ML15118A327

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Insp Repts 50-269/97-18,50-270/97-18 & 50-287/97-18 on 971228-980207.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML15118A327
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 03/05/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A253 List:
References
50-269-97-18, 50-270-97-18, 50-287-97-18, NUDOCS 9803180070
Download: ML15118A327 (38)


See also: IR 05000269/1997018

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

-.Docket Nos:

50-269, 50-270, 50-287, 72-04

Report No:

50-269/97-18, 50-270/97-18, 50-287/97-18

Licensee:

Duke Energy Corporation

Facility:

Oconee Nuclear Station, Units 1, 2, and 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

December 28, 1997 -.February 7. 1998

O

Inspectors:

M.

Scott, Senior Resident Inspector

S.-Freeman, Resident Inspector

E. Christnot, Resident Inspector

D. Billings, Resident Inspector

Paul Kellogg, Regional Inspector (Section E8.2)

Jerry Blake, Regional Inspector (Section M1.4)

Nick Economos, Regional Inspector (Section E1.1)

Approved by: C. Ogle, Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9803180070 980305

PDR ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2, and 3

NRC Inspection Report 50-269/97-18.

50-270/97-18, 50-287/97-18

'This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant.support. -The-report covers a six-week

period of.resident inspection, and the results of announced inspections by

three regional based inspectors.

Operations

Operations personnel satisfactorily shut down Unit 1 following a steam

generator tube leak. The licensee identified a related procedure

problem that resulted in a Non-Cited Violation.

Operations

satisfactorily performed the shutdown and overall once through steam

generator configuration control work. The licensee drained the reactor

coolant system in a controlled fashion to reduced inventory levels five

times during the work. This problem is also discussed in Section M1.4.

(Section 01.3)

Operations personnel displayed a good questioning attitude that allowed

them to detect an unexpected power increase during letdown flow

instrument calibrations. This problem is also discussed in Section

M3.1. (Section 01.4)

The licensee exited a 24-hour limiting condition for operation on the

Unit 3 reactor building emergency hatch without fully understanding that

a Technical Specification interpretation did not relieve them of the

surveillance requirements for further testing. This issue was left

unresolved pending review of past.practices. (Section 01.5)

The licensee carefully tested and satisfactorily replaced a Unit 1

control rod, which had latching problems. Operations and engineering

provided good overall controls during the rod freedom of motion test.

(Section 01.6)

Operations satisfactorily manipulated Unit 1 to cold shutdown for

repairs and investigation of a 2 gallon per minute leak from a crack on

a one-inch drain line off the pressurizer surge line. Operations made

appropriate notifications and reports. (Section 01.7)

An apparent lack of agreement between the Safe Shutdown Facility diesel

technical manual and operations procedures will be tracked through an

unresolved item. (Section 03.1)

2

The licensee and its primary vendor removed and disassembled a

malfunctioning Unit 1 control rod mechanism, finding no definitive

problem. The overall inspection work was performed in a satisfactory

manner, with care to detect as-found conditions. (Section M1.2)

During the pressurizer surge line drain line work, pipe removal and

reinstallation practices and controls were generally acceptable. Health

physics personnel appropriately supported the maintenance activities.

ne rework item was observed that is discussed as a violation in

Inspection Report 50-269,270,287/98-01. (Section M1.3)

The December 28, 1997, Unit 1 shutdown for primary-to-secondary leakage

that was the result of past repairs where there had been an apparent

over-reliance on the results of visual inspections, and less than

adequate appreciation for primary water stress corrosion cracking.

(Section M1.4)

A violation was identified for failure to revise a high pressure

injection system letdown flow instrument calibration procedure following

modification of the Unit 3 integrated control system. (Section M3.1)

During inspection and testing of Safe Shutdown Facility 600 volt

breakers, several problems were identified by the licensee. The

licensee satisfactorily addressed the immediate equipment.problems.

Several issues regarding grease hardening and trip device past

operability were identified. (Section M3.2)

On January 30, 1998, the licensee was granted verbal enforcement

discretion on statements in their TS regarding TS surveillance

performance intervals. The licensee submitted a TS change to allow

eighteen-month periodicity of surveillance instead of a refueling outage

periodicity. The inspectors had reviewed the change for completeness.

Additional followup on the enforcement discretion will be tracked under

an unresolved item. (Section X2)

Engineering

Replacement of the cracked one-inch drain line on the pressurizer surge

line was consistent with applicable code requirements. A lack of

attention to detail in the planning phase of welding the replacement

line caused a significant job delay and the need to cut and re-weld a

new weld on the line. Engineering provided adequate support and took an

active role in determining the root cause of the crack. Welding,

nondestructive examination, and process control activities were

satisfactory. Stress analysis calculations determined that thermal

stratification and hanger loads on the drain line exceeded code

allowable usage factor requirements on the drain line nozzle.

(Section E1.1)

Three examples of a violation resulting from procedural inadequacies

were identified. An engineering supported troubleshooting procedure did

not minimize risk to equipment and was not completely validated prior to

performing work. Use of the procedure on Unit 2 integrated control

3

system wiring resulted in unexpected system responses. The other two

examples are discussed in Section E2.2. (Section E2.1)

Two additional examples of the violation resulting from procedural

inadequacies were identified on the Keowee Hydroelectric units. One

example involved the.motor operated automatic voltage adjusters on both

Keowee units not being adjusted in accordance with their applicable

drawings due to lack of procedural detail.

The other example involved

missed in-service tests on both Keowee Hydroelectric units due to

engineering not converting a temporary test into a periodic test of lube

oil valves. (Section E2.2)

A Non-Cited Violation was identified for failure to follow procedures

controlling modifications as discussed in Licensee Event Report 50

269/97-10, regarding reactor building sump issues. (Section E8.1)

The licensee was making good progress in the installation of the service

water modifications. Modifications on Unit 2 should be completed during

the March 1998 outage. (Section E8.2)

Plant Support

A Non-Cited Violation was identified for failure to perform a continuous

fire watch as required by the selected license commitments. The

licensee had performed hourly fire watches instead of continuous fire

watches when they removed the Unit 2 and 3 startup transformers fire

protection deluge system from service. (Section F1.1)

Report Details

Summary of Plant Status

Unit 1 began the report period at approximately 54 percent power, performing

integrated control system testing. On December 28, 1997, the unit began

equired shutdown activities following the identification of a primary-to

secondary leak. During the heat up following completion of inspection and

repairs to both steam generators, a leak was identified on the pressurizer

surge line drain. At the end of the report period, the unit was in cold

shutdown.

Unit 2 began and ended the report period at 100 percent power.

Unit 3 began and ended the report period at 100 percent power.

Review of Updated Final Safety Analysis Report (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the observed

plant practices, procedures, and parameters.

I. Operations

01

Conduct of Operations

01.1 'General Comments (71707)

Using Inspection Procedure 71707., the inspectors conducted frequent

-reviews of ongoing plant operations. In

general, the conduct of

operations was professional and safety-conscious; specific events and

noteworthy observations are detailed in the sections below.

01.2 Operations Clearances (71707)

The inspectors reviewed the following clearances during the inspection

period:

.97-4445

Unit 3 Seal Supply Filter Swap

98-0207

Unit 1 Component Cooling Water Cooler

The inspectors observed that the clearances were properly prepared and

authorized and that the tagged components were in the required positions

with the appropriate tags in place.

01.3 Unit 1 Once Through Steam Generators (OTSG) 1A Tube End Weld Leaks

a. Inspection Scope (71707, 93702)

On December 28, 1997. the licensee detected radioisotopes in the

secondary system of Unit 1. The unit was at 54 percent power conducting

a power escalation following the refueling outage. The licensee

2

initiated a controlled shutdown and Problem Investigation Process (PIP)

report 1-97-4641 (with a failure investigation process team). The

inspectors observed the controlled shutdown of the unit, the once

through steam generator (OTSG) work, and subsequent return of the unit

to service. The inspectors also reviewed Licensee Event Report 97-11

written to document the event. A regional inspector was detailed to the

site in order to follow the repairs. Section M1.4 addresses

nondestructive inspections and engineering details of the problem and

related repairs.

b. Observations and Findings

Sequence of Events

On December 27, 1997, the licensee completed an integrated control

system (ICS) load rejection test from approximately 25 percent power.

About one hour after the end of the ICS test segment, radiation process

monitor RIA-40 for the condenser steam air ejectors went into alarm.

Following the guidance of PT/O/A/0230/01, Radiation Monitor Check,

Revision 109C, operations reset the RIA-40 alert alarm setpoint at twice

background level. However, the operations crew involved overlooked a

note on the next page of the procedure which indicated that if RIA-40

alarmed, samples should be taken to verify the leak rate. At shift

turnover the next morning, the shift discussed the reset of RIA-40. The

oncoming operators indicated that a sample was needed, and one was

subsequently taken~at 8:08 a.m., on December 28.1997. Confirmatory

samples in the afternoon of that same day confirmed a tube leak. The

licensee then entered the emergency operating procedure for an OTSG tube

leak. At 3:07 p.m. a unit shutdown was initiated. At 3:32 p.m. the

licensee completed a 10 CFR 50.72 notification to the NRC duty officer.

The unit was off line at 4:46 p.m.

Tube Leak Detection

The first indication of the primary-to-secondary leak was on the

condenser steam air ejector radiation monitor. At the time of the RIA

40 alarm and reset on December 27, 1997, historical trend data indicated

small but progressive increases in radiation levels. Additionally, the

RIA-16 (1A main steam line) monitor did trend up slightly, but did not

reach the alarm setpoint (2.5 millirem (mr) per hour setpoint with a

maximum attained value of slightly higher than 0.06 mr per hour).

The inspectors were informed that radiation instruments such as the

condenser steam air ejector monitor, will show increases in background

and may show small spikes due to power changes and material releases

from deposits in the secondary breaking loose. The inspectors were also

informed that historically during startups, RIA-40 required a reset of

its setpoint to compensate for normal background increases.

