ML063130383
ML063130383 | |
Person / Time | |
---|---|
Site: | Wolf Creek |
Issue date: | 11/09/2006 |
From: | Geoffrey Miller NRC/RGN-IV/DRP/RPB-B |
To: | Muench R Wolf Creek |
References | |
IR-06-004 | |
Download: ML063130383 (37) | |
See also: IR 05000482/2006004
Text
November 9, 2006
Rick A. Muench, President and
Chief Executive Officer
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS 66839
SUBJECT: WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION
REPORT 05000482/2006004
Dear Mr. Muench:
On October 7, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at your Wolf Creek Generating Station. The enclosed integrated report documents the
inspection findings which were discussed on October 6, 2006, with Mr. S. E. Hedges, Vice
President Operations and Plant Manager, and other members of your staff.
This inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
Within these areas, the inspection consisted of selected examination of procedures and
representative records, observation of activities, and interviews with personnel.
This report documents one NRC-identified finding and two self-revealing findings of very low
safety significance (Green). All of these findings were determined to involve violations of NRC
requirements. Additionally, two licensee-identified violations which were determined to be of
very low safety significance (Green), are listed in Section 4OA7 of this report. The NRC is
treating these violations as noncited violations consistent with Section VI.A.1 of the NRC
Enforcement Policy because of the very low safety significance and because the findings were
entered into your corrective action program. If you contest these noncited violations or the
significance of these noncited violations, you should provide a response within 30 days of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional
Administrator, U.S. Nuclear Regulatory Commission Region IV, 611 Ryan Plaza Dr, Suite 400,
Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Wolf Creek
Generating Station.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, your response (if any) will be made available electronically for public inspection in
the NRC Public Document Room or from the Publicly Available Records component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Wolf Creek Nuclear Operating Corporation -2-
Should you have any questions concerning this inspection, we will be pleased to discuss them
with you.
Sincerely,
/RA/
Geoffrey B. Miller, Chief
Project Branch B
Division of Reactor Projects
Docket: 50-482
License: NPF-42
Enclosure:
NRC Inspection Report 05000482/2006004
w/attachment: Supplemental Information
cc w/enclosure:
Vice President Operations/Plant Manager
Wolf Creek Nuclear Operating Corp.
P.O. Box 411
Burlington, KS 66839
Jay Silberg, Esq.
Pillsbury Winthrop Shaw Pittman LLP
2300 N Street, NW
Washington, DC 20037
Supervisor Licensing
Wolf Creek Nuclear Operating Corp.
P.O. Box 411
Burlington, KS 66839
Chief Engineer
Utilities Division
Kansas Corporation Commission
1500 SW Arrowhead Road
Topeka, KS 66604-4027
Office of the Governor
State of Kansas
Topeka, KS 66612
Wolf Creek Nuclear Operating Corporation -3-
Attorney General
120 S.W. 10th Avenue, 2nd Floor
Topeka, KS 66612-1597
County Clerk
Coffey County Courthouse
110 South 6th Street
Burlington, KS 66839-1798
Chief, Radiation and Asbestos
Control Section
Kansas Department of Health and
Environment
Bureau of Air and Radiation
1000 SW Jackson, Suite 310
Topeka, KS 66612-1366
Chief, Radiological Emergency
Preparedness Section
Kansas City Field Office
Chemical and Nuclear Preparedness
and Protection Division
Dept. of Homeland Security
9221 Ward Parkway
Suite 300
Kansas City, MO 64114-3372
Wolf Creek Nuclear Operating Corporation -4-
Electronic distribution by RIV:
Regional Administrator (BSM1)
DRP Director (ATH)
DRS Director (DDC)
DRS Deputy Director (RJC1)
Senior Resident Inspector (SDC)
SRI, Callaway (MSP)
Branch Chief, DRP/B (GBM)
Senior Project Engineer, DRP/B (FLB2)
Team Leader, DRP/TSS (RVA)
RITS Coordinator (KEG)
J. Lamb, OEDO RIV Coordinator (JGL1)
ROPreports
WC Site Secretary (SLA2)
W. A. Maier, RSLO (WAM)
R. E. Kahler, NSIR (REK)
SUNSI Review Completed: __gbm___ ADAMS: : Yes G No Initials: __gbm__
- Publicly Available G Non-Publicly Available G Sensitive : Non-Sensitive
R:\_REACTORS\_WC\2006\WC2006-04RP-SDC.wpd
SRI:DRP/B RI:DRP/B SRA:DRS C:DRS/OB C:DRS/PSB
SDCochrum:sa JRGroom RLBywater RLNease MPShannon
E - GBMiller E - GBMiller /RA/ /RA/ /RA/
11/9/06 11/8/06 11/3/06 11/2/06 11/3/06
C:DRS/EB2 C:DRS/EB1 C:DRP/B
LJSmith JAClark GBMiller
/RA/ /RA/ /RA/
11/7/06 11/3/06 11/9/06
OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket: 50-482
License: NPF-42
Report: 05000482/2006004
Licensee: Wolf Creek Nuclear Operating Corporation
Facility: Wolf Creek Generating Station
Location: 1550 Oxen Lane NE
Burlington, Kansas
Dates: July 8 through October 7, 2006
Inspectors: S. D. Cochrum, Senior Resident Inspector
T. B. Rhoades, Resident Inspector
J. R. Groom, Resident Inspector
P. J. Elkmann, Emergency Preparedness Inspector
M. E. Murphy, Senior Operations Engineer
Approved By: G. B. Miller, Chief, Project Branch B
-1- Enclosure
TABLE OF CONTENTS
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 12
1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18
1EP4 Emergency Action Level and Emergency Plan Changes . . . . . . . . . . . . . . . . . 19
1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21
4OA3 Follow-up of Events and Notices of Enforcement Discretion . . . . . . . . . . . . . . 23
4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
4OA7 Licensee-Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
LIST OF ITEMS OPENED AND CLOSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-5
-2- Enclosure
SUMMARY OF FINDINGS
IR 05000482/2006004; 07/08/06 - 10/7/06; Wolf Creek Generating Station; Operability
Evaluations, Identification and Resolution of Problems, and Event Follow-up.
This report covered a 3-month inspection by resident and health physics inspectors. The
inspection identified three Green findings, all of which were noncited violations. The
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the
significance determination process does not apply may be Green or be assigned a severity
level after NRC management review. The NRCs program for overseeing the safe operation of
commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process,"
Revision 3, dated July 2000.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Initiating Events
- Green. The inspectors reviewed a self-revealing noncited violation of Technical
Specification 5.4.1.a involving the licensee's failure to follow a procedure that
resulted in a loss of coolant charging flow during a planned surveillance. The
licensee entered this issue into their corrective action program as Condition
Report 2006-0002030.
The failure to follow station procedures was considered a performance
deficiency. This finding was more than minor because it affected the human
performance attribute of the initiating events cornerstone and the cornerstone
objective to limit the likelihood of those events that upset plant stability and
challenge critical safety functions. Using Manual Chapter 0609, Significance
Determination Process, Phase 1 worksheets, this finding screened to a Phase 2
analysis because it affected both the initiating events and mitigating system
cornerstones. The inspectors performed a Phase 2 analysis using Appendix A,
"Technical Basis For At Power Significance Determination Process," of Manual
Chapter 0609, "Significance Determination Process," and the Phase 2
worksheets for the Wolf Creek Generating Station. Based on the results of the
Phase 2 analysis, the finding is determined to have very low safety significance.
The inspectors also determined that the finding has crosscutting aspects in the
area of human performance associated with work practices because the
operators failure to use appropriate human error prevention techniques, such as
self-checking, peer-checking, and the operators choice to proceed in the face of
uncertainty, resulted in a loss of coolant charging flow (Section 4OA3).
