ML15118A104

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Insp Repts 50-269/96-05,50-270/96-05 & 50-287/96-05 on 960316-23.Violations Noted.Major Areas Inspected: Circumstances Surrounding Unit 3 Reactor Trip Event on 960316
ML15118A104
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 04/17/1996
From: Crlenjak R, Harmon P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A101 List:
References
50-269-96-05, 50-269-96-5, 50-270-96-05, 50-270-96-5, 50-287-96-05, 50-287-96-5, NUDOCS 9605140289
Download: ML15118A104 (15)


See also: IR 05000269/1996005

Text

REG4

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/96-05, 50-270/96-05 and 50-287/96-05

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC

28242-0001

Docket Nos.:

50-269, 50-270 and 50-287

License Nos.:

DPR-38, DPR-47 and DPR-55

Facility Name:

Oconee Units 1, 2 and 3

Inspection Conducted: March 16-23, 1996

Inspectors:

i-

-_

__

P. E. Harmon, S 0or Resident Inspector

Date Signed

P. Humphrey, Resident Inspector

P. Fillion, Reactor Inspector

D. Forbes, Reactor Inspector

D. Jones, Reactor Inspector

L. Wie

Project Mapa

Approved by:

  • 7

R. . Crlenja

,

ranch Ch f

Dafe Si ned

Division of Reactor Projects

SUMMARY

Scope:

This special inspection was conducted to review the circumstances

surrounding the Unit 3 reactor trip event on Saturday, March 16, 1996.

The trip occurred during the performance of a test on the electrical

system. The Senior Resident Inspector was on-site at the start of the

event and was subsequently supported by other NRC inspectors who

promptly arrived on-site to participate in the special inspection

effort.

The circumstances surrounding the event included several complications:

(1) a temporary loss of off-site power and delayed restoration of

off-site power; (2) tripping of the reactor coolant pumps and subsequent

natural circulation core cooling for approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />; and

(3) Condensate System pressure surge (water hammer) and the spread of

condensate polishing resin throughout the system. The scope of the

inspection included:

(1) root cause determination; (2) evaluation of

trip transient analysis and system response; (3) evaluation of licensee

ENCLOSURE 2

9605140289 960417

PDR

ADOCK 05000269

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PDR

III)

2

performance; and (4) corrective actions for the root cause and other

equipment problems.

Results:

The licensee accurately identified the root cause. The root cause was

determined to be a vibration-induced actuation of a load shed relay.

The relay was found to be improperly assembled.

(paragraph 2.3)

The licensee's event analysis properly identified all abnormal

indications and their causes. The Post Trip Review was complete and

thorough. (paragraph 5.0)

Corrective actions were comprehensive and well managed. All identified

pre-startup items were adequately addressed.

(paragraph 5.0)

Operators were very effective in managing the trip. Management was

effective in providing oversight and applying resources. The

Significant Event Investigation Team compiled an accurate sequence of

events and provided valuable input for corrective actions.

(paragraphs 3.2. and 3.3)

One Violation was identified for failure to make a 4-hour report as

required by 10 CFR 50.72.

(paragraph 3.1)

A weakness was identified concerning the length of time required to

regain off-site power. (paragraph 2.2)

A concern was identified regarding the schedule for implementation of a

modification to defeat the fast transfer of the reactor coolant pump

buses.

(paragraph 4.0)

ENCLOSURE 2

REPORT DETAILS

Acronyms used in this report are defined in paragraph 8.0.

1.0

PERSONS CONTACTED

Licensee Employees

  • B. Peele, Station Manager
  • E. Burchfield, Regulatory Compliance Manager

D. Coyle, Systems Engineering Manager

  • J. Davis, Engineering Manager
  • W. Foster, Safety Assurance Manager

J. Hampton, Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

J. Smith, Regulatory Compliance

G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

  • L. Azzarello

Other licensee employees contacted included office, operations,

engineering, maintenance, chemistry/radiation, and corporate personnel.

