ML15118A259

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Insp Repts 50-269/97-12,50-270/97-12 & 50-287/97-12 on 970727-0906.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML15118A259
Person / Time
Site: Oconee  
Issue date: 10/06/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A257 List:
References
50-269-97-12, 50-270-97-12, 50-287-97-12, NUDOCS 9710230065
Download: ML15118A259 (53)


See also: IR 05000269/1997012

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269. 50-270, 50-287, 72-04

License Nos:

DPR-38, DPR-47, DPR-55. SNM-2503

Report No:

50-269/97-12. 50-270/97-12, 50-287/97-12

Licensee:

Duke Energy Corporation

Facility:

Oconee Nuclear Station, Units 1, 2, and 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

July 27 - September 6, 1997

Inspectors:

M. Scott, Senibr Resident Inspector

S. Freeman, Resident Inspector

E. Christnot, Resident Inspector

D. Billings, Resident Inspector

R. Moore, Regional Inspector (Sections E4.2, E8.5 to E8.9)

H. Whitener. Regional Inspector (Sections M8.6,.8.7)

N. Economos, Regional Inspector (Sections M8.3 to M8.5)

W. Stansberry, Regional Inspector (Sections S1 to S5. S8)

Approved by:

C. Ogle, Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9710230065 971006

PDR

ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2, and 3

NRC Inspection Report 50-269/97-12,

50-270/97-12, and 50-287/97-12

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a six-week

period of resident inspection, as well as the results of announced inspections

by four regional inspectors.

Doerations

Receipt and storage of the new fuel in the spent fuel pool was

conducted with appropriate procedures and good communications.

(Section 01.2)

0

During the discovery and evaluation period of increased reactor

coolant system leakage from valve 2LP-1, the inspectors concluded

that: operators were following the applicable Technical

Specifications conservative decision making was evident: and

management was involved with the evaluation. The inspectors

considered the licensee's actions prudent and well thought out.

(Section 01.3)

o

The inspectors concluded that the Unit 2 planned shut down and

cooldown activities for 2LP-1 work were performed effectively.

(Section 01.4)

o

A Non-Cited Violation was identified for a motor operated valve

design deficiency implementation addressed in licensee event

report 50-269/95-08. (Section 08.3)

Maintenance

0

The inspectors concluded that the maintenance activities listed in

the general work observation section were completed thoroughly and

professionally. (Section M1.1)

o

During licensee maintenance activities to determine letdown

storage tank reference leg fluid evaporation, the inspectors

concluded that the replacement of the Unit 2 instrumentation test

tees was performed in accordance with approved procedures with

quality control and supervisory oversignt.

The inspectors also

concluded that no appreciable evaporation occurred. The

performance of the personnel invo ved was considered excellent.

(Section M1.2)

During the dual Keowee Hydro Plant outage. the inspectors

concluded that maintenance activities were accomplished in

accordance with approved procedures, personnel were knowledgeable

in the systems, practiced good engineering judgement, and had

sufficient supervi sory oversight.

The inspectors also concluded

Enclosure 2

that the material condition of the equipment observed was good.

(Section M2.1)

The failure to detect a potentially unacceptable valve stroke

surveillance in a timely fashion is identified as a weakness.

However, licensee management's disposition of the issue when

identified was good. Corrective items were appropriately

addressed or captured by the licensee's corrective action program.

(Section M3.1)

O

During this period, the licensee increased the normal operating

voltage of the Keowee main transformer and the unit startup

transformers by altering transformer tap positions. The work was

performed on a QA-1 safety-related piece of equipment without

using the work order invoked procedure (the procedure was struck

through or lined out as allowed under local instructions). An

inspector followup item was identified to review the requirements

concerning quality assurance with regard to safety related

equipment.

(Section M3.2)

Engineering

o

During a prorammatic review of the Updated Final Safety Analysis

Report, the ficensee discovered that a fuel enrichment statement

had not been addressed by the 10 CFR 50.59 evaluation.

The

licensee entered the discrepancy into their corrective action

program.

'An Unresolved Item has been opened.

(Section E1.1)

o

The inspectors concluded that the Keowee Hydro Plant modifications

were installed in accordance with app roved packages with

supervisory and engineering oversight.

The replacement of the

voltage regulator motor timer was an example of good engineering

activities. (Section E1.2)

o

The licensee initiated adequate measures to track and evaluate

water hammers in the various piping systems. (Section E2.1)

The partial discharge test of the Keowee Hydro Plant underground

cable was under the control of engineering personnel.

The

activities were conducted in a deliberate and professional manner.

The test was performed without difficulty. (Section E2.2)

O

An existing minor body to bonnet leak worsened on a Unit 2 Low

Pressure Injection valve that was unisolatable from the RCS.

The

inspectors concluded that the expected leak repair activities:

were discussed with appropriate management involvement: had good

engineering input

had appropriately developed procedures; and had

an approved method for injecting approved sealant with appropriate

Enclosure 2

3

on-line sealing guidance for ASME Class 1 and 2 components.

(Section E2.3)

During a degraded grid undervoltage relay setpoint change, workers

did not have as-found set points evaluated due to a potential

procedure problem. This test control issue was left as an

unresolved item until the licensee completed a corrective action

review.

The licensee understood the nature of the problem and

initiated appropriate corrective evaluation. (Section E3.1)

o

Engineering and site management have recently instituted a new

focus and direction for the plant through process improvement

efforts.

Preliminary output from the effort Kos been positive.

(Section E4.1)

o

The licensee implemented appropriate measures to incorporate

lessons learned from the Unit 3 integrated control system

modification into the Unit 1 modification. Design and operational

deficiencies identified in the Unit 3 modification were adequately

addressed for Unit 3 and addressed in the Unit 1 design and

modification implementation procedure changes. (Section E4.2)

0

Engineering management has instituted a practice of monthly system

engineer tours with non-licensed operators. (Section E4.3)

Plant Support

o

The inspectors identified a violation for test personnel exiting a

contaminated area without properly removing protective clothing.

(Section R4.1)

o1

During an August emergency plan drill, control room drill

personnel showed a good questioning attitude and properly used

three-way communications. (Section P1.1)

o

The licensee used compensatory measures that ensured the

reliability of security related equipment and devices. (Section

S1i)

o

The access controls for vital areas were in compliance with the

Physical Security Plin. (Section S2.1)

0

An incident of failure to secure safeguards information properly

was a licensee identified, non-repetitive, corrected, non-willful

event. Consequently, a Non-Cited Violation was issued. (Section

S4.2)

The security force was being trained according to the Training and

Qualification Plan and regulatory requirements. (Section S5.1)

Enclosure 2

14

Two incidences of failure to notify security of the termination of

personnel in a timely manner were licensee identified, non

repetitive, corrected, non-willful events. Consequently, a Non

Cited Violation was issued. (Section S8.1)

During a fire drill. the inspectors concluded that the method

employed for attacking the fire was appropriate, the drill.

scenario was good, fire brigade personnel exercised good fire

fighting techniques, and the post-fire drill briefing was

effective. (Section Fi.1)

Enclosure 2

Reoort Details

SLmmary of Plant Status

Unit 1 began and ended the period at achievable power (73 percent with one

reactor coolant pump out-of-service).

Unit 2 began the period at 100 percent power shutting down on September 4, to

repair valve 2LP-1. The unit remained shutdown for the rest of the period.

Unit 3 remained at 100 percent power for the entire period.

Review of Uodated Final Safety Analysis Reoort (UFSAR) Commitments

While performing inspections discussed in this report, the inspertors reviewed

the applicable portions of the UFSAR that related to the areas ispected. The

inspectors verified that the UFSAR wording was consistent with the observed

plant practices, procedures, and/or parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure-71707. the inspectors conducted frequent

reviews of ongoing plant operations. In general the conduct of

operations was professional and safety-conscious: specific events and

noteworthy observations are detailed in the sections below.

01.2 Preparation For Refueling

a. Inspection Scope (607051

The inspectors used Inspection Procedure 60705 to verify the adequacy of

procedures for the conduct of refueling.

b. Observations and Findings

Unit 1 received new fuel for its upcoming refueling outage scheduled to

begin September 18. 1997.

The inspectors observed portions of the receipt, inspection, and storage

of new fuel in the spent fuel pool (SFP). Quality Assurance (QA)

personnel w.re on hand to verify cleanliness of the fuel and to take

receipt. Observations of the movement of spent fuel within the SFP in

preparation of the receipt of the new fuel and maintenance activities on

the upender were also made. SFP water clarity was excellent.

Enclosure 2

2

c. Conclusions

Receipt and storage of the new fuel in the SFP was conducted with

approPriate procedures and good communications.

01.3 Unit 2 Reactor Coolant System (RCS) Leakage from 2LP-1; Low Pressure

Injection (LPI)

Suction Valve

a.

Insoection Scooe (71707. 93702)

Beginning August 27. Unit 2 operators observed a slight increase in RCS

leakage.

Entry into the reactor building (RB) revealed additional

leakage from valve 2LP-1 beyond that which had been identified during a

May 22. 1997. startup (0.04 gallons per minute (gpm),

see Section 02.1

of Inspection Report (IR) 50-269.270.287/97-05). Operations called the

Senior Resident on August 30 keeping him informed. The residents

followed the licensee actions through the remainder of the inspection

period.

b. Observations and Findings

Several entries into the Unit 2 RB and leak rate checks revealed slowly

increasing leakage from the valve 2LP-1 seal ring area. The seal ring

provides a gasket-like seal between the body and bonnet of the valve.

Fhe valve is the first LPI valve off of the RCS and is unisolatable from

the RCS. The unidentified leakage from the Unit 2 RCS increased from

0.17 gpm on July 27, to 0.32 gpm on August 18. and to 0.86 gpm on August

31. 1997.

On August 31, an inspector responded to the site and observed, reviewed.

and discussed the leakage with licensee personnel.

The amount of

identified leakage from the valve pressure seal was determined (from a

direct measurement during a RB entry) to be from 0.28 gpm to 0.35 gpm.

The possible repair actions.were discussed. Options identified by the

licensee included a re-torque of bonnet to body fasteners, an over

torque of these same fasteners, and/or injection with sealing material.

The inspectors were informed that the re-torque could be performed by

licensee personnel if needed, the over-torque would need approval by the

vendor, and the injection of a sealing material would have to be agreed

to by the vendor, the sealing material contractor, and licensee

engineering personnel. The inspectors were also informed that overall

corrective action plan would require management approval. (Additional

observations are found in section E2.3 of this report.)

On August 31. the inspectors reviewed the applicable Technical

Specifications (TS) and observed that:. TS 3.1, Reactor Coolant System,

Section 3.1.6, Leakage, Subsection 3.1.6.1 states, in part, that the

reactor must be shut down if the total leakage exceeds 10 gpm. TS

Subsection 3.1.6.2 states, in part, that the reactor must be shut down

Enclosure 2

3

if the unidentified leakage exceeds 1 gpm. The inspectors were informed

by the licensee that the 0.28 gpm value for measured leakage would be

applied as identified leakage.

Based on engineering recommendation, site management reached the

  • conclusion that the plant was required to be shutdown to effect leak

injection repairs. On September 4 with the valve leakage stabilized

around 0.5 gpm, the unit was brought off line electrically, the reactor

was shutdown, and the RCS partially depressurized. Replacement of the

seal ring would have required cold shutdown and core off load.

c. Conclusions

During the discovery and evaluation period of increased RCS leakage from

valve 2LP-1, the inspectors concluded that: operators were following the

applicable TS: conservative decision making was evident; and management

was involved with the evaluation. The inspectors considered the

licensee's actions were prudent and well thought out.

01.4 Unit 2 Shutdown Observations

a. Insoection Scope,(71707. 61726)

The inspectors observed shut down and cooldown activities in the Unit 2

control room on September 4 and 5.

b. Observations and Findings

The unit was shutdown and cooled down to 250 degrees Fahrenheit (F) and

350 pounds per square inch gauge (psig).

This was done to make repairs

to a leaking pressure seal in valve 2LP-1. The plant shutdown and

cooldown below hot shutdown conditions was characterized by clear

operator communications, effective control by shift supervision, and

management oversight. Operators used appropriate procedures, performed

a control rod timing test, and maintained close monitoring of the

letdown storage tank level.