Due to the low radiation levels, the leak was not readily detectable.

Although secondary off-gas process monitoring is generally the first

indication of an OTSG tube leak, the small size of the 1A OTSG leak and

the minimal isotopic migration to the secondary made this leak

3

particularly difficult to detect.. The leakage was relatively free of

isotopes due to the recently refueled core, overall cleanliness of the

primary, and limited size of the leak.

Likewise, the chemistry department could not positively identify a leak

with the 8:00 a.m. samples, but similarly could not disprove its

presence. The xenon isotope was in low concentration in the primary.

he licensee used the minimum detectable limit, an artificial number,

for the isotopic concentration in the leakage rate calculation. This

calculation produced an initial leak rate of 260 gallons per day (gpd)

following the first sample.

RIA-16 for the 1A steam line indicated an increasing trend. The RIA-17

monitor for the lB steam line was flat-lined. Given this and the

inability to disprove a leak, the licensee drew a second series of

samples and analyzed them in the early afternoon (there was a 90 minute

sample preparation time). As the power was increased by the time of the

second sample, the xenon isotope in the primary was elevated and

slightly above the minimum detectable level.

The licensee introduced

this value into the leak rate calculation which resulted in a higher

leak rate of 404 gpd. With the low isotopic levels in the primary and

the change in power, the licensee believed that there was no true

increase in the leakage rate between the 8:00 and 11:00 a.m. samples.

At that point, with no radiation process monitors in an alarm state, the

licensee decided to shut down the unit. The secondary and turbine

building sumps received very small increases in radiation levels.

The inspectors determined that had rimary and secondary chemistry

samples been drawn at the time of te initial RIA-40 alarm, it was

inconclusive that the licensee would have detected the leak since there

was very little radiation specie concentration in the secondary.

Adequacy of Radiation Monitor Procedure

The inspectors reviewed the RIA-40 instructions contained in Procedure

PT/0/A/0230/01 and observed that they were not adequate from two

perspectives. First, the requirement for sampling was contained in the

"notes" of the procedure outside the procedural text. Second, the

direction to take samples contained a "should" statement.

The subject procedure was not adequate in that policy intent or prudent

requirements were not positively and clearly stated as required in

Nuclear Site Directive 703, Administrative Instructions for Site

Procedures, revision date December 30, 1997, Section 703.5, Preparation

of Procedures. Subsection 4 of the directive indicated, in part, "That

all instructions should be clear and precise. Ambiguous and vague

wording or implied action should be eliminated from the procedure."

Additionally, Regulatory Guide 1.33,.Revision 2, which is invoked under

the licensee's topical report, states that "shall" statements are to be

used instead of "should" statements where the procedural step is of

sufficient importance. Operations management stated.policy was to take

the samples with an alarm of RIA-40.

0II

4

An operations management review of the tube leak events on or before

January 8, 1998 (prior to LER issuance), initiated correction actions to

be available for the next startup and normal plant operation.

Operations, in conjunction with Chemistry, performed the following

corrective actions: (1).discussed the sampling expectations with the

operations crew of December 27, 1997: (2)

provided the sampling

expectations to the other operational shifts; (3)

incorporated what had

been notes in the previous revision of PT/0/A/0230/01 as requirements

and added enhancements in the reset of RIA-40: (4)

changed annunciator

response Procedure 1SA-8/D-10, Radiation Monitoring, to clearly state

samples were to be taken by chemistry when RIA-40 went into alarm

(instead of referring to another complex document): (5)

rewrote

Procedure OP/0/A/1106/31, Control of Secondary Contamination, to enhance

rocedure usefulness and integration with the above PT. Inadequate

rocedure PT/O/A/0230/01 was identified as a violation. This non

repetitive, licensee identified and corrected violation is identified as

a Non-Cited Violation (NCV) consistent with Section VII.B.1 of the NRC

Enforcement Policy, NCV 50-269/97-18-01: Inadequate RIA Procedure.

Performance of Operating Crews

The rapid shutdown of the unit following confirmation of the tube

leakage on December 28, 1998, was well controlled by operations

personnel.

Between January 1 and January 15. 1998, the unit was drained five.. times

to reduced inventory levels. This was done to permit nozzle dam.

installation or removal in

the Unit 1 OTSGs. An inspector was present

for each of these draindowns, observing good control of the evolutions.

With the number of draindowns performed, the licensee had reduced the

activity to near routine, but retained the correct operational

perspective. Control room operators provided oversight for tube sheet

pressure tests that were similarly properly controlled.

c. Conclusions

Operations personnel satisfactorily shut down Unit 1 following a steam

generator tube leak. The licensee identified a related procedure

problem that resulted in a Non-Cited Violation. Operations

-satisfactorily performed the shutdown and overall once through steam

generator configuration control work. The licensee drained the reactor

coolant system in a controlled fashion to reduced inventory levels five

times during the work.

01.4 Unit 3 Power Change Due to Letdown Flow Calibration

a. Inspection Scope (71707)

The inspectors reviewed the operational aspects of an unexpected power

increase on Unit 3. The maintenance controlled procedural aspects are

discussed in Section M3.1.

5

b. Observations and Findings

.

On January 15, 1998, while Unit 3 was at 100 percent power and

instrumentation technicians were calibrating letdown flow

instrumentation, operations personnel observed a slight decrease in the

core thermal power best one hour average and a slight increase in

megawatt output.

Operations personnel notified reactor engineering, who identified that

the letdown flow signal was an input to the thermal power calculation

and that the thermal power calculation provided feedback to ICS.

Following consultation with reactor engineering and completion of the

evaluation, operations stopped the letdown flow calibration and reduced

core thermal power demand by 0.2 percent.

When the letdown flow signal was set to zero during the calibration,

core thermal power feedback to ICS decreased by 0.15 percent. In

response. ICS adjusted feedwater flow enough to bring core thermal power

back to 100 percent. However, since only the letdown signal was zero

and not actual letdown flow, core thermal power never decreased and the

adjustment by ICS caused actual core thermal power to exceed 100

percent. Licensee calculations determined that shift average power

increased from 99.95 to 99.98 percent of rated power over an hour and a

-

half period and that'core thermal power reached a maximum of 100.10

percent of rated power. After reviewing TS and the reactor engineering

power calculations, the inspectors-determined that no power limits were

exceeded.

c. Conclusions

Operations personnel displayed a good questioning attitude that allowed

them to detect an unexpected power increase during letdown flow

instrument calibrations.

01.5 Unit 3 Reactor Building (RB) Emergency Hatch

a. Inspection Scope (71707)

The inspectors reviewed the circumstances surrounding testing and

operability-of the Unit 3 RB Emergency Hatch.

b. Observations and Findinqs

On January 19, 1998, the licensee was performing Procedure

PT/0/A/0150/08B. RB Emergency Hatch Leak Rate Test, Revision 25, and

entered the hatch to remove strongbacks from-the inner door as required

by procedure. U

pon exiting the hatch, the licensee found that the outer

door would not close properly. The licensee declared the outer door

inoperable and entered a 24-hour Limiting Condition for Operation in

accordance with TS 3.6.3.a.

The licensee investigated the outer door and found that a small air

pocket had been trapped behind the outer 0-ring. Maintenance personnel

6

removed the air and closed the outer door properly. The licensee

determined that no maintenance had been done; therefore, no further

testing was required. Based on this, the licensee declared the outer

door operable and exited TS 3.6.3.a.

Further investigation by the operations staff continued into January 20,

1998. On the next shift, the licensee determined that the hatch was

inoperable due. to an inoperable door gasket, and that a leak test of the

outer door double seal was required. The licensee again declared the

outer door inoperable and entered a seven-day LCO in accordance with TS 3.6.3.a.2. The licensee subsequently made the starting time for the LCO

retroactive to the previous day when the hatch was originally declared

inoperable. The licensee completed a test of the outer door 0-rings

using Procedure PT/0/A/0150/09A, RB Emergency Hatch Outer Door 0-Ring

Leak Rate Test. Revision 13. The outer door was subsequently declared

operable and TS 3.6.3.a. was exited. The licensee documented the

occurrence in PIP report 3-98-272.

The inspectors reviewed TS 3.6.3 and TS 4.4.1.5.2, reviewed control room

and shift work manager logs, and interviewed personnel involved both in

the maintenance of the door and in the initial decision to exit TS 3.6.3.a without performing any further testing. The inspectors

determined that whether or not maintenance was performed did not affect

the need for further testing. TS 4.4.1.5.2 stated that either a full

hatch test or a leak test of the outer door double seal was required

within three days of initial opening. The licensee had interpreted this

TS to allow opening the outer door without further testing if the door

was opened to remove strongbacks following a full hatch test. However.

the inspectors determined the TS interpretation did not relieve the

licensee of the-surveillance requirement and therefore further testing

was required.

The licensee did not violate any TS in this case because the door was

reseated and tested within twenty-four hours. However, the existence of

a TS interpretation indicated the outer door may have been opened in the

past without proper surveillance testing. The circumstances surrounding

this issue will be tracked as URI 50-287/97-18-02: Containment Air Lock

Testing, pending review of past surveillance practices concerning

containment air lock testing.

c. Conclusions

The licensee exited a 24-hour limiting condition for operation on the

Unit 3 reactor building emergency hatch without fully understanding that

a Technical Specification interpretation did not relieve them of the

surveillance requirements for further testing. This issue was left

unresolved pending review of past practices.

7

01.6 Unit 1 Control Rod 7 of Group 5 Failure to Latch

a. Inspection Scope (71707. 93702, 37551, 92703)

.,On January 19, 1998. while performing a test, control rod 7 in group 5

would not withdraw in group control.

The inspectors were immediately

  • notified of the problem and.-followed the licensee's activities. This

rod had a similar problem with operation on December 22, 1997,

(Inspection Report 50-269,270.287/97-16, Section 01.5).

b. Observations and Findings

On January 19, 1998. at approximately midnight, while performing

Procedure PT/0/A/305/01, Reactor Manual Trip Test, Revision 8, control

rod 7 of group 5 would not respond to an out command. During the drop

test done the previous day, the rod had operated normally. The licensee

attempted to move the control rod by repeating activities done in

December 1997, when the rod had exhibited out motion problems.