  • Attended Exit Interview

2.0

EVENT DESCRIPTION (93702)

2.1

System Description and Alignment Immediately Prior to the Event

The on-site emergency power supply consists of two hydro units. When

the control system senses the need for emergency power, one hydro unit

is automatically aligned to supply power to plant auxiliaries via an

isolated 230 KV (Yellow) bus, also referred to as the Overhead Line.

The other hydro unit is automatically aligned to supply power via a

13.8 KV cable, referred to as the Underground Line. A 100 KV

transmission system, supplemented with an off-site gas turbine, can

supply power to the plant buses.

At the onset of the March 16, 1996, Unit 3 reactor trip event, the

licensee was in the process of performing Periodic Test PT/O/A/0610/22,

Degraded Grid, Switchyard Isolation and Keowee Overfrequency Protection

Functional Test. This test verifies, in part, that the emergency

electrical system has the capability of performing its function when

called on to do so.

The three Oconee units were at full power. In

accordance with the test procedure, both 87.5 MVA rated hydro units were

generating to the grid at about 74 MW each. The 100 KV system was in

ready standby with the gas turbine running. Automatic fast transfers of

plant auxiliaries and RCP buses from the unit auxiliary transformer to

the startup transformer were disabled by placing transfer switches in

the manual mode.

Three 230 KV motor operated disconnect switches at

breakers 21, 24, and 33 were open to help protect the units from

potential interaction with portions of the system under test.

II

2

2.2

Trip Description and Sequence of Events

At 1:17:47 pim., on March 16, 1996, simulated signals were injected to

initiate emergency alignment of the emergency power system. Plant

auxiliaries in all three units should have continued to operate, being

powered from their respective unit auxiliary transformer. Instead,

there was a simultaneous spurious actuation of a single set of contacts

in a Unit 3 auxiliary relay which caused tripping of a hotwell pump, a

booster pump, and two heater drain pumps in the Unit 3 secondary system.

One condensate booster pump started automatically as designed. Within

about 14 seconds, another condensate booster pump was manually started.

These events were followed by a condensate system pressure transient

which led to feedwater pump trips due to low suction pressure, and a

Unit 3 reactor/turbine trip at 1:18:45 p.m. Operators entered the

Emergency Procedures for the plant trip. Units 1 and 2 were unaffected,

remaining at full power.

The Condensate System transient was accompanied by a water hammer in the

Condensate lines which ruptured several heat exchanger gasket seals and

allowed dislocation of powdex resins. As designed, power was

automatically restored to the plant buses 21 seconds after the unit

trip. The power source was one Keowee unit via the 230 KV Yellow bus

(Overhead Line). This particular alignment was the result of being in

the test procedure when the trip occurred. Grid power was available at

the 230 KV Red bus. The RCS was in natural circulation, because

automatic fast transfer of the RCPs had been disabled as explained

above. Operators did not start the RCPs at the earliest opportunity

allowed by the emergency operating procedures.

Instead, the decision

was made to first parallel the Keowee unit and the Yellow bus to the

grid. The decision to wait until off-site power was restored was

primarily based on a concern that if a problem occurred during

paralleling, having the RCPs already running would create another loss

of forced circulation. With a lower heat load, natural circulation

would be more difficult to initiate the second time around. In

addition, the natural circulation in progress was stable and was an

acceptable operating mode.

At about 4:48 p.m., the Yellow bus and Keowee Unit supplying it was

synchronized to the grid (Red bus).

The delay of approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />

to restore off-site power from when it was available was due to several

factors:

The transfer procedure required transferring control of Keowee

from local to remote. A previous control transfer of Keowee from

Oconee (remote) to Keowee (local) had resulted in a Keowee unit

trip and damage to a breaker closing coil due to an error by the

Keowee operator making the transfer. Although this transfer was

in the opposite direction, operators wanted to review the

circumstances to prevent another Keowee trip. This was determined

not to be a concern after reviewing the previous event.