Management on shift was present in the

control room. A yet to be approved total RCS leakage computer program

was being observed for correctness of function during the shutdown- this

program will be utilized as an operator aid as part of a corrective

action (EA 97-297, 298) when finally approved. The program operated as

expected during the shutdown.

c. Conclusions

The inspectors concluded that the Unit 2 planned shut down and cooldown

activities for 2LP-1 work were performed effectively.

Enclosure 2

4

02

Operational Status of Facilities and Equipment

02.1 General Plant Tours

The inspectors used Inspection procedure 71707 to walkdown accessible

portions of the following safety-related systems:

o

Keowee Hydro Plant

0

Unit 1 and Unit 3 High Pressure Injection (HPI) Pump Areas

0

Unit 1 LPI and Spray Pump Area

o

Condenser Circulating Water (CCW) Intake Area

0

Unit 1 and 2 Penetration Rooms

o

Unit 2 Reactor Building

o

Unit 1, 2. and 3 Low Pressure Service Water (LPSW) Pump Areas

Equipment operability, material condition, and housekeeping were

acceptable in all cases. Several minor discre2ancies were brought to

the icensee's attention and were corrected.

the inspectors identified

no substantive concerns as a result of these walkdowns.

08

Miscellaneous Operations Issues (92901, 92700)

08.1

(Closed) Violation (VIO) 50-269.270.287/95-27-01: Inadequate Procedures,

Two Examples

This violation addressed two examples of inadequate procedures. The

first example was a failure to make a four-hour report as required for

having a train of LPI out of service. Nuclear Station Directives (NSD)

202 has been reviewed and revised to prevent recurrence.

The second examole was an inadequate block tag out that allowed the

removal of a relief valve which resulted in a spill. The inspector

verified that OP/1,2.3/1502/08, Block Tagout Procedure, was revised to

designat.e relief valves as boundary valves, if aoplicable. The

inspector verified training had been completed for operations shift and

staff personnel.

The inspector also completed a search of the Problem

Investigation Process (PIP) database for other items related to

inadequate relief valve tagouts or reportability errors. No items were

found that appeared to be related. These items are closed.

08.2 (Closed) Unresolved Item (URI) 50-269.270.287/96-20-01: Standby Shutdown

Facility (SSF) Past Operability

During a site-wide review of uncertainties in engineering calculations

(started in August, 1996, IR 50-269.270.287/96-16), potential

shortcomings in the 1988 revision "0" of SSF Pressurizer Level

Instrument .Loop Uncertainty Calculation OSC-2746 were identified. A

preliminary review indicated that the SSF pressurizer heaters could

potentially be uncovered prior to reaching this heater group's

Enclosure 2

electrical cutoff setpoint. This was based on the fact that the

reference leg calculation used a reference leg water temerature of 68F

instead of a hypothetical maximum RB temiioerature of 271F.

The SSF

heaters were located within Group B. Bank 2. of tie pressurizer heaters

at a maximum height of 44 inches inside of the pressurizer.

Their 126

kilowatts of heat is required to be available within two hours after a

loss of offsite power in order to establish and maintain natural

circulation. The nine SSF heater elements must be operable for startup.

Engineering initiated investigation of the potential problem.

OSC-6847. Revision 0. SSF Pressurizer Level Uncertainty in Support of

PIP 97-0273, indicated that post-reactor trip pressurizer water level

for the worst case condition would reach a level of 47 inches. Thus,

the SSF required unenergized heaters would not be uncovered.

Pressurizer and RCS volumes would recover from this level and return to

approximately 100 inches prior to the SSF heaters being required on a

design basis SSF event.

Therefore, with the then existing indication

and control system setpoints. the heaters would have been operable. The

inspectors reviewed the calculations, discussed the findings with

engineering, reviewed the UFSAR sections 7.7.5.2 and 9.6: reviewed TSs 3.18 and 4.20. Further, the inspectors agreed with the conclusions of

PIP 97-0273 on the subject. Additionally, the licensee per PIP 97-0273

was enhancing several points in the SSF event scenario documentation and

procedures and have redoneOSC-2347 calculation (revision 2) including

the new boundary conditions and assumptions. This URI is closed.

08.3 (Closed) Licensee Event Report (LER) 50-269/95-08: Containment

Isolation Valve Inoperable Due To Deficient Design Condition (Inclusive

of Revision 1)

The substance of the LER is also found in two other documents.

IR 50-269,270.287/95-30, Section 3.0 discussed an abnormal/failed

November 27. 1995. stroke test of 1RC-6 which is a Unit 1 pressurizer

fluid sample valve and RB isolation boundary valve. The failure was

discovered when the valve stroked faster than expected. PIP 1-095-1570

addressed past operability finding the valve past technically inoperable

since a motor operated valve (MOV) gear and valve type replacement in

May 31, 1990. With an incorrect gear ratio installed, the valve would

not have closed 'against high (RCS) differential pressure under accident

conditions while in a sampling mode of operation. Normally, during

sampling, flow is isolated downstream of 1RC-6. The paired series

isolation valve. 1RC-7 (springto close pneumatic valve), was operable

and would have provided isolation of the sample line. The licensee

reviewed other valves on all three units for similar problems. Valve

3RC-5, a pressurizer steam space sample valve which is not routinely

used, was also found to be inoperable (January 24. 1996. review, PIP 3

96-179).

Enclosure 2

6

With the 1995 discovery of the 1RC-6 problem and the subsequent 3RC-5

problem. the licensee took appropriate immediate and long term

corrective actions.

The valves were aDropriately dispositioned and

the licensee submitted a timely LER and followed it with a supplement

(revision 1 dated February 19. 1996).

An NRC search of the licensee's

problem reporting data-base indicated no other examples of similar type

events within the two years prior to the time of the event.

The root cause for 1RC-6 problem and the 3RC-5 corrective action review

was determined to be deficient design changes. The valves and their

operators where changed in 1987 (3RC-5) and 1990 (1RC-6)..

During the

like-for-like valve operator change.out. the (incorrect) operator gear

ratios were not checked on the replacement Limitorque type SMB

operators. The design change to the valve operator and valve did not

specify the correct gear ratio for either valve.

Subsequent valve

testing in 1992 of both valves did not identify the gear ratio problems.

The licensee's valve testing program was fully implemented in 1993 and

the 1995 testing of 1RC-6 did identify the problem. The lack of early

(1992 or at installation work package review) problem identification

prevented entry into any operationally limiting TS 3.6.3.c limiting

condition for operation (LCO) prior to the 1995 discovery date.

Revision 1 of the subject LER indicated that had an accident occurred

during Unit 1 pressurizer sampling, the outboard isolation valve. 1RC-7,

would have closed to provide necessary isolation. Since 1990. 1RC-7

had no work history or stroke time problems.

With only 1RC-7 closed,

leakage through this sampling enetration would have been low enough to

meet TS 4.4.1.2.3 penetration leakage criteria.

This design deficiency was a violation of 10 CFR 50. Appendix B.

Criterion III. Design Control, in that desigp control processes did not

ensure that imoortant design aspects were reviewed and controlled.

Accordingly, the inspector concluded that this failure to comply n

represented a licensee-identified and corrected violation. This non

repetitive. licensee-identified-and corrected violation is identified as

a Non-Cited Violation (NCV). consistent with Section VII.B.1 of the NRC

Enforcement Policy. NCV 50-269.287/97-12-01. MOV Design Deficiency

Implementation. This LER and Revision 1 to it are closed.

08.4

(Discussed- ODen) VIO 50-269,270.287/96-05-01: Failure to Make Proper

10 CFR 50.72 Notification

Since this subject violation was identified, several other documents

have been issued or events occurred that may impact item closure. These

are as follows:

On June 19, 1997, a letter from the NRC's Office for Analysis and

Evaluation of Operational Data (AEOD) was issued regarding the

licensee's reporting practices.

Enclosure 2

7

On July 30. 1997. the Region II NRC office issued Inspection

Report 50-269, 270. 287/97-11 that addressed a reporting practice

(Section IV)

which has vet to be resolved.

o

On August 27, 1997.

EA97-297. 298 Notice of Violation was issued

that included enforcement discretion for a licensee reporting

practice (cover letter and enclosure 2).

o

On September 4. 1997, the licensee issued a letter responding to

the June 19 AEOD letter. In that letter, the licensee .asked for a

meeting to discuss reporting practices.

Until the above components are reviewed and discussed, this item shall

remain open.

II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Insoection Scooe (62707. 61726)

The inspectors observed all or portions of the following maintenance

activities.

o

IP/0/A/0310/012B

Engineered Safeguards System Logic

Surveillance Test Online Channel 3

o

PT/3/A/.0202/11

High Pressure Injection System

Performance Test

o

OP/0/A/1102/06 Encl. 3.3

Procedure For Removal From and

Return To Service of 6900/4160/600

Volt Breakers

0

MP/OA/1500/008

New Fuel Receipt

o .

Work Order (WO) 97052701-13

Replace STAR Modules 3ICSCORC06,

3ICSCORCO7. and 3ICSCORCOS

0

WO 97027649-01

Change Degraded Relay Setpoints

Enclosure 2

8

b. Observations and Findinas

The inspectors found the work performed under these activities to be

professional and thorough.

All work observed was performed with the

work package present and in use. Technicians were experienced and

knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

c. Conclusion

The inspectors concluded that the maintenance activities listed above

were completed thoroughly and professionally.

M1.2 Evaporation in Reference Legs for Letdown Storage Tank (LDST) (Unit 2)

a.

-section

_Scooe_627071

The inspectors observed and reviewed the activities involved with the

Unit 2 LDST level instrument reference legs. IR 50-296.270,287/97-02.

identified concerns involving the instrumentation for the LDSTs in Units

1. 2, and 3. The specific maintenance activities observed were to check

for evaporation from the reference legs. IR 50-269.270,287/97-08, an

Augmented Inspection Team (AIT) report, also identifies concerns

involving compression fittings.

b. Observations and Findings

On July 28. the inspectors observed instrumentation and electrical

(I&E)

maintenance workers perform a verification test for possible

evaporation from both of the LDST reference legs.

If evaporation had

occurred, the level would have indicated higher than actual.

Prior to the work activities, the inspectors attended a pre-job briefing

in the I&E work shop. The pre-job briefing emphasized expectations for

items such as safety, questioning attitude, and following procedures.

At the work site, the inspectors observed that the test tees, with

compression fittings, on the level instruments, 2HPI LT 0033P1 and P2.

were replaced with new ones prior to the testing activities. The

inspectors noted, from a review of procurement documents. that the tees

were Swagelok and were American Society of Mechanical Engineers (ASME).

Section III, certified. The inspectors also observed, during the

installation, the following:

that the threads on the tee's and fittings

were inspected the tubing and tee's were inspected for foreign

material and the fittings were verified as being snug tight by the use

of a template. The inspections and verification were performed by a

quality control inspector and the technicians. A leakage test was

performed satisfactorily after the installation.

Enclosure 2

The inspectors also reviewed the following documents and procedures:

Procedure IP/0/A/0075/010. Instrument Line, Impulse Line Filling.

Revision (Rev) 3;

o

Procedure IP/0/A/5090/001, Tube Fitting and Tubing Installation.

Rev 1:

W

WO 97043780 with tasks 01, 02 and 03; and

o

Procedure IP/0/B/0202/001F. High Pressure Injection System Letdown

Storage Tank Level Instrument Calibration, Rev 31.

Among the concerns identified in the AIT inspection report. Section

M8.1.b. Compression Fitting Issues, were: the mixing of parts from

different manufacturers: foreign material exclusion: and the over

tightening of fittings.

The inspectors observed during the review of

procedure IP/0/A/5050/001 the following:

section 3.1.4.B stated, in part, do not mix or interchange parts

of tube fittings from different manufacturers;

o

enclosure 4.8. Swagelok Fittings Installation, of the procedure,

section 4.8.3 required a check for no foreign material:

o

section 4.8.3. of the enclosure, required a check for no

scratches, deformations, or damaged threads:

o

a note following section 4.8.10. insert tubing with fittings,

stated, if resistance is felt when threading nut finger tight the

fitting should be replaced; and

o

section4.8.11 required that the fittings be tightened to snug

tight.

The fittings on the level instruments were changed when it was

discovered that resistance was felt when finger tightening the nuts.

