ML15118A270

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Insp Repts 50-269/97-14,50-270/97-14 & 50-287/97-14 on 970907-1018.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML15118A270
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 11/17/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A267 List:
References
50-269-97-14, 50-270-97-14, 50-287-97-14, NUDOCS 9711250360
Download: ML15118A270 (58)


See also: IR 05000269/1997014

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270. 50-287. 72-04

License Nos:

DPR-38, DPR-47, DPR-55, SNM-2503

Report No:

50-269/97-14, 50-270/97-14. 50-287/97-14

Licensee:

Duke Energy Corporation

Facility:

Oconee Nuclear Station, Units 1, 2, and 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

September 7 - October 18, 1997

Inspectors:

M. Scott, Senior Resident Inspector

S. Freeman, Resident Inspector

E. Christnot, Resident Inspector

D. Billings, Resident Inspector

N. Economos, Regional Inspector (Sections M1.10, M1.11.

M1.12, M8.3, and M8.4)

D. Forbes, Regional Inspector (Sections R1.1, R1.2, and

R7.1)

P. Fredrickson, Branch Chief (Sections 08.4, 08.5. M8.1,

M8.2, and E8.4)

Approved by:

C. Ogle, Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9711250360 971117

PDR ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2, and 3

NRC Inspection Report 50-269/97-14,

50-270/97-14,

and 50-287/97-14

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a six-week

period of resident inspection, as well as the results of announced inspections

by three regional based inspectors.

Operations

In general, the conduct of operations was professional and safety

conscious.

(Section 01.1)

The inspectors concluded that both the shutdown and startup of

Unit 3 were performed appropriately. (Section 01.3)

The licensee did not perform a required Technical Specification

surveillance on Units 1 and 3 during the last refueling.

The

affected units were shutdown at the time of discovery and

performance of the surveillance indicated that the involved

instruments were within tolerance.

The licensee issued a Licensee

Event Report after the end of the inspection period. Further

follow up of this issue will be tracked under the Licensee Event

Report.

(Section 01.4)

During a forced shutdown to replace the 3B reactor building

cooling unit fan motor, the licensee successfully completed an

extensive and complex surveillance of.the replacement 3B high

pressure injection pump. The pump had been replaced in parallel

with the reactor building cooling unit fan motor to preclude a

possible future shutdown due to an observed gradual pump

degradation. (Section 01.5)

An Unresolved Item was identified dealing with the failure to

follow the low temperature over pressure procedure guidance.

(Section 03.1)

Poor administrative controls of isolation of Technical

Specification required low pressure service water loads resulted

in a negative finding on the control of out-of-service equipment.

(Section 03.2)

The licensee accurately determined the cause of adverse trends in

configuration control and developed corrective actions to reverse

the trends. However, by the end of the inspection period, the

licensee had not implemented all these actions. Consequently,

configuration control trends remain unchanged. (Section 08.1)

The licensee has completed annual operational assessments in the

areas of communications and procedures. The contents of the

Enclosure 2

2

assessments were relevant to improving plant activities and safety

performance. (Section 08.2)

The inspectors identified a violation for a failure to follow Lee

Steam Station Operating Procedure, Emergency Power Or Back-up

Power To Oconee, which caused the loss of CT-5 and the consequent

loss of Oconee main feeder busses on June 20, 1997.. (Section

08.4)

The inspectors identified a violation for a failure to provide

appropriate instructions for resetting Switchgear 1X lockout in

Keowee Alarm Response Guide SA1/E-04, 600V SWGR IX Lockout Relay.

(Section 08.5)

Maintenance

The inspectors concluded that general maintenance activities were

completed thoroughly and professionally. (Section M1.1)

Overall, maintenance troubleshooting and quarantine of parts in

response to the observed breaker closing coil failure on Keowee

Hydro Unit 2 was good. The replacement of the Y relay timers on

the Keowee safety-related Westinghouse DB-25 and 50 breakers was a

conservative corrective action. (Section M1.2)

Keowee preventive maintenance and testing activities were

general ly completed thoroughly with procedures and work orders at

the job site. The inspectors concluded that with the 1A sump pump

check valve leaking, the 1B sump pump was able to pump at 35 gpm.

This is sufficient to pump down the wheel well sump due to the 2

gpm limit on leakage. Although pump discharge check valve leakage

had been a previous work-around, new valves are scheduled for

installation in the near future. (Section M1.3)

During performance of major modifications to the Units 1 and 2 low

pressure service water piping, the majority of the observed work

was professionally and properly carried out. One of the plugs

installed in a 42-inch pipe was stranded in the pipe when removal

was attempted. Corrective action will occur outside the

inspection period with the licensee forming a Failure

Investigation Process team to investigate the cause and recommend

a possible resolution.

(Section M1.4)

The inspectors concluded that the Unit 3 main turbine generator

voltage regulator automatic card was adjusted in accordance with

procedures and with engineering and supervisory oversight. The

adjustments were consistent with the latest vendor information.

(Section M1.5)

Although problems did occur during emergency start testing of the

Enclosure 2

3

Keowee Hydro Units, overall, the tests were carried out properly

with good pre-job briefs, good test performance, and proper

equipment control.

During testing, a field flash breaker coil

failed (smoldered). Licensee actions in response were

appropriate. (Section M1.6)

Increased leakage from the 2LP-1 valve's body to bonnet joint

resulted in a Unit 2 shutdown to allow for a satisfactory seal

injection repair. The licensee applied appropriate operational

experience review and met current NRC guidance during the repair

effort. Operational controls during the period were good. Final

repair will occur at the next refueling or fuel off load.

(Section M1.7)

Upper surge tank work was well-engineered with good technical work

control. Overall, initial tank condition was good. Use of

uncovered wood in the tanks with minimal foreign material control

was an example of foreign material process weakness that the

licensee addressed prior to work performance. (Section M1.8)

The licensee provided excellent work control in the

lifting/removal of the 1A1 reactor coolant pump with health

physics personnel providing positive support. The pump's impeller

.was missing part of one vane and exhibited what appeared to be

cavitation damage on other vanes. A licensee evaluation was in

progress. (Section M1.9)

A nuclear station modification to replace certain valves and

associated piping in the high pressure injection system was being

performed following applicable code requirements. Prefabricated

subassemblies exhibited good workmanship attributes and material

records were retrievable and in order. Nondestructive

examinations met applicable code requirements: they were performed

and the results interpreted in a conservative manner. (Section

M1.10)

Low pressure service water system modifications to replace certain

valves and LPSW pump minimum flow lines were well planned. Valve

and pipe replacements were being installed consistent with

applicable code requirements and quality criteria.

(Section

M1.11)

Volumetric inservice inspection of designated welds was performed

satisfactorily by qualified and well trained personnel following

approved nondestructive examination procedures.

(Section M1.12)

To reduce the likelihood of peeling polar crane paint and

extensive hanger paint intrusion into refueling activities, the

licensee installed a protective foreign material tent over the

Unit 1 refueling cavity. This was installed prior to opening the

Enclosure 2

0II

4

reactor coolant system and commencing fuel off-load. (Section

M2.1)

The inspectors identified a weakness in the foreign material

exclusion program based on multiple examples of poor foreign

material exclusion practices. (Section M3.1)

The inspectors identified a violation for a failure to translate

.

information from a Westinghouse technical manual to the licensee's

maintenance procedure for the DB-25 circuit breakers.

(Section

M8.1)

The inspectors identified a non-cited violation for a failure to

provide detailed guidance in the preventive maintenance procedure

for measuring the timer settings for the Y coil in DB-50 breakers.

(Section M8.2)

Engineerino

The inspectors identified one violation in which improper

assessment of emergency feedwater valve operation resulted in a

recurrence of a previous component failure in the emergency

feedwater system. (Section E1.1)

The failure to ensure complete removal of unqualified thermal

insulation from the reactor buildings caused an inaccurate

calculation of operability and resulted in a violation based on

inadequate corrective action. (Section E1.2)

The inspectors concluded that the engineering real-time support

for a Keowee Hydro Unit emergency start test was effective.

The

performance of the failure investigation group in identifying the

failure mechanism for the Y relay timer was excellent. A review

of the present timer logic network for possible modification is

considered an example of good safety attitudes. (Section E2.1)

The test of reactor building cooling unit breakers was performed

in accordance with an approved procedure, by knowledgeable

personnel. and with engineering oversight. The inspectors

considered the breaker testing activities by the engineering,

maintenance, and procurement quality assurance personnel to be

good. (Section E2.2)

Failure to evaluate heavy load lifts over safety-related

components while Unit 1 was above cold shutdown conditions

resulted in a violation. (Section E3.1)

The inspectors identified a violation for a failure to implement a

modification inside the licensee's approved modification process.

Enclosure 2

5

resulting in the modification not receiving a post-modification

test. (Section E8.4)

Plant Support

Based on observations and procedural reviews, the inspectors

determined the licensee was effectively maintaining controls for

personnel monitoring, control of radioactive material,

radiological postings, and radiation area and high radiation area

controls as required by 10 CFR Part 20. (Section R1.1)

The inspectors determined the licensee's programs for controlling

exposures as low as reasonably achievable were effective and

management demonstrated strong support for the program. (Section

R1.2)

A violation was identified, with two examples, for inadequate

radiation protection practices and controls which allowed entry

into a posted radiation area without proper dosimetry. (Section

R1.3)

The inspectors determined that the licensee was performing Quality

Assurance audits and effectively assessing the radiation

protection program as required by 10 CFR Part 20.1101. The

inspectors also determined the licensee was completing corrective

actions in a timely manner. (Section R7.1)

Enclosure 2

Report Details

Summary of Plant Status

Unit 1 operated at 73 percent power, limited by three Reactor Coolant Pumps

(RCPs). until its shutdown September 18, 1997. for a normal refueling outage.

Unit 2 was shutdown from 100 percent power on September 4. 1997. for seal

injection. repairs to a non-isolable valve (2LP-1), off the Reactor Coolant

System (RCS). Following completion of the repairs, Unit 2 resumed power

operations on September 11, 1997. and remained at power through the remainder

of the inspection period.

Unit 3 was shutdown from 100 percent power on September 27. 1997, to replace

the 3B reactor building cooling unit (RBCU)

fan motor, as well as the

degrading 3B High Pressure Injection (HPI)

pump.

The unit was returned to

power on October 11, 1997.

Review of Updated Final Safety Analysis Report (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected.

The

inspectors verified that the UFSAR wording was consistent with the observed

plant practices, procedures, and parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707. the inspectors conducted frequent

reviews of ongoing plant operations. In general the conduct of

operations was professional and safety-conscious: specific events and

noteworthy observations are detailed in the sections below.

01.2 Keowee Hydro Unit (KHU) Emergency Start Test

General Comments (71707)

The inspectors observed the performance of the Keowee emergency start

test conducted on September 16. 1997. This test occurred over several

days, with delays due to instrumentation problems and an equipment

failure. This is discussed in Section M1.6 and E2.1 of this report.

During this period, operations personnel were positive in their control

of Technical Specification (TS) electrical equipment.

Enclosure 2

7

01.3 Unit 3 Shutdown and Startup Observations (71707)

a. Inspection Scope (71707)

The inspectors observed Unit 3 shutdown activities on September 27 and

startup activities on October 10 and 11. Unit 3 was shutdown due to a

testing failure of the 3B RBCU fan motor.

The motor had failed during

survei lance PT/O/A/0160/06 (Problem Investigation Process (PIP) 3-97

3068).

Specifically, the running fan was shutdown from fast speed and

it failed to restart in slow speed, requiring unit shutdown and motor

replacement. (See Section E2.2.)

b. Observations and Findinqs

The motor failure placed the unit in a Limiting Condition for Operation

(LCO) that could not be satisfied without a unit shutdown. The licensee

shutdown the unit prior to the end of the LCO time limit.

Both shutdown and startup were characterized by clear operator

communications, effective control by shift supervision, and management

oversight.

Shift management was present in the control room.

The plant

manager was also present for the startup in a management overview

capacity. During unit heat up prior to startup, the licensee identified

leakage of 2 drops per minute and 12 drops per minute from two different

RCS temperature instruments.

The licensee evaluated these leaks as

acceptable. It was observed that RCS leakage had not increased since

the unit restart.

c. Conclusion

The inspectors concluded that both the shutdown and startup of Unit 3

were performed appropriately.

01.4 Missed TS Surveillance

a. Inspection Scope (61726)

On October 10, 1997. the licensee discovered that the maintenance

performed surveillances (IP/0/A/0203/001C) for the low pressure

injection ([PI) flow and reactor building (RB)

spray flow instruments

(TS Table 4.1-1, Item 29) were not performed at their last required due

date (i.e., at the respective refueling outage for Units 1 and 3).

The

inspectors followed the licensee activities.

b. Observations and Findings

On October 10, the licensee called the inspectors to inform them that TS

surveillance performance mistakes had occurred on Units 1 and 3. This

was just prior to the Unit 3 startup following replacement of a RBCU fan

Enclosure 2

8

inspectors verified that Unit 2 surveillances had been performed.

The licensee performed the overdue surveillances on Unit 3 and then on

Unit 1. The results indicated that the flow instruments were within

tolerance. The licensee was investigating this issue at the end of the

inspection period.

c. Conclusions

The licensee did not perform a required TS surveillance on Units 1 and 3

during the last refue ing. The affected units were shutdown at the time

of discovery and performance of the surveillance indicated that the

involved instruments were within tolerance. The licensee issued a

Licensee Event Report after the end of the inspection period.