ENCLOSURE 2

3.

Several discussions were conducted with management and engineering

concerning whether to perform a dead bus or live bus transfer.

Operators wanted to review the corrective action taken for the

problems with paralleling during the 1992 Loss of Off-site Power

event.

Slow or delayed response of the Keowee speed control during the

actual synchronizing steps caused extra caution on the part of the

operators making the transfer.

The cumulative effect of these delays resulted in an inordinate amount

of time to restore off-site power. Since no complications or problems

(other than slow Keowee speed response) were encountered, the time taken

to complete the maneuver is considered a weakness. While each of the

actions taken could be considered conservative, the inspectors

determined that some of the training and decision-making during this

period should be examined to facilitate off-site restoration during

future events.

RCPs 3B1 and 382 were started at about 9:12 p.m. and 9:36 p.m.,

respectively. This allowed the operators to exit Emergency Procedure

EP/1/A/1800/01. Operators had not exited the EP because the Subsequent

Actions section requires starting RCPs before exiting. Following the

restoration of forced circulation, efforts continued to clean up

displaced condensate polishing resins. This was accomplished by short

cycle recirculation of the condensate through a restored resin bed.

At approximately 11:00 p.m., management decided to cool down and

depressurize the RCS to a point where decay heat removal via the LPI

system could be placed in service. This decision was reached after the

extent of the resin contamination was determined. The licensee

considered that continued use of the secondary side systems as a heat

sink for the reactor would be a challenge to the operators, especially

while trying to clean up these systems at the same time.

Actual unit cooldown began at approximately 5:50 a.m., on March 17.

During the cooldown, the licensee attempted to use the Unit 2 MDEFW pump

.and water supply to feed Unit 3 steam generators. This would allow more

flexibility in cleaning up the Unit 3 Condensate System and provide an

additional source of water for the cooldown.

The procedure for

implementing this alignment was revised just prior to use. The

procedure change allowed a single Unit 2 MDEFW pump (rather than two

pumps) to supply both Unit 3 steam generators.

When this arrangement

was initiated at 11:47 a.m., operators had difficulty controlling

levels.

The Unit 2 MDEFW pumps were stopped and the Unit 3 pumps were

placed back in service at approximately 12:57 p.m. The LPI system was

placed in service at approximately 5:15 a.m., on March 18. While the

LPI system was being aligned for the DHR mode, operators observed level

decreases in the Letdown Storage Tank (LDST), indicating leakage past

ENCLOSURE 2

4

isolation valves from the LDST into the LPI system. The cause was later

determined to be leakage past manual isolation valves 3LP-40 and 3LP-41.

The valves were manually tightened shut, and the leakage stopped.

2.3

Root Cause of Initiating Transient and Reactor Trip

The root cause of the event was determined to be incorrect assembly of

auxiliary relay 3RLS1X. The relay was a style D23MRD704A1 manufactured

by Cutler-Hammer Co., having 120 VDC coils. This relay had a base

assembly, a four-contact front deck (middle section) and a four-contact

front attachment (upper section).

The armature shaft was composed of

three pieces threaded together. The licensee determined that the

armature shaft pieces for the middle and upper sections were not

completely threaded together. This had the effect of decreasing the

contact gap of one contact in the upper section from the normal 50 - 70

mils to 5 mils. The contact with the 5 mil gap momentarily closed when

it was subjected to vibration. The vibration was caused by simultaneous

operation of several relays in an adjacent cabinet. The momentary

contact closure caused one of three "load shed" relays to operate, which

caused the tripping of pumps described in Paragraph 2.2. As a result,

relays which were being operated as part of the test caused the

vibration which resulted in actuation of a "load shed" relay that was

not part of the test. As of the end of the report period, the licensee

had not been able to identify why the armature shaft was not completely

threaded together. The relay and its component parts could have been

improperly assembled by the vendor, by the licensee, or could have

undergone age/use related movement after being placed in service. The

resident inspectors will continue to follow this item via the licensee's

corrective action program.

