ML15118A136

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Insp Repts 50-269/96-10,50-270/96-10 & 50-287/96-10 on 960602-0713.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering,Plant Support,Plant Status & Review of UFSAR Commitments
ML15118A136
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 08/12/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A134 List:
References
50-269-96-10, 50-270-96-10, 50-287-96-10, NUDOCS 9608230086
Download: ML15118A136 (21)


See also: IR 05000269/1996010

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270, 50-287, 72-04

License Nos:

DPR-38, DPR-47, DPR-55, SNM-2503

Report No:

50-269/96-10, 50-270/96-10, 50-287/96-10

Licensee:

Duke Power Company

Facility:

Oconee Nuclear Station, Units 1, 2 & 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

June 2 - July 13, 1996

Inspectors:

P. Harmon, Senior Resident Inspector

G. Humphrey, Resident Inspector

N. Salgado, Resident Inspector

N. Economos, Reactor Inspector

L. King, Reactor Inspector

L. Stratton, Safeguards Inspector

Approved by:

R. V. Crlenjak, Chief, Projects Branch 1

Division of Reactor Projects

ENCLOSURE 2

9608230086 960812

PDR ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2 & 3

NRC Inspection Report 50-269/96-10,

50-270/96-10, 50-287/96-10

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a 6 week

period of resident inspection; in addition, it includes the results of

announced inspections by two regional inspectors. A Safeguards inspector

provided closure for an open item and the Project Manager provided information

for an engineering issue.

Operations

Unit 2 experienced a dropped rod which required a power reduction

to 55%, and the resetting of the High Flux Trip setpoints and the

Flux/Flow/Imbalance trip setpoints. Maintenance technicians did

not reset the Flux/Flow/Imbalance trip setpoints within the 4

hours required by Technical Specifications. This was identified

as Violation 50-269,270,287/96-10-01.

(Section 01.2)

Maintenance

Technicians performing surveillance activities on the

nonsafety-related Component Cooling Water system did not follow

the step sign-off process required by the procedure. This was

identified as a weakness in the use of and adherence to

procedures. (Section M1.2)

-

The present Inservice Testing program and procedures at Keowee are

adequate to perform the required testing. The implementation of

the modification for the turbine guide bearing oil system will

allow increased testing for that system. (Section M1.3)

-

The inspector concluded that failure to perform inspection of

activities affecting quality by individuals other than those who

performed the activity was a violation of 10 CFR 50, Appendix B,

Criterion X requirements. Violation 50-269,270,287/96-10-03:

Weld Procedure Qualifications Welded, Tested, Certified and

Approved By Same Individual, was identified. (Section M1.5.3)

Engineering

The licensee's evaluation of the hydrogen ignition during the

welding of a dry cask storage canister at Point Beach as it

related to ONS was considered a strength.

(Section E1.1)

A minor violation concerning the licensee's failure to request

relief for Oconee Units 1, 2, and 3 Reactor Vessel Weld WR35 was

identified as Non-Cited Violation 50-269,270,287/96-10-02: Failure

To Request Relief. (Section E3.1)

ENCLOSURE 2

Plant Support

-

The inspector concluded that the licensee conducted emergency

response drill 96-02 professionally and thoroughly.

(Section Pl)

At the licensee's corporate office, the inspector reviewed

corrective actions relative to the finding that the licensee

allowed a vendor to continue to implement their access

authorization program after determining the vendor failed to

provide assurance that the individuals granted unescorted access

were trustworthy and reliable. Corrective actions were timely and

included a.complete audit of the vendor's records and program.

Arrangements have been made to audit the licensee's Access

Authorization Program by the Regulatory Audits group beginning

October 28, 1996.

(Section Si)

0

ENCLOSURE 2

Report Details

Summary of Plant Status

Unit 1 operated at or near full power throughout the reporting period.

Unit 2 operated at or near full power until July 6, 1996, when the unit

reduced power to 55% in response to a dropped control rod (paragraph 01.2).

The unit was returned to full power at 5:30 a.m. on July 7, 1996.

Unit 3 operated at or near full power throughout the reporting period.

Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner contrary

to the Updated Final Safety Analysis Report (UFSAR) description highlighted

the need for a special focus review that compares plant practices, procedures,

and/or parameters to the UFSAR descriptions. While performing inspections

discussed in this report, the inspectors reviewed the applicable portions of

the UFSAR that related to the areas inspected. The inspectors verified that

the UFSAR wording was consistent with the observed plant practices,

procedures, and/or parameters. As addressed in Section M2.1, Reactor

Protection System testing frequency differences were identified between the

Technical Specifications and the UFSAR.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general the conduct of

operations was professional and safety-conscious; specific events and

noteworthy observations are detailed in the sections below.

01.2 Dropped Control Rod On Unit 2

a. Inspection Scope (93702)

On July 6, 1996, at 2:10 a.m., Unit 2 control rod 3 in Group 7 dropped

approximately 18% into the core as displayed on the position indication.