The

licensee's efforts, which included replacement of the control rod power

cable, failed to restore function. Several days.later, the plant was

drained to a point above reduced inventory conditions (approximately 100

inches in the pressurizer) for re lacement of the control rod drive

(CRD). The inspectors observed the satisfactory drain, manual rod

motion and freedom testing, removal of the CRD. and inspection of the

CRD by the vendor (see Section M1.2). Operations and engineering

provided good overall controls during the rod freedom of motion test.

nable to identify a cause for the rod motion problem, the licensee sent

the mechanism to a .vendor for further testing.

Retest of the new mechanism was satisfactory. The inspectors reviewed

the test times, which were within the expected and TS values. The

licensee subsequently continued preparations for unit startup.

c. Conclusions

The licensee carefully tested and satisfactorily replaced a Unit 1

control rod, which had latching problems. Operations and engineering

provided good overall controls during the rod freedom of motion test.

01.7 Oconee Unit 1 Cold Shutdown for Primary Leak

a. Inspection Scope .(71707,93702,62707)

Following the completion of repairs to the CRD, the licensee discovered

a small leak on the pressurizer surge line drain line. The licensee

immediately notified the residents and NRC headquarters of the problem.

The inspectors followed the recovery activities and repair efforts.

b. Observations and findings

Operations personnel had been warming Unit 1 to hot shutdown conditions.

The plant was at 2100 psig and 500 degrees at midnight on January 26.

1998. Operations had observed an increase in the rate of normal sump

8

pumping. Reactor building leakage was estimated to be approximately 2.0

9pm. At midnight, a non-licensed operator (NLO) was sent into the RB to

investigate the increased leakage. The operator found a weld area crack

on a 90-degree elbow on the one-inch diameter pressurizer surge line

drain that was spraying water vapor. The operator reported this

information to the control room at 12:47 a.m. At 1:00 a.m., the

licensee began a cooldown of the plant. For the observed conditions,

the licensee entered the excessive leakage abnormal procedure and TS 3.1.6.3. At 1:10 a.m., operations notified the senior resident, who

came to the site to review licensee actions. At 1:38 a.m., the licensee

initiated a one-hour non-emergency phone call to the NRC's headquarters

operations officer. The unit completed .a

normal cooldown over the

remainder of the night with all observed parameters remaining within

acceptable limits. The licensee initiated an investigation and an

engineering manager was on site interviewing personnel by 3:00 a.m. At

5:00 a.m., the plant was at 550 psig and 337 degrees F with the licensee

preparing to go on low temperature over pressure protection. The RB

leakage trended down with RCS pressure. Based on personnel safety

risks, the licensee made no further RB entries.

The plant was drained to above reduced inventory level to repair and

investigate the weld problem over the next several days. The crack in

the drain line was about 1/4 of the way around an elbow. This activity

was well planned and supported by the investigative team direction. See

Sections M1.3 and E1.1 for drain piping inspection details and repairs.

c. Conclusions

Operations satisfactorily manipulated Unit 1 to cold shutdown for

repairs and investigation of a 2 gpm leak from a crack on a one-inch

drain line off the pressurizer surge line. Operations made appropriate

notifications and reports.

03

Operations Procedures and Documentation

03.1 Standby Shutdown Facility (SSF) Diesel Generator Operation

a. Inspection Scope (71707, 62707)

The inspectors observed the operation of the SSF diesel generator on

February 6, 1998, during post-maintenance operation to return the SSF

diesel generator back to service following scheduled maintenance.

b. Observations and Findins

During low idle maintenance operation, the licensee identified that

turbo lube oil pressure was low on the A engine. Operations reviewed

Procedure OP/O/A/600/10, Enclosure 4.5 SSF Diesel Generator Auto Idle

Start, Revision 22. and contacted maintenance and engineering personnel

nearby. While troubleshooting the low turbo oil pressure, maintenance

identified that the installed engine revolutions per minute (rpm)

tachometer was reading approximately 30 rpm low on hand-held calibrated

0II

9

tachometers. The engine speed was less than the value stipulated in

applicable operations procedure.

The system engineer identified that the operations procedure specified a

different engine rpm value than the diesel technical manual. The

technical manual stipulated an idle speed of 490 RPM. The operations

procedure stipulated an idle speed of 400 - 450 RPM.. Operations and

system engineering continued to review the differences in the two

procedures.

At the close of the inspection period, NRC review of the technical

manual versus the operations procedure issue was not complete.

Followup of this issue will be under Unresolved Item (URI) 50

269,270,287/97-18-03: SSF Diesel Generator Operation. This issue is

unresolved pending additional NRC review of the maintenance and

operations activities associated with the operation of the SSF diesel

for return to service following maintenance.

c. Conclusions

An apparent lack of agreement between the SSF diesel technical manual

and operations procedures resulted in an URI.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707, 61726)

The inspectors observed all or portions of the following maintenance

activities:

WO 97053234

Change Out of Reactor Coolant Pump Seal

Injection Filters

OP/3/A/1104/02

Enclosure 3.8. Swapping Seal Supply Filters,

Revision 85C

PT/0/A/0620/09

Keowee Hydro Operation-Control Room Start,

Revision 16

OP/1/A/1102/01

Controlling Procedure for Unit Start Up,

Revision 2 8, Enclosure 4.18, Reactor Building

Tour at Hot Shutdown

PT/1/A/0711/01

Zero Power Physics Testing, Revision 30,

Enclosure 13.7, Approach to Criticality (Group

5, Rod 7 problem on January 22, 5:48 a.m.)

MP/1&2/A/1140/

CRDM Shim Driver Removal and Replacement,

16

Revision 3

10

5001137-00

Babcock and Wilcox Procedure, dated January 20,

1998, Type A Shim CRDM Refurbishment

WO 97094576-1

Inspect Unit 1 Component Cooling Cooler Tubes

WO 98009938

Inspect 2A Low Pressure Injection (LPI) Pump

Boric Acid-Covered Casing Bolts

IP/O/A/0305/01B Reactor Protection Systems (RPS) Channel B Pump

Power Monitor Instrument Calibration, Revision

31

IP/O/A/0305/015 RPS Removal From and Return to Service for

Channel ABC.D, Revision 16

PT/O/A/0610/22

Degraded Grid Switch Isolation and Keowee

Overfrequency Functional Test. Revision 9

OP/0/A/1600/10

Enclosure 4.5, SSF Diesel Generator Auto Idle

Start, Revision 22

P/0/A/1810/014

Valves and Piping-Welded-Removal and

Replacement - Class A through F. Revision 26

WO 97056137

Troubleshoot and Repair Unit 2 Integrated

Control System

.

PT/0/A/0610/22

Degraded Grid. Switchyard Isolation, and Keowee .

Overfrequency Protection, Revision 8

TT/0/A/2200/16

Keowee Hydro Unit 2 Turbine Guide Bearing Oil

System Test, Revision 1

TT/0/A/0620/34

Keowee Emergency Blackout Start Test, Revision 0

PT/3/A/0600/12

Turbine Driven Emergency Feedwater Pump,

Revision 48

b. Observations and Findings

All work observed was performed with the work package present and in

use. Technicians were experienced and knowledgeable of their assigned

tasks. The inspectors frequently observed supervisors and system

engineers monitoring job progress. Quality control personnel were

present when required by procedure. When applicable, appropriate

radiation control measures were in place.

The inspectors were in the switchyard during the degraded grid test

(PT/0/A/0610/22) observing proper operational configuration controls of

the yard breakers and proper breaker operation. Operations personnel in

the switchyard maintained good communications with the control room

personnel and used good command and control techniques when talking with

the test director.

11

During observations of the boric-acid inspection (WO 98009938) in the 2A

Low Pressure injection (LPI) pump room (63), the inspectors observed

that Teflon tape was being used in several locations on the Unit 2 low

pressure injection (LPI) system. Notably, the tape was used on pump

casi.ng plugs and system instrumentation connection points.

Inspectors

had also observed its use on the Unit 3 LPI system. Following inspector

questions on this observation, the licensee commenced a detailed

inspection observing the use of the Teflon tape in numerous locations on

the systems and documented it in PIP report 2-98-455. The report

indicated that piping specifications did not allow the use of the tape,

but did not render the system inoperable. The tape was to be evaluated

on a case by case basis with followup corrective actions. This finding

was identified as URI 50-269,270,287/97-18-04: Teflon Tape Use on the

LPI System.

c. Conclusions

The inspectors concluded that the maintenance activities listed above

were generally completed thoroughly and professionally. One URI was

initiated for the use of Teflon tape on the LPI system.

M1.2 Control Rod Drive Testing and Inspection

a. Inspection Scope (62707)

As indicated in Section 01.6, Group 5 Rod 7 had failed to latch on

January 19, 1998. The inspectors observed manual testing of the rod in

the core and subsequent disassembly of the removed control rod drive

mechanism.

b. Observations and Findings

The licensee developed a special test procedure to manually test the

freedom of motion of the subject rod. Before test performance, an

evaluation of the procedure was satisfactorily completed and the on-site

review committee reviewed the details of the entire evolution. For test

conditions, the reactor was in cold condition and depressurized with an

adequate shutdown margin available. The licensee performed the freedom

of motion test through the intact CRD housing with conditions very

similar to a normal rod unlatch conditions. The inspectors verified

that the conditions were appropriate for the work. With the inspectors

present on January 22, 1998, the licensee used a chainfall to lift the

rod from the core approximately 12 inches and then return it to its rest

condition. The movement met the acceptance criteria with no rod motion

or reactivity problems identified. The licensee readied and removed the

CRD for examination.

On January 25, 1998, the inspectors observed the disassembly of the

removed mechanism. Vendor representatives were in air fed hoods,

communication headsets, and full body plastic suits for the work. The

inspectors could view the work through windows in the special sealed

plastic tent constructed for the work.

