ML15118A120

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Insp Repts 50-269/96-04,50-270/96-04 & 50-287/96-04 on 960310-0420.Violations Noted.Major Areas Inspected:Plant Operations,Maintenance & Surveillance Testing,Engineering, & Plant Support
ML15118A120
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 05/20/1996
From: Crlenjak R, Harmon P
NRC (Affiliation Not Assigned)
To:
Shared Package
ML15118A117 List:
References
50-269-96-04, 50-269-96-4, 50-270-96-04, 50-270-96-4, 50-287-96-04, 50-287-96-4, NUDOCS 9606120069
Download: ML15118A120 (43)


See also: IR 05000269/1996004

Text

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UNITED STATES

0

NUCLEAR REGULATORY COMMISSION

REGION II

0

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/96-04, 50-270/96-04 and 50-287/96-04

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.: 50-269, 50-270 and 50-287

License Nos.:

DPR-38, DPR-47 and DPR-55

Facility Name: Oconee Units 1, 2 and 3

Inspection Conducted: March 10, 1996 - April 20, 1996

Inspectors:

N<KOf

Inspectors

'e"o

ispecC6r

ieS~e

P. E. Harmon, Senior Reside

igned

J. L Coley, Reactor Inspec r

N. Economos, Reactor Inspector

D. B Forbes, Reactor Inspector

P. G. Humphrey, Resident Inspector

D. W. Jones, Reactor Inspector

L. P. King, Reactor Inspector

R. L..Moore, Reactor Inspector

N. L. Sa

o, Resident Inspector

J. W.

r

/, cto

tor

Approved by:

R. .

rlenja , Branch C ef

Dite

igned

Division of Reactor Proj cts

SUMMARY

Scope:

Inspections were conducted by the resident and/or regional inspectors in the

areas of plant operations, maintenance and surveillance testing, engineering,

and plant support.

Results:

Plant Operations

During a rod exercise test, a control rod did not fully insert when

dropped from 10% withdrawn, paragraph 2.3. Two valves left partially

open allowed RCS water from the decay heat mode lineup to be diverted to

the Borated Water Storage Tank, paragraph 2.4.

ENCLOSURE 2

9606120069 960520

PDR

ADOCK 05000269

GPDR

2

Maintenance

Fuel handling personnel damaged a new fuel assembly during equipment

checkout. Weaknesses in the licensee's procedure were identified,

paragraph 3.1.6. A 4160 volt breaker failed during testing due to

hardened grease in the breaker closing mechanism, paragraph 3.1.7.

Required testing of charcoal filters had not been performed as required

by TS, paragraph 3.2.4. An Unresolved Item was identified regarding the

licensee's resolution of recurring failures to a Main Steam valve and a

Low Pressure Service Water cooler outlet valve, paragraphs 3.3.2 and

3.3.3. A Non-Cited Violation was documented for deficiencies in the

procedure for adjusting chevron type valve packing, paragraph 3.3.5.

Engineering

One Violation was identified for failure to follow procedure for drawing

control, paragraph 4.3. One Unresolved Item was identified concerning

the operability of the SSF, Paragraph 4.1. The engineering self

assessment was effective in identifying strengths and problems in the

engineering area. Both the PORC and the NSRB oversight committees

functioned effectively in evaluating engineering activities. A sample

review of Nuclear Safety Modifications at Oconee identified no

programmatic problems. The safety evaluation program(10 CFR 50.59) was

being performed in an adequate manner, paragraph 4.2. The accuracy of

Keowee low voltage electrical drawings had improved following licensee

actions to correct errors identified in 1995, paragraph 4.3.

Although an example was identified in which a Vital-to-Operations

designated drawing was not updated, drawing distribution control was

generally good. Operability evaluations were adequately supported and

management review of operability evaluations was appropriately

challenging, paragraph 4.4.

Plant Support

Radiation Protection personnel performing a routine survey found a

slightly contaminated thermocouple in the scrap metal dumpster being

used for outage trash disposal, paragraph 3.1.4. The licensee's

Radiation Protection program was effectively implemented. The licensee

continued to improve upon ALARA initiatives, particularly in the

reduction of outage doses. The program to control liquid and gaseous

radioactive effluents was effective. The projected offsite doses from

those effluents were well within limits. The annual total body dose

estimate to the maximum exposed member of the public, calculated from

the 1995 environmental sampling results, was less than one quarter of a

mrem, paragraph 5.0.

6

ENCLOSURE 2

REPORT DETAILS

Acronyms used in this report are defined in paragraph 9.0.

1.

Persons Contacted

Licensee Employees

D. Berkshire, Senior Scientist, Radiation Protection

R. Bond, Director, Work Process

S. Bryant, Internal Assessment, Radiation Protection

  • M. Bailey, Regulatory Compliance

S. Capps, Project Management

T. Coleman, Technical Specialist, Inservice Inspection

T. Coutu, Operations Support Manager

D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

R. Dobson, Modifications Manager

  • W. Foster, Safety Ass urance Manager

J. Hampton, Vice President, Oconee Nuclear Station

  • G. Hamrick, Manager, Chemistry

D. Hubbard, Maintenance Superintendent

B. Jones, Manager, Training

C. Little, Electrical Systems/Equipment Manager

B. Millsaps, Mechanical/Civil Equipment Engineering Manager

  • D. Nix, Engineer, Regulatory Compliance

B. Norris, -Supervisor, Chemistry

B. Peele, Station Manager

G. Rothenberger, Operations Superintendent

J; Twiggs, Manager, Radiation Protection

B

J. Smith, Regulatory Compliance

P. Street, Supervisor Mechanical Engineering

R. Sweigart, Work Control Superintendent

" Attended exit interview.

Other licensee employees contacted included office, operations,

engineering,'maintenance, chemistry/radiation, technicians, craftsmen,

and corporate personnel.

2.0

PLANT OPERATIONS (71707 and 92901)

The inspectors reviewed plantoperations throughout the reporting period

to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls. Control room logs,

shift turnover records, temporary modification log, and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted on day and night shifts, during

weekdays and on weekends.

Inspectors attended some shift changes to

evaluate shift turnover performance. Actions observed were conducted as

required by the licensee's Administrative Procedures.

The complement of

2

licensed personnel on each shift inspected met or exceeded the

requirements of TS.

Operators were responsive to plant annunciator

alarms and were cognizant of plant conditions.

Plant tours were taken throughout the reporting period on a routine

basis.

During the plant tours, ongoing activities, housekeeping,

security, equipment status, and radiation control practices were

observed.

2.1

Plant Status

Unit 1 operated at or near full power throughout the reporting period.

Unit 2 operated at full power until March 28, 1996, when the unit began

shutting down for a scheduled 33-day End-Of-Cycle 15 Refueling Outage.

The outage schedule was extended until May 10, 1996, to incorporate

additional steam generator (SG) tube plugging.

Unit 3 operated at full power until March 16, 1996, when the unit

tripped during the performance of PT/O/A/0610/22, Degraded Grid

Switchyard Isolation, and Keowee Overfrequency Protection Functional

Test as documented in NRC Inspection Report 269,270,287/96-05. The unit

was returned to full power operation on March 26, 1996, and remained at

full power throughout the rest of the inspection period.

2.2

Mid-loop/Reduced Inventory Activities

During the Unit 2 End-Of-Cycle 15 Refueling Outage, the licensee reduced

RCS Inventory and reached the mid-loop operations level on April 1,

1996. This was done for the purpose of installing nozzle dams in the

steam generators. The inspectors reviewed the licensee's program prior

to the reduction of RCS inventory and verified that the requirements

were met while operating at the reduced inventory levels as specified in

procedure OP/1/A/1103/11, Draining and Nitrogen Purging of RCS,

Enclosure 3.6, Requirements for Reducing Reactor Vessel Level to < 50"

on LT-5. This procedure stipulated the sequence and steps required for

reduction of RCS inventory and mid-loop operation. It further specified

the precautions and limitations to be adhered to while in mid-loop.

The inspector verified that the requirement for two independent trains

of RCS level monitoring was met while at reduced inventory. This was

accomplished by use of two permanently installed instruments (LT-5A and

LT-5B) and two temporary ultrasonic instruments. Level indications were

displayed in the CR on the LT-5A and LT-5B indicators, the Inadequate

Core Cooling Monitor, and on the Operator Aid Computer.

The inspector verified that two trains of core exit thermocouples were

available and utilized while at reduced inventory, as well as that two

sources of inventory makeup and cooling were available for operation.

Multiple sources of offsite power were also available. The inspector

ENCLOSURE 2

3

reviewed the licensee's contingency plans to repower vital busses from

available alternate electrical power supplies in the event of the loss

of the primary source.

Unit 2 was in reduced inventory status for approximately 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />.

During that time, the licensee implemented and maintained the

requirements specified by procedure while accomplishing reduced

inventory operations without incident. The inspector concluded that

this reduced inventory evolution was well coordinated and controlled.

2.3

Reactor Manual Trip Test, PT/0/A/305/01, and Control Rod Drive Trip Time

Testing, PT/0/A/0300/01.

The inspector reviewed documentation from the Unit 3 reactor manual trip

test that was performed on March 24, 1996, to verify CRDM operability

prior to unit restart. Control rod drive groups, 1 through 7, were

individually withdrawn to 10 percent and tripped. Control rod drive

breakers were verified to open upon pressing the reactor manual trip

pushbutton. Although the test was to verify that the control rod drive

breakers opened, a problem was experienced in that control rod #9 in

group 5 indicated that it remained at 7 percent withdrawn and all other

rods within the group indicated fully inserted at 0 percent withdrawn.

Operators took immediate actions to verify that an adequate shutdown

margin existed and to get plant management involved to resolve the

problem. The exact cause of the rod indication problem was not

determined. However, it was the general consensus that the rod drop

inertia was very low because of dropping the rod from only 10 percent

out of the core and being in the hydraulic damper region of the rod drop

area. This hydraulic area is designed to slow drop speed to prevent rod

damage.

A PORC meeting reviewed the problem and made the decision to perform

PT/0/A/0300/01, Control Rod Trip Time Testing, which involved pulling

the rods, one group at a time, to the full-out position, trip the group,

and record the time required for the rods to drop into the core. Each

group, 1 thru 7, were tested and all rods fell into the core within

acceptable time limits.

Problem Investigation Process, 3-096-0594, was generated to document and

track the issue for further evaluation and long-term corrective actions.

This issue is addressed further in paragraph 3.2.2, Reactor Manual Trip

Test.

2.4

LPI Valve Leakage

During the Unit 3 trip and cooldown on March 16 and 17, the LDST level

began decreasing when the LPI system was valved in to place the unit in

the decay heat removal mode. The licensee investigated and determined

that two manual valves, LP 40 and LP 41 were partially open and leaking

ENCLOSURE 2

4

by their seats. The valves are in the LPI recirculation back to the

BWST and are normally shut. One valve was open 3/4 turn and the

otherwas open 1 turn. The leakage through the valves back to the BWST

was approximately 10 gpm. The valves are located in a difficult

position for manual operation, and the licensee concluded they were

inadvertently left partially open the last time they were operated.

The licensee has imposed a limit of 5 gpm total leakage from the sump

recirculation flow path back to the BWST. This limit ensures that the

10 CFR 100 release limits would not be exceeded. This is considered a

secondary release path from the BWST following a core damage accident.

A limit of 2 gph for direct leakage from the recirculation flow path is

stipulated in T.S. 4.5.5, Low Pressure Injection System Leakage.

The licensee performed a past operability evaluation and determined that

although the self-imposed secondary leakage path limit was exceeded, the

particular case event would not have exceeded 10 CFR part 100 limits.

The LPI System was therefore operable.

Within the areas reviewed, there were no Violations or Deviations identified.