The inspector interviewed operators and technicians, reviewed control

room logs, procedures, and associated Technical Specifications (TS).

SII

b. Observations and Findings

At 3:20 a.m. the control rod dropped into the core while the licensee

was attempting to manually realign the rod with its group. The licensee

entered abnormal procedure AP/2/A/1700/15, Dropped Control Rods.

Power

was reduced manually to 55 percent by the Operators in a controlled

manner. TS 3.5.2.2.d required in part that the nuclear overpower trip

setpoints based on flux and flux/flow/imbalance be reduced to 65.5

percent within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the power reduction. The licensee reduced the

setpoints associated with the flux. The licensee discovered at 12:15

p.m. that the flux/flow/imbalance setpoints had not been reduced. The

licensee notified the NRC as required by 10 CFR Part 50.72 that Unit 2

had entered TS 3.0.3 after failing to reset the flux/flow/imbalance

setpoints within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of dropping the control rod. The licensee's

failure to meet the requirements of TS 3.5.2.2.d is being identified as

Violation 50-270/96-10-01, Failure To Change Flux/Flow Imbalance

Setpoint.

The licensee identified that the rod dropped because of a blown fuse on

one of the six phases of the control rod drive stator. The licensee

replaced the blown fuse and verified that the control rod drive stator

was functional.

Unit 2 was returned to full power at 5:30 a.m., on July

7, 1996.

c. Conclusions

The inspector concluded that the licensee was in violation of TS 3.5.2.2.d, and identified Violation 50-270/96-10-01, Failure To Change

Flux/Flow/Imbalance Setpoint.

02

Operational Status of Facilities and Equipment

02.1

Engineered Safety Feature System Walkdowns (71707)

The inspectors used Inspection Procedure 71707 to walkdown accessible

portions of the following safety-related systems:

Keowee Hydro Station

Low Pressure Injection System

Emergency Feedwater System

Spent Fuel Pool

Equipment operability, material condition, and housekeeping were

acceptable in all cases. Several minor discrepancies were brought to

the licensee's attention and were corrected. The inspectors identified

no substantive concerns as a result of these walkdowns.

ENCLOSURE 2

3

08

Miscellaneous Operations Issues (92901)

08.1

(Closed) VIO 269,270,287/94-38-01: Failure to Follow Keowee Transfer

Procedure

On December 11, 1994, Keowee Hydro Unit 1 was not operated in accordance

with OP/0/A/1106/019, Keowee Hydro at Oconee, Enclosure 3.4, in that

operational control of the hydro unit was transferred from remote to

local (using OP/O/A/2000/041, Keowee Modes of Operation) with the unit

operating at speed-no-load conditions instead of being shutdown. The

transfer of control with the unit operating at speed-no-load conditions

resulted in overheating the generator field breaker closing coil and a

loss of excitation to the operating hydro unit. Keowee procedure

OP/0/A/2000/041 did not contain steps to transfer control using the

remote/local switch. Therefore, the Keowee Hydro Operator had no written

instructions to shutdown the operating hydro unit prior to transferring

control from remote to local.

The inspector verified that Keowee procedure OP/0/A/2000/041 was revised

to give Keowee operators instructions which would prevent control

transfer while the Keowee unit was operating. The inspector also

verified that OP'n/A/1106/019 was revised to provide guidelines for

control transfers. The Keowee operators were trained on the revisions

made to OP/O/A/2000/041, specifically, remote to local transfers. This

item is closed.

II. Maintenance

Al

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62703)

The inspectors observed all or portions of the following maintenance

activities:

W096041837

3CCW-11 Perform Mech/Ele PM on Operator

Limitorque-Preventative Maintenance

ON3IPA0305001

RPS Chan B Pump PWR Monitor Calibration

IP/0/A/0310/012B Engineered Safeguards System Logic Subsystem 1

LPI Channel 3 Online Test

IP/O/A/0310/013B Engineered Safeguards System Logic Subsystem 2

LPI Channel 4 Online Test

ENCLOSURE 2

4

S WO 96025532

RPS Channel D Pump Power Monitor Calibration

-

WO 95045276

NSM-32881 Part D, Replace Power Battery Chargers

-

PT/1/A/2200/019

KHU-1 Turbine Sump Pump IST Surveillance

-

WO 96000002

U-2, LPSW To RCPM, LPI, RB Component Cooler

Calibration

b. Observations and Findings

The inspectors found the work.performed under these activities to be

professional and thorough. All work observed was performed with the

work package present and in active use. Technicians were experienced

and knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

c. Conclusion

The inspectors concluded that the Mainterance activities listed above

were completed thoroughly and professionally.

