IR 05000483/2011005
ML120380522 | |
Person / Time | |
---|---|
Site: | Callaway |
Issue date: | 02/07/2012 |
From: | O'Keefe N NRC Region 4 |
To: | Heflin A Union Electric Co |
References | |
IR-11-005 | |
Download: ML120380522 (76) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I V 1600 EAST LAMAR BLVD ARLINGTON, TEXAS 76011-4511 February 7, 2012 Mr. Adam C. Heflin, Senior Vice President and Chief Nuclear Officer Union Electric Company P.O. Box 620 Fulton, MO 65251 Subject: CALLAWAY PLANT - NRC INTEGRATED INSPECTION REPORT NUMBER 05000483/2011005
Dear Mr. Heflin:
On December 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Callaway Plant. The enclosed integrated inspection report documents the inspection findings, which were discussed on January 3, 2012, with Mr. F. Diya, Vice President Nuclear Operations, and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Four NRC-identified and three self-revealing findings of very low safety significance were identified during this inspection. Six of these findings were determined to involve violations of NRC requirements. Further, licensee-identified violations which were determined to be of very low safety significance are listed in this report. The NRC is treating these violations as non-cited violations, consistent with Section 2.3.2 of the NRC Enforcement Policy.
If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV, 1600 East Lamar Boulevard, Arlington, Texas 76011-4511; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Callaway Plant. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report; with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at the Callaway Plant.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of
Adam C. Heflin, Senior Vice President and Chief Nuclear Officer -2-NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Neil OKeefe, Chief Project Branch B Division of Reactor Projects Docket: 05000483 License: NPF-30
Enclosures:
NRC Inspection Report 05000483/2011005 w/Attachments: Supplemental Information O
REGION IV==
Docket: 05000483 License: NPF-30 Report: 05000483/2011005 Licensee: Union Electric Company Facility: Callaway Plant Location: Junction Highway CC and Highway O Dates: September 24 through December 31, 2011 Inspectors: D. Dumbacher, Senior Resident Inspector Z. Hollcraft, Resident Inspector C. Alldredge, Health Physicist G. Apgar, Operations Engineer K. Clayton, Senior Operations Engineer A. Fairbanks, Reactor Inspector S. Hedger, Operations Engineer C. Long, Senior Resident Inspector D. Reinert, Reactor Inspector L. Ricketson, Senior Health Physicist L. Willoughby, Senior Project Engineer Accompanied By: T. Buchanan, Operations Engineer Approved By: N. OKeefe, Chief, Project Branch B Division of Reactor Projects-1- Enclosure
SUMMARY OF FINDINGS
IR 05000483/2011005, 09/24/2011 - 12/31/2011; Callaway Plant; Integrated Resident and
Regional Report; Inservice Inspection Activities, Licensed Operator Requalification,
Maintenance Risk Assessments and Emergent Work Control, Postmaintenance Testing and Event Follow-up.
The report covered a 3-month period of inspection by resident inspectors and an announced baseline inspections by region-based inspectors. Six Green non-cited violations and one Green finding of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined using Inspection Manual Chapter 0310, Components Within the Cross-Cutting Areas. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,
Revision 4, dated December 2006.
NRC-Identified Findings and Self-Revealing Findings
Cornerstone: Initiating Events
- Green.
The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,
Criterion V, for the failure to have procedures that ensured that hand files and wire brushes designated for stainless steel weld preparation were stored separately from hand files and wire brushes used on carbon steel. The licensee took corrective actions to remove the stainless steel designations from stainless steel tools that were mixed with tools used on carbon steel, established segregated locations in tool rooms for the separation of abrasive tools, and trained tool room attendants to properly store and mark abrasive tools designated for use on stainless steel. This issue was entered into the licensees corrective action program as Callaway Action Request 201108921.
Inspectors determined that the failure to assure that hand files and wire brushes designated for exclusive use on stainless steel were stored separately from tools used on other materials was a performance deficiency. This finding was more than minor because it was associated with the equipment performance attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and, if left uncorrected, could become a more significant safety concern. Inspectors performed a Phase 1 screening in accordance with Inspection Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, and determined that the finding was of very low safety significance because the issue would not result in exceeding the technical specification limit for identified reactor coolant system leakage or affect other mitigating systems resulting in a total loss of their safety function. This finding has a cross-cutting aspect in the area of problem identification and resolution, associated with the corrective action program, because the licensee did not thoroughly evaluate problems such that the resolutions addressed causes and extent of conditions, as necessary. Specifically, the licensees response to Callaway Action Request 201107806 identified contaminated tools as the cause of rusting on the motor-driven auxiliary feed pump room cooler stainless steel piping, but the licensee took no further action to identify the cause of the contamination P.1(c).
(Section 1R08)
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a non-cited violation of 10 CFR Part 55.46(c),
Plant-Referenced Simulators, for failure of the licensee to ensure that the plant-referenced simulator demonstrated expected plant response to transient and accident conditions to which the simulator has been designed to respond.
Specifically, the licensee failed to ensure simulator modeling of power-operated relief valve and pressurizer safety valve operation was consistent with the actual plant, introducing the potential for negative operator training. Due to errors made in modeling updates after steam generator replacement in 2005, each pressurizer safety valve was sized in the simulator to allow approximately 3.3 times higher than the design flow rate in the actual plant, and each power operated relief valve was sized to allow approximately 3.5 times higher than the design flow rate capacity provided in the actual plant. The licensee documented their corrective actions for this issue in Callaway Action Request 201101255.
The failure of the licensees simulator staff to ensure that the plant-referenced simulator demonstrated expected plant response to transient and accident conditions for which the simulator has been designed to respond was a performance deficiency. The performance deficiency is more than minor because it adversely impacted the human performance attribute of the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Additionally, if left uncorrected, the performance deficiency could have become more significant in that training on related accident scenarios could have a negative impact on how licensed operators would respond to an actual event in the control room. Using Manual Chapter 0609, Significance Determination Process, Phase 1 worksheets, and the corresponding Appendix I,
Licensed Operator Requalification Significance Determination Process, the finding was determined to have very low safety significance (Green) because there was no actual event at the plant similar to the simulator scenario where inappropriate actions were taken in the control room based on training with incorrectly sized components in the simulator. This finding has no cross-cutting aspect assigned because the cause was not representative of current licensee performance. (Section 1R11.2.b.1)
- Green.