The inspectors observed the check for evaporation from the LDST

reference legs. An as-found reading for reference leg P2 was taken and

indicated 86.72 inches. The reference leg was felled in accordance with

procedure IP/0/A/0075/010. An as-left reading was taken and indicated

86.62 inches. The same process was performed on reference leg P1 with

the as-found indicating 86.48 inches and the as-left indicating 86.44

inches. This procedure was last performed three months ago. The

maximum allowed difference per procedUre IP/0/B/0202/001F was 0.75

.

inches. The inspectors noted with the differences in the as-found and

the as-left indications being 0.04 inches and 0.10 inches that no

appreciable evaporation occurred.

Enclosure 2

10

c. Conclusions

During licensee maintenance activities to determine LDST reference leg

fluid evaporation, the inspectors concluded that the replacement of the

Unit 2 instrumentation test tee's were performed in accordance with

aporoved procedures with Quality Control and supervisory oversight.

The performance of the personnel involved was considered excellent.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Maintenance and Material Condition of Keowee Hydroelectric Plant (KHP)

a.

Insoection ScoDe (62707)

During a dual KHP outage. the inspectors observed, reviewed, and

discussed major maintenance activities on and the material condition of

equipment at the KHP. The activities involved the KHP Unit 1 and Unit 2

voltage regulators, batteries, and the hydraulic water turbine governor

systems. The material condition included various pumps, air

compressors, and fire protection deluge systems.

b. Observations and Findinqs

The major maintenance activities were controlled by maintenance WO and

procedures. Among the WOs observed were those listed in section M1.1 of

this report. Among the procedures used were the following:

0

IP/0/A/2005/003, Westinghouse Voltage Regulator Test

0

IP/0/A/3000/026, Battery Corrosion and Connector Resistance

0

IP/0/A/0100/001,.Controlling Procedure for Troubleshooting and

Corrective Maintenance

0

MP/1(2)/A/2200/001, Keowee Governor Oil Pumps Assemblies

Inspection and Maintenance

o

MP/1(2)/A/2200/003. Keowee Governor Inspection and Maintenance

o

MP/1(2)/A/2200/006,

Keowee Permanent Magnet Generator and Speed

Switches

o

OP/0/A/1107/011, Removal and Restoration of Current

Transformer - Reactor Coolant Above 200 Degrees F

The maintenance activities included:

0

disassembling the connectors on 28 KHP battery cells, removing

corrosion, reassembling, and checking connector resistance

Enclosure 2

1

checking and adjusting the voltage regulators for proper operation

disassembling. inspecting, cleaning. and reassembly of components

within the governor and the permanent magnet generator assemblies

During the work activities on the components in the governor for KHP

Unit 1. maintenance personnel observed that the shutdown solenoid and

net head comparator sub-assembly was loose.

The mounting bolts had

backed out but not far enough for the sub-assembly to fall.

The bolts

were inspected by the system engineer, reinstalled, and torqued to 30

foot-pounds using thread locking compound.

The corresponding Unit 2

sub-assembly was checked immediately but did not appear to be loose.

After Unit 1 was returned to service, the Unit 2 subassembly mounting

bolts were similarly inspected, reinstalled, and also torqued to 30

foot-pounds with the locking compound present.

The inspectors observed that during the performance on Unit 1. of

Section 10.9, Voltage Error Detector Module Test, of procedure

IP/0/A/2005/003. the technicians were having difficulty with the Unit 1

module adjustments.

The difficulty with the adjustment was because the

gain on the card was at the high end of its range: this condition

probably had been that way since Keowee unit startup but had not

affected unit performance.

The inspectors observed that the gain on

both the KHP 1 and 2 modules were readjusted to a- more median prescribed

(lower) setting. The gain adjustment of the voltage error detector

module card was an example of good engineering and supervisory

oversight.

c.

Conclusions

During the dual Keowee Hydro Plant outage, the inspectors concluded that

maintenance activities were accomplished in accordance with approved

procedures, personnel were knowledgeable in the systems. practiced good

engineering judgement. and had sufficient supervisory oversight. The

inspectors also concluded that the material condition of the equipment

observed was good.

M3

Maintenance Procedures and Documentation

M3.1

Stroke Time Testinq of Safety Related Valves (Units i

2 and 3

a.

Inspection Scooe (61726)

As a result of a supervisory review, licensee personnel discovered that

a Unit 2 HPI suction valve potentially did not meet the stroke time

acceptance criteria during a surveillance test.

The discovery was made

six days after the completion of the test.

Enclosure 2

b. Observations and Findinas

Licensee personnel performed a surveillance on July 31 which stroke time

tested HPI suction valve 2HP-25.

(The valve and 2HP-24 are suction

valves in the HPI system.)

An approval review of the surveillance was

performed on Aug ust 6. During the review, it was discovered that the

valve potentially did not meet the stroke time acceptance criteria. The

stroke time was recorded as 14 seconds and the acceptance range was 11

to 13 seconds. The UFSAR time limit for this valve was 14 seconds

(integer valUe). The valve was declared inoperable, a stroke time test

was re-performed, the procedure tester was sought for interview, and a

PIP was initiated.

On August 7, the inspectors attended a management meeting at which all

HPI suction valve testing for all units was discussed.

Among the topics

of discussion were the stroke time testing and the lifting of links

during engineered safeguards (ES) testing of the valves. The lifting of

the links disabled the automatic operation of the suction valves. The

rounding off of stroke time testing results was also discussed.

The

inspectors were informed that the valve was retested and indicated a

time of 13.48 seconds that was consistent with the interview debrief of

the July 31 procedure tester.

During fact finding,.it was found that

this particular valve traditionally tested around this stroke time

length.

The PIP described the problem as a recording error where the

tester had mistakenly written down the maximum time as the stroke test

time.

.A decision at the management meeting was made to place the ES testing

procedures for the suction valves on hold, initiate changes to the

applicable procedures, and implement the procedure changes..

The inspectors observed, reviewed, and discussed this issue with the

licensee. As a result of observations and discussions four concerns

were identified.

The first concern involved the stroke time testing

review of valve 2HP-25.

The second concern involved the lifting of

links during testing. The third concern was associated with the second

and involved entering an applicable limiting condition for operation

(LCO)

during the time that the links were lifted.

The fourth concern

involved Dersonnel performing stroke time testing, and other testing, in

that results were rounded off.

Among the items reviewed for the concerns were:

0

Procedure PT/2/A/0152/11, HPI System Stroke Test. Revision 3;

PIP 2-097-2421, Stroke time of 2HP-25 recorded at 14 seconds:

o

Procedure PT/0/A/0310/012A, ES Logic Subsystem 1 On Line Test,

Change 26 and Revision 27:

Enclosure 2

13

PIP 0-097-2429. ES testing of HPI suction valves: and

PPT/0/A/0310/013A. ES Logic Subsystem 2 On Line Test. Revisions 31

and 32.

The inspectors observed from the review the following:

section 9.0. subsection 9.1, of stroke test procedure directed

that times be rounded off up or down to whole numbers;

o

section 10.9.5, subsections 10.9.5.b. c. and d of change 26 of the

logic subsystem 1 test directed electrical links be lifted and the

operators be informed that Unit 1. 2, or 3 HP-24 valve will not be

aDle to perform the intended safety function (during this out-of

service period):

o

section 10.9.5 and subsections 10.9.5.b. c and d of revision 31 of

the subsystem 2 test directed the same activities except Unit 1.

2, or 3 HP-25 valve was affected: and

o

revisions 27 and 32 respectively removed the requirement to open

the electrical links.

The inspectors' review results of the above concerns are as follows:

o

The operations staff did not remember such a recording error

previously nor had they had a previous problem in the reviewing

stroke test data on the shift that it was accomplished.

Inspectors reviewed the PIP data base to substantiate this

information. As a result of this isolated case, the inspectors

observed that unit operations supervisors were directed via

written shift guidance to review and verify the results of the

operations test group's acceptance criteria.

O

The licensee had historically lifted the ES signal links to

prevent reactivity changes during ES logic testing in that the

orated water storage tank (BWST)

head of water could flow into

the suction of HPI pumps.

Due to recent operations department

agreements and procedure changes LDST pressure has been increased

during testing to account for BWST head thereby minimizing

reactivity changes. Testing of suction valves have been altered to

delete the lifting of the links.

o

The inspectors reviewed the historical operator logs for the

reriods when suction valve surveillance was performed. Applicable

COs were entered when the links were lifted.

o

At the direction of operations management, specific round off

requirements have and are being added to the valve stroke

Enclosure -2

14

procedures.

Also, as a side issue, although a preliminary

overview of their personnel revealed no problems,

I&E staff have

agreed to review their rounding off methodology in the near

future.

The PIP corrective action and other information became available as the

investigation proceeded. The management decisions and licensee's

preliminary corrective actions determined that: in this case, rounding

of stroke time was performed incorrectly and that individual has been

counseled; the length of time it took to review the stroke test was

excessive but was an isolated case (with procedure changes forthcoming):

removal of valve control electrical links was unnecessary and

procedurally deleted: and overall valve testing expectations have been

clarified.

The licensee revealed additional facts concerning the valves. A valve

open position of approximately 17 percent would provide sufficient flow

for the HPI pumps. This would occur at 3-4 seconds after start of

stroke. One HPI suction valve would provide enough flow for all three

HPI pumps.

c. Conclusions

The failure to detect a potentially unacceptable valve stroke

surveillance in a timely fashion is identified as a weakness. However,

licensee management's disposition of the issue when identified was good.

Corrective items were appropriately addressed or captured by the

licensee's corrective action program.

M3.2 Startup Transformer Tan Chanoes

a.

InsDection Scone (62707)

During this period, the licensee increased the normal operating voltage

of the Keowee main transformer and the unit startup transformers by

altering transformer tap positions. The inspectors observed portions

of this work (see Section P1.2).

b. Observations and Findins

During the startup transformer tap changing activities, maintenance

reviewers closing the work package initiated

PIP 3-97-2600 on the work

covered under the minor modification OE 9370.

The PIP identified two

questions dealing with (1) the acceptability of reusing aluminum bolts,

and, (2) the fact that a WO invoked procedure was not used during the

work (the procedure was struck-through or lined-out as allowed under

local instructions). Based on their review of this issue and

examination of the fasteners, the inspectors have no concerns with the

reuse of the fasteners. The rationale in the PIP for the second problem

Enclosure 2

SII

was that the work was being performed on a QA-1 (safety-related) niece

of 20Ui pment and the PIP originator felt that the lined out orocedure

shoul'd have involved QA inspection on the work. The i nspector.will

review the requirements concerning QA with regard to safety-related

work.

This is identified as Inspector Followup Item (IFI) 50

269,270.287/97-12-04. Maintenance Oversight.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed)_LER 50-287/95-01: Packing Leak Due to Inappropriate Action

Results in Unit Shutdown

IR 50-269.270.287/95-17 discussed this event and described the root

cause. The licensee has subsequently implemented a corrective action

plan (described in PIP 3-095-0923) that included repacking two steam

valves which had been packed using the same packing as the failed valve.

changing two procedures to provide for better verification of packing

follower installation, and purchasing a fiber optic camera to allow for

better inspection of valve stuffing boxes.

The inspectors reviewed the plan and determined it was adequate.

The

insDectors found the corrective actions specified in PIP Report 3-095

0923 imolemerted as stated except for the procedure changes'.

Corrective

Action humber 3 specified three changes to Procedures MP/O/A/1200/001.

Valves - Non NRC 89-10 - Adjusting and Packing: and MP/O/A/1200/001D.

Valves - NRC 89-10 - Re placing and Adjusting Packing. One of the

changes specified a double verification step had been added for

technicians to sign that the packinq follower was not cocked.

The

inscectors found this steD in Procedure MP/O/A/1200/001 but not in

Procedure MP /O/A/1200/001b.

Procedure MP/O/A/1200/001D only contained a

caution on cocked packing followers.

The inspectors later determined,

after discussions with maintenance manacptment. that procedure changes

specified in Action Number 3 were actually implemented by Corrective

Action Number 4 to' the PIP report and that maintenance Dersonnel had

incorrectly specified the procedure changes in Action Number 3 after

Action Number 4 had been completed.

The inspectors agreed the

corrective actions had been implemented, however,

the inspectors also

considered the documentation in the PIP report to be poorly done without

proper attention to detail.

