRC dated

March 9, 1995, specified actions to address these concerns. The

action items included a modification to provide a remote refill

capability, calculations to evaluate radiation levels and quantify

time allowances for refill', and procedures to provide guidance for

the refill activity.

The radiation level analysis was documented in PIP 0-096-0345,

dated February 16, 1996, and determined dose rates at various pool

levels. The maximum dose rate, one foot above the racks, was

50,000 R/hr. The 2,000,000 R/hr value referenced in NRC Report

50-269,270,287/94-31 was a very rough approximation which was not

supported by a detailed calculation. The refill methodology was

proceduralized in MP/O/A/3009/012A, Emergency Plan for Refilling

Spent Fuel Pools, dated December 21, 1995. This methodology

required support from local fire departments to provide at least

two fire trucks to pump water from the lake via a filter unit to

ENCLOSURE

25

the SFPs. The procedure stated that the refill pumping system

should be available 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> after initiation of SSS RC make up.

Calculation OSC-619, Analysis for Use of SFP Inventory for SSS,

Revision 9, determined that SFP level would be lowered to one foot

above the racked fuel assemblies in 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Agreements with the

local fire stations and filter unit suppliers had been negotiated.

The limiting factor was the time allowance of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for the

filter unit delivery. The licensee was attempting to acquire the

filter unit for storage in the SSS facility.

Calculation OSC-6051, Verification of Alternate Method Used to

Fill SFPs Following Operation of SSF RC Make Up System, Revision

1, analyzed the capabilities for the make up source and developed

a method of monitoring SFP level via RCM pump suction pressure.

The inspectors field verified the modification which allowed

remote refill of the Unit 1/2 SFP. Installation of a remote fill

system for the Unit 3 SFP is scheduled for latter this year. The

inspectors concluded the licensee had completed the committed

corrective actions and adequately resolved this issue.

4.7.2 (Open) Violation 270/94-08-02, Inoperability of 2A Emergency

Feedwater Pump

On December 29, 1993, the licensee discovered water leaking from

pressure switch 2PS0386. This switch monitors the discharge

pressure of the 2A Main Feedwater Pump and sends a signal to start

the 2A Motor Driven Emergency Feedwater (MDEFW) Pump on low

discharge pressure of the main feedwater pump. During the switch

replacement, the electrical leads were lifted which resulted in

the elimination of a Unit 2 direct current (DC) ground that had

existed since December 14, 1993. The licensee's failure to take

aggressive action to locate and correct the ground on the DC

electrical system resulted in the prolonged condition. The issue

of allowing DC grounds to exist without performing an extensive

effort to find and eliminate the problem had previously been

identified by the NRC as a weakness and documented in NRC

Inspection Report 50-269,270,287/93-26.

An operability assessment completed on February 8, 1994,

determined that grounded pressure switch 2PS0386 had caused the 2A

MDEFW Pump to be inoperable from December 14-30, 1993. The time

that the emergency feedwater pump was considered inoperable

exceeded the seven days allowed by TS 3.4.2.a. Failure to meet

the requirement specified by the TS was identified as Violation

50-270/94-08-02. As a result of exceeding the TS limit, the

licensee submitted an LER (270/94-01) on March 10, 1994.

Corrective actions included replacing the subject pressure

switches on all three units. Additionally, the licensee developed

a report entitled "125 VDC Vital Instrumentation and Control

ENCLOSURE

ll

26

System Ground Detection, Location, and System Operation Design

Study," dated February 1, 1995. This report made recommendations

to resolve the ground issue. These recommendations included

installing ground detection equipment with the required

sensitivity, acquiring portable ground locating equipment with the

desired accuracy, and implementing proposed comprehensive alarm

response procedures. Accordingly, Violations 270/94-08-02 is

considered closed.

NRC Inspection Report 269,270,287/95-14 reviewed the ground issue

at Oconee. In this report the inspector reviewed the ground

design study and concluded that the implementation of the

recommendations would constitute acceptable corrective action to

resolve this issue in the long-term. At the time of Inspection

Report 95-14, the recommendations in the design study were still

under review by licensee management. As of the end January 1996

most of the recommendations were implemented. Ground alarm

response procedures were incorporated into the licensee's FSAR

Chapter 16, Selected Licensee Commitments (SLC 16.8.5) on January

4, 1996, and portable ground locating equipment had been

purchased. New ground detection equipment with improved ability

to detect higher resistance grounds (5000 ohms versus 500 ohms for

the existing equipment) had been purchased and was onsite but was

not scheduled to be installed until 1998 (NSM 3004). The

inspector questioned the proposed implementation date of 1998.