The linkage between operation of the test relays and momentary closure

of the problem contact was demonstrated in a special test. This test

was reviewed and witnessed by the inspectors. After the cause had been

proven, the problem relay was replaced. The special test was repeated

to show that the problem had been corrected. The licensee has

determined that 210 of the relays are installed in safety-related

applications. It should be noted that the safety related function of

the subject relays, including the failed relay, are not affected by this

failure. The licensee has developed a schedule for inspecting a

representative sample of these relays. The sample will be expanded to

100% if any additional relays are found to not meet the acceptance

criteria currently being developed. The resident inspectors will

continue to review this item.

2.4

Root Cause of Resin Dispersement

The transient in the Condensate System caused resin to be backflushed

from the polishing demineralizers into the condenser hotwells. When the

hotwell pumps restarted, the polishing demineralizers were bypassed and

ENCLOSURE 2

5

the resin was transported throughout the condensate system rather than

being redeposited onto the polishing demineralizers.

The licensee determined that the resin was backflushed from the resin

beds when the Condensate System pressure surge (water hammer) occurred.

A bypass valve automatically opens to bypass the resin beds, as well as

the resin filter downstream of the beds, on a low booster pump suction

pressure. Hotwell pump check valves were believed to have failed to

fully seat during the backflow condition, allowing the resins to be

carried into the hotwell.

From there, the resins were pumped into the

Condensate System through the open resin bed bypass valve. The bypass

line does not contain a resin filter or trap. The hotwell pump check

valves were later radiographed to determine their position. No problems

were found with these valves.

The ruptured heat exchanger seals, caused by the water hammer in the

condensate lines during the transient, allowed leakage of water and

resin from the system in several locations of the turbine building.

Upon discovery of the resin in that leakage, the licensee promptly began

sampling of the secondary system to determine the extent of the resin

contamination and aligned the feedwater system to minimize further

spread of that contamination. The EFW pumps were used to provide

feedwater to the steam generators from the upper surge tank rather than

from the condensate hotwell which was known to be contaminated. A small

amount of resin was transported to the steam generators when water from

the condensate storage tank, which contained some resin material, was

used as makeup water for the upper surge tank.

3.0

ASSESSMENT OF LICENSEE PERFORMANCE (93702)

3.1

Assessment of Operator Performance in Response to the Event

The Senior Resident Inspector was on-site to witness the performance of

PT 0/A/0610/22. When the trip occurred at the initiation of the test,

the inspector was able to observe operator response and assess

performance. The control room shift crew was extremely effective in

controlling the plant after the trip. The SRO clearly directed the

whole crew, and communications were excellent. Conservative decisions

were made throughout the event.

Some exceptions to the effective operator performance were noted:

SRO Started a Condensate Booster Pump:

When the spurious operation of

the load shed relay caused tripping of several plant auxiliaries, the

SRO on shift attempted to mitigate the transient by quickly starting a

condensate booster pump. This was done without informing the shift

crew. The alarm printer shows the pump was started 14 seconds after the

load shedding occurred, and 12 seconds after the standby booster pump

automatically started.

Starting the additional booster pump may have

ENCLOSURE 2

  • I6

caused the booster pump suction pressure to drop even lower, leading to

.a booster pump trip and the eventual Unit 3 trip.

Delayed/Inadequate Notification:

Pursuant to 10 CFR 50.72(b)(2)(ii) the

licensee should have notified the NRC Operations Center of the reactor

trip within four hours of the event. However, notification was made

approximately 8k hours after the trip occurred. In addition to the late

report, the report which was eventually made did not describe the

extended natural circulation mode, the loss of off-site power, or the

resin displacement-event. This failure to make proper notification as

required by 10 CFR 50.72 is identified as Violation 50-269,270,287/96

05-01, Failure To Make Proper 10 CFR 50.72 Notification.