Further

follow up of this issue will be tracked under the Licensee Event Report.

01.5 Abnormal HPI Pump Configuration for Full Flow Test

a. Inspection Scope (71707, 61726)

As a part of the forced shutdown for the 3B RBCU repairs, the licensee

decided to replace the 3B HPI pump to preclude a subsequent possible

forced outage. The inspector followed the replacement, especially the

off-normal testing of the pump.

b. Observations and Findings

Normally, an HPI pump is full flow tested at the end of an outage with

the RCS at atmospheric pressure, ambient plant conditions, and the steam

generator RCS handholds open to containment pressure. Following the

replacement of the 3B HPI pump, the licensee decided to perform the

inservice full flow test with the RCS at about 340 degrees F and 370

psig and a pressurizer level of approximately 120 inches.

This testing

condition was markedly different from that normally used for outage full

flow testing and required special testing.

Preparations for the test and inspector observations were as follows:

-

The inspector found the simulator training for the evolution

excellent with attentive procedure writers, a senior reactor

operator, a general office engineer, and training personnel on

hand to debug the test procedure and address any concerns that the

operations shift crews had. An operations manager observed the

training.

-

The licensee contacted other Babcock and Wilcox (B&W)

plants and

questioned their staff about full flow testing.

They had obtained

a test that had been successfully utilized at another facility

that was very simila.r to the mode of testing that they had planned

Enclosure 2

9

a test that had been successfully utilized at another facility

that was very similar to the mode of testing that they had planned

to utilize and incorporated its salient points into their test.

-

The licensee had debugged the test using the system and component

engineers.

-

The test had been thoroughly reviewed by the plant review

committee.

The test was completed as predicted with the pump performing in an

acceptable manner. The pump slightly exceeded the manufacturer's pump

head curve. Data collected during the test was compared with previous

tests and used to enhance simulator response.

c. Conclusions

During a forced shutdown to replace the 3B RBCU fan motor, the licensee

successfully completed an extensive and complex surveillance of the

replacement 3B HPI pump. The pump had been replaced in parallel with

the RBCU fan motor to preclude a possible future shutdown due to a

observed gradual pump degradation.

02

Operational Status of Facilities and Equipment

02.1 Unit 1 Outage Schedule

Due to a multitude of problems, Unit 1 ended the period 10 days behind

schedule. Because of the potential for thermal heat stress, due to

auxiliar fan coolers not being initially available, the licensee could

not sa ey perform many reactor building entries to complete early

outage work. Additionally, the polar and jib cranes in the RB required

additional work and repairs. The refueling machinery broke down several

times during its setup and early operation requiring additional repair

time. The licensee indicated that the refueling machinery is to be

replaced next outage.

03

Operations Procedures and Documentation

03.1 Failure to Follow Low Temperature Over Pressure (LTOP)

Procedure

a. Inspection Scope (71707)

The inspectors reviewed procedures, problem investigation forms, and

interviewed personnel following the identification of a LTOP procedure

problem.

Enclosure 2

10

b.

Observations and Findings

TS 3.1.2.9 requires two trains of LTOP be operable when the RCS is less

than or equal to 325 degrees F and an RCS vent path capable of

mitigating the most limiting LTOP event is not open. Two trains of LTOP

consist of: (1) one train being the power operated relief valve set at

less than or equal to 480 psig; and (2) controls to assure 10 minutes

are available for operator action to mitigate an LTOP event.

Procedure OP/1/A/1104/49, Low Temperature Overpressure Protection,

requires verification that pressurizer levels 1, 2. and 3 are not in

Inserted Value, Scan Lockout, or No Alarm Check on the Operational Aid

Computer (OAC)

to meet TS 3.1.2.9.

The Shift Turnover Checklist and

PT/1/A/600/01, Periodic Instrument Surveillance, requires checks to be

made to ensure the requirements remain in effect during LTOP conditions.

If these conditions cannot be met, a dedicated LTOP operator must be

established.

On September 19, 1997, with the RCS less than 325 degrees and LTOP

required, two of the three required pressurizer alarms were placed in

OAC "no alarm status" for low pressurizer level without stationing a

dedicated LTOP operator. This resulted in the second train of LTOP

being in a -degraded state for 62 minutes before operators recognized and

replaced the alarm points back in service. However, this was within the

4-hour LCO time constraint.

The licensee is continuing to evaluate the cause and corrective actions

for this occurrence under PIP report 1-097-3047.

This item will be

identified as Unresolved Item (URI) 50-269/97-14-01, Failure to Follow

LTOP Procedure, pending completion of the evaluation.

c. Conclusions

An URI was identified dealing with the failure to follow the LTOP

procedure guidance.

03.2 Premature Exit of TS LCO

a. Inspection Scope (71707)

The inspector reviewed the circumstances surrounding the Unit 2 exit of

an LCO prior to completing all required actions.

b. Observations and Findings

For Units 1 and 2 there is a shared low pressure service water (LPSW)

system. TS 3.3.7 requires 3 LPSW pumps to be operable. The TS bases

states that 2 LPSW pumps are required provided that one unit is defueled

and the following LPSW loads are isolated on the defueled unit (in this

Enclosure 2

0II

11

case Unit 1): reactor building cooling units, component cooling cooler,

main turbine oil tank coolers, reactor coolant pumps, and low pressure

injection coolers.

On October 10. 1997, at 4:20 a.m.. Units 1 and 2 entered a 72-hour LCO

per TS 3.3.7 following removal of the C LPSW pump from service for

outage related work. The LCO expiration date was October 13, 1997, at

4:20 a.m. Unit 2 exited the LCO at 8:43 a.m. on October 12, 1997, with

the completion of Unit 1 core off-load and Unit 1 LPSW load isolations

performed by the day shift Operations crew. In its defueled state. Unit

1 had no LCO.

On October 12, 1997, with the first LCO supposedly exited, preparations

were in progress to remove electrical bus 1TC from service for outage

work. This would remove the A LPSW pump from service and place Unit 2

in a second 72-hour LCO until the A LPSW pump could be powered from 2TC

(approximately one hour).

Prior to the second LCO entry, the night

shift operators questioned the administrative controls for the Unit 1

LPSW loads previously isolated for compliance with the first LCO.

Subsequently, all loads which should have been isolated were found to be

isolated except for the LPSW to the Unit 1 component cooling cooler.

The cooler isolation valves were found open with flow through the

cooler. At this point, operations isolated the Unit 1 component cooling

cooler, revised the log to show exiting the LCO (October 12, 1997, at

4:30 a.m.), initiated PIP 2-097-3488, and informed operations

management. They verified and tagged the other LPSW loads with white

control tags. Importantly, due to the night shift's attention to

detail, the second LCO was not entered until the first LCO conditions

were met for a proper exit and the first LCO was properly exited prior

to the end of its 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limit.

Discussions with operations personnel verified that, in this case. there

were no tags hung for the initial entry into the first LCO. Local

instructions did not specifically require tags to be hung.

Historically, no positive means had been required to control equipment

isolated during an outage for TS reasons. The licensee will evaluate

and correct the causes following completion of the PIP evaluation.

c. Conclusions

Poor administrative control of the isolation of TS required loads

resulted in a negative finding on the control of out-of-service

equipment.

Enclosure 2

12

08

Miscellaneous Operations Issues (92901)

08.1 Assessment of Mispositioning Events

a. Inspection Scope

Licensee management observed that configuration problems had an adverse

trend. After the 3LP-40. 3HP-5, and 2HP-96 misposition events that

occurred in the last 12 months, the licensee formed a Continuous

Improvement Team (CIT) to review misposition problems at the Oconee

site. The residents validated the database used by the team and

reviewed the assessment output.

b. Observations and Findings

Beginning February 27, 1997, the licensee identified an adverse trend in

configuration control over the previous several months.

The licensee

documented this trend in PIP 0-097-0737 and organized a CIT to

investigate the trend and provide solutions.

The CIT attributed the

cause of the trend to several factors, including work practices and work

processes. It was determined that a large majority (76 percent) of the

mispositioning events from January 1996 to July 1997 were caused by

either inattention to detail or misjudgement.

The CIT recommended seven

main corrective actions and several sub-actions to address these

concerns. As of this inspection period, the licensee had implemented

one of these recommendations and partially implemented two others.

One partially implemented CIT recommendation called for verification of

worker skills regarding human performance. The corrective action

documented in PIP 0-097-0737 for this recommendation indicated that a

practical factors skills test would be developed and implemented for the

maintenance and work control groups before June 1998. Additionally, the

inspectors observed the practice of having managers present during

critical plant evolutions specifically checking on human performance.

The inspectors determined that this activity did indeed verify these

skills.

The inspectors agreed that the licensee accurately determined the cause

of adverse configuration control trends. The inspectors further agreed

that some of the developed corrective actions were adequate to reverse

the trends. However, the trend of overall configuration control

problems has remained constant. Mispositionings have not worsened, but

neither has any improvement been noted. Significant problems did occur

during the first part of 1997. Since the shift in management emphasis

has occurred, the significance of the mispositionings has not been as

great. Implementation of additional corrective action may reduce the

number of mispositionings.

Enclosure 2

c. Conclusions

The licensee accurately determined the cause of adverse trends in

configuration control and developed corrective actions to reverse the

trends. However, by the end of the inspection period, the licensee had

not implemented all these actions. Configuration control trends remain

unchanged.

08.2 Licensee Operational Internal Assessments

a. Inspection Scope

After several operational problems during this Systematic Assessment of

Licensee Performance (SALP) period, the licensee refocused, adding

emphasis to their normal annual assessment. These assessments are

performed in accordance with the licensee's Nuclear Policy Manual. NSD

607, Appendix A, Group Assessments. The assessments were in the

following areas:

-

Operations Communications SA-97-29 (ON)(OPS) of August 8, 1997,

through September 11, 1997

-

Operations Procedures 97-38 (ON)(OPS) of October 1. 1996, through

October 1, 1997

The inspectors validated the issues and reviewed the assessment output.

b. Observations and Findings

As a product of their annual assessment process, the operations group

completed two assessments that were meaningful, producing good overall

recommendations and findings. The assessments were sensitive to issues

addressed in recent augmented inspections and NRC operations licensing

comments on annunciator response guidance and three-way communication

discussed in Inspection Report (I

R) 50-269.270.287/97-05. The

communication assessment produced changes to existing procedural

guidance with 28 clear recommendations. The procedure groups had

increased the procedure change rate from 140 changes per year in 1996 to

396 in 1997 through (September 1997). This increase in procedure

production was indicative of a higher awareness of procedure problems

and less of a tendency to work around them. Accompanying the higher

production rate was an increase in demand rate with production lagging

behind a new demand of 330 change requests yet to be processed for 1997.

Highlights of the communications assessment recommendations were:

preplanning of re-qualification cycle with management involvement;

operations crew round sheet review at shift briefing shall be

Enclosure 2

14

consistent between shifts:

operations shift meeting improvements to provide improved shift to

shift turnover and focus at the meeting;

standardization of communication techniques;

systematic review of alarm response guides for the removal of

instructional steps and the placing of those steps in appropriate

procedures;

creation of a video for standard simulator communications;

develop procedural usage guidance and training on operations

radios (dead spaces in plant);

purchase cellular phones for non-licensed operator (NLO)

and

operator usage;

0

improve external communication through training and management

oversight; and

improve NRC, plant staff, and management notification process.

The notification improvements have begun. starting with an informational

badge containing a call-out list that was distributed to the on-shift

managers.

Highlights of the procedure assessment that have been implemented were

as follows:

-

procedure owners had been designated:

-

shift personnel were involved.in the procedure review process:

-

lower tolerance for procedure deficiencies had been clearly

communicated with the staff;

-

procedures found missing any critical parts are removed from use;

and

-

a qualified reviewer and reactivity management review checklist

has been incorporated into the procedure review checklist.

The inspectors have observed many of the above improvements during the

last several months inclusive of the reactivity review check sheet with

procedure changes and many additional corrective action items dealing

with procedure related problems. Although special evolutions drove

their creation, recently issued and used procedures for the Unit 3 full

Enclosure 2

15

flow test and the Unit 1 startup on three RCPs were professionally

competent instructions.

c. Conclusions

The licensee has completed annual operational assessments in the areas

of communications and procedures. The contents of the assessments were

relevant to improving plant activities and safety performance.

08.3 (Closed) URI 50-269,270,287/97-01-05: LPSW Piping to the RB Cooling

Inoperability

This issue was captured under URI 50-269,270.287/97-01-05 and LER 50

269,270,287/97-002. Due to the complexity of this Generic Letter 96-06

issue, it will not be closed until approximately mid 1998.

PIPs 97

0240, 0310, and 0311 are the internal licensee corrective action

documents. Paft operability will be examined during the LER closure

review. According y, this URI is closed.

08.4 Conduct of Lee Steam Station Operations

a. Inspection Scope (92901)

The inspectors eviewed the results of the Augmented Inspection Team

(AIT) NRC Inspection Report 50-269,270.287/97-11. Section 01.1. for

ossible NRC enlforcement action related to the circumstances involving

ee Steam Station for the Oconee event of June 20, 1997.

b. Observations and Findings

As documented in the AIT report, on June 20. 1997. Oconee was in the

p

rocess of perfbrming Surveillance Procedure PT/1/A/0610/06. 100 Kilo

Volt (KV) Power Supply From Lee Steam Station. This surveillance was

required by TS 4 6.7 to be performed at least every 18 months, usually,

concurrent withian Oconee Unit 1 refueling outage. In addition to

Procedure PT/1/A/0610/06, Procedure OP/0/A/1107/03A. Oconee Nuclear

Station and LeelSteam Station and Lee Procedure Emergency Power Or Back

up Power To Ocoee were also used to accomplish the surveillance.