M1.2 Unit 2 Condenser Circulating Water (CCW) Pump B Rotameter and Flow

Switch, W096040910

a. Inspection Scope

On June 11, 1996, the inspector observed calibration of the flow switch

on the lube water to the 2B CCW Pump.

b. Observations and Findings

Calibration procedure IP/O/B/0261/004, Enclosure 11.2.2.b, CCW Pump B

Rotameter and Flow Switch, was being utilized to perform the

calibration. However, the inspector observed multiple steps being

signed off when he approached the technicians. In addition, the

inspector noted that the last step which was signed off was in advance

of performing the activity specified in that step (step 10.2.22.c,

Isolation Valve).

The inspector questioned the technicians regarding signing off multiple

steps. The individuals told the inspector that they believed that the

nonsafety-related procedure did not specifically require the steps to be

signed off one at a time as they were completed.

The equipment being calibrated was not safety-related, but the licensee

confirmed that management's expectations for performing this work were

'the same as for safety-related equipment. That is, the steps are to be

ENCLOSURE 2

signed off as they are performed. The technicians were counseled by

their supervisor on adherence to procedures.

c. Conclusion

The inspector concluded that a failure to maintain current documentation

of the steps performed indicated a weakness in procedure adherence.

M1.3 Conduct of IST Program At Keowee Hydro Station

a. Inspection Scope

The inspector reviewed the licensee IST program that was applicable to

the Keowee generating station. The licensee's submittal of the IST

program was reviewed to ensure that all of the critical components that

are applicable were included in the program and that where differences

to ASME Section XI existed that justification for the differences was

included in the submittal. The temporary and periodic tests were also

reviewed. PIPs that were written on the system were reviewed to

determine if there were any equipment failures.

b. Observations and Findings

All of the critical equipment for Keowee was listed for testing in the

IST program with the exception of skid mounted equipment. The skid

mounted equipment was tested under the Appendix B program. The licensee

had stated this in their IST program submittal.

A review of the temporary test procedures and the periodic tests

indicated that the applicable testing was being performed. The

licensee's testing to date has been performed using temporary test

procedures.

Periodic test procedures have been developed to replace the

temporary test procedures.

The licensee plans to modify the turbine guide bearing oil system so

that individual components can be tested. The inspector reviewed the

proposed modification drawings and periodic test procedure. The

inspector determined that the modification will allow testing of the

pumps and valves which is not possible under the present installation.

The modification is due to be installed in September 1996.

The inspector reviewed the completed quarterly tests for the fall of

1995 and the first quarter of 1996. No problems were identified. The

inspector reviewed three PIPs associated with the system. Corrective

action had been completed for the PIPs.

c. Conclusions

The present IST program and procedures are adequate to perform the

required testing. The implementation of the modification for the

ENCLOSURE 2

6

turbine guide bearing oil system will allow increased testing for that

system.

M1.4 Surveillance Observation (61726)

a. Inspection Scope

The inspector observed all or portions of the work activities required

in the following work orders:

Inspection Procedure

Title

IP/O/A/3000/001

Instrumentation and Control Battery

Daily Surveillance

IP/O/A/300/011

Instrumentation and Control Battery

Quarterly Surveillance

b. Observations and Findings

The inspector reviewed the above procedures to verify that requirements

specified in Technical Specification 4.6.9 and referenced in the subject

procedures were accurately delineated, that appropriate reviews had been

performed, that instruments and/or test equipment were appropriately

identified and calibrated. A pre-job briefing was held to discuss the

objectives of the activity and to review safety precautions while

working around the cells. The surveillance was performed in a careful

and unhurried manner following procedural instructions. Each cell was

checked for evidence of corrosion and degradation around the terminals.

Each cell was tested for voltage, specific gravity, temperature and

electrolyte level.

Data from each cell was documented in the

appropriate enclosure provided in the procedure. Technicians were

qualified to perform their task with training received under the

licensee's training and qualification system. The surveillance was

conducted in a well-planned and orderly manner following procedural

requirements.

M1.5 Maintenance Observation (62703)

M1.5.1

Replacement Mechanical Operator for Valve CCW-267

a. Inspection Scope

This work effort was performed to replace the operator on valve CCW-267

which was discovered broken in the conduct of a system pump test on

June 3, 1996.

b. Observations and Findings

The valve was identified as a QA-1 condition active valve, that ensures

Safe Shutdown Facility (SSF) Auxiliary Service Water System (ASW) pump

minimum flow requirements are met. This valve is also used to isolate

ENCLOSURE 2

7

Flow through the SSF, ASW test line at the start of a SSF event to avoid

diverting flow away from the Steam Generators (S/Gs).

The work was performed as minor modification No. OE-9246 under Work

Order No. 96046304-01. The maintenance procedures (MP) used to perform

the task of removal and replacement were MP/O/A/1800/005, Torque

Miscellaneous Fasteners and MP/O/A/1210/007, Operator Limitorque-SMB/SB

Series Removal and Replacement. This valve appears on flow Diagram No.