2.5

Operations Area Followup Issues

2.5.1 (Closed) URI 270/95-03-03, Valve Configuration

The inspector reviewed Unresolved Item 270/95-03-03, Valve

Configuration, and determined that a similar issue of configuration

control had been subsequently addressed in Violation 269,270,287/95-18

01, Inadequate Configuration Control.

Based on the open violation, URI

270/95-03-03 is closed.

2.5.2 (Closed) LER 269/94-02, Inappropriate Action Results In False High

Steam Generator Level, Causing Loss of Main Feedwater And Reactor

Trip

On February 26, 1994, at approximately 6:57 a.m. Unit 1 experienced an

anticipatory reactor trip on loss of both main feedwater pumps. The

loss of both feedwater pumps was caused by an indicated high steam

generator water level signal in the integrated control system (ICS).

The indicated high water level resulted when the neutral wire was lifted

from an internal ICS power supply to the feedwater valve D/P circuitry

that had failed and was smoking. The lifted neutral wire also resulted

in the loss of power to the 1B1 and 1B2 SG signal monitors which

simulated high SG level in the lB SG. As documented in NRC IR

269,270,287/94-07 the post trip response was normal and emergency

feedwater initiated as required to maintain SG levels and maintain the

unit in hot shutdown. The ICS power supply was replaced and the unit

was returned to service at 1:37 a.m., on February 27, 1994.

ENCLOSURE 2

5

The licensee determined that the root cause of the this event was

inappropriate action. A contributing cause was equipment failure due to

the failure of the output loading resistor in the ICS power system. As

previously mentioned the ICS power supply was replaced and the circuit

was tested. The licensee removed the daisy chain neutral wiring

configuration which placed an unnecessary burden on I&E personnel from

the Main Feedwater Valve D/P ICS power supplied on Unit 1 and Unit 2.

Unit 3 did not have the daisy chain neutral wiring configuration. The

inspector reviewed all completed WOs. The licensee discussed this event

with the I&E personnel as part of their corrective action. The

inspector concluded that all corrective actions associated with this LER

were complete. This item is closed.

2.5.3

(Closed) IFI 50-269,270,287/94-37-02, Monitor General Fundamentals

Examination (GFE) Results For Improved Performance.

During the December 1994 inspection, NRC reviewed the recent performance

of operator training classes in the General Fundamentals Examination

area. The overall performance was considered poor, and the licensee

proposed several corrective actions to improve the program. The

inspectors concluded that the root causes identified and the corrective

actions proposed appeared to be comprehensive and adequate, but

determined that the program performance should be monitored to ensure

the adequacy of the corrective actions.

During the inspection period, the inspectors reviewed the recent results

of the GFE class performance. The results indicate that the corrective

actions applied to address the previous weaknesses had been effective.

All students passed the examination, with the lowest grade at 92% and

the class average at 95%. This item is closed.

3.0

Maintenance and Surveillance Testing (62703, 61726, 62700, and 92902)

3.1

Maintenance Activities

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work that

was not within the skill of the craft. Activities, procedures and work

orders were examined to verify that proper authorization and clearance

to begin work was given, cleanliness was maintained, exposure was

controlled, equipment was properly returned to service, and limiting

conditions for operation were met. The following are maintenance

activities which were observed or reviewed in whole or in part.

3.1.1 NSM-22873, AKI Modify MFDW Control On MSLB, WO 950773

On March 13, 1996, the inspector observed activities in progress during

the installation of the brackets and tubing for the mounting of pressure

transmitters associated with the main steam line isolation modification.

ENCLOSURE 2

6

The modification was to isolate feedwater in the event of a main

steamline break inside containment to prevent over-pressurization and

possible containment rupture. Portions of this Unit 2 modification were

being performed prior to the refueling outage (Unit 2 EOC 15) scheduled

for March 28, 1996, to ensure ample time for the process tie-ins and

testing during the outage.

The work effort was in accordance with the design documents and work was

performed to acceptable standards.

3.1.2 Install STAR Equipment For PIF In RPS Ch. A,B,C,&D, WO 95056617

On April 1, 1996, the inspector reviewed activities in progress to

replace the existing Unit 2 Bailey 880 analog-based RPS

Flux/Imbalance/Flow trip strings in RPS Channels A,B,C,&D with B&W

Nuclear Technologies digital-based STAR module trip string. Each STAR

module trip string consists of a Serial Bus Isolation Module, a STAR

Processor module and an Analog Voltage Isolation Module.

The inspector determined that a thorough safety evaluation had been

performed for the modification and the work activity was in accordance

with the procedure guidance. All work had been properly documented and

the documentation was current.

3.1.3 ICS Unit Load Demand Load Limits Calibration, WO 96006915

The inspector reviewed calibration of the ICS unit load control module.

The effort was performed on April 1, 1996, and was in accordance with

the applicable procedure, IP/O/B/0321/002, ICS/Unit Load Demand Load

Limits.

The work observed was performed to acceptable standards.

3.1.4 Hot Thermocouple Found In Dumpster, WO 94023013

On April 8, 1996, while performing a routine survey of scrap metal

dumpster contents the licensee identified a thermocouple, 2TE0106, in

the dumpster reading 400 corrected counts per minute using an RM-14

frisker. The licensee performed a computer search to identify a WO

associated with the thermocouple. The licensee identified that the

thermocouple was associated with WO 94023013-03, TDEFW Install

Hangers/Tray. The maintenance crew involved with the disposal of the

thermocouple thought that because RP had performed swipes of the area

and the thermocouple was removed from a dry socket the equipment was

clean. On April 11, 1996, the licensee performed some additional

training for maintenance personnel to discuss lessons learned from this

incident. One of the main issues covered was that, as a good practice,

all equipment removed from the turbine building would be frisked prior

to disposal.

The inspector concluded that the licensee's routine survey

acted as a successful barrier to improper disposal of the thermocouple.

ENCLOSURE 2

7

S

3.1.5 Change Voltage Taps On Keowee's Main Step Up Transformer,

ON0E-9047

On April 17, 1996, the inspector observed portions of the licensee's

implementation of minor modification, ONOE-9047, Change Voltage Taps On

Keowee's Main Step Up (MSU) Transformer. As described in the associated

10 CFR 50.59 evaluation, the change of the transformer's taps did not

alter the function of the transformer. The tap change only increased

the transformer voltage from 218,500 volts to 224,250 volts. The

increase in system voltage initiated the need to change the taps on the

Keowee's MSU transformer. Keowee generating voltage remained the same

(13.8 kV) after the tap change. The inspector concluded that the work

observed was performed to acceptable standards.

3.1.6 New Fuel Assembly Damage

On April 8, 1996, fuel assembly (FA) NJO88U was damaged when refueling

operators attempted to place it in the Unit 1/2 Spent Fuel Storage

Building East upender and traverse carriage.

The FA was a new, unburned

assembly. The operation being performed was a check-out of the upenders

after counterweights had been adjusted. The licensee was using an

actual FA rather than the dummy FA because the dummy weight and weight

distribution are not equivalent to an actual assembly. The FA was first

placed in the West upender carriage, traversed into the Reactor

Building, and removed without incident. When the same process was

attempted for the East upender, the operators experienced several

problems, which eventually resulted in damage to a single grid strap in

the new assembly.

After the successful check-out of the West upender, the refueling bridge

was moved to the indexing mark for the East upender, and the FA was

lowered from the mast into the upender. At approximately 3 feet into

the upender carriage, the hoist underload limit stopped the hoist. The

underload limit indicates the FA has encountered resistance sufficient

to take some of the FA weight off the load cell for the hoist. The

operators raised the FA back into the mast, and repositioned the bridge

according to directions from the fuel handling "spotter."

The spotter,

using binoculars, saw that the FA was misaligned over the upender

carriage and directed the bridge operator to move in the north direction

via manual indexing. After repositioning approximately 1/4 inch, the FA

was again lowered into the upender. The FA again experienced contact

and an underload limit. The operators attempted several minor bridge

position changes, and eventually moved the bridge as much as 3 inches

from the original indexing mark.

At least one of the position changes occurred while the fuel assembly

was partially inserted. A-later root cause evaluation determined that

the fuel assembly was damaged during the repositioning while the bottom

of the FA was partially stuck in the upender. The upender itself was

found to be out of position from true vertical.

The root cause of the

ENCLOSURE 2

8

upender aligned from true vertical is still under investigation by the

licensee. When operators drove the bridge to reposition over what the

spotters saw as the true upender position, the FA was distorted. The

distortion forced the FA out of the alignment guides inside the mast.

When the operators attempted to raise the assembly back into the mast,

the grid strap was damaged slightly at two corners. When operators

realized the FA was stuck and couldn't be raised or lowered, they

indexed back toward the index mark. The assembly was then successfully

raised back into the mast. The FA was returned to the vendor (B&W) and

repaired.

The licensee performed a root cause and Human Performance Evaluation.

The evaluation determined that the damage was due to manual indexing of

the bridge while the fuel assembly was inserted and lodged in the

upender carriage. The operators moved the bridge as much as 3 inches

off the indexing mark in an attempt at aligning the mast over the

upender. Since a fuel assembly has almost no lateral strength or

support, the assembly was sprung out of alignment and sustained damage

during the subsequent withdrawal into the mast.

During and prior to this event, there was no effective restriction on

manual repositioning or indexing while a fuel assembly is out of the

mast. This is identified as a weakness in the licensee's fuel handling

procedure. Prior to resuming fuel handling, the licensee implemented

procedure changes to restrict indexing whenever the fuel assemblies are

not fully retracted into the mast. The inspector reviewed the

licensee's assessment, root cause evaluation, and corrective actions.

The licensee's actions were thorough and accurate. The corrective

actions were appropriate for the event.

3.1.7 4160 Volt Breaker Failure

On March 9, 1996, during testing of the Emergency Power Switching Logic,

4160 volt breaker 2S2 failed to close when the breaker close circuit was

actuated. The breaker is the tie for Standby Bus 2 to Main Feeder Bus

2. The breaker is a type ABB Series HK 4kV volt, 3000 amp. The breaker

was examined and found to have binding of the closing mechanism's spring

guide sleeves. The two closing springs are double springs with an inner

and outer spring and sliding sleeves between the springs. The sleeves

have close clearances and require lubrication (grease) to eliminate

sliding friction when the springs expand to close the breaker. The

licensee determined that the grease on the sleeves had hardened and

caused binding of the mechanism. The spring/sleeve assembly had not

been periodically cleaned and lubricated since initial installation,

approximately 17 years ago.

The licensee's root cause evaluation determined that the manufacturer's

technical manual did not specifically refer to a requirement to grease

the spring/sleeve assembly. The only reference is to "periodically

grease the operating mechanism."

The licensee had interpreted the

ENCLOSURE 2

9

operating mechanism as the linkages and pivot points in the breaker

mechanism, and had not considered the spring/sleeve assembly to be part

of the operating mechanism. NRC Information Notice (IN) 93-26, "Grease

Solidification Causes Molded-Case Circuit Breaker Failure To Close"

described a grease hardening failure mechanism. The IN did not

specifically refer to the spring/sleeve mechanism as requiring

lubrication. The IN referred to recommendations for switchgear

maintenance including Westinghouse Owners Group guidelines on DB and DS

breaker maintenance, industry guidance such as National Electrical

Manufacturers Association (NEMA) publications, and American National

Standards Institute/Institute of Electrical and Electronic Engineers

(ANSI/IEEE) standards. The licensee had received and reviewed the

information in the IN, but had not identified the spring/sleeve assembly

as a lubrication point.

The licensee replaced the spring/sleeve assembly for the 2S2 breaker,

and disassembled all other breakers of the same type. Several other

breakers were found with hardened grease, but were not binding in

operation. All the breakers were cleaned, lubricated, and placed back

in service. A change to the maintenance procedure (SI/O/A/2400/013)

Refurbishing 5HK, 7.5HK, and 15 HK Air Circuit Breakers, was implemented

which stipulates periodic cleaning and lubrication of the breakers.