Procedure OP/O/A/1107/03A primarily involved verification of certain

breaker alignments prior to starting the Lee gas turbines.

On June 20, 1997. at the request of Oconee. Lee operators had paralleled

the 6C gas turbine to the grid per Enclosure 6.1 of Lee operating

procedure Emergency Power or Backup Power to Oconee.

The Lee control

operator (LOA)

and Lee assistant control operator (LOB)

were performing

steps for the 60 Lee gas turbine in the Lee control room and were also

monitoring the control boards for the three operating fossil units.

The

LOA and LOB werd notified by Oconee operators that breaker alignments at

Oconee were complete, and Lee Operators could initiate steps to dedicate

Enclosure 2

16

Lee.

The alignment that dedicated Lee were steps 6.1.5 through steps

6.1.9 of Enclosure 6.1 of Lee steam station operating procedure. Step

6.1.5, first required switcher 89-3 to be closed and then step 6.1.6

required switcher 89-2 to be open.

The Lee operator performed steps

6.1.5 and steps 6.1.6 in reverse. First, opening switcher 89-2 caused

the operating 6C Lee gas turbine generator to be separated from the

grid, causing it to slightly overspeed.

When 89-3 was closed, the 6C

Lee gas turbine was now slightly tied out-of-phase with respect to the

grid. This caised a voltage surge which resulted in OCB-13 and breakers

SLi and SL2 tripping. Consequently, CT-5 was deenergized, resulting in

the loss of voltage on the Oconee main feeder busses (MFBs),

and causing

Keowee Units 1 and 2 to emergency start. The 6C Lee turbine generator

continued to operate, following the separation from the system.

The

gas turbine continued running until it was stopped by Lee operators 20

minutes after the event. Failure to follow the Lee Station Procedure as

dictated by thd Oconee periodic test procedure is a violation of TS 6.4.1 and is identified as Violation (VIO) 50-269,270,287/97-14-02:

Failure to Adequately Implement Lee Station Procedure.

c. Conclusions

The inspectors identified a violation for a failure to follow Lee Steam

Station Operating Procedure Emergency Power Or Back-Up Power To Oconee

which caused the loss of CT-5 and the consequent loss of Oconee MFBs on

June 20. 1997.

08.5 Adequacy of Keo ee Alarm Response Guide (ARG)

a. Inspection Scope (92901)

The inspectors reviewed the results of the NRC AIT Inspection Report 50

269,270,287/97-11, Section 01.2. for possible NRC enforcement action

related to the adequacy of Keowee ARG SA1/E-04, 600V SWGR 1X Lockout

Relay, Revision 7.

b. Observations and Findings

As documented in the AIT report, on June 23. 1997. after a Switchgear 1X

lockout, the Ke6wee operator referenced ARG SA1/E-04. Subsequently, the

operator, after noticing that no protective relay action had occurred,

checking the position of the breaker impact springs in Air Circuit

Breaker (ACB) 5 and ACB 7, and contacting the on-call technical support

specialist, reset the impact spring in ACB 7 and reset the lockout relay

for Switchgear 11X.

This action resulted in ACB 5 and ACB 7 attempting

to close and then tripping open.

The inspectors noted that the licensee had characterized the cause of

the blown fuses as an unanticipated circuit operation following the

operator's actioh to reset the lockout condition.

As immediate

Enclosure 2

17

corrective action, the licensee revised ARG SA1/E-04 (and also ARG

SA2/E-04),

to gequire the transfer scheme for Switchgear 1X and

Switchgear 2X to be placed in manual (in lieu of automatic), prior to

the resetting of a lockout condition in order to preclude both breakers

(ACB 5 and ACB 7 or ACB 6 and ACB 8) that supply power to the associated

switchgear from receiving close signals at the same time. The

inspectors condluded that ARG SA1/E-04 was inadequate because it allowed

the operator td reset the lockout with the transfer scheme in automatic,

which caused the unanticipated circuit response and blown fuses.

The

inspectors alsd concluded that this inadequacy was self-revealing.

Failure to provide ARG SA1/E-04 with appropriate instructions is a

violation of TSi 6.4.1 and is identified as VIO 50-269,270,287/97-14-03:

Failure to Provide Appropriate Lockout Reset Instructions in ARG SA1/E

04.

c. Conclusions

The inspectors Identified a self-revealing violation for a failure to

provide appropriate instructions for resetting. a Switchgear 1X lockout

in Keowee ARG S 1/E-04. 600V SWGR 1X Lockout Relay.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707. 61726)

The inspectors observed all or portions of the following maintenance

activities:

WR 97039351

DC Grounds

WOs 97083263

Replace Y Relay Timers on KHU Field

thrd

and Field Supply Breakers

97083267

WO 97070657

Check/Calibrate Unit 3 Generator Auto

Voltage Regulator

WO 97084027

Remove and Test Unit 3 RBCU B Breaker

WO 97080988

Repair and Test KHU 2 Field Breaker

WO 97004486

Repair Stuck Float KHU-1 AC Sump Pump

  • 0

WO 97082577

3B RBCU Failed to Start

Enclosure 2

18

WO 97084015

Perform Char Analysis on Unit 3A RBCU

Motor

WO 97084329

RBCU 3B motor removal

WO 97076613

Leak Repair Bonnet Leak on 2LP-1

TSM-1376

Minor Modification for Leak Repair on 2LP

1

IP/0/A/3000/018A

Ground Hog DC System Ground Location

MP/0/A/1800/016

System Leakage Repairs Using Vendor

I

Injection Methods

PT/1/A/2200/019

KHU-1 Turbine Sump Pump 1ST Surveillance

PT/0/A/0620/016

Keowee Hydro Emergency Start Test

TN/2/A/1376/TSM/00M

Leak Repair Bonnet Leak on 2LP-1

ONQE 10447

Perform 14-inch and 36-inch Wet Taps On

the LPSW A Line

  • ON 1301

Units 1 and 2 LPSW Pumps Minimum Flow

Lines (Outage Portion)

IP/0/B/0200/023B

RCP Motor Temperature, Speed, and

Vibration Instrumentation Calibration and

Logic Test

WO 97081682-01

Corrective WO for Unit 2 Voltage Regulator

B Chattering and Has Smokey Odor

IP/S/A/0100/001

Controlling Procedure for Troubleshooting

and Corrective Maintenance

PT/i

and 3/A/0251/027

HPI Pump Developed Head Test [at power]

OP/K/A/110e3/11

Drain and Nitrogen Purge of the RCS to

Less Than 50 Inches

MP/O0/A/1800/022

Directions for Using a Video Camera to

Look at Potentially Damaged Marbo Plug

IP/0/A/3011/014

1FDW-19 Infrared Thermography Scanning for

Electri cal Components

Enclosure 2

19

0 PT/0/A/0750/13

Miscellaneous Visual Inspection of Fuel

Assemblies

b. Observations and Findings

The inspectors found the work performed under these activities to be

professional and thorough. All work observed was performed with the

work package present and in use. Technicians were experienced and

knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

The visual inspection of the fuel assemblies during the Unit 1 core off

load identified 4 fuel assemblies with slipped spacer grids and 22

assemblies with minor grid damage. These occurrences are captured by

PIP 1-97-3381. Based on their evaluation, the licensee will make core

reload changes as necessary.

c. Conclusion

The inspectors concluded that the maintenance activities listed above

were completed thoroughly and professionally.

M1.2 Keowee Breaker Repairs and Timer Change Out

a. Inspection Scope (62707)

The inspectors observed and reviewed maintenance activities involved

with the failed closing coil on the KHU 2 generator field breaker.

The

coil failed during KHU performance testing. Sections M1.6 and E2.1 of

this report discuss the failure.

b. Observations and Findings

The inspectors reviewed procedure IP/O/A/2001/003B, Inspection and

Maintenance of DB-50, DB-25. and DBF-16 Circuit Breakers and Work Order

(WO) 97080988. The inspectors observed portions of the maintenance

activities. The activities consisted of the following:

removal and quarantine of the breaker with the failed coil:

checking the replacement breaker from the warehouse:

setting up the test equipment for the performance of the

inspection procedure on the replacement breaker;

performance of the inspection procedure: and

Enclosure 2

20

0 installation of the replacement breaker.

Following completion of the above maintenance activities, KHU 2 was

tested and returned to operable status.

This event was discussed in PIP K-97-2983. Based on the failed relay

coil root cause, the licensee made the conservative decision to change

out the Y relay timers in all safety-related breakers of this type. The

timers were located in the direct current (DC)

generator field breakers

and the alternating current (AC) field supply breakers for both Keowee

units, as well as the spare breakers. The inspectors observed the work

activities (similar to those discussed above), reviewed the procedure,

and discussed the results with licensee personnel.

c. Conclusions

Overall, maintenance troubleshooting and quarantine of parts in response

to the observed breaker closing coil failure on Keowee Hydro Unit 2 was

good. The replacement of the Y relay timers on the Keowee safety-related

Westinghouse DB-25 and 50 breakers was a conservative corrective action.

M1.3 KHU 1 Inservice Testing and Preventive Maintenance

a. Inspection Scope (62707)

The inspectors reviewed and observed inservice testing (IST) and

preventive maintenance (PM) activities at the KHU. The PMs involved

circuit breakers and the IST involved the turbine wheel well sump pumps.

b. Observations and Findings

The quarterly PMs were performed on the generator field AC supply

breaker, the DC field breaker, and the air circuit breakers (ACB). A

previous failure of an ACB was caused by an air leak. The PM required

that a check for air leaks be performed. No air leaks were observed.

The inspectors observed the use of procedure PT/1/A/2200/019, KHU-1

Turbine Sump Pump.IST Surveillance, Revision 4. The sump pumps are

associated with TS 3.7, but are not addressed in the TS or the Selected

Licensee Commitments as attendant equipment. One pump will keep the

sump pumped and water off the important equipment in the area protected

by the sump. The KHU wheel wells have a continuous leak-off of less

than 2 gpm required by procedure. The procedure verified that the leak

off was less than 2 gpm. The test included pump performance and

vibration data collection.

The sump system is equipped with a DC driven pump (iB)

and an AC driven

pump (lA).

The pumps were each expected to remove 400 gallons from the

wheel well sump in seven to eight minutes. The 1 pump took between 11

Enclosure 2

0

21

and 12 minutes during the initial test. The inspectors observed that

the check valve on the 1A pump was leaking and diverting water back to

the sump. Accordingly, the normally open discharge valve on the 1A pump

was closed by procedure and the test was re-performed. Adequate results

were then obtained for the 1B pump. The inspectors observed that the

check valve on the 1B pump did not leak back to the sump during the 1A

test.

The time for the 1A pump was between seven and eight minutes.

The poor performance of the 1A discharge check valve was a potential

work-around that has been recently re-recognized and addressed by the

licensee. PIP K-95-1343 had been open since October 1995 on this check

valve issue. Minor modifications, one for each KHU (OEs-10468 and

10470), have been initiated to replace the check valves on all four

pumps (two per KHU) under work packages. Replacement valve availability

ad caused some of the corrective action delay. New stainless steel

valves, in lieu of bronze material, were scheduled to be installed in

the January 1998, time frame.

c. Conclusions

Maintenance and testing activities were generally completed thoroughly

with procedures and work orders at the job site. The inspectors

concluded that with the 1A sump pump check valve leaking the 1B sump

pump was able to pump at 35 gpm.

This is sufficient to pump down the

wheel well sump due to the 2 gpm limit on leakage. Although pump

discharge check valve leakage had been a previous work-around, new

valves are scheduled for installation in the near future.

M1.4 LPSW Modification ON0E 10447

a. Inspection Scope (62707,37551)

The inspector reviewed the procedures, interviewed personnel, and

observed activities associated with the modifications on the common LPSW

system for Units 1 and 2. (For further details on the modifications,

see Section M1.11)

b. Observations and Findings

The inspector observed the pipe preparation and welding of several wet

taps for Marbo plug installation, including the 36-inch wet tap

connection for the 42-inch LPSW pipe. Procedures were on hand with

adequate supervisory and quality control personnel monitoring the

activities. During the placement of the 36-inch isolation valve, it was

identified that the valve, when opened, would impact .a

support.

A

second issue was identified in that the valve and equipment to be used

to cut the pipe were not QA-1 qualified. These items were properly

identified and resolved satisfactorily.

Enclosure 2

22

An additional problem was identified during the attempted removal of the

36-inch Marbo plug when the plug failed to be withdrawn and lodged in

the isolation valve. The plant was in a stable condition and the work

performers were prompt in making checks of the system and its condition,

notifying Operations immediately.

The licensee initiated a Failure

Investigation Process (FIP) team and PIP 1-97-3621 to resolve the

problems.

c. Conclusions

During performance of major modifications to the Units 1 and 2 LPSW

piping the majority of the observed work was rofessionally and

properiy carried out. One of the plugs installed in a 42-inch pipe was

stranded in the pipe when removal was attempted. Corrective action will

occur outside the inspection period with the licensee forming a FIP team

to investigate the cause and recommend a possible resolution.