The inspectors further determined that, at the time of the event.

maintenance personnel did not properly follow procedures when repacking

Valve 3RC-3, constituting a violation of 10 CFR 50. Appendix B,

Criterion V, Procedures.

This non-recetitive. licensee-identified, and

corrected violation is being treated as a Non-Cited Violation,

consistent with Section VII.B.I of the NRC Enforcement Policy, NCV 50

287/97-12-08. Failure to Followi Valve Packing Procedure.

Enclosure 2

16

M8.2 (Closed) LER 50-287/95-02: Drop of Control Rod Group Due to Unknown

Cause Results in Reactor Trip

This event was discussed in IR 50-269,270.287/95-18. No new issues were

revealed by the LER.

M8.3 (Discussed - Open) VIO 50-269.270.287/96-10-03: Weld Procedure

Qualifications Welded, Tested, Certified and Approved by Same Individual

This violation was identified when the inspectors determined that the

licensee's weld procedure qualification program failed to provide an

independent QA review for the qualification process.

The licensee acknowledged the violation on September 11.

1996.

The

licensee attributed the violation to a lack of sufficient guidance in

the Duke Power Welding Program. Procedure L-100 in that it did not

reflect the independent QA review requirement of American National

Standards Institute (ANSI)

N-18.7-76.

Corrective actions taken to address this oroblem included discussion

with technical personnel to assure that they understood the QA

requirement for independent review of qualification records.

Also. the

licensee revised the subject document such that it requires that the QA

review be performed by an individual other than the one who performed

the qualification.

By this review, the inspectors ascertained that the revised procedure.

L-100. did not include directly or by reference the applicable QA

documents, e.g., Duke's QA Topical Report. Duke- or ANSI 18.7-76. The

licensee plans to revise the subject procedure to reference the

applicable QA commitments.

The inspectors discussed this observation with the cognizant engineer

who agreed to discuss it with management before incorporating it. in the

L-100 procedure. The inspectors indicated that this item will remain

open until final action had been taken on this matter.

M8.4

Closed) URI 50-269.270.287/96-17-04: Engineering Evaluation for the

Replacement of Carbon With Stainless Steel Piping

This item was identified due to a concern over the possibility that

large diameter e.g., greater than or equal to 24-inch, carbon steel

piping could have been replaced with piping made from stainless steel

material without sufficient engineering analysis to verify adequacy as

required by Revision 17 of theapp licable pipe specification PS300.4.

The licensee's review of data collected during tne pipe branch

connection analysis revealed that there was only one location per unit

where this substitution could have taken place.

This location was

identified as a 24-inch diameter pipe section, downstream of the "D

Enclosure 2

SII

17

heater drain tank pumps.

This pipe section connects the heater

vent/drain system to the condensate system.

Through discussions with the cognizant engineer and review of applicable

drawings. the inspector verified that Pipe replacement in the

aforementioned location had not taken place.

The inspectors concluded

that the licensee's investigation and findings were satisfactory.

M8. S-(Discussed - Ooen) VIO 50-269.270.287/96-17-09:

LPSW Modification Did

Not Meet ASME Code Section Xi Non-Destructive Examination (NDE)

Requirements

This violation was identified when the insoectors determined that the

licensee had failed to perform Code required examinations on certain

newly fabricated welds in the LPSW "B" line header.

The licensee acknowledged the violation on March 12,

1997 and listed the

corrective actions taken to fix the problems and the actions taken to

preclude their recurrence.

Through di scussi ons with cognizant personnel

and a review of records, the inspectors verified that the subject welds

were successfully hydrostatically tested per code requirements.

QA

Welding Technical Support and Engineering had been assigned specific

responsibilities and were given auoropriate training for implementing

special code requirements as applicable. Also, certain process control

forms had been revised to address more clearly post-maintenance testing

requirements, e.g.. hydro versus an alternate test method. Steps taken

to preclude the recurrence of this problem were addressed as near and

long term corrective actions in PIP 0-097-1691.

These actions were the

result of a Quality Improvement Team (QIT) assessment of Oconee's Post

Maintenance/Modification Testing (PMT)

Program.

Previous root cause

inspections found that the program was fragmented and that there 'was not

sufficient technical support and management oversight to assure that the

program served its intended function.

A summary of the major recommendations made by the QIT included:

development of a comDrehensive guidance document addressing PMT

activities: establish scheduling ties and reporting methods: establish a

PMT Working Group: establish a test .coordinator and adequately staff PMT

functions: and formalize weld process control and PMT testing

requi rements.

These recommendations were subsequently evaluated and

grouped into short and long term categories in PIP 0-097-1691.

The short term recommendations were to be resolved prior to the upcoming

Unit 1 refueling outage.

The insoectors stated that this matter would

remain ooen until the inspectors had an opportunity to review the

identified short term recommendations for adequacy prior to the

aforementioned outage.

Enclosure 2

18

M8.6

(Closed) IFI 50-269.270.287/93-20-01:

Instrument Impulse Lines and

Associated Inservice Inspection (ISI) Requirements

The inspectors had identified instrument impulse lines off of safety

related Emergency Core Cooling Systems (ECCS)

which were seismic, QA-1,

safety related lines up to the first instrument root valve (pressure

boundary) and were non-seismic, non-safety related lines from the root

valves to the instruments. The inspectors had raised the concern that a

loss of inventory or release of radiation could occur if the non-seismic

portions of the lines fail since the root valves to.these non-safety

related instruments are normally open valves.

The licensee performed an investigation of this situation -and a review

of documents to determine the required status of these lines.

PIP

report No. 0-094-0309 was opened to track actions and document results

of this investigation. The inspectors reviewed UFSAR Section 3.9.3.1.3.

and a letter dated May 6. 1996, from Duke Power Company (J. W. Hampton)

to the NRC formally acknowledging a verbal commitment made to the NRC to

upgrade .ECCS instrument lines to QA-1 status.

Also, the insoectors

reviewed the evaluations and corrective actions described in PIP 0-094

0309. reviewed portions of a draft calculation, OSC-6163, which .

documented the results of instrument line walk down inspections, and

confirmed that plant drawings and instrument details had been upgraded

to show the instrument impulse lines as QA-1.

QA-1 status assures that

these lines will be maintained i.n accordance with 10CFR50. Appendix B.

The inspectors also reviewed several walkdown packages. Wal kdown check

sheets included items such as the following:

verify instrument line is flexible enough to absorb the thermal

and seismic movements;

0

verify sufficient clearance exist such that seismic interaction

with adjacent equipment is not a concern:

o

verify instrument line is sufficiently supported to ensure failure

will not occur during a seismic event: and.

o

verify instrument valve is sufficiently supported to ensure that

failure will not occur during a seismic event.

The insoectors concluded that through the corrective actions the

licensee has met the coimmitment made to the NRC to upgrade the ECCS

instrument impulse lines to QA-1 status.

Enclosure 2

19

M8.7 (Closed) URI 50-269/96-04-04: Root Cause Assessment of Failures to

Valves 1MS-77 and 1LPSW-254

This item involved failures of valves in two separate systems which are

discussed below.

1MS-77, Second Stage Reheater Al Inlet Valve

1MS-77, a non-QA-1, non-safety related valve, failed to go closed on

demand. Troubleshooting showed the valve to be wedged in the backseat

with the thermal overloads tripped. When attempting to recycle the

valve the breaker tripped instantly. The licenee's investigation

determined that the open limit switch was set at 2 percent when the

procedure required 5 percent.

The licensee concluded that the valve was

going into the backseat every time the valve was fully opened.

This

resulted in requiring an excessive amount of motor torque to pull the

valve off of its backseat.

This problem then led to the motor on the

valve operator failing and causing the breaker to trip.

The licensee concluded that the valve failed because of improper valve

set up. The cause was personnel error. The root cause was considered

inadequate training. Training and Qualification Guide, ETQS # MOV-Q

LIMITORQUE, was amended to highlight this condition. The inspectors

reviewed the guide and confirmed the revised training instructions.

Additionally, the inspectors reviewed the task completion comments, PIP

.1-096-0417, and procedure IP/0/A/3001/010, "Maintenance Of Limitorque

Valve Operators."

The procedure was considered adequate and this issue

was considered resolved.

LPSW Valve 1LPSW 254. LPI Cooler Outlet Isolation

Valve 1LPSW-254 is the Unit 1 train A LPI cooler outlet isolation valve.

Valve 1LPSW-251 is the flow control valve for the same cooler and is

located immediately upstream of 1LPSW-254. Due to numerous LPSW system

component failures in the past, an adverse condition was identified.

The licensee's identification, testing, and proposed corrective actions

are identified and tracked in PIP 0-095-1491. Because of the similar

configurations of the LPSW cooler installations. this PIP is applicable

to all three Oconee Units.

A review of the numerous LPSW comoonent failures indicated that

vibration problems were principal'contributors.

Therefore, the licensee

performed extensive vibration testing and component inspections. The

results indicated that the excessive LPSW system vibrations were caused

by flow induced cavitation through the flow control valves. Based on

the vibration study and component inspection, the licensee had developed

an Urgent Nuclear Station Modification (NSM)

3022 which will.be

implemented on each unit at the next refueling outage.

The inspectors

Enclosure 2

20

reviewed portions of the Unit 1 modification package, NSM 13022. This

modification will replace flow control valves 1LPSW-251 and 1LPSW-252.

and associated downstream isolation valves 1LPSW-254 and 1LPSW-256. with

valves designed to reduce the flow induced cavitation and noise. Also,

flow control valves will be relocated to increase the distance between

flow Control and isolation valves.

Carbon steel piping immediately

downstream of the flow control valves will be replaced by stainless

steel piping.

The inspectors concluded that the licensee had identified the root cause

and developed necessary actions to correct the vibration problem. The

Unit 1 modification package had been developed and was scheduled for

implementation at the next Unit 1 refueling outage (September 1997).

Units 2 and 3 will receive the same modification. The licensee stated

that these modifications are in the preparation stage and will be

implemented at the next refuel-ing outage for each unit.

The inspectors concluded that the licensee had identified the root cause.

and taken action to correct the problem and prevent recurrence.

I II. E ngjneerng

El

Conduct of Engineering

E1.1 UFSAR Fuel Load Requirements

a.

Scooe of Inspection (71707. 37551)

Through Oconee site initiated PIP 0-97-2511. the licensee identified

that fuel enrichment had not been as specified in the UFSAR Section

4.3-3.1.4. This was discovered during a recent (August 13, 1997)

internal site review of the UFSAR.

b. Findings and Observations

The UFSAR section stated in part that "Each fuel rod is identified by an

enrichment code, and the desi gn of the reactor is such that only one

enrichment is used Per assembly."

This was not the case in all Oconee

units (starting in 1994 on Unit 2).

There are currently multiple

batches of fuel in use at Oconee that have axial blankets (regions of

reduced enrichment at the upper and lower ends of the fuel rods). Also,

the fuel currently being received for the upcoming Uni't 1 outage

contains fuel pins of varying enrichment within the same assembly (this

is the first such fuel used at Oconee). The 10 CFR 50.59 review that

was generated by the corporate office for this upcoming Unit 1 fuel load

change did not address this UFSAR statement. TS 6.9 covered fuel

analysis methodology and other NRC - licensee transmittals had

Enclosure 2

21

previously approved fuel design techniques with stringent critical

parameter limits.

Previous fuel reload and 10 CFR 50.59 analysis were being reviewed by

the licensee and a root cause analysis was on-going to determine how the

UFSAR requirement was overlooked. The licensee has stated in the above

PIP that the there is no present operability concern. Until the

licensee completed their 10 CFR 50.59 and fuel load UFSAR revie,, this

item will be identified as URI 50-269,270.287/97-12-02. Fuel Load UFSAR

Statements.

c. Conclusions

During a programmatic review of the UFSAR. the licensee discovered that

a fue enrichment statement had not been addressed by the 10 CFR 50.59

evaluation. The licensee entered the discrepancy into their corrective

action program.

An URI has been identified on this issue.