The inspectors identified a finding associated with the conduct of simulator performance testing because the licensee was not testing in accordance with the standards of ANSI/ANS 3.5-1998. Specifically, the licensee did not include relief valve flow in their 2010 test of transient (10) of
ANSI/ANS 3.5-1998, Appendix B, Section B3.2.1, "Slow Primary System Depressurization to Saturated Condition with Pressurizer Relief or Safety Valve Stuck Open. The licensee initiated corrective action documented in Callaway Action Request 201107912.
Conducting simulator performance testing that was not in accordance with the ANSI/ANS 3.5-1998 standard was a performance deficiency. The performance deficiency is more than minor because it adversely impacted the human performance attribute of the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Additionally, if left uncorrected, the performance deficiency could have become more significant in that not completing the required simulator testing annually can lead to not detecting and correcting errors in the simulator so that it models the actual plant correctly. Using Manual Chapter 0609, Significance Determination Process,
Phase 1 worksheets, and the corresponding Appendix I, Licensed Operator Requalification Significance Determination Process, the finding was determined to have very low safety significance (green) because there was no actual event caused by not modeling the actual plant correctly. This finding has no cross-cutting aspect assigned because the cause was not representative of current licensee performance. (Section 1R11.2.b.2)
- Green.
The inspectors identified a non-cited violation of 10 CFR 50.65(a)(4),
Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, involving the licensees failure to assess and manage outage risk related to significant switchyard work. Specifically, the licensee allowed risk significant relay test work to result in loss of one of two offsite safety related 4 kV power feeds to the plant during Refueling Outage 18. With Callaway Plant in Mode 6,
Refueling, the risk assessment for October 21, 2011, and the Outage Shutdown Management Plan prohibited significant switchyard work. However, at 1:21 p.m.,
emergency diesel generator A bus NB01 became deenergized due to improper switchyard testing. Callaway Action Request 201108888 was initiated to develop corrective actions.
Failure to properly assess and manage the risk of significant switchyard work during a high decay heat condition was a performance deficiency. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
The offsite power system was affected by this event. Using Manual Chapter 0609, Appendix G, Attachment 1, Checklist 4 - PWR Refueling Operation: RCS level > 23 OR PWR Shutdown Operation with Time to Boil
> 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> And Inventory in the Pressurizer, this finding was determined to be of very low safety significance because it did not increase the likelihood of a loss of reactor coolant system inventory, did not degrade the ability to terminate a leak path or add reactor coolant system inventory when needed, and did not degrade the ability to recover decay heat removal, if lost. This finding has a cross-cutting aspect in the area of human performance associated with the resources component because Procedure EDP-ZZ-01129, Callaway Plant Risk Assessment, Attachment 6, Step 6.c, was not sufficiently complete and accurate to define significant switchyard work H.2(c). (Section 1R13)
- Green.
The inspectors reviewed a Green self-revealing non-cited violation of 10 CFR Part 50 Appendix B, Criterion V, Procedures, involving the licensees failure to correctly install a ground test device for the train A safety-related 4160 volt switchgear, NB01. During maintenance on the train A safety related bus, workers improperly placed a ground test device with 2000 ampere stab adapters into the 1200 ampere breaker cubicle (for the residual heat removal pump). This damaged the switchgear connection point and caused the breaker to fail, rendering the pump inoperable. The reactor was defueled so the residual heat removal system was not required by technical specifications at the time, but the bus was required to be removed from service for repairs. The licensee repaired the bus connection point, and the pump was retested satisfactorily. This finding was entered into the licensee's corrective action program as Callaway Action Request 201109122.
Failure to install the correctly configured ground and test device into the NB0101 cubicle of the NB01 switchgear was a performance deficiency. This is more than minor because it is associated with the human performance attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, improper maintenance caused the residual heat removal pump to become unavailable.
Because no fuel was in the vessel at the time of the event, the inspectors referred the issue to a Region IV senior reactor analyst for the significance determination. The analyst used NRC Inspection Manual 0609, Appendix G,
Shutdown Operations Significance Determination Process, to evaluate the significance of the finding. Since all of the fuel had been removed from the vessel there was no potential for core damage (the delta core damage frequency was zero). Therefore, the finding is of very low safety significance (Green). The finding has a cross-cutting aspect in the area of human performance associated with the resources component in that the licensee failed to ensure training of maintenance personnel was adequate to assure nuclear safety H.2(b).
(Section 1R19)
- Green.
The inspectors reviewed a Green self-revealing non-cited violation of Technical Specification 5.4.1.a, Procedures, involving the failure to isolate an electrical power supply during maintenance on control room air conditioning system train A. Specifically, while removing an electrical cabinet for maintenance, workers discovered an energized lead that was supposed to have been isolated for the work. Workers failed to stop work and make appropriate notifications. As a result, when the lead was reterminated, it grounded the bus and caused inverter NN11 to shift to an alternate power supply. This caused operators to make an unplanned entry into a 24-hour shutdown technical specification action statement. The licensee restored normal power to inverter NN11 within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. This issue was entered into the corrective action program as Callaway Action Request 201107612.
Failure to stop work when a lockout tagout isolation was discovered to be inadequate was a performance deficiency. This finding is more than minor because it is associated with the configuration control attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, inverter NN11 was rendered less reliable by the improper maintenance. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this finding was determined to be of very low safety significance because it did not create a loss of system safety function of a single train for greater than the technical specification allowed outage times, and did not affect seismic, flooding, or severe weather initiating events. This finding has a cross-cutting aspect in the area of human performance associated with the work practices component because licensee personnel failed to stop in the face of uncertainty or unexpected circumstances H.4(a). (Section 4OA3.1)
- Green.
The inspectors reviewed a self-revealing non-cited violation of Technical Specification 5.4.1.a, Procedures, involving the failure to ensure compliance with relay test maintenance procedures associated with electrical switchyard work that affected the performance of safety related equipment. On October 21, 2011, Callaway Plant was in Mode 6 with switchyard activities in progress to test transfer trip and lockout relay devices. At 1:21 p.m. the control room operators received several annunciators indicating that diesel generator bus A and its safety related loads had become deenergized. An improperly operated lockout relay had cascaded a test signal onto other components in the plant electrical system. This issue was entered into the corrective action program as Callaway Action Request 201108691.