The inspectors witnessed the disassembly, inspection, and reassembly of

several of the breakers. Corrective actions were comprehensive and

thorough.

3.2- Surveillance Activities

The inspectors observed surveillance activities to ensure they were

conducted with approved procedures and in accordance with site

directives. The inspectors reviewed surveillance performance, as well

as system alignments and restorations. The inspectors assessed the

licensee's disposition of any discrepancies which were identified during

the surveillance. The following are surveillance activities which were

observed or reviewed in whole or in part.

3.2.1 Steam Generator Secondary Hot Soak, Fill, Drain and Layup,

OP/3/A/1106/08

On March 24, 1996, the inspector observed portions of operations

procedure OP/3/A/1106/08, Steam Generator Secondary Hot Soak, Fill,

Drain and Layup. The licensee had to generate a new enclosure for

OP/3/A/1106/08 to perform a steam generator blowdown. The new Enclosure

3.24, Steam Generator Blowdown, was performed to maintain chemistry

control at RCS temperature <250 F. The inspector concluded that the

licensee adhered to the guidance of the associated procedure. No

problems were identified.

0

ENCLOSURE 2

10

3.2.2 Reactor Manual Trip Test, PT/0/A/305/01

On March 24, 1996, while the licensee was performing PT/O/A/305/01,

Reactor Manual Trip Test, rod #9 of group 5 failed to indicate that its

position was zero percent. The rod indicated it was seven percent

withdrawn with all other rods in the group indicating zero percent

withdrawn. The licensee generated PIP 3-096-0594 to address this

problem.

The licensee performed a 10CFR part 50.59 evaluation for a restricted

change to PT/0/A/305/01 for performing rod exercising while the unit was

shutdown. To withdraw the rod for retesting, the procedure as written

required driving the rods in and aligning rod position indicators (PI).

The licensee determined if the rod was actually binding within the fuel

assembly, driving in could possibly damage the control rod. Therefore,

a restricted change as documented as Enclosure 13.4 allowed pulling the

individual rod back out for retesting without PI alignment to determine

whether the indication was accurate and the rod was actually not fully

inserted. The inspector observed the performance of Enclosure 13.4 of

PT/0/A/305/01 in the control room. The Enclosure was repeated three

times successfully with good indication. No further problems were

identified.

.

3.2.3 3RC-164 and 3RC-165 Inoperable, PT/3/A/0150/22A

On April 7, 1996, while performing PT/3/A/0150/22A, Operational Valve

Stroke Test, 3RC-164 could not be closed via its reach rod and 3RC-165

could not be opened or closed via its reach rod. The licensee initiated

PIP 3-095-0703 and PIP 3-096-0704 to address these issues.

These RC sampling valves provide two functions. One is to be capable of

being opened via its reach rod to obtain a post-accident RCS sample at

the Post Accident Liquid Sampling System (PALS) panel.

The second

function is to be capable of being closed via its reach rod to isolate

containment after the samples are obtained.

The licensee determined that both valves were presently inoperable and

past inoperable since December 10, 1995, which was the date of the last

successful stroke test.

With the valves being inoperable the licensee

did not have a method to obtain a post accident sample of the RCS via

the PALS panel.

The licensee repaired the valves on April 20, 1996, as

documented in WO-95047472 and WO-95047471. The'licensee plans on

replacing the valves during upcoming outage. With the valves repaired,

the licensee was within its 90% operability limit for the panel as

described in the licensee's PALS-NUREG 07373 Position. The inspector

concluded that the licensee's actions were appropriate to address the

problem.

ENCLOSURE 2

11

3.2.4 Charcoal Filter Testing Requirements

On April 2, 1996, the licensee determined that the surveillance testing

performed per TS 4.5.4, Penetration Room Ventilation System, was not the

testing specified in the TS.

The TS requires that the filter system be

declare inoperable if testing is not performed per ANSI N510-1975.

Since 1992 the testing actually performed by the licensee is per ASTM

D3803-1989. Although the licensee considers the testing performed is

more current, conservative, and in general use throughout the industry,

the TS is specific regarding the testing to be performed. Therefore,

the licensee decided to conservatively declare the Penetration Room

Ventilation System inoperable and enter the LCO for TS 3.15.1. Since

the LCO for TS 3.15.1 requires the shutdown of all three Oconee units

within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> if the system is found to be inoperable, the licensee

requested an emergency TS change to surveillance requirement 4.5.4. NRC

reviewed the emergency TS change request and issued the change at

approximately 7:00 p.m., on April 2, 1996. The change to the

surveillance requirements stipulates that the testing performed on the

charcoal filters is conducted per ASTM D3803-1989.

Although the evaluation performed by the licensee's Engineering

department concluded that the testing actually performed was adequate to

ensure functional operability of the filters and the system, the

licensee decided to declare the system inoperable, enter the LCO, and

process an -emergency TS change. The inspector considers the actions

taken by the licensee to have been conservative, and ensured full

compliance with the requirements.

3.3

Maintenance Implementation

The inspectors observed/reviewed portions of selected maintenance

activities as detailed below to determine if these activities were

conducted in accordance with TS requirements, approved procedures and

appropriate industry codes and standards. In addition to verification

that procedures were followed and TS requirements were met, the

inspectors verified that personnel were knowledgeable and qualified,

that post maintenance testing (PMT), was performed and was appropriate

and, that calibrated measuring and testing devices were used.

3.3.1 Condensate System Valve ON1C-VA0061

A review of work history (WH) reports from 2/4/93 to the

present,disclosed the following information:

WO-93009557-01 (2/4/93) This WO was written to correct an alignment

problem between the limit switch and the valve shaft. Work was

completed on 2/11/93 and the valve functioned properly; however, the

root cause of the problem was not determined.

ENCLOSURE 2

12

WO-95055195-01,-07 (7/16/95) This WO was written to investigate and

correct a pinging noise coming from the subject valve or associated

piping, to rebuild the actuator and perform a leak check. By record

review and through discussions with cognizant licensee personnel the

inspectors learned that the pinging ceased when the bypass around the

subject valve was throttled open and it returned when the bypass was

closed. The subject valve was identified as a Fisher butterfly flange

valve, 7600 Series. The valve was removed from the line and inspected

without finding evidence of a foreign object. The valve was repacked

and reinstalled in the line. The licensee stated that a visual

inspection inside the line failed to detect a foreign object. The

licensee could only speculate on the nature or origin of the suspected

foreign object. However, they concluded that if a foreign object did

exist, it likely came to rest in the bottom of the cooler just

downstream from the subject valve where it would not pose a significant

threat to the system. The licensee plans to look for this object when

access to the cooler becomes available during the next refueling outage.

WO-96017607 (2/28/96) This WO was written to investigate a problem with

the 1C-61 Moore Controller which did not perform its intended function

during the Unit 1 trip on 2/28/96. By record review and through

discussions with cognizant licensee personnel, it was learned that the

valve failed to open on demand from the controller. The licensee's

investigation determined that the problem was related to a

malfunctioning valve positioner which was subsequently replaced. During

subsequent testing it was noted that the valve was sluggish to respond

to a signal from a close to an open position. To correct the problem,

the licensee replaced the relay assemblies used to control both valve

positions. Through this review the inspector concluded that the

licensee's corrective actions were appropriate as the controller was

returned to normal operation.

3.3.2 Main Steam Valve 1MS-77

A review of WH records from (10/1/92) to the present disclosed the

following information.

WO-92074505-01 (10/1/92) This WO was written when the subject valve

failed to close in auto mode during power reduction. An inspection by

maintenance disclosed that one of the phases at the MCC had opened on

overload. Following reset of the overload, Operations cycled the valve

which operated satisfactorily. A functional test verified the valve's

operability.

WO-94027312-01 (5/1/94) This WO was written in response to a breaker

trip on power decrease. Upon investigation, maintenance discovered a 25

ohm phase to ground, on phase Z with the breaker open.

No failures were

identified and the trip settings were increased from 2 to 2.5. The

valve could not be cycled fully until the next scheduled Unit outage.

ENCLOSURE 2

13

WR-95019982 (4/27/95) Although no work order was written for this

problem, maintenance inspected the subject valve when it failed to close

on demand from the control room. The problem was attributed to one of

the three phase overloads having-tripped and not resetting. This

problem was corrected by changing the overload block. Following this

corrective action, Operations cycled this valve and determined that it

worked normally.

WO-96017559-01 (2/29/96) This WO was written when the limitorque

operator on this valve failed to close in response to a turbine trip

signal.

An inspection by maintenance found the valve disc was wedged

against the back seat of the valve. Subsequently, the valve's open

limit was adjusted to specification. However, when it was cycled to

test operability the breaker tripped when energized. Additional testing

revealed that the operator motor had degraded and required replacement.

A functional test following motor replacement showed the valve was

functioning satisfactorily. On 2/28/96 the licensee issued PIP 1-096

0417 to evaluate the problem. The evaluation determined that

circumstances suggested that Maintenance had set the operator's open

limit too close to the back seat of the valve causing it to travel

against the back seat whenever it was fully opened. This required an

excessive amount of torque to free the valve disc from its open

position. The heat generated was sufficient to trip the breaker on

thermal overload and it eventually caused the motor to fail.

Through this review the inspectors determined that this valve had a

history of maintenance related problems in that critical settings which

are vital to good performance were not closely controlled. Each time the

valve failed, the symptom was fixed without addressing the root cause of

the problem. Although PIP 1-096-0417 evaluated the reasons for the

valve's failure, the root cause and the steps taken to prevent its

recurrence were not addressed. Until the licensee completes an

evaluation for root cause this is identified as Unresolved Item (URI)

269/96-04-04, Root Cause Assessment of Failures to Valves 1MS-77 and

1LPSW-254.

3.3.3 Low Pressure Service Water Valve 1LPSW-254

A review of WH reports from 6/15/94 to the present disclosed the

following corrective maintenance activity.

WO-94045550-01 (6/15/94) This WO was written to investigate and repair

adverse conditions which resulted in restricted flow through valve

1LPSW-254.

WO-95085230-01 (11/7/95) was written to inspect the subject valve's

operator for a sheared key and to determine the reason for the low flow

to 1A LPI cooler. Upon investigation maintenance discovered that the

low flow problem was due to the failure of the subject valve. Through

discussions with cognizant licensee personnel and by review of WH

ENCLOSURE 2

14

reports and PIP 1-095-136, dated 11/6/95, the inspectors ascertained the

following information. The subject valve is a manually operated, Fisher

10 inch butterfly valve 150# Class model No A31A.

Within these areas the licensee's investigation of the failure revealed

that the key connecting the operator to the stem had vibrated out of the

keyway thus allowing the disc to partially close and restrict flow to

the 1A LPI cooler. The vibration was due to cavitation induced by

control valve 1LPSW-251. As stated in the PIP, the degree of cavitation

and the resultant vibration are influenced by the flow velocity through

valve 1LPSW-251 which decreases and levels off as the flow rate

increases.

Also, by records review the inspectors determined that in 1988 the

licensee issued a station Problem Report to address a similar failure on

this valve which was attributed also to cavitation and vibration. These

findings led to a Design Study - completed on June 20, 1991.

From this

study, the licensee replaced, during the 1992 outage (1EOC-14), valves

1LPSW-251 and -254, under modification NSM ON-12888. However, it

appears that this valve replacement did not address or correct the root

cause of the problem as evidenced by the recurrence of this valve's

failure on 11/6/95, for the same reason. On this date, the problem was

identified when the LPI system was being aligned to perform the 1A LPI

cooler test portion of Procedure PT/0/A/251/18 "LPI Cooler test."