E1.2 Modifications to Startup Transformers and Keowee Voltage Requlators

a. Inspection Scope (37828)

The inspectors observed, reviewed, and discussed the installation of

minor modifications (MM)

to the startup transformers, the degraded grid

relays, the KHP main transformer, and the KHP voltage regulators. The

activities started on August 18 and completed on August 22. During this

time frame, maintenance activities were also observed and are documented

in Sections M2.1 and 3.2 of this report.

b. Observations arid Findings

The MM installations observed were the following:

0

MM. 10264, changed the set point on the degraded grid relays:

o

MM 9368, changed the taps on startup transformer CT 1. (similar

MMs were performed on startup transformers CT2 and 3 as well as

the KHP main transformer);

0

MMs 9323 and 9324, installed a new logic network in the KHP Unit 1

and 2 voltage regulators ; and

a

MM 9375, changed the relay settings for the KHP main transformer.

The MM for the voltage regulators were installed in order to return the

base and voltage adjusters to a preset level when an emergency start

signal is received. When the units are operating to the grid the

regulators may be set at a voltage output different from the required

emergency start output.

Enclosure 2

22

The ins ectors observed the post modification testing.

Durin testing

of the Unit 2 KHP regulator, a small electric motor timer failed to meet

a time required. The motor was replaced under engineering direction and

the MM was successfully tested. The test of the startup transformers

and the KHP main transformer indicated adequate output voltages.

c. Conclusions

The inspectors concluded that the Keowee Hydro Plant modifications were

installed in accordance with approved packages with supervisory and

engineering oversight. The replacement of the voltage regulator motor

timer was an example of good engineering activities.

E2

Engineering Support of Facilities and Equipment

E2.1 Water Hammer Status

a. Inspection Scope (37551)

The inspector reviewed engineering evaluations of water hammer issues

documented in various PIPs. The licensee had a severe water hammer

event in 1996 as discussed in IRs 50-269,270,287/96-13 and

50-269,270.287/96-15.

b. Observations and Findings

Following the heater drain line break in late September 1996. the

licensee had become more sensitive to water hammer issues.

Since that

date, approximately 30 PIPs have been generated to have engineering

evaluate water hammers that have been identified.

For example, these

water hammers have been identified in the main steam reheater drain

piping. steam separator reheater drain piping, main feedwater piping,

and auxiliary steam piping.

Engineering continues to evaluate and

monitor water hammers as they occur. No major problems have been

identified with water hammers to date.

c. Conclusions

The licensee initiated adequate measures to track and evaluate water

hammers in the various piping systems.

E2.2

Partial Discharge Testing of Electrical Power Cables (Keowee)

a. Insoection ScopeL375511.

The inspectors observed, reviewed, and discussed, with the licensee's

engineering personnel, the performance of a partial discharge test

(PDT).

The test was performed on the underground 1.3.8 kilo-volt (kV)

power cable feeds from the KHP to the transformer CT.

Enclosure 2

23

b. Observations and Findings

On August 5, 1997, licensee personnel and a vender representative

(vender-rep) performed a PDT on the six, two per phase. KHP underground

power cables. The cables are each rated at 10 kV phase-to-phase. 8 kV

phase-to ground, and operate at 13.8 kV phase-to-phase. The cables are

approximately 4000 feet long.

The test equipment used by the vendor-rep was especially fabricated for

the licensee. It consisted of a view screen, a computer, an operating

keyboard, and a floppy drive. The equipment also had calibration

devices.

The inspectors observed the determinating and terminating of the cables,

the hook up of the test leads, and the performance of the PDT by the

vender-rep. The inspectors observed that the activities were documented

in WO 96089265 and procedure IP/0/A/2000/01, Power and Control Cable

Inspection and Maintenance, Revision 4. The test set up contained a low

power/high voltage alternating current source, a high voltage interface

device, hookup wiring, and the special test equipment. The PDT on each

cable was performed at rated and at 110 percent of rated phase-to-ground

voltage.

The inspectors also observed and concluded from the reviews,

observation, and discussions the following:

0

the oversight of determinating and terminating of the power cables

and the identifying of the specific cables was performed by onsite

engineering personnel;

o

personnel from corporate and the McGuire Nuclear Station were at

the KHP observing the test and were briefed by the vender-rep and

engineering personnel;

the PDT was performed by the skill of the vendor-rep, with

assistance and oversight from engineering personnel;

0

information on how the test equipment functioned and how to

operate it was shared by the vendor-rep and site personnel:

o

the vender rep established a preset trigger level for detecting

partial discharges;

o

a step-by-step procedure for the operation of the test equipment

was not available;

o

however, view screen pictures. with explanations, showing various

aspects of the PDT were available; and

Enclosure 2

24

the maximum voltage applied during the test was set by engineering

personnel and was from 9.02 to 9.4 kV.

The inspectors were informed and observed that no partial discharges

were detected above the preset trigger level at rated voltage and at 110

percent of rated phase to ground voltage. The inspectors were also

informed that, based on the results of the PDT, the six cables were in

excellent condition.

c. Conclusions

The PDT of the Keowee Hydro Plant underground cable was under the

control of engineering personnel.

The activities were conducted in a

deliberate and professional manner. The test was performed without

difficulty.

E2.3 Pressure Seal Leak On Valve 2LP-1 (Unit 2)

a. Inspection Scooe (37551)

The inspectors observed, reviewed, and discussed with licensee

management. operations, maintenance, and engineering personnel the

corrective action plan for the pressure seal leak in valve 2LP-1.

The

leak is also discussed in section 01.3 of this report. The inspectors

also attended working level and management level meetings at which the

leak was discussed.

b. .Observations and Findings

The inspectors used NRC Part 9900 Technical Guidance, On-Line Leak

Sealing Guidance for ASME Code Class 1 and 2 Components, dated July 15.

1997, during the observations and reviews of the leak sealing

activities. Among the items reviewed were the following:

0

Temporary Modification (TM) 1376, Seal Leak Repa.ir on Valve 2LPI

1:

0

procedure TN/1/A/1376/TSM/00M, Installation of TSM-1376:

o

10 CFR 50.59. Unreviewed Safety Question Evaluation, for TSM-1376;

o

procedure PT/2/A/0152/12. Stroke Testing: and

a

maintenance WO 97076613-01.

The insorctors attended several meetings, with both management and

engineering, during which the valve was discussed.

The inspectors also

attended P ant Operating Review Committee (PORC)

meetings which also

Enclosure 2

25

discussed the leak. The inspectors observed during-the meetings and

reviews the following:

Managers, i ncluding senior managers. were actively involved in the

assessment, options, and evaluation of the leak;

o

engineering personnel stated that the injection would be made into

a void above the pressure seal ring of the valve, therefore, the

pressure boundary was not involved;

a

licensee personnel considered the valve as being operable and

would remain capable of performing the required safety function

throughout the sealing activity;

o

the injection would be performed with the primary system at 360 to

380 psig and at 260 to 300 degrees F;

o

following the expected successful injection, with the leak

stopped, the valve would be stroked to verify operability;

o

the cause of the leak was not specifically discussed

(historically, an :ngineering evaluation on this valve had existed

since the May 22. 1997 startup):

o

the valve fasteners were observed to be intact, by the use of

video tape, and they appeared to be covered by the boric acid and

water solution escaping from the leak:

o

engineering personnel stated that the small amount of sealant to

be injected, (20 cubic inches maximum), the number of holes

drilled (six maximum), the number of injections allowed (maximum

of two), and the location of the holes would not affect 1.e

structural integrity of the valve:

o

a plan was discussed which directed that should the seal fail

during the repair activity personnel were to evacuate the reactor

building as quickly as possible: and

o

engineering personnel stated that the valve would be disassembled,

inspected, and the seal ring would be replaced, possibly with a

new type, during the next refueling outage.

The inspectors were informed that the valve was a cast valve and

technical information only gave minimum thicknesses and not actual

thicknesses. The use of a physical drill stop would not apply under

these conditions. The method to be used was.that the holes would be

drilled slowly, by hand, and would be stooped as soon as pressurized

water was reached. The inspectors were also informed that if the leak

Enclosure 2

26

could not be stoyped the plant would be taken to cold shutdown and

defueled for rep acement of the pressure seal.

At the end of this report period Unit 2 was at the planned reoair

temperature and pressure. The sealing activity had not started..

c. Conclusions

An existing minor body to bonnet leak worsened on a Unit 2 LPI valve

that was unisolatable from the RCS.

The inspectors concluded that .the

expected leak repair activities: were discussed with appropriate

management involvement; had good engineering input; had appropriately

developed procedures; and had an aproved method for injecting approved

sealant with appropriate on-line sealing guidance for ASME C ass 1 and 2

components.

E3

Engineering Procedures and Documentation

E3.1

Degraded Voltage Relay As-Found Condition

a.

Inspection Scope (62707.

37551).

The inspectors observed the performance of WO 97027649-01, Change

Degraded Relay Setpoints.

b. Observations and Findings

This work order implemented MM ONOE-10264: 27YBDGX. Y. Z Degraded Grid

Relay Set Points, which changed the 230KV degraded grid undervoltage

relay setpoints by changing the calibration procedure.and then

reca :brating the relays using the revised procedure.

On August 18, 1997 technicians changed the setpoints on Degraded Grid

Undervoltage Relays 27YBDGX, 27YBDGY. and 27YBDGZ by recalibrating the

relays to the new setpoints specified in the modification. The

technicians used Procedure IP/0/A/4980/27G, IPE 27N Relay. Revision 5.

which had been revised to incorporate the new setpoints, to perform the

setpoint change.

When technicians measured as-found setpoint values for

the relays, the values were out-of-tolerance from those specified in the

procedure.

However, the technicians did not notify engineering of the

out-of-tolerance as-found condition because Procedure IP/0/A/4980/27G

contained a step permitting the option of not reporting an out-of

tolerance as-found condition if the condition resulted from a procedure

change. The revised procedure did not give any guidance as to whether

the relay was actually within the tolerance specified from the previous

calibration.

The inspectors discussed this with engineering personnel who stated

their expectations were for all out-of-tolerance conditions to be

Enclosure 2

27

reported to engineering who would then determine whether or not the

condition warranted further corrective action.

The inspectors also

reviewed several other relay calibration procedures and found all of

them to contain a step permitting the option of not reporting an if the

condition resulted from a procedure change. The licensee entered the

condition into their PIP 0-097-2796.

The circumstances surrounding this issue will be tracked as

URI 50-269.270.287/97-12-03, Relay As-Found Conditions, pending review

of: 1) the administrative requirements for documentation and evaluation

of as-found test conditions, and 2) the determination of the extent to

which the option of not reporting an out-of-tolerance as-found condition

existed.

c. Conclusions

During a degraded grid undervoltage relay setpoint change. workers did

not have as-found set points evaluated due to a potential procedure

problem. This was left as an unresolved test control issue until the

licensee completed a corrective action review.

The licensee understood

the nature of the problem and initiated appropriate corrective

evaluation.

E4

Engineering Staff Knowledge and Performance

E4.1

Management Activities

a. Insoection Scooe (37551. 40500)

During the period, the inspector observed manacement activities at the

site.

b. Observations and Findings

During this period, the licensee has initiated several new process

improvement efforts.

The inspectors have observed that engineering

operability evaluation progress, plant concerns, and action register

items have been added to the agendas of the three main plant meetings.

This has been formalized in trackable handouts that are actively

discussed at each of the meetings. The increased level of detail and

the focus that these provide is noteworthy.

The residents attended engineering daily review meetings that have

evaluated: the engineering work in progress to suDDort the plant; plant

deficiency closeout progress; and modification package pcogress. PIP

backlogs have been reduced and additional engineering support added.

Several plant management requested assessments have been accomplished

during tne past several months.

These have focused on understanding

Enclosure 2

28

plant interactions and problem areas.

The inspectors have attended

several of the exit meetings of these assessments and local management

has responded well to the negative findings particularly in the areas of

welding and post modification and maintenance testing controls.

Also,

the equipment mispositioning assessment has been on going with recent

recommendations delivered in PIP 97-2292. The licensee has a major

electrical reliability assessment to be completed by the end of the

year.

The Site Vice President has held several meetings to communicate clear

expectations. He has met with managers and has held a large plant staff

general meeting at a local auditorium to clearly discuss recent plant

problems and re-identification of expectations. The senior resident

attended a portion of the large general meeting and found the

presentation to be informative with the message well defined.

c.

Conclusions

Engineering and site management have recently instituted a new focus and

direction for the plant through process improvement efforts.