-3- Enclosure
Cornerstone: Mitigating Systems
- Green. The inspectors identified a noncited violation of 10 CFR Part 50,
Appendix B, Criterion V, regarding the failure to implement administrative
Procedure AP 28-011, Resolving Deficiencies Impacting SSCs, Revision 1.
Procedure AP 28-011 requires that, during the operability determination process,
a reasonable expectation must exist that the structure, system, or component is
operable and that the prompt determination process will support that expectation.
Contrary to this requirement, reasonable expectation was not established for a
deficiency affecting safety-related Barton pressure transmitters. The licensee
entered this issue into their corrective action program as Condition Report 2006-
000895.
The failure to implement Procedure AP 28-011 following identification of a
potential degraded condition was a performance deficiency. This finding was
more than minor because it affected the equipment performance attribute of the
mitigating systems cornerstone and the cornerstone objective to ensure the
availability, reliability, and capability of systems that respond to initiating events.
Using Manual Chapter 0609, Significance Determination Process, Phase 1
worksheets, the inspectors determined that the finding is of very low significance
because it did not represent a loss of a safety function or operability and was not
potentially risk significant due to external events. The inspectors also
determined that this finding has crosscutting aspects in the human performance
area associated with decision making in that the licensee failed to use
conservative assumptions in decision making and verify the validity of underlying
assumptions for operability of the pressure transmitters, which resulted in
indeterminate pressure transmitters remaining in service (Section 1R15).
Cornerstone: Barrier Integrity
- Green. A self-revealing noncited violation of Technical Specification 5.4.1.a was
identified for the failure to close Valves EC-V025 and -V033 during a lineup to
recirculate the refueling water storage tank through the spent fuel pool cleanup
system. These two systems were cross-connected for approximately 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />,
which resulted in approximately 1200 gallons of spent fuel pool water being
inadvertently transferred to the refueling water storage tank. The licensee
entered this issue into their corrective action program as Condition Report 2006-
000589.
The failure to completely close Valves EC-V025 and -V033 was a performance
deficiency. This finding is more than minor because it is associated with the
barrier integrity cornerstone attribute of configuration control and affected the
cornerstone objective to maintain functionality of the spent fuel pool system.
Using Manual Chapter 0609, Significance Determination Process, Phase 1
worksheets, the inspectors determined that the finding is only of very low
significance because the finding only affected the barrier function of the spent
fuel pool. The inspectors also determined that the finding has crosscutting
aspects in the area of human performance associated with work practices
-4- Enclosure
because the operators failed to use appropriate human error prevention
techniques, such as peer-checking and not proceeding in the face of uncertainty.
This led to 1200 gallons of spent fuel pool water being inadvertently transferred
to the refueling water storage tank (Section 4OA2.2)
B. Licensee-Identified Violations
Violations of very low safety significance, which were identified by the licensee have
been reviewed by the inspectors. Corrective actions taken or planned by the licensee
have been entered into the licensees corrective action program. These violations and
corrective actions are listed in Section 4OA7 of this report.
-5- Enclosure
REPORT DETAILS
Summary of Plant Status
The plant started the inspection period at 100 percent rated thermal power. On September 24,
2006, the licensee reduced reactor power to 97 percent to replace a seal on heater drain
Pump B for planned maintenance. After completion of maintenance on September 29, 2006,
the reactor was returned to 100 percent power. On October 1, 2006, the licensee reduced
reactor power to 97 percent to replace a seal on heater drain Pump A for planned maintenance.
After completion of maintenance on October 4, 2006, the reactor was returned to 100 percent
power and remained at or near this power level until October 7, 2006, when the Wolf Creek
Generating Station main output breakers were opened to begin Refueling Outage 15.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R01 Adverse Weather Protection (71111.01)
Readiness for Seasonal Susceptibilities
a. Inspection Scope
The inspectors completed a review of the licensee's readiness of seasonal
susceptibilities involving high outdoor temperatures. The inspectors: (1) reviewed plant
procedures, the Updated Safety Analysis Report (USAR), and Technical
Specifications (TS) to ensure that operator actions defined in adverse weather
procedures maintained the readiness of essential systems; (2) walked down portions of
affected systems to ensure that adverse weather protection features were sufficient to
support operability, including the ability to perform safe shutdown functions;
(3) evaluated operator staffing levels to ensure the licensee would maintain the
readiness of essential systems required by plant procedures; and (4) reviewed the CAP
to determine if the licensee identified and corrected problems related to adverse
weather conditions.
C July 19, 2006, verification of the licensees preparations for impending high
outdoor temperatures and response to increasing cooling lake temperatures.
Documents reviewed by the inspectors included:
- Procedure GEN HW-001, Hot Weather Operation, Revision 2
- Procedure C-KC303, ESWS Pumphouse Concrete Neat Line Plan at EL 2000,
Revision 17
- Procedure SYS EF-205, ESW/CIRC Water Cold Weather Operations,
Revision 17
- Procedure STN EF-020A, ESW Train A Warming Line Verification, Revision 3
-6- Enclosure
- Procedure J-K4EF99, Non-Process Connected and In Line Electrical
Instruments, Revision 4
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment (71111.04)
Partial System Walkdowns
a. Inspection Scope
The inspectors: (1) walked down portions of the risk important systems listed below and
reviewed plant procedures and documents to verify that critical portions of the selected
systems were correctly aligned; and (2) compared deficiencies identified during the
walkdown to the licensee's USAR and CAP to ensure problems were being identified
and corrected.
C July 27, 2006, Train A residual heat removal during a Train B residual heat
removal outage
C August 15, 2006, Train A essential service water during a Train B essential
service water outage
Documents reviewed by the inspectors included:
- Checklist CKL EJ-120, RHR Normal System Lineup, Revision 34
- Drawing M-13EJ01, Piping Isometric Residual Heat Removal System Auxiliary
Bldg Train A, Revision 13
- Checklist CKL EF-120, Essential Service Water Valve, Breaker and Switch
Lineup, Revision 40
- Drawing SK-M-13EF06, Piping Isometric Essential Service Water SYS. Aux.
BLD. A & B Train Supply and Return, Revision E
- Drawing M-13EF02, Piping Isometric Essential Service Water SYS Aux. Bldg. A
Train Supply, Revision 9
- Wolf Creek Generating Station USAR, Revision 19
The inspectors completed two samples.
-7- Enclosure
b. Findings
No findings of significance were identified
1R05 Fire Protection (71111.05)
.1 Quarterly Inspection
a. Inspection Scope
The inspectors walked down the plant areas listed below to assess the material
condition of active and passive fire protection features and their operational lineup and
readiness. The inspectors: (1) verified that transient combustibles and hot work
activities were controlled in accordance with plant procedures; (2) observed the
condition of fire detection devices to verify they remained functional; (3) observed fire
suppression systems to verify they remained functional; (4) verified that fire
extinguishers and hose stations were provided at their designated locations and that
they were in a satisfactory condition; (5) verified that passive fire protection features
(electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration
seals, and oil collection systems) were in a satisfactory material condition; (6) verified
that adequate compensatory measures were established for degraded or inoperable fire
protection features and that the compensatory measures were commensurate with the
significance of the deficiency; and (7) reviewed the CAP to determine if the licensee
identified and corrected fire protection problems.
- July 26, 2006, boron thermal regeneration system letdown heat exchanger room,
1976 level of the auxiliary building
- July 26, 2006, boric acid tank Rooms A and B, 1976 level of auxiliary building
- July 27, 2006, Train B residual heat removal heat exchanger room
- July 27, 2006, pipe chase room, 1988 level of the auxiliary building
- August 16, 2006, control building, 2073 level
- September 29, 2006, turbine building, 2033 level
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed six samples.
b. Findings
No findings of significance were identified.