OFD 133A-2.5 (J-11) Rev. 25. Because an exact replacement of the

original manual actuator (Model B320-40) was not available, the licensee

used a similar actuator (Model B320-50) made by the same manufacturer

(Limitorque).

The inspector reviewed the above mentioned documents including the

replacement evaluation, the unreviewed safety question evaluation

(10 CFR 50.59), and the Problem Investigation Process (PIP) Report No.

4-096-1101 dated June 3, 1996. The inspector observed disassembly of

the broken actuator, inspected the broken parts and the replacement

component following installation. By review of the work package and

through discussions with cognizant QA personnel, the inspector verified

that QC inspections were performed during the reassembly as required,

and that a post-maintenance functional test showed the valve was

operational.

M1.5.2 Spent Fuel Canister Closure Weldment Welder Performance Qualification

a. Inspection Scope

To observe the conduct of welder performance qualification test to

assure compliance with ASME Code Section IX, Regulatory and Procedure

Requirements.

b. Observation and Findings

At the time of this inspection, the licensee was in the process of

requalifying a welder to weld the closure joint on a spent fuel

canister. The test was being conducted using the machine gas tungsten

arc welding process with remote visual control to the requirements of

Field Weld Data Sheet, No. L-165B Rev. 1. Within these areas, the

inspector checked the power supply unit, and the wire feed equipment and

the remote visual control console for physical condition, operability,

and evidence of calibration as applicable. The test was performed on a

3/8" plate in the flat 1G position. Joint contour involved a typical 37

1/2 degree open groove with backing. During the test, the inspector

observed filler metal deposition over several passes and verified that

the weld was being fabricated within the essential variables of QW-360,

ASME Code,Section IX and the parameters of FWDS L-165B, Rev. 1. Also,

through observation and discussion with the welder being requalified,

the inspector determined that he had adequate knowledge and expertise

with the process and technique to requalify successfully. Following the

close of this inspection, the individual monitoring the test and

responsible for evaluating the test coupons for integrity provided the

ENCLOSURE 2

8

inspector with a copy of the performance qualification record showing

that the welder had passed requalification requirements.

M1.5.3 Review of Weld Procedure Qualification Records

a. Inspection Scope

The inspector reviewed weld procedure and associated Field Weld Data

Sheet qualification records to verify compliance with ASME Code Section

IX, Regulatory and Procedural requirements.

b. Observation and Findings

PIP NO. 0-095-1409 was written to document a concern over the apparent

lack of independent inspections in the conduct of welding procedure

qualifications. In this regard, the inspector ascertained that the

problem as described in the subject PIP involved a review of the

licensee's welding procedure qualification record L-137D. The

inspector's review of this qualification record showed that the

individual who qualified the process did the brazing, tested the coupons

for code acceptance, certified the results as meeting code requirements,

and approved the procedure. In addition, the inspector noted that the

above mentioned PIP identified additional examples of weld procedure

qualifications where the same individual had performed a number of the

activities described above during the qualification process. Following

are examples where this same individual performed a number of activities

and functions during the qualification process.

L-129D

L-131D

L-133D

L-134D

L-137D

Weld\\Braze Test

A

A

A

A

A

Test Coupons

A

A

A

A

A

Certify Results

A

B

B

B

A

Approve Procedure

A

B

B

B

A

Qualify Process

A

A

A

A

A

QA Review

B

A

A

A

B

By review of the organizational chart the inspector ascertained that

both individuals (A and B) work in the same organization, the metallurgy

laboratory. Both individuals work for the same supervisor and are

essentially charged with similar tasks which suggests a lack of

independence between two separate functions, welding and inspections.

In discussing this issue with site mechanical maintenance and safety

assurance managers, the inspector expressed concern over the adequacy of

the welding program as implemented by Procedure L-100, Rev. 13, in that

it does not preclude the same individual from performing in the role of

a craft/welder, a QC inspector, a QA reviewer, and a certifier of his

own work. The licensee's cognizant engineer indicated that an

investigation of this practice was being pursued through the PIP process

and that a decision was expected to be reached by July 1, 1996. In

conclusion, the inspector stated that failure to perform inspection of

activities affecting quality by individuals other than those who

ENCLOSURE 2

9

performed the activity was a violation of 10 CFR 50, Appendix B,

Criterion X requirements. Violation 50-269,270,287/96-10-03: Weld

Procedure Qualifications Welded, Tested, Certified and Approved by same

Individual, was identified.

M1.5.4 Steam Generator (S/G) Tube Maintenance: Eddy Current Examination

Results, Unit 2 (73755)

a. Inspection Scope

Through discussions with cognizant personnel and by review of eddy

current examination records the inspector ascertained inspection results

and corrective actions taken by the licensee before returning both S/Gs

to service. The following table depicts a summary of the number of

tubes examined, the type of examination performed, and corrective

actions taken.