Preliminary output from the effort has been positive.

E4.2 Unit 1 Integrated Control System (ICS) Modification

a. Insoection Scope (37550)

The inspector reviewed the licensee's activities to incorporate lessons

learned from the Unit 3 ICS modification into the upcoming Unit 1 ICS

modification.

Applicable regulatory requirements included 10 CFR 50 Appendix B. Updated Final Safety Analysis Report (UFSAR). and American

National Standards Institute (ANSI) N45.2.11 - 1974, Quality Assurance

Requirements for the Design of Nuclear Power Plants.

b. Observattons and Findings

The licensee identified deficiencies during the Unit 3 ICS

post-modification.testing which were entered into the PIP process for

tracking and resolution. An ICS design feature which initiated

automatic feedwater valve control when the ooerator station was in

manual and a steam generator (SG)

low level limit was reached caused

operator confusion (PIP 3-97-0854).

This feature will remain in Unit 3

until the next Unit 3 outage. The design feature was deleted from the

Unit 1 design as demonstrated by revision DB to Unit 1 drawing 0.M.

201.H-0183.001. Feedwater Control, Loop A Valves and Low Level Limits.

Poor control at low power/low feed flow conditions due to the power/flow

error signal inconsistency at this condition was corrected by a square

root extractor function in the module code for Unit 3 (PIP 3-97-0858).

The Unit 1 design was changed to use the level transmitter in the linear

mode which provided a more reliable power/flow error signal.

Enclosure 2

29

Inadvertent shift of the ICS component STAR modules to hand (manual)

mode was noted (PIP 3-97-1015).

The cause was determined to be a

characteristic of the module self-checking circuit which was corrected

by requiring three points per self-check rather than one.

This

modification was being programmed into the individual STAR modules. The

program code correction implemented to resolve feedwater

valve cycling at ten to fifteen percent power resulted in the

inadvertent deletion or overwrite of required program code functions

(PIP 3-97-0910).

The corrective action added barriers to the process

for ICS program code revisions.

c. Conclusion

The licensee implemented appropriate measures to incorporate lessons

learned from the Unit 3 ICS modification into the Unit 1 modification.

Design and operational deficiencies identified in the Unit 3

modification were adequately addressed for Unit 3 and addressed in the

Unit 1 design and modification implementation procedure changes.

E4.3 Expandino Engineerin. Knowledoe Base

a. Insoection Scope (71707.-37551

During the course of this period; inspectors observed engineering

personnel in the control room and in the plant making rounds with the

non-licensed operators (NLO).

b.

Observations and Findings

Engineering management provided direction that their staff become more

operationally focused. Part of this philosophy was direction for system

engineers to perform monthly walkdowns of systems and to accompany a

non-licensed operator on rounds. The inspectors observed this being

implemented in several instances.

Site engineers were observed to be in the Unit 1 and 2 common control

room at the operations morning briefing. The operations Onshift Manager

indicated-that these engineers would be going with the NLO on their

plant rounds and should be provided any support and information that

they requested.

c. Conclusions

Engineering management has instituted a practice of monthly system

engineer tours with non-licensed operators.

Enclosure 2

30

E8

Miscellaneous Engineering Issues (92903)

E8.1

(Discussed - ODen) Deviation (DEV) 50-269.270.287/94-24-04: Design Basis

Requirements for the Penetration Room Ventilation System (PRVS)

IR 50-269,270.287/94-24 discussed the issue of leakage from the PRVS.

Testing in 1992 had revealed that the PRVS ability to maintain a

negative pressure was affected by auxiliary building air handling

unit/fan combinations. The licensing basis assumes all leakage into the

penetration room will be filtered prior to release. There is no

provision for any leakage to bypass the PRVS via leakage into the

auxiliary building. The only method to ensure all leakage into the

penetration room gets filtered is to have the penetration room airtight

or at a negative pressure with respect to its surroundings (i.e. both

the atmos here and the auxiliary building) during an accident. The

licensee has completed extensive testing and sealing of identified leak

paths from the penetration room to other surrounding rooms.

The licensee has decided to pursue a licensing approach by uodating the

current off-site dose calculations to presently accepted methodology.

This will allow the deletion of the PRVS from TS.

Implementation of the

TS and UFSAR changes have been assigned due dates of December 31. 1997

and July 5, 1998. respectively.

E8.2 Li.ussed - Op en) IFI 50-29.270.287/95-03-01: Clarification of TS 3.3.1

This item addressed HPI operability requirements below 60 percent power.

In November 1990 with their then existing engineering analysis, the

licensee identified that below 60 percent power an injection line nozzle

break could result in insufficient flow to the reactor core assuming a

single failure if only two HPI pumps were operable.

The licensee 'has

committed to revise TS 3.3.1. The revision was submitted to NRC on

March 31. 1997. Due to events involving the HPI pumps in April of 1997,

the licensee has committed to conduct an HPI reliability study. This

study is due to be submitted to the NRC on December 31. 1997. The TS

revision will be completely processed following the review of the

reliability study; segments of the revision may be completed earlier,

based on a September 4. 1997, licensee docketed request.

E8.3

(Closed) ADarent Violation (EEI

50-269.270.287/96-03-02 (EA 96-090):

Inoperability of Containment Hydrogen Control Systems

This item addressed a lack of drainage for condensate that could block

flow during operation of the hydrogen recombiner.

This issue was closed

by letter dated April 16,

1996. granting enforcement discretion.

Enclosure 2

31

E8.4 (Closed) LER 50-270/95-02: Incorrect Timer Setting Due to a Design

Deficiency Results in a Reactor Trip

The reactor trip of Unit 2 was discussed in IR 50-269,270.287/95-06.

The LER stated that modifications would be installed in each unit to

change the timer set points for the loss of excitation relays. The

inspectors observed that minor modifications ON0E 8045, 8051. and 8085

were installed on Units 1. 2. and 3. respectively, which changed the set

points.

The set points were raised from 0.8 to 30 seconds. The LER

also stated that a review would be performed so that other protective

relay timers would be set as required. The review was completed and

processes are in place, such as procedure changes and minor

modifications, to ensure that both safety related and non-safety related

relays have.adjustment information. Based on the licensee's actions

this LER is closed.

E8.5 (Closed) VIO 50-287/97-02-06: Inadequate Control of Purchased Material

and Equipment

This item addressed inadequate procurement control activities which

contributed to the receipt and installation of a safety related eight

inch ball valve (LP-40) which did not meet the Duke Power specification

referenced in the purchase order. The incorrect reverse acting valve

contributed to a loss of RCS shutdown inventory on February 1. 1997.

Additional issues associated with this item included an operation's poor

practice for manual valve position verification and maintenanceIs poor

communication of the abnormal equipment configuration represented by the

reverse acting valve.

The licensee's response to the violation, dated July 2. 1997, specified

corrective actions to address performance deficiencies by the

procurement, operations, and maintenance organizations. The inspector

reviewed a licensee vendor follow up audit, operations and maintenance

procedure revisions, and training documentation which documented

completion of the corrective actions stated in the licensee's response.

The inspector concluded that the procurement, operations. and

maintenance performance deficiencies which contributed to the

installation of the incorrect safety related valve (LP-40) were

adequately resolved.

E8.6 (Closed) VIO 50-269.270.287/97-02-08: Inadequate Corrective Action and

Design Control for Reactor Building Cooling Unit (RBCU)

Fuses

This item addressed the licensee's inadequate corrective action to

resolve an identified incorrect fuse installation in the RBCUs.

The

corrective action did not adequately evaluate the equipment design to

determine the appropriate fuse size and type for the application.

Additionally, the corrective action did not identify the operability

Enclosure 2

32

significance of the issue and did not properly categorize the associated

PIP.

The licensee response to the violation dated July 2, 1997. specified

corrective actions to include a root cause analysis, minor modifications

to install the correct fuses, PIP program improvements in screening PIPs

for significance, and clarified responsibilities for fuse selection.

The root cause analysis was documented in PIP 0-097-1109, dated April 1,

1997. The minor modification to replace the fuses were completed in

January. 1997. The PIP screening process was revised in late 1996.

which was after the inappropriate categorization of the original RBCU

fuse issue PIP. The inspector concluded this item was adequately

resolved.

E8.7

Closed) IFI 50-269.270.287/95-14-01: Qualification Extension of Keowee

Batteries

This item was initiated to follow up on the licensee's qualification

extension of the Keowee batteries from ten to twenty years. The initial

qualification extension report reviewed by the inspector in 1995

indicated that several battery cells did not meet the electrical

capacity requirement following the seismic test. The test report did

not address the failed cells and therefore the qualification was not

conclusive. The licensee subsequently contracted with a vender, Nuclear

Logistics Incorporated (NLI), to evaluate the battery for qualification

extension. The qualification was documented in Keowee Battery

Qualification Calculation, C-017-050-1. dated August 22, 1996.

Calculation C-017-050-01 based the ten-year qualification extension on

two separate tests conducted at Wyle laboratories on similar batteries.

The seismic test which verified the structural/mechanical properties was

documented in Wyle test report 44681-2 dated February 1. 1981.

This

test was performed on a similar but heavier battery which was

conservative for the Keowee battery application. The battery was

artificially aged.which resulted in loss of cell electrolyte but did not

impact the results of the structural/mechanical properties.

Wyle test report No. 45110-1. dated March 21, 1996,

for NLI verified the

electrical properties of the battery for extension by testing a similar

battery which had been naturally aged for 24 years. As in the previous

test, the battery was subjected to seismic vibration conditions which

enveloped the seismic test response spectra for the Keowee batteries.

Electrical testing after the vibration test verified the batteries.

exceeded the 80 percent capacity required to establish qualification.

The conclusion of qualification calculation C-017-050-01 was that the

Keowee batteries were qualified for a total of 20 years, which included

the 10-year extension.

The inspector concluded the qualification

extension was appropriately supported by testing and analysis.

Enclosure 2

33

E8.8 (Discussed-Ooen) IFI 50-269.270.287/96-03-04: Installation of New Ground

Detection System

This item addressed the licensee's planned actions to improve their

limited capability to detect vital direct current (DC) system grounds.

A 1995 study of the issue recommended several actions to improve the

capability to detect grounds. The study established a 500 ohm.critical

value for grounds which impact safety related equipment. The present

setpoint for the ground detection system is 1500 ohms which would

provide detection before impact on safety related equipment.

The study

indicated that balance of plant equipment could be impacted by less

significant grounds, i.e., those greater than 1500 ohms and not

detectable by the present ground detection system. This impact could.

result in plant transients which could eventually challenge the plant

safety systems. The modification to install the more sensitive qround

equipment, although tentatively planned, is not currently scheduled or

developed. Due to the importance of the new ground detection system

this item remains open to track implementation of this modification.

E8.9

(Closed) Deviation 50-269.270.287/95-09-03: Fatigue Analysis for RCS

Auxiliary Piping

This item addressed the fact that RCS auxiliary piping had not been

inspected. designed, and tested as Class I piping in accordance with

USAS B31.7, Code for Pressure Piping, Nuclear Power Piping, dated

February, 1968, as stated in the UFSAR. The piping had been designed,

tested and inspected as Class II piping.

The licensee's response to the

deviation dated July 21.

1995, stated that a fatigue analysis of the RCS

auxiliary piping would be performed to establish that the Class I Code

requirements were met. It further stated that a schedule for the Diping

analysis would be developed by March 1, 1996 and all analysis would be

completed by August 31. 1999. Additionally, the UFSAR would be updated

to reflect the as-built condition until the fatigue analysis was

complete.d.

The inspector reviewed the RCS auxiliary piping fatigue analysis

schedule which was provided to the NRC by a Duke Power lettor dated,

February 22, 1996, and verified the scheduled commitments were being met

up to the date of this inspection. These included awarding a vendor

contract to perform the analysis and development of the applicable

specifications.

The UFSAR amendment dated December 31. 1996, stated the

Class I piping analysis would be completed on August 31. 1999. Based on

completed and scheduled corrective actions, the inspector concluded this

item was adequately being addressed and tracked.