M1.5 Adiustment of the Unit 3 Generator Voltage Requlator

a. Inspection Scope (62707. 92902)

The inspectors reviewed and observed the calibration check and

adjustment of the Unit 3 main generator voltage regulator automatic

card. The calibration check and adjustment were performed as a result

of a Unit 2 trip on July 6. 1997. The licensee committed to perform a

check of the Unit 3 regulator during the next unit outage.

b. Observations and. Findings

The inspectors documented in IR 50-269.270.287/97-10 the calibration

check and adjustment of the voltage regulator on the Unit 2 main

generator. Licensee personnel used the same procedures and methods for

the check and adjustment of the Unit 3 main generator voltage regulator

as were used on Unit 2. The same technical personnel also performed the

activities.

The section of the voltage control circuit that was checked was the

auto-regulator circuit board which contained a first stage amplifier and

a second stage amplifier. The as-found condition indicated that the

gain for the first stage amplifier was approximately 3.55 to 1 and the

second stage 5.6 to 1. This resulted in an overall gain of

approximately 20 to 1. The requirement per procedure was a gain of 2 to

1 for the first stage and 8 to 1 for the second stage. This would

result in an overall required gain of 16 to 1.

Obtaining the best possible adjustment, the technical personnel adjusted

the first stage gain to 2.06 to 1 and the second stage to 7.8 to 1 with

an overall gain of approximately 16 to 1. The technicians were thorough

and methodical in their actions. The inspectors did not consider the

Enclosure 2

23

as-found overall gain of approximately 20 to 1 as excessive compared to

the required 16 to 1. This unit had responded well during a recent grid

fault that is one of the possible occurrences to which this circuit

responds.

c. Conclusions

The inspectors concluded that the Unit 3 main turbine generator voltage

regulator automatic card was adjusted in accordance with procedures and

with engineering and supervisory oversight. The adjustments were

consistent with the latest vendor information.

M1.6 KHU Emergency Start Test

a. Inspection Scope (61726)

On September 13. the inspectors reviewed, observed, and discussed the

KHU emergency start performance test. The test was a complex

surveillance and required management oversight. The inspectors were

informed that portions of this test were being performed for the first

time on an integrated basis following a modification to the system.

b. Observations and Findings

The complex surveillance was controlled by performance test procedure

PT/0/A/0620/19. Keowee Hydro Unit Emergency Start Test. Revision 22.

The purpose of the test was as follows:

to demonstrate operability of the KHUs' emergency start channel

from each control room and each cable room (Channels A and B);

to demonstrate each KHU will reach rated speed and voltage in less

than or equal to 23 seconds:

to verify KHUs' ACB closes automatically to the underground path;

to verify actuation and times for time delay relays for ACBs 1. 2.

3. and 4 close permissives; and

to demonstrate that each KHU can supply equal to or greater than

25 megawatts (MW) to the system grid.

The inspectors reviewed the test procedure and the management oversight

briefing paper. The inspectors attended the pre-job briefing and

discussed the procedure with licensee personnel.

The inspectors

observed the installation of digital relay timers at the KHUs. The

inspectors also observed operator activities in the Oconee Unit 3

control room and at the KHUs.

Enclosure 2

24

During the performance of the test, the inspectors observed testing

activities up to Section 12.5. To Test Keowee Emergency Start from Unit

3 Control Room (CR),

Subsection 12.5.5, Record Times From Digital

Timers.

The timers associated with ACBs 1, 2 and 3 did not pick up and

the relay times were not recorded.

The timers were installed on

terminal links in selected KHU cabinets and were to time the actuation

of ACBs 1. 2, and 3.

An operability issue was raised concerning the relays for the ACBs.

With the timers not picking up, the issue was whether or not the relays

actuated as required. The test was re-performed up to the relay

actuation with stopwatches being used to time the ACB relays. The

timers again failed to respond, but the visual timing of the relays

indicated acceptable operation.

The test was terminated and the KHUs

were returned to a normal lineup. The licensee found that the timers

were setup for a low trigger signal and they had actuated

prematurely/spuriously on existing circuitry noise.

The licensee made changes to the procedure for the timers to measure

relay contact position, and Revision 23 was issued. On September 16,

1997, the inspectors reviewed,. observed, and discussed the revised

procedure with licensee personnel. The inspectors attended the pre-job

briefing, observed the installation of the digital timers across the ACB

control relays, and observed operator activities.

The inspectors observed portions of the test up to Section 12.6. To Test

Keowee Emergency Start From Unit 3 Cable Room, Subsection 12.6.6. Test

of Channel B. During the performance of this subsection the inspectors

observed a large amount of smoke coming from the KHU-2 generator field

breaker cubicle. KHU-2 was tripped off the line and the breaker was

racked out from the cubicle. Although a large amount of smoke was

present from the field breaker closing coil, no visible flames were

observed. The test was terminated and KHU-2 was declared inoperable.

PIP K-97-2983 and a FIP team were initiated.

The field breaker was exchanged with a breaker obtained from the

warehouse and bench tested satisfactorily. KHU-2 was subsequently

returned to operable status. Additional comments and details on this

item are in Sections M1.2 and E2.1 of this report.

c. Conclusions

For the completed parts of the tests, the inspectors concluded that:

they were performed in accordance with both revisions of the procedure

the pre-job briefings were thorough and well conducted: the participants

demonstrated a questioning attitude concerning operability tests of the

underground path and the ACB timers; the operator actions taken when

smoke was observed were appropriate; operations maintenance of KHU

operability status was appropriate; and management and engineering

Enclosure 2

25

oversight were present. Theactions taken to verify the function of the

ACB re ays were good.

M1.7 Leak Repair of Valve 2LP-1

a. Inspection Scope (62707.37551)

On August 29, 1997, operators detected increased RB unidentified

leakage. As indicated in IR 50-269.270,287/97-12, a RB entry identified

leakage from valve 2LP-1, the LPI suction line isolation valve. The

inspectors observed activities associated with repair of valve 2LP-1.

b. Observations and Findings

The inspectors documented in IR 50-269.270.287/97-12, engineering

activities involved with temporary site modification TSM-1376 and PIP 2

97-2736. The modification was initiated to stop a pressure seal leak on

valve 2LP-1. The inspectors continued to observe, review, and discuss

the modification with licensee personnel. The inspectors also attended

meetings at which TSM-1376 was discussed.

The valve and plant were maintained above cold shutdown for seal

injection repair of the valve. Additionally, the valve had to be

maintained operable throughout the repair; it was opened and maintained

open until post repair stroke tests. The inspectors were informed and

observed that the leakage from valve 2LP-1 had reduced significantly

when the Unit 2 temperature and pressure were lowered from hot shutdown.

The licensee had wanted to initially maintain valve temperature above

250 degrees F for injection sealant reaction purposes. However, the

leakage from the valve resulted in the temperature of the valve falling

below 200 degrees F.

The originally selected sealing compound, referred to as Deacon 800T-N.

had a temperature range of 200 to 900 degrees F with a reaction

temperature of 250 degrees F. The inspectors attended a management

meeting held on September 7, 1997, at which the use of a different

sealing compound.was approved.

The new sealant. referred to as Deacon

400R-N, has a range of 50 to 400 degrees F and reacted with water.

The change in the sealant affected documents previously approved.

Accordingly, the inspectors reviewed the following documents:

Procedure TN/2/A/1376/TSM/00M, Installation of Temporary

Modification TSM-1376;

10 CFR 50.59 evaluation screening for change to TSM-1376 procedure

TN/2/A/1376/TSM/OOM:

Procedure MP/0/A/1800/016, System Leakage Repairs Using Vendor

Enclosure 2

SII

26

Injection Method; and

Work Order 97076613, Leak Repair Bonnet Leak 2LP-1.

The inspectors made the following observations:

the initial measurements at the valve to identify the location of

the four holes to be drilled;

the accounting for such items as drill bits, punches, pneumatic

drills, taps, parts, hand tools, etc., taken into the work area;

coverage of the overall activities by the health physics

personnel;

drilling by hand, tapping, and the installation of the

shutoff/vent valves;

the oversight by maintenance supervision and engineering: and

the final drilling into the valve cavity.

The inspectors noted that those measurements taken by the vendor

personnel for the hole location, the depth of the drilling, and the

shutoff valve thread engagements were accomplished using adequate depth

gauges and calipers. The inspectors also noted that the vendor

personnel consistently used second party verifications for all

measurements.

The inspectors also observed that when the final drilling was in

progress, and the valve cavity was breached, water would come out around

the drill bit. The vendor personnel would immediately remove the drill

bit and close the shutoff/vent valve. This action kept the amount of

additional leakage to a minimum.

A total of 11 cubic inches of the sealing compound, was injected into

the valve, to stop the leak. During the unit startup. the valve was

visually checked for leakage at 500 psig intervals increasing pressure.

No leakage was identified. The temperature of the valve body was

monitored at rated RCS temperature and pressure and indicated 98 degrees

F.

The inspectors discussed the cure-time required for the type Deacon

400R-N sealing compound. The licensee personnel were not aware of the

required cure time for the material. The vendor personnel were able to

identify the cure time as four hours.

The sealant sat for greater than

six hours with no valve operation and the plant at a constant

temperature and pressure. The valve was satisfactorily stroke tested

after the six-hour period.

Enclosure 2

27

The inspectors concluded that the temporary modification was installed

using approved procedures with maintenance supervisory and engineering

oversig t. The inspectors considered the activities performed by the

vendor personnel performing the drilling and injection activities as

excellent.

The inspectors also concluded that the following two items

were not fully addressed by the licensee prior to the modification

activities:

At the management meetings the possibility of the valve cooling

down to a temperature less than 250 degrees F was only briefly

discussed. Had this item been addressed further, plans for an

alternate sealing compound could have been pre-approved.

The cure-time for the type Deacon 400 R-N compound was not

captured in the revised modification package.

These two items did not affect the final installation of the minor

modification.

The inspectors considered the items as minor weaknesses

in the modification activities associated with the 2LP-1 valve leak

repair. The licensee had indicated that cure times would be captured in

associated repair documentation (PIP 97-2736).

c. Conclusions

Increased leakage from the 2LP-1 valve's body to bonnet joint resulted

in a plant shutdown to allow for a satisfactory seal injection repair.

The licensee applied appropriate operational experience review and met

current NRC guidance during the repair effort.

Operational controls

during the period were good. Final repair will occur at the next

refueling or fuel off load.

M1.8 Upper Surge Tank (UST) Inspections

a. Inspection Scope (62707)

IR 50-269.270,287/97-05. Section E1.1, discussed inspections of the Unit

3 USTs 3A and 3B. A NRC violation was issued for inadequate weld

inspection. This period, the licensee continued with the Unit 1 UST

outage inspections (Minor Modification OE-9270, VN 9270B) with the

inspector accompanying quality control (QC)

and engineering personnel

for observations at the job site.

b. Observations and Findings

The work instruction (TN/1/A/9270/MM/01C)

provided clear guidance on the

overall job scope. During the initial job walk down with QC, the QC

inspector pointed out that the stiffener welds made by the original N

stamp vendor were not clearly T by T welds and asked for clarification

on acceptance criteria on those welds. Engineering provided a package

Enclosure 2

28

change prior to inspection and repair commencement.

The tanks looked to

be in reasonably good shape. without major stress or deterioration

indications.

Prior to work commencement, the inspectors observed that wood had been

used inside of the USTs for a scaffold and drain port cover. It was

treated for fire protection, but did not have plastic sheathing for the

prevention of wood debris spread. Procedure NSD 104 indicated that wood

used in such applications "should" be covered with plastic for foreign

material exclusion (FME) purposes. Section M3.1 of this report

addresses FME weaknesses such as this example. Prior to commencement of

the work, the licensee covered the wood with plastic.

c. Conclusions

The UST work was well-engineered with good technical work control.

Overall, initial tank condition was good. Use of uncovered wood in the

tanks with minimal foreign material control was an example of foreign

material process weakness that the licensee addressed prior to work

performance.

M1.9 lA1 Reactor Coolant Pump Removal

a. Inspection Scope (62707)

As discussed previously, the 1A1 RCP had mechanical problems that

required it to be taken out of service and ultimately replaced.

During

its removal from the RCS, the inspectors observed pump body to casing

fastener destructive removal, the actual lifting of the pump out of its

casing, and the placement of the pump into its handling stand for

inspection and root cause failure determination.

b. Observations and Findings

The observed work was performed in a careful and methodical manner.

Particularly, the preparation for and the actual lift of the pump from

the volute were performed in a professional manner. Prior to the lift,

the crew careful y vacuumed the crack area between the pump casing and

top of the pump package to positively prevent material from entering the

soon-to-be-opened RCS. Health physics worked closely with the crew in

limiting dose and maintaining conditions safe for work.

One vane of the pump's impeller was missing approximately six inches of

the outside edge that was roughly triangular in shape.

The apparent

height of the missing piece was about three inches. The piece appeared

to have been mostly eroded away, but there were possible indications of

abrupt breakage on some of the uneven edges. Five of the seven vanes

showed through wall wear, possibly due to cavitation. The licensee was

to provide an evaluation of the failure outside of the inspection

Enclosure 2

0II

29

period. with an independent evaluation provided by the pump vendor.

Additionally, the licensee had planned future inspections of the second

pump (1A2) in that same loop and the other two pumps in the B loop. The

1icensee was scheduling additional inspections of the RCS and vessel for

vane debris.

c. Conclusion

The licensee provided excellent work control in the lifting and removal

of the 1A1 reactor coolant pump with health physics personnel providing

positive support. The pump's impeller was missing part of one vane and

exhibited what appeared to be cavitation damage on other vanes. A

licensee evaluation was in progress.