Failure to establish the safe working conditions per the transfer trip procedure and failure to operate the lockout relay in the manner specified by the lockout relay procedure were performance deficiencies. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, one of the two offsite power feeds to the plant was lost. Using Manual Chapter 0609 Appendix G Attachment 1, Checklist 4 - PWR Refueling Operation: RCS level
> 23 OR PWR Shutdown Operation with Time to Boil > 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> And Inventory in the Pressurizer, this finding was determined to be of very low safety significance because it did not increase the likelihood of a loss of reactor coolant system inventory, did not degrade the ability to terminate a leak path or add reactor coolant system inventory when needed, and did not degrade the ability to recover decay heat removal. This finding has a cross-cutting aspect in the area of human performance associated with the work controls component because the electrical relay test technicians, onsite engineering, and work control staff failed to adequately maintain interfaces to communicate and safely coordinate significant switchyard activities to ensure proper human performance H.3(b).
(Section 4OA3.2)
Licensee-Identified Violations
Violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and corrective action tracking numbers (condition report numbers) are listed in Section 4OA7.
REPORT DETAILS
Summary of Plant Status
Callaway Plant began the inspection period at full power. On October 15, 2011, the licensee shut the plant down to start Refueling Outage 18. The plant was returned to full power on November 30, 2011. Callaway operated at full power for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
Readiness for Seasonal Extreme Weather Conditions
a. Inspection Scope
The inspectors performed a review of the adverse weather procedures for seasonal extremes (e.g., extreme low temperatures). The inspectors verified that weather-related equipment deficiencies identified during the previous year were corrected prior to the onset of seasonal extremes, and evaluated the implementation of the adverse weather preparation procedures and compensatory measures for the affected conditions before the onset of, and during, the adverse weather conditions.
During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Final Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that plant personnel were identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:
- October 24, 2011, cold weather walkdown of essential service water, refueling water storage tank, condensate storage tank, and various building penetrations This activity constitutes completion of one readiness for seasonal adverse weather sample as defined in Inspection Procedure 71111.01-05.
b. Findings
No findings were identified.
1R04 Equipment Alignments
.1 Partial Walkdown
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant systems:
- October 6, 2011, emergency core cooling systems (charging and safety injection)alignment for cold overpressure mitigation when reactor coolant system was less than 275 degrees Fahrenheit
- October 21, 2011, containment equipment hatch motor emergency power portable diesel
- November 20, 2011, emergency core cooling system injection lineup prior to entering Mode 3
- November 22, 2011, auxiliary feedwater train A lineup following Mode 4 testing The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Final Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of four partial system walkdown samples as defined in Inspection Procedure 71111.04-05.
b. Findings
No findings were identified.
.2 Complete Walkdown
a. Inspection Scope
On October 16, 2011, the inspectors performed a complete system alignment inspection of the essential service water system following startup after essential safety features actuation sequence testing to verify the functional capability of the system. The inspectors selected this system because it was considered safety significant in the licensees probabilistic risk assessment. The inspectors inspected the system to review mechanical and electrical equipment line ups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. The inspectors reviewed a sample of past and outstanding work orders to determine whether any deficiencies significantly affected the system function.
In addition, the inspectors reviewed the corrective action program database to ensure that system equipment-alignment problems were being identified and appropriately resolved. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one complete system walkdown sample as defined in Inspection Procedure 71111.04-05.
b. Findings
No findings were identified.
1R05 Fire Protection
Quarterly Fire Inspection Tours
a. Inspection Scope
The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
- October 13, 2011, reactor building prior to Refueling Outage 18 shutdown, fire area RB
- November 19, 2011, reactor building during transition to Mode 4, fire area RB
- November 20, 2011, control building 1974 foot essential service water pipe space, Room 3101, fire area C-1
- December 2, 2011, essential service water pump rooms, trains A and B, rooms U104 and U105, fire areas UNPH and USPH
- December 9, 2011, diesel generator room train B, room 5201, fire area D-2 The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of five quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.
b. Findings
No findings were identified.
1R06 Flood Protection Measures
a. Inspection Scope
The inspectors reviewed the Final Safety Analysis Report, the flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; reviewed the corrective action program to determine if licensee personnel identified and corrected flooding problems; inspected underground bunkers/manholes to verify the adequacy of sump pumps, level alarm circuits, cable splices subject to submergence, and drainage for bunkers/manholes; and verified that operator actions for coping with flooding can reasonably achieve the desired outcomes. The inspectors also inspected the areas listed below to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers.
- October 7 and 10, 2011, inspection of underground cable vaults for the essential service water system These activities constitute completion of one bunker/manhole sample as defined in Inspection Procedure 71111.06-05.
b. Findings
No findings were identified.
1R07 Heat Sink Performance
a. Inspection Scope
The inspectors reviewed licensee programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for the October 15, 2011, component cooling water train B heat exchanger thermal performance test. The inspectors verified that the performance test was satisfactorily conducted and reviewed for problems or errors; the licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger Performance Monitoring Guidelines, the licensee properly utilized biofouling controls; the licensees heat exchanger inspections adequately assessed the state of cleanliness of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one heat sink inspection sample as defined in Inspection Procedure 71111.07-05.
b. Findings
No findings were identified.
1R08 Inservice Inspection Activities
.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water
Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control (71111.08-02.01)
a. Inspection Scope
The inspectors observed six nondestructive examination activities and reviewed two nondestructive examination activities that included three types of examinations. The licensee did not identify any relevant indications accepted for continued service during the nondestructive examinations.
