ML091350187
ML091350187 | |
Person / Time | |
---|---|
Site: | Prairie Island |
Issue date: | 05/14/2009 |
From: | Jack Giessner Reactor Projects Region 3 Branch 4 |
To: | Wadley M Northern States Power Co |
References | |
IR-09-002 | |
Download: ML091350187 (37) | |
See also: IR 05000282/2009002
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION III
2443 WARRENVILLE ROAD, SUITE 210
LISLE, IL 60532-4352
May 14, 2009
Mr. Michael D. Wadley
Site Vice President
Prairie Island Nuclear Generating Plant
Northern States Power Company, Minnesota
1717 Wakonade Drive East
Welch, MN 55089
SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2, NRC
INTEGRATED INSPECTION REPORT 05000282/2009002; 05000306/2009002
Dear Mr. Wadley:
On March 31, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated
inspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed report
documents the inspection findings, which were discussed on April 8, 2009, with you and other
members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents one self-revealed and four NRC-identified findings of very low
safety significance. Three of these findings were determined to involve violations of
NRC requirements. Additionally, a licensee-identified violation which was determined to
be of very low safety significance is listed in this report. However, because of the very low
safety significance, and because the issues were entered into your corrective action program,
the NRC is treating these findings as Non-Cited Violations (NCVs) in accordance with
Section VI.A.1 of the NRC Enforcement Policy.
If you contest any NCV, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN.: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional
Administrator, Region III; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Prairie
Island Nuclear Generating Plant. In addition, if you disagree with the characterization of any
finding in this report, you should provide a response within 30 days of the date of this inspection
report, with the basis for your disagreement, to the Regional Administrator, Region III, and the
NRC Resident Inspector Office at the Prairie Island Nuclear Generating Plant. The information
you provide will be considered in accordance with Inspection Manual Chapter 0305.
M. Wadley -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document
Room or from the Publicly Available Records (PARS) component of NRC's document system
(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
Sincerely,
/RA/
John B. Giessner, Chief
Branch 4
Division of Reactor Projects
Docket Nos. 50-282; 50-306;72-010
License Nos. DPR-42; DPR-60; SNM-2506
Enclosure: Inspection Report 05000282/2009002; 05000306/2009002
w/Attachment: Supplemental Information
cc w/encl: D. Koehl, Chief Nuclear Officer
J. Anderson, Regulatory Affairs Manager
P. Glass, Assistant General Counsel
Nuclear Asset Manager
J. Stine, State Liaison Officer, Minnesota Department of Health
Tribal Council, Prairie Island Indian Community
Administrator, Goodhue County Courthouse
Commissioner, Minnesota Department
of Commerce
Manager, Environmental Protection Division
Office of the Attorney General of Minnesota
Emergency Preparedness Coordinator, Dakota
County Law Enforcement Center
M. Wadley -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document
Room or from the Publicly Available Records (PARS) component of NRC's document system
(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
Sincerely,
/RA/
John B. Giessner, Chief
Branch 4
Division of Reactor Projects
Docket Nos. 50-282; 50-306;72-010
License Nos. DPR-42; DPR-60; SNM-2506
Enclosure: Inspection Report 05000282/2008005; 05000306/2008005
w/Attachment: Supplemental Information
cc w/encl: D. Koehl, Chief Nuclear Officer
J. Anderson, Regulatory Affairs Manager
P. Glass, Assistant General Counsel
Nuclear Asset Manager
J. Stine, State Liaison Officer, Minnesota Department of Health
Tribal Council, Prairie Island Indian Community
Administrator, Goodhue County Courthouse
Commissioner, Minnesota Department
of Commerce
Manager, Environmental Protection Division
Office of the Attorney General of Minnesota
Emergency Preparedness Coordinator, Dakota
County Law Enforcement Center
DOCUMENT NAME: PRAI/PRA 2009 009.doc
G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE RIII
NAME JGiessner:dtp
DATE 05/14/09
OFFICIAL RECORD COPY
Letter to M. Wadley from J. Giessner dated May 14, 2009
SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2, NRC
INTEGRATED INSPECTION REPORT 05000282/2008005; 05000306/2008005
DISTRIBUTION:
RidsNrrPMPrairieIsland
RidsNrrDorlLpl3-1 Resource
RidsNrrDirsIrib Resource
Patrick Hiland
Kenneth Obrien
Cynthia Pederson (hard copy - IRs only)
DRPIII
DRSIII
Patricia Buckley
ROPreports Resource
U.S. NUCLEAR REGULATORY COMMISSION
REGION III
Docket Nos: 50-282; 50-306;72-010
License Nos: DPR-42; DPR-60; SNM-2506
Report No: 05000282/2009002; 05000306/2009002
Licensee: Northern States Power Company, Minnesota
Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2
Location: Welch, MN
Dates: January 1 through March 31, 2009
Inspectors: K. Stoedter, Senior Resident Inspector
P. Zurawski, Resident Inspector
D. Betancourt, Reactor Engineer
N. Feliz, Reactor Inspector
Approved by: J. Giessner, Chief
Branch 4
Division of Reactor Projects
Enclosure
TABLE OF CONTENTS
SUMMARY OF FINDINGS ...........................................................................................................1
REPORT DETAILS .......................................................................................................................4
Summary of Plant Status...........................................................................................................4
1. REACTOR SAFETY ...........................................................................................4
1R01 Adverse Weather Protection (71111.01) .....................................................4
1R04 Equipment Alignment (71111.04) ................................................................6
1R05 Fire Protection (71111.05) ...........................................................................7
1R07 Annual Heat Sink Performance (71111.07) .................................................8
1R11 Licensed Operator Requalification Program (71111.11) .............................9
1R12 Maintenance Effectiveness (71111.12) .......................................................9
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) 10
1R15 Operability Evaluations (71111.15) ...........................................................11
1R18 Plant Modifications (71111.18) ..................................................................13
1R19 Post-Maintenance Testing (71111.19) ......................................................14
1R22 Surveillance Testing (71111.22) ................................................................16
1EP6 Drill Evaluation (71114.06) ........................................................................19
4. OTHER ACTIVITIES ........................................................................................20
4OA1 Performance Indicator Verification (71151) ...............................................20
4OA2 Identification and Resolution of Problems (71152) ....................................21
4OA5 Other Activities ..........................................................................................22
4OA6 Management Meetings ..............................................................................24
4OA7 Licensee-Identified Violations ....................................................................24
SUPPLEMENTAL INFORMATION ...............................................................................................1
KEY POINTS OF CONTACT.....................................................................................................1
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED .........................................................1
LIST OF DOCUMENTS REVIEWED.........................................................................................3
LIST OF ACRONYMS USED ....................................................................................................7
Enclosure
SUMMARY OF FINDINGS
IR 05000282/2009002, 05000306/2009002; 01/01/2009 - 03/31/2009; Prairie Island Nuclear
Generating Plant, Units 1 and 2; Adverse Weather Protection, Operability Evaluations, Post-
Maintenance Testing, Surveillance Testing, and Other Activities.
This report covers a 3-month period of inspection by resident and regional inspectors.
One self revealed and four inspector-identified Green findings were identified. Three
findings were considered Non-Cited Violations of NRC regulations. The significance of
most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual
Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the
SDP does not apply may be Green or be assigned a severity level after NRC management
review. The NRCs program for overseeing the safe operation of commercial nuclear power
reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated
December 2006.
A. NRC-Identified and Self-Revealed Findings
Cornerstone: Initiating Events
- Green. The inspectors identified a finding of very low safety significance and a
Non Cited Violation of Technical Specification 5.4.1 due to operations personnel
failing to implement abnormal operating procedures following an unexpected control
rod insertion on November 6, 2008. Corrective actions for this issue included revising
licensed operator training and providing guidance to operations personnel on the need
to enter abnormal operating procedures following the receipt of an entry condition.
The inspectors determined that this finding was more than minor because the failure to
enter abnormal operating procedures to respond to unexpected conditions could result in
incorrect actions being taken following a plant event (a more significant safety issue).
The inspectors concluded that this issue was of very low safety significance because the
finding was not a loss of coolant accident initiator, was not an external events initiator,
and would not have resulted in both the likelihood of a reactor trip and that mitigating
systems equipment would not have been available. The inspectors determined that this
finding was cross-cutting in the Human Performance, Work Practices area because the
licensee had not effectively communicated expectations regarding procedural
compliance following the receipt of an abnormal operating procedure entry condition
(H.4(b)). (Section 4OA5.1)
Cornerstone: Mitigating Systems
- Green. The inspectors identified a finding of very low safety significance on
January 13, 2009, due to the fire protection system pumps being unable to auto start,
as designed, in response to a low fire header pressure condition. Corrective actions
for this issue included unthawing the sensing line, verifying the screenhouse ventilation
systems configuration, revising the normal screenhouse ventilation procedure to ensure
that it provided guidance on shutting down the exhaust fans, and repairing several
normal screenhouse ventilation system equipment deficiencies.