Flux/Flow Imbalance Trip:

On March 17, while in cooldown mode, a

reactor trip signal was generated due to flux/flow imbalance. This trip

occurred when operators stopped RCP 381 due to high vibration. The STAR

module sensed zero flow in RCP loop B, and initiated the trip as

designed. Operators were not aware of this design feature of the

recently installed STAR module. The fact this trip signal was generated

indicates there was inadequate training on and knowledge of a recently

modified system. At the time of this trip, the trip breakers had been

reset, but rods had not been pulled.

3.2

Assessment of Licensee Management Performance

Management oversight was extensive for the planned electrical system

test. Both the Plant Manager and the Engineering Manager were on-site

for the pre-job briefing and the conduct of the test.

The inspector

attended all team meetings following the trip and was able to directly

observe the decision-making process at each meeting.

Management provided clear direction to the operators throughout the

event. Operations personnel were involved and consulted in all decision

making.

Management was especially effective in three areas:

Assembling and Controlling Additional Resources: Bringing in and

controlling additional personnel, while coordinating with the shift

crew, relieved the shift crew of that responsibility. As a result, the

shift crew was able to properly focus on the plant conditions and

evolutions. Several maintenance and engineering disciplines were

already on-site during the test, and others were contacted and scheduled

as needed.

Secondary System Cleanup: The Chemistry Manager and other chemistry

personnel were brought in shortly after the displaced resin was

identified. This resulted in an accurate assessment of the extent of

the resin dispersion and an effective cleanup. This was effective as

evidenced by the prompt assessment that powdered resin had been

ENCLOSURE 2

7

dispersed throughout the Condensate Polishing System and alignment of

the feedwater system to minimize any further transport of resin to the

steam generators.

Chemistry management was also effective in recovery from the transient.

The secondary system was aligned to return water from the secondary

system to the condenser in order to remove residual resin from the

system using the condensate polishers. Soak and flush procedures were

also successfully used to remove residual resin from the steam

generators. Sampling results confirmed the success of both of those

actions. The inspectors reviewed analytical results for parameters

routinely used to monitor water quality in secondary system component:

and determined that the chemistry control parameters were quickly

returning to normal ranges and specifications as delineated in Chemistry

Manual 3.8. Chemistry management planned to continue the necessary

system cleanup actions in order to achieve normal secondary water

chemistry before restart of the unit.

Troubleshooting and Root Cause Determination: Management provided

excellent direction for quarantining, isolating, and preserving evidence

for the suspected components.

Even after the 3RLS1X relay was

identified as the probable cause, the troubleshooting effort continued

to investigate other possibilities. A Failure Investigation Process

(FIP) evaluation was used as the root cause and troubleshooting guide.

Special tests were designed and conducted to replicate the conditions of

the event which was suspected as producing the vibrations in the relay

panel.

These tests provided evidence that the relay was in fact passing

voltage and current for several milliseconds when the panel vibrations

were reproduced. As a result, the licensee preserved the condition of

the relay and was able to identify it as the clear root cause. After

replacing the relay with a bench-tested relay, the vibration-producing

test was rerun, and the new relay was not affected.

Bench testing

revealed the failed relay had contacts with out of tolerance gaps as

described in paragraph 2.3.

3.3

Assessment of SEIT Investigation

Shortly after the trip, licensee management considered the circumstances

of the trip and the possible relationship of the emergency power system

testing warranted an independent investigation through the SEIT proces..

The SEIT was assembled and arrived on-site during the morning of March

17.

The SEIT was chartered under a standard Duke Power Company charter

for such teams.

The charter included preparation of a sequence of

events (SOE), evaluation of the root cause, and providing short-term

(pre-startup) and long-term recommendations. The SEIT exited March 21

with preliminary findings and recommendations. The licensee agreed to

complete all short-term items prior to starting up Unit 3.