Basically, the test calls for a flow rate of 5000-5200 gpm of LPSW

through the lA LPI cooler. However, when Operations opened 1LPSW-251 to

raise the LPSW flow from 2500 gpm to 5000+ gpm the meter indicators

showed no change in flow rate in the 1A LPI cooler. Since identifying

the failed key problem on 11/6/95, the licensee made several attempts to

use a key that would withstand the rigors of operating conditions. This

was finally achieved by using a longer key, equal to the length of the

keyway, and capturing the key in place by bolting a washer plate to the

end of the shaft. The evaluation of system operability document in

Section 9 of PIP 1-095-1396 addressed operability from 1EOC-14 (12/3/92)

to 1EOC-16 (11/2/95), design basis requirements, and root cause

analysis. It concluded that during the above time frame it could not be

determined whether full LPSW flow could have been maintained to the 1A

LPI cooler for the duration of accident mitigation. Also, because under

existing valve conditions sufficient justification could not be obtained

to guarantee that during that time frame 1LPSW-254 would have remained

in the fully open position upon initial ES activation, the 1A LPI train

was considered inoperable. The Licensee issued a Licensee Event Report

LER 269/95-07 (Rev. 1) pursuant to 10 CFR 50.73 requirements. In

addition, the licensee issued PIP 0-095-1491 to address and track the

proposed resolution and corrective actions to be taken on this problem.

The licensee's System Engineering Group was leading an effort to

evaluate the 1LPSW system vibration problem to determine necessary

correction actions.

Pending completion of the evaluation this item is

unresolved (URI 269/96-04-04) as identified above in paragraph 3.3.2.

ENCLOSURE 2

15

The issues associated with LER 269/95-07, Rev. 1,

discussed above, will

be tracked in this unresolved item. LER 269/95-07, Rev. 1 is considered

closed.

3.3.4 SSF Diesel, Periodic Test

WO 96018726-01 I/R the Governor Control on SSF Diesel Generator

While performing PT/0/A/600/21, SSF Diesel Generator Operation, on March

4, 1996, diesel governor and generator control problems were

experienced. The diesel was shutdown and subsequently restarted per

OP/0/A1600/10 and speed increased to 900 RPM. At this point the

governor was cycling with noticeable change in engine speed indicated on

the engine tachometer. The diesel was again shutdown, but later

restarted and paralleled to Unit 2. At this time problems were

encountered with control on speed, VARs, voltage, and watts. The diesel

was shutdown, placed in a 7-day LCO and Work Request 96009782 was

written.

WO 96018726-01 was also issued to investigate and repair the governor

control on the SSF diesel generator. A diesel vendor representative

arrived at the site to assist in the troubleshooting and repair

activities. The vendor representative determined by questioning

licensee personnel, that the problem was electrical and that symptoms

indicated an intermittent control signal to the governor. The vendor

representative then developed and recommended additional instructions

for troubleshooting the SSF diesel generator which included visual

verifications, governor response and electrical input/output checks.

On March 5, 1996, the inspectors reviewed the work order, the additional

troubleshooting instructions provided by the vendor representative, and

procedure IP/0/A/0100/001 which was the controlling procedure for

troubleshooting and corrective maintenance. Troubleshooting activities

were also observed with the diesel in auto-idle-start and at normal

rated speed with the diesel removed from the grid, tied to the

generator, and loaded with the auxiliary service water pump. All

governor inputs and outputs were checked and found to be correct. The

diesel ran smoothly during the entire run.

Further investigation then

focused on the motor operated potentiometer (MOP) as the most probable

cause of the previously reported diesel instability. A test was

performed to verify the satisfactory operability of the MOP. No erratic

operation occurred during the troubleshooting analysis. The license

concluded that the initial problem had been caused by the MOP having a

wiper-to-winding interference and this interference had been "cleaned

off" during the unloading of the diesel generator. For further

verification that the diesel would run satisfactorily, operations

performed a 60 minute run with the diesel tied to the grid for full

load. All systems operated as designed.

S

ENCLOSURE 2

16

As a result of troubleshooting the governor operation, Problem

Investigation Process (PIP) form 1-096-0461 was issued on March 5, 1996,

and the licensee determined that the following preventive measures

should be taken: (1) keep a spare governor module in stock, (2) have a

"matched pair" of actuators set up and installed as a long-term solution

to load sharing between the two tandem engines, (3) consider upgrading

  • from the MOP reference system to a later more stable digital reference

unit, and (4) personnel responsible for the operability and maintenance

of the SSF diesel generator attend further training on the SSF

installation specific governor system. In addition, operations elected

to perform PT/0/A/0400/11 (which is a quarterly SSF diesel generator

test) four additional times on a weekly basis to see if the problem

recurred. No problems occurred during these four tests, and the diesel

generator was returned to the normal test schedule.

3.3.5 WO-96018085-01 I/R Valve 1HP-120

This work order was issued on March 3, 1996, to determine why valve 1HP

120 was sticking and conduct an appropriate repair. Valve 1HP-120 is

used to maintain the proper level of water in the pressurizer. The

licensee suspected the valve was sticking because the packing was too

tight and issued MP/0/A/1200/001, a generic procedure entitled:

"Adjusting and Packing," to loosen the packing nuts several flats. The

inspectors selected this corrective maintenance to observe and on March

5, 1996, met with the maintenance lead technician to coordinate the

inspection. The inspectors discovered, however, the procedure had been

rejected by the lead technician and needed to be revised because it did

not give instructions for loosening the packing. The next day the

inspectors again met with the maintenance supervisor to observe the

corrective maintenance on this valve. This time the inspectors

discovered that the procedure had been rejected by the maintenance

supervisor because the cover page of the procedure specifically

prohibited its use on chevron packing. However, the inspectors had

reviewed the maintenance history of this valve going back two outages in

time. This history had indicated that this valve had the same reported

problem on December 26, 1995, and the packing nuts were subsequently

loosened two flats at that time. Discussions with the maintenance

supervisor concerning the previous maintenance revealed that this

procedure had inadvertently been used to loosen the nuts at that time.

The inspectors also examined previous records where the valve had been

repacked and found that another procedure for refurbishing the valve had

been used to repack the valve each time. However, the licensee did not

have a procedure for loosening chevron packing. Failure to have and use

an applicable procedure which covers the corrective maintenance to be

performed on a high temperature/high pressure safety-related valve is a

violation of NRC requirements. This licensee-identified and corrected

violation is being treated as a Non-Cited Violation, consistent with

Section VII.B.1 of the NRC Enforcement Policy: Non-Cited Violation 50

269/96-0401, Inadeguate Procedure Used to loosen lackingi Nuts on

Chevron Packing. The licensee subsequently decided not to work on valve

ENCLOSURE 2

17

9

1HP-120 at that time, because operations reported the valve was

functioning correctly. A review of the maintenance history, however,

indicated that this valve had a history of sluggish and rough movement,

but had not been disassembled for inspection in over seven years.

Discussions with the licensee revealed that PIP NO. 1-096-0461 had been

issued and plans were being made to disassemble the valve next outage to

evaluate the root cause of the valve sticking. A review of the

equipment failure history, conducted by the licensee, revealed that this

problem existed on the same valve in Units 2 and 3.

3.4

Maintenance Area Followup Issues

3.4.1 (Closed) IFI 95-05-01 Limited Access Weld Examinations

The inspector met with cognizant licensee personnel to discuss and

review the status of limited access weld examinations documented in

Inspection Report 95-05. All welds in this category have been

identified and classified according to the action required to achieve

code compliance. Examinations have been performed when practicable and

for others, requests for code relief have been submitted to NRR.

Accordingly, the inspector closed this item and will continue to monitor

the status of this matter as a routine inspection item.

.

Within this area, one Non-Cited Violation was identified in paragraph 3.3.5.

4.0

ENGINEERING (37551, 37550, 40500, and 92903)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

4.1

Operability Of High Pressure Injection Valves

On March 19, 1996, the licensee notified the NRC per 10 CFR 50.72 that

as a result of evaluating Generic Letter 89-10 data, an engineering

analysis determined that inboard containment isolation valves 2HP-3 and

3HP-3 (Letdown Cooler A outlet) may not be able to close against full

differential pressure under certain accident scenarios. A single

failure of their associated outboard containment isolation valves (2HP-5

and 3HP-5) for the subject containment penetration could potentially

result in the failure to isolate the containment following an accident.

As a result, the licensee closed 2HP-3 and 3HP-3. PIP 0-096-0544 was

generated on March 18, 1996, to document, evaluate, and track the issue

to completion. The licensee subsequently retracted the associated 50.72

report on April 10, 1996, when further engineering analysis revealed

that 2HP-3 and 3HP-3 were both past and presently operable. This

analysis was reported to have evaluated the valves during each

millisecond of the design basis accident and concluded that the valves

could have stroked against the expected differential pressures during

ENCLOSURE 2

18

the design basis accident. Based on the licensee's evaluations, valves

HP-3 & 4 (Letdown Cooler B outlet) for Units 1, 2, & 3 are operable for

a design basis accident scenario.

On March 20, 1996, the licensee reported to the NRC per 10 CFR 50.72

that reactor coolant system letdown valves HP-3 and HP-4 on Units 1,2,&

3 were not capable of closing during an event which requires the SSF to

be placed in operation. Engineering analysis determined these valves

may not be able to close against full differential pressure under

certain accident scenarios.

These valves are required to close to

prevent loss of reactor coolant system inventory during an SSF event.

For an SSF event where pressures could reach 2790 psid, valves HP-3 & 4

for each of the 3 units were determined to be past and presently

inoperable. Consequently, the licensee changed their abnormal operating

procedures to require the operators to close valve HP-5 for the affected

unit prior to leaving the control room to activate the SSF. Valve HP-5

is down stream of the HP-3 and 4 valves and will reduce the higher

differential pressures across these valves once they begin to close. As

a result, valves HP-3 & 4 for Units 1, 2, & 3 are operable.

The past inoperability of Units 1, 2, & 3 valves HP-3 & 4 causes the SSF

Reactor Coolant Makeup System to be inoperable in excess of TS 3.18.4,

which in turn causes the SSF to be inoperable. The TS requires the SSF

_RC Makeup System and the SSF to be operable when the RCS is above 250

degrees F, or restored to operable status within 7 days. As a result of

the discerned inability of the valves to close against design pressure,

the RC makeup System and the SSF may have been inoperable from initial

installation until March 20, 1996, when the procedure change was

effected. The licensee was still evaluating this item at the close of

the inspection period. This item will be identified as an Unresolved

Item pending completion of the licensee's evaluation of the closure

capability of the isolation valves: Unresolved Item 269,270,287/96-04

02, Potential Inoperability Of SSF Due To Inoperable Isolation Valves.

4.2

Engineering

The inspectors reviewed documentation and observed activities related to

the following areas: engineering self-assessment, oversight groups,

modifications, 50.59 safety evaluations, drawing control, operability

evaluations, and follow up on previously identified NRC findings.

4.2.1 Engineering Self-Assessment

The inspectors reviewed an engineering self-assessment that had been

performed during a two week period in October 1995. Discussions were

held with the engineering supervisor that had been in charge of the

assessment and some of the findings were discussed in detail.

The

assessment was conducted using INPO and NRC performance objectives and

ENCLOSURE 2

19

guidelines. The results of the areas identified indicated that the

assessment was self critical.

Some of the findings indicated that there were problems with scheduling

and prioritizing of engineering work; communications needed improving

both internally and with groups outside of engineering; problems meeting

established modification schedules were identified; etc. The assessment

was well received by engineering management and a commitment was made to

followup on the recommendations provided by the team. This assessment

was issued in January 1996 and quarterly review meetings are to be held

to followup on the current status of all the recommendations.