This finding was more than minor because if left uncorrected, the failure to protect
mitigating systems equipment from the effects of extreme cold temperatures could
1 Enclosure
result in the system failing to function when needed. The inspectors determined that
this finding was of very low safety significance because it was assigned a low fire
degradation rating as specified in the Fire Protection Significance Determination
Process. This finding was determined to be cross-cutting in the Human Performance,
Resources area because the licensee failed to have a complete and accurate normal
screenhouse ventilation procedure to ensure that operation of the system would not
result in the freezing of mitigating systems equipment during extreme cold weather
conditions (H.2(c)). No violations of NRC requirements occurred because the fire pumps
could have been started manually if needed and because the normal screenhouse
ventilation system was nonsafety-related. (Section 1R01.1)
- Green. The inspectors identified a finding of very low safety significance and a
Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions,
Procedures, and Drawings, for the failure to adequately implement Procedure
FP-OP OL-01, Operability Determination, to assess the capability of the 122 Control
Room Chilled Water Pump to meet its mission time following the discovery of increased
pump vibrations. Corrective actions for this issue included revising the operability
recommendation and repairing the degraded pump.
This finding was more than minor because, if left uncorrected, failure to adequately
implement the operability procedure could result in safety-related components been
incorrectly declared operable rather than inoperable or operable, but non-conforming
(a more significant safety concern). This finding was of very low safety significance
because the finding did not represent an actual loss of safety function of a single train for
longer than its Technical Specification allowed outage time. The inspectors concluded
that this finding was cross-cutting in the Human Performance, Decision Making area
because the licensee failed to validate the underlying assumptions made when
determining the continued operability of a safety-related component (H.1(b)).
(Section 1R15.1)
- Green. The inspectors identified a finding of very low safety significance on
February 25, 2009, due to operations and maintenance personnel failing to identify a
turbocharger coolant vent line fretting condition during a D5 emergency diesel generator
post-maintenance test or during previous D5 operations. The lack of identification
resulted in D5 operating with degraded conditions prior to the fretting issue being
evaluated in the corrective action program. Corrective actions for this issue included
performing an ultrasonic examination of the fretted area in support of an evaluation to
determine whether the pipe needed to be replaced prior to declaring the diesel generator
operable. The licensee also documented the untimely identification of the issue within
its corrective action program.
This finding was more than minor because if left uncorrected, the failure to identify,
evaluate, and correct equipment issues could result in returning safety-related
equipment to service with deficiencies that impact the ability of the equipment to perform
its safety function (a more significant safety concern). The inspectors determined that
the finding was of very low safety significance because it was not associated with an
actual loss of safety function and did not screen as potentially risk significant due to a
seismic, flooding, or severe weather initiating event. The inspectors considered the
finding to be cross-cutting in the Problem Identification and Resolution, Corrective Action
Program area because operations and maintenance personnel failed to identify this
issue in a timely manner commensurate with its safety significance (P.1(a)). No
2 Enclosure
violations of NRC requirements occurred because D5 was not operable at the time this
issue was identified and corrective actions were taken before it became operable.
(Section 1R19.1)
Cornerstone: Barrier Integrity
- Green. A self-revealed finding and Non-Cited Violation of Prairie Island Nuclear
Generating Plant Operating License DPR-42, Section C.1, was identified on
January 2, 2009, due to the failure to maintain Unit 1 reactor power below the thermal
power limitations stated in the facility operating license. Corrective actions for this issue
included revising all associated operating procedures to ensure that operations
personnel take action to lower reactor power if power levels exceed the licensed thermal
power limitations.
The inspectors determined that this issue was more than minor because if left
uncorrected the operation of the reactor beyond the limits specified in the operating
license could become a more significant safety concern. The inspectors determined that
this issue was of very low safety significance because the finding was only associated
with the fuel aspect of the Barrier Integrity Cornerstone and no core thermal limits were
violated. The inspectors determined that this finding was cross-cutting in the Human
Performance, Resources area because the licensee failed to have complete, accurate
and up-to-date procedures regarding the maintenance of licensed thermal power levels
(H.2(c)). (Section 1R22.1)
B. Licensee-Identified Violations
Violations of very low safety significance that were identified by the licensee have been
reviewed by inspectors. Corrective actions planned or taken by the licensee have been
entered into the licensees corrective action program. These violations and corrective
action tracking numbers are listed in Section 4OA7 of this report.
3 Enclosure
REPORT DETAILS
Summary of Plant Status
Operations personnel operated Unit 1 at or near full power until February 27, 2009, when
reactor power was reduced to 48 percent to perform turbine testing. Operations personnel
returned the reactor to full power levels on February 28, 2009. Additional power reductions
were performed during the inspection period to allow for routine testing of plant components.
Unit 2 began the inspection period operating at full power. Unit 2 remained at this power level
through the remainder of the inspection period.
1. REACTOR SAFETY
Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and
1R01 Adverse Weather Protection (71111.01)
.1 Adverse Weather Condition - Extreme Cold Conditions
a. Inspection Scope
In mid-January 2009, the area around the Prairie Island Nuclear Generating Plant
experienced extreme cold temperatures. During this time, the licensee initiated
corrective action program document (CAP) 1165338 due to discovering that the sensing
line used to provide an automatic start signal to the fire pumps was frozen. The
inspectors reviewed the CAP, control room logs, outstanding work orders on the
screenhouse ventilation system, and the licensees apparent cause report to determine if
there was significant impact to mitigating systems and fire protection related equipment.
The inspectors also reviewed the licensees winter readiness and screenhouse normal
ventilation procedures to determine how the ventilation system was prepared for cold
weather conditions. Specific documents reviewed during this inspection are listed in the
Attachment.
This inspection constituted one actual adverse weather condition sample as defined in
Inspection Procedure 71111.01-05.
b. Findings
Introduction: The inspectors identified a Green finding due the fire protection system
pumps being unable to auto start, as designed, in response to a low fire header pressure
condition. This happened due to the freezing of a fire protection sensing line such that
the fire pumps would not have automatically started following a fire.
Description: During a control room panel walkdown on January 13, 2009, a licensed
operator identified that fire protection header pressure was 85 pounds and decreasing.
At this pressure, the operator expected to find the jockey pump and all three fire pumps
running. They were not. The operator checked the plant computer and found that the
jockey pump had been cycling on and off as expected. However, the jockey pump had
stopped cycling approximately 30 minutes prior to the operator discovering the low
4 Enclosure
header pressure condition. The operator informed the shift supervisor of the fire
protection system status and actions were taken to manually start the screenwash
pump to pressurize the fire header.
The licensee inspected the screenhouse for potential freezing issues following this
event. No other issues were found. However, the 21 screenhouse exhaust fan was
found running. The licensee believed that the 21 screenhouse exhaust fan was likely
started during a warm winter day to maintain screenhouse temperatures. The fan was
not shut down once the screenhouse temperatures decreased. The 11 screenhouse
exhaust fan dampers were also partially open due to a previously identified equipment
issue. These conditions led to the continuous introduction of cold outside air into the
screenhouse to the point of freezing the sensing line. The 21 screenhouse exhaust fan
was subsequently stopped. This allowed temperatures in the sensing line area to
increase and thaw out the line.
The inspectors reviewed the licensees apparent cause report for this event. The
licensee concluded that the sensing line froze due to operations personnel failing to
follow Administrative Work Instruction 5AWI 15.5.1, Plant Equipment Control Process.
Contributing causes were the inadequate guidance in Operating Procedure C37.5,
Screenhouse Normal Ventilation, and the failure to sufficiently question lower than
expected screenhouse temperatures. The inspectors reviewed the procedures
referenced in the apparent cause report and disagreed with the licensees conclusions.
Specifically, Section 6.6.22 of 5AWI 15.5.1 stated that the Equipment Status Control Log
was required to be used if the position of a piece of equipment was changed by a
process other than a procedure, checklist, work order or clearance order. The
inspectors reviewed Operating Procedure C37.5 and found that the 21 screenhouse
exhaust fan was operated per step 4.1 which stated, on warm days when the traveling
screen area exceeds 50 degrees, the 11 [21] screenhouse exhaust fans shall be run as
necessary to prevent overheating of the pump area. As a result, the inspectors
determined that the Equipment Status Control Log was not required to be used to
document the starting of the 21 screenhouse exhaust fan.
The licensee also documented two equipment deficiencies within the apparent
cause reports body. However, the licensee concluded that these deficiencies were
not event contributors. The inspectors disagreed with this conclusion. As stated above,
the 11 screenhouse exhaust fan dampers were found partially open due to a previously
identified condition. The inspectors reviewed the licensees computer database and
found two May 2008 work orders to refurbish/rebuild various screenhouse ventilation
exhaust dampers. In addition, the apparent cause report documented that the control
room indication that would have been used to determine if the 21 screenhouse exhaust
fan was running was non-functional. The inspectors searched the licensees database
again and found that this deficiency was first identified in April 2008. Although
operations personnel had requested that the light be repaired by July 2008, no work had
been done to correct this condition. The inspectors contacted the work control staff and
requested the status of the work orders discussed above. The inspectors were informed
that the 11 screenhouse exhaust fan work order had been rescheduled three times due
to a lack of planning resources. This work order was scheduled for completion on
May 4, 2009. The other ventilation work order had been rescheduled once due to parts
issues. This work order was scheduled for completion on April 13, 2009. Lastly, the
work order associated with the control room indicating light was scheduled for
5 Enclosure
completion on April 6, 2009. The inspectors planned to review the completion of these
work orders as part of their hot weather readiness review.