ENCLOSURE 2

8

The inspectors reviewed the SEIT's SOE and determined that it was

complete and accurate. The SEIT's SOE was in close agreement with the

Oconee post-trip report SOE and a SOE compiled by the inspectors.

The SEIT concurred with the Oconee root cause determination.

Recommendations provided by the SEIT adequately addressed the actions to

be taken prior to startup. The inspectors concluded that the SEIT was'

an effective process which provided additional confidence that the

licensee's on-site assessment, root cause and corrective actions were

thoroughly addressed.

4.0

EQUIPMENT PROBLEMS

(93702)

The post-trip review indicated that the safety-related systems had

worked as designed, with the exception of the relay that initiated the

event.

The licensee identified several equipment problems, and

adequately addressed them prior to plant startup. Some of the problems

were caused by the water hammer, while others were revealed during the

event but were not caused by it.

LP-40/41 Leakage:

When the operators attempted to place the LPI system

in operation in the DHR mode, the water level in the LDST began

decreasing. The operators determined that two closed manual valves,

(3LP-40 and 3LP-41) were leaking past their seats.

This allowed LPI

pump discharge to recirculate back to the BWST. The valves were

manually tightened approximately one turn in the shut direction, and the

leakage from the LPI system stopped. The licensee believes the previous

alignment of these valves did not fully seat them in the shut position.

The valves are located in difficult positions for manual operation, and

the previous positioning may not have fully shut the valves. The

licensee checked the position of the same valves on Unit 1 and Unit 2

and found no problems. A Past Operability evaluation will determine if

the valves' position would have constituted an operability concern

during a hypothetical LOCA event.

Heat Exchanger Seal Failures:

The pumps in the Condensate System are

normally started with their discharge isolation valves shut to prevent

flow-induced pressure surges. During this event, the pumps were stopped

and restarted in rapid succession without normal system startup

alignments. This resulted in rapid flow decreases and pressure drops,

followed immediately by rapid flow increases and pressure increases.

Several sections of the Condensate System have long vertical runs which

are especially susceptible to water hammer effects. The water hammers

created intense, short-lived pressure spikes throughout the system. The

pressure spikes resulted in blown seals and gaskets in several heat

exchangers.

Water was observed leaking from the Generator Stator Cooler

and the Generator Hydrogen cooler. All gaskets were replaced and leak

checked.

ENCLOSURE 2

9

Water Hammer Damage To Safety-Related Components:

The licensee walked

down the Feedwater System and the Emergency Feedwater System and did not

find evidence of any damage. The licensee concluded that the water

hammer was limited to the Condensate System and the heat exchangers in

that system.

Unexpected Recloser Operation: Two 230 KV transmission lines running

between the Jocassee switchyard and the Oconee switchyard connect to the

Yellow bus through circuit breakers 12 and 15.

These circuit breakers

were equipped with a recloser programmed for one reclosing at two

seconds.

For all previous times that Periodic Test 0/A/0610/22 was

conducted, the procedure called for blocking the recloser during the

test. For the March 16 test, the procedure had been revised to remove

that particular step.

Plant engineers, based on review of the control

circuit diagrams, thought that the recloser would not generate a reclose

signal during the test. It appeared that the synchrocheck relay within

the recloser would not allow reclosing to a dead bus.

What actually

took place during the March 16 test was that the "switchyard isolate"

signal initiated-a-trip signal to breakers 12 and 15 (among other

breakers).

The Yellow bus became isolated as designed. Two seconds

following the trip signal, breakers 12 and 15 reclosed and immediately

tripped due to the permanent trip signal from "switchyard isolate."

When breakers 12 and 15 closed, the "switchyard isolate complete" signal

was interrupted. This reset a timer, which caused breaker 9 to close at

10.5 seconds rather than the programmed 8.5 seconds. This additional

two-second delay in establishing emergency power was not significant in

that the accident analysis time was not exceeded. As a result of this

information obtained from the periodic test, the licensee initiated the

following three corrective actions:

All recloser circuits at the Oconee switchyard would be corrected

such that they would operate as shown on the drawings (i.e., not

reclose to a dead bus).