The inspectors directly observed the following nondestructive examinations:
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Chemical and 2-BG-02-S056-A Ultrasonic Volume Control 4 inch Straight Tee to 4 inch Pipe Residual Heat 2-EJ-02-C018-IWA Dye Penetrant Removal Piping Support
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE High Pressure Snubber EM01R024112A Visual Coolant Injection High Pressure Snubber EM01R021112A Visual Coolant Injection High Pressure Snubber EM01R027112A Visual Coolant Injection High Pressure Snubber EM01R026112B Visual Coolant Injection The inspectors reviewed records for the following nondestructive examinations:
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE 2-BB-01-S401-10 Reactor Coolant 3 inch Nozzle to 3 inch x 1.5 inch Ultrasonic Reducer 2-BB-01-S201-15 Reactor Coolant 3 inch Nozzle to 3 inch x 1.5 inch Ultrasonic Reducer During the review and observation of each examination, the inspectors verified that activities were performed in accordance with the ASME Code requirements and applicable procedures. The inspectors also verified the qualifications of all nondestructive examination technicians performing the inspections were current.
The inspectors directly observed a portion of the following welding activity:
SYSTEM WELD IDENTIFICATION WELD TYPE Shielded Metal Arc Main Feedwater 07010303-500 Welding The inspectors reviewed records for the following welding activity:
SYSTEM WELD IDENTIFICATION WELD TYPE Chemical and Shielded Metal Arc 08007500-500 Volume Control Welding The inspectors verified, by review, that the welding procedure specifications and the welders had been properly qualified in accordance with ASME Code,Section IX, requirements. The inspectors also verified, through observation and record review, that essential variables for the welding process were identified, recorded in the procedure
qualification record, and formed the bases for qualification of the welding procedure specifications. Specific documents reviewed during this inspection are listed in the attachment.
These actions constitute completion of the requirements for Section 02.01.
b. Findings
Introduction.
Inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion V, for the failure to have procedures that ensured that hand files and wire brushes designated for stainless steel weld preparation were stored separately from hand files and wire brushes used on carbon steel.
Description.
During inspection of the auxiliary building tool room in the radiologically controlled area, inspectors identified that hand files and wire brushes designated for either stainless steel or carbon steel weld preparation were not stored separately.
Additionally, inspectors noted that although one hand file was marked for use on stainless steel, the file was rusty and, therefore, most likely was used on carbon steel.
Inspectors were concerned that the failure to separate tools used for stainless steel weld preparation from tools used for carbon steel preparation could result in the contamination of stainless steel welds by carbon steel and affect the material integrity and corrosion resistance of these welds.
Inspectors reviewed Procedure APA-ZZ-00660, Control of Special Processes and System Cleanliness, Revision 12, and concluded that the procedure was inadequate to ensure the segregation of abrasive tools designated for use on stainless steel from tools used on carbon steel. Step 4.4.4 stated, Tools marked for use only on stainless steel are stored in a designated location in the Maintenance Tool Room. Inspectors determined that this statement in the procedure did not provide adequate instruction to personnel to maintain abrasive tools for use on stainless steel separate from abrasive tools meant for use on other materials. Additionally, Step 4.4.5, stated, Tools marked for use on stainless steel and which inadvertently are used on carbon steel shall have their markings removed or permanently covered and then transferred to the General Tool Storage for general use. Inspectors concluded that the licensee had not removed the stainless steel markings from the file that appeared to have been used on carbon steel.
The licensee investigated the inspectors concerns and concluded that the storage of files and wire brushes designated for use only on stainless steel in the auxiliary building tool room was not meeting the expectations established in Procedure APA-ZZ-00660. In particular, there was no segregation of files or wire brushes and there were files designated for use on stainless steel that were rusty and may have been used on carbon steel. The licensee took immediate action to remove the stainless steel designations from tools used on stainless steel that were mixed with tools used on carbon steel.
Additionally, the licensee planned to set up segregated locations in tool rooms for the separation of abrasive tools that are designated for use on stainless steel from those used on other materials. The licensee also planned to reinforce the standards to the tool room attendants to properly store and mark abrasive tools designated for use on
stainless steel and to question the requester of abrasive tools for the end use location so the appropriate tool could be provided.
The inspectors also reviewed documentation from one instance in which contaminated wire brushes had contributed to corrosion on stainless steel piping. Callaway Action Request 201107806, dated September 29, 2011, was written to address questions from the NRC resident inspectors regarding whether rust on stainless steel room cooler piping in the motor-driven auxiliary feedwater pump rooms could cause degradation to the piping. The licensee walked down the room cooler piping and stated that the rust was believed to have been caused by using contaminated stainless steel brushes. In other words, cross-contamination from a tool that had been used to do work on carbon steel had then been used on the stainless steel piping. The licensee concluded that the rust was superficial and would not induce any degradation.
This issue was entered into the licensees corrective action program as Callaway Action Request 201108921.
Analysis.
Inspectors determined that the failure to assure that hand files and wire brushes designated for exclusive use on stainless steel were stored separately from tools used on other materials was a performance deficiency. This finding was more than minor because it was associated with the equipment performance attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and, if left uncorrected, would become a more significant safety concern. Inspectors performed a Phase 1 screening in accordance with Inspection Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, and determined that the finding was of very low safety significance (Green) because the issue did not result in exceeding the technical specification limit for identified reactor coolant system leakage or affect other mitigating systems resulting in a total loss of their safety function. This finding has a cross-cutting aspect in the area of problem identification and resolution, associated with the corrective action program, because the licensee did not thoroughly evaluate problems such that the resolutions addressed causes and extent of conditions, as necessary. Specifically, the licensees response to Callaway Action Request 201107806 identified contaminated tools as the cause of rusting on the motor-driven auxiliary feed pump room cooler stainless steel piping, but the licensee took no further action to identify the cause of the contamination P.1(c).
Enforcement.
Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion V, states, in part, Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
The control of tools used on stainless steel was an activity affecting quality, and was implemented by Procedure APA-ZZ-00660, Control of Special Processes and System Cleanliness, Revision 12. Steps 4.4.4 and 4.4.5 required, in part, that tools marked for use only on stainless steel be stored in a designated location and tools designated for use on stainless steel have the markings removed if used on carbon steel. Contrary to the above, prior to October 25, 2011, the licensee failed to prescribe and accomplish the
separation and appropriate designation of tools used on stainless steel. This issue was entered into the licensees corrective action program as Callaway Action Request 201108921. Because this finding was determined to be of very low safety significance and was entered into the licenses corrective action program, this violation is being treated as a non-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000483/2011005-01, Failure to Ensure Separation of Stainless Steel and Carbon Steel Hand Files and Wire Brushes.