Although the freezing of the sensing line was identified by a licensed operator during a
control room panel walkdown, this finding is NRC identified because the inspectors
found previously unknown weaknesses in the licensees evaluation of this issue.
Analysis: The inspectors determined that the fire protection system pumps being unable
to auto start, as designed, in response to a low fire header pressure condition was a
performance deficiency and a finding that was required to be assessed using the Fire
Protection Significance Determination Process (SDP). The inspectors determined that
this finding was more than minor because if left uncorrected, the failure to protect
mitigating systems equipment from the effects of extreme cold temperatures could result
in the system failing to function when needed to respond to an event. This finding
impacted the Mitigating Systems Cornerstone. The inspectors assigned a fixed fire
protection systems finding category to this issue. This finding was also assigned a low
degradation. The inspectors concluded that this finding was of very low safety
significance (Green) per step 1.3.1 (assignment of a low degradation rating) of the Fire
Protection SDP. This finding was determined to be cross-cutting in the Human
Performance, Resources area because the licensee failed to have a complete and
accurate normal screenhouse ventilation procedure to ensure that operation of the
system would not result in the freezing of plant equipment during extreme cold weather
conditions (H.2(c)) (FIN 05000282/2009002-01; 05000306/2009002-01).
Enforcement: No violations of NRC requirements were identified because the fire
pumps could have been manually started if needed and because the normal
screenhouse ventilation system was not safety-related.
1R04 Equipment Alignment (71111.04)
.1 Quarterly Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant
systems:
- 122 Control Room Chiller;
- 11 and 12 Auxiliary Feedwater Pumps; and
- 12 Diesel-Driven Cooling Water Pump.
The inspectors selected these systems based on their risk significance relative to the
reactor safety cornerstones at the time they were inspected. The inspectors attempted
to identify any discrepancies that could impact the function of the system, and, therefore,
potentially increase risk. The inspectors reviewed applicable operating procedures,
system diagrams, Updated Safety Analysis Report (USAR), Technical Specification (TS)
requirements, outstanding work orders, CAPs, and the impact of ongoing work activities
on redundant trains of equipment in order to identify conditions that could have rendered
the systems incapable of performing their intended functions. The inspectors also
walked down accessible portions of the systems to verify system components and
6 Enclosure
support equipment were aligned correctly and operable. The inspectors examined the
material condition of the components and observed operating parameters of equipment
to verify that there were no obvious deficiencies. The inspectors also verified that the
licensee had properly identified and resolved equipment alignment problems that could
cause initiating events or impact the capability of mitigating systems or barriers and
entered them into the corrective action program with the appropriate significance
characterization. Documents reviewed are listed in the Attachment.
These activities constituted four partial system walkdown samples as defined in
IP 71111.04-05.
b. Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05)
.1 Routine Resident Inspector Tours (71111.05Q)
a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on the
availability, accessibility, and condition of firefighting equipment in the following
risk-significant plant areas:
- 11 and 12 Battery Rooms (Zone 1);
- 21 and 22 Battery Rooms (Zone 35);
- 715-foot Auxiliary Building (Zone 46);
- Auxiliary Feedwater Room (Zone 2); and
- 715-foot Unit 1 Auxiliary Building and Hot Chemistry Laboratory (Zone19).
The inspectors reviewed the areas to assess if the licensee had implemented a fire
protection program that adequately controlled combustibles and ignition sources within
the plant, effectively maintained fire detection and suppression capability, maintained
passive fire protection features in good material condition, and had implemented
adequate compensatory measures for out of service, degraded or inoperable fire
protection equipment, systems, or features in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk
as documented in the Individual Plant Examination of External Events with later
additional insights, their potential to impact equipment which could initiate or mitigate a
plant transient, or their impact on the licensees ability to respond to a security event.
Using the documents listed in the attachment, the inspectors verified that fire hoses and
extinguishers were in their designated locations and available for immediate use; that
fire detectors and sprinklers were unobstructed; that transient material loading was
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
be in satisfactory condition. The inspectors also verified that minor issues identified
during the inspection were entered into the licensees corrective action program.
Documents reviewed are listed in the Attachment to this report.
These activities constituted five quarterly fire protection inspection samples as defined in
IP 71111.05-05.
7 Enclosure
b. Findings
No findings of significance were identified.
.2 Annual Fire Protection Drill Observation (71111.05A)
a. Inspection Scope
On March 31, 2009, the inspectors observed the fire brigade during a simulated fire
in the turbine building water treatment area. Based on this observation, the
inspectors evaluated the readiness of the licensees fire brigade to fight fires. The
inspectors verified that the licensee staff identified deficiencies; openly discussed
them in a self-critical manner at the drill debrief, and took appropriate corrective
actions. Specific attributes evaluated were: (1) proper wearing of turnout gear and
self-contained breathing apparatus; (2) proper use and layout of fire hoses;
(3) employment of appropriate fire fighting techniques; (4) sufficient firefighting
equipment brought to the scene; (5) effectiveness of fire brigade leader communications,
command, and control; (6) search for victims and propagation of the fire into other plant
areas; (7) smoke removal operations; (8) utilization of pre-planned strategies;
(9) adherence to the pre-planned drill scenario; and (10) drill objectives. Documents
reviewed are listed in the Attachment to this report.
These activities constituted one annual fire protection inspection sample as defined by
IP 71111.05-05.
b. Findings
No findings of significance were identified.
1R07 Annual Heat Sink Performance (71111.07)
.1 Heat Sink Performance
a. Inspection Scope
The inspectors reviewed the licensees inspection of the D1 emergency diesel generator
heat exchangers to verify that the licensee identified potential heat exchanger
deficiencies. The inspectors viewed the as-found pictures of each heat exchanger to
assess the overall material condition of the equipment and to determine whether the
material condition impacted the ability of the heat exchangers to perform their safety
function. The inspectors reviewed the licensees heat exchanger tube plugging
calculations and compared the calculation results to the actual number of tubes plugged
in each heat exchanger. The inspectors also reviewed heat exchanger issues entered
into the licensees corrective action program to ensure that issues were being resolved
in a timely manner based upon the importance to safety.
This annual heat sink performance inspection constituted one sample as defined in
IP 71111.07-05.
8 Enclosure
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program (71111.11)
.1 Resident Inspector Quarterly Review (71111.11Q)
a. Inspection Scope
On February 23, 2009, the inspectors observed a crew of licensed operators in the
simulator during licensed operator requalification examinations to verify that operator
performance was adequate, evaluators were identifying and documenting crew
performance problems, and training was being conducted in accordance with licensee
procedures. The inspectors evaluated the following areas:
- licensed operator performance;
- crews clarity and formality of communications;
- ability to take timely actions in the conservative direction;
- prioritization, interpretation, and verification of annunciator alarms;
- correct use and implementation of abnormal and emergency procedures;
- control board manipulations;
- oversight and direction from supervisors; and
- ability to identify and implement appropriate TS actions and Emergency Plan
actions and notifications.
The crews performance in these areas was compared to pre-established operator action
expectations and successful critical task completion requirements. Documents reviewed
are listed in the Attachment to this report.
This inspection constituted one quarterly licensed operator requalification program
sample as defined in IP 71111.11.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
.1 Routine Quarterly Evaluations (71111.12Q)
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk
significant systems:
- 480 Volt Electrical System, and
- Normal Screenhouse Ventilation System.
The inspectors reviewed events such as where ineffective equipment maintenance had
resulted in valid or invalid automatic actuations of systems and independently verified
9 Enclosure
the licensee's actions to address system performance or condition problems in terms of
the following:
- implementing appropriate work practices;
- identifying and addressing common cause failures;
- scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
- characterizing system reliability issues for performance;
- charging unavailability for performance;
- trending key parameters for condition monitoring;
- ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
- verifying appropriate performance criteria for structures, systems, and
components/functions classified as (a)(2) or appropriate and adequate goals and
corrective actions for systems classified as (a)(1).
The inspectors assessed performance issues with respect to the reliability, availability,
and condition monitoring of the system. In addition, the inspectors verified maintenance
effectiveness issues were entered into the corrective action program with the appropriate
significance characterization. Documents reviewed are listed in the Attachment to this
report.
This inspection constituted two quarterly maintenance effectiveness samples as defined
in IP 71111.12-05.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
.1 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the licensee's evaluation and management of plant risk for the
maintenance and emergent work activities affecting risk-significant and safety-related
equipment listed below to verify that the appropriate risk assessments were performed
prior to removing equipment for work:
- Work Week 0902 including planned maintenance on the cooling water and
charging systems;
- Emergent work due to the inoperability of the 11 and 21 residual heat removal
(RHR) systems;
- Emergent work due to the loss of the Blue Lake 345 kilovolt offsite power line
while the D5 and D6 emergency diesel generators were inoperable;
- Work Week 0909 including planned maintenance on the 2R, 2RX, and 2RY
transformers; and
- An emergent overpower T instrument failure.