12

The disassembly and inspection process did not identify a definitive

cause for the failure to latch. Corrosion product buildup was found

inside the mechanism, but the vendor described this as normal when

compared with other disassembled mechanisms. A thrust bearing locking

nut was three turns loosened. The locking cup for the nut had not been

sufficiently deformed to lock the nut completely. The licensee

indicated that this by itself was not the problem. The roller bearings

that drive the rod could still be pulled into the lead screw. The rotor

assembly parts that electrically pulled out to allow engagement of the

rollers showed grooves on their outside diameter. Grooves were in the

corrosion product coating. The vendor indicated that this indicated that

the parts were probably reaching their maximum outward movement.

The licensee and vendor removed the subject mechanism to the vendor's

contaminated test facility for further dynamic testing. The overall

inspection work was performed in a satisfactory manner and with care to

detect as-found conditions.

c. Conclusions

The licensee and its primary vendor removed and disassembled a

malfunctioning Unit 1 control rod mechanism, finding no definitive

problem. The overall inspection work was performed in a satisfactory

manner, with care to detect as-found conditions.

M1.3

Pressurizer.Drain-Line Removal and Installation

  • a. Inspection Scope (71707. 62707, 37551)

As-indicated in Section 01.7, the drain line from the pressurizer surge

line developed a leak on January 26. 1998. After plant depressurization

and drain to approximately 60 inches on LT-5. the line was removed and

replaced. The inspectors observed the line removal, replacement, and

re-welding.

b. Observations and Findings

After meeting appropriate plant conditions for the work, operations

released WO 98009597-05, to remove the one-inch diameter line. The line

consisted of the pressurizer surge line to drain line nozzle joint, a

short vertical run, four elbows and three short pieces of pipe arranged

in "C"

configuration, and then a straight, vertical twenty-foot run of

pipe to the equipment drain header near the basement level.

The piping

was per plan with five "U" bolt hangers on the twenty-foot run.

The

inspectors verified the plant was in stable condition for work

performance and appropriate clearances had been set.

At the first pipe

cut at the surge line drain line nozzle, no water was observed (only

dripping). The pipe end moved 1.75 inches down and 1.25 inches toward

the reactor vessel when cut. The motion was in a plane created by the

four elbows in the expansion segment of the drain line. This freed

motion indicated that the piping was under some residual stress that had

placed a preload on the piping. Analysis of the piping arrangement is

discussed in Section El.1. The supporting health physics and

13

maintenance personnel worked well together, taking adequate precautions

to make the work progress smoothly, maintaining adequate radiological

controls, and practicing good foreign material control.

The inspectors observed portions of the prefabrication of the

replacement piping in the machine shop and the class one welds made in

the RB. The work went well with good foreign material practices being

observed. Upon radiographic inspection of the prefabrication work, two

of seven butt weld joints were found to have inadequate fusion; and

therefore requiring rework. This use of prefabrication was an

acceptable methodology and practice.

The RB work was well controlled

with proper use of purge gases. Weld interpass temperatures were

appropriately monitored. The licensee stated that the radiographs were

acceptable on all completed and Duke Quality Assurance accepted welds.

While welding one of the joints, purge paper was used to plug the surge

line connection and keep condensate from the weld area. An excessive

amount of this dissolvable paper was used and it did not dissolve after

the welds were completed requiring further repairs. This is-further

discussed in Inspection Report 50-269,270,287/98-01.

c. Conclusions

During the pressurizer surge line drain line work, pipe removal and

reinstallation practices and controls were generally acceptable. Health

physics personnel appropriately supported the maintenance activities.

One rework item was observed that is discussed as a violation in

Inspection Report 50-269.270.287/98-01.

M1.4 Unit 1A Once Through Steam Generator (OTSG) Primary-to-Secondary Leakage

a. Inspection Scope (50002)

The inspectors reviewed the circumstances of, and the corrective action

for, the primary-to-secondary OTSG leakage that led to the December 28,

1997, shutdown of Unit 1.

b. Observations and Findings

On December 28, 1997, during start-up from a refueling outage, Oconee

Unit 1 was required to shut down due to primary-to-secondary leakage.

Plant chemistry personnel measured the leakage to be greater than 400

gpd from the 1A OTSG. When the 1A OTSG was opened for inspection, leak

testing showed that the primary source of leakage was at the interface

between the upper (hot leg) tubesheet and the OTSG tubes. Minor leakage

was also found at a remote welded plug location on the lower (cold leg)

tubesheet.

The configuration of the connections between the OTSG tubes and the

upper tubesheet is unique in the Oconee 1A OTSG. This uniqueness is the

result of field repairs to the upper tubesheet after foreign material

during hot functional testing damaged it in 1972. In the standard

connection between OTSG tubes and the upper tubesheet of a Babcock and

14

Wilcox (B&W) OTSG, the tubes protruded approximately 3/s to 112 inches

beyond the top of the tubesheet: the tubes were partially rolled in

the

tubesheet to provide the mechanical connection; and fillet welds

connected the outside of the tubes with the tubesheet to provide the

seals. The untubed lane of tubesheet holes was plugged with button

plugs that were fillet welded into place. In the Oconee 1A OTSG, the

tubesheet and tube connections were repaired by machining the damaged

tube ends flush with the top of the tubesheet; re-rolling the top of the

tube in the tubesheet: and seal welding over the seam between the tube

and the tubesheet to repair the hot functional damage. Encapsulating

the plugs with a weld overlay repaired the row of button plugs in the

untubed lane.

After the December 28, 1997, shutdown, initial test results in the 1A

OTSG indicated that there were eleven leak locations and three different

types of leaks. After the first repair attempts, subsequent test

results identified eight leaking locations; seven of these locations had

not been previously identified, and one of these provided a fourth type

of leak.

Leakage from Button Plug Locations Adjacent to Tube Location 77-7

A section of the weld overlay encapsulating the button plug row,

adjacent to tube location 77-7, had been machined away: this machined

area appeared to be the major source of leakage. Tube location 77-7 had

been plugged during the Spring 1994 refueling outage, and itwas during

this evolution that the section of weld overlay was machined away. B&W

nonconformance reports 94-00271 and 94-00271-01 reported a sequence of

-events in which attempts to install a remote welded plug at location 77

7 were unsuccessful, due to interference from the adjacent weld overlay.

At the time that a portion of the weld overlay was removed, the new

configuration was left as-modified, with the understanding that the

machining should not have encroached on the original button plug weld.

The leaking area of the weld overlay was manually repair welded and

successfully leak-tested. A full examination of the weld overlay area

showed that the area adjacent to location 77-7 was the only location

where metal had been removed to install an adjacent plug.

Remote Welded Plug (RWP) leaks

The RWP at location 87-61 in the lower tubesheet of OTSG 1A and the RWP

at location 97-92 in the upper tubesheet of OTSG 1B had been installed

during the past refueling outage (RFO 1EOC-17) as a result of tubes

being pulled for inspection. (RWPs in OTSG B were examined after a

review of records showed that 7 of 28 RWPs installed in OTSG B during

the past outage had experienced rejects during welding.)

Both of these

RWPs had experienced two rejects prior to final weld acceptance.

The two leaking RWPs were manually weld-repaired and successfully leak

tested. The licensee's review of RWP records from the last outage

showed that 2 of 23 RWPs in OTSG A, and 7 of 28 RWPs in OTSG B had

experienced weld rejects during installation. This reject rate of 25

15

percent in OTSG B, and 17 percent overall appears to be rather high for

a remote welding process.

The licensee's corrective actions for this problem included leak testing

of future RWPs and requiring the contractor to review the welding

process to determine if enhancements could be made to reduce the reject

rate.

Tube Seal Weld Leaks

Nine locations on the OTSG 1A upper tubesheet were found to be leaking

during bubble testing after shutdown; these locations were 40-1, 145-1,

144-1, 140-1, 139-1, 137-2, 136-6,75-126, and 12-71. After re-rolling

these tubes in the tubesheet, (using a recently qualified re-rolling

technique) one of the original locations, 136-6, and eight additional

locations, (116-2, 148-41, 147-46, 144-2, 146-51,81-124, 116-1, and

144-56) were found to be leaking. All of the seal-weld, leak locations

were at, or near, the periphery of the tubesheet.

The apparent root cause of the s'eal weld leakage was postulated to be a

stress corrosion cracking (SCC) phenomena brought on by the machining of

the tubesheet surface during the repairs in 1972. A licensee requested

review of the accident analyses for the Oconee OTSGs showed that during

a main steam line break (MSLB), flexure of the tubesheet is postulated

to cause dilation of the peripheral holes near the surface of the

tubesheet, thereby transferring the axial MSLB loads from the rolled

joint to the seal welds, which have been shown to be susceptible to SCC.

(The MSLB analyses for the Oconee units predicted.much higher axial .

loads on the upper tubesheet than did the MSLB analyses for other B&W

once through steam generators. The absence of main steam isolation

valves in the Oconee design apparently contributed to these higher

loads.)

The licensee had recently qualified a re-rolling process (due to

indications in the upper tubesheet roll transition area) which places a

new rolled joint about three inches below the top of the tubesheet. The

MSLB accident analysis showed that the new location would not be

significantly affected by the postulated MSLB hole dilation.

To correct this potential problem, the licensee re-rolled greater than

1700 peripheral tubes in the upper tubesheet of OTSG 1A. The final

acceptance of the re-rolled tubes included eddy current testing and leak

testing. After the completion of testing, forty tubes were removed from

service by plugging: two tubes, (75-126, and 144-1) were due to seal

weld.leakage after re-roll: six tubes, (3-32, 3-34, 44-1,84-131, 136-6,

and 150-6) were due to unacceptable eddy current indications at or below

the re-rolled area; and thirty-two tubes, (1-12, 5-3, 5-44, 8-56, 20-84,

22-1, 23-7, 25-1,36-113, 37-1. 42-1,53-126, 60-129,65-130, 67-130,74-125, 83-132,85-130, 87-130,88-129, 102-123, 130-93, 137-1, 138-75,

139-73, 143-60, 147-44, 147-46, 148-38, 148-41, 149-32, and 151-10) were

because the.configuration of the re-rolled area did not meet acceptance

standards.-

16

Manual Welded Plug Leak

After conletion of the repairs.to the weld overlay area adjacent to

location 77-7, subsequent leak testing showed a pinhole leak in the

manual weld of location 75-8. This tube location was extremely close to

the leaks in the weld overlay, and therefore this leakage was masked

during the initial leak testing of the OTSG.