-8- Enclosure
.2 Annual Inspection
a. Inspection Scope
On July 24, 2006, the inspectors observed a fire brigade drill to evaluate the readiness
of licensee personnel to prevent and fight fires, including the following aspects: (1) the
number of personnel assigned to the fire brigade, (2) use of protective clothing, (3) use
of breathing apparatuses, (4) use of fire procedures and declarations of emergency
action levels, (5) command of the fire brigade, (6) implementation of prefire strategies
and briefs, (7) access routes to the fire and the timeliness of the fire brigade response,
(8) establishment of communications, (9) effectiveness of radio communications,
(10) placement and use of fire hoses, (11) entry into the fire area, (12) use of firefighting
equipment, (13) searches for fire victims and fire propagation, (14) smoke removal,
(15) use of prefire plans, (16) adherence to the drill scenario, (17) performance of the
evaluators critique, and (18) restoration from the fire drill. The licensee simulated a fire
in the station service transformer.
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance (71111.07)
a. Inspection Scope
The inspectors reviewed Wolf Creek programs, verified performance tests against
industry standards, and reviewed critical operating parameters and maintenance records
for the containment heat exchangers. The inspectors verified that: (1) performance
tests were satisfactorily conducted for the heat exchangers and reviewed for problems
or errors; (2) Wolf Creek utilized the periodic maintenance method outlined in Electric
Power Research Institute NP-7552, Heat Exchanger Performance Monitoring
Guidelines; and (3) the containment cooling system was correctly categorized under the
maintenance rule.
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
-9- Enclosure
1R11 Licensed Operator Requalification Program (71111.11)
.1 Biennial Review
a. Inspection Scope
This inspection was held during the 2006 biennial examination testing cycle. The
inspectors reviewed the overall pass/fail results of the individual job performance
measure operating tests, simulator operating tests, and written examinations
administered by the licensee during the operator licensing requalification cycles and
biennial examination. Eighteen crews participated in simulator operating tests, and job
performance measure operating tests, totaling 49 licensed operators.
During the inspection, the NRC inspectors reviewed and observed biennial examination
simulator job performance measures, in-plant job performance measures, the simulator
static examination, written examination, licensed operator classroom instruction, and the
plant control room crew. They also reviewed a sample of licensed operator annual
medical forms and procedures governing the medical examination process.
The inspectors assessed the methods and effectiveness of the licensees processes
for revising and maintaining its licensed operator requalification training program up to
date, including the use of feedback from plant events and industry experience
information. The inspectors reviewed the licensees training review group activities,
including the licensees ability to assess the effectiveness of its licensed operator
requalification training program and their ability to implement appropriate corrective
actions. This evaluation was performed to verify compliance with 10 CFR 55.59c,
"Requalification Program Requirements," and the licensees site access training
program.
The inspectors also assessed the adequacy and effectiveness of the remedial training
conducted since the previous biennial requalification examinations and the training from
the current examination cycle to ensure that they addressed weaknesses in licensed
operator or crew performance identified during training and plant operations. The
inspectors reviewed remedial training procedures and individual remedial training plans.
This evaluation was performed in accordance with 10 CFR 55.59c, "Requalification
Program Requirements," and with respect to the licensees site access training
program.
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
-10- Enclosure
.2 Resident Inspector Quarterly Review
a. Inspection Scope
The inspectors observed testing and training of senior reactor operators and reactor
operators to identify deficiencies and discrepancies in the training, to assess operator
performance, and to assess the evaluator's critique during the training scenarios listed
below.
- June 2, 2006, loss of shutdown cooling
- August 30, 2006, steam generator tube rupture with a loss of instrument air
Documents reviewed by the inspectors included:
- Simulator Scenario LR5004003 006, loss of RHR
Simulator Scenario LR5004010 000, intersystem LOCA
- Operations Requalification Cycle 06-05 schedule, Revision 000
- Procedure AP 21-001, Conduct of Operations, Revision 36
The inspectors completed two samples.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
Resident Inspector Quarterly Review
a. Inspection Scope
The inspectors reviewed the maintenance activities listed below to: (1) verify the
appropriate handling of structure, system, and component (SSC) performance or
condition problems; (2) verify the appropriate handling of degraded SSC functional
performance; (3) evaluate the role of work practices and common cause problems; and
(4) evaluate the handling of SSC issues reviewed under the requirements of the
maintenance rule, 10 CFR Part 50, Appendix B, and the TSs.
- August 2, 2006, Tcold wide-range temperature instrument, Work Order 06-056523
- August 11, 2006, stator cooling water system, Function CE-01
Documents reviewed by the inspectors included:
- Engineering Desktop Instruction EDI 23M-050, Monitoring Performance to
Criteria and Goals, Revision 3
-11- Enclosure
- PIR 2005-2152
- Work Order 06-056523
The inspectors completed two samples.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
a. Inspection Scope
Risk Assessment and Management of Risk
The inspectors reviewed the assessment activities listed below to verify:
(1) performance of risk assessments when required by 10 CFR 50.65 (a)(4) and
licensee procedures prior to changes in plant configuration for maintenance activities
and plant operations; (2) the accuracy, adequacy, and completeness of the information
considered in the risk assessment; (3) that the licensee recognizes, and/or enters as
applicable, the appropriate licensee-established risk category according to the risk
assessment results and licensee procedures; and (4) that the licensee identified and
corrected problems related to maintenance risk assessments.
- August 14-19, 2006, Train B essential service water outage and Train B
emergency diesel generator outage
- September 5-8, 2006, Train A residual heat removal pump and Train A coolant
charging pump outage
Documents reviewed by the inspectors are listed in the attachment.
Emergent Work Control
The inspectors: (1) verified that the licensee performed actions to minimize the
probability of initiating events and maintained the functional capability of mitigating
systems and barrier integrity systems; (2) verified that emergent work-related activities
such as troubleshooting, work planning/scheduling, establishing plant conditions,
aligning equipment, tagging, temporary modifications, and equipment restoration did not
place the plant in an unacceptable configuration; and (3) reviewed the USAR and CAP
to determine if the licensee identified and corrected risk assessment and emergent work
control problems.
-12- Enclosure
- August 6, 2006, emergent work on instrument air dryer, Work Order 06-056595
- August 7, 2006, opening main generator output Breakers 345-50 and 345-60 for
Transformer SF-6 gas addition
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed four samples.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a. Inspection Scope
The inspectors: (1) reviewed plant status documents, such as operator shift logs,
emergent work documentation, deferred modifications, and standing orders, to
determine if an operability evaluation was warranted for degraded components;
(2) referred to the USAR and design basis documents to review the technical adequacy
of licensee operability evaluations; (3) evaluated compensatory measures associated
with operability evaluations; (4) determined degraded component impact on any TSs;
(5) used the significance determination process to evaluate the risk significance of
degraded or inoperable equipment; and (6) verified that the licensee has identified and
implemented appropriate corrective actions associated with degraded components.
- May 27, 2006, Barton Model 763 and 763A gage pressure transmitters
- August 1, 2006, Class 1E electrical equipment air conditioning Unit A (SGK05A)
unloader
- August 17, 2006, emergency diesel Generator B jacket water leak
Documents reviewed by the inspectors included:
- Condition Report 2006-000895
- Industry Technical Information Program 02005
- Operability Evaluation XX-06-003
- Procedure AP 28-001, Operability Evaluations, Revision 14
- Work Request 00077-93
The inspectors completed three samples.
-13- Enclosure
b. Findings
Introduction: The inspectors identified a Green noncited violation (NCV) of 10 CFR
Part 50, Appendix B, Criterion V, regarding the failure to implement Administrative
Procedure AP 28-011, Resolving Deficiencies Impacting SSCs, Revision 1.