M1.10 Modification to Replace Valves and Associated Piping in the Unit 1 HPI

System

a. Inspection Scope (73753)

The inspector determined the adequacy of work activities in regards to

the replacement of certain stop and check valves along with small bore

piping in the HPI system:

b. Observations and Findings

Background

Nuclear Station Modification ON-12975 was issued to control the work for

replacing the existing HPI valves 1HP-126, 1HP-127. 1HP-152 and 1HP-153

with new angle check valves. 2 V,-inch diameter. In addition, the

licensee wi l add two 2 V2-inch diameter globe valves to each line for

isolation purposes. The replacement check valves include two one-inch

drain valves on the downstream side of the seating surface to allow for

leak testing. This modification was initiated to replace the subject

valves which performed poorly due to corrosion related problems and for

improvement of performance. Following installation and testing, the new

valves will be closed and used as the isolation valves to prevent RCS

backflow into the HPI system.

Procedure TN/1/A/12975/0/AMI was issued to provide instructions and

documentation for the work activities performed. The modification was

being performed under the American Society of Mechanical Engineers

(ASME) Code Section XI. 1989 Edition. Repair and Replacement IWA-4000.

Weld fabrication inspection and testing were controlled by American

National Standards Institute (ANSI) B31.7, 1968 Edition. Piping was

being replaced up to the safe ends, however, the safe ends and their

function were not affected by the subject modification. The safe ends

were scheduled for visual examination from the pipe internal diameter to

determine their condition. The valves, piping, fittings and

Enclosure 2

30

support/restraints were classified, QA-1 condition. Post-modification

pressure testing of replacement components was scheduled to be done

under Procedure MP/O/A/1720/016.

At the time of this inspection (September 29 - October 2, 1997) the

licensee had completed the welding and nondestructive examinations of

the subassemblies which included the replacement valves and associated

piping. Installation had been delayed until the primary system could be

drained down to the required level.

Observation

As such, the inspector inspected completed subassembly welds to verify

compliance with the above-mentioned code, quality of workmanship and

appearance. In addition, the inspector reviewed quality records for

replacement components, filler metal used and welder performance

qualification. As required by the controlling codes, completed welds

were radiographed to satisfy construction code and preservice inspection

requirements. The applicable radiographic procedures for this

evaluation were NDE-10A, Revision 19 and 12A. Revision 9. The welds

were shot once, in accordance with Procedure NDE-10A, Rev. 19. however,

they were reviewed to the acceptance standards of both procedures to

satisfy construction code and ASME Code Section XI preservice inspection

requirements. Radiographs for the following welds were reviewed to

verify compliance with applicable requirements.

  • eld

Size (inches)

Component

Results

1-RC-201-92

2.5 x 0.375

Valve to Pipe

No

rejectable

indications

(NRI)

1-HP-282-90

4.0 x 0.531

Valve to Pipe

NRI

1-RC-201-91

2.5 x 0.375

Valve to Pipe

NRI

1-RC-200-166

2.5 x 0.375

Valve to Pipe

NRI

1-RC-200-160

2.5 x 0.375

Valve to Pipe

NRI

1-RC-199-150

2.5 x 0.375

Valve to Pipe

NRI

1-RC-199-149

2.5 x 0.375

Valve to Pipe

NRI

By this review, the inspector ascertained that film and radiographic

qualities met the applicable code requirements. The licensee's reviews,

interpretation and documentation of film artifacts and weld indications

Enclosure 2

31

were accurate and.fully documented.

c. Conclusion

A nuclear station modification (NSM)

to replace certain valves and

associated piping in the HPI system was being performed following

applicable code requirements. Prefabricated subassemblies exhibited

good workmanship attributes and material records were retrievable and in

order. Nondestructive examinations met applicable code requirements;

they were performed and the results interpreted in a conservative

manner.

M1.11 Modification to Replace LPSW Valves and Associated Piping (Unit 1)

a. Inspection Scope (62700.55050)

The inspector determined by observation, document review and discussions

with technical personnel, the adequacy of work activities relative to

this modification.

b. Observation and Findings

Backoround

Modifications to the LPSW system to improve system operability and

reliability were in progress at the time of this inspection, September

29 - October 2, 1997.

The modifications were identified as NSM ON

12977, 13001 Part AM2 and 13022. The inspector reviewed the subject

modification packages and held discussions with the cognizant engineers

to gain a better understanding of corrective actions taken and

improvements in plant operabi ity to be achieved by this work effort.

Following is a synopsis of objectives to be achieved by each of the

above modifications.

NSM-12977 Part AMI:

The purpose of this modification was to replace the LPI cooler shell

outlet valves (1LPSW-4 and 5), the RCP inlet isolation valve (1LPSW-6)

and RCP outlet isolation valve (1LPSW-15).

These valves were made from

carbon steel (CS) material which has exhibited rapid degradation in the

service water environment. Valves 1LPSW-4 and 5 will be replaced with

stainless steel (SS) ball valves which are designed to throttle flow

during accident conditions. Two vent valves (1LPSW-947 and 948) were

planned to be added upstream of 1LPSW-4 and 5 to facilitate routine

system testing.

Valves 1LPSW-6 and 15 have internal parts made of

carbon steel material and the licensee planned to rep ace them with full

port SS ball valves with containment isolation valve shutoff

characteristics.

The licensee also intends to replace check valves

1LPSW-75 and 76, located down stream of 1LPSW-4 and 5 respectively,

Enclosure 2

0II

32

because they do not serve a design basis or operational purpose and

their removal will improve system reliability.

NSM-13001. Part AM2:

This modification addresses the installation of minimum flow piping,

valves around each LPSW pump and associated components to assure minimum

flow after engineered safeguards (ES) signals had been removed from

valves 1LPSW-4 and 5. In addition, this modification along with other

LPSW system changes should ensure adequate net positive suction head is

available at the LPSW pumps during all design basis conditions.

The

licensee had determined that this portion of the LPSW system was

required for the mitigation of a design basis accident and therefore, it

had been designated safety-related. As such. all piping and components

were designated QA-1 condition. Instrumentation that maintained LPSW

system pressure boundary were also designated QA-1 condition. The

replacement pipe and associated components come under Duke Class F

category and therefore will be inspected in accordance with ASME Code

Section XI Subsection IWD requirements.

NSM-13022, Rev. 0 Part AM1:

This modification was developed to reduce flow induced cavitation and

vibration in the LPSW system at the LPI cooler flow control valves

(1LPSW-251 and 252).

The modification relocates and replaces the

subject valves to correct the problem.

In addition. manual isolation butterfly valves (1LPSW-254 and 256).

directly downstream from the subject flow control valves. have

experienced significant degradation and are planned to be replaced with

alike valves made from SS material. A failure associated with the iLPI

cooler train, ultimately caused the LPSW system to be designated as a

Maintenance Rule Al system.

All subject valves in this NSM were identified as Duke Class F category

and therefore were QA-1 condition. The Unit 1 LPSW system isolation for

this NSM were bounded by the installation of wet taps/Marbo Plugs

downstream of isolation valves lLPSW-254 and 256. The bulk of the work

involved in this NSM was located in the auxiliary and turbine buildings.

Installation of the wet taps was performed under Minor Modification

ONOE-10447. This modification called for the installation of a 14-inch

diameter wet tap on the LPSW non-essential header and a 36-inch diameter

wet tap on to the LPSW A header. This work was performed under

procedure TN/1/A/10447/MM/AM1. The controlling code of this activity

was ANSI B31.1, 1968 Edition.

Enclosure 2

0I

33

Observation

The inspector performed a walk through inspection to observe completed

work and work in progress. Line installation, weld appearance and

workmanship were satisfactory. Quality records for replacement

components were reviewed and determined to be satisfactory.

c. Conclusion

LPSW system modifications to replace certain valves and LPSW pump

minimum flow lines were well planned. Valve and pipe replacements were

being installed consistent with applicable code requirements and quality

criteria

M1.12 Inservice Inspection of Safety-Related Welds (Unit 1)

a. Inspection Scope (73753)

Through work observation, procedure and records review, the inspector

determined the adequacy of inservice inspection activities during the

present refueling outage.

b. Observations and Findings

The inspector observed surface and volumetric examination on two welds

of the core flood system.

The subject welds were identified as

follows:

Item

Weld No.

Description

Results

B09.011.089

1-53A-02-68L

Pipe to Valve

Root condition..

verified by RT

B09.011.091

1-53A-02-50L

Ell to Pipe

Root condition.

verified by RT

The ultrasonic examination was performed with Procedure NDE-600 which

complied with the requirements of ASME Code Section XI. 1989 Edition and

had been reviewed and approved by the Authorized Nuclear Inspector (ANI)

and the licensee's Level III examiner. The examination was performed by

well trained personnel in a conservative manner such as reviewing

previously shot radiographs and using supplementary transducers to

further investigate apparent indications. The surface examination

(i.e., liquid penetrant on the subject welds) was performed with

procedure NDE-35 which complied with applicable code requirements. The

examination was performed in a satisfactory manner by well trained

personnel.

Results of this examination showed both welds to be free of

rejectable indications. A review of inspection records and

Enclosure 2

34

certifications for materials used, equipment and personnel were

satisfactory.

c. Conclusion

Volumetric inservice inspection of designated welds was performed

satisfactorily by qualified and well trained personnel following

approved nondestructive examination procedures.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Reactor Building Coatings

a. Inspection Scope (71707)

As indicated in Inspection Report 50-269.270.287/96-20, Reactor Building

(RB)

coatings were not in optimal condition requiring an evaluation for

each of the three RBs.

Just prior to the September 18. 1997, Unit 1

outage start, the inspectors pointed out that the peeling paint in the

overhead of the Unit 1 RB may pose problems during the refueling phase

of the outage.

b. Observations and Findings

During the inspection documented in JR 50-269,270.287/96-20. the

residents encountered a number of conditions that required technical

evaluation by the licensee. Tape. loose paint, and insulation without

supporting documentation were found in significant quantities in various

locations in all the units' RBs.

Following the recent Unit 1 shutdown, the license installed a tent over

the refueling cavity and reactor vessel area. The need to protect from

foreign material entry was recognized in PIP 97-1971, as implemented by

WO 97-084586 and TM 1380. During routine inspector RB tours, the tent

was effective in keeping falling paint from entering the RCS and

attendant support systems.

As emergent work, the licensee planned to attempt inspection and re

coating of the peeling paint on the polar crane and the building spray

framework and supports this outage. Late in the inspection period, a

vendor estimating the job discovered asbestos in the zinc undercoat that

may postpone the job. Remaining loose coating material will be

evaluated prior to closeout of the Unit 1 RB.

The licensee planned to implement new procedure MP/0/B/3005/012.

Containment Inspections/Close Out Procedure, at the end of outage.

This

is a result of a previous NRC Violation (IR 50-269,270,287/96-20).

If

properly implemented. the procedure should provide adequate assurance

that the RB will be in good condition prior to power operations.

Enclosure 2

35

c. Conclusions

To reduce the likelihood of peeling polar crane and extensive hanger

paint intrusion into refueling activities, the licensee installed a

protective foreign material tent over the refueling cavity.

This was

installed prior to opening the RCS and commencing fuel off-load.

M3

Maintenance Procedures and Documentation

M3.1

Weakness in the Procedure for Foreign Material Exclusion (FME)

a. Inspection Scope (62707)

During the inspection period, the inspectors identified a weakness in

the procedural controls for FME with several examples.

b. Observations and Findings

On October 7. 1997. the inspector entered the RB to observe refueling

activities. Prior to entry into the refueling canal area, the inspector

observed the canal FME monitor in a location that precluded direct

observation of the canal/FME zone. While in the canal FME area. the

inspector observed a flashlight without a lanyard being used by licensee

personnel over the canal FME zone. Upon exiting the canal FME zone the

inspector observed another individual. a different canal FME monitor.

reading a magazine. Site management was informed. While touring the

RB. the inspector identified that piping work above the emergency sump

had resulted in a large amount of grinding debris in and around the

emergency sump area. The RB coordinator was informed. The RB

coordinator had already taken note of the area and notified maintenance

for cleanup. In each of the above cases, no specific licensee procedure

was violated.

During the Unit 1 outage, the emergency feedwater (EFW)

recirculation

valve and the turbine driven emergency feedwater (TDEFW)

pump were

disassembled. During inspector tours of the areas, the recirculation

valve and the TDEFW pump were observed to have minimal FME coverage, in

that plastic bags were draped over the openings and parts were laid out

without covers or organization. As discussed in Section M1.8 of this

report, the upper surge tank was entered for observation of welds and

the inspector noted that the wood cover for the opening to the

condensate system was not covered with plastic. After questioning the

responsible engineer, the wood and the area were covered in plastic to

prevent foreign material intrusion into the system.

On October 16, 1997. during work in the spent fuel pool, a vendor.

dropped a 3/16 inch allen wrench into the spent fuel pool.

An

Enclosure 2

36

underwater camera was used to locate the wrench on the bottom of the

spent fuel pool underneath the fuel racks. This has been evaluated to

pose no future problem with fuel movement. The wrench did have a

lanyard attached, but the lanyard was not sufficient to prevent the tool

from falling into the spent fuel pool.

The inspector discussed these observations with radiation protection and

maintenance management. Personnel involved in the issues addressed

above were re-instructed in management's expectations for the canal FME

duties. Additionally, areas were covered and tools and parts were

removed or covered as appropriate. As discussed in Section E1.1. the

EFW recirculation valves have had three failures due to foreign material

entry. The EFW system takes suction on the condenser hot well, which is

difficult to maintain clean. These failures cannot be directly

attributed to recent FME program observations. No events have been

identified that are attributable to recent FME problems.

c. Conclusions

The inspectors identified a weakness in the FME program based on

multiple examples of poor FME practices.