4.2.2 Oversight Groups

The inspectors reviewed the activities of the Plant Operations Review

Committee (PORC) and the Nuclear Safety Review Board (NSRB). A review

was made of the PORC requirements in Section 16.13-3 of the site Conduct

of Operations document. On two occasions during the inspection period

regional inspectors attended a meeting of the PORC. One meeting was

held to review an operable but degraded condition for a power range

nuclear instrument (3NI-8). There was a free exchange of ideas,

questions, and discussions. The second PORC meeting involved a report

of the changes In the Shutdown Risk Assessment for the scheduled Unit 2

refueling outage due to schedule changes. Another issue involved

operability concerns for valves HP-3 and HP-4. The two valves are

considered operable in the emergency mode with a one percent margin.

The recommended solution on two units was to cut the valves out and turn

them around which would cause the valves to function against

differential pressure without the aid of the electric motor (therefore

no one percent margin would be present). Another unit would be left as

is with the one percent margin. During the exchange of information and

ideas between the various engineering groups, it was evident to the PORC

members that there was a difference of opinions on the one percent

margin. Based on this PORC did not agree with the recommendations and

asked engineering to come back with a revised plan for PORC review. In

addition to these meetings, the inspectors reviewed a sample of 18 PORC

meeting minutes dating back to 1994. In this sample of minutes there

were other examples where PORC rejected ideas or asked for a revised

plan.

The inspectors reviewed the TS requirements for the NSRB board including

functions, organization, and the areas that the board will review. A

review was performed of the minutes for the 1994, 1995, and 1996 board

meetings. It was noted that the findings and remarks were detailed.

Several remarks or observations were made in the Oconee engineering area

by the board. One concern from the September 1995 meeting addressed a

suggestion for continued management attention to ensure proper staffing

level and utilization of engineering resources. Another continuing

concern in the same minutes regarded the adequacy for planning,

scheduling, and independent reviews for refueling outages. In the

ENCLOSURE 2

20

latest meeting (February 1996) a remark for Oconee engineering stated

that the system engineering group appears diverted to design base

document reviews versus plant support. Some of the remarks of the NSRB

appear similar to those -identified during the engineering self

assessment. In conclusion both of the groups were functioning

effectively in evaluating engineering and other activities.

4.2.3 Modifications and Safety Evaluations

The inspectors reviewed the following modifications to determine if they

complied with the existing directive at time of implementation. The

initial and final scoping document and the 10 CFR 50.59 for each

modification was reviewed along with the necessary post modification

testing requirements.

NSM-12873 Modify main feedwater control on Main Steam Line

Break(Unit 1)

NSM-12923 Upgrade Safety Related Instrumentation for LPSW flow

through decay heat coolers 1A & 18,

add switches for 1LPSW-251 and

252

NSM-32879 Replace the Letdown Storage Tank Makeup

Controller/Totalizer and provide bypass capabilities (Unit 3)

NSM-22963 Unit 2 Reactor Building Cooling Unit replacement

NSM-32905 Redundant Level Monitoring for the Reactor Vessel when

shutdown (Unit 3)

The inspectors reviewed all correspondence associated with NSM-12873

because a review of the modification indicated that it was not in

compliance with IE Bulletin 80-04. The licensee stated in the 10 CFR

50.59 that the modification was an enhancement to their previous

submittal and took credit for operator action to close the main

feedwater block valve within 120 seconds to avoid overpressurization of

the containment if the main feedwater control valve sticks open. The

licensee also requires the operators to respond within 20 seconds if the

control valve is in manual position to avoid overpressurization of the

containment. IE Bulletin 80-04 requires safety-related instrumentation

and requires that the design be single failure proof. A review of the

modification testing showed documentation that the Main Feed Water

(MFDW) control valves did not close off in the 20 seconds as stated in

correspondence. An analysis was done by the licensee to allow a 25

second closure. The inspectors reviewed documentation that stated that

the MFDW control valves and the MFDW startup control valves must close

within a total of 25 seconds of reaching the MFDW isolation circuitry

setpoint. This was documented by calculations OSC-5233 and OSC-5373.

The licensee agreed to provide the inspector with the calculations to

support a 25 second closing time. The inspector interviewed licensee

ENCLOSURE 2

21

training personnel, reviewed the EOPs, and ascertained that the EOPs

contained guidance for a.steam line break. The licensee personnel

stated that operators had received training on the simulator and were

able to respond within the allowable time frames.

Documentation reviewed by the inspector indicated that the NRC was aware

that the modification did not meet the requirements of IE Bulletin 80-04

and had accepted the licensee's design. Specifically, a licensee letter

titled "Supplemental Response to IE Bulletin 80-04 Delay of NRC

Commitment Item," dated June 14, 1995, stated, "The MFDW equipment being

controlled by the new MSLB circuitry is non-safety related and was never

intended to be safety-related. Therefore, this equipment is not single

failure proof. However, the associated pressure transmitters, logic,

and control circuitry installed by this modification for mitigation of a

MSLB will be safety-related (QA-1). Therefore, these components will be

redundant and single failure proof."

The NRC responded in a letter

dated June 30, 1995, and although the letter did not specifically

address the acceptance of the non-safety and non-single failure proof

portions the modification was accepted.

The inspectors reviewed LER 269/93-06, Design Deficiency Results in a

Condition Outside the Design Basis of Containment For A Main Steam Line

Break. Based on the licensee's response and the statement in the LER

that "The equipment required to mitigate the consequences of the MSLB is

environmentally qualified and would perform its safety function" refers

to the equipment being qualified to 60 psig, the LER is closed.

A review of PLAN, the management tool used to determine the progress of

the modifications, revealed that it was a useful tool for tracking

progress.

The inspectors concluded that there were no programmatic problems with

the modification program as a result of the review of the above

modifications. The inspectors also concluded that for these

modifications the 10 CFR 50.59 program was being followed according to

procedure. During this inspection, the inspectors did not evaluate the

minor modification program.

4.3

Drawing Control

The inspectors reviewed elements of drawing control which included

drawing accuracy and drawing distribution control.

Previous NRC

inspections had identified drawing deficiencies associated with drawing

accuracy (NRC Inspection Reports 50-269,270,287/95-20 and 95-27). In

particular, these deficiencies were associated with inconsistencies

between Keowee electrical drawings and the as-built condition in the low

voltage electrical (logic) cabinets. The inspectors reviewed the

licensee's actions to resolve Keowee drawing accuracy deficiencies and

actions planned to assess the accuracy of Oconee station electrical

drawings. Drawing distribution control was reviewed by evaluating the

ENCLOSURE 2

22

consistency of the revisions of Vital to Operations (VTO) drawings

between the master index and the satellite control drawing locations.

In conjunction with the Keowee Upgrade Project, an as-built verification

of Keowee electrical drawings was performed in 1993. Deficiencies or

errors were identified as editorial Station Problem Reports (SPRs).

Drawing errors were again identified in October 1995 during the

implementation of a modification of the Keowee logic configuration.

This resulted in an extensive walkdown of the low voltage cabinets which

identified further errors. The licensee initiated Problem Investigation

Program reports (PIPs) PIP 0-95-1461 and PIP 0-95-1577 to evaluate the,

errors and track resolution. The evaluation identified that the drawing

errors were non-functional (i.e., the errors did not impact the function

of circuits, logic, or components). Additionally, the majority of the

errors had been previously identified in the 1993 verification and had

not been corrected. The SPR process provided no time constraints on

resolution of editorial SPRs.

The major cause of drawing errors was

inadequate as-built verification during construction. The 1995 errors

were identified in the above PIPs and minor modifications were

implemented which corrected the errors. The inspectors verified the

corrective actions of the PIPs adequately addressed the drawing errors

and performed a sample as-built verification of Keowee electrical

cabinets 1LC1, 1LC2, and CB8. No drawing errors were identified. The

inspectors concluded that the licensee had improved the accuracy of

Keowee low voltage electrical drawings.

The inspectors reviewed the licensee's planned actions to assess the

accuracy of Keowee high voltage electrical cabinets and Oconee station

electrical drawings. Project PLAN ON-96-0039, Implement Emergency Power

Improvement Plan, provided an activity schedule for these actions. The

Keowee high voltage cabinets (i.e., 600 VAC motor control centers and

switchgear, were scheduled for as-built verification in November 1996).

The Oconee station-drawings have been maintained by a QA program since

construction. The Keowee drawings were not subject to similar controls

until 1993, which contributed to their deficient quality. Although the

Oconee station drawings were better controlled, potential drawing errors

could exist due to deficient as-built verification during construction.

The Oconee station safety-related Electrical cabinet drawings were

scheduled for as-built verification from June 1996 to April 1998. The

licensee had conducted a modification documentation completion and

drawing update program in 1995. This program had eliminated the drawing

backlog. The inspectors concluded the licensee had scheduled

appropriate actions to assess the accuracy of Keowee high voltage

electrical cabinets and Oconee station safety-related electrical

drawings.

The licensee recently conducted a self-assessment of engineering drawing

quality (Report No. SA-96-13-ON-SRG) at the request of the Modifications

organization. This organization was responsible for drawing accuracy

and control.. The assessment was conducted by the Safety Review Group

ENCLOSURE 2

23

(SRG) from February 1 - March 11, 1996, and primarily consisted of a

review of the 1995 PIP data base to assess potential adverse trends in

drawing quality. Of the 86 drawing related PIPs the root cause of the

above problems was determined to be deficient as-built verifications

during the station construction.- An additional cause was determined to

be deficient drawing update activity from modifications. The conclusion

was that an adverse drawing trend was not apparent at Oconee. The

licensee was in the process of establishing a standard for drawing

quality to facilitate future monitoring of performance in this area.

The inspectors concluded the SRG review of engineering drawing quality

provided an effective assessment which was independent of the staff

responsible for the drawing activities.

The inspectors reviewed drawing distribution control. There were

approximately ten satellite locations for controlled drawings, which

included the three control rooms, the work control center and

engineering locations. The staff was knowledgeable of the distribution

control process and conscientious in fulfilling their responsibilities.

Following the elimination of the drawing backlog discussed previously,

the licensee established additional time constraints for updating

drawings to prevent development of a backlog. These included two days

to update VTO drawings after modification installation and 60 days for

non-VTO drawings. The inspectors noted there were less than five

outstanding drawing changes exceeding 60 days which indicated the

process was.effective in assuring drawings were updated. A sample of

approximately 65 drawings were selected to compare the revision status

of the satellite locations and the master index. One example was

identified in which the field revision was inconsistent with the master

drawing index. This example is discussed in the following paragraph.

The exception not withstanding, the inspectors concluded that the

overall drawing distribution process was well controlled.

The inspectors identified a VTO drawing in the Unit 1 control room which

was not appropriately updated from a 1994 modification,.NSM 52875.

Elementary Electrical Diagram 0-803, AC Circuits 230 Kv Switchyard, PCBs

26 & 27, revision 10, was in the control room; revision 11 which

incorporated the NSM was in the master index. Further investigation

determined that the October 19, 1994, drawing transmittal which included

this and 33 other drawings had not been processed. As a result, a total

34 drawings associated with NSM 52875 had not been updated. This

included 10 VTO drawings in the Unit 1, 2, and 3 control rooms and two

other controlled drawing satellite locations. The NSM was related to

monitoring components and circuits for switchyard parameters; therefore,

there was no apparent impact on the capability of operators to perform

their activities. However, this is an example of non-compliance with QA

program requirements for drawing control. This item is identified as

Violation 50-269,270,287/96-04-03, Failure to Follow Procedure for

Drawing Controls.

ENCLOSURE 2

24

4.4

Operability Evaluations

The inspectors reviewed the licensee's process for accomplishing

operability evaluations, selected a sample of operability evaluations,

and observed the PORC review and approval of a completed evaluation.