The numbers in parentheses represent the original work scope quantities

planned or estimated:

Activity

A H/L

A C/L

B H/L

B C/L

1. MRPC 1-690 plugs - 20

54

0 (35)

78

0 (40)

H/L (orig. included

c/1 baseline)

2. MRPC Lane/Wedge

227

N/A

222

N/A

3. Bobbin/Plus Pt. sleeves

278/57(278)

N/A

266/54(266) N/A

(all 1-690) (orig.

included plus Pt. all)

4. Re-expanded rolls

0

2

1

1

5. 0.510 Bobbin (100%)

15,393

15,263

coil probe

6. MRPC special interest

1213 (680)

2124(1094)

tubes

7. Plug removal

none

none

8. Tubes plugged

199 (61)

213(65)

9. Tube Pulls

4 full length from 2A cold leg

A review of Unit 2 steam generator maintenance data on tubes plugged

following this outage (EOC-15) was as follows:

S/G

Tubes Plugged

% Of Tubes Plugged

Plug Limit Tubes Sleeved

2A

337

2.17%

10% max*

277

2B

481

3.10%

10% max*

261

  • The licensee is performing analysis to raise the plugging limit to 15%

per S/G.

ENCLOSURE 2

10

M1.5.5 S/G 2A Upper Head-to-Tubesheet Weld With Subsurface Flaw Indication

a. Inspection ObJective:

Provide a summary of the licensee's ISI examination findings in the

upper head-to-tubesheet weld No. 2-SGA-WG58-1, including disposition of

the indication identified and NRR's safety evaluation.

b. Discussion:

As required by the licensee's Third Ten Year interval examination,

inspection of the subject weld was performed during the 1996 EOC-15

refueling outage per ASME Code Section XI, 1989 edition requirements.

Examination of this weld was also performed during the two previous

intervals.

During the first interval, this weld was examined in 1982 during the

fifth refueling outage per ASME Code,Section XI, 1974 edition

requirements. The weld was re-examined during the second interval in

1990 during the eleventh outage per ASME,Section XI, 1980 edition

requirements.

Examination of the weld during the 1996 refueling outage led to the

identification of a subsurface ultrasonic indication that exceeded code

allowable size. The indication was located close to the midplane of the

weldment and measured 56 inches in length, 0.8 inches in depth, and was

located 3.8 inches from the outer and 3.9 inches from the inner weld

surface. Because the indication exceeded code allowable flaw size, the

licensee evaluated the indication under IWB-3600 and Appendix A code

requirements. This evaluation showed the weld was acceptable under IWB

3132.4, Acceptance by Analytical Evaluation. This paragraph references

IWB-2420 which requires re-examination of the flaw during the next three

inspection periods for monitoring for possible growth. On May 2, 1996,

the licensee communicated this finding and analytical results by

telephone to NRR who indicated that as required by IWB-3134, details of

the evaluation and analysis had to be submitted for their review and

approval before the plant could resume operations. On May 3, 1996, the

licensee submitted the requested information to NRR who reviewed and

accepted the evaluation and analysis as the basis for continued

operation with the proviso for re-examination of the weld as required by

the code.

M2

Maintenance Procedures and Documentation

M2.1 Testing of the Unit 2 Reactor Protective Channels

a. Inspection Scope (61726)

The inspectors reviewed Section 7.2, Reactor Protective System (RPS), of

the FSAR which requires that RPS Channel A be electrically trip tested

for every input up to and including the channel trip relay within one

ENCLOSURE 2

11

week of unit-startup. It further required that the B, C, and 0 channels

be tested consecutively within the following 45 day periods.

b. Observations and Findings:

The inspectors questioned the licensee as to how this requirement was

met after the Unit 2 Refueling Outage was completed and returned to

service on May 7, 1996. In response, the licensee informed the

inspectors that the sequence of testing the RPS channels was not

performed as outlined in the FSAR. The A channel was not tested within

the one week requirement as specified in the FSAR. Channel A was tested

on June 13, 1996, under the requirements specified in WO 96043107.

The TS was changed by Amendment No. 199 to Facility Operating License

DRP-38, Amendment No. 199 to Facility Operating License DPR-47, and

Amendment No. 196 to Facility Operating License DRP-55 to require that

the testing for each RPS channel be performed within a time period not

to exceed 45 days but not in a particular sequence. The TS change was

approved and received by the licensee on April 13, 1996.

Although the FSAR had not been changed, a proposed change that

incorporated the TS amendments had been prepared and was scheduled to be

presented to the NRC on June 30, 1996.

c. Conclusion:

The inspectors concluded that the licensee's effort to review and update

the FSAR was acceptable for the issue identified.