These activities were selected based on their potential risk significance relative to the
reactor safety cornerstones. As applicable for each activity, the inspectors verified that
10 Enclosure
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
and complete. When emergent work was performed, the inspectors verified that the
plant risk was promptly reassessed and managed. The inspectors reviewed the scope
of maintenance work, discussed the results of the assessment with the licensee's
probabilistic risk analyst or shift technical advisor, and verified plant conditions were
consistent with the risk assessment. The inspectors also reviewed TS requirements and
walked down portions of redundant safety systems, when applicable, to verify risk
analysis assumptions were valid and applicable requirements were met.
These maintenance risk assessments and emergent work control activities constituted
five samples as defined in IP 71111.13-05.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
.1 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following issues:
to the Reactor Coolant System Hot Legs;
- Unit 2 Safety Injection System Voids;
- 11 and 21 RHR Voids in Minimum Flow Lines;
- Charging Pump Oil Compatibility Issues;
- Missing Cotter Pins on D6 Emergency Diesel Generator;
- 122 Control Room Chilled Water Pump High Vibrations;
- 22 Turbine-Driven Auxiliary Water Pump High Vibrations;
- Breaker 222E-3 Voltage Outside of Acceptable Range;
- High Crankcase Vacuum on D2 Emergency Diesel Generator; and
- Potentially Missing Fire Damper between Control Room Chiller Area and
Auxiliary Building.
The inspectors selected these potential operability issues based on the risk-significance
of the associated components and systems. The inspectors evaluated the technical
adequacy of the evaluations to ensure that TS operability was properly justified and the
subject component or system remained available such that no unrecognized increase in
risk occurred. The inspectors compared the operability and design criteria in the
appropriate sections of the TS and USAR to the licensees evaluations, to determine
whether the components or systems were operable. Where compensatory measures
were required to maintain operability, the inspectors determined whether the measures
in place would function as intended and were properly controlled. The inspectors
determined, where appropriate, compliance with bounding limitations associated with the
evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
documents to verify that the licensee was identifying and correcting any deficiencies
associated with operability evaluations. Documents reviewed are listed in the
Attachment to this report.
11 Enclosure
This operability inspection constituted ten samples as defined in IP 71111.15-05.
b. Findings
Introduction: The inspectors identified a Green finding and a Non-Cited Violation (NCV)
of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,
for the failure to adequately implement Procedure FP-OP-OL-01, Operability
Determination, to adequately assess the capability of the 122 Control Room Chilled
Water Pump to meet its mission time following the discovery of increased pump
vibrations.
Description: In September 2008, the 122 Control Room Chilled Water Pump was placed
on an increased test frequency due to the discovery of higher than expected outboard
bearing vibrations. Specifically, vibration levels as high as 0.0256 inches per second
were recorded. This value exceeded the alert level established by the Inservice Testing
Program. In December 2008, the licensee performed routine testing of the 122 Control
Room Chilled Water Pump using Surveillance Procedure (SP) 1161B, Control Room
Train B Chilled Water Pump Quarterly Test, and found that the outboard bearing
vibration levels had increased to approximately 0.0317 inches per second. Due to the
adverse vibration trend, operations personnel requested that an operability
determination be performed to assess the continued and long-term operability of the
122 Control Room Chilled Water Pump.
The inspectors reviewed the licensees operability recommendation and found that the
licensee had concluded that the pump would continue to operate for its required mission
time. However, the mission time was not specifically stated in the document as required
by the operability determination Procedure FP-OP-OL-01, Operability Determination.
The inspectors asked several engineering individuals to provide the mission time for the
122 Control Room Chilled Water Pump. The inspectors needed this information to
perform an independent evaluation of the pumps performance. The licensee initially
told the inspectors that the increased vibrations had no impact on the chilled water
pumps operability because the total increase in vibrations was small. The inspectors
reviewed the actual vibration data and found that the licensees statement had failed to
consider that the increasing vibration trend had started in May 2008 rather than
September 2008. Following this discussion, the inspectors again requested the
122 Control Room Chilled Water Pumps mission time. After approximately 1 week, the
engineering staff informed the inspectors that the mission time was 30 days. Using this
information, the inspectors agreed that the pump would have continued to perform its
safety function. However, the inspectors concluded that the licensees initial operability
evaluation was inadequate because the licensee failed to specify the pumps required
mission time and justify why the pump would have continued to operate. The licensee
revised the operability evaluation following discussions with the inspectors.
Maintenance personnel replaced the 122 Control Room Chilled Water Pump outboard
bearings on February 7, 2009.
Analysis: The inspectors determined that the failure to adequately implement Procedure
FP-OP-OL-01, Operability Determination to justify the continued operability of the 122
Control Room Chilled Water Pump was a performance deficiency that required
evaluation using the SDP. The inspectors determined that the finding was more than
minor because, if left uncorrected, failure to adequately implement the operability
procedure could result in safety-related components been incorrectly declared operable
12 Enclosure
rather than inoperable or operable, but non-conforming (a more significant safety
concern). This finding affected the Mitigating System Cornerstone. The inspectors
concluded that this finding was of very low safety significance (Green), because the
finding did not represent an actual loss of safety function of a single train for longer than
its TS allowed outage time. Additionally, the inspectors determined that this finding was
cross-cutting in the Human Performance, Decision Making area because the licensee
failed to verify the validity of underlying assumptions used in operability decisions
(H.1(b)).
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
and Drawings, requires, in part, that activities affecting quality be prescribed and
accomplished by procedures appropriate for the circumstances. The licensee
implemented the operability determination process (an activity affecting quality) using
Procedure FP-OP-OL-01, Operability Determination. FP-OP-OL-01 required, in part,
that the licensee assess the capability of a system to meet its mission time as part of the
operability process. Contrary to the above, on December 26, 2008, the licensee failed to
adequately assess the continued operability of the 122 Control Room Chilled Water
Pump due to the failure to include the specific mission time and adequately justify why
the pump would continue to run for this time period. Because this finding was of very
low safety significance, and because it was entered into the corrective action program as
CAP 1162312, this violation is being treated as an NCV consistent with Section VI.A of
the Enforcement Policy (NCV 05000282/2009002-02;05000306/2009002-02).
Corrective actions for this issue included revising the operability determination with
additional information to justify the continued pump operability for the required mission
time and replacement of the outboard bearings.
1R18 Plant Modifications (71111.18)
.1 Temporary Plant Modifications
a. Inspection Scope
The inspectors reviewed the following temporary modification:
- Alternate Power Source to Closed Circuit Television Camera.
The inspectors compared the temporary configuration change and associated
10 CFR 50.59 screening and evaluation information against the design basis, the USAR,
the TS, and other documents as applicable, to verify that the modification did not affect
the operability or availability of the affected system and was adequate for the intended
purpose. The inspectors also compared the licensees information to operating
experience information to ensure that lessons learned from other utilities had been
incorporated into the licensees decision to implement the temporary modification. The
inspectors, as applicable, performed field verifications to ensure that the modification
was installed as directed; the modification operated as expected; modification testing
adequately demonstrated continued system operability, availability, and reliability; and
that operation of the modification did not impact the operability of any interfacing
systems. Lastly, the inspectors discussed the temporary modification with licensee
personnel to ensure that the individuals were aware of how extended operation with the
temporary modification in place could impact overall performance.
13 Enclosure
This inspection constituted one temporary modification sample as defined in
IP 71111.18-05.
b. Findings
No findings of significance were identified.
1R19 Post-Maintenance Testing (71111.19)
.1 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed the following post-maintenance activities to verify that
procedures and test activities were adequate to ensure system operability and functional
capability:
- D1 Emergency Diesel Generator 24-Month Inspection;
- Unit 2 Overpower T Summing Amplifier Replacement;
- 21 Cooling Water Strainer Agastat Relay Replacement;
- D5 Emergency Diesel Generator Overhaul; and
- D1 Emergency Diesel Generator Lube Oil Heat Exchanger Replacement.
These activities were selected based upon the structure, system, or component's ability
to impact risk. The inspectors evaluated these activities for the following (as applicable):
the effect of testing on the plant had been adequately addressed; testing was adequate
for the maintenance performed; acceptance criteria were clear and demonstrated
operational readiness; test instrumentation was appropriate; tests were performed as
written in accordance with properly reviewed and approved procedures; equipment was
returned to its operational status following testing (temporary modifications or jumpers
required for test performance were properly removed after test completion), and test
documentation was properly evaluated. The inspectors evaluated the activities against
TS, the USAR, 10 CFR Part 50 requirements, licensee procedures, and various
NRC generic communications to ensure that the test results adequately ensured that the
equipment met the licensing basis and design requirements. In addition, the inspectors
reviewed corrective action documents associated with post-maintenance tests to
determine whether the licensee was identifying problems and entering them in the
corrective action program and that the problems were being corrected commensurate
with their importance to safety. Documents reviewed are listed in the Attachment to this
report.
This inspection constituted five post-maintenance testing samples as defined in
IP 71111.19-05.
b. Findings
(1) Failure to Identify D5 Coolant Vent Line Fretting in a Timely Manner
Introduction: The inspectors identified a Green finding for the failure to identify and
evaluate a fretted D5 turbocharger coolant vent line in a timely manner.