Nuclear Station Directive (NSD) 203, Operability, revision 4, provided

guidance for the development of operability evaluations. Document NSD

208, Problem Investigation Process, provided additional guidance for

operability evaluations. The primary vehicle for operability

evaluations was the More Significant Event (MSE) PIPs. The inspectors

selected a sample of approximately fifteen MSE PIPs from the previous

two years and reviewed the associated operability evaluations to verify

that conclusions were adequately supported by design or performance

information. Also reviewed was the independent check and approval

process required by NSD 203. Additionally the inspectors observed the

PORC review of an operability evaluation related to a power range

nuclear instrument (3NI-8) being in an operable but degraded condition.

The inspectors concluded that the MSE PIP operability evaluations were

adequately supported by design and performance information and that the

conclusions were adequately communicated to Operations via the

memorandum process described by NSD 203. The PORC reviewers

appropriately challenged Engineering to support the assumptions and

conclusions of the operability evaluation related to safety-related

valves HP-3 and HP-4 being operable in an emergency mode with a one

percent margin.

4.5

Engineering Followup Issues

4.5.1 (Closed) Apparent Violation 50-269,270,287/94-21-01, Keowee Air Circuit

Breaker (ACB) Air System Not Controlled as QA Safety Related System.

(Violation EA 94-125-01014)

This item identified that the Keowee ACB air system was not

appropriately covered by the licensee's Quality Assurance (QA) program.

For example, the Quality Standards Manual-did not show the air system as

QA-1, QA program controls consistent with the system's importance to

safety were not applied for maintenance and modifications activities,

and there was no system control drawing. The lack of these controls

resulted in a system air leakage which contributed to an unanticipated

lockout of the overhead emergency power path in June 1994. The

licensee's corrective actions specified in the response to the violation

dated September 23, 1994, included a modification to enhance the air

system logic and incorporation of QA controls consistent with the

system's importance to safety.

The inspectors verified that the ACB air system was added to the Quality

Standards Manual, a controlled system drawing (KFD-107A1.1, Flow Diagram

of ACB Air System, revision C) had been developed, and QA level

procedures had been developed for inspection and maintenance of the ACBs

which included the air system. The Keowee electrical and mechanical

ENCLOSURE 2

25

support systems were evaluated in November 1994 to determine if other

support systems required upgraded quality controls. Several mechanical

components were added to NSD 307, Quality Standards Manual, revision 7,

as a result of the evaluations. Work orders dated July 1994

demonstrated that the check valve problems which caused the system

leakage were corrected. The logic modifications were implemented with

NSM 52966 which remains open pending completion of post modification

testing. This modification incorporated appropriate QA controls for

safety-related equipment. The inspectors concluded the licensee's

completed and scheduled corrective actions adequately resolve this item.

4.5.2 (Closed) IFI 50-269,270,287/95-30-02, Propane Issue

This item concerned the NRC's questioning the design, placement, and

documentation requirements associated with propane tanks that supplied

heaters placed in the reactor building personnel hatch areas. The

inspectors reviewed PIP 0-096-0025 that documented the problem and

discussed the resolution with the system engineer. Unit 2 was the only

unit that was not in compliance with the fire code because of the

distance of the propane tanks to a safety-related building. However,

the licensee has removed these propane tanks from the site for all three

units and capped the lines. This resolves the issue and the item is

closed.

4.5.3 (Open) Deviation 50-269,270,287/94-24-05, Improper Code Classification

This item identified that the licensee did not classify the high

pressure injection minimum flow piping properly. Since this piping may

see recirculated reactor building sump water following a LOCA, the

piping should be ASME Class II (licensee Class"B"). The inspectors

discussed this item with the licensee and since more actions have to be

taken this item will remain open.

4.5.4 (Closed) IFI 269/94-16-04, HPI Pump Runout Flow Testing

A review was made of Calculation OSC-5909, Test Acceptance Criteria for

High Pressure Injection Pump Developed Head. The inspectors found that

the operable pump required for the duration of an accident had 25

percent conservatism. The HPI pump which is required to be available in

ten minutes had a conservatism of 12.6 percent. Seven percent of this

allowable by the ASME Code (Sec. XI) and 5.6 percent allowed for

instrument error. A review of the calculation and discussions with the

system engineer indicated that time was available to take operator

action before runout occurred. The inspector also reviewed whether the

HPI pump 2B was installed within the necessary guidelines during the

last outage. The inspector's review of the calculation showed it was

within the acceptable guidelines and the inspector discussed the results

of the baseline curve with the component engineer. The baseline was

lower than expected but still within the acceptable limits. A decision

was made to use that pump continuously during the last cycle. Unit 2

ENCLOSURE 2

26

started down for a refueling outage during this inspection and a

decision was made to replace the pump because it had degraded an

additional 60 psig. This could be due to normal wear. There was not

enough previous data under full flow testing to make this judgement.

The licensee intends to disassemble the pump to determine if there are

any noticeable problems. This item is closed.

4.5.5 (Closed) LER 269/95-06, LPI Past Inoperable Due to

Inadequate Vendor Information Causing Calculation Errors

The inspectors reviewed Calculation OSC-5121, LPI Pump Runout Analysis

and determined that the different Cv (flow coefficient) for the LPI

throttle valves would not have contributed to a runout condition. This

LER was closed.

4.'5.6 (Closed) LER 269/93-06 Design Deficiency In a Condition Outside the

Design Basis of Containment for a Main Steam Line Break.

The inspectors reviewed the response to the LER and had discussions with

the licensee. It appears logical that the equipment required to mitigate

the consequences of the MSLB is environmentally qualified and would

perform its safety function. This item was closed on the basis of the

licensee statement that EQ was done for a containment pressure of 60

psig.

4.5.7 (Closed) IFI 270/94-11-01, Slow Transfer Of The "E" Breakers

During a Unit 2 reactor trip on April 6, 1994, the "E" breakers did not

transfer the tripped unit to the startup transformer as rapidly as

designed. During an investigation into the event, the licensee

determined that a modification which included the addition of auxiliary

relays would be necessary to get the fast transfer. The problem was

determined to exist on the other two units also.

The licensee implemented design changes to modify the existing

circuitry; ONOE 7442 (Unit 1), ON0E 7477 (Unit 2), and 7478 (Unit 3).

The modifications have been completed for Units 1 and 2, and Unit 3 is

scheduled to be modified during the next refuelling outage. Based on

these actions, this item is closed.

Within this area, One Violation (paragraph 4.3) was identified for failure to

follow procedures for drawing control, and one Unresolved Item (paragraph

4.1) was identified for a potential inoperability of the SSF due to isolation

valve operability.

ENCLOSURE 2

27

5.0

PLANT SUPPORT (71750, 83750, 84750, AND 92904)

The inspectors 'assessed selected activities of licensee programs to

ensure conformance with facility policies and regulatory requirements.

During the inspection period, the following areas were reviewed:

Radiological Controls, Physical security and Fire protection.

5.1

Administrative Controls for External Exposure

This area was reviewed to determine whether personnel dosimetry,

administrative controls, and records and reports of external radiation

exposure met regulatory requirements.

10 CFR 20.1201(a) requires in part, that each licensee control the

occupational dose to individual adults.

The inspector reviewed and discussed with licensee representatives TEDE

exposures for plant and contract personnel for the period of 1995.

Through review of selected dose records and discussions with licensee

representatives, the inspector confirmed that all TEDE exposures

assigned during the period were within 10 CFR Part 20 limits.

5.2

Personnel Dosimetry

10 CFR 20.1502(a) requires in part, each licensee monitor occupational

exposure to radiation and supply and require the use of individual

monitoring devices.

The licensee's dose tracking system tracked personnel exposures in order

to ensure adherence to procedural administrative allowances as well as

10 CFR Part 20 limits.

The inspector conducted random interviews with radiation workers in the

RCA and observed personnel logging into the ED system. From

observations, the inspector noted personnel were properly utilizing the

ED system and were knowledgeable of their personal dose, and proper

response to ED alarms.

Based on direct observation, discussion and review of records, the

inspector determined personnel dosimeters were being effectively

utilized.

5.3

Internal Exposure Control

10 CFR 20.1502(b) requires each licensee to monitor the occupational

intake of radioactive material by and assess the committed effective

dose equivalent (CEDE) to:

ENCLOSURE 2

28

(1) Adults likely to receive, in one year, an intake in excess of

10 percent of the applicable ALI in Table 1, Columns 1 and 2 of

Appendix B to 10 CFR 20.1001-20.2401; and

(2) Minors and declared pregnant women likely to receive, in one year,

a committed effective dose equivalent in excess of 0.05 rem.

This area was reviewed to determine the adequacy of licensee's use of

process and engineering controls to limit exposures to airborne

radioactivity, adequacy of respiratory protection program, licensee's

administrative controls for assessing the CEDE in radiation and airborne

radioactive materials areas, and assessments of individual intakes of

radioactive material and records of internal exposure measurements and

assessments.

The inspector discussed with the licensee, respirator reduction efforts

with respect to engineering controls to be used by the licensee to

enhance ALARA concepts. Discussions with licensee personnel identified

the licensee was using worksite ventilation and decontamination methods

as engineering controls to limit airborne radioactivity in work areas.

The licensee informed the inspector that their investigative limit for

internal exposures was 0.050 Rem per exposure and that when the sum of

the individual internal exposures reached 0.100 Rem per year, the sum of

the CEDE would be added to the individuals Total Effective Dose

Equivalent (TEDE), which was within regulatory requirements. Only 1

worker received internal exposure that met the licensee investigative

limit in 1995 and 2 workers had received internal exposures at

investigative limits in 1996 at the time of the inspection.

Based a review of records, and discussions with licensee personnel, the

inspector determined that the licensee was using engineering controls to

minimize internal exposure and that the licensee's program for

monitoring, assessing, and controlling internal exposures was conducted

in accordance with regulatory requirements with no exposures in excess

of 10 CFR Part 20 limits identified.

5.4

Operational and Administrative Controls

The inspector reviewed Operational and Administrative controls for

entering the RCA and performing work. These controls included the use of

RWPs to be reviewed and understood by workers prior to entering the RCA.

The inspector reviewed selected RWPs for adequacy of the radiation

protection requirements based on work scope, location, and conditions.

For the RWPs reviewed, the inspector noted that appropriate protective

clothing, respiratory protection, and dosimetry were required. During

tours of the plant, the inspector observed the adherence of plant

ENCLOSURE 2

29

workers to the RWP requirements. The inspector also performed

independent radiation surveys of selected areas in the Auxiliary

Building to confirm RWP exposure information and no discrepancies were

identified.

The inspector found the licensee's program for RWP implementation to

adequately address radiological protection concerns and to provide for

proper control measures.

5.5

Control of Radioactive Materials and Contamination, Surveys, and

Monitoring

10 CFR 20.1501(a) requires each licensee to make or cause to be made

such surveys as (1)

may be necessary for the licensee to comply with the

regulations and (2) are reasonable under the circumstances to evaluate

the extent of radioactive hazards that may be present.

10 CFR 20.1904(a) requires the licensee to ensure that each container of

licensed material bears a durable, clearly visible label bearing the

radiation symbol and the words "Caution, Radioactive Material," or

"Danger, Radioactive Material." The label must also provide sufficient

information (such as radionuclides present, and the estimate of the

quantity of radioactivity, the kinds of materials and mass enrichment)

to permit individuals handling or using the containers, to take

precautions.to avoid or minimize exposures.

The inspector reviewed selected records of routine and special radiation

and contamination surveys performed and discussed the survey results

with licensee representatives. The inspector discussed labeling

procedures, practices, and storage of radioactive material with licensee

personnel during the facility tours.

During tours of the plant, the inspector independently verified

radiation levels in portions of the Auxiliary Building were in

accordance with licensee survey results.