Description: On June 27, 2006, the inspectors identified an inadequate evaluation of a
deficiency impacting the operability of several safety-related pressure transmitters.
On May 18, 2006, PRIME Measurement Products issued a Nuclear Industry Advisory
that Barton Model 763 and 763A gage pressure transmitters and Model 764 differential
pressure transmitters may have defective external lead-wire connectors. The advisory
described a defect where the insulated portions of the wires in the connectors may not
be embedded deeply enough into the epoxy potting used to structurally support the
soldered wire connections and establish a seal to protect the solder connections from
shorting. The advisory warned that shorting of conductors could occur in an electrically
conductive accident environment. The advisory stated the affected transmitters were
manufactured after May 1982 and shipped from the factory prior to April 1, 2006.
Transmitters manufactured prior to June 1982 and assembled with heat shrinking
embedded in the epoxy potting were not subject to the concerns of the PRIME advisory.
PRIME recommended that all connectors in transmitters manufactured after May 1982
be inspected for exposure of the external lead wire conductors at the surface of the
connector and that any transmitter with exposed conductors should be considered
defective and replaced. Because of the design and configuration of the transmitters, the
inspections would necessitate the connector be unscrewed from the transmitter and the
external lead wires flexed 90 degrees to ensure the insulated portions of the wires are
securely embedded in the epoxy potting material. On June 21, 2006, following
inspection of warehouse stock potentially affected by the PRIME advisory, Callaway
plant made a 10 CFR Part 21 report notifying the NRC of defects in Barton pressure
transmitters.
Based on preliminary information from Callaway Plant, Wolf Creek Generating Station
initiated Condition Report 2006-000895 on June 19, 2006, to assess the applicability of
the 10 CFR Part 21 report. The licensee determined that the affected Barton models
were used onsite with a total of 39 safety-related transmitters installed. Significant
functions supported by the affected transmitters were main steam pressure indication
and trip functions, steam generator level indiction and trip functions, pressurizer level
indication and trip functions, and reactor coolant system wide-range pressure
indications. System engineering performed an operability evaluation to assess if any of
the installed transmitters were defective. As part of the operability justification basis,
system engineering referred to previous inspections performed by instrumentation and
control technicians under Work Request 00077-93. These inspections were performed
in 1993 and were in response to Westinghouse Letter SAP-92-182 that identified the
potential for damage to lead wire insulation on Barton pressure transmitters. The letter
identified a potential defect caused by lead wire rubbing against the internal threads of
the housing boss, resulting in insulation damage. Westinghouse recommended that
each transmitter be inspected for wire insulation damage; however, this only required
inspection at the entrance to the transmitter housing. Work Request 00077-93
-14- Enclosure
contained steps to inspect the transmitters addressed in the Westinghouse letter, which
included removing the conduit flex cable and conduit connector and inspecting the
transmitter lead wire at point of exit from the transmitter housing. The inspection criteria
established in the work order only required that the wire insulation be smooth,
unblemished, and free of nicks. Specifically, the work order did not contain the
requirements to unscrew the connector from the transmitter and that the external lead
wires be flexed 90 degrees to ensure the insulated portions of the wires are securely
embedded in the epoxy potting material as recommended in the current PRIME
advisory.
The licensee performed inspections on June 27, 2006, of two Barton pressure
transmitters affected by the PRIME advisory that were not included in the scope of the
1993 inspections. The resident inspector observed the inspections of these two
transmitters. In both cases, the inspection revealed that the transmitters were
assembled with heat shrinking embedded in the epoxy potting and, therefore, not
subject to the advisory. However, the inspectors questioned how the 1993 inspections
could identify the defective condition. Specifically, the inspectors questioned how the
previous inspections could take credit to identify the insulated portions of the wires were
securely embedded in the epoxy potting material, since the connectors were not
unscrewed from the transmitter and the external lead wires were not flexed 90 degrees.
Additionally, the inspectors noted that the lead wires and epoxy potting are inaccessible
without removal of the connector; therefore, the recommended inspection could not be
completed.
A review of the inspections performed in 1993 revealed 14 Barton pressure transmitters
manufactured without heat shrinking embedded in the epoxy potting and, therefore,
potentially affected by the PRIME advisory. The licensee inspected several spare lead
wire assemblies in stock and found one with a defect in the epoxy, but has not inspected
spare and installed Barton pressure transmitters.
Procedure AP 28-011 requires that, during the operability determination process, a
reasonable expectation must exist that the SSC is operable and that the prompt
determination process will support that expectation. Contrary to this requirement,
reasonable expectation was not established because the 1993 inspections did not
support the engineering judgement used. The licensee failed to inspect installed Barton
pressure transmitters and identify transmitters with known potential manufacturing
defects. In response to this finding, the licensee has developed an accelerated
schedule for inspection of the potentially affected transmitters as part of Condition
Report 2006-000895.
Analysis: The failure to implement Procedure AP 28-011 following identification of a
potential degraded condition was a performance deficiency. This finding was more than
minor because it affected the equipment performance attribute of the mitigating systems
cornerstone and the cornerstone objective to ensure the availability, reliability, and
capability of systems that respond to initiating events. Using Manual Chapter 0609,
Significance Determination Process, Phase 1 worksheets, the inspectors determined
that the finding is of very low significance because it did not represent a loss of a safety
function or operability and was not potentially risk significant due to external events.
-15- Enclosure
The inspectors also determined that this finding has crosscutting aspects in the human
performance area associated with decision making in that the licensee failed to use
conservative assumptions in decision making and verify the validity of underlying
assumptions for operability of the pressure transmitters.
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and
Drawings," states, in part, that activities affecting quality shall be prescribed by
documented instructions, procedures, or drawings, of a type appropriate to the
circumstances and shall be accomplished in accordance with these instructions,
procedures, or drawings." Administrative Procedure AP28-011, Resolving Deficiencies
Impacting SSCs, Revision 1, step 6.4, requires the licensee to document a basis for
reasonable assurance of operability based on analysis, test, experience, or judgement
or declare the system inoperable. Contrary to this, the licensee failed to document a
reasonable assurance or declare affected equipment inoperable in the absence of a
reasonable assurance of operability. Because the violation was of very low safety
significance and has been entered into the licensees CAP as Condition Report 2006-
000895, this violation is being treated as an NCV, consistent with Section VI.A of the
Enforcement Policy: NCV 05000482/2006004-01, Inadequate inspections of potentially
defective pressure transmitters.
1R19 Postmaintenance Testing (71111.19)
a. Inspection Scope
The inspectors selected the below listed postmaintenance test activities of risk
significant systems or components. For each item, the inspectors: (1) reviewed the
applicable licensing basis and/or design-basis documents to determine the safety
functions; (2) evaluated the safety functions that may have been affected by the
maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested
the safety function that may have been affected. The inspectors either witnessed or
reviewed test data to verify that acceptance criteria were met, plant impacts were
evaluated, test equipment was calibrated, procedures were followed, jumpers were
properly controlled, the test data results were complete and accurate, the test
equipment was removed, the system was properly realigned, and deficiencies during
testing were documented. The inspectors also reviewed the USAR and CAP to
determine if the licensee identified and corrected problems related to postmaintenance
testing.