The weld pinhole, at location 75-8, was manually weld-repaired and

successfully leak tested. The licensee is considering the addition of

leak testing to the acceptance criteria for future manual welds.

The inspectors reviewed the licensee's root cause process and report,

and observed OTSG inspection and recovery activities. Activities

observed included visual inspections, leak-testing, re-rolling, and eddy

current inspections. Based on the reviews of video tapes of the tube

sheet inspections, reviews of 1974 and 1977 documentation, and

observation of recovery activities, the inspectors agreed with the root

cause(s) and corrective action conclusions reached by the licensee's

investigation team. In particular, the inspectors agreed with the

conclusions that pointed to an apparent over-reliance on visual

inspections for acceptance of welds, and the 'need for leak testing of

future OTSG work. The inspectors concluded th*at past corrective actions

had not adequately considered the role of primary water stress corrosion

cracking. (It

was not a viable consideration during the tubesheet

repairs in 1972, and the weld overlay modification in 1994.)

The long term corrective..actions recommended by-the licensee's

investigation team charged the licensee's OTSG Maintenance Group with

ensuring that the contractor's welding and inspection procedures and

acceptance criteria were modified to preclude recurrence. The

inspectors agreed that the licensee's responsible organization, the OTSG

Maintenance Group, should adopt a more questioning attitude toward the

contractor's procedures and criteria.

c. Conclusions

The December 28, 1997, Unit 1 shutdown for primary-to-secondary leakage

was the result of past repairs, where there had been an apparent over

reliance on the results of visual inspections, and less than adequate

appreciation for primary water stress corrosion cracking.

M3

Maintenance Procedures and Documentation

M3.1 Unexpected Effect of Letdown Flow Calibration on Unit 3 Thermal Power

Best

a. Inspection Scope (62707)

The inspectors reviewed the maintenance aspects of an unexpected power

increase on Unit 3. The details of what happened and the operational

aspects of the power increase have been included in Section 01.4.

17

b. Observations and Findings

On January 15, 1998, maintenance personnel were calibrating letdown flow

instrumentation in accordance with Procedure IP/0/B/0202/01h, High

Pressure Injection System Letdown Flow Instrument Calibration, Revision

16, when core thermal power began to increase. The licensee

- investigated and determined the cause of the power increase was the

effect that chan ing letdown flow signal had on the ICS. The licensee

determined that letdown flow was an input into the secondary thermal

power calculation performed by the operator aid computer (OAC). This

thermal power calculation was used by the ICS as a feedback signal for.

core thermal power.

The licensee suspended the calibration, placed Procedure IP/0/B/0202/01h

on administrative hold, and initiated PIP report 3-098-0232. The

licensee began a review of procedures affected by the OAC core thermal

power calculation and subsequently determined that Procedure

P/0/B/0202/01h had not been identified as affecting the core thermal

power calculation or the ICS when ICS was returned to service after

modification on March 27, 1998.

The inspectors reviewed applicable site documents to understand the

modification interaction process. Documents reviewed were as follows:

Procedure IP/0/B/0202/01h; Problem Report 3-098-0232; Modification ON

32989, 3EOC16-ICS Replacement, Revision 0; and Nuclear Station Directive

(NSD) 301, Nuclear Station Modifications (NSM), Revision 13.

Additionally, the inspectors interviewed-licensee personnel on how

procedures affected by plant modifications are identified and changed.

NSD 301, Section 301.3.1.11, stated that the superintendent of

maintenance was responsible for -identifying and developing any

instrumentation procedure revisions required as a result of modification

work. NSD 301, Sections 301.5.4.4 and 301.6.3.7, stated that prior to

acceptance of a modification by operations, all procedure revisions

would be completed. With the modification of the ICS, neither procedure

IP/0/B/0202/01h nor modification ON-32989 addressed or made any mention

of an impact on ICS by letdown.flow calibration. The inspectors also

identified that the maintenance department lacked a section level

procedure governing the process for identification and revision of

procedures affected by modifications.

TS.6.4.1.e requires the station to be maintained in accordance with

approved procedures for maintenance of equipment which could affect

nuclear safety. The failure to revise Procedure IP/0/B/0202/01h to

include effects of modifications to the ICS is a violation (VIO) of this

TS and is identified as VIO 50-269,270,287/97-18-05: Failure to Revise

Procedure Following ICS Modification.

c. Conclusions

The inspectors identified a violation for failure to revise a high

pressure injection system letdown flow instrument calibration procedure

following modification of the Unit 3 ICS.

18

M3.2 Oconee 600 Volt K-line Breakers

a. Inspection Scope (62707)

On February 2. 1998, the SSF was removed from service for maintenance.

Included in the maintenance was testing and inspection of six Asea Brown

Boveri (ABB) K-line 600 Volt load center OXSF breakers. During the

testing, problems were discovered. The inspectors observed portions of

the repair and retesting.

b. Observations and Findings

During the SSF maintenance, the licensee discovered some breaker

lubrication and breaker trip time delay problems. These problems were

promptly brought forward for management attention and problem reports 4

98-515 and 516 were initiated. One breaker had sufficient hardening of

its grease such that it may not have reclosed completely if it had

tripped. These breakers have no automatic re-latching capability. The

remaining five breakers had operated satisfactorily during as-found

testing, but upon inspection, they did exhibit signs of grease hardening

that required work. All six breakers were satisfactorily disassembled,

greased, and retested. In addition, the over-current trip devices

(identified as SS4G) for three of the breakers were found out-of

tolerance (under.time by 2 to 8 seconds) for the long time delay minimum

acceptance criteria. These devices were replaced with new ones. The

licensee was evaluating the impact of the out-of-tolerance condition on

past operability and determining root cause of the problem. Inspector

review of breaker coordination revealed that there appeared to be no

safety-problem.

There are approximately thirty-seven other safety-related K-line

breakers on-site. There are eleven per unit with four common to all

units. These .breakers are normally closed and contain no under voltage

trip circuits. They are supplied from three redundant power trains,

each of which are supplied independently from one of the three 4160 volt

switchgear, as described in the UFSAR. The breakers only function would

be to trip if a safety device were to fail.

If one of the 600 volt

breakers failed to trip, its 4160 volt supply breaker would open. The

failure of one train of 600 volt safety power is an evaluated condition

during a design basis event.

The licensee was to evaluate the following:

  • -

grease hardening impact on a preventive maintenance schedule

trip device impact on SSF K-line breaker preventive maintenance

and

past operability evaluation on SSF trip device supplied breakers

Pending resolution of this issue, this is identified as Inspector

Followup Item (IFI) 50-269,270.287/97-18-06: K-line Breaker Issues.

19

c. Conclusion

During the inspection and testing of the SSF 600 volt breakers, several

problems were identified by the licensee. The licensee satisfactorily

addressed the immediate equipment problems. There were several issues

regarding grease hardening and trip device past operability. An IFI was

initiated on those issues.

III. Engineering

El

Conduct of Engineering

E1.1 Steam Leak in Unit 1 Pressurizer Surge Line (PSL) Drain Line

a. Inspection Scope (55050)

The inspectors determined by observation of completed welds and document

review, the adequacy of replacing the drain line on the PSL. The

governing code was the American Society of Mechanical Engineers (ASME),

Section XI, 1989 Edition with no Addenda, and the American National

Standards Institute (ANSI) B31.7. 1968 Edition. The drain line was

identified as Duke Class A piping. The leak occurred near the PSL and

could not be isolated. The replacement was performed under Work Order

98009597-5.

b. Observation and Findinqs

On February 2, 1998, the inspector visited.Oconee Unit 1 to inspect

repairs to the PSL drain line steam leak attributed to a crack near a 90

degree elbow weld on the expansion loop of the drain line. The leak was

discovered on January 27. 1998. Through discussion w.ith technical

personnel and document review, the inspectors learned that on the

morning of January 27. 1998, Oconee Unit 1 was heating up and

pressurizing the RCS to the hot shutdown condition. During this time,

operation personnel identified a leak in the RCS, which they

subsequently verified as a steam leak in the PSL drain line. The leak

was found at an elbow weld on the expansion loop of the drain line. The

drain line was bounded by the PSL and valve 1RC-18 near the equipment

drain line header, at the basement floor level. It was determined that

the leak rate was 1.7 gallons per minute.

Following plant cooldown and

cold shutdown, the licensee removed the failed section of the line with

a cut at the outlet of the PSL drain line nozzle and another just below

the expansion loop. The welds on the drain line section were liquid

penetrant inspected. There were no additional cracks found. Selected

samples of straight piping and elbows were sent to the Lynchburg

Technology Center for a metallurgical investigation. A review of the

metallurgical investigation report disclosed that the failure resulted

from stress corrosion cracking, which originated on the intrados of the

third 90-degree elbow from the PSL drain line nozzle. The aggressive

material associated with this type of failure mechanism was chlorides.

The licensee believes that these chlorides came from combustion of

material containing polyvinyl chlorides during a 1973 fire in the

reactor building 1A cavity. PIP report 1-098-0357 was issued to

0II

20

document this event and the metallurgical investigation that was

performed to determine the apparent root cause of the failure.

Replacement Piping, Installation and Testing

At the time of this inspection on February 2, 1998, the replacement

drain line had been installed. The -inspector inspected the new welds,

reviewed the weld packages and the associated radiographs, all of which

were found to be satisfactory.