The licensee stated that NSM 3004 was deferred until the 1998 time

frame due to the cost of implementation. The inspector concluded

that the licensee had adequate provisions in place to respond to

ground alarms. However, the inspector remained concerned that due

to the currently installed ground detector's threshold for

detecting a ground (500 ohms or less resistance to ground) the

Vital DC System could be severely degraded without actuating the

alarm. Therefore, implementation will be followed under IFI

269,270,287/96-03-04, Installation of New Ground Detection

Equipment.

4.7.3 (Closed) LER 270/94-01, Technical Specification Limit Exceeded Due

To Equipment Failure

This event and associated issues are captured in Violation

269,270,287/94-08-02 which is addressed in sub-paragraph 4.7.2

above. Accordingly, this LER is closed.

5.0

PLANT SUPPORT (71750)

The inspectors assessed selected activities of licensee programs to

ensure conformance with facility policies and regulatory requirements.

During the inspection period, the areas of Radiological Controls,

Physical security and Fire Protection were reviewed.

ENCLOSURE

27

5.1

Liquid Waste Spill, CP/O/B/5200/54

On February 16, 1996, a technician noted that the flow totalizer was

steadily decreasing when transferring from recirculating liquid waste

(LW) to processing the LW. Due to this abnormal indication, the

technician shutdown the "A" LW feed pump. While evaluating the

situation, the technician identified a spill in Room 227. The

technician notified the CR and RP. At the time of the incident the

licensee approximated the spill to equate to 150 gallons. The

technician entered Room 227 and identified that a backflush hose

installed per a temporary modification had blown off. With RP approval,

the technician reconnected the hose. The licensee determined that the

hose failure was due to the use of the wrong size hose clamp. The

technician called another technician for support in evaluating the

situation. The two technicians identified another leak in the "D"

demineralizer manway. The licensee determined that this leak came from

a gasket that was incorrectly installed in the manway. The licensee

initiated a root cause evaluation per PIP 4-096-0314 to determine the

actual cause of the problem. The resident will continue to follow this

issue for final resolution.

Within the areas reviewed, no violations or deviations were identified.

6.0

REVIEW OF FSAR COMMITMENTS

A recent discovery of a licensee operating their facility in a manner

contrary to the FSAR description highlighted the need for special

focused review that compares plant practices, procedures and/or

parameters to the FSAR description. While performing the inspections

which are discussed in this report, the inspectors reviewed the

applicable portions of the FSAR that related to the areas inspected.

The following inconsistencies were noted between the FSAR and the plant

practices, procedures, and parameters observed by the inspectors:

FSAR 9.1.4.2.3 stated that water level over the fuel assemblies is

maintained at a minimum 23.5 feet. Plant procedures specify the

minimum water level at minus two feet from the 840 foot elevation

which would result in 21.5 feet of water above the fuel racks.

NRC deviation 50-269,270,287/95-30-03 identified this item.

SER Amendment 90, 90, 87 stated that if SFP water temperature was

initially 125 degrees F, boiling would occur greater than 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />

after loss of SFP cooling. Calculation OSC-4998 for Unit 1/2 Heat

Up Rate, determined that the actual time to boil could occur in

less than 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> for higher heat loads.

SER Amendment 90, 90, 87 stated that the required make up rate

will be less than 70 gpm for Unit 1/2 SFP. This addressed water

loss due to boil off only and did not account for the 29 gpm RCP

ENCLOSURE

28

seal supply. The combination would exceed the 70 gpm value. This was

not a concern since the refill capacity exceeded 150 gpm.

SER Amendment No. 123, 123, 120 stated that the time of 15 and 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />

for Unit 3 SFP boiling in the normal and abnormal heat load conditions

respectively, was sufficient to provided emergency SFP make up.

The

procedure MP/0/A/3009/012A, Emergency Plan for Refilling SFPs, dated

December 21, 1995, specified 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> for completion of the pumping

system for SFP refill and 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> as the upper limit to begin pumping

to the pool.

SER Amendment No. 90, 90, 87 references maximum normal and abnormal

predicted heat loads, values which will not be accurate when the higher

enrichment fuel assemblies are transferred to the SFP in future

refueling outages.

The inspectors concluded that discrepancies existed in the SER, but they did

not constitute Deviations. A Deviation from FSAR requirements was identified

is Paragraph 4.4.1 of this report.

7.0

EXIT

The inspection scope and findings were summarized on March 14, 1996, by P.