M8

Miscellaneous Maintenance Issues

M8.1 Evaluation of Maintenance Procedure for DB-25 Circuit Breakers

a. Inspection Scope (92902)

The inspectors reviewed the results of the AIT NRC Inspection Report 50

269.270.287/97-11. Section M1.2. for possible NRC enforcement action

related to adequacy of the licensee's maintenance procedure for the DB

25 circuit breaker to the recommendations in the manufacturer's

instruction manual. The licensee's maintenance procedure was contained

in Procedure IP/O/A/2001/003B. Inspection and Maintenance of DB-50. DB

25 and DBF-16 Air Circuit Breakers, dated July 23. 1996. The

manufacturer's recommendations were contained in Westinghouse Electric

Corporation Publication I.B. 33-850-1 and 2E. Instructions for De-ion

Air Circuit Breakers Types DB-15, DB-25, DB-F and DBL-25. 600 Volts AC,

250 Volts DC, which became effective May 1965.

b. Observations and Findings

As documented in the AIT report, as of June 20, 1997, Procedure

IP/O/A/2001/003B did not contain a recommendation from Westinghouse

Publication I.B. 33-850-1 and 2E to "Check for over-adjustment [of

contacts] by manually pulling the moving contact away from the

stationary contact, with the breaker in the closed position. It

should

be possible to obtain at least 1/64-inch gap between the contacts."

Enclosure 2

37

This step was not in the Oconee

rocedure for DB-25 circuit breakers.

The inspectors determined that this over adjustment could result in an

inadvertent "trip free" condition for the breaker. This missing step

resulted in a June 20. 1997. KHU DB-25 field flash breaker failure

mechanism not being initially evaluated. Subsequent performance of this

step on July 17. 1997, resulted in the verification of adequate

adjustment. Failure to maintain the station in accordance with approved

maintenance procedures with appropriate instructions is a violation of

TS 6.4.1 and is identified as VIO 50-269.270.287/97-14-04: Failure to

Implement Vendor Recommendation for DB-25 Circuit Breakers.

c. Conclusions

The inspectors identified a violation for a failure to translate

information from a Westinghouse technical manual to the licensee's

maintenance procedure for the DB-25 circuit breakers.

M8.2 ACB Timer Calibration

a. Inspection Scope (92902)

The inspectors reviewed the results of the NRC AIT Inspection Report 50

269.270.287/97-11. Section M1.1, for possible NRC enforcement action

related to calibration of the timers for the Y coil in each closing

control circuit for ACBs 5, 6. 7. and 8. The procedure used for these

calibrations was Procedure IP/0/A/2001/003B. Inspection and Maintenance

for DB-50. DB-25. and DBF-16. Air Circuit Breakers, Revision 4.

b. Observations and Findings

As documented in the AIT report on June 26. 1997, the licensee

determined that in the past. the technicians performing the timer

calibrations were hooking up their test equipment in such a manner that

the measured time delay included normal breaker travel time along with

the Y timer delay as opposed to just the Y timer delay. This was

because the calibration procedures lacked detailed guidance.

The

licensee issued work orders to check the timer settings and breaker low

voltage operation to ensure that the Y coil timers in all DB-50 breakers

were adjusted properly and that the breakers were currently operable.

Also, the AIT report stated that since all timers checked following the

June 23. 1997, event were found with settings well below the required

set point, past operability of the Keowee DB-50 breakers was

questionable. Licensee low voltage testing revealed that all were

operable, except ACB-6. The breaker was subsequently determined to have

been operable. For procedure corrective action, the.licensee updated

the timer preventive maintenance procedure to include specific details

to ensure that the timer set points were calibrated properly.

Failure

to rovide IP/O/A/2001/003B with appropriate instructions is a violation

of TS 6.4.1. This non-repetitive, licensee-identified, and corrected

Enclosure 2

38

violation is being treated as a Non-Cited Violation (NCV).

consistent

with Section VII.B.1 of the NRC Enforcement Policy.

This is identified

as NCV 50-269,270,287/97-14-05: Failure to Provide Appropriate

Instructions for Calibrating Y Coil Timers in DB-50 Breakers.

c. Conclusion

The inspectors identified a non-cited violation for a failure to provide

detailed guidance in the preventive maintenance procedure for measuring

the timer settings for the Y coil in DB-50 breakers.

  • M8.3

(Closed) VIO 50-269,270.287/96-10-03: Weld Procedure Qualifications

Welded, Tested. Certified and Approved by Same Individual

The licensee's corrective actions on this violation were reviewed and

documented in NRC Inspection Report 269.279.287/97-12. That report

documented that although the licensee had taken appropriate actions to

address the concerns delineated in the violations, the inspector noted

that the revised controlling procedure (L-100) did not reference Duke's

QA topical Report, QA-1 which addressed 10 CFR 50. Appendix B and the

requirement for an independent QA review of welding procedure

qualification records. During the current inspection, the inspector

determined by review that the 1icensee had included by reference the QA

Topical in Revision 22 of the subject procedure. This item is closed.

M8.4 (Closed) VIO 50-269.270.287/96-17-09:

LPSW Modification Did Not Meet

ASME Code Section XI Nondestructive Examination Requirements

The licensee's corrective actions in response to this violation were

documented in NRC Inspection Report 269.270.287/97-12. paragraph M8.5.

The licensee's action plan for resolving identified problems, grouped

the activities into short and long term objectives. Work on the short

term objectives was to be implemented by the start of Unit 1 refueling

outage EOC 17. As such, during the current inspection the inspector

reviewed the status of the short term corrective actions and held .

discussions with cognizant personnel to obtain an update on this matter.

Through this work effort the inspector determined that essentially all

short term objectives had been achieved. The long term objectives

involved development of post-maintenance testing guidelines, procedures

and controls to prevent recurrence of similar type problems in this

area. Also, through this work effort the inspector concluded that the

licensee had taken sufficient actions to address the short term

objectives and was actively pursuing the long term objectives.

Because

of the actions taken and of those planned to address ownership and

controls in this area, this item is closed.

Enclosure 2

0II

39

III. Engineering

El

Conduct of Engineering

E1.1 EFW Automatic Recirculation Valve

a. Inspection Scope (61726)

Motor driven (EFW)

pump 3B failed its performance test because the

automatic recirculation valve failed to open. The inspectors reviewed

the circumstances surrounding this event.

b. Observations and Findings

On October 2. during Performance Test PT/3/A/0600/013.

Motor Driven

Emergency Feedwater Pump Test, automatic recirculation (ARC)

valve 3FDW

380 failed to pass recirculation flow as required. This resulted in

pump discharge pressure increasing to 1480 psig. Subsequent

investigation by the licensee revealed that a small portion of a rivet

lodged between the main disc and seat prevented the main disc from

closing: thereby, keeping the recirculation valve from opening.

Valve 3FDW-380, a Yarway 7100 Series ARC valve, has been designed to

operate as a combination check valve, flow sensor. and recirculation

control valve.

It has been designed for the main disc to open and close

in response to system flow and to control the recirculation portion of

the valve in order to maintain

ump discharge pressure below the pipe

design pressure of 1420 psig. The vendor has stated that debris as

smal

as 1/16 inch could prevent the main disc from closing and the

recirculation portion of this composite valve from opening.

Yarway 7100

Series ARC valves have been installed on the discharge of the motor

driven emergency feedwater pumps for all Oconee units. The turbine

driven EFW pumps have orifice plates.

The licensee determined from the site PIP database that foreign material

had also prevented a 7100 Series ARC recirculation valve from opening on

two previous occasions. On February 2. 1997. valve 1FDW-380 failed

during performance testing due to a piece of wood on the main seat.

Discharge pressure reached 1448 psig. On February 24. 1997, Valve 3FDW

380 also failed during performance testing. The licensee attributed the

failure to foreign material even though they were unable to find any.in

the seat (possibly moved during post event manipulation).

The licensee

documented three events in PIP Reports 1-097-0505, 3-097-0696, and 3

097-3285.

After the first failure, as documented in PIP Report 1-097-0505. system

engineering proposed to install a strainer in the main flow path for the

Enclosure 2

40

ARC valves. System engineering later rejected this proposal on the

grounds that it could introduce new failure modes for the system.

System engineering further stated that failure of the recirculation

valve to open did not affect the ability of the emergency feedwater

system to deliver the required flow to the steam generators, and that,

because the recirculation valve failures had only occurred during

testing at cold shutdown conditions/alignments, no failures were

expected during actual emergency conditions. After the first failure

the licensee indicated that foreign material intrusion would likely

occur again, but the risk was acceptable because the failures would

occur at cold shutdown while the system was not needed. System

engineering finally decided that strainers would be installed in the

recirculation pilot assembly of the ARC valves. These strainers have

not yet been installed.

After the third ARC failure, the residents held several discussions with

the licensee. After an emergency system start, the flow control valves

may throttle or cycle providing low or no flow from the EFW system to

maintain steam generator level.

During these instances, the

recirculation valve could fail throttled (recirculation portion not

open) and emergency feedwater pump discharge pressure could exceed 1420

psig (shutoff head) with the subsequent opening of the flow control

valve. The likelihood of failure while in emergency operation was

possible and not evaluated by the licensee for low decay heat conditions

or changes in suction source from the UST to the hot well (possible

primary debris containing volume). It was pointed out that operators

had no instrument indication of pump recirculation flow and had not been

procedurally directed to check or maintain EFW pressure less than 1420

psig. The licensee stated that exceeding 1420 psig for a small amount

of time would be acceptable under ANSI B31.1 for the piping. However.

the inspectors understood this was not acceptable as a permanent

solution for the piping. Pumps running at shutoff head fail within a.

short period and are not avai able again for emergency use. The

inspectors also understood that strainers in the recirculation pilot

assembly of the ARC valves would not correct the problem of foreign

material on the main seat preventing the recirculation portion of the

valve from opening.

The inspectors determined that, because of repeat failures, the lack of

corrective action constituted a violation of 10 CFR Part 50 Appendix B.

Criterion XVI. Accordingly, this is identified as VIO 50-269,287/97-14

06: Failure to Take EFW Recirculation Valve Corrective Action. This

appeared to be caused by the improper assessment that failure of the

recirculation valve to open would not affect the ability of the

emergency feedwater system to deliver the required flow during potential

debris induced failure. The inspectors understood that the valves had

been installed in 1994 and had no operational problems until the three

occurrences this current calendar year.

Enclosure 2

41

3590 on October 16. changed procedures, and took compensatory

actions/measures to lessen the possible challenges to the ARC valves and

the motor driven portion of the EFW system.

The PIP was modified

October 21 to indicate interim corrective actions.

c. Conclusions

The inspectors identified one violation in which improper assessment of

emergency feedwater valve operation resulted in a recurrence of a

previous component failure in the emergency feedwater system.

E1.2 Unqualified Thermal Insulation Found in the Reactor Buildings

a. Inspection Scope

The inspectors have been following the activities of the licensee

regarding URI 50-269.270.287/96-20-05, Past Operability of RB

Recirculation Flow Path.

In June, the licensee found additional

insulation in all three RBs (Inspection Report 50-269.270.287/97-10..

Section E1.1).

Recently, the licensee found additional, similar

insulation in nearly inaccessible regions of the Unit 1 RB.

Also, the

licensee had received testing results on the undesirable insulation from

a vendor.

The resident reviewed the information and viewed pictures of

the newly found insulation.

b. Observations and Findings

After the June discovery of additional insulation, the licensee had left

an open corrective action to look at all areas that could not be

reasonably inspected while at low power or with the plant thermally hot.

A recent licensee tour of Unit 1 revealed approximately 50 square feet

of additional unqualified or previously undesirable insulation.

These

insulation bats which were firmly attached to RCS piping were found

behind cages that cover the RCS piping where it enters the vessel shield

wall. The licensee did a limited inspection of Unit 3, which was also

shutdown and did not find any undesirable insulation at the same

locations as Unit 1.. Unit 2 was still at power with the open commitment

to be re-inspected.

In the recent past, the licensee had contracted with a vendor to test

the same undesirable insulation type to determine if it would cause

recirculation flow path problems. The NRC had deferred closure of the

URI until the evaluation was complete. The vendor determined that the

insulation would not float and therefore could not be transported to

block the RB emergency sump.

In October 1997, the licensee had completed an operability calculation

on the insulation following testing of the insulation.

Testing which

had found.the undesirable insulation to sink readily was documented in

Enclosure 2

42

PIPs 1-097-1924, 2-097-1957. and 3-097-1950. The RB emergency sump was

found to be past and presently operable.

Failure to verify complete removal of all unqualified insulation for the

period of January 1997 until October 1997 from the RBs is a violation of

10 CFR 50, Appendix B, Criterion XVI and is identified as VIO 50

269,270.287/97-14-07: Inadequate Corrective Actions for Calculation of

Emergency Sump Operability. This was documented in PIP 0-097-1971 as an

operability evaluation performed with inaccurate input.

c. Conclusions

The failure to ensure complete removal of unqualified thermal insulation

from the reactor buildings was identified as a violation based on

inadequate corrective action.