During plant heat up, the licensee determined that there was no flow in

the drain line. An investigation determined that a plug, which was made

from purge paper and used to prevent water from dripping on the drain

line welds during fabrication, was lodged in the pipe and would not

dissolve as expected. For more details on this matter see Inspection

Report 50-269,270,287/98-01. Following an evaluation of the potential

impact that the paper material could have on the RCS, the licensee

decided to cut the line, remove the plug by mechanical means, re-weld

the line and fill up the system for testing. By review of the above

mentioned PIP report, the inspector ascertained that the failure

investigation process team had identified an engineering or design error

in the stress analysis calculation (OSC 4349) of the drain line system.

A description of the error was documented in PIP report 1-098-465.

Error in Stress Analysis Calculations

A review of PIP .report 1-098-465 disclosed that from the time Unit 1

commenced operation, until approximately September 19. 1981, support

S/R59-0-478A-H9 was on the drain line near the PSL drain line nozzle.

The support was removed per NRC Bulletin 79-14 reanalysis request.

Monitoring of the PSL movement in response to IEB 88-11, disclosed that

the PSL was susceptible to thermal stratification that resulted in

greater movement than originally addressed. In 1991, the licensee

reanalyzed the PSL. However, the present review revealed that the re

analysis addressed only stresses from the configuration without support

S/R 59-0-478A-H9. The licensee's subsequent analysis of stress

conditions prior to the removal of S/R59-0-478A-H9 indicated that

certain locations on the drain line and the drain line nozzle were

significantly over stressed. This over stressed condition was

identified as an indicator of cycling the stress range beyond twice the

yield point, which appears to have been mostly responsible for the

initiation of the crack. However, in reference to the drain line, the

licensee determined that the stress overload condition had been

rectified by the removal of S/R 59-0-478A-H9 and the removal of the

original drain line. The drain line was replaced from the drain nozzle

down to a location on the vertical run below the expansion loop.

Oualification of Drain Line Nozzle for Continued Operation

In addition to this analysis, the licensee performed a calculation to

evaluate the flaw tolerance of the PSL drain line nozzle. A review of

the results disclosed that the subject nozzle was capable of performing

its required function for all design loading for one fuel cycle. During

  • .

21

this time frame the licensee will re-evaluate the problem and determine

the appropriate corrective action to be taken to bring the drain nozzle

into compliance with the applicable code requirements. On February 2,

1998, the licensee discussed this matter with the staff at Nuclear

Reactor Regulation (NRR),.who agreed with the licensee's methodology.

No operability issues on this matter were identified during this call.

The licensee plans to continue power operation for one fuel cycle, which

provides sufficient time to decide the appropriate actions that will be

taken to return the PSL drain line nozzle into compliance with

applicable code and UFSAR requirements. This matter was identified as

an inspector followup item to allow for a review and verification that

the subject nozzle had been returned to compliance with code

requirements and FSAR commitments, IFI 50-269/97-18-07:

Pressurizer

Surge Line Drain Line Nozzle Loads Exceed Stress Analysis Limits.

c. Conclusion:

Replacement of the cracked one-inch drain line on the pressurizer surge

line was consistent with applicable code requirements. A lack of

attention to details in the planning phase of welding the replacement

line caused a significant job delay and the need to cut and re-weld a

new weld on the line. Engineering provided adequate support and took an

active role in determining the root cause of the crack. Welding.

nondestructive examination, and process control activities were

satisfactory. Stress analysis calculations determined that thermal

stratification and hanger loads on the drain line, exceeded code.

allowable usage factor requirements, on the drain line nozzle.

E2

Engineering Support of Facilities and'Equipment

E2.1 Unit 2 Integrated Control System Neutron Error Spikes

a. Inspection Scope (62707, 92903)

The inspectors observed, between January 6 and 7, 1998, troubleshooting

activities, engineering support, operator actions, and prejob briefings

relating to the Unit 2 ICS neutron error spikes.

b. Observations and Findings

The ICS neutron error spikes were occurring randomly and were causing

unwarranted control rod movements. The problem was captured in PIP

2-97-4615. Engineering had begun power monitoring of the ICS and had

narrowed down the problem to several components. Prior to the

troubleshooting activities the average temperature module started a

decreasing trend. This resulted in minor rod movements.

Among the specific items observed by the inspector were: the replacement

of two relays associated with the average temperature; tracing of the

power lead which was to be lifted inside ICS cabinet number 6 for

various modules associated with the neutron error signal; the

replacement of a potentially degraded connector plug for a module in the

ICS; and the prejob briefings for the replacement of the relays and the

22

connector plug. The inspector had not observed the hand-over-hand

tracing of the neutral line that was to be lifted for the repair work.

Engineering and instrumentation personnel had written a trou leshooting

procedure for the work.

On January 7, 1998, the inspectors observed that during the prejob

briefing for the replacement of the connector plug, the engineer

informed the operators that the activity would have minimal impact on

the unit. The lifting of the black power lead on the connector plug per

the troubleshooting procedure, would result in the loss of startup feed

water flow indications that were not needed at full power. When

maintenance personnel lifted the white neutral wire, several events,

both expected and unexpected occurred. Expected changes such as the 2A

and 2B startup feedwater flow indication being lost occurred. The

following items that were unexpected also occurred: the 2A and 2B main

feedwater flow indication was lost: the smart analog signal select

(SASS) system detected a loss of main feedwater indications on the A and

B loops and selected a good indication; and the 2A and 2B main feedwater

pump controllers shifted from the automatic mode to the manual mode of

operation. In this condition, the unit controls would not have

responded to a feedwater pump automatic runback. Correct SASS system

operation prevented a plant trip. The encountered problems were

documented in PIP report 2-98-44.

The shift operations manager directed the engineer and the technicians

to stop work, to review the activity, and to determine the extent of the

loss of ICS modules and relays. The review:indicated that the white

neutral wire was attached.to modules and relays in ICS cabinets other

than those originally identified. The procedure manipulation affected

these other components. Subsequently the licensee personnel involved

found all other neutral wire connected components. The other components

not previously identified were visually difficult to see. After

satisfying operations of the completeness of their more recent tracing

and completion of procedure changes, the repair work was completed

successfully.

During the initial work on January 7, 1998, maintenance had not

adequately traced the white neutral lead. This error had been

introduced into the licensee's troubleshooting procedure. 10 CFR 50,

Appendix B, Criteria V. Instructions, Procedures, and Drawings, '

conformed to by the licensee's quality assurance program, requires that

activities affecting quality shall be prescribed by documented

instructions, procedures, and drawings of a type appropriate to the

circumstances and shall be accomplished in accordance with these

instructions, procedures, and drawings. NSD 703, Administrative

Instructions for Station Procedures, Revision 17, Section 703.5,

Preparation of Procedures, states, in part, that procedures shall be

written to minimize risk to equipment and should, when appropriate,

instruct persons performing the procedure what responses to expect from

their actions. Further, as required by the NSD, the licensee had not

validated the procedure to ensure usability and operational correctness.

The troubleshooting procedure written for the repair (WO 98000451)

failed to meet these requirements.. This failure is identified as an.

(II

23

example of VIO 50-269,270,287/97-18-08: Failure to Establish and

Implement Procedures - Three Examples.

c. Conclusions

The inspectors identified the first of three examples of a violation

involving procedural inadequacies. (The other two examples are

discussed in Section E2.2.)

An engineering supported troubleshooting

procedure did not minimize risk to equipment and was not completely

validated prior to performing work. Use of the procedure on Unit 2 ICS

wiring resulted in unexpected system.responses.

E2.2 Keowee Testing. Failure to Start, and In-Service Testing

a. Inspection Scope (37551, 92903)

The inspectors observed and reviewed engineering support for testing

involving the Keowee Hydroelectric Plant (KHP). The inspectors

responded to the KHP for observations and reviews of engineering support

when: on January 9. 1998. the Unit 2 generator failed to start in the

normal mode; on January 14, 1998, voltage adjust did not run to preset

as expected during testing: and, on January 20, 1998, both of the KHP

units were out of service due to a missed in-service test.

b. Observations and Findinqs

On January 9: 1998, the KHP operations personnel started the KHP Unit 1

generator, which successfully paralleled automatically to the grid as

expected. When the Unit 2 KHP generator was started, it came up to

rated speed, received a UNIT 2 INCOMPLETE.START alarm, and tripped. The

KHP units were being started to.control Keowee Lake level.

The inspectors observed and reviewed activities involved with

engineering support, troubleshooting- information gathering for root

cause, prejob briefings for the various work activities, and the

adjustment of the motor operated automatic voltage regulator. The

troubleshooting identified an open coil in a time delay relay (Agastat

90X1A/TD).that prevented the regulator from shifting to automatic

control. With the regulator not shifting to automatic, the unit

received the incomplete start alarm and tripped.- The licensee replaced

the relay, tested the unit, and returned it to operable status.

The inspectors observed, during the troubleshooting, that the regulator

was not adjusted in accordance with drawing KEE-212-5, Elementary

Diagram Excitation System Motor Operated Auto Voltage Adjuster, Revision

8, a Quality Assurance (QA) Condition 1 drawing. The inspectors found

that Procedure IP/0/A/2005/003, Keowee Hydro Station Westinghouse WTA

Voltage Regulator Test, Revision 23, did not contain adequate detail to

properly set up the voltage adjuster. The procedure did not address the

unused timing cams in the adjuster that, if unaccounted for, could cause

operational problems.

(The unaccounted for cams had not caused

operational problems at discovery.)

Following the Unit 2 adjustment,.

the Unit 1 regulator was checked and was also not in accordance with the

24

applicable drawing. Subsequently, the licensee properly adjusted both

cams. During the work, the operational status of the Keowee units was

properly addressed. These voltage adjusters had been previously worked

by the above procedure.