- August 4, 2006, safety injection Pump B
- August 17, 2006, emergency diesel Generator B
- August 21, 2006, technical support center un-interruptible power supply
- August 31, 2006, component cooling water Pump A
- September 7, 2006, emergency diesel Generator A
-16- Enclosure
- September 28, 2006, main steam isolation valve actuation logic 15 Vdc power
supply
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed six samples.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing (71111.22)
a. Inspection Scope
The inspectors reviewed the USAR, procedure requirements, and TSs to ensure that the
listed surveillance activities demonstrated that the SSCs tested were capable of
performing their intended safety functions. The inspectors either witnessed or reviewed
test data to verify that the following significant surveillance test attributes were
adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
controls; (7) test data; (8) testing frequency and method demonstrated TS operability;
(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of
American Society of Mechanical Engineers code requirements; (12) updating of
performance indicator data; (13) engineering evaluations, root causes, and bases for
returning tested SSCs not meeting the test acceptance criteria were correct;
(14) reference setting data; and (15) annunciators and alarms setpoints. The inspectors
also verified that the licensee identified and implemented any needed corrective actions
associated with the surveillance testing:
- July 20, 2006, Surveillance STS JE-003B, Diesel Generator NE02 Day Tank
Water Removal, Revision 11A
- July 27, 2006, Surveillance STN EJ-001B, Leakage Inspection Program of RHR
System, Revision 0
Revision 25
Revision 2
- September 7, 2006, Surveillance STS IC-615A, Slave Relay Test K615 Train A
Safety Injection, Revision 19
Documents reviewed by the inspectors included:
-17- Enclosure
- Surveillance STS JE-003B, Diesel Generator NE02 Day Tank Water Removal,
Revision 11A
- Surveillance STN EJ-001B, Leakage Inspection Program of RHR System,
Revision 0
- Surveillance STS IC-615A, Slave Relay Test K615 Train A Safety Injection,
Revision 19
- Wolf Creek Generating Station USAR, Revision 19
The inspectors completed five samples.
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications (71111.23)
a. Inspection Scope
The inspectors reviewed the USAR, plant drawings, procedure requirements, and TSs
to ensure that the temporary modification was properly implemented. The inspectors:
(1) verified that the modification did not have an affect on system operability/availability,
(2) verified that the installation was consistent with the modification documents,
(3) ensured that the postinstallation test results were satisfactory and that the impact of
the temporary modification on permanently installed SSCs were supported by the test,
(4) verified that the modifications were identified on control room drawings and that
appropriate identification tags were placed on the affected drawings, and (5) verified that
appropriate safety evaluations were completed. The inspectors verified that the
Licensee identified and implemented any needed corrective actions associated with
- September 5, 2006, Tavg element 2 wiring change (Temporary Modification
Order 05-018-SB-00)
Documents reviewed by the inspectors included:
- Temporary Modification Order 05-018-SB-00
- Drawing M-12BB01, Piping & Instrumentation Diagram Reactor Coolant System,
Revision 25
-18- Enclosure
- Drawing 8809D51, Thot Loop Protection I Card Frame Cabinet Interconnecting
Wiring Diagram, Revision 5A
- Work Orders 05-278177 and 05-278455
The inspectors completed one sample.
b. Findings
No findings of significance was identified.
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
a. Inspection Scope
The inspector performed an in-office review of Revision 7 to Wolf Creek Generating
Station Emergency Plan Implementing Procedure Form APF 06-002-01, "Emergency
Action Levels," received July 12, 2006. This revision updated the bases for Emergency
Action Level 9, "Loss of Plant Control/Security Compromise," to correctly describe the
classification of a hostile force located in the licensee protected area, in accordance
with NRC Bulletin 2005-002, "Emergency Preparedness and Response Actions for
Security-Based Events."
The revision was compared to the previous revision, to the criteria of NUREG-0654,
"Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and
Preparedness in Support of Nuclear Power Plants," Revision 1; to the criteria of Nuclear
Energy Institute (NEI) 99-01, "Methodology for Development of Emergency Action
Levels," Revision 2; to NRC Bulletin 2005-002; and to the standards in 10 CFR 50.47(b)
to determine if the revision was adequately conducted following the requirements of
10 CFR 50.54(q). This review was not documented in a safety evaluation report and did
not constitute approval of licensee changes; therefore, these revisions are subject to
future inspection.
Documents reviewed by the inspectors included:
- Emergency Plan Implementing Procedure Form APF 06-002-01, Emergency
Action Levels, Revision 7
- NRC Bulletin 2005-002, Emergency Preparedness and Response Actions for
Security-Based Events
- NUREG-0654, Criteria for Preparation and Evaluation of Radiological
Emergency Response Plans and Preparedness in Support of Nuclear Power
Plants, Revision 1
-19- Enclosure
- NEI 99-01, Methodology for Development of Emergency Action Levels,
Revision 2
The inspector completed one sample.
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation (71114.06)
a. Inspection Scope
For the below listed drill and simulator-based training evolution contributing to
drill/exercise performance and emergency response organization performance
indicators, the inspectors: (1) observed the training evolution to identify any
weaknesses and deficiencies in classification, notification, and protective action
requirements development activities; (2) compared the identified weaknesses and
deficiencies against licensee identified findings to determine whether the licensee is
properly identifying failures; and (3) determined whether licensee performance is in
accordance with the guidance of the NEI 99-02, Regulatory Assessment Indicator
Guideline, Revision 4, acceptance criteria.
- July 20, 2006, dropped fuel assembly leads to radiological emergency
Documents reviewed by the inspectors included:
- Emergency Planning Drill 06-SA-02
- NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 4
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
4. OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
a. Inspection Scope
Cornerstone: Mitigating Systems
The inspectors sampled licensee submittals for the performance indicator listed below
for the period March 2004 through May 2006. The definitions and guidance of
NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 4, were used to verify
-20- Enclosure
the licensees basis for reporting each data element in order to verify the accuracy of
performance indicator data reported during the assessment period. The inspectors
reviewed licensee event reports, monthly operating reports, and operating logs as part
of the assessment. Licensee performance indicator data were also reviewed against
the requirements of Procedure AP 26A-007, "NRC Performance Indicators," Revision 4,
and "Performance Improvement and Learning Desktop Instruction, NRC Performance
Indicator Program Owner Guidance, Revision 2. The inspectors reviewed various
licensee indicator input information to determine the accuracy and completeness of the
performance indicator.
C Safety system functional failures
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed one sample in this cornerstone.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
.1 Routine Review of Identification and Resolutions of Problems
a. Inspection Scope
The inspectors performed a daily screening of items entered into the licensee's CAP.
This assessment was accomplished by reviewing work requests, work orders, and
performance improvement requests and attending corrective action review and work
control meetings. The inspectors: (1) verified that equipment, human performance, and
program issues were being identified by the licensee at an appropriate threshold and
that the issues were entered into the CAP; (2) verified that corrective actions were
commensurate with the significance of the issue; and (3) identified conditions that might
warrant additional followup through other baseline inspection procedures.
b. Findings
No findings of significance were identified.
.2 Selected Issue Followup
a. Inspection Scope
In addition to the routine review, the inspectors selected the below listed issue for a
more in-depth review. The inspectors considered the following during the review of the
licensee's actions: (1) complete and accurate identification of the problem in a timely
manner; (2) evaluation and disposition of operability/reportability issues;
(3) consideration of extent of condition, generic implications, common cause, and
-21- Enclosure
previous occurrences; (4) classification and prioritization of the resolution of the
problem; (5) identification of root and contributing causes of the problem;
(6) identification of corrective actions; and (7) completion of corrective actions in a timely
manner.
- May 28, 2006, Condition Report 2006-000589 refueling water storage
tank (RWST) level increase
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed one sample.
b. Findings
Introduction: A Green self-revealing NCV of TS 5.4.1.a was identified for the failure to
close Valves EC-V025 and -V033 during a lineup to recirculate the RWST through the
spent fuel pool (SFP) cleanup system. As a result, approximately 1200 gallons of water
was pumped from the SFP to the RWST.