The inspector also identified

that survey instrumentation and continuous air monitors observed in use

within the RCA were operable and currently calibrated. The inspector

noted that all containers and materials inspected were labeled to denote

the radiological hazards present.

Discussions with licensee management identified continuing efforts to

minimize radioactive waste. The licensee generated approximately 3500

cubic feet of radioactive waste in 1995 which was below the licensee's

original 1995 goal of 6570 cubic feet.

During facility tours, the inspector noted that contamination control

and general radiological housekeeping practices were adequate. At the

time of the inspection, contaminated square footage was approximately

0.006 percent (813 square feet) of the total Radiological Controlled

ENCLOSURE 2

30

Area (RCA) of 126,311 square feet. The licensee averaged approximately

0.03 percent (4000 square feet) of the total RCA as contaminated area

during a normal refueling outage.

The inspector detected contamination in an area adjacent to a

contamination boundary in the Auxiliary Building. Water routed to a

drain line in the contaminated area had apparently migrated beyond the

posted contamination boundary. The licensee initiated immediate

corrective action to survey and appropriately control the area to

prevent further spread of the contamination. The inspector reviewed

personnel contamination records for 1995 and 1996. The licensee had

accumulated 592 PCEs for all three units in 1995. This included 2

refueling outages and 2 forced outages. Of the PCEs accumulated in 1995,

approximately 381 occurred during the Unit 3 outage which had high

activity levels in the Reactor Coolant System due to failed fuel.

The

failed fuel contributed to approximately 91 Iodine contaminations and

107 particle contaminations. At the time of the inspection, the

licensee had accumulated approximately 30 PCEs in 1996. Records

reviewed determined the licensee was tracking and trending personnel

contamination events.

Based on observations during tours of the facility, procedure reviews,

and discussions with licensee personnel, the inspector identified that

the licensee's posting and control policies for radiation areas, high

radiation areas, very high radiation areas, airborne radioactivity

areas, contamination areas, and radioactive material storage areas were

appropriate and that the licensee was conducting surveys to comply with

procedural requirements using appropriate instrumentation. The

inspector determined the licensee was meeting FSAR facilities and

equipment requirements for those areas inspected.

5.6

Program for Maintaining Exposures As Low As Reasonably Achievable

(ALARA)

10 CFR 20.1101(b) requires that each licensee use, to the extent

practicable, procedures and engineering controls based upon sound

radiation protection principles to achieve occupational doses and doses

to members of the public that are ALARA.

The inspector discussed ALARA goals and annual exposures with licensee

management and determined the organizational structure and

responsibilities for the ALARA staff were clearly defined in

organizational charts. The inspector determined that the licensee's

ALARA policy and objectives were adequately addressed in General

Employee Training (GET).

Areas reviewed included source term reduction, ALARA accomplishments,

and future ALARA plans. A discussion with licensee representatives and

a review of pertinent records determined the licensee had established an

annual site exposure goal for 1995 of approximately 420 person-rem. The

ENCLOSURE 2

31

licensee's 1995 annual site exposure goal was based on operational

exposure and dual Unit refueling outages. Site exposure actually

accrued in 1995 was approximately 303.9 person-rem for an average 1995

dose per reactor of approximately 101 person-rem. The site's actual

1995 exposures were based on operational exposure, two refueling

outages, and two forced outages. The site's 3 year average through 1995

was approximately 120 person-rem per Unit. The licensee's

crudburst/shutdown procedures used during the last 1995 Unit 1 refueling

outage removed 285 curies of Cobalt 58 and 1.7 curies of Cobalt 60 which

contributed to lower source term activity and lower outage exposures.

Total outage dose was 73 person-rem compared to the previous refueling

outage dose of 125 person-rem. The lower outage dose was largely

attributed to the reduced number of RWP hours used to perform tasks.

The licensee informed the inspector the reduced number of RWP hours was

achieved through worker efficiency and minimizing the number of workers

performing a task. Future ALARA plans to reduce dose and enhance

radiological controls included increased use of video equipment in

conjunction with audio communications and wireless teledosimetry.

Based on discussions with licensee management and records reviewed the

inspector determined the licensee had continued to improve upon ALARA

initiatives and meeting ALARA goals, particularly relating to outage

dose reductions. The licensee was continuing to meet FSAR ALARA program

commitments.

5.7

Radiological Effluent Controls

Technical Specification (TS) 6.6.1.4 and Section 16.11-9 of the Final

Safety Analysis Report (FSAR) described the reporting schedule and

content requirements for the Annual Radioactive Effluent Release

Reports. The reports were required to be submitted before May 1 of each

year covering the operation of the facility during the previous calendar

year.

(Prior to 1994, radioactive effluent release reports were

required to be submitted on a semi-annual basis.)

Summaries of the

quantities of radioactive material in liquid and gaseous effluents

released from the facility and an assessment of the radiation doses due

to those releases were required to be included in the reports.

The effluent data presented in Table 1 below were compiled from the

licensee's effluent release reports for the years 1989 through 1995.

The inspector reviewed the preliminary report for the year 1995 and

discussed it's content and the data presented in Table 1 with the

licensee.

ENCLOSURE 2

32

Table 1

Effluent Release Summary for Oconee Units 1, 2, and 3

Activity Released (curies)

Liquid Effluents

Gaseous Effluents

Fission and

Dissolved

Activation

Noble

Noble

Year

Products

Tritium

Gases

Gases Halogens Particulates Tritium

1989

3.88

1023

6.36

8970

3.11E-2

1.76E-2

118

1990

3.11

992

1.17

8830

1.69E-2

1.59E-2

101

1991

1.40

1130

2.86

3450

4.06E-2

8.50E-2

109

1992

2.58

998

3.12

3280

2.13E-2

8.35E-1

64

1993

0.47

1100

0.53

658

2.20E-2

1.06E-1

44

1994

0.37

909

0.92

3500

4.71E-2

.08E-1

43

1995'

0.39

835

0.18

1290

2.25E-2

9.38E-1

43

Preliminary values - Report due May 1, 1996

Annual Doses

Liquid Effluents

Maximum

Total Body Dose Percent of.

Organ Dose

Percent of

Year

(Limit: 9 mrem)

Limit

(Limit: 30 mrem)

Limit

1989

0.62

6.91

2.61

8.70

1990

0.99

11.00

1.47

4.90

1991

0.36

3.97

0.47

1.57

1992

0.29

3.22

0.58

1.93

1993

0.13

1.44

0.17

0.57

1994

0.43

4.78

0.62

2.07

1995'

0.24

2.67

0.40

1.33

Preliminary values -

Report due May 1, 1996

ENCLOSURE 2

33

Gaseous Effluents

Maximum Organ Dose

Air Dose

[From Iodine, Tritium,

(Limits: Gamma 30 mrad, Percent of

and Particulates]

Percent of

Year

Beta 60 mrad)

Limit

(Limit: 45 mrem)

Limit

1989

Gamma 0.047

0.16

0.31

0.70

Beta 0.145

0.24

1990

Gamma 0.067

0.22

0.11

0.24

Beta 0.19

0.32

1991

Gamma 0.026

0.09

0.24

0.54

Beta 0.059

0.10

1992

Gamma 0.034

0.11

0.12

0.27

Beta 0.057

0.09

1993

Gamma 0.005

0.02

0.02

0.04

Beta 0.018

0.03

1994

Gamma 0.088

0.29

0.42

0.93

Beta 0.244

0.41

1995

Gamma 0.051

0.17

0.11

0.24

Beta 0.098

0.16

Preliminary values - Report due May 1, 1996

The licensee provided the following information regarding the amounts of

activity released during 1995 and the resulting doses from those

releases. Less than one half of a curie of activity was released as

fission and activation products in liquid effluents during each of the

last three years (1993, 1994, and 1995).

This was partially achieved by

processing laundry water and miscellaneous waste water through powdered

resin before release. This additional step in liquid radwaste

processing was begun during 1992 and continued through 1995. The resin

used for this treatment had initially been used in the condensate

polishers. Radwaste personnel found that mixing the waste water with the

partially spent resin for several hours in a storage tank provided

sufficient contact between the water and the resin to significantly

reduce the activity concentration in the water. During the mixing

operation additional activity was deposited on the resin. The resin was

then disposed of by shipment to a licensed waste processor for

incineration. The decrease in the activity released as dissolved noble

gases in liquid effluents was a result of the continuous agitation of

the liquid radwaste as it was being accumulated in the radwaste

collection tanks for treatment. The initial purpose for agitating the

waste water was to keep particulates in suspension in order to capture

them during waste treatment rather that allow them accumulate as sludge

in the collection tanks. The agitation also liberated dissolved gases

ENCLOSURE 2

34

from the waste water. The licensee indicated that the majority of the

activity released in gaseous effluents was generated during

depressurization of the reactor coolant systems in the initial stages

outages, either forced outages or refueling outages. The decrease in

the activity released as noble gas in gaseous effluents during 1995 was

a result of fewer Unit 3 outages during that year as compared to 1994.

The activity in the Unit 3 reactor coolant system had been higher than

the activity in the coolant systems of the other two units for several

years due to leaking fuel. No leaking fuel was returned to the Unit 3

core during the 1995 refueling outage and the licensee expects the

gaseous activity released from Unit 3 to decrease during the current

fuel cycle.

As indicated in Table 1, the annual total body and organ doses from

liquid effluents were less than 3 percent of their limits. The air and

organ doses from gaseous effluents were less than 1 percent of their

limits.

The effluent release report indicated that during 1995 there were no

unplanned releases and no effluent monitors inoperable for more than 30

days.

Based on the above reviews, it was concluded that the licensee had

implemented and maintained an effective program to control liquid and

gaseous radioactive effluents. The projected offsite doses resulting

from those effluents were well within the limits specified in the TSs

and 40 CFR 190.

5.8

Radiological Environmental Monitoring Program

Technical Specification (TS) 6.4.4.f required the licensee to establish,

implement, and maintain a program to monitor the radiation and

radionuclides in the environs of the plant as described in Chapter 16 of

the Final Safety Analysis Report (FSAR). The sampling locations, types

of samples or measurements, sampling frequency, types and frequency of

sample analysis, reporting levels, and analytical lower limits of

detection (LLDs) were specified in FSAR section 16.11-6. TS 6.6.1.5 and

FSAR section 16.11-10 delineated the requirements for submitting, the

submittal dates, and the content of the Annual Radiological

Environmental Operating Reports. The reports were required to be

submitted prior to May 1 of each year and to provide an assessment of

the observed impact on the environment resulting from plant operations

during the previous calendar year.

The inspector reviewed the licensee's preliminary 1995 Annual

Radiological Environmental Operating Report and discussed its content

with the licensee. The report included the following: a description of

the program, a summary and discussion of the results for each exposure

pathway, analysis of trends and comparisons with previous years and

preoperational studies, and an assessment of the impact on the

ENCLOSURE 2

35

environment resulting from plant operations. The report also included

the results of the Land Use Census and the results of the

Interlaboratory Comparison Program required by TS 6.4.4.f and FSAR

section 16.11-6. The following observations for the various exposure

pathways were made by the licensee through their evaluation of the 1995

environmental monitoring program data, and documented in the report, or

were noted by the inspector during the review of the report.

Airborne - No man-made radionuclides were detected on any of the

312 particulate filter samples collected during 1995.

1-131 was

not detected in any of the 312 charcoal cartridges collected

during 1995 but Cs-137 was detected in 6 of those cartridges. The

observed Cs-137 concentrations were below the required lower limit

of detection (LLD).

Since Cs-137 was not detected on the

corresponding particulate filters, it was concluded that, as was

found during previous investigations of this phenomenon, the Cs

137 was an-active constituent of the charcoal.