10 CFR 50 Appendix B, Criteria V. Instructions, Procedures, and

Drawings, conformed to by the licensee's QA program, requires that

activities affecting quality shall be prescribed by documented

instructions, procedures, and drawings of type appropriate to the

circumstances and shall be accomplished in accordance with these

instructions, procedures, and drawings. The failure to have a detailed,

adequate procedure for adjusting the motor operated regulator in

accordance with drawing KEE-212-5, Revision 8, is a violation of these

requirements. NSD 703, Administrative Instructions for Station

Procedures, Revision 17, Section 703.5, Preparation of Procedures,

Subsection 4, subsection requirements stated, in part, that procedures

shall be written in adequate detail to ensure accurate results. This

item is identified as an example of VIO 50-269,270,287/97-18-08: Failure

to Establish and Implement Procedures - Three Examples. The licensee

initiated a failure investigation team and problem report K-98-106.

On January 14, 1998, during the performance of test PT/O/A/0610/22,

Degraded Grid, Switchyard Isolation, and Keowee Over Frequency

Protection, Revision 8, the KHP Unit 2 did not return to the preset

automatic generator voltage level as required. With support from

engineering, a defective Cutler-Hammer Type D87 timer relay was

discovered. The.timer fai.led to allow enough-time for the motor

operated automatic voltage adjuster to run the voltage back to the

preset level. The licensee replaced the timer relay and the test was

successfully completed. The inspectors found that type D87 timer relays

had failed on a previous occasion. The licensee initiated a second

failure investigation and PIP report K-98-211. The licensee has sent

both of the failed relays to vendors for evaluation. Pending additional

inspector review of the licensee's efforts in this area, this is

identified as IFI 50-269,270,287/97-18-09: Review of the Root Cause

Analysis for Agastat Time Delay and Type D87 Timer Relays.

On January 20, 1998, during a quarterly surveillance and maintenance

outage for KHP Unit 2, it was discovered that an in-service test (IST)

had not been performed when required on both KHP units. Both units were

declared inoperable and the appropriate TS and selected licensee

commitment was entered. The inspectors found that a temporary IST

Procedure TT/0/A/0620/16, KHU-1 Turbine Guide Bearing Oil System Test,

Revision 1, was not converted to a performance test (PT).

This resulted

in an IST of check valves in the oil system for Keowee Unit 1 not being

performed within the required time frame. The required ISTs were

performed using the temporary procedure and both KHP units were declared

operable.

NSD 300. ASME Section XI Program, Revision 2. states, in part, that the

nuclear site engineering organization is responsible for interfacing

with the station organization to prepare written test procedures. Not

0II

25

converting the temporary procedure to a PT is a violation of this.

requirement. This item is identified as an example of VIO 50

269,270,287/97-18-08:

Failure to Establish and Implement Procedures

Three Examples.

At the end of the report period, licensee personnel had completed a

review of temporary procedures for conversion to permanent procedures

with no discrepancies identified. The licensee was also conducting root

cause determinations for the open coil on the time delay relay and the

failed timer.

c. Conclusions

Two additional examples of a three-example violation involving procedure

inadequacies were identified. Section E2.1 discusses the first example

of the violation. The two additional examples occurred on the Keowee

Hydroelectric units. One example involved the motor operated automatic

voltage adjusters on both Keowee units not being adjusted in accordance

with their applicable drawings due to a lack of procedural detail.

The

other example involved missed ISTs on both Keowee Hydroelectric units

due to a failure by engineering to convert a temporary test into a

periodic test on lube oil valves.

E8

Miscellaneous Engineering Issues (92903.92700)

E8.1 <(Discussed) LER 50-269/97-10: Inadequate.Analysis of.Emergency Core

Cooling System (ECCS) Sump.Inventory Due to Inadequate.Design Analysis.

This event was discussed in Inspection Report 50-269,2701287/97-16. The

inspectors reviewed the completed evaluation in the LER. During the

flow velocity evaluation, the licensee identified that the refueling

canal drains contained basket type strainers which could become clogged

and trap approximately forty thousand gallons of ECCS and reactor

coolant system line break fluid.

The reactor cavity drain had a flange installed with an open 3/4-inch

pipe nipple that could also become blocked and trap approximately sixty

thousand gallons of fluid. UFSAR section 3.8.3.1. "Description of the

Internal Structures," states that the reactor cavity was designed

structurally to contain core flooding water up to the level of the

reactor nozzles. Framatome Technology Incorporated was contacted by

engineering and confirmed that this was an original design issue that

was later determined to be unnecessary. The flange on Unit 3 was

removed at some unknown time.

The strainers in the fuel transfer canal drains were installed

approximately ten years ago during a refueling outage to maintain dose

rates during decontamination As Low As Reasonably Achievable (ALARA).

Individuals interviewed remembered this to be with verbal concurrence

from engineering to remove them prior to operation and reinstall the

approved perforated strainer plate. The original strainer plates were

never reinstalled.

26

The system engineering evaluation concluded on January 8, 1998, that the

increase in transport velocity did not affect the operability of the

reactor building emergency sump. Therefore the sump was determined to

be both past and present operable.

Neither the removal of the flange nor the installation of the strainers

was evaluated as a modification to the plant through the station

modification process. NSD 301, NSM, Revision 12, Section 301.1.1,

indicates that it applies to all structures, systems, and components

located within the nuclear facility. Section 301.2 further indicates

that changes to these structures, systems, and components are considered

modifications and require implementation packages. The licensee has

subsequently evaluated the removed Unit 3 flange, removed the flanges on

the other two units, and, as indicated above, removed the strainers.

This non-repetitive, licensee identified and corrected violation is

being treated as a NCV consistent with Section VII.B.1 of the NRC

Enforcement Policy. This is identified as NCV 50-269.270.287/97-18-10:

Failure to Follow Modification Procedures. This LER will remain open

ending review of additional issues concerning the Borated Water Storage

ank level and the RB emergency sump level identified at the end of the

report period.

E8.2 (Open) Inspector FollowUp Item 50-269.270.287/96-13-03: Service Water

System Modifications and Testing.

The service water system operational performance inspection (SWSOPI) had

identified several issues with respect to the design and operation of

the low pressure service watersystem. (LPSW)

and the emergency condenser

circulating water (ECCW) systems. These issues included the cooling and

-sealing supply to the condenser circulating water (CCW) pumps and

motors, maintaining the CCW conduits full of water during siphon

operation, the net positive suction head (NPSH) requirements for the

LPSW pumps, and the quality condition of certain structures, systems and

components (SSC) required to maintain the siphon. The licensee had

committed, in a letter dated December 28, 1995, to perform certain

modifications to upgrade the ECCW system. These modifications included

providing an LPSW supply to the CCW pumps and motors, changes to the

PSW system to ensure adequate NPSH. installing an emergency siphon

vacuum system, and upgrading and reclassifying portions of the CCW

system to QA-1. The five major modifications have been broken down into

approximately eighty implementation parts and minor modifications.

The inspectors reviewed the licensee's progress in implementing these

modifications. The following implementation parts have been completed:

LPSW minimum flow recirculation piping has been installed on all three

units; trenches have been installed from the radioactive waste trench to

the intake dike and essential siphon vacuum (ESV) building: the

emergency safeguards signal for LPSW 4 and 5 has been removed from Units

1 and 2: new LPSW pump impellers have been installed in Units l and 2;

Unit 1 CCW pump discharge valve control circuitry has.been upgraded and

the new isolation valves for the non-essential turbine building LPSW

loads have been installed and related control switches moved to the

control rooms.

27

The inspectors reviewed work in progress, which included completion of

the ESV building and installation of the ESV pumrs, tanks, valves,

power, and instrumentation; installation of the PSW headers from Unit

1, 2 and 3 in the turbine building; and installation of the LPSW and ESV

piping in the trench to the intake dike.

The inspectors discussed the licensee's LPSW implementation plans for

the Unit 2 outage, currently planned for March 1998. The implementation

parts to be completed during the March outage as currently planned will

complete the LPSW modifications on Unit 2. Testing of the ECCW siphon

will be conducted on Unit 2 following completion of the modifications.

The licensee's current plans are to complete Unit 3 modifications during

the fall 1998 outage and the remaining Unit 1 modifications during the

spring 1999 outage.

The inspectors concluded that the licensee had made good progress in the

installation of the modifications considering the intervening events

(feedwater heater line rupture and rework on the balance of plant

systems) and the size of the LPSW modifications.

This item will remain open pending the completion of the modifications

on all three units and completion of post modification testing.

IV.

Plant Support Areas

P8

Miscel aneous. EP Issues (92904)

. P8.1 Severe Accident Management Guideline (SAMG) Training

Severe accident mitigation guidelines were written to identify options

available when plant conditions place the operators outside the current

emergency operating procedures. The inspectors reviewed training

materials and observed actual SAMG training provided to plant personnel.

There were 442 employees that received introductory training on the

existence and basis for the SAMGs: 171 of which continued training for

the assessment and mitigation strategies. These employees were from

shift operations, nuclear engineering, and technical support center

personnel. One hundred and seventeen then completed self-paced

computer-based training on the science of severe accidents. The licensee

also conducted table top drills for 131 of the original 442 employees.

The training was completed on December 19, 1997, and the licensee posted

a letter to the NRC describing the training. The inspectors attended

parts of the training, finding the training and guidelines to be .of

sufficient detail for the intended purpose.

P8.2 Meeting With Local Emergency Preparedness Officials

The resident inspectors met with local officials following the

completion' of the Systematic Assessment of Licensee Performance (SALP)

meeting on January 8, 1998. The purpose of the meeting was to introduce

the new inspectors to the officials and to allow discussion of any

concerns the officials may have. No concerns were identified by local

officials.