As an interim measure, the reclosers for breakers 12 and 15 were

disabled.

If necessary, a modification will be implemented to block the

reclosing upon a "switchyard isolate" signal.

As far as could be determined during the inspection, the recloser

problem existed since initial plant startup.

It represents a problem

because the actual operation of the circuit was different than shown on

the drawing. The inspector concluded that there was no opportunity for

the licensee to identify the problem prior to conducting the periodic

test in its latest form.

Automatic Fast Transfer of RCPs:

Circuit breaker control circuits

included an automatic fast transfer of the reactor coolant pumps from

ENCLOSURE 2

10

the unit auxiliary transformer to the startup transformer upon a

generator trip. This feature created a potential problem in relation to

one scenario. The scenario of concern was when there is an External

Grid Trouble Protection System actuation, but not a unit trip. This

results in the 230 KV Yellow bus being energized from a hydro unit

(Keowee) and isolated from any other buses.

The reactor coolant pumps

would be powered from the main generator through the unit auxiliary

transformer. Should a unit trip occur from this configuration, a fast

transfer of the reactor coolant pumps to the Yellow bus would take

place. This is a transfer between two unsynchronized buses not

supervised by a synchrocheck relay. Therefore, an out-of-phase transfer

must be assumed. This could result in high transient current, which

could result in saturation of current transformers in the startup

transformer differential protection. This would result in lockout of

the startup transformer, as well as a loss of off-site power and one

path for emergency power. The Abnormal Operating Procedures include a

step to place the breaker mode selector switch in manual upon a

"switchyard isolate" alignment, thus blocking the fast transfer

described above. Nevertheless, this leaves a time period of

vulnerability (perhaps 5 minutes) which was a concern. The licensee

stated that they identified this same concern and a plant modification,

aimed at automatically blocking the fast transfer of the reactor coolant

pumps whenever a "switchyard isolate" signal is present, had been

approved. The inspector noted this modification (identified as NSM

2983) was on the three-year schedule. It was scheduled for the Unit 3

March 1998 outage, the October 1998 Unit 1 outage, and the March 1999

Unit 2 outage. The inspectors expressed to licensee management that they

should consider expediting the schedule for this modification, because

it had greater safety significance than indicated by the present

schedule.

5.0

CONFIRMATORY ACTION LETTER AND PRE-STARTUP REQUIREMENTS (92703)

On March 18, 1996, the Regional Administrator for NRC Region II issued a

Confirmation of Action Letter (CAL) to the Licensee. The CAL delineated

the following conditions and actions to be taken by the licensee prior

to restart of Oconee Unit 3.

Conduct a comprehensive investigation to evaluate equipment and

personnel response of the trip event, including a detailed

evaluation of the root cause of the event.

  • Complete

the investigation by the SEIT. Evaluate the findings of

the Oconee staff including the SEIT and implement appropriate

corrective actions.

Conduct a walkdown of Keowee systems verifying that the present

alignment is appropriate to supply emergency power to all three

Oconee Units. Notify NRC before using Keowee in a manner that

ENCLOSURE 2

11

will decrease the reliable supply of emergency power to Oconee.

This includes operating with both Keowee hydro units to the grid.

Verify the Lee Steam Station is available to provide electric

power to Oconee on short notice, and notify NRC of any subsequent

change in its availability.

Meet with the NRC to discuss the results of the above items,

including a discussion of future Keowee testing plans. Obtain

concurrence from the Regional Administrator prior to entering

Mode 2.

The inspectors confirmed full compliance with the provisions of the CAL.