.2 Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)
a. Inspection Scope
The inspectors reviewed the results of the licensees bare metal visual inspection of the reactor vessel upper head penetrations and verified that there was no evidence of boric acid challenging the structural integrity of the reactor head components and attachments. The inspectors also verified that the required inspection coverage was achieved and limitations were properly recorded. The inspectors verified that the personnel performing the inspection were certified examiners of their respective nondestructive examination method. Specific documents reviewed during this inspection are listed in the attachment.
These actions constitute completion of the requirements for Section 02.02.
b. Findings
No findings were identified.
.3 Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)
a. Inspection Scope
The inspectors evaluated the implementation of the licensees boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspectors reviewed the documentation associated with the licensees boric acid corrosion control walkdown as specified in Procedure QCP-ZZ-0548, Boric Acid Walkdown for Reactor Coolant System Pressure Boundary, Revision 7. The inspectors also reviewed the visual records of the components and equipment. The inspectors verified that the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components. The inspectors also verified that the engineering evaluations for those components where boric acid was identified gave assurance that the ASME Code wall thickness limits were properly maintained. The inspectors confirmed that the corrective actions performed for evidence of boric acid leaks were consistent with requirements of the ASME Code. Specific documents reviewed during this inspection are listed in the attachment.
These actions constitute completion of the requirements for Section 02.03.
b. Findings
No findings were identified.
.4 Steam Generator Tube Inspection Activities (71111.08-02.04)
a. Inspection Scope
The inspection procedure specified performance of an assessment of in situ screening criteria to assure consistency between assumed nondestructive examination flaw sizing accuracy and data from the Electric Power Research Institute (EPRI) examination technique specification sheets. It further specified assessment of appropriateness of tubes selected for in situ pressure testing, observation of in situ pressure testing, and review of in situ pressure test results. No conditions had been identified that warranted in situ pressure testing.
The inspection procedure specified confirmation that the steam generator tube eddy current test scope and expansion criteria meet Technical Specification requirements, EPRI guidelines, and commitments made to the NRC. The inspectors evaluated the recommended steam generator tube eddy current test scope established by Technical Specification requirements. The inspectors compared the recommended test scope to the actual test scope and found that the licensee had accounted for all known flaws and had, as a minimum, established a test scope that met Technical Specification requirements, EPRI guidelines, and commitments made to the NRC. The scope of the licensees eddy current examinations of tubes in all four steam generators included:
- 100 percent eddy current bobbin probe examinations, full length tube end to tube end
- Eddy current X-probe examinations of the outer three rows of tubesheet periphery and no-tube lanes
- X-probe or rotating coil examinations of any tubes with potential loose parts indications
- Special interest +Point probe diagnostic examinations including anti-vibration bar wear, bobbin probe non-quantifiable indications, and 20 percent of bobbin probe ding indications The inspection procedure required confirmation that the licensee inspected all areas of potential degradation, especially areas that were known to represent potential eddy current test challenges such as the top-of-tubesheet, tube support plates, and U-bends.
The inspectors confirmed that all known areas of potential degradation were included in the scope of inspection and were being inspected.
No new degradation mechanisms were identified during the inspection. The only indications of degradation detected during the eddy current inspections were small wear
indications at the anti-vibration bar intersections. The licensee plugged any tubes with wear indications of 28 percent or greater. The licensee plugged a total of 29 tubes with anti-vibration bar wear indications. No indications of loose parts or loose part wear were detected from either the top of tubesheet +Point inspections or the visual inspections of the top of the tubesheet.
The licensee performed inspections of secondary side components including the steam drums and loose parts trapping system, and performed a foreign material search and retrieval. If loose parts or foreign material on the secondary side were identified, the inspection procedure specified confirmation that the licensee had taken or planned appropriate repairs of affected steam generator tubes and that they inspected the secondary side to either remove the accessible foreign objects or perform an evaluation of the potential effects of inaccessible object migration and tube fretting damage. At the time of the inspection, no foreign material had been identified.
Finally, the inspection procedure specified review of one to five samples of eddy current test data if questions arose regarding the adequacy of eddy current test data analyses.
The inspectors did not identify any results where eddy current test data analyses were inadequate.
These actions constitute completion of the requirements of Section 02.04.
b. Findings
No findings were identified.
.5 Identification and Resolution of Problems (71111.08-02.05)
a. Inspection scope
The inspectors reviewed 20 Callaway action requests which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. The specific Callaway action requests reviewed are listed in the documents reviewed section. From this review the inspectors concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also had an effective program for applying industry inservice inspection operating experience. Specific documents reviewed during this inspection are listed in the attachment.
These actions constitute completion of the requirements of Section 02.05.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program (71111.11 and 71111.11B)
.1 Quarterly Review
a. Inspection Scope
On November 29, 2011, the inspectors observed a crew of licensed operators in the plants simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
- Licensed operator performance
- Crews clarity and formality of communications
- Crews ability to take timely actions in the conservative direction
- Crews prioritization, interpretation, and verification of annunciator alarms
- Crews correct use and implementation of abnormal and emergency procedures
- Control board manipulations
- Oversight and direction from supervisors
- Crews ability to identify and implement appropriate technical specification actions and emergency plan actions and notifications The inspectors compared the crews performance in these areas to preestablished operator action expectations and successful critical task completion requirements.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one quarterly licensed-operator requalification program sample as defined in Inspection Procedure 71111.11.
b. Findings
No findings were identified.
.2 Biennial Inspection
The licensed operator requalification program involves two training cycles that are conducted over a 2-year period. In the first cycle, the annual cycle, the operators are administered an operating test consisting of job performance measures and simulator scenarios. In the second part of the training cycle, the biennial cycle, operators are administered an operating test and a comprehensive written examination.
a. Inspection Scope
To assess the performance effectiveness of the licensed operator requalification program, the inspectors conducted personnel interviews, reviewed both the operating tests and written examinations, and observed ongoing operating test activities.