28

F1

Control of Fire Protection Activities

F1.1 Transformer Fire Watches

a. Inspection Scope (71750)

On January 17, 1998,.the licensee determined that they had not

established appropriate fire watches during the out-of-service periods

for two transformers. The inspectors followed the licensee's activities

and corrective actions.

b. Observations and Findings

On January 17, 1998, at approximately 2:00 p.m., the operations staff

determined that they had not implemented fire watches in accordance with

a site instruction. Operations generated problem report 98-0255 and

notified the inspectors. Operations personnel had taken the deluge fire

protection and detection systems out-of-service for the startup

transformers on Units 2 and 3. They had accomplished the preventive

maintenance on CT2 and CT3 on January 15, 1998. Operations was

preparing to take the systems out on Unit 1 when it was discovered that

elected Licensee Commitment 16.9 and NSD 316, Fire Protection (dated

December 30, 1997), had been misapplied. Specifically, hourly fire

watches had been.established instead of the continuous fire watches as

required by both instructions. Operations personnel had mistakenly

thought that they had not taken the .detection system out-of-service when

the fire water header was isolated on each of the two transformers. The

decision point regarding hourly or continuous fire watches was in the

procedure, but it did not specify what took the detection system out-of

service. Making the correct decision required an understanding of the

transformer fire suppression system. The licensee placed appropriate

watches on Unit 1. NSD 316 was scheduled to be enhanced to point out

that the detection system was disabled with the isolation of the

transformers' fire header. This non-repetitive, licensee identified and

corrected violation is being treated as an NCV consistent with Section

VII.B.1 of the NRC Enforcement Policy. This is identified as NCV 50

270,287/97-18-11: Failure to Implement Continuous Fire Watches During

Transformer Deluge System Maintenance..

c. Conclusions

An NCV was identified for failure to perform a continuous fire watch as

required by the fire protection program and selected licensee

commitments. The licensee had performed hourly fire watches instead of

continuous fire watches when the fire protection deluge system was taken

out of service for the startup transformers on Units 2 and 3.

29

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on February 11, 1998. The

licensee acknowledged the findings presented. No proprietary

information was identified to the inspectors.

X2

Notice of Enforcement Discretion for Units 2 and 3

a. Inspection Scope (92903)

The licensee has had many regular outage schedule disruptions, due to

many forced outages on all three plants in the last several years.

The

realization of associated surveillance schedule problems led the

licensee to have discussions with the NRC and produce several TS

submittals. The inspectors followed the activities and read the TS

submittals for correctness.

b. Observations and Findings

On January 15. 1998, the licensee submitted a TS change request in

accordance with 10 CFR 50.90. The requested amendment titled, Request

for Technical Specification Amendment for Test and Calibration,

consisted of a proposed one-time extension to the instrument channel

test frequency for several instruments and engineering safeguards

channel surveillances. The NRC.was processing that change in accordance

with the normal thirty-day comment period. Several days later, the

licensee discovered more TS driven surveillances that had not been

included in the January 15 submittal. The licensee engaged the NRC in

discussion about including these additional items in the January 15

submittal.

Due to NRC process requirements, NRR could not include those

additional surveillances in a timely manner to support Unit 2

surveillance due dates. The end of initial TS surveillance grace limit

for the potentially overdue low pressure injection cooler performance

test surveillance was February 14, 1998. while the unit refueling was

scheduled for March 13. 1998. The licensee then questioned the NRC

whether they could perform the surveillances scheduled to be completed

at refueling outages, at other times. The response from NRR in NRC

headquarters was that surveillances specified for refuelings per TS must

be completed during refueling outages. On January 30, 1998, the

licensee submitted a request for a Notice of Enforcement Discretion

(NOED) for Refueling Outage Frequency Surveillances. NRR had verbally

granted the discretionary enforcement to the licensee on January 30,

1998. After the granting of discretionary enforcement, the licensee

submitted a February 2, 1998, TS change altering the surveillance

frequency dates. The change which affected 93 surveillances, aligned

the Oconee TS with the NRC approved standard TS. That left several

surveillances to be performed later in February 1998 while Unit 2 was at

power operation, which was after the end of this inspection period.

30

The inspectors reviewed the proposed new TS for content. The licensee

appeared to have identified all the locations in the TS were refueling.

refueling outage, or "RF" (abbreviation for refueling frequency) had

been used. The licensee was submitting a page change to the last

submittal correcting a paragraph 4.2.2 change back to refueling-outage

frequency from eighteen months. These involved inspections of the core

barrel to core support shield caps that-should be inspected each outage.

This change was due to be issued on or about February 19, 1998.

Several items are planned or have occurred in response to the above

administrative events. The NRC performed a review of the surveillance

rocess, which is discussed in Inspection Report 50-269,270,287/98-01.

RR has issued or planned to issue the required documentation on the

licensee's submittals. The licensee was to issue an LER on the required

surveillance issue. Pending further review, this will be identified as

URI 50-269.270,287/97-18-12:

Refueling Outage Surveillance NOED.

c. Conclusions

On January 30, 1998, the licensee was granted verbal enforcement

discretion on statements of their TS regarding surveillance performance

intervals. The .licensee submitted a TS change to allow eighteen-month

periodicity of surveillance instead of a refueling outage periodicity.

inspectors had reviewed the change for completeness. Additional

followup on the enforcement discretion will be tracked under an

unresolved item.

X3

NRC Management Meetings

On December 16, 1997, Mr. Hugh Thompson, Jr., Deputy Executive Director

for Regulatory Programs and Mr. Luis Reyes, Regional Administrator.

Region II,

were at the site to tour the facility and meet with licensee

personnel.

0II

31

Partial List of Persons Contacted

Licensee

,E. Burchfield. Regulatory Compliance Manager

T. Coutu, Scheduling Manager

D. Coyle, Mechanical Systems Engineering Manager

T. Curtis, Operations Superintendent

B. Dobson, Mechanical/Civil Engineering Manager

W. Foster, Safety Assurance Manager

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Engineering Manager

W. McCollum, Vice President, Oconee Site

M. Nazar, Manager of Engineering

B. Peele, Station Manager

J. Smith, Regulatory Compliance

J. Twiggs, Manager, Radiation Protection

Other licensee employees contacted during the inspection included technicians,

maintenance personnel, and administrative personnel.

NRC

D. LaBarge, Project Manager

Inspection Procedures Used

IP37551

Onsite Engineering

IP50002

Steam Generators

IP55050

ASME Welding

IP61726

Surveillance Observations

IP62707

Maintenance Observations

IP71707

Plant Operations

IP71750

Plant Support Activities

IP92700

Onsite Followup of Written Event Reports

IP92903

Followup-Engineering

IP92904

Followup-Piant Support

IP93702

Prompt Onsite Response to Events

Sta0enrtr

32

Items Opened, Closed, and Discussed

50-269/97-18-01

NCV

Inadequate RIA Procedure (Section 01.3)

50-269,270,287/97-18-02

URI

Containment Air Lock Testing (Section

01.5)

50-269,270.,287/97-18-03

URI

SSF Diesel Generator Operation (Section

03.1)

50-269,270,287/97-18-04

URI

Teflon Tape Use on the LPI System (Section

M1.1)

50-269,270,287/97-18-05

VIO

Failure to Revise Procedure Following ICS

Modification (Section M3.1)

50-269.270,287/97-18-06

IFI

K-line Breaker Issues (Section M3.2)

50-269/97-18-07

IFI

Pressurizer Surge Line Drain Line Nozzle

Loads Exceed Stress Analysis Limits

(Section E1.1)

50-269,270,287/97-18-08

VIO

Failure to Establish and.Implement

Procedures - Three Examples (Sections E2.1

and E2.2)

50-269,270.287/97-18-09

IFI

Review of the Root Cause Analysis for

Agastat Time Delay and Type D87 Timer

Relays (Section E2.2)

50-269,270,287/97-18-10

NCV

Failure to Follow Modification Procedures

(Section E8.1)

50-270.287/97-18-11

NCV

Failure to Implement Continuous Fire

Watches During Transformer Deluge System

Maintenance (Section F1.1)

50-269,270,287/97-18-12

URI

Refueling Outage Surveillance NOED

(Section X2)

Closed

None

Discussed

50-269/97-10

LER

Inadequate Analysis of ECCS Sump Inventory

Due to Inadequate Design Analysis (Section

E8.1)

33

50-269,270,287/96-13-03

IFI

Service Water System Modifications and

Testing (Section E8.2)

List of Acronyms

ABB

Asea Brown Boveri

ALARA

As Low As Reasonably Achievable

ANSI

American National Standard

ASME

American Society of'Mechanical Engineers

B&W

Babcox and Wilcox

CFR

Code of Federal Regulations

CCW

Condenser Circulating Water

CRD

Control Rod Drive

ECCS

Emergency Core Cooling System

ECCW

Emergency Condenser Circulating Water

ESV

Essential Siphon Vacuum

F

Fahrenheit

GPD

Gallows per Day

GPM

Gallons Per Minute

ICS

Integrated Control System

IFI

Inspector Followup Item

IST

In Service Testing

KHP

Keowee Hydro (electric) Plant

LER

Licensee Event Report

LCO

Limiting Condition for Operation

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

MSLB

Main Steam Line Break

mR

Millirem

NCV

Non-Cited Violation

NLO

Non-Licensed Operator

NOED

Notice of Enforcement Discretion

NPSH

Net Positive Suction Head

NRC

Nuclear Regulatory Commission

NRR

Nuclear Research and Regulation

NSD

Nuclear System Directive

NSM

Nuclear Station Modification

DAC

Operator Aid Computer

ONS

Oconee Nuclear Station

OTSG

Once Through Steam Generator

PDR

Public Document Room

PIP

Problem Investigation Process

PSIG

Pounds Per Square Inch Gauge

PSL

Pressurizer Srge Line

PT

Performance Test

QA

Quality Assurance

RB

Reactor Building

RCS

Reactor Coolant System

REV

Revision

RIA

Radiation Indication and Alarm

RPM

Revolutions Per Minute

RWP

Remote Weld Plug

34

SAMG

Severe Accident Management Guideline

SASS

Smart Analog Signal Select [system]

SCC

Stress Corrosion Cracking

OTSG

Once Through Steam Generator

SSC

Structure, Systems & Components

SSF

Safe Shutdown Facility

SWSOPI

Service Water System Operational Performance Inspection

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

VIO

Violation

WO

Work Order