14 Enclosure
Description: During the early afternoon of February 25, 2009, the inspectors performed
an observation of ongoing D5 emergency diesel generator overhaul activities. During
this observation, the inspectors identified that the turbocharger coolant vent line had a
potentially significant fretted condition adjacent to a retaining U-bolt. At the time of this
observation, the D5 emergency diesel generator was out of service and undergoing its
12-hour post-maintenance test. In addition, the licensee was nearing the 11th day of a
14-day limiting condition for operation (LCO) period. The inspectors observed the fretted
condition approximately 15 minutes into the post-maintenance test (PMT).
Once observed, the inspectors discussed the fretted condition with a maintenance
supervisor and an operator involved with the PMT. At the time, the inspectors
understood that the supervisor or operator would formally identify and communicate the
fretting issue to the outage control center and through the corrective action process.
The morning of February 26, 2009, the inspectors discovered that licensee personnel
had not documented the fretting issue in the corrective action system until the 12-hour
PMT was complete. In addition, there was very little communication between the
individuals the inspectors spoke with and the outage control center. The inspectors
concluded that the lack of communications resulted in incurring additional maintenance
rule unavailability time and extending the LCO by approximately 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br />.
The licensee subsequently performed an ultrasonic examination of the fretted area to
determine whether the piping needed to be replaced. The ultrasonic examination
showed that the vent pipe was sufficient for continued operation because the pipes wall
thickness was greater than the minimum allowable. The licensee also obtained
correspondence from the vendor that stated that the pipe could be kept in service. The
licensee planned to replace the vent line during the next D5 overhaul using Work Request 43216. The licensee also reinforced the need for timely communication of
issues to ensure that additional unavailability was not incurred unnecessarily.
Analysis: The inspectors determined that the failure to identify, communicate, and
evaluate discrepant conditions in a timely manner during this post maintenance test or
during previous D5 operation was a performance deficiency that required evaluation
using the SDP. The inspectors determined that the finding was more than minor
because if left uncorrected, the failure to identify, communicate, and evaluate issues in a
timely manner could result in unexpected equipment performance or improperly
returning equipment to service following maintenance (a more significant safety issue).
The inspectors concluded that this finding was of very low safety significance because
the finding did not result in an actual loss of safety function and did not screen as
potentially risk significant due to a seismic, flooding, or severe weather initiating event.
Additionally, the inspectors considered the finding to be cross-cutting in the Problem
Identification and Resolution, Corrective Action Program area because operations and
maintenance personnel failed to identify this issue in a timely manner commensurate
with its safety significance (P.1(a)) (FIN 05000306/2009002-03).
Enforcement: No violations of NRC requirements were identified because the D5
emergency diesel generator was inoperable when this condition was found. Corrective
actions for this issues included performing an ultrasonic examination to determine
whether the pipe needed to be replaced prior to declaring the diesel generator operable
and reinforcing the need for timely communication of equipment issues during TS LCO
conditions.
15 Enclosure
1R22 Surveillance Testing (71111.22)
.1 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether
risk-significant systems and equipment were capable of performing their intended safety
function and to verify testing was conducted in accordance with applicable procedural
and TS requirements:
- Bus 16 Load Sequencer Test (Routine);
- Unit 1 Control Rod Quarterly Exercise (Routine);
- Bus 26 Load Sequencer Test (Routine);
- 12 Containment Spray Pump Quarterly Test (IST);
- 12 Motor-Driven Auxiliary Feedwater Pump Quarterly Flow and Valve Test (IST);
- D2 Emergency Diesel Generator 24-Hour Endurance Run (Routine);
- D5 Emergency Diesel Generator Monthly Surveillance (Routine); and
- Unit 1 Turbine-Driven Auxiliary Feedwater Pump Monthly Test (Routine).
The inspectors observed in plant activities and reviewed procedures and associated
records to determine the following:
- did preconditioning occur;
- were the effects of the testing adequately addressed by control room personnel
or engineers prior to the commencement of the testing;
- were acceptance criteria clearly stated;
- plant equipment calibration was correct, accurate, and properly documented;
- measuring and test equipment calibration was current;
- test equipment was used within the required range and accuracy, and applicable
prerequisites described in the test procedures were satisfied;
- test frequencies met TS requirements to demonstrate operability and reliability;
tests were performed in accordance with the test procedures and other
applicable procedures; jumpers and lifted leads were controlled and restored
where used;
- test data and results were accurate, complete, within limits, and valid;
- test equipment was removed after testing;
- where applicable for inservice testing activities, testing was performed in
accordance with the applicable version of Section XI, American Society of
Mechanical Engineers code, and reference values were consistent with the
system design basis;
- where applicable, test results not meeting acceptance criteria were addressed
with an adequate operability evaluation or the system or component was
declared inoperable;
- where applicable for safety-related instrument control surveillance tests,
reference setting data were accurately incorporated in the test procedure;
- where applicable, actual conditions encountering high resistance electrical
contacts were such that the intended safety function could still be accomplished;
- prior procedure changes had not provided an opportunity to identify problems
encountered during the performance of the surveillance or calibration test;
16 Enclosure
- equipment was returned to a position or status required to support the
performance of its safety functions; and
- all problems identified during the testing were appropriately documented and
dispositioned in the corrective action program.
Documents reviewed are listed in the Attachment to this report.
This inspection constituted six routine surveillance testing samples and two inservice
testing samples as defined in IP 71111.22, Sections -02 and -05.
b. Findings
Introduction: A green self-revealed finding and an NCV of Prairie Island Nuclear
Generating Plant Operating License DPR-42, Section C.1, was identified due to the
failure to maintain Unit 1 reactor power below the thermal power limitations stated in the
facility operating license.
Description: On January 2, 2009, operations personnel tested the 11 turbine-driven
auxiliary feedwater (TDAFW) pump using SP 1102, 11 TDAFW Pump Monthly Test.
While performing this test, the control room received an alarm and identified that Unit 1
thermal power had momentarily spiked above 100 percent. Step 4 of Annunciator
Response Procedure (ARP) 47013-0303 stated that the control room operators were
only required to take action to reduce thermal power if the last five minute thermal power
average exceeded 100 percent. Control room personnel checked the latest five minute
average and determined that the average was not greater than 100 percent. As a result,
no actions were taken to reduce Unit 1 reactor power.
Unit 1 thermal power continued to momentarily spike above 100 percent approximately
eight additional times during the TDAFW test, which was conducted over a 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />
period. Operations personnel documented this condition in CAP 1164293. The
inspectors reviewed the CAP and learned that the prior performances of SP 1102 were
conducted with the main turbine operating in the valve position control mode. This mode
of turbine operation allowed the position of the turbine control valves to remain relatively
unchanged even though a portion of the steam flowing to the turbine was diverted to
operate the 11 TDAFW pump. On January 2, 2009, operations personnel performed
SP 1102 with the main turbine operating in first stage pressure mode. This mode of
turbine operation allowed the control valves to move to maintain turbine first stage
pressure constant while diverting steam to the 11 TDAFW pump. This resulted in an
increase in reactor thermal power. The highest reactor power level achieved was
100.1 percent.
The inspectors reviewed ARP 47013-0303, Operating Procedure 1C1.4, Unit 1 Power
Operation, Section Work Instruction (SWI) O-50, Reactivity Management, NRC
Regulatory Issue Summary (RIS) 2007-21, Adherence of Licensed Power Limits, and
RIS 2007-21, Revision 1. The inspectors determined that the licensee had revised the
ARP, Operating Procedure 1C1.4, and SWI O-50 to more clearly define the term steady
state following the NRCs August 23, 2007, issuance of RIS 2007-21. The inspectors
determined that the document changes were non-conservative because they allowed
operations personnel to intentionally operate the reactor above the licensed thermal
power level for short periods of time.
17 Enclosure
The inspectors also reviewed the meeting minutes from a June 12, 2008, meeting
between the NRC and the Nuclear Energy Institute (NEI). During this meeting, the NRC
was concerned about how a proposed NEI position statement on maintenance of
licensed power limits would address a situation similar to the one that occurred at Prairie
Island on January 2, 2009. Individuals from NEI stated that situations such as the one
discussed above would be addressed by step 4.2.1 of the NEI Position Statement. The
NEI individuals also stated that if operations personnel found that core thermal power
was above the licensed limitation, action would be taken to reduce power below the
licensed limit in a timely manner even though the 2-hour average may still be below the
limit.
The inspectors reviewed the NEI Position Statement on the Licensed Power Limit
dated June 23, 2008. Step 4.2.1 of the Position Statement reads as follows:
No actions are allowed that would intentionally raise core thermal
power above the licensed power limit for any period of time.
Small, short-term fluctuations in power that are not under the
direct control of a licensed operator are not considered
intentional.
In addition, Section 4.4 of the NEI Position Statement documented that the following
actions constituted performance deficiencies:
- Intentional raising of reactor power above the licensed power limit, and
- Failure to take prudent action prior to a pre-planned evolution that could cause a
power increase to exceed the licensed power level.