The inspectors interviewed six licensee personnel, including operators, instructors/evaluators, and training supervisors, to determine their understanding of the policies and practices for administering requalification examinations. The inspectors also reviewed operator performance on the written exams and operating tests. These reviews included observations of portions of the operating tests by the inspectors. The operating tests observed included six job performance measures (JPMs) and two dynamic simulator scenarios that were used in the current biennial requalification cycle.
These observations allowed the inspectors to assess the licensee's effectiveness in conducting the operating test to ensure operator mastery of the training program content. The inspectors also reviewed medical records of nine licensed operators for conformance to license conditions and the licensees system for tracking qualifications and records of license reactivation for four operators.
The results of these examinations were reviewed to determine the effectiveness of the licensees appraisal of operator performance and to determine if feedback of performance analyses into the requalification training program was being accomplished.
The inspectors interviewed members of the training department and reviewed minutes of training review group meetings to assess the responsiveness of the licensed operator requalification program to incorporate the lessons learned from both plant and industry events. Examination results were also assessed to determine if they were consistent with the guidance contained in NUREG 1021, "Operator Licensing Examination Standards for Power Reactors," Revision 9, Supplement 1, and NRC Manual Chapter 0609, Appendix I, "Operator Requalification Human Performance Significance Determination Process."
In addition to the above, the inspectors reviewed examination security measures, simulator fidelity, and existing logs of simulator deficiencies.
The inspectors completed one inspection sample of the biennial licensed operator requalification program.
b. Findings
1.
Introduction.
The inspectors identified a Green non-cited violation of 10 CFR Part 55.46(c), Plant-Referenced Simulators, for the failure of the licensee to ensure that the plant-referenced simulator demonstrated expected plant response to transient and accident conditions to which the simulator has been designed to respond.
Specifically, the licensee failed to ensure that simulator modeling of power-operated relief valve operation was consistent with the actual plant, introducing the potential for negative operator training.
Description.
During the January 2011 NRC initial licensed operator exam, NRC examiners observed that during a simulated full anticipated transient without scram with a loss of offsite power, relief of high reactor coolant system pressure through power operated relief valves and pressurizer safety valves lowered pressure enough to cause a safety injection actuation. The safety injection actuation signal setpoints are established to protect the reactor coolant system during loss of coolant accidents and steam line break events. Since the simulated anticipated transient without scram with loss of offsite power event should not have caused a safety injection actuation, NRC examiners questioned the licensee as to why this safety injection actuation occurred in the simulator for this circumstance. Licensee staff informed NRC examiners that this occurrence in the simulator was seen as normal, but continued to investigate it further.
Testing of the simulator, detailed in document SIFT # 20110018, Record 7284, revealed that each pressurizer safety valve was sized in the simulator to allow approximately 3.3 times higher than the design flow rate in the actual plant. In addition, each power operated relief valve was sized to allow approximately 3.5 times higher than the design flow rate capacity provided in the actual plant.
Following a steam generator replacement project in November 2005, updates were made to the simulator to account for the various design changes in the plant. The licensee did not identify that changes were made to the plant parameters in question, which introduced the errors into the simulator model.
The licensee documented their corrective actions for this issue in Callaway Action Request 201101255. The sizing of the power-operated relief valves and pressurizer safety valves were corrected in the simulator to match actual design values, and issues with the steam generator condenser steam dump valves were identified by the licensee as part of this testing and subsequently corrected in the simulator.
Analysis.
Failure of the licensees simulator staff to ensure that the plant-referenced simulator demonstrated expected plant response to transient and accident conditions for which the simulator was designed was a performance deficiency. The performance deficiency is more than minor because it adversely impacted the human performance attribute of the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Additionally, if left uncorrected, the performance deficiency could have become more significant in that training on related accident scenarios could have a negative impact on how licensed operators would respond to an actual event in the control room. Using Manual Chapter 0609, Significance Determination Process, Phase 1 worksheets, and the corresponding Appendix I, Licensed Operator Requalification Significance Determination Process, the finding was determined to have very low safety significance (Green) because there was no actual event at the plant similar to the simulator scenario where inappropriate actions were taken in the control room based on training with incorrectly sized components in the simulator.
This finding has no cross-cutting aspect assigned because the cause was not representative of current licensee performance. The errors were introduced into the simulator model in 2005.
Enforcement.
Title 10 of the Code of Federal Regulations Part 55.46(c), Plant-Referenced Simulators, requires, in part, that plant-referenced simulators demonstrate expected plant response to transient and accident conditions to which the simulators have been designed to respond. Contrary to the above, from November 2005 to January 2011, the licensee failed to ensure that its plant-referenced simulator demonstrated expected plant response to transient and accident conditions to which it has been designed to respond. Specifically, changes made to the simulator as a result of the steam generator replacement project introduced sizing errors for the pressurizer safety valves and power-operated relief valves into the simulator model. This had the potential to cause negative operator training in the simulator. Because this finding is of very low safety significance and has been entered into the licensees corrective action program as Callaway Action Request 201101255, this violation is being treated as a non-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy:
NCV 05000483/2011005-02, Failure to Maintain Simulator Fidelity.
2.
Introduction.
The inspectors identified a Green finding associated with the conduct of simulator performance testing because the licensee was not testing in accordance with the standards of ANSI/ANS 3.5-1998. Specifically, the licensee did not include relief valve flow in their 2010 test of transient
- (10) of ANSI/ANS 3.5-1998, Appendix B, Section B3.2.1, Slow Primary System Depressurization to Saturated Condition with Pressurizer Relief or Safety Valve Stuck Open.
Description.
In order to maintain an NRC approved simulation facility, the licensee is required to conduct performance testing throughout the life of the simulator to ensure that it can be used to model control manipulations consistent with the actual plant. The licensee committed to conducting this testing by using industry standard ANSI/ANS 3.5, Nuclear Power Plant Simulators for Use in Operator Training and Examination.