M8

Miscellaneous Maintenace Issues (92902, 90712)

M8.1

(Closed) VIO 269/94-28-01: Failure To Follow Procedure (Breaker

Installation)

On September 12, 1994, during the performance of TN/1/A/2881/0/DL1, step

8.8.10, which required that internal wiring of the replacement breaker

assembly be verified by performing a meg ohm (continuity) check between

the conductors, was not performed prior to installing breaker 1XO-F1AT

in motor control center 1XO. The breaker leads had been inadvertently

reversed during the modification process and this resulted in the loss

of MCC 1XO when the breaker compartment stabs contacted the bus bars due

to a phase to phase short. Loss of 1XO resulted in the loss of the

majority of the Unit 1 radiation monitors, as well as pressurizer spray

control.

The inspector verified the corrective actions described in the

licensee's response letter, dated November 17, 1994, to be reasonable

and complete. This violation is closed.

M8.2 (Closed) LER 269/94-05: Containment Isolation Valve Technically

Inoperable.

This event was discussed in NRC Inspection Report 50-269,270,287/94-32

and was dispositioned as Non-Cited Violation 50-269/94-32-02, Inoperable

ENCLOSURE 2

12

Containment Isolation Valve Due To Maintenance Error. Accordingly, this

LER is closed.

M8.3

(Closed) LER 287/94-01: Reactor Trip On False High Level Indication Due

To Equipment Failure.

This LER describes the reactor trip that occurred on March 1, 1994, when

a defective heater drain tank level switch caused a false high drain

tank level signal to be generated. The resulting transient and the

licensee's corrective actions were addressed in detail in Inspection

Report 50-269,270,287/94-08. As corrective actions were considered

appropriate, this LER is closed.

III. Engineering

El

Conduct of Engineering (37551, 37550)

E1.1 Hydrogen Accumulation During the Welding of a Spent Fuel Canister

a. Inspection Scope

The inspector reviewed the licensee's actions in response tu Information

Notice 96-34, Hydrogen Gas Ignition During Closure Welding Of A VSC-24

Multi-Assembly Sealed Basket.

b. Observations and Findings

The licensee performed an evaluation, Calculation OSC - 6580, to

determine the amount of hydrogen that would be generated when welding

the lid on the canisters that are utilized to store spent fuel in the

ONS ISFSI.

This evaluation was in response to the combustible gas burn

at Point Beach Nuclear Plant when a welder began welding the lid to the

canister. The ONS canisters have an aluminum coating inside whereas the

canister at Point Beach was coated with a Carbo Zinc-11 material.

The results of the ONS evaluation revealed that the "worst case"

hydrogen yields at ONS could reach 1.7 volume percent, but nominally

would not exceed 0.26 volume percent for the ONS equipment. A second

calculation utilizing the Carbo Zinc-11 coated spent fuel canisters like

those utilized at Point Beach revealed that a volume of 40.80 percent

could be obtained. Based on this calculation, the licensee determined

that the corrosion of aluminum was not enough to generate sufficient

hydrogen during the time period of concern to reach the lower

flammability limit for hydrogen even for the most conservative case.

Actual measurements were made during welding of canister #37 which

revealed a hydrogen content of 2.05 volume percent. Although this

amount is less than the lower flammability limit, the licensee is

further evaluating the source of the hydrogen.

ENCLOSURE 2

c. Conclusion

13

The licensee's actions in taking a proactive role in evaluating the

Point Beach Incident as it related to ONS was considered a strength.

E3

Engineering Procedures and Documentation

E3.1

Failure to Reauest Relief

The project manager identified that the licensee had not requested

relief related to the Reactor Pressure Vessel Circumferential Head Weld

on Units 1, 2, and 3 since at least the beginning of the Second

Inservice Inspection Interval.

Section XI of the ASME Code Examination

Category B-A, Item B1.21, requires 100% volumetric examination of

accessible length of one circumferential head weld as defined by Figure

IWB 2500-3. The licensee did not meet the requirements of TS 4.2.1

which states that inservice examination of ASME Code Class 1, 2, and 3

components shall be performed in accordance with Section XI of the ASME

Boiler and Pressure Vessel Code and applicable addenda as required by 10

CFR 50, Section 50.55a(g)(4), to the extent practicable within the

limitations of design, geometry and materials of construction of the

components, except where specific written relief has been granted by the

Commission. The licensee is in the process of requesting relief for

Oconee Units 1, 2, and 3 Reactor Vessel Weld WR35. This failure

constitutes a violation of minor significance and is being treated as a

Non-Cited Violation consistent with Section IV of the NRC Enforcement

Policy.

This issue will be identified as NCV 50-269,270,287/96-10-02,

Failure To Request Relief.

E8

Miscellaneous Engineering Issues (92903, 90712)

E8.1

(Closed) LER 50-269/94-01, Seismic/LOOP Event May Result In The Loss Of

Post Accident Cooling Due To Design Deficiency

The licensee identified on December 30, 1993, during a walkdown of the

CCW System, 4 valves on Units 1, 2, and 3 that did not appear on the CCW

flow diagrams. The valves and some instrument tubing were located near

buoyancy restraints on the system. Due to the potential for interaction

during a seismic event, an operability evaluation was performed. The

results of the evaluation revealed that these valves could be sheared

and result in the system becoming inoperable due to the intake of air at

the interface points. This intake of air could be sufficient to defeat

the siphon mode of operation during a loss of offsite power (LOOP).