Enclosure 2

34

IV. Plant Su port Areas

R4

Staff Knowledge and Performance in Radiological Protection and Control

(RP&C)

R4.1 Test Technicians Radioloical Practices

a. Inspection Scope (71750)

The inspectors observed the radiological practices of test technicians

performing testing on the Unit 3 HPI System.

b. Observations and Findings

On August 27. 1997 during performance of PT/3/A/0202/11, HPI System

Performance Test, technicians made pump pressure readings inside a

contaminated area and communicated with the control room via a phone

outside the contaminated area.

As protective clothing the technicians

wore cotton liners and rubber gloves on their hands with cloth booties.

and rubber covers on their shoes. Both technicians made readings and

talked with the control room. When crossing the contaminated area

boundary, the inspectors observed each technician remove shoe covers and

rubber gloves, leave them inside the contaminated area boundary, and

exit the area wearing the cloth booties and cotton gloves.

Upon re

entry, the technicians put on the same rubber gloves and shoe covers

that had been removed earlier.

This practice occurred more than once

while the inspectors were watching.

When questioned, the test technicians indicated that they felt the

practice to be acceptable based on their past experience, however.

licensee radiological personnel indicated this was not an acceptable

practice without the direcL assistance of radiation protection

personnel.

No radiation protection personnel were present at the job

and radiQlogical personnel only provided general procedural guidance on

the use of the practice.

The licensee has established a System Radiation Protection Manual in

order to meet the requirements of 10 CFR Part 20 and the technical

specifications.

The inspectors reviewed Procedure 1-13. Use of

Protective Clothing and Related Equipment. Revision 2 from this manual.

Step 5.3 of this procedure described the process for removing protective

clothing and instructed users to "Remove booties as you transfer to the

step-off pad which is considered clean."

The inspectors determined that

test technicians failed to follow Procedure 1-13 when removing

protective clothing while performing the HPI System Performance Test on

August 27. 1997 and this constituted a violation of 1OCFR Part

20.1101(a).

This will be identified as Violation 50-287/97-12-05,

Failure to Remove Protective Clothing.

Enclosure 2

c. Conclusions

The inspectors identified a violation for test personnel exiting a

contLami nated area without properly removing protective clothing.

P1

Conduct of EP Activities

P1.1

Emeroency Planning Drill

a. Insoection Scooe (71750)

The inspectors observed portions of the emergency drill conducted August

26. 199

b. Observations and Findinas

During the scenario, the plant experienced a simulated earthquake with a

magnitude of greater than 0.05g. The procedure for damage assessment

required an examination of the tendon gallery in order to confirm the

earthquake magnitude and directed the plant be taken to cold shutdown if

the magnitude was greater than 0.05g. Personnel in the simulated

control room challenged the Technical Support Center (TSC) on the length

of time taken to assess the earthquake magnitude with the plant in'

hot

shutdown conditions. Control room personnel also challenged the TSC on

the decision to remain in hot shutdown with water present in the LPI

pump rooms. Control room personnel felt the plant should be taken to

cold shutdown before conditions in the LPI rooms degraded any further.

The decision to remain in hot shutdown later proved to be correct.

however, the challenges by control room Dersonnel showed a good

questioning attitude. Control room personnel also used three-way

communications extensively during the scenario, particularly when

performing emergency operating procedures.

c. Conclusions

During an August emergency plan drill, control room personnel showed a

good questioning attitude and properly used three-way communications.

S1

Conduct of Security and Safeguards Activities

S1.1 Comoensatory Measures

a. Inspection Scone (81700)

The inspector evaluated the licensee's program for compensatory measures

of security equipment that was not functioning as committed to in the

Physical Security Plan (PSP) and procedures. This was to ensure that

the implemented measures were equal or better that the commitments made

by the licensee.

Enclosure 2

36

b. Observations and Findings

The three compensatory measures operational during this inspection were

reviewed. These measures compensated for inoperable equipment and

consisted of the application of specific procedures to assure that the

effectiveness of the security system was not reduced.

c. Conclusions

Through observations, interviews. and documentation review, the

inspector concluded that the licensee used compensatory measures that

ensured the reliability of security related equipment and devices. This

evaluation verified that the licensee employed compensatory measures

when security equipment fails or its performance was impaired. The

inspector found no violations of regulatory requirements in this area.

S2

Status of Security Facilities and Equipment

S2.1 Vital Area Access Controls

a. Inspection Scope (81700)

The inspector evaluated the licensee's program to control access of

packages, personnel, and vehicles to the vital areas according to

criteria in the PSP.

b. Observations and Findings

The inspector's review was to ensure that the licensee provided

appropriate access controls for the vital areas.

Personnel, hand-carried packages or material, delivered packages or

material, and vehicles were searched before being admitted to the

protected area and, subsequently, the vital areas. Security personnel

searched for firearms, explosives, incendiary devices, and other items

that could be used for radiological sabotage. These searches were

either by physical search or by search equipment. Security personnel

searched certain delivered packages and materials, approved by NRC and

specifically designated by the licensee, within vital or protected

areas. This was for reasons of safety, security, or operational

necessity. Vehicle searches included'a search of the cab, engine

compartment. undercarriage, and cargo areas.

The inspector found the following circumstances concerning personnel

access control. A picture badge identificat.ion system was used for

personnel who were authorized unescorted access to protected and vital

areas. A coded, numbered badge system was used for personnel authorized

unescorted access to vital areas. The code corresponded to vital areas

to which individuals authorized access. Picture badges issued to non

Enclosure 2

37

licensee personnel indicated areas and periods of authorized access

information magnetically encoded and showed that no escort was required.

Personnel displayed their badges while within the vital area, and

returned them upon leaving the protected area. Visitors authorized

escorted access to the protected area were issued a badge that showed an

escort was required, and were escorted by licensee-designated escorts

while in the vital area.

Unescorted access to vital areas was limited

to personnel who required such access to do their duties. Security

personnel controlled access to the reactor containment when frequent

access was necessary to assure that only authorized personnel and

material entered the reactor containment.

Access control program records were available for review and contained

sufficient information for identification of persons authorized access

to the vital areas.

The licensee maintained access records of keys, key

cards, key codes, combinations, and other.related equipment during a

person's employment or for the duration of use of these items.

The inspector found the following circumstances concerning control of

the entry and exit of packages and material to the vital area. Security

personnel confirmed the authorization of, and identified packages and

material at access control portals before allowing them to be delivered.

The licensee used security force personhel to identify and confirm the

authorization of material before allowing it to enter reactor

containment.

The inspector found the following circumstances concerning vehicle

access control.

Individuals who controlled the admittance control

hardware that allowed vehicle access to vital areas were armed, within

the vital area, or had control of the keys that open the vital area.

Security force personnel escorted non-designated vehicles while within

the protected and vital area.. No vehicle entered licensees' vital areas

during this inspection.

c. Conclusions

This evaluation of the vital area access controls for packages,

personnel and vehicles revealed that the criteria of tie PSP were

carried out. The inspector identified no violations of regulatory

requirements in this area.

S4

Security and Safeguards Staff Knowledge and Performance

S4.2 Control of Safeguards Information

a. Insoection Scone (81810)

The inspector reviewed PIP 4-097-2397 concerning an electrical systems

engineer's (ESE) Safeguards container that had not been properly

Enclosure 2

38

secured. This review was to determine whether Safeguards Information

(SGI), as defined in 10 CFR 73.21. Nuclear Systems Directive 206.

"Safeguards and Information Controls." Rev. 5. dated June 16. 1997, and

Security Guideline - 17. "Safeguards Workplace Procedures." dated August

7. 1997, had been disclosed or compromised.

b. Observations and Findings

The licensee's investigation revealed the following:

o

Between the hours of 5:37 p.m., August 4, 1997 and 5:52 a.m.

August 5. 1997 a drawer of an ESE safeguard container was left

unsecured in the Engineering Safeguards Work Area (ESWA).

The safeguard's container was within the protected area.

o

The ESWA was monitored by an alarm system.

The main entrance door

was controlled by an electrical keypad lock.

The second door was

locked from inside. Review of the annunciator records/logs showed

that no entries into the ESWA during the above time were made.

o

All documents within the container were accounted for based upon a

review of container contents against the containerinventory

listing.

The immediate corrective action was the securing of the container and

it's content. Intermediate and long term corrective actions were as

follows:

0

Corrective action concerning the individual who left the container

unsecured had not been completed during this inspection.

Counseling was recommended in the PIP.

A final barrier was added at the egress point from the ESWA to

remind personnel to self-check the security of the ESWA.

Additional signage was added to remind personnel of the need to

self-check the area.

o

All site "Routine Users" of SGI were made aware of the incident to

enhance their security awareness.

o

All site "Routine Users" of SGI were reminded of the importance of

using self-checking processes to ensure compliance with the SGI

control program.

Security Guideline -18, states, "SGI not being utilized, must be secured

in

designated containers.'

This non-repetitive. non- willful, licensee

identified, and corrected violation is being treated as a Non-Cited

Enclosure-2

39

Violation, consistent with Section VII.B.1 of the NRC Enforcement

Policy. NCV 50-269,270.287/97-12-06. Failure to Secure a Safeguard

Container That Stored Safeguards Information.

c. Conclusions

This incident of failure to secure safeguards information was a licensee

identified, non-repetitive, corrected, non-willful event. Consequently,

a Non-Cited Violation was issued.

SS

Security Safeguards Staff Training and Qualification

S5.1 Security Training and Oualification

a. Insoection Scope (81700)

The inspector interviewed security personnel and reviewed security

personnel training and qualification records to ensure that the criteria

in the Security Personnel Training and Qualification Plan (T&QP) were

b. Observations and Findings

The inspector interviewed ten security non-supervisor personnel, three

supervisors, and witnessed approximately 14 other security personnel in

the erformance of their duties. Members of the security force were

know edgeable in their responsibilities, plan commitments and

procedures. Sixteen randomly selected training records were reviewed by

the inspector concerning training, firearms. testing, job/task

performance and requalification.

The inspector found that armed response personnel had been instructed in

the use of deadly force as required by 10 CFR Part 73. Members of the

securityorganization were requalified at least every twelve months in

the performance of their assigned tasks, both normal and contingency.

This included the conduct of physical exercise requirements and the

completion of the firearms' course. Through the records review and

interviews with security force personnel, the inspector found that the

requirements of 10 CFR 73, Appendix B. Section 1.F. concerning

suitability, physical and mental qualification data, test results, and

other proficiency requirements were met.

c. Conclusions

The security force was being trained according to the T&QP and

regulatory requirements. There were no violations of regulatory

requirements identified in this area.

Enclosure 2

40

S8

Miscellaneous Security and Safeguards Issues

S8.1

Protected Area Access Control

a. Inspection SCODe (71750)

The inspector evaluated the licenseeIs program to control access of

terminated personnel according to criteria in Chapter .6 of the PSP and

appropriate directives and procedures.

b. Observation and Findings

This was to ensure that the licensee had positive access controls of

personnel entering and exiting the protected area.

During a review of

entries in the Safeguards Event Log. the inspector noted two events of

orotected area badges of favorably terminated personnel that had not

been deactivated in a timely manner.

These two events involved two

employees, with no instances of gaining access to the protected area

after they were terminated from employment and unauthorized to access

the protected area. The two events were caused by contractor/vendor

management failing to notify security within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after favorable

termination. Dates of the events were both on January 9, 1997.

The

corrective actions were prompt, comprehensive and effective to prevent

recurrence. The licensee's analysis and corrective actions of the two

events were documented in PIP 0-97-0136. The cause of the events was

human error, not programmatic. These events were violating Nuclear

Policy Manual-Volume 2. Nuclear System Directive 218. "Notification

Responsibilities for Termination." paragraph B.1, Rev. 0. dated June 27.

1996 that states in effect that for voluntary and involuntary

termination, that management shall.be responsible for verbally notifying

site security to delete the terminated individuals badge.

Because the events were licensee identified, effective in corrective

action, con-repetitive. non-willful, and not a programmatic issue, the

violation is being treated as a Non-Ci.ted Violation, consistent with

Section VII.B.1 of the NRC Enforcement Policy, NCV 50-269.270.287/97

12-07, Failure to Notify Security of Terminated Employees.

c. Conclusion

Two incidences of failure to notify security of the termination of

personnel were licensee identified, non-repetitive, corrected, non

willful events. Consequently, a Non-Cited Violation was issued.