Description: On May 27, 2006, the RWST was placed into recirculation through the SFP
cleanup system using Procedure SYS EC-121, Recirculation of the RWST Through the
Fuel Pool Cleanup System, Revision 11, for maintenance purposes. Approximately
25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> after placing the system into recirculation, the control room received
annunciator alarm RWST Lev HILO. Control room indication showed that the RWST
level had increased approximately 0.4 percent. After recognizing that placing the RWST
into recirculation was the only change that had been made to the system, station
operators were dispatched to determine the cause of the alarm. It was discovered that
the SFP level had decreased approximately 1 inch since placing the RWST into
recirculation. The control room directed station operators to verify the valve lineup and
discovered that Valves EC-V0025 and -V0033 were not fully closed. This resulted in an
unexplained rise in RWST level and a lowering of SFP level. Both valves were
subsequently fully closed and levels were stabilized. These valves are used to isolate
the SFP cooling heat exchanger from the SFP cleanup system during recirculation of
the RWST. These two systems were cross-connected for approximately 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />,
which resulted in approximately 1200 gallons of SFP water being transferred to the
RWST.
The licensee noted that difficult manually-operated valves were not being identified and
entered into the CAP; therefore, the licensee identified the failure to enter the difficult
manually-operated valves into the CAP as the root cause. Due to the lack of
documentation in CAP, the evaluation noted that the most probable cause was failure to
fully close both valves. However, the apparent cause evaluation and corrective actions
failed to address the procedural compliance and human performance aspects of why the
valves were not fully closed. Based on followup interviews by the inspectors, the plant
operators stated that the valves were operated with little difficulty and the procedure
contains a caution that leakage pass-through Valves EC-V025 and -V033 will allow
water to transfer from the SFP to the RWST. It was also noted that the operator did
perform a self-check, but failed to ask for a peer-check, even though one was available.
-22- Enclosure
Analysis: The failure to completely close Valves EC-V025 and -V033 was considered a
performance deficiency. This finding is more than minor because it is associated with
the barrier integrity cornerstone attribute of configuration control and affected the
cornerstone objective to maintain functionality of the SFP system. Using Manual
Chapter 0609, Significance Determination Process, Phase 1 worksheets, the
inspectors determined that the finding is only of very low significance because the
finding only affected the barrier function of the SFP. The inspectors also determined
that this finding has crosscutting aspects in the problem identification and resolution
area associated with the CAP, based on the failure to identify and enter issues into the
CAP with a low threshold.
Enforcement: TS 5.4.1.a, Procedures, requires that written procedures be
established, implemented, and maintained covering the activities specified in
Appendix A, Typical Procedures for Pressurized Water Reactors, of Regulatory
Guide 1.33, Quality Assurance Program Requirements, February 1978. Appendix A,
Item 3.h, requires procedures for SFP cooling system operation. Station
Procedure SYS EC-121, Recirculation of the RWST Through the Fuel Pool Cleanup
System, Revision 11, step 6.1.3, requires that Valves EC-V025 and -V033 be closed
when placing the RWST in recirculation through the SFP cleanup system. Contrary to
the above procedure, on May 27, 2006, an operator failed to close Valves EC-V025 and
-V033. Because this finding is of very low safety significance and was entered into the
licensee's CAP as Condition Report 2006-000589, this violation is being treated as an
NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
NCV 05000482/2006004-02, Failure to completely close SFP valves resulted in a loss
of SFP water inventory.
4OA3 Followup of Events and Notices of Enforcement Discretion (71153)
Personnel Performance During Nonroutine Evolutions, Events and Transients
a. Inspection Scope
The inspectors: (1) reviewed operator logs, plant computer data, and/or strip charts for
the below listed evolutions to evaluate operator performance in coping with nonroutine
events and transients; (2) verified that operator actions were in accordance with the
response required by plant procedures and training; and (3) verified that the licensee
has identified and implemented appropriate corrective actions associated with personnel
performance problems that occurred during the events sampled.
- On June 22, 2006, the inspectors observed site response to a portable air
monitor alarm in the radwaste building at the 1976 foot level. Following the start
of a volume control tank purge on the chemical volume control system, the purge
was secured due to unexpected excessive moisture in the oxygen flow meter to
the recombiner inlet. After approximately 10 minutes of draining the moisture,
the purge was re-initiated. Approximately 40 minutes after restarting the purge,
airborne activity levels increased in the radwaste building and the volume control
tank purge was secured. The licensee determined that the unexpected airborne
activity was caused by opening Valve HA-V0706 to drain the moisture which
-23- Enclosure
provided a flow path of trapped volume control tank gases from the waste gas
compressor to atmosphere. The operation of Valve HA-V0706 was not
controlled by procedure and was not compatible with the purge system lineup at
the time. This resulted in an unplanned monitored release inside the radwaste
building. Section 4OA7 describes enforcement aspects of this event.
- On September 14, 2006, the inspectors reviewed the response of the control
room operators to a loss of charging flow. During surveillance testing of check
valves in the chemical and volume control system, the control room operators
received the charging low flow and reactor coolant pump seal injection low flow
annunciators, in addition to observing a small transient on pressurizer level and
volume control tank level and temperature. The control room recognized that
charging flow was lost and responded by starting the opposite train centrifugal
charging pump. This action restored normal charging flow and stabilized
pressurizer level. Miscommunication between two station operators resulted in
an isolation of the running charging header with the opposite charging header
secured.
Documents reviewed by the inspectors are listed in the attachment.
The inspectors completed two samples.
b. Findings
Loss of Charging Flow
Introduction: A self-revealing Green NCV of TS 5.4.1.a involving the licensee's failure to
follow a procedure that resulted in a loss of coolant charging flow during a planned
surveillance.
Description: On September 14, 2006, the licensee performed surveillance
Procedure STS BG-210, "CVCS Inservice Check Valve Test, Revision 22. This
procedure tested check valve operability for multiple trains of the chemical and volume
control system. The licensee conducted a pre-evolution brief in accordance with
Procedure AP 22-001, Conduct of Pre-Job Briefs and Post-Job Briefs, Revision 8;
however, an operations trainee designated to provide peer checks did not attend the
brief. Following the pre-evolution brief, three operators were dispatched to the auxiliary
building with copies of the applicable procedures.
The operators successfully completed testing of the check valves associated with the
Train A centrifugal charging pump. Procedure STS BG-210 then directed the Train B
cooling charging pump be placed in service in accordance with Procedure SYS BG-201,
"Shifting Charging Pumps," Revision 41. With the Train A centrifugal charging pump
running, the control room directed the station operators to open Valve BG8483C,
cooling charging Pump B discharge isolation valve. Following the opening of
Valve BG8483C, Procedure SYS BG-201 required six actions to be completed prior to
-24- Enclosure
closing Train A charging header isolation Valve BG8483A. Included in these steps was
a requirement to start the Train B centrifugal charging pump and stop the Train A
centrifugal charging pump.
Miscommunication between two of the station operators resulted in confusion as to what
step in the procedure was required next. Without direction from the control room and
without receiving a peer check, a station operator closed Valve BG8483A, the Train A
centrifugal charging pump discharge isolation valve. Although a field copy of the
procedure was available, it was not referenced. This resulted in isolating the charging
flow to the reactor coolant system and reactor coolant pump seal injection flow. Several
annunciators were received in the control room, including the charging low flow and the
reactor coolant pump seal injection low flow alarms. Additionally, a small transient was
observed on pressurizer level and volume control tank level and temperature. The
control room recognized that charging flow had been lost and reactor coolant pump seal
injection flow had been reduced and immediately started Train B centrifugal charging
pump. This action prevented a complete loss of reactor coolant pump seal injection
flow, restored normal charging flow, and stabilized pressurizer level.