An investigation into the situation revealed that the buoyancy

restraints were installed on July 18, 1991, October 14, 1992, and June

22, 1992, for Units 1, 2, and 3, respectively. The evaluation

determined that air leakage could be sufficient to cause the loss of

siphon effect and therefore the units would have been inoperable since

the dates that the restraints were installed.

ENCLOSURE 2

14

The licensee implemented a minor modification to increase the clearance

between the buoyancy restraints and the instrument lines to reduce the

potential for failure with respect to a seismic event. In addition, the

valves were added to the flow diagram drawings. The inspector reviewed

the system and determined that the interferences in question had been

corrected. This LER is closed based on the licensee's efforts to

identify, report and correct the deficiency.

E8.2 (Closed) VIO 269,270,287/94-28-03: Corrective Actions Associated With

Turbine Bypass Valves Randomly Repositioning Not Adequate.

On August 10, 1994, the Unit 3 "B" steam generator was blown down to a

dry condition when the turbine bypass valves for that steam header

randomly repositioned following power restoration to the Integrated

Control Circuit module controlling the valves. The licensee had been

aware of the potential for this event for several months. However, the

preventive measures which were implemented were ineffective in

preventing the dryout event.

The licensee replaced the ICS modules with an equivalent module which

does not randomly reposition the bypass valves. The inspectors

confirmed that the new modules Were installed for -ll three Oconee units

on August 13, 1994. This item is closed.

E8.3

(Closed) Unresolved Safety Issue (USI) A-26:

Reactor Pressure Vessel

Pressure Transient Protection

The inspector reviewed the documentation and inspection efforts for USI

A-26, and concluded that the modifications had been completed and

documented in previous inspection reports. The final open item for this

USI was Inspector Followup Item 50-269,270,287-98-36-03, Revised Low

Temperature Overpressure (LTOP) System Operability. This IFI was closed

and documented in Inspection Report 50-269,270,287-91-31. This IFI was

considered closed based on implementation of Technical Specification 3.1.2.9, which specifies requirements for assuring operability of the

LTOP system. USI A-26 is closed.

IV. Plant Support Areas

P1

Conduct of Emergency Preparedness Activities

On June 26, 1996, the inspector observed portions of activities

associated with the licensee's emergency response drill 96-02. The

initiation of the drill scenario involved a S/G Tube Rupture in the 1A

S/G. An Alert was declared, and the technical support center (TSC) was

activated. The inspector observed activities with manning the TSC. The

inspector concluded that the licensee conducted the drill professionally

and thoroughly.

ENCLOSURE 2

15

Si

Conduct of Security and Safeguards Activities

a. Inspection Scope (TI 2515/127)

On April 25, 1991, the Commission published 10 CFR 73.56, Personnel

Access Authorization Requirements for Nuclear Power Plants, which

required licensees to fully implement their Access Authorization Program

(AAP) by April 27, 1992.

By letter dated July 1, 1994, the licensee

submitted Revision 0 to .the Catawba, McGuire, and Oconee Physical

Security Plans committing to the requirements of 10 CFR 73.56 and NRC

Regulatory Guide 5.66, Access Authorization Program for Nuclear Power

Plants.

The Nuclear Management and Resources Council (NUMARC) has published

NUMARC 89-01, "Industry Guidelines for Nuclear Power Plant Access

Authorization Programs," dated August 1989, which was adopted by NRC's

Regulatory Guide 5.66 as an Appendix. During an inspection of the

licensee's AAP conducted November 13-17, 1995, it was noted that for

approximately 11 months, the licensee allowed a vendor to continue to

implement their AAP after determining the vendor failed to assure that

individuals granted unescorted access were trustworthy and reliable. On

June 17, 1996, at the Duke Power Company Corporate Office, the inspector

reviewed the corrective actions implemented by the licensee in response

to this identified violation (VIO 50-269,270,287/95-24-02).

b. Observations and Findings

The licensee performed a 100 percent audit of the vendor's access

authorization records and program during the period of December 4-8,

1995, to confirm acceptability of the vendor's AAP. Three findings were

noted by the licensee with respect to three individuals granted

unescorted access prior to the completion of background investigations.

These three background investigations were completed during the audit.

No derogatory information was revealed. Additionally, the vendor

responded to these findings and delineated corrective actions in a

letter to the licensee dated December 14, 1995.