The required annual testing detailed in this standard included transient performance tests, where the licensee conducts simulator tests on eleven specific transients specified in Appendix B, Section B3.2 of the standard. For these transients, it also specified which plant parameters have to be recorded as part of the tests. In 2010, as part of conducting these annual transient performance tests, the licensee conducted a test on transient (10)of ANSI/ANS 3.5-1998, Appendix B, Section B3.2.1, Slow Primary System Depressurization to Saturated Condition with Pressurizer Relief or Safety Valve Stuck Open. Appendix B, Section B3.2.5 specifically included relief valve flow. This parameter was modeled in the licensees simulator, but they did not include its measurement as part of their test (per document SIFT 20100001, Test # T2770). The licensee initiated corrective action documented in Callaway Action Request 201107912, which included adding this parameter to the scope of the annual test. Failing to include relief valve flow in the testing data contributed to the facilitys failure to identify that they had not modeled the size of power-operated relief valves and pressurizer safety valves correctly.
Analysis.
Conducting simulator performance testing that was not in accordance with ANSI/ANS 3.5-1998 was a performance deficiency. The performance deficiency is more than minor because it adversely impacted the human performance attribute of the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and
capability of systems that respond to initiating events to prevent undesirable consequences. Additionally, if left uncorrected, the performance deficiency could have become more significant in that not completing the required simulator testing annually can lead to not detecting and correcting errors in the simulator so that it models the actual plant correctly. In fact, a simulator fidelity issue with relief valve flow was missed by the licensee because of the failure to conduct this testing sufficiently, which had the potential to negatively impact training. Using Manual Chapter 0609, Significance Determination Process, Phase 1 worksheets, and the corresponding Appendix I, Licensed Operator Requalification Significance Determination Process, the finding was determined to have very low safety significance (Green) because there was no actual event caused by not modeling the actual plant correctly.
This finding has no cross-cutting aspect assigned because the cause was not representative of current licensee performance. The licensee reviewed their annual testing records and determined the measurement of relief valve flow has not been included in their annual testing for at least 10 years.
Enforcement.
No violation of regulatory requirements was identified. Because this finding does not involve a violation and has very low safety significance, it is identified as FIN 05000483/2011005-03: Failure to Conduct Simulator Testing in Accordance with ANSI/ANS 3.5-1998.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk significant systems:
- Essential service water pump room ventilation damper system, Callaway Action Request 201105700
- Reactor coolant sample system containment isolation valve leakage, Callaway Action Requests 201102158 and 201110163 The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
- Implementing appropriate work practices
- Identifying and addressing common cause failures
- Scoping of systems in accordance with 10 CFR 50.65(b)
- Characterizing system reliability issues for performance monitoring
- Charging unavailability for performance monitoring
- Trending key parameters for condition monitoring
- Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)
- Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of two quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.
b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
- September 28, 2011, planned risk associated with emergency diesel generator train B supply fan maintenance and surveillance testing of the turbine-driven auxiliary feedwater pump
- October 19, 2011, planned yellow risk due to reactor coolant system level being 6 inches below the reactor vessel head flange while in Mode 6
- October 21, 2011, an unplanned risk condition was revealed when significant switchyard work caused a loss of one train of offsite power
- November 12, 2011, placement/lift of the reactor upper internals
- November 14, 2011, planned yellow risk due to the reactor coolant system level being at reduced inventory with the reactor head installed
- November 21, 2011, risk evaluation for atmospheric steam dump valve ABPV00001 being out of service greater than 7 days as Callaway Plant transitioned from Mode 3 to online. The inspectors reviewed licensee risk document PRAER 11-361.
- November 21, 2011, planned yellow risk associated with taking the turbine-driven auxiliary feedwater pump out of service in Mode 3 The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of seven maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.
b. Findings
Introduction.
The inspectors identified a Green violation of 10 CFR 50.65(a)(4),
Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, involving the licensees failure to manage outage risk related to significant switchyard work. Specifically the licensee allowed risk significant relay test work to result in loss of one of two offsite power feeds to the plant during Refueling Outage 18.
Description.
On October 21, 2011, Callaway Plant was in Mode 6, Refueling, with the reactor head removed. Preparations were being made to remove the reactor vessel upper internals. Emergency diesel generator A was out of service. Switchyard activities to test lockout relay devices were also in progress. Shutdown cooling flow for the reactor coolant system was provided by residual heat removal pump B.
Callaway Procedure EDP-ZZ-01129, Callaway Plant Risk Assessment, Attachment 6 covered Mode 6 - Refueling Operations greater than 23 feet above the reactor vessel flange. This procedure required that operators and work control personnel evaluate plant risk associated with susceptibility to a loss of offsite power due to personnel errors or equipment failures. The risk assessment for October 21, 2011, and the Outage
Shutdown Management Plan prohibited significant switchyard work during this Mode 6 work window. Step 6.c of Attachment 6 to Procedure EDP-ZZ-01129 defined risk-significant switchyard work as any activity that could result in a loss of offsite power to the plant. However, the Refueling Outage 18 Shutdown Management Plan provided two examples of significant switchyard work. One of these examples involved relay testing activities. The risk plan industry operating experience section specifically stated that human errors during switchyard activities have resulted in industry events such as loss of shutdown cooling.
At 1:21 p.m., the control room operators received several annunciators indicating that emergency diesel generator A, bus NB01, had become deenergized and was in a lockout condition. The operators noticed that the electrical feed to the bus through breaker 52-3 from the switchyard safeguards transformer B had opened and that the other bus feeder breakers were also open. The loss of bus NB01 was caused by lockout relay testing when the relay test engineer incorrectly assumed that a proper test setup existed. The inspectors identified that the licensee did not perform the risk management action to prevent significant switchyard work during the mode 6 condition. The inadvertent loss of bus NB01 resulted in a loss of one of the two residual heat removal pumps, but not shutdown cooling flow. Callaway Action Request 201108888 was initiated to develop corrective actions. (See NCV 05000483/2011005-07 in Section 4OA3.)
Analysis.
Failure to properly assess and manage the risk of significant switchyard work during a high decay heat condition was a performance deficiency. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The offsite power system was rendered less reliable by this event. Using Manual Chapter 0609, Appendix G, Attachment 1, Checklist 4 - PWR Refueling Operation: RCS level > 23 OR PWR Shutdown Operation with Time to Boil > 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> And Inventory in the Pressurizer, this finding was determined to be of very low safety significance because it did not increase the likelihood of a loss of reactor coolant system inventory, did not degrade the ability to terminate a leak path or add reactor coolant system inventory when needed, and did not degrade the ability to recover decay heat removal, if lost. This finding has a cross-cutting aspect in the area of human performance associated with the resources component because Procedure EDP-ZZ-01129, Attachment 6, Step 6.c, was not sufficiently complete and accurate to define significant switchyard work. Specifically, it defined the concept of limiting the likelihood of human performance errors but then implied that switchyard risk was only related to vehicles and cranes in the area H.2(c).