Based upon discussions with licensee personnel, a review of plant data and procedures,
and the information provided above, the inspectors determined the performance of
SP 1102 was an activity that was under the direct control of the licensed operators. In
addition, the licensee failed to take prudent action to lower reactor power prior to
performing SP 1102 even though there was a potential that the performance of this test
could cause reactor power to exceed the licensed power level. Lastly, the inspectors
concluded that once operations personnel identified that Unit 1 was operating above the
licensed power limit, no action was taken to reduce Unit 1 power levels. The failure to
take action to reduce Unit 1 reactor power constituted intentional operation above the
licensed thermal power limit.
Analysis: The inspectors determined that the failure to operate the Unit 1 reactor in
accordance with Prairie Island Nuclear Generating Plant Facility Operating License
DPR-42, Section C.(1), Maximum Power Level, was a performance deficiency that
required an evaluation using the SDP. The inspectors determined that this issue was
more than minor because if left uncorrected the operation of the reactor beyond the
limits specified in the operating license could become a more significant safety concern
and was the direct result of intentional operation above the limit specified in the
operating license. The finding affected the Barrier Integrity Cornerstone for the fuel
barrier and the instances where the licensed thermal power limit was exceeded were of
short during and low peak values (i.e., 100.1 percent). The inspectors determined that
this issue was of very low safety significance (Green) because it only impacted the fuel
aspect of the Barrier Integrity Cornerstone and no core thermal limits were violated. The
inspectors determined that this finding was cross-cutting in the Human Performance,
18 Enclosure
Resources area because the licensee failed to have complete, accurate, and up-to-date
procedures regarding the maintenance of licensed thermal power levels (H.2(c)).
Enforcement: Section C.1 of Prairie Island Nuclear Generating Plant, Unit 1, Facility
Operating License DPR-42 states that the licensee is authorized to operate the facility at
steady state reactor core power levels not in excess of 1650 megawatts thermal.
Contrary to the above, on January 2, 2009, operations personnel operated the facility at
steady state reactor core power levels in excess of 1650 megawatts thermal.
Specifically, reactor core power levels momentarily spiked above 1650 megawatts
thermal nine times during the performance of SP 1102, 11 TDAFW Pump Monthly
Test. However, because this violation is of very low safety significance and was
entered into your corrective action program as CAP 1164293, it was treated as an NCV
consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000282/2009002-04).
Corrective actions for this issue included issuing operations guidance to ensure that
actions were taken to lower reactor power if power levels exceeded the limit specified in
the operating license, revising SWI O-50 to reflect that reactor power should be lowered
prior to performing tests that could cause unacceptable increases in reactor power, and
revising SP 1102 to provide guidance regarding potential impacts on reactor power
during the performance of this test.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation (71114.06)
.1 Training Observation
a. Inspection Scope
The inspector observed simulator training evolutions for licensed operators on
January 14 and February 5, 2009, which required emergency plan implementation by
an operations crew. This evolution was planned to be evaluated and included in
performance indicator data regarding drill and exercise performance. The inspectors
observed event classification and notification activities performed by the crew. The
focus of the inspectors activities was to note any weaknesses and deficiencies in the
crews performance and ensure that the licensee evaluators noted the same issues and
entered them into the corrective action program. As part of the inspection, the
inspectors reviewed the scenario package and other documents listed in the Attachment
to this report.
This training inspection constituted two samples as defined in IP 71114.06-05.
b. Findings
No findings of significance were identified.
19 Enclosure
4. OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
.1 Unplanned Scrams per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical
Hours performance indicator (PI) for Units 1 and 2 for the period from the first quarter of
2008 through the first quarter of 2009. To determine the accuracy of the PI data
reported during those periods, guidance contained in NEI Document 99-02, Regulatory
Assessment Performance Indicator Guideline, Revision 5, was used. The inspectors
reviewed the licensees operator narrative logs, corrective action program reports, event
reports and applicable NRC Inspection Reports to validate the accuracy of the
submittals. The inspectors also reviewed the licensees corrective action database to
determine if any problems had been identified with the PI data collected or transmitted
for this indicator. Documents reviewed are listed in the Attachment to this report.
This inspection constituted two unplanned scrams per 7000 critical hours samples as
defined in IP 71151-05.
b. Findings
No findings of significance were identified.
.2 Unplanned Scrams with Complications
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Scrams with
Complications PI for Units 1 and 2 for the period from the first quarter of 2008 through
the first quarter of 2009. To determine the accuracy of the PI data reported during those
periods, guidance contained in NEI Document 99-02, Regulatory Assessment
Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the
licensees operator narrative logs, corrective action program reports, event reports and
applicable NRC Inspection Reports to validate the accuracy of the submittals. The
inspectors also reviewed the licensees corrective action database to determine if any
problems had been identified with the PI data collected or transmitted for this indicator.
Documents reviewed are listed in the Attachment to this report.
This inspection constituted two unplanned scrams with complications samples as
defined in IP 71151-05.
b. Findings
No findings of significance were identified.
20 Enclosure
.3 Unplanned Transients per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Transients per 7000
Critical Hours PI for Units 1 and 2 for the period from the first quarter of 2008 through the
first quarter of 2009. To determine the accuracy of the PI data reported during those
periods, guidance contained in NEI Document 99-02, Regulatory Assessment
Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the
licensees operator narrative logs, corrective action program reports, event reports and
applicable NRC Inspection Reports to validate the accuracy of the submittals. The
inspectors also reviewed the licensees corrective action database to determine if any
problems had been identified with the PI data collected or transmitted for this indicator.
Documents reviewed are listed in the Attachment to this report.
This inspection constituted two unplanned transients per 7000 critical hours samples as
defined in IP 71151-05.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
.1 Routine Review of items Entered Into the Corrective Action Program
a. Scope
As part of the various baseline inspection procedures discussed in previous sections of
this report, the inspectors routinely reviewed issues during baseline inspection activities
and plant status reviews to verify that they were being entered into the licensees
corrective action program at an appropriate threshold, that adequate attention was being
given to timely corrective actions, and that adverse trends were identified and
addressed. Attributes reviewed included: the complete and accurate identification of the
problem; that timeliness was commensurate with the safety significance; that evaluation
and disposition of performance issues, generic implications, common causes,
contributing factors, root causes, extent of condition reviews, and previous occurrences
reviews were proper and adequate; and that the classification, prioritization, focus, and
timeliness of corrective actions were commensurate with safety and sufficient to prevent
recurrence of the issue. Minor issues entered into the licensees corrective action
program as a result of the inspectors observations are included in the attached List of
Documents Reviewed.
These routine reviews for the identification and resolution of problems did not constitute
any additional inspection samples. Instead, by procedure they were considered an
integral part of the inspections performed during the quarter and documented in
Section 1 of this report.
21 Enclosure
b. Findings
No findings of significance were identified.
.2 Daily Corrective Action Program Reviews
a. Scope
In order to assist with the identification of repetitive equipment failures and specific
human performance issues for follow-up, the inspectors performed a daily screening of
items entered into the licensees corrective action program. This review was
accomplished through inspection of the stations daily corrective action document
packages.
These daily reviews were performed by procedure as part of the inspectors daily plant
status monitoring activities and, as such, did not constitute any separate inspection
samples.
b. Findings
No findings of significance were identified.
4OA5 Other Activities
.1 (Closed) Unresolved Item 05000282/2008005-06; 05000306/2008005-06: Abnormal
Operating Procedure Entry Conditions
Introduction: The inspectors identified a Green finding and an NCV of TS 5.4.1 due to
the failure to implement Procedure FP-G-DOC-03, Procedure Use and Adherence.
The failure to implement FP-G-DOC-3 resulted in the failure to implement the
appropriate abnormal operating procedure following the uncontrolled insertion of control
rods on November 6, 2008.
Description: In NRC Inspection Report 2008005, the inspectors documented a concern
due to operations personnel not entering an abnormal operating procedure following
unexpected control rod movement into the reactor core. The inspectors reviewed
procedures and interviewed operations and training personnel and determined that the
operators had received training that fostered a philosophy that abnormal operating
procedures were not required to be entered if the cause of the abnormal operating
condition was known.
The inspectors reviewed Procedure FP-G-DOC-03 and found that step 4.1 defined
activities affecting quality as follows:
Activities that affect or reasonably could affect the safety-related
function of nuclear plant structures, systems, components, and
parts. Activities included are designing, purchasing, fabricating,
handling, shipping, storing, cleaning, erecting, installing,
inspecting, testing, operating, maintaining, repairing, refueling and
modifying.
22 Enclosure
In addition, step 5.1.1 of Procedure FP-G-DOC-03 required that all personnel shall
perform activities affecting quality using working copies of continuous or reference use
procedures.
The inspectors determined that the operation of the reactor following the uncontrolled
control rod insertion was an activity affecting quality. In addition, 2C5 AOP 2,
Uncontrolled Insertion of a Rod Control Cluster Assembly, was designated as a
continuous use procedure. Based upon the information discussed above, the inspectors
determined that the operators were procedurally required to have entered 2C5 AOP 2
following the unexpected control rod insertion.