On March 22, the Regional Administrator.and members of his staff met

with the licensee at Oconee Nuclear Station. At the meeting, the

licensee provided a briefing on the status of Unit 3, details of the

SEIT findings, and discussed the root cause. All remaining items

required for startup were listed and presented at the meeting.

Following the meeting, the inspectors reviewed the licensee's completion

of all required items and confirmed their satisfactory completion. As a

result of the NRC review of the licensee's conformance with the CAL, and

completion of all required startup items, the Regional Administrator

approved closure of the CAL and startup of Oconee Unit 3 on March 25,

1996.

The unit was restarted later that day.

The licensee submitted to

NRC a letter, Response to Oconee Unit 3 Confirmation of Action Letter,

dated March 25, 1996. This letter detailed the compliance with the CAL.

As part of the inspection effort to ensure completion of the CAL items,

the inspector reviewed the licensee Post Trip Review Report. The report

independently identified the root cause, and listed the corrective

actions required prior to unit startup. The report was accurate and

comprehensive. All required actions were completed.

6.0

UFSAR REVIEW

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for additional

verification that licensees were complying with UFSAR commitments.

During an approximate two month time period, all reactor inspections

will provide additional attention to UFSAR commitments and their

incorporation into plant practices, procedures and/or parameters.

While performing the inspections which are discussed in this report the

inspectors reviewed the applicable portions of the UFSAR that related to

the areas inspected. The inspectors verified that the UFSAR wording was

consistent with the observed plant practices, procedures and/or

parameters.

ENCLOSURE 2

12

7.0

EXIT MEETING

The inspection scope and findings were summarized on March 27, 1996, by

P. Harmon with those persons indicated by an asterisk in paragraph 1.

The inspector described the areas inspected and discussed in detail the

inspection results. A listing of inspection findings is provided.

Proprietary information is not contained in this report.

Dissenting

comments were not received from the licensee.

Item Number

Status

Description and Reference

VIO 269,270,289/

Open

Failure to Make Proper 10 CFR 50.72

96-05-01

Notification

8.0

ACRONYMS

ACB

Air Circuit Breaker

ALARA

As Low As Reasonably Achievable

BHUT

Bleed Holdup Tank

BTO

Block Tagout

BWST

Borated Water Storage Tank

CAL

Confirmation of Action Letter

CFR

Code of Federal Regulations

CC

Component Cooling

CCW

Condenser .Circulating Water

CR

Control Room

DBA

Design Basis Accident

DHR

Decay Heat Removal

EFW

Emergency Feedwater

EPSL

Emergency Power Switching Logic

EOC

End Of Cycle

ES

Engineered Safeguards

FDW

Feedwater

FIP

Failure Investigation Process.

GL

Generic Letter

GPM

Gallons Per Minute

HP

Health Physics

HPI

High Pressure Injection

ICS

Integrated Control System

I&E

Instrument & Electrical

IR

Inspection Report

KHU

Keowee Hydro Unit

KV

Killovolts

LCO

Limiting Condition for Operation

LDST

Letdown Storage Tank

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

ENCLOSURE 2

MDEFW

Motor Driven Emergency Feedwater

MPManeac

Prcdr

MVAMillion Volts-Amps

MWMegawatts

NCVNon-Cited Violation

NLCNon-Licensed Operator

NSMNuclear Station Modification

NSDNuclear System Directive

EPOperating Experience Program

ONSOconee Nuclear Station

PSIDPounds Per Square Inch Differential

PSIGPounds Per Square Inch Gauge

PMPreventive Maintenance

PIPProblem Investigation Process

RCPReactor Coolant Pump

RCSReactor Coolant System

REMRoentgen Equivalent Man

RPSReactor Protection System

RFORefueling Outage

SEITSignificant Event Investigation Team

SOERSignificant Operating Event Report

SFPSpent

Fuel Pool

Senior Reactor Operator

Technical Specification

Updated Final Safety Analysis Report

RaWork Control Center

R

iWork

Order

ENCLOSURE 2

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