The licensee failed to have a procedure in place to audit small vendor

AAPs. The licensee developed "Procedure for Evaluating

Contractor's/Vendor's Access Authorization and Fitness For Duty

Programs," Revision 1, dated January 19, 1996. This procedure outlines

the responsibility of the auditor in relation to conducting audits of

vendors not being reviewed under a joint utility audit. In addition,

the Manager, Workforce Processing's role, in the area of acceptance of a

vendor's AAP, is documented. Previously, these two individuals'

responsibilities were not clearly delineated. The procedure also

outlines necessary steps in cases of nonconformance by a vendor to

assure action is taken to correct the deficiencies, or upon

determination, having the vendor removed from the approved

contractor/vendors list of acceptable AAPs.

ENCLOSURE 2

16

Licensee procedure "Access Authorization Program," Reviqion 8, has been

revised to reflect clear responsibility of the Manager, Workforce

Processing. The licensee has incorporated audit function

responsibilities for vendor programs as well as the Manager, Workforce

Processing's responsibilities to ensure that vendor/contractor employees

meet Duke Power Company and NRC requirements, before being granted

unescorted access. The procedure also provides clarification with

respect to temporary access authorization requirements.

In a letter dated January 22, 1996, the licensee committed to performing

a full audit of their AAP. Upon further discussion with licensee

representatives, the inspector was informed this audit would be

conducted during the period of October 28 - November 8, 1996. The

licensee stated the audit report would be made available for review.

c. Conclusions

Based on document and record review and discussion with licensee

representatives, the inspector found the licensee's corrective actions

to be thorough and timely. The licensee's procedures now more clearly

define responsibility between Workforce Processing and the audit review

group to better prevent recurrence of the violation. This item is

closed.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on July 18, 1996. The licensee

acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

Partial List of Persons Contacted

Licensee

B. Peele, Station Manager

M. Bailey, Acting Regulatory Compliance Manager

D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

W. Foster, Safety Assurance Manager

J. Hampton, Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

.

J.

Smith, Regulatory Compliance

G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

ENCLOSURE 2

17

NRC

D. LaBarge, Project Manager

Inspection Procedures Used

IP 71707:

Plant Operations

IP 61726: Surveillance Observations

IP 62703: Maintenance Observation

IP 71750:

Plant Support Activities

IP 37551:

Onsite Engineering

IP 92901:

Followup -

Plant Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup -

Engineering

IP 90712:

LER Followup

IP 93702:

Prompt Onsite Event Response

IP 37550:

Engineering

IP 40500:

Problem Identification, Resolution and Prevention

TI 2515/127: Access Authorization

Items Opened, Closed, and Discussed

Opened

50-270/96-10-01

VIO

Failure To Change Flux/Flow/Imbalance Setpoint

(Section 01.2)

50-269,270,287/96-10-03 VIO

Weld Procedure Qualifications Welded,

Tested,

Certified

and

Approved

By

Same

Individual

(Section M1.5.3)

50-269,270,287/96-10-02 NCV

Failure To Request Relief (Section E3)

Closed

50-269,270,287/94-38-01 VIO

Failure to Follow Keowee Transfer Procedure

(Section 08.1)

50-269/94-28-01

VIO

Failure To

Follow Procedure During Breaker

Installation (Section M8.1)

50-269/94-05

LER

Containment Isolation Valve Technically

Inoperable (Section M8.2)

50-269/94-01

LER

Seismic/LOOP Event May Result In The Loss Of Post

Accident

Cooling

Due

to

Design

Deficiency

(Section E8.1)

50-269,270,287/95-24-02 VIO

Failure To Assure Individuals Granted Unescorted

Access Were Trustworthy And Reliable (Section S1)

USI A-26

USI

Reactor

Pressure

Vessel

Pressure

Transient

Protection (Section E8.3)

ENCLOSURE 2

18

50-287/94-01

LER

Reactor Trip On False High Level Indication Due

To Equipment Failure (Section M8.3)

50-269,270,287/94-28-03 VIO

Corrective Actions Associated With Turbine Bypass

Valves

Randomly

Repositioning

Not

Adequate

(Section E8.2)

List of Acronyms

AAP

Access Authorization Program

ASW

Auxiliary Service Water

CFR

Code of Federal Regulations

CCW

Condenser Circulating Water

DPC

Duke Power Company

EOC

End Of Cycle

IR

Inspection Report

ISFSI

Independent Spent Fuel Storage Installation

IST

In Service Test

ISI

In Service Inspection

KHU

Keowee Hydro Unit

LER

Licensee Event Report

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

LTOP

Low Temperature Overpressure

MP

Maintenance Procedure

NCV

Non-Cited Violation

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

NUMARC

Nuclear Management and Resources Council

ONS

Oconee Nuclear Station

PSID

Pounds Per Square Inch Differential

PSIG

Pounds Per Square Inch Gauge

PM

Preventive Maintenance

PIP

Problem Investigation Process

QA

Quality Assurance

QC

Quality Control

RCS

Reactor Coolant System

RPS

Reactor Protection System

S/G

Steam Generator

SSF

Safe Shutdown Facility

TS

Technical Specification

TSC

Technical Support Center

WCC

Work Control Center

WO

Work Order

ENCLOSURE 2