Analysis: The inspectors concluded that the failure to follow Procedure FP-G-DOC-03
and enter 2C5 AOP 2 following the unexpected insertion of multiple control rods was a
performance deficiency that required an evaluation using the SDP. The inspectors
determined that this finding was more than minor because the failure to enter
procedures to respond to unexpected plant conditions could result in incorrect actions
being taken following a plant event (a more significant safety issue). This finding
affected the Initiating Events Cornerstone. The inspectors determined that this issue
was of very low safety significance because the finding was not a loss of coolant
accident initiator, was not an external events initiator, and would not have resulted in
both the likelihood of a reactor trip and that mitigating systems equipment would not
have been available. The inspectors determined that this finding was cross-cutting in
the Human Performance, Work Practices area because the licensee had not effectively
communicated expectations regarding procedural compliance following equipment
issues where the cause of the issue was known (H.4(b)).
Enforcement: Technical Specification 5.4.1 requires that written procedures be
established, implemented, and maintained covering the applicable procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
Section 1.d of Regulatory Guide 1.33, Revision 2, Appendix A requires that written
procedures be established, implemented and maintained regarding procedural
adherence.
Step 5.1.1 of Procedure FP-G-DOC-03, Procedure Use and Adherence, required that
all personnel shall perform activities affecting quality using working copies of continuous
or reference use procedures.
2C5 AOP 2, Uncontrolled Insertion of a Rod Control Cluster Assembly, was designated
as a continuous use procedure.
Contrary to the above, on November 6, 2008, operations personnel failed to
operate the Unit 2 reactor (an activity affecting quality) using Abnormal Operating
Procedure 2C5 AOP 2 following the uncontrolled insertion of multiple control rods.
However, because this violation is of very low safety significance (Green) and was
entered into your corrective action program as CAPs 1158505 and 1159133, it was
treated as an NCV consistent with Section VI.A.1 of the Enforcement Policy
(NCV 05000282/2009002-05;05000306/2009002-05). Corrective actions for this issue
included providing guidance to all operations personnel regarding the need to enter
abnormal operating procedures regardless of whether the cause of a condition is known
and revisions to licensed operator training.
23 Enclosure
.2 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the inspection period, the inspectors conducted observations of security force
personnel and activities to ensure that the activities were consistent with licensee
security procedures and regulatory requirements relating to nuclear plant security.
These observations took place during both normal and off-normal plant working hours.
These quarterly resident inspector observations of security force personnel and activities
did not constitute any additional inspection samples. Rather, they were considered an
integral part of the inspectors' normal plant status review and inspection activities.
b. Findings
No findings of significance were identified.
4OA6 Management Meetings
.1 Exit Meeting Summary
On April 8, 2009, the inspectors presented the inspection results to Mr. Michael Wadley
and other members of the licensee staff. The licensee acknowledged the issues
presented. The inspectors confirmed that none of the potential report input discussed
was considered proprietary.
4OA7 Licensee-Identified Violations
Cornerstone: Mitigating Systems
10 CFR Part 50, Appendix B, Criterion V, requires in part, that activities affecting
quality shall be accomplished in accordance with procedures appropriate to the
circumstance. Contrary to the above, on February 12, 2009, licensee personnel
failed to perform surveillance testing on the 12 Containment Spray Pump in
accordance with the surveillance procedure. Specifically, operations personnel failed
to adhere to procedural requirements regarding a 30 minute full flow time restriction
for the 12 Containment Spray Pump. In addition, operations personnel did not obtain
vibration readings at the specified reference points. These procedure compliance
failures resulted in the surveillance exceeding the 30 minute restriction by
approximately 1.5 minutes. Additionally, horizontal and axial vibration readings were
taken in an alternate location due to accessibility issues resulting from a scaffold.
Corrective actions for this issue included a procedure change and an evaluation of
the vibration data. The licensee entered this issue into the corrective action program
as CAP 1169248.
ATTACHMENT: SUPPLEMENTAL INFORMATION
24 Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
M. Wadley, Site Vice President
J. Sorensen, Director Site Operations
K. Ryan, Plant Manager
T. Allen, Business Support Manager
J. Anderson, Regulatory Affairs Manager
L. Clewett, Operations Manager
B. Flynn, Safety and Human Performance Manager
R. Hite, Radiation Protection and Chemistry Manager
D. Kettering, Site Engineering Director
R. Madjerich, Production Planning Manager
J. Muth, Nuclear Oversight Manager
S. Northard, Performance Improvement Manager
M. Schmidt, Maintenance Manager
J. Sternisha, Training Manager
Nuclear Regulatory Commission
J. Giessner, Reactor Projects Branch 4 Chief
T. Wengert, Office of Nuclear Reactor Regulation Project Manager
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
05000282/2009002-01; FIN Failure to Protect Fire Protection Equipment from Effects of
05000306/2009002-01 Extreme Cold Temperatures (Section 1R01.1)05000282/2009002-02; NCV Failure to Follow Procedures During Performance of
05000306/2009002-02 Operability Evaluations (Section 1R15.1)05000306/2009002-03 FIN Failure to Follow Procedure During D5 Post-Maintenance
Testing (Section 1R19.1)05000282/2009002-04 NCV Failure to Adhere to Licensed Power Level Specified in
Operating License (Section 1R22.1)05000282/2009002-05; NCV Failure to Follow Procedure Use and Adherence Procedure
05000306/2009002-05 Following Receipt of Abnormal Operating Procedure Entry
Condition (Section 4OA5.1)
Closed
05000282/2009002-01; FIN Failure to Protect Fire Protection Equipment from Effects of
05000306/2009002-01 Extreme Cold Temperatures (Section 1R01.1)05000282/2009002-02; NCV Failure to Follow Procedures During Performance of
05000306/2009002-02 Operability Evaluations (Section 1R15.1)
1 Attachment
05000306/2009002-03 FIN Failure to Follow Procedure During D5 Post-Maintenance
Testing (Section 1R19.1)05000282/2009002-04 NCV Failure to Adhere to Licensed Power Level Specified in
Operating License (Section 1R22.1)05000282/2009002-05 NCV Failure to Follow Procedure Use and Adherence Procedure
05000306/2009002-05 Following Receipt of Abnormal Operating Procedure Entry
Condition (Section 4OA5.1)05000282/2008005-06; URI Abnormal Operating Procedure Entry Conditions05000306/2008005-06 (Section 4OA5.1)
Discussed
None
2 Attachment
LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC inspectors reviewed the documents in their entirety but rather that
selected sections of portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
1R01 Adverse Weather
- Department Clock Reset Yellow Sheet; no date
- Human Performance Investigation Report; no date
- Operating Procedure C37.5; Screenhouse Normal Ventilation; Revision 7
- Test Procedure 1637; Winter Plant Operations; Revision 39
- CAP 1167617; Inappropriate Guidance Given to Verify Winter Preparedness;
January 31, 2009
- Operating Instruction 09-06; no date
- Administrative Work Instruction 5AWI 15.5.1; Plant Equipment Control Process; Revision 27
- CAP 1135065; 21 Non-Safeguards Screenhouse Vent Trouble Light Lit During Operation;
April 21, 2008
1R04 Equipment Alignment
- C37.11; Chilled Water Safeguard System Operation; Revision 21
- C37.11.1Chilled Water Safeguards System; Revision 18
- Integrated Checklist C1.1.20.7-5; D2 Diesel Generator Valve Status; Revision 20
- Integrated Checklist C1.1.20.7-6; D2 Diesel Generator Auxiliaries and Room Cooling Local
Panels; Revision 10
- Integrated Checklist C1.1.20.7-7; Diesel Generator D2 Main Control Room Switch and
Indicating Light Status; Revision 13
- Integrated Checklist C1.1.20.7-8; D2 Diesel Generator Circuit Breakers and Panel Switches;
Revision 16
- C28.2; Auxiliary Feedwater System - Unit 1; Revision 44
- C1.1.35-3; Cooling Water System; Revision 28
1R05 Fire Protection