Enclosure 2

41

F1

Control of Fire Protection Activities

F1.1 Fire Drill

a. InSDection Scooe (71750. 92904)

The inspectors observed a fire drill on August 15.

b. Observations and Findings

The area selected for the drill was the maintenance support building

located next to the turbine building. Among the items observed were:

  • 0

Fire Brigade (FB) personnel responded to the assembly area dressed

out in appropriate fire gear;

a

the FB leader exercised good command and control;

o

FB personnel were aware of the location of additional self

contained breathing apparatus oxygen bottles:

0

control room personnel provided overall direction during the drill

and entered tne applicable emergency classification:

0

the controllers gave clear and precise information to the FB

leader and personnel regarding the simulated fire, this included

colored photographs: and

a post-fire drill briefing was conducted.

One noteworthy licensee identified drill deficiency was identified.

A

person left in the area by the controllers was not found when the Fire

rigade leader directed that a search of the area be made.

A minor

deficiency was identified in the area of communications which involved

fire fighting team identification.

Both of these items were discussed

at the post-drill briefing.

c.

Conclusions

The inspectors concluded that the method employed for attacking the fire

was appropriate, the drill scenario was good. fire brigade personnel

exercised good fire fighting techniques. and the post-fire drill

briefing was effective.

Enclosure 2

42

V. Management Meetings

X1

Exit Meeting Summary

The inspectdrs presented the inspection results to members of licensee

management at the conclusion of the inspection on September 10. 1997.

The licensee acknowledged the findings presented.

X2

Escalated Enforcement Results

On July 23, 1997, a Predecisional Enforcement Conference for EA Case

Nos.97-297 and 97.298. covered in Inspection Reports. 97-07 and 97-08,

respectively, was

eld in the Regional Office with the Licensee in

attendance. The following apparent violations (EEls) were discussed:

EFI 50-269.270.287/97-07-01

EEI 50-269,270.287/97-07-02

EEI 50-287/97-08-01

EELI 50-287/97-08-02

FEI 50-269.270,287/97-08-03

EE1 50-269.270.287/97-08-04

EEI 50-287/97-08-05

Following the conference,, a Notice of Violation (NOV)

was issued on

August 27, 1997.

Based on the NOV issued, the above EEls are closed and

the violations identified in the above Notice of Violation will be

tracked as:

VIO EA 97-298 01012

Failure to Adhere to Technical

Specification Requirements for the Unit 3

High Pressure Injection System

VIO EA 97-297 02013

Failure to Establish Measures to Assure

Cracks in High Pressure Injection Safe End

Nozzles Are Promptly Identified and

Correc ted

VIO EA 97-297 02023

Failure to Take Corrective Action for

Temperature Differentials in the Safety

Related High Pressure Injection Makeup

Piping

VIO EA 97-298 03014

Failure to Follow Operations Procedures

During the Unit 3 Cooldown on May 3. 1997

VIO EA 97-298 04014

Failure to Follow Operations Procedures

Relating to Low Temperature Overpressure

Protection Recuirements

Enclosure 2

43

VIO EA 97-298 05014

Failure to Follow Maintenance Procedures

for the Installation of Tubing Caps

VIO EA 97-298 06014

Failure to Assure Design Configuration

Control was Maintained for Letdown Storage

Tank Level Instrumentation Valves

Partial List of Persons Contacted

Licensee

E. Burchfield, Regulatory Comoliance Manager

T. Coutu, Operations Support Ianager

D. Coyle, Systems Engineering Manager

T. Curtis, Operations Superintendent

J. Davis, Engineering Manager

B. Dobson, Systems Engineering Manager

W. Foster. Safety Assurance Manager

J. Ham pton. Vice President, Oconee Site

D. Hubbard. Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

B. Peele, Station Manager

J. Smith. Regulatory Compliance

NRC

D. LaBarge, Project Manager

Inspection Procedures Used

IP37550

Engineering

IP37551

Onsite Engineering

IP37828

Installation and Testing of Modifications

IP40500

Effectiveness of Licensee Controls In Identifying and Preventing

Probl ems

IP60705

Prepartion for Pefueling

IP61726

Surveillance Observations

IP62707

Maintenance Observations

IP71707

Plant Operations

IP71750

Plant Support Activities

IP81700

Physical Security Program For Power Reactors

IP81810

Protection of Safeguards Information

IP92700

OnsiteFollovup of Written Event Reports

IP92901

Followup - Plant Operations

IP92902

Followup - Maintenance

IP92903

Followup - Engineering

IP92904

Followup-Plant Support

1P93702

Prompt Onsite Response to Events

Enclosure 2

44

Items Opened, Closed, and Discussed

Ocened

50-269,287/97-12-01

NCV

MOV Design Deficiency Implementation

(Section 08.3)

50-269,270,287/97-12-02

URI

Fuel Load UFSAR Statements (Section E1.1)

50-269,270.287/97-12-03

URI

Relay As-Found Conditions (Section E3.1)

50-269,270,287/97-12-04

IFI

Maintenance Oversight (Section M3.2)

50-287/97-12-05

VIO

Failure to Remove Protective Clothing

(Section R4.1)

50-269,270.287/97-12-06

NCV

Failure to Secure a Safeguard Container

That Stored Safeguards Information

(Section S4.2)

50-269,270,287/97-12-07

NCV

Failure to Notify Security of Terminated

Employees (Section S8.1)

50-287/97-12-08

NCV

Failure to Follow Valve Packing Porcedure

(Section M8.1)

EA 97-298-01012

VIO

Failure to Adhere to Technical

Specification Requirements for the Unit 3

High Pressure Injection System (Section

X2)

EA 97-297-02023

VIO

Failure to Take Corrective Action for

Temnerature Differentials in Safety

Related High Pressure Injection Makeup

Piping (Section X2)

EA 97-297-02013

VIO

Failure to Establish Measures to Assure

Cracks In High Pressure Injection Safe End

Nozzles Are Promptly Identified and

Corrected (Section X2)

EA 97-298-03014

VIO

Failure to Follow Operations Procedures

During the Unit 3 Cooldown on May 3, 1997

(Section X2)

EA 97-298-04014

VIO

Failure to Follow Operations Procedures

Relating to Low Temperature Overpressure

Protection Requirements (Section X2)

Enclosure 2

45

.

EA 97-298-05014

VIG

Failure to Follow Maintenance Procedures

for the Installation of Tubing Caps

(Section X2)

EA 97-298-06014

VIO

Failure to Assure Design Configuration

Control was Maintained for Letdown Storage

Tank Level Instrumentation Valves (Section

X2)

Closed

50-287/97-08-01

EEl

Failure to Adhere to Technical

Spec ificat ion Operability Requirements for

the HPI System on Unit 3 (Section X2)

50-287/97-08-02

EEI

Failure to Follow Operations Procedures

During the Unit 3 Cooldown and/or Event

Response on May 3. 1997 (Section X2)

50-269,270,287/97-08-03

EEl

Failure to Take Adequate Corrective

Actions for Conditions Adverse to Quality.

(Section X2)

50-269,270,287/97-08-04

EEl

Failure to Provide Adequate Design Control

Measures for, the Letdown Storage Tank,

Level and Pressure Instrumentation

0

(Section X2)

50-287/97-08-05

EEI

Failure to Make a Report Within the Time

Required by 10 CFR 50.72 (b) (Section X2)

50-269.270,287/95-27-01

VID

Inadequate Procedures Two Examples

(Section 08.1)

50-269,270.287/96-20-01

URI

SSF Past Operability (Section 08.2)

50-269/95-08. Revision 0

LER

Containment Isolation Valve Inoperable Due

to Deficient Design Cond-tion (Section

08.3)

50-269/95-08, Revision 1

LER

Containment Isolation Valve Ino erable Due

to Deficient Design Condition (ection

08.3)

50-287/95-01

LER

Packing Leak Due to Inappropriate Action

Results in.Unit Shutdown (Section M8.1)

Enclosure 2

46

50-287/95-02

LER

Drop of Control Rod Group Due to Unknown

Caus -e Result-LS in Reactor Trip (Section

M8.2)

50-269,270,287/96-17-04

URI

Engineering Evaluation for the Replacement

of Carbon With Stainless Steel Piping

(Section M8.4)

50-269,.270,287/93-20-01

IFI

Instrument Impulse Lines and Associated

ISI Requirements (Section M8.6)

50-269/96-04-04

URI

Root Cause Assessment of Failures to

Valves 1MS-77 and iLPSW-254 (Section M8.7)

50-269,270,287/96-03-02

El

Inoperability of Containment Hydrogen

Control Systems (Section E8.3)

50-270/95-02

LER

incorrect Timer Setting Due to a Design

Deficiency Results in a Reactor Trip

(Section E8.4)

50-287/97-02-06

VID

inadequate Control of Purchased Material

and Equipment (Section E8.5)

50-269,270,287/97-02-08

VID

Inadequate Corrective Action and Design

Control for Reactor Building Cooling Unit

Fuses (Section E8.6)

50-269,270.287/95-14-01

iFI

Qualification Extension of Keowee

Batteries (Section E8.7)

50-269,270,287/95-09-03

DEV

Fatigue Analysis for RCS Auxiliary Piping

(Section E8.9)

50-269,270,287/97-07-01

EEl

Inadequate Implementation of Augmented

inspections (Section X2)

50-269.270,287/97-07-02

EEI

Inadequately Addressed Thermal

Strati fication (Section X2)

Discussed

50-269,270,287/96-05-01

V/1

Failure to Make Proper 10 CFR 50.72

Notification (Section 08.4)

50-269U270,287/96-10-03

VIO

Weld Procedure Qualifications Welded.

Tested, Certified and Approved b Same

Individl

(Section M8.3)

Enclosure 2

47

50-269.270,287/96-17-09

VIO

LPSW Modification Did Not Meet ASME Code

Section XI Non-Destructive Examination

Requirements (Section M8.5)

50-269,270,287/94-24-04

DEV

Design Basis Requirements for the

Penetration Room Ventilation System

(Section E8.1)

50-269,270,287/95-03-01

IFI

Clarification of TS 3.3.1 (Section E8.2)

50-269,270.287/96-03-04

IFI

Installation of New Ground Detection

System (Section E8.8)

List of Acronyms

AEOD

Office of Analysis and Evaluation of Operational Data

AIT

Augmented Inspection Team

ANSI

American National Standard

ASME

Americab Society of Mechanical Engineers

BWST

Borated Water Storage Tank

CFR

Code of Federal Regulations

CCW

Condenser Circulating Water

DC

Direct Current

ECCS

Emergency Core Cooling System

EE I

Apparent Violation

ESWA

Engineering Safe uards Work Area

ETQS

Training and Quaiication Guide

ES

Engineered Safeguards

F

Fahrenheit

GPM

Gallons Per Minute

HPI

High Pressure Injection

ICS

Integrated Control System

I&E

Instrument & Electrical

IE

IFIInspector

Report

IRInspection Repor

ISI

Inservice Inspection

KHP

Keowee Hydro (electric) Plant

KV

KiloVolt

LDST

Letdown Storage Tank

LER

Licensee Event Report

LCO

Limiting Condition for Operation

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

MM

Minor Modification

MOV

Motor Operated Valve

NCV

Non-Cited Violation

NDE

Non-Destructive Examination

NLO

Non-Licensed Operator

NRC

Nuclear Regulatory Commission

Enclosure 2

0NSM

Nuclear Stati on Mdfcto

NSD

Nuclear System Directive

ONS

Oconee Nuclear Station

PDR

Public Document Room

PDT

Partial Discharge Test

PIP

Problem Investigation Process

PMT

Post Maintenance/Modification Testino

'PORC

Plant Operating Review Committee

PRVS

Penetration Room Ventilation System

PSIG

Pounds Per Square Inch Gauge

PSP

Physical Security Plan

PT

Performance Test

QA

Quality Assurance

QIT

Quality improvement Team

RB

Reactor Building

RBCU

Reactor Building Cooling Unit

RCS

Reactor Coolant System

REV

Revision

SFP

Spent Fuel Pool

SG

Steam Generator

SGI

Safeguards Information

SSF

Safe Shutdown Facility

TM

Temporary Modification

T&QP

Training and Qyalification Program

TS

Technical Specification

TSC

Technical SuUSort Center

0

UFSAR

Updated FinalV Safety Analysis Report

URI

Unresolved Item

VI

Violation

MO

Work Order

Enclosure 2