E2

Engineering Support of Facilities and Equipment

E2.1 Keowee Emergency Start Test and Circuit Breaker Coil Failure

a. Inspection Scope (37551. 92903)

The inspectors observed and reviewed the engineering support activities

involved with the KHU emergency start test and a circuit breaker coil

overheating. Comments on the performance of the test and the

maintenance activities on the failed coil are in Sections M1.2 and M1.6

of this report.

b. Observations and Findings

On September 13 and 16, 1997. the inspectors observed the performance of

a test of the KHU emergency start logic system. Based on the previously

discussed test and equipment problems, the licensee initiated PIP K-097

2939 for the timers and FIP K-097-2983 for the overheating of the

breaker closing coil. The problem investigation indicated that the

relays involved with the timers functioned properly. This was based on

a visual observation and manual timing of the relays during a retest.

The failure investigation indicated that the overheating of the closing

coil for the field breaker involved the X relay. Y relay timer, and the

Y relay logic network. The test procedure required that the KHU

emergency start logic be tested for both Channels A and B from the

Oconee remote stations. These included the control rooms and the cable

rooms. The test also required that start signals be initiated while the

KHU were operating. Each start signal would activate the X relay, Y

relay timer, and Y relay logic. During a start signal initiation the Y

timer failed to time out. This resulted in closing current being

applied to the closing coil, through the X relay, continuously for

approximately 20 minutes: thereby causing the coil to overheat.

The Y

Enclosure 2

0II

43

relay timer and Y relay de-energized the X relay after 0.3 seconds of a

close signal.

The FIP group was able to identify and to duplicate the failure

mechanism of the Y timer. The group also interfaced with the vendor on

the failure. Based on the results of the groups' activities, the timers

on the generator field supply breakers and the field breakers were

changed out. The inspectors were informed that engineering would

examine the present breaker timer logic network for possible

modification.

c. Conclusions

The inspectors concluded that the engineering real-time support for the

KHU test was effective. The performance of the failure investigation

group in identifying the failure mechanism for the Y relay timer was

excellent. A review of the present timer logic network for possible

modification is considered an example of good safety attitudes.

E2.2 Testing of the Unit 3B RBCU Motor and Breaker

a.

Inspection Scope (37551)

The inspectors observed, reviewed, and discussed with licensee personnel

tests performed on the RBCU motors and breakers. The tests included a

Time Domain Reflectometry (TDR) test and a trip test of the 3B RBCU

motor supply breaker.

b. Observations and Findinos

The tests on the breakers were performed at the Quality Assurance

breaker testing facility. The criteria required that each of the three

phases of the breaker trip at 2400 amps to 3150 amps. Prior to the trip

test, breaker resistance readings in milli-ohms were taken from each

phase. The results indicated that the B phase had a higher resistance

compared to the other phases by a factor of three. The engineer

overseeing the activities indicated that there would be some reluctance

in reinstalling the breaker and using it. The trip test on phases A and

C indicated a trip of the removed breaker at approximately 2600 amps.

The test on phase B was terminated when the breaker still had not

tripped at 5230 amps. The engineer declared the removed breaker

defective. A new breaker was obtained, tested, and installed.

TDR tests were performed on various motors, such as Unit 1 RBCU motor IA

and all the Unit 3 RBCU motors. The tests included both the high and

low speed windings and were from phase to phase, as well as from phase

to ground. All of the tests were satisfactory.

Enclosure 2

44

c. Conclusions

Testing on the breakers was performed in accordance with an approved

procedure, by knowledgeable personnel, and with engineering oversight.

he inspectors considered the breaker testing activities by the

engineering, maintenance, and procurement quality assurance personnel to

be good.

E3

Engineering Procedures and Documentation

E3.1 Inadequate Engineering Analysis of Heavy Load Lifts Over the Borated

Water Storage Tank (BWST)

a. Inspection Scope (37551. 71707)

The inspector interviewed operations and engineering personnel on

operation of a large crane near the Unit 1 RB.

The inspector also

reviewed procedures and documentation associated with the crane testing.

b. Observations and Findings

On September 12. 1997, a 4100-series Manitowoc crane rated at 230 tons.

entered the protected area and was parked near the Unit 1 BWST. The BWST

is adjacent to an existing RB steam line and abuts the RB with a short

intervening section of LPI suction piping between them.

The inspectors

observed the crane in operation lifting materials to the top of the Unit

1 RB on September 15. 1997.

The lifts were being made over the BWST to

prevent lifting material over the steam lines. Due to plant layout.

choice of crane location was very limited. Unit 1 was not shutdown

until September 18, 1997. Therefore, lifts of heavy materials that

could have possibly impacted the BWST and affected the function of

safety-related equipment was made while the unit was still at power.

The inspectors questioned licensee personnel regarding an evaluation 'of

this evolution. The licensee provided the inspectors information

relating to crane qualifications and maintenance. A letter to file

describing this evolution for Unit 2 in 1990 was also included.

The

inspectors questioned whether this evolution had been re-evaluated for

the lifts while Unit 1 was still operating. The licensee initiated PIP

0-097-3044 to evaluate lifting over the BWST.

The licensee also

identified that there was a possibility of damage to an LPI line and

valve LP-28, which if damaged during certain system alignments, could

cause draining of the Spent Fuel Pool and lead to offsite dose

consequences.

MP/O/B/1710/015, Reactor Building Power Scaffold - Load and Functional

Test was used to load test the Reactor Building Power Scaffold (RBPS).

There was no procedure used to lift the composite pieces of the RBPS to

the top of the RB. These lifts were made over the BWST and the LPI line.

Enclosure 2

45

The BWST and 1LP-28 are safety-related components. NUREG 0612 requires

licensees to evaluate risk associated with heavy lifts over safety

related components. This item will be identified as VIO 50-269/97-14

08: Inadequate Engineering Evaluation for Lifts over Safety-Related

Components.

c. Conclusions

Failure t@ evaluate heavy load lifts over safety-related components

while Unit 1 was above cold shutdown conditions resulted in a violation.

E8

Miscellaneous Engineering Issues (92903, 90712)

E8.1 (Closed) URI 50-269.270.287/96-20-05: Past Operability of RB

Recirculation Flow Path

Based on the discussion in Section E1.2 this item is closed.

E8.2 (Closed) LER 50-269/93-01 (Revisions 1 and 2): Design Deficiency Results

in the Technical Inoperability of the Oconee Emergency Power Source Due

to a Postulated Failure of Keowee Hydro Units

The event date for this item was January 11. 1993.

The initial LER

(dated February 10, 1993) was closed in IR 50-269.270.287/93-20. based

on the actions taken by the licensee in 1993.

The initial issue of

concern was the lack of conservatism in the then existing Keowee

engineering calculations. Subsequent revisions (Revision 1 - dated

August 1, 1994 and Revision 2 - dted July 13. 1995) to the LER

addressed engineering issues that resulted from NRC inspections.

The

initial [ER and the revisions covered a time period of approximately two

and one-half years.

The initial and subsequent problems discussed in the LERs dealt with the

Keowee units potentially under different conditions, causing a loss of

generated power. As the primary issue developed, additional details

regarding engineering refinements were identified. Out of those issues

two violations of NRC requirements were identified.

The licensee

captured their engineering efforts in a series of PIPs indicated below.

During the review of this LER. the inspectors evaluated the following

related documents:

OP/O/A/2000/041, Keowee Modes of Operation, Revisions 8 through 16

Inspection Report 50-269.270.287/93-20

PIP 0-93-0041, Loss of Excitation When Keowee Load Rejects as a

Result of ES [Engineering Safeguards Actuation], dated January 11,

1993

Enclosure 2

46

PIP 0-94-0649, Keowee Units Supplying Above Normal Frequency

Following Load Rejection, dated May 16. 1994

PIP 5-95-0113, Keowee Power Limits Based on Non-Conservative

Calculation [Calculation OSC-6003], dated January 26, 1995

PIP 0-95-0330, Keowee Change OSC-6003 for Added Conservatism,

dated March 15, 1995

NRC Inspection Report 50-269,270,287/95-03 (violation 02.

Calculation Errors Associated with Keowee Output Limit)

NRC Inspection Report 50-269,270,287/95-06 (violation 01,

Inadequate Corrective Action for Control of Keowee Operating

Limits)

NRC Inspection Report 50-269,270,287/95-27 (violation closure)

0

NRC Inspection Report 50-269,270,287/96-12 (violation closure)

0

Selected Licensee Commitment 16.8. Subsection 16.8.4. Keowee

Operational Restrictions

Engineering Directives Manual Section 101.4.2.4, Assumptions

Engineering Directives Manual Section 101.4.3. Verification and

Certification

Engineering Directives Manual Section 101.4. Regulatory

Requirements

The culmination of the above resulted in documentation and procedures to

control Keowee generation during normal and emergency operation. Based

on the inspectors' reviews, the close out of the viol ations, and the

actions taken by the licensee, Revisions 1 and 2 of this LER are closed.

E8.3 (Closed) URI 50-269,270,287/97-02-07:

Non-Conservative Setting of the

LTOP Controls

This item was identified on February 25, 1997, when the licensee was

performing a review of the LTOP portion of the Improved Technical

Specification Conversion Project. The item concerned the setting of the

travel stops on the HP-120 valves. These valves are the normal make-up

valves to the RCS for all three units. The potential non-conservative

setting involved the HPI flow if operation of more than one HPI pump was

to occur during LTOP conditions. The item also concerned the

operability of LTOP flow paths. The licensee made a 10 CFR 50.72.

notification on April 17, 1997. After further analysis the notification

Enclosure 2

0II

47

was rescinded on June 16, 1997.

The inspectors reviewed the licensee's evaluation documented in PIPs 0

097-0710 and 5-097-1204. The PIPs stated, in part, the following:

the travel stops were adjusted for a flow of 70 to 80 gpm to limit

the amount of RCS coolant make up:

the setting is based on the operators having 10 minutes to correct

failed open HP-120 valves when LTOP controls are required:

an analysis, using the most restrictive data, indicated that the

maximum flow from two pumps operating, with a failed open valve,

would be less than the analyzed maximum allowable flow: and

the procedures used for adjusting the travel stops would be

changed to require both pumps to be in operation when the stops

are adjusted.

The inspectors reviewed Procedures OP/1. 2. and 3/A/1104/49. Low

Temperature Overpressure Protection, (Revision 6 for Unit 1 and Revision

7 for Units 2 and 3).

The inspectors observed that Enclosure 4.9. HP

120 Travel Stop Setup, of the procedures required that both HPI pumps be

in operation when adjusting the travel stops.

The inspectors also

observed that the 70 gpm adjustment was for a unit shutdown and the 80

gpm was for startup.

The inspectors concluded that the LTOP flow limitations would not have

been exceeded and the flow paths would have been operable. Based on

this review, this item is closed.

E8.4 Evaluation of Overvoltaoe Relay Set Point Chance

a. Inspection Scope (92903)

The inspectors reviewed the results of the NRC AIT Inspection Report 50

269.270,287/97-11, Section E1.2. for possible NRC enforcement action

related to a set point change made to an overvoltage relay in the

voltage regulator circuitry for the Keowee Hydro Units.

b. Observations and Findinas

As documented in the AIT report, a 53-31T relay set point was changed

outside the licensee's plant modification process. The change was made

via a calculation and calibration. The inspectors determined that the

set point change was basically a safety-related plant modification:

however, no post-modification test was specified or performed. This

post-modification testing omission resulted in an unanticipated relay

cycling phenomena created by the design change remaining Undetected

Enclosure 2

48

until June 1997. The reason that the relay was not working as intended

was that the KC-2023 calculation did not include all the relevant design

inputs. The design inputs not considered were that the 53-31T relay

would see low frequencies and the set point of the SV style relay varies

directly with frequency.

Failure to develop and implement the set point

change inside the Oconee design change process and without verifying the

design change adequacy is a violation of 10 CFR 50. Appendix B.

Criterion III and is identified as VIO 50-269.270.287/97-14-09:

Failure to Conduct Post-Mod Testing on Keowee Overvoltage Relay.

c. Conclusions

The inspectors identified a violation for a failure to implement a

modification inside the licensee's approved modification process,

resulting in the modification not receiving a post-modification test.

IV.

Plant Support Areas

R1

Radiological Protection and Chemistry Controls

R1.1 Tour of Radiological Protected Areas

a. Inspection Scope (83750)

The inspectors reviewed implementation of selected elements of the

licensee's radiation protection program as -required by 10 CFR Parts

20.1201. 1501. 1502. 1601. 1703, 1802. 1902. and 1904. The review

included observation of radiological rotection activities including

personnel monitoring controls, contro of radioactive material.

radiological surveys/postings, and radiation area/high radiation area

controls.

b. Observations and Findinqs

During tours of the auxiliary building and radioactive waste

storage/handling facilities, the inspectors reviewed survey data and

performed selected independent radiation and contamination surveys to

verify area postings. Observations and survey results determined the

licensee was effectively controlling and storing radioactive material.

During plant tours, the inspectors observed that Extra High Radiation

Areas (Locked High Radiation Areas) were locked as required by licensee

procedures and all other high radiation areas observed were

appropriately controlled as required by licensee procedures. Dosimetry

controls for these areas observed were also established in Radiation

Work Permits (RWPs) as required by licensee procedures.

A review of the licensee's records determined the licensee was

maintaining approximately 126,081 square feet (ft

2) of floor space as a

Radiologically Controlled Area (RCA).

Records reviewed also determined

Enclosure 2

0

49

the licensee maintained approximately 800 ft2 or less than 1 percent of

the RCA as contaminated area during non-outage periods.

During the

current outage period the licensee was maintaining approximately

6,000 ft2 as contaminated area.

The inspectors reviewed Personnel Contamination Event (PCE)

reports

prepared by the licensee to track, trend, determine root cause, and any

necessary follow up action forepersonnel contaminations.