Analysis: The failure to follow station procedures was considered a performance
deficiency. This finding was more than minor because it affected the human
performance attribute of the initiating events cornerstone and the cornerstone objective
to limit the likelihood of those events that upset plant stability and challenge critical
safety functions. Using Manual Chapter 0609, Significance Determination Process,
Phase 1 worksheets, this finding screened to a Phase 2 analysis because it affected
both the initiating events and mitigating system cornerstones. The inspectors performed
a Phase 2 analysis using Appendix A, "Technical Basis For At Power Significance
Determination Process," of Manual Chapter 0609, "Significance Determination Process,"
and the Phase 2 worksheets for the Wolf Creek Generating Station. The inspectors
assumed that the loss of all charging and seal injection flow would lead to loss of reactor
coolant system inventory and ultimately a plant trip. Dominant sequences from the
Phase 2 analysis were a plant trip with a loss of main and auxiliary feedwater combined
with a loss of early inventory high pressure injection, a loss of high pressure
recirculation, and a loss of primary feed and bleed. Based on the results of the Phase 2
analysis, the finding is determined to have very low safety significance. The Phase 2
analysis was verified by a Region IV senior reactor analyst. The inspectors also
determined that the finding has crosscutting aspects in the area of human performance
associated with work practices because the operators failed to use appropriate human
error prevention techniques, such as self-checking, peer-checking, and not proceeding
in the face of uncertainty.
Enforcement: TS 5.4.1.a, Procedures, requires that written procedures be
established, implemented, and maintained covering the activities specified in
Appendix A, Typical Procedures for Pressurized Water Reactors, of Regulatory
Guide 1.33, Quality Assurance Program Requirements, February 1978. Appendix A,
Item 3.n, requires procedures governing operation of the chemical and volume control
system. Procedure SYS BG-201, "Shifting Charging Pumps," Revision 41, step 6.4.6
requires that if centrifugal charging Pump A is running, then start centrifugal charging
Pump B prior to step 6.4.7, which requires Valve BG8482A to be locked closed.
-25- Enclosure
Contrary to the above, an operator shut Valve BG8483A, the centrifugal charging
Pump A discharge isolation valve, prior to establishing Train B charging flow. Because
this violation was of very low safety significance and was entered in the CAP as
Condition Report 2006-002030, this violation is being treated as an NCV consistent with
Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2006004-03, Failure to
follow procedure results in loss of coolant charging flow.
4OA5 Other Activities
.1 (Closed) Temporary Instruction 2515/169, Mitigating Systems Performance Index
(MSPI) Verification
a. Inspection Scope
During this inspection period, the inspectors completed a review of the licensees
implementation of the MSPI in accordance with the guidance provided in Temporary
Instruction 2515/169. The review examined the licensees implementation Document,
WCNOC-163, MSPI Basis Document, Revision 1, and verified that established system
boundaries and monitored components were consistent with guidance provided in
NEI 99-02, Reactor Oversight Process Performance Indicators, Revision 4. The
inspectors examined surveillances that the licensee determined do not render the train
unavailable for greater than 15 minutes and are, therefore, not used in unavailability
calculations. The inspectors also examined activities identified by the licensee that do
not render an MSPI train unavailable due to credit for operator recovery. As part of this
review, the recovery actions were verified to be uncomplicated and contained in written
procedures.
Additionally, the inspectors reviewed the baseline MSPI unavailability time using plant
specific values for the period of 2002 to 2004. The verification included all planned and
unplanned unavailability. The plant-specific data for 2005 to 2006 was also reviewed to
ensure the licensee properly accounted for the actual unavailability hours of MSPI
systems. For the same period, the MSPI component unreliability data was examined to
ensure the licensee identified all failures of monitored components. The accuracy and
completeness of the reported unavailability and unreliability data was verified by
reviewing out-of-service logs, operating logs, and corrective action documents. The
unavailability and unreliability data was compared with performance indicator data
submitted to the NRC to ensure that any discrepancies would not result in a change to
the index color.
b. Findings
No findings of significance were identified. This completes the inspection requirements
for this TI.
-26- Enclosure
4OA6 Meetings, Including Exit
On July 31, 2006, the inspector presented the inspection results to Mr. T. East,
Superintendent of Emergency Planning, who acknowledged the findings. The inspector
confirmed that proprietary information was not provided or examined during the
inspection.
On August 31, 2006, the inspectors conducted a debrief meeting to present the licensed
operator requalification inspection results to the Licensee's management team. The
licensee was informed that a final exit for the inspection would be conducted after the
requalification program was completed and the NRC had reviewed the final results. On
September 20, 2006, a final exit, which described the inspection results, was conducted
by the inspectors via telephone with Ms. M. Guyer, Superintendent of Operations
Training. The inspectors asked the licensee whether any materials examined during the
inspection should be considered proprietary. No proprietary information was identified.
On October 6, 2006, the resident inspectors presented the inspection results of the
inspections to Mr. S. Hedges, Vice President Operations and Plant Manager, and other
members of the licensee's management staff. The licensee acknowledged the findings
presented. The inspectors verified that no proprietary information was provided during
the inspection.
4OA7 Licensee-Identified Violations
The following violations of very low significance (Green) were identified by the licensee
and are violations of NRC requirements which meet the criteria of Section VI of the
NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.
- TS 5.4.1.a, Procedures, requires that written procedures be established,
implemented, and maintained covering the activities specified in Appendix A,
Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33,
Quality Assurance Program Requirements, February 1978. Appendix A,
Item 7.c, requires procedures for gaseous effluent system control. Contrary to
this requirement, Procedures SYS HA-200, Gaseous Radwaste System
Operations, Revision 22, and SYS HA-205, Operation of Gas Analyzer Racks,
Revision 23, did not control the use of Valve HA-V0706 to drain moisture from
the flow meters. However, on June 22, 2006, licensee personnel operated this
valve, which resulted in an unplanned release. This event is described in the
CAP as Condition Report 2006-000398. This finding was determined to be of
very low safety significance because it did not affect the licensees ability to
assess dose impact to the public.
- License Condition 2.C.(5)(a) states that the licensee shall maintain in effect all
provisions of the approved fire protection program as described in the Standard
Nuclear Unit Power Plant System Final Safety Analysis Report for the facility
through Revision 17, the Wolf Creek site addendum through Revision 15, and as
approved in the safety evaluation report through Supplement 5. The fire
protection program states that it will comply with the technical requirements of
-27- Enclosure
Appendix R,Section III.G.2 to 10 CFR Part 50, which requires cables whose fire
damage could prevent the operation of safe shutdown functions be physically
protected from fire damage. The fire protection program states that 3-hour fire
barriers are required for Fire Areas C-35 and A-6. Contrary to this requirement,
the licensee failed to ensure that the required 3-hour fire barriers between Fire
Areas C-35 and A-6 were functional without compensatory measures in place.
The fire barriers as installed provided approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of fire endurance.
This issue is described in the CAP as Performance Improvement
Request 2006-001970. This finding was determined to be of very low safety
significance because the fire barrier was assigned a fire containment moderate
degradation rating since there was still some defense-in-depth benefit and it
provided a minimum of 20 minutes fire endurance for the areas.