Harmon with those persons indicated by an asterisk in paragraph 1. Interim

exits were conducted on February 16, 1996, and February 29, 1996. The

inspector described the areas inspected and discussed in detail the inspection

results. A listing of inspection findings is provided. Proprietary

information is not contained in this report. Dissenting comments were not

received from the licensee.

Item Number

Status

Description and Reference

EEI 269,270,287/96-03-02

Open

Apparent VIO: Inoperability of

Containment Hydrogen Control Systems

(paragraph 4.2)

URI 269,270,287/96-03-01

Open

LPSW Suction Pressure Discrepancies

(paragraph 4.1)

URI 269,270,287/96-03-03

Open

Adequacy of Information for SFP/SSF

Interface (paragraph 4.3.4)

IFI 269,270,287/96-03-04

Open

Installation of New Ground Detection

Equipment (paragraph 4.7.2)

IFI 269,270,287/95-26-02

Closed

Review Test Program for Mechanical

Components at Keowee to Resolve

EDSFI Finding 6.b (paragraph 3.3)

ENCLOSURE

29

IFI 269,270,287/95-26-03

Closed

Purpose and Limitations of the

List of SSCs in the Quality

Standards Manual (paragraph

3.4.1)

URI 269,270,287/94-31-06

Closed

High SFP Radiation Levels

(paragraph 4.7.1)

VIO 270/94-08-02

Closed

Inoperability of 2A Emergency

Feedwater Pump (paragraph

4.7.2)

LER 270/94-01

Closed

Technical Specification Limit

Exceeded Due to Equipment

Failure (paragraph 4.7.3)

EEI 269,270,287/96-02-01

Closed

Apparent VIO: Inadequate

Control Over Fuel Assembly

Movement (paragraph 3.4.4)

VIO EA 96-019-01013

Open

Inadequate Procedural Control

Over Movement of Fuel

Assemblies in the Spent Fuel

Pool (paragraph 3.4.4)

8.0

ACRONYMS

ACB

Air Circuit Breaker

ALARA

As Low As Reasonably Achievable

BHUT

Bleed Holdup Tank

BTO

Block Tagout

BWST

Borated Water Storage Tank

CFR

Code of Federal Regulations

CC

Component Cooling

CCW

Condenser Circulating Water

CR

Control Room

DBA

Design Basis Accident

DC

Direct Current

EEI

Apparent Violation

EFW

Emergency Feedwater

EPSL

Emergency Power Switching Logic

EOC

End Of Cycle

ES

Engineered Safeguards

E6 BTU/hr

1 million British Thermal Units per hour

FW

Feedwater

FWPT

Feedwater Pump Turbine

FSAR

Final Safety Analysis Report

GL

Generic Letter

GPM

Gallons Per Minute

HP

Health Physics

ENCLOSURE

I

30

HPI

High Pressure Injection

ICS

Integrated Control System

IFI

Inspector Followup Item

I&E

Instrument & Electrical

IR

Inspection Report

KHU

Keowee Hydro Unit

LDST

Letdown Storage Tank

LER

Licensee Event Report

LCO

Limiting Condition for Operation

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

MDEFW

Motor Driven Emergency Feedwater

MP

Maintenance Procedure

MVA

Mega Volts-Amps

MW

Megawatts

NCV

Non-Cited Violation

NLO

Non-Licensed Operator

NPSHA

Net Positive Suction Head Absolute

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

OATC

Operator At The Controls

ONS

Oconee Nuclear Station

OEP

Operating Experience Program

PSID

Pounds Per Square Inch Differential

PSIG

Pounds Per Square Inch Gauge

PM

Preventive Maintenance

PIP

Problem Investigation Process

QA

Quality Assurance

QC

Quality Control

QSM

Quality Standards Manual

RC

Reactor Coolant

RCM

Reactor Make-up

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RCW

Recirculating Cooling Water

REM

Roentgen Equivalent Man

RFO

Refueling Outage

R/hr

Roentgen per hour

RP

Radiation Protection

RPS

Reactor Protection System

RFO

Refueling Outage

SER

Safety Evaluation Report

SFP

Spent Fuel Pool

SLC

Selected Licensee Commitments

SOER

Significant Operating Event Report

SRP

Standard Review Plan

SSC

Systems, Structures and Components

SSF

Standby Shutdown Facility

ENCLOSURE

31

SSS

Safe Shutdown System

TS

Technical Specification

URI

Unresolved Item

VDC

Volts Direct Current

VIO

Violation

WCC

Work Control Center

WO

Work Order

ENCLOSURE