Drinking Water - Gross beta activity was detected in 19 of the 26

samples collected from the two indicator locations and in 9 of the

13 samples collected from the one control location. The highest

concentration observed was 10 pCi/1 which was above the required

LLD of 4 pCi/l.

H-3 was detected in 5 of the 10 composite samples

collected from the two indicator locations but the highest

concentration observed was less than on fourth of the required

LLD.

Surface Water - Other than K-40, which occurs naturally in the

environment, H-3 was the only radionuclide detected in the 10

surface water samples collected during 1995. The highest H-3

concentration observed was 11,400 pCi/1, which was well below the

reporting level of 20,000 pCi/1.

Milk - Cs-137 was the only radionuclide, other than naturally

occurring K-40, detected in the milk samples. A total of 78 milk

samples were collected from 3 dairies. Cs-137 was detected in one

sample collected from one indicator location and in one sample

collected from the control location. The observed concentrations

were less than the required LLD.

Broadleaf Vegetation - Cs-137 was detected in 2 of the 48 samples

collected from the indicator locations and in 11 of the 12 samples

collected from the control location. The highest concentration

observed was less than 16 percent of the required reporting level.

Shoreline Sediment - Mn-54, Co-58, Co-60, Cs-134, and Cs-137 were

detected in low concentrations (<250 pCi/kg) in some of the

samples collected from the two indicator locations and Cs-137 was

detected in one of the samples collected from the control

location. The highest concentrations observed for Cs-134, and Cs

ENCLOSURE 2

36

137 were less that their required LLDs. No LLDs were specified in

the FSAR for Mn-54, Co-58, or Co-60. No reporting levels for

sediment were specified in the FSAR but doses from shoreline

sediments were well below environmental dose limits. The

calculated total body dose to the maximally exposed individual was

less than one thousandth of a mrem per year.

Fish - Cs-134, and Cs-137 were detected in most of the fish

samples collected during 1995 but the highest concentrations

observed were less than their required LLDs.

Direct Gamma Radiation - Exposures measured at 41 locations during

1995 here not significantly different form exposures measured

during preoperational studies.

Dose estimates calculated from environmental monitoring program data

were in reasonable agreement with dose estimates calculated from

effluent data and were within 40 CFR 190 dose limits. The annual total

body dose estimate to the maximum exposed member of the public,

calculated from the 1995 environmental sampling results, was less than

one quarter of a mrem. The report documented the licensee conclusion

that plant operations had no significant radiological impact on the

health and safety of the general public or the environment.

The inspectors also observed the collection of environmental samples at

3 air sampling stations and 2 dairies. The inspectors determined that

the sampling locations were consistent with their descriptions in the

FSAR and that the samples were in accordance with procedures

CP/0/B/2005/11 "Airborne Radioiodine and Particulate Sampling" and

CP/0/B/2005/10 "Milk Sampling".

Based on the above reviews and observations, the inspector concluded

that the licensee had complied with the sampling, analytical, and

reporting program requirements, that the radiological environmental

monitoring program had been effectively implemented and that plant

operations had no significant radiological impact on the health and

safety of the general public or the environment.

5.9

Environmental Monitoring Quality Assurance Program

TS 6.4.4.f and FSAR section 16.11-6 required the licensee to participate

in an interlaboratory comparison program and to include a summary of the

program results in the Annual Radiological Environmental Operating

Report. The licensee's report for 1995 provided a summary of the

results from the licensee's participation in the Environmental

Protection Agency's (EPA's) Environmental Monitoring Systems Laboratory

Intercomparison Program. The report also included descriptions of the

various types of samples analyzed and the analyses performed, and an

evaluation of the analytical results.

ENCLOSURE 2

37

Fourteen samples were analyzed for a total of 28 analytical results.

Three analytical results exceeded the EPA control limit. The licensee

investigated those analyses, which were performed on the same day, and

determined that the samples had been cross-contaminated. Corrective

actions to prevent recurrenceincluded refined receipt and tracking of

samples, isolation of lab work by potential activity, identification of

specific glassware for specific types of samples, improved cleaning

procedures for glassware and counter surfaces, use of blanks to identify

contamination, and improved procedures for data reviews.

Based on the licensee's overall performance in the EPA crosscheck

program, it was concluded that an effective quality assurance program

had been maintained for analysis of environmental samples.

5.10 Meteorological Monitoring Program

Section 2.3.3.2 of the Final Safety Analysis Report (FSAR) described.the

operational and surveillance requirements for the meteorological

monitoring instrumentation. Near real-time meteorological data were

required to be collected, summarized, and stored by the Operator Aid

Computer (OAC) system. Weekly equipment calibration and maintenance

checks and semiannual calibration checks were required to be performed

by prescribed station procedures.

The inspector reviewed the procedures listed below and determined that

they included provisions for performing the required semiannual

calibration checks on the meteorological monitoring instrumentation.

IP/O/B/1601/011

"Teledyne Geotech Series 21 Wind Speed Module Channel

Calibration"

IP/O/B/1601/012

"Teledyne Geotech Series 21 Model 21.21-1 Wind

Direction Processor Channel Calibration"

IP/O/B/1601/014

"Teledyne Geotech Platinum RDT T/Delta T Processor

Channel Calibration"

The inspector reviewed records of semiannual calibrations of wind speed,

wind direction and air temperature instrumentation performed during

September 1994 and May 1995 and determined that the calibrations were

performed in accordance with the above procedures and at the required

frequency.

Based on the above reviews and observations, it was concluded that

calibration of the meteorological instrumentation had been adequately

maintained.

5.11 Plant Support Followup Issues

The following open items were reviewed using licensee reports,

inspection record review, and discussions with licensee personnel, as

appropriate:

ENCLOSURE 2

38

5.11.1(Closed) VIO 269,270,287/95-015-01, Failure To Properly Frisk Personnel

This violation involved multiple examples of workers and equipment

leaving the RCA without a proper frisk being performed. The inspector

reviewed licensee corrective actions to the' VIO: the licensee reduced

the number of RCA exit points from 10 to 5; eliminated of the RCA buffer

zone which previously allowed personnel from RCAs and non-RCA to cross

through the same area lending confusion to what personnel and material

must be frisked when exiting the buffer zone; and assigned personnel to

periodically monitor exits to identify any problems with frisking of

personnel or hand held items. The inspector reviewed licensee

monitoring schedules for observing control points and licensee

observation findings. The inspector also observed frisking practices at

control points and did not identify any problems in this area. Based on

licensee actions performed and inspector observations, VIO

269,270,287/95-015-01 is closed.

Within the areas reviewed, Violations and Deviations were not identified.

6.0

REVIEW OF UFSAR COMMITMENTS

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report (UFSAR) description

highlighted.the need for a special focused review that compares plant

practices, procedures and/or parameters to the UFSAR descriptions.

While performing the inspections discussed in this report, the

inspectors reviewed the applicable portions of the UFSAR that related to

the areas inspected. The inspectors verified that the UFSAR wording was

consistent with the observed plant practices, procedures and/or

parameters.

7.0

OTHER NRC PERSONNEL ONSITE

On April 16 and 17, 1996, Mr. H. Berkow, Project Director, NRR, and Mr.

L. Wiens, Project Manager, NRR were on site for a plant tour and to

discuss issues regarding the licensee's performance during the current

SALP cycle. On April 29, 1996, Mr. E. Merschoff, Director, Division of

Reactor Projects, Region II was on site to tour the Unit 2 Reactor

Building, Auxiliary Building, and the Turbine Building.

8.0

EXIT

The inspection scope and findings were summarized on April 24, 1996 with

those persons indicated by an asterisk in paragraph 1. Interim exits

were conducted on March 21, 1996, and March 28, 1996 .

The inspector

described the areas inspected and discussed in detail the inspection

results. A listing of inspection findings is provided. Proprietary

information is not contained in this report. Dissenting comments were

not received from the licensee.

ENCLOSURE 2

I

39

Item Number

Status

Description and Reference

NCV 269,270,287/96-04-01

Closed

Inadequate Procedure For Adjusting Chevron

Packing (Paragraph 3.3.5)

URI 269,270,287/96-04-02

Open

Potential Inoperability of SSF Due To

Inoperable Isolation Valves (Paragraph

4.1)

VIO 269,270,287/96-04-03

Open

Failure to Follow Procedure for Drawing

Controls (Paragraph 4.3)

VIO 269,270,287/95-15-01

Closed

Failure to Properly Frisk Personnel

(Paragraph 5.11.1)

EEI 269,270,287/94-21-01

Closed

Keowee Air Circuit Breaker (ACB) Air

System Not Controlled as QA Safety Related

System (Paragraph 4.5.1)

IFI 269,270,287/95-30-02

Closed

Propane Issue (Paragraph 4.5.2)

DEV 269,270,287/94-24-05

Open

Improper Code Classification (Paragraph

4.5.3)

IFI 269/94-16-04

Closed

HPI Pump Runout Flow Test (Paragraph

4.5.4)

LER 269/95-06

Closed

LPI Past Inoperable Due to Inadequate

Vendor Information Causing Calculation

Errors (Paragraph 4.5.5)

LER 269/93-06

Closed

Design Deficiency In a Condition Outside

the Design Basis of Containment for a Main

Steam Line Break (Paragraph 4.5.6)

URI 269/96-04-04

Open

Root Cause Assessment of Failures to

Valves 1MS-77 and 1LPSW-254 (Paragraphs

3.3.2 and 3.3.3)

LER 269/95-07, Rev.1

Closed

LPI Technically Inoperable (Paragraph

3.3.3)

8.0

ACRONYMS

ACB

Air Circuit Breaker

ALARA

As Low As Reasonably Achievable

ASME

American Society For Mechanical Engineers

BHUT

Bleed Holdup Tank

BTO

Block Tagout

ENCLOSURE 2

40

BWST

Borated Water Storage Tank

CFR

Code of Federal Regulations

CC

Component Cooling

CCW

Condenser Circulating Water

CPM

Counts Per Minute

CR

Control Room

CRDM

Control Rod Drive Mechanism

DBA

Design Basis Accident

D/P

Differential Pressure

ED

Electronic Dosemetry

EEI

Apparent Violation

EFW

Emergency Feedwater

EPSL

Emergency Power Switching Logic

EOC

End Of Cycle

ES

Engineered Safeguards

FW

Feedwater

GL

Generic Letter

GPM

Gallons Per Minute

GPH

Gallons Per Hour

HP

Health Physics

HPI

High Pressure Injection

ICS

Integrated Control System

I&E

Instrument & Electrical

IFI

Inspector Followup Item

IR

Inspection Report

KHU

Keowee Hydro Unit

LDST

Letdown Storage Tank

LER

Licensee Event Report

LCO

Limiting Condition for Operation

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

MP

Maintenance Procedure

MSLB

Main Steam Line Break

MVA

Mega Volts-Amps

MW

Megawatts

NCV

Non-Cited Violation

NLC

Non-Licensed Operator

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

ONS

Oconee Nuclear Station

OEP

Operating Experience Program

PCE

Personnel Contamination Exposure

PSID

Pounds Per Square Inch Differential

PSIG

Pounds Per Square Inch Gauge

PM

Preventive Maintenance

PIP

Problem Investigation Process

RCA

Radiological Controlled Area

RCS

Reactor Coolant System

ENCLOSURE 2

44

  • I

41

REM

Roentgen Equivalent Man

RWP

Radiation Work Permit

RPS

Reactor Protection System

RFO

Refueling Outage

SOER

Significant Operating Event Report

SFP

Spent Fuel Pool

SSF

Standby Shutdown Facility

TEDE

Total Effective Dose Equivalent

TDEFW

Turbine Driven Emergency Feedwater

TS

Technical Specification

URI

Unresolved Item

VIO

Violation

WCC

Work Control Center

WO

Work Orders

WR

Work Request

ENCLOSURE 2