ATTACHMENT: SUPPLEMENTAL INFORMATION
-28- Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
T. J. Garrett, Vice President Engineering
S. E. Hedges, Vice President Operations and Plant Manager
R. A. Muench, President and Chief Executive Officer
K. Scherich, Director Engineering
M. Sunseri, Vice President Oversight
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
05000482/2006004-01 NCV Inadequate inspections of potentially defective pressure
transmitter (Section 1R15)05000482/2006004-02 NCV Failure to completely close SFP valves resulted in a loss
of SFP water inventory (Section 4OA2.2)05000482/2006004-03 NCV Failure to follow procedure results in loss of coolant
charging flow (Section 4OA3)
DOCUMENTS REVIEWED
In addition to the documents referred to in the inspection report, the following documents were
selected and reviewed by the inspectors to accomplish the objectives and scope of the
inspection and to support any findings:
Section 1R05 Fire Protection
Procedure AP 10-102, Control of Combustible Materials, Revision 10
Procedure AP 10-106, Fire Preplans, Revision 3
Procedure AP 21B-003, Control of Temporary Equipment, Revision 5
Procedure E-1F9905, Fire Hazard Analysis, Revision 0
Surveillance STN KC-206, Spray and Sprinkler System Functional Testing, Revision 13
Condition Report 2006-002256
Section 1R07 Heat Sink Performance
Procedure MP EN-171, ESW Train A Post LOCA Flow Balance, Revision April 1994, performed
October 20, 1994
A-1 Attachment
Procedure TMP TS-50, ESW Train B Post LOCA Flow Balance, Revision 0, performed
November 1, 1991
Surveillance STN EF 022A, ESW Train A Post LOCA Flow Balance, Revision 4, performed
May 10, 2005
Procedure TMP EN-173, ESW Train A Post LOCA Flow Balance, Revision 1, performed
October 19, 1994
Surveillance STN EF 022A, ESW A Post LOCA Flow Balance, Revision 1, performed May 9,
2005
Surveillance STN PE-037A, ESW Train A Heat Exchanger Flow and DP Trending, Revision 9,
performed February 20, 2006
Surveillance STN PE-037A, ESW Train A Heat Exchanger Flow and DP Trending, Revision 10,
performed August 8, 2006
Surveillance STN PE-037B, ESW Train A Heat Exchanger Flow and DP Trending, Revision 10,
performed February 12, 2006
Surveillance STN PE-038, Containment Cooler Performance Test, Revision 7, performed
April 19, 2004
Proto-Power Corporation User Documentation for Heat Exchanger Modeling Software,
Revision 4.10
Calculation SA-90-057, Specific Acceptance Criteria and Operations of the Containment Fan
Coolers, Revision 0
EDI 23L-004, Proto-HX Heat Exchanger Test Data Uncertainty, Desk Top Instruction,
Revision 0
EDI 23L-003, Proto-HX Heat Exchanger Testing Software, Revision 0
Calculation AN-97-005, Containment Temperature and Pressure Response, Revision 0
Calculation M-620-00117 W01, Cooling Coil Curves, September 10, 1991
Section 1R13 Maintenance Risk Assessments and Emergent Work Control
Procedure AP 22C-003, Operational Risk Assessment Program, Revision 11
2006 Work Week 308 risk profile
2006 Work Week 311 risk profile
2006 Work Week 313 risk profile
A-2 Attachment
Section 1R19 Postmaintenance Testing
Conditional Release for Installation/Testing 06-288426-002
Procedure AP 16E-002, Post Maintenance Testing Development, Revision 5
Procedure AP 24D-003, Receipt Inspections, Revision 9A
Purchase Order 736014, Revision 1
Procedure SYS EF-200, Operation of the ESW System, Revision 26
Procedure SYS KJ-123, Post Maintenance Run of Emergency Diesel Generator A, Revision 35
Surveillance STS KJ-011B, DG NE02 24 Hour Run, Revision 16
Surveillance STS KJ-015A, Manual/Auto Fast Start, Sync and Loading of EDG NE01,
Revision 21
Work Orders 05-279245-000, 06-287374-000, 06-288426-000, and 06-288429-000
Section 4OA1 Performance Indicator Verification
Engineering Desktop Instruction EDI 23M-050, Monitoring Performance to Criteria and Goals,
Revision 3
Licensee Event Reports 2004-002-00, -006-00, 2005-002-00, -004-00, -005-00, and
2006-002-00
NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 4
Performance Improvement and Learning Desktop Instruction, NRC Performance Indicator
Program Owner Guidance, Revision 2
Performance Improvement Requests 2004-2765 and 2005-2152
Procedure AP 26A-007, NRC Performance Indicators, Revision 4
Section 4OA2 Identification and Resolution of Problems
Procedure SYS EC-121, Recirculation of the RWST Through the Fuel Pool Cleanup System,
Revision 11
Reportability Evaluation Request 2006-010
A-3 Attachment
Condition Reports:
CR 2006-1549 CR 2006-2062 CR 2006-2196
CR 2006-1750 CR 2006-2072 CR 2006-2204
CR 2006-1752 CR 2006-2074 CR 2006-2209
CR 2006-1764 CR 2006-2092 CR 2006-2211
CR 2006-1796 CR 2006-2097 CR 2006-2213
CR 2006-1829 CR 2006-2103 CR 2006-2217
CR 2006-1864 CR 2006-2115 CR 2006-2222
CR 2006-1886 CR 2006-2125 CR 2006-2223
CR 2006-1895 CR 2006-2133 CR 2006-2231
CR 2006-1899 CR 2006-2159 CR 2006-2233
CR 2006-1900 CR 2006-2161 CR 2006-2281
CR 2006-1904 CR 2006-2175 CR 2006-2282
CR 2006-1925 CR 2006-2178 CR 2006-2321
CR 2006-1946 CR 2006-2186
CR 2006-1967 CR 2006-2189
CR 2006-2028 CR 2006-2190
CR 2006-2054 CR 2006-2194
Section 4OA3 Followup of Events and Notices of Enforcement Discretion
Condition Reports 2006-1752 and 2006-2030
Procedure AP 15C-002, Procedure Use and Adherence, Revision 22
Procedure AP 21-001, Conduct of Operations, Revision 36
Procedure AP 22-001, Conduct of Pre-Job Briefs and Post-Job Briefs, Revision 8
Procedure SYS BG-201, Shifting Charging Pumps, Revision 41
Surveillance STS BG-210, CVCS Inservice Check Valve Test, Revision 22
Procedure SYS HA-200, Gaseous Radwaste System Operations, Revision 22
Procedure SYS HA-205, Operation of Gas Analyzer Racks, Revision 23
Section 4OA5 Other Activities
MSPI verification of unavailability data changes due to CW and critical hours
MSPI verification of unavailability input/baseline data
MSPI verification of unreliability input/baseline data
WCNOC-163, Mitigating System Performance Index (MSPI) Basis Document, Revision 1
Surveillance STN OQT-001A, Operations A Train Quarterly Tasks, Revision 23
Surveillance STS AL-101, MDAFW Pump A Inservice Pump Test, Revision 35
Surveillance STS AL-104, TDAFW ESF Response Time, Flow Path Verification and Check
Valve Testing, Revision 13
Surveillance STS AL-201C, Turbine Driven Auxiliary Feedwater System Inservice Valve Test,
Revision 4
A-4 Attachment
Surveillance STS AL-212, MDAFP Comprehensive Pump Testing, Flow Path Verification and
CV Testing, Revision 10
Surveillance STS BG-205, CVCS Inservice Valve Test, Revision 20
Surveillance STS BG-212B, Train B CCP Discharge Check Valve Inservice Test, Revision 2
Surveillance STS IC-208, 4KV Loss of Voltage and Degraded Voltage TADOT NB02 Bus -
Separation Group 4, Revision 2A
Surveillance STS IC-634B, Slave Relay Test - Train B Steam/Feed Isolation, Revision 16
Surveillance STS IC-805B, Channel Calibration of NB02 Grid Degraded Voltage, Time Delay
Trip, Revision 10
LIST OF ACRONYMS
CAP corrective action program
MSPI mitigating systems performance index
NCV noncited violation
NEI Nuclear Energy Institute
NRC Nuclear Regulatory Commission
RWST refueling water storage tank
SFP spent fuel pool
SSC structure, system, and component
TS Technical Specification
USAR Updated Safety Analysis Report
A-5 Attachment