The licensee

had continued efforts in 1997 to reduce personnel contaminations.

Approximately 154 PCEs had occurred in 1997. which was a significant

reduction from the previous two years. In 1997 the licensee was

averaging approximately 16 PCEs/month as compared to 35 PCEs/month in

1996 and 49 PCEs/month in 1995.

The inspectors reviewed and discussed

licensee efforts to reduce the percentage of personnel contaminations

occurring outside of posted contaminated areas.

The licensee had

executed some actions to reduce contamination from getting into clean

areas.

Based on several recently identified examples of personnel failing to

follow RWP requirements, the inspectors reviewed RWPs established for

working in or entering various plant areas. The RWPs were reviewed for

adequacy of the radiation protection requirements based on work scope,

location, and conditions.

For the RWPs reviewed, the inspector noted

that appropriate protective clothing and dosimetry were required.

During tours of the plant, the inspectors observed the adherence of

plant workers to the RWP requirements.

c. Conclusions

Based on observations and procedural reviews, the inspectors determined

the licensee was effectivey maintaining controls for personnel

monitoring, control of radioactive material. radiological postings, and

radiation area and high radiation area controls as required by

10 CFR Part 20.

R1.2 Occupational Radiation Exposure Control Proaram

a. Inspection Scope (83750)

The inspectors reviewed the licensee's implementation of 10 CFR

20.1101(b) which requires that the licensee shall use, to the extent

practicable. procedures and engineering controls based upon sound

radiation protection principles to achieve occupational doses and doses

to members of the public that are as low as reasonably achievable

(ALARA).

Enclosure 2

50

b. Observations and Findings

The inspectors interviewed licensee personnel and reviewed records of

ALARA program results and activities.

The licensee demonstrated strong management support in the area of ALARA

as indicated by source term reduction efforts in the 3 units and by

establishing challenging exposure goals.

The licensee was effectively

tracking and trending dose rate reduction efforts in 1997 for outage and

non-outage tasks.

An effective Unit 1 chemical shutdown peroxide

crudburst had resulted in reactor building dose rate reductions of

approximately 3 millirem/hour.

This crudburst also resulted in reducing

steam generator tube sheet dose rate averages at the high contact survey

points by approximately 1.3 rem/hour. Exposure history s for all 3

units had continued to trend downward based on ALARA initiatives. The

licensee had established an annual exposure projection for 1997 of

approximately 204 person-rem or 68 person-rem/unit.

At the time of the

inspection, the licensee was tracking approximately 130.6 person-rem

year-to-date, which was below year-to-date estimates of 192.5 person

rem.

However, the licensee was approximately four days behind in the

Unit 1 End of Cycle (EOC)-17 refueling outage schedule and was

anticipating total person-rem to increase closer to estimates as the

outage progressed.

During tours of the facility, the inspectors attended pre-job briefings.

observed RP technicians controlling access to work areas. In addition

the inspectors observed RP technicians briefing workers in the work

areas as radiological conditions changed. Good use of shielding,

teledosimetry, remote cameras and wireless communications systems for

controlling personnel exposures during maintenance evolutions was

observed.

c. Conclusions

The inspectors determined licensee management demonstrated strong

support for ALARA and the licensee's programs for controlling exposures

ALARA were effective.

R1.3 Inadequate Radiation Protection Controls

a. Scope (71750)

The inspector used Inspection Procedure 71750 while touring to observe

RP practices ensuring compliance with regulations and licensee

procedures.

Enclosure 2

51

b.

Observations and Findinqs

On September 26, 1997. while touring the turbine floor area, the

inspector observed a contractor exiting a roped off radiation area (RA)

without electronic dosimetry. The area is above the control valves for

the Unit 1 turbine.

The Unit 1 turbine is considered a radioactive

materials area due to contamination.

The inspector notified the on

shift RP supervisor and met with the contractor and the RP supervisor to

determine the details.

The contractor stated that he had entered the RA from the ground floor

from a ladder to run an extension cord.

He then proceeded through the

RA to another ladder and exited on the turbine floor, crossing the RA

rope with the posting.

The RP supervisor stated that the lower ladder

should have been posted or removed.

He then left to notif RP

personnel/scaffolding personnel to either post or remove the lower

.

adder.

On October 1, 1997, the inspector observed another individual inside a

posted area also without electronic dosimetry directing crane movement.

The individual exited the area upon observing the inspector realizing he

did not have the proper dosimetry.

Appropriate RP personnel were

notified. RP stated the previous incident had been discussed with all

workers and they were aware of the need to wear proper dosimetry.

These two examples were identified as VIO 50-269,270.2871/97-14-10:

Inadequate Radiation Protection Posting and Controls.

c. Conclusions

A violation was identified, with two examples, for inadequate radiation

protection practices and controls which a lowed entry into a posted

radiation area without proper dosimetry.

R7

Quality Assurance in Radiological Protection and Chemistry Activities

R7.1 Quality Assurance in Radiation Protection and Chemistry

a. Inspection Scope (83750)

10 CFR 20.1101 requires that the licensee periodically review the RP

program content and implementation at least annually. Licensee periodic

reviews of the RP program were reviewed to determine the adequacy of

identification and corrective actions.

b. Observations and Findinas '

Reviews by the inspectors determined that Quality Assurance audits and

self-assessment efforts in the area of RP were accomplished by reviewing

Enclosure 2

52

RP procedures, observing work, reviewing industry documentation, and

performing plant walkdowns to include surveillance of work areas by

supervisors and technicians during normal work coverage. Documentation

of problems by licensee representatives was included in Quality

Assurance audits and self-assessment reports.

During the inspection, the inspectors reviewed the licensee's self

assessment processes for evaluating several licensee identified problems

in the area of radiation protection activities and determined that

corrective actions were included in PIPs and were being completed in a

timely manner.

c. Conclusions

The inspectors determined that the licensee was performing Quality

Assurance audits and effectively assessing the radiation protection

program as required by 10 CFR Part 20.1101.

The inspectors also

determined the licensee was completing corrective actions in a timely

manner.

Si

Conduct of Security and Safeguards Activities

S1.1 Observation of Security Staff

a. Inspection Scope (71750)

The inspector toured the Central Access Station (CAS), Secondary Access

Station (SAS).

Access Control Station (ACS).

and various patrol stations

to observe security personnel and operations.

b. Observations and Findings

The stations observed were well maintained. CAS and SAS alarm panels

and monitoring devices were maintained with clear view and few alarms.

Security personnel were attentive at all stations observed and were

prompt in acknowledging all alarms. The inspector completed a tour of

the Protected Area on night shift to verify ]ighting.

The PA lighting

was verified adequate. no problems or discrepancies noted.

Security

personnel were attentive to their stations. Lighting and equipment was

verified adequate and free of alarms.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on October 22, 1997. The

licensee acknowledged the findings presented. No proprietary

information was identified to the inspectors.

Enclosure 2

0II

53

Partial List of Persons Contacted

Licensee

E. Burchfield, Regulatory Compliance Manager

T. Coutu. Scheduling Manager

D. Coyle, Mechanica] Systems Engineering Manager

T. Curtis, Operations Superintendent

B. Dobson, Mechanical/Civil Engineering Manager

W. Foster. Safety Assurance Manager

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Engineering Manager

W. McCollum, Vice President, Oconee Site

M. Nazar, Manager of Engineering

B. Peele, Station Manager

J. Smith, Regulatory Compliance

J. Twiggs, Manager,' Radiation Protection

Other licensee employees contacted during the inspection included technicians.

maintenance personne], and administrative personnel.

NRC

D. LaBarge, Project Manager

Inspection Procedures Used

IP 37550

Engineering

IP 37551

Onsite Engineering

IP 37828

Installation and Testing of Modifications

IP 40500

Effectiveness of Licensee Controls in Identifying and Preventing

Problems

IP 60705

Preparation for Refueling

IP 61726

Surveillance Observations

IP 62707

Maintenance Observations

IP 71707

Plant Operations

IP 71750

Plant Support Activities

IP 81700

Physical Security Program For Power Reactors

IP 81810

Protection of Safeguards Information

IP 83750

Occupational Exposure

IP 90712

LER Review

IP 92700

Onsite Follow up of Written Event Reports

IP 92901

Follow up - Plant Operations

IP 92902

Follow up - Maintenance

IP 92903

Follow up - Engineering

IP 92904

Follow up - Plant Support

IP 93702

Prompt Onsite Response to Events

Enclosure 2

IP400

54

Items Opened, Closed, and Discussed

Ooened

50-269/97-14-01

URI

Failure to Follow LTOP Procedure (Section

03.1)

50-269,270.287/97-14-02

VIO

Failure to Adequately Implement Lee

Station Procedure (Section 08.4)

50-269.270,287/97-14-03

VIO

Failure to Provide Appropriate Lockout

Reset Instructions in ARG SA1/E-04

(Section 08.5)

50-269.270,287/97-14-04

VIO

Failure to Implement Vendor Recommendation

for DB-25 Circuit Breakers (Section M8.1)

50-269.270,287/97-14-05

NCV

Failure to Provide Appropriate

Instructions for Calibrating Y Coil Timers

in DB-50 Breakers (Section M8.2)

50-269.287/97-14-06

VIO

Failure to take EFW Recirculation Valve

Corrective Action (Section E1.1)

50-269,270.287/97-14-07

VIO

Inadequate Corrective Actions for

Calculation of Emergency Sump Operability

(Section E1.2)

50-269/97-14-08

VIO

Failure to Follow Procedure for Lifts Over

Safety Related Components (Section E3.1)

50-269.270,287/97-14-09

VIO

Failure to Conduct Post-Mod Testing on

Keowee Overvoltage Relay (Section E8.4)

50-269.270.287/97-14-10

VIO

Inadequate Radiation Protection Posting

and Controls (Section R1.3)

Closed

50-269,270,287/97-01-05

URI

LPSW to RB Cooling Inoperability (Section

08.3)

50-269.270,287/96-17-09

VIO

LPSW Modification Did Not Meet ASME Code

Requirements (Section M8.4)

50-269,270,287/96-10-03

VIO

Weld Procedure Qualifications. Welded.

Tested. Certified and Approved by Same

Individual

(Section M8.3)

Enclosure 2

55

50-269,270,287/97-02-07

URI

Non-conservative Setting of the LTOP

Controls (Section E8.3)

50-269/93-01, Revision 1 & 2 LER

Design Deficiency Results in the Technical

Inoperability of the Oconee Emergency

Power Source Due to a Postulated Failure

of Keowee Hydro Units (Section E8.2)

50-269.270.287/96-20-05

URI

Past Operability of RB Recirculation Flow

Path (Section E8.1)

List of Acronyms

ACB

Air Circuit Breakers

ACS

Access Control Stations

AIT

Augmented Inspection Team

ALARA

As Low As Reasonably Achievable

ANSI

American National Standard

ASME

American Society of Mechanical Engineers

ANI

Authorized Nuclear Inspector

ARC

Automatic Recirculation

B&W

Babcock and Wilcox

BWST

Borated Water Storage Tank

CALC

Calculation

CAS

Central Access Station

CIT

Continuous Improvement Team

CFR

Code of Federal Regulations

CR

Control Room

CS

Carbon Steel

DC

Direct Current

ED

Electronic Dosimetry

EDM

Engineering Directive Manual

EFW

Emergency Feedwater

EOC

End of Cycle

ES

Engineered Safeguards

F

Fahrenheit

FIP

Failure Investigation Process

FME

Foreign Materia] Exclusion

FSAR

Final Safety AnalysisReport

ft2

square feet

GPM

Gallons Per Minute

HPI

High Pressure Injection

ICS

Integrated Control System

IR

Inspection Report

IST

Inservice Testing

KHU

Keowee Hydro Unit

KV

Kilo Volt

LER

Licensee Event Report

Enclosure 2

56

LCO

Limiting Condition for Operation

LOA

Lee Control Operator

LOB

Lee Assistant Control Operator

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

LTOP

Low Temperature Over Pressure

Milli-ohm

Resistance Measurement

MFB

Main Feeder Buses

MW

Megawatts

NCV

Non-Cited Violation

NLO

Non-Licensed Operator

NRC

Nuclear Regulatory Commission

0AC

PCE

Operations Aid Computer

PCE

Personnel Contamination Events

PDR

Public Document Room

PIP

Problem Investigation Process

PM

Preventive Maintenance

PORC

Plant Operating Review Committee

PRVS

Penetration Room Ventilation System

PSIG

Pounds Per Square Inch Gauge

PSP

Physical Security Plan

PT

Performance lest

QA

Quality Assurance

QC

Quality Control

RA

Radiation Area

RB

Reactor Building

  • RBCU

Reactor Building Cooling Unit

RBPS

Reactor Building Power caffold

RCA

Radiation Control Area

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RCZ

Radiation Control Zone

REV

Revision

RP

Radiation Protection

RWP

Radiation Work Permit

SALP

Systematic Assessment of Licensee Performance

SAS

Secondary Access Station

SG

Steam Generator

SGI

Safeguards Information

SLC

Selected Licensee Commitments

SNM

Special Nuclear Material

SRD

Self-Reading Pocket Dosimeter

SS

Stainless Steel

SSF

Safe Shutdown Facility

TDEFW

Turbine Driven Emergency Feedwater

TDR

Time Domain Reflectometry

TLD

Thermoluminescent Dosimetry

TM

Temporary Modification

T&QP

Training and Qualification Program

Enclosure 2

0anFee ue

57

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

UST

Upper Surge Tank

VIO

Violation

WO

Work Order

Enclosure 2