- Safe Shutdown Analysis
- Fire Hazards Analysis
- Procedure F5, Appendix A; Fire Plan Maps; Various Revisions
1R07 Heat Sinks
- CAP 1166096; D1 Lube Oil Heat Exchanger Inspection Results; January 20, 2009
- PINGP 1066; Cooling Water/Fire Protection or Cooling Water Heat Exchanger Inspection
Reports; January 19, 2009
- Calculation ENG-ME-479; Tube Plugging Criteria for Unit 1 Diesel Generator Heat
Exchangers; Revision 1
- D1 Heat Exchanger Eddy Current Test Results; January 2007
3 Attachment
- Electric Power Research Institute Document NP-7552; Heat Exchanger Performance
Monitoring Guidelines; December 1991
1R11 Licensed Operator Requalification
- P9160S-001 Attachment SQ-61; Simulator Cycle Quiz #61; Revision 0
1R12 Maintenance Effectiveness
- QF-0739; Response to NRC Questions on Screenhouse Ventilation System; March 12, 2009
- QF-0739; Response to NRC Questions regarding Maintenance Rule Scoping for Screenhouse
Ventilation System; March 9, 2009
1R13 Maintenance Risk Assessment and Emergent Work
- Operating Procedure 1C20.5; Unit 1 - 4.16Kv System; Revision 15
- SP 2118; Verifying Paths from the Grid to the Unit 2 Buses; Revision 27
1R15 Operability Evaluations
- WO 376103; Contingency for Venting Gas from Piping
- WO 376103-01; Work Plan to Vent Air from the Common RHR Piping from the RCS Hot Legs
- CAP 1165976; Gas Void Found at Location 1RH-04; January 19, 2009
- CAP 52302; RHR Hot Leg Suction Piping Water Hammer Event; January 9, 1999
- CAP 1166196; Mobilgear 629 Oil Inadvertently Added to Charging Pump; January 21, 2009
- Mobil SHC 600 Series Product Specification (#629 Synthetic Lubricant)
- Mobil 600 Series Product Specification (#629 Lubricant)
- CAP 1164489; 22 TDAFW Pump Vibration Increasing; January 6, 2009
- CAP 1162312; 122 Control Room Chilled Water Pump Has Pump Outboard Bearing High
Vibes; December 12, 2008
- SP 1161B; Control Room Train B Chilled Water Pump Quarterly Test ; Revision 11
- CAP 1165083 As Found Voltage Outside of Acceptable Range During Performance of
MCC PE-G7 for Breaker 222E-3; January 9, 2009
- PE MCC-G7; MCC Electrical Preventive Maintenance for GE7700 Line MCCS; Revision 26
- CAP 1169673; D5 Engine 2 Cylinder 5B Cotter Pin Missing; February 17, 2009
- CAP 1169761; D5 Engine 1 Cylinders 4B and 5B Cotter Pins Missing; February 17, 2009
- CAP 1169673/1169761 Past Operability Review
- WO 351271; Replace Specific D5 Pistons and Cylinders
- CAP 1169673/1169761; FME Recovery Plan
- CAP 1166196; Mobilgear 629 Oil Inadvertently Added to Charging Pump; January 21, 2009
- Mobil SHC 600 Series Product Data Sheet
- Mobil 600 Series Product Data Sheet
1R19 Post-maintenance Testing
- PM 3001-2-D1; D1 Diesel Generator Inspection (034-011); Revision 25
- CAP 1166428; Loose Bolting Found on D1 After Step Signed Off as Complete;
January 22, 2009
- WO 327265-10; Verify Torque on D1 Components; January 22, 2009
- PINGP 1631; Safety Issues Stop Work Form (Sign-off of D1 PM Without Work Being
Completed); January 22, 2009
4 Attachment
- CAP 1166428-02; Maintenance Rework Evaluation - D1 Vertical Drive Inspection Cover
Loose Bolting; no date
- CAP 1166428; Department Clock Reset - Yellow Sheet; January 28, 2009
- WO 377710; Troubleshooting Log; January 25, 2009
- WO 377710; D1 Diesel Generator Tripped on High Crankcase Pressure
- CAP 1166680; D1 High Crankcase Pressure Trip During PMT Activities; January 25, 2009
- CAP 1164948; Fairbanks Morse Unable to Supply Technical Representative Services for D1;
January 9, 2009
- CAP 1165574; D1 Work Removed from Work Window 0903 at T-1 Due to Organization
Misalignment; January 15, 2009
- CAP 1166484; D1 Liner Replacement Complex Work Plan for Work Window 0916;
January 23, 2009
- Administrative Work Instruction 5AWI 3.15.10; Emergency Diesel Generator Compensatory
Measures; Revision 1
- SP 1118; Verifying Paths from the Grid to Unit 1 Buses; Revision 22
- SP 2118; Verifying Paths from the Grid to Unit 2 Buses; Revision 27
- CAP 1167727; Unexpected LCO Entry - Blue Channel OPDT Setpoint; February 2, 2009
- WO 378143; 2TM-403V Delta T SP2 Calculator Special Summing Amp
- WR 42509; 2TM-403V OPDT Summing Unit Failed at 50% with 2 Bistables
- Work Plan 378143-01; Replace Summing Amplifier 2TM-403V; Revision 000
- WO 97368; Perform PMT / RTS Testing for 21 Cooling Water Strainer
- CAP 1169378; 21 Cooling Water Strainer Time Delay Relay Tested Outside Range
- WR 42859; 21 Cooling Water Strainer Time Delay Relay Tested Outside Range
- OPR 1165620; 21 Cooling Water Strainer Backwash Valve Failed to Open in the Required
Time
- NRC Information Notice 2008-05; Fires Involving Emergency Diesel Generator Exhaust
Manifolds; April 12, 2008
- 1C20.7 AOP 1; Failure of D1 or D2 Lube Oil Keep Warm System; Revision 6
- FP-G-DOC-03; Procedure Use and Adherence; Revision 5
- FP-WM-WOE-01; Work Order Execution Process; Revision 3
- CAP 1170902; D5 Engine 1 Coolant Vent Line Has Fretting On Pipe; February 26, 2009
- FP-PA-ARP-01; CAP Action Request Process; Revision 21
1R22 Surveillance Test
- SP 1095; Bus 16 Load Sequencer Test; Revision 24
- WO 357241; SP 1095 Bus 16 Load Sequencer Test
- SP 1047; Control Rod Quarterly Exercise (Unit 2); Revision 36
- WO 357246; SP 1047 Control Rod Quarterly Exercise
- SP 2095; Bus 26 Load Sequencer Test; Revision 23
- WO 358531; SP 2095 Bus 26 Load Sequencer Monthly Test
- SP 1101; 12 Motor-Driven Auxiliary Feedwater Pump Quarterly Flow and Valve Test;
Revision 49
- WO 371230; 12 Motor-Driven Auxiliary Feedwater Pump Quarterly Flow and Valve Test
- SP 1090B; 12 Containment Spray Pump Quarterly Test; Revision 15
- WO 358919; 12 Containment Spray Pump Quarterly Test
- CAP 1169248; SP 1090B Not Completed Due to Exceeding 30 Minute Time Limit;
February 12, 2009
- CAP 1169333; Containment Spray Pump Surveillance Procedure 30 Minute Time Limit Places
Undue Time Pressure on Operations.
- CAP 1169342; 12 CS Pump Discharge Pressure Gauge Root Valve; February 13, 2009
5 Attachment
- CAP 1171730; Vibration On 12 CS Pump Showing Adverse Trend; March 04, 2009
- FP-G-DOC-03; Procedure Use and Adherence; Revision 5
- FP-G-DOC-04; Procedure Processing; Revision 8
- H10.1; ASME Inservice Testing Program; Revision 23
- WO 359161; SP 1335 D2 Diesel Generator 18-Month 24-Hour load Test
- SP 1335; D2 Diesel Generator 18-Month 24-Hour Load Test; Revision 9
- CAP 1168913; Load Transient While Performing SP 1335 D2 24-Hour Test;
February 11, 2009
- Control Room Operating Logs; January 2, 2009
- NEI Letter from John C. Butler to Timothy J. Kobetz, NRC; NEI Position Statement on the
Licensed Power Limit; dated June 23, 2008
- NRC Memorandum from Timothy Kolb to Timothy J. Kobetz; Summary of RIS 2007-21,
Adherence of Licensed Power Limits, Working Group Meeting with NEI to Discuss NEI
Guidance Document, Draft Revision 6 and NRC Comments; July 2, 2008
1EP6 Emergency Preparedness Drills
- P9160S-001 DEP 1; Cycle 08G DEP Scenario; Revision 0
4OA2 Identification and Resolution of Problems
- CAP 1164401; OPR 01163835 Does Not Include All Uncertainties (GL-08-01);
January 5, 2009
- CAP 1164691; NRC Concern on LER 2-08-01 (CC/HELB); January 7, 2009
- CAP 1164836; D5 and D6 Fuel Oil Drain Valves Leaking By; January 8, 2009
- CAP 1164893; Evaluate Potential for Insulation Issue Due to Ongoing Work; January 9, 2009
- CAP 1164930; Operator Response to Fire Scenario Did Not Match F5 Appendix B;
January 9, 2009
- CAP 1165467; NRC License Renewal Walkdown Fuel Oil System Observation;
January 14, 2009
- CAP 1165460; NRC license Renewal Walkdown Fuel Oil System 22 DDCLP; January 14,
- CAP 1165453; NRC license Renewal Walkdown Fuel Oil Minor Leakage D2 Day Tank;
January 14, 2009
- CAP 1165424; NRC License Renewal Walkdown FO-2-4 Leakage; January 14, 2009
- CAP 1165352; NRC Question on Calculation GEN-PI-055 Timing; January 14, 2009
4OA7 Licensee-Identified Findings
- CAP 1169248; SP 1092B Not Completed Due to Exceeding 30 Minute Time Limit;
February 12, 2009
6 Attachment
LIST OF ACRONYMS USED
ADAMS Agencywide Document Access Management System
ARP Annunciator Response Procedure
CAP Corrective Action Program Document
CFR Code of Federal Regulations
DRP Division of Reactor Projects
LCO Limiting Condition for Operation
NCV Non-Cited Violation
NEI Nuclear Energy Institute
NRC U.S. Nuclear Regulatory Commission
PARS Publicly Available Records
PI Performance Indicator
PMT Post-Maintenance Test
RIS Regulatory Issue Summary
SDP Significance Determination Process
SP Surveillance Procedure
SWI Section Work Instruction
TDAFW Turbine-Driven Auxiliary Feedwater
TS Technical Specifications
USAR Updated Safety Analysis Report
7 Attachment