Enforcement.
Paragraph (a)(4) of 10 CFR 50.65 of the Maintenance Rule requires licensees to assess and manage plant risk related to maintenance activities during all modes of plant operation. Contrary to the above, on October 21, 2011, the licensee failed to adequately assess and manage risk related to switchyard maintenance activities. Callaway Plant procedures covering plant risk controls allowed significant switchyard work to affect the availability of components supporting offsite power and
shutdown cooling. Specifically, because of the inadequacy of Callaway Plant risk Procedure EDP-ZZ-01129, Callaway Plant Risk Assessment, Attachment 6, Step 6.c, the licensee did not effectively manage the risk associated with significant switchyard work. This conflict resulted in loss of one of two offsite power feeds and one train of shutdown cooling equipment. Because this finding is of very low safety significance and was entered into the licensee's corrective action program as Callaway Action Request 201108888, this violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000483/2011005-04, Failure to Adequately Assess and Manage Outage Risk Associated with Significant Switchyard Work.
1R15 Operability Evaluations and Functionality Assessments
a. Inspection Scope
The inspectors reviewed the following issues:
- October 18, 2011, Callaway Action Request 201108490, degraded containment coating
- November 21, 2011, Callaway Action Request 201109948, centrifugal charging pump A seal leak
- November 23, 2011, Callaway Action Request 201110012, digital rod position indication data cabinet A failure for control rods B10 and B06
- November 23, 2011, Callaway Action Request 201110034, turbine-driven auxiliary feedwater pump packing leak The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Final Safety Analysis Report to the licensee personnels evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.
Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of four operability evaluations inspection samples as defined in Inspection Procedure 71111.15-05
b. Findings
No findings were identified.
1R18 Plant Modifications
.1 Temporary Modifications
a. Inspection Scope
To verify that the safety functions of important safety systems were not degraded, the inspectors reviewed the following temporary modification:
- Temporary modification TM 11-0004, installation of thermal performance test equipment for containment cooler SGN01D The inspectors reviewed the temporary modification and the associated safety-evaluation screening against the system design bases documentation, including the Final Safety Analysis Report and the technical specifications, and verified that the modification did not adversely affect the system operability/availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers.
These activities constitute completion of one sample for temporary plant modifications as defined in Inspection Procedure 71111.18-05.
b. Findings
No findings were identified.
.2 Permanent Modifications
a. Inspection Scope
The inspectors reviewed key affected parameters associated with energy needs, materials, replacement components, timing, heat removal, control signals, equipment protection from hazards, operations, flow paths, pressure boundary, structural, process medium properties, licensing basis, and failure modes for the permanent modifications listed below.
- Modification MP 10-0003, installation of check valves in normal service water piping to the essential service water system
- Modification MP 10-0004, sequence change for opening essential service water valves The inspectors verified that modification preparation, staging, and implementation did not impair emergency/abnormal operating procedure actions, key safety functions, or operator response to loss of key safety functions; postmodification testing will maintain the plant in a safe configuration during testing by verifying that unintended system interactions will not occur; systems, structures and components performance characteristics still meet the design basis; the modification design assumptions were appropriate; the modification test acceptance criteria will be met; and licensee personnel identified and implemented appropriate corrective actions associated with permanent plant modifications. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of two samples for permanent plant modifications as defined in Inspection Procedure 71111.18-05.
b. Findings
No findings were identified.
1R19 Postmaintenance Testing
a. Inspection Scope
The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
- September 30, 2011, Technical Support Center heating ventilation and air conditioning installation postmaintenance test, Job 11000199
- October 14, 2011, alternate emergency power supply diesel postmaintenance test after changing output breaker relay settings, Job 11004604
- October 26, 2011, postmaintenance testing (blue seat checks) of reactor coolant system and safety injection accumulator check valve repairs (BB8948A and EP8956A), Jobs 07003942 and 10006323
- October 29, 2011, postmaintenance testing of NB01, Job 04503768
- November 21, 2011, postmaintenance testing of valve ALHV10, Job 10513172
- November 19, 2011, postmaintenance testing of valve ALHV07, Job 05517259
- November 20, 2011, postmaintenance testing of centrifugal charging pump A, Job 11006744
- November 22, 2011, postmaintenance testing (pressure test) of reactor coolant system pressure isolation valves, Job 10509409 The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities for the following:
- The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed
- Acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate The inspectors evaluated the activities against the technical specifications, the Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of eight postmaintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.
b. Findings
Introduction.
The inspectors reviewed a Green self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Procedures, involving the licensees failure to correctly install a ground test device for safety related 4160 volt switchgear, NB01, train A.
Description.
On October 29, 2011, with the reactor defueled, plant operators attempted to start residual heat removal pump A as part of the fill and vent procedure for system restoration. When the operator took the control room switch to start, the pump did not start. Workers near the breaker noted that it closed, the springs charged, and then reopened after the operator in the control room secured the pump. The pump was declared inoperable and the evolution was stopped. The licensee's troubleshooting determined that during previous maintenance, workers had improperly placed a ground test device with 2000 ampere stab adapters into 1200 ampere breaker cubicle NB0101 (for the residual heat removal pump). This damaged the switchgear connection points (rosettes) in the cubicle such that when the normal breaker was reinstalled the rosettes would not engage. This resulted in the breaker not energizing the pump when closed.
Subsequent investigation revealed that while conducting Maintenance Procedure 04503768/520 (Install Ground Devices in NB01 for Ductor Testing) the workers incorrectly believed that the 01 cubicle of switchgear busses always require a
2000 ampere cubicle. However, safety-related busses NB01 and NB02 have a different numbering scheme and the 01 cubicle is occupied by a different breaker, in this case the 1200 ampere breaker for the residual heat removal pump.
The maintenance procedure that directed workers to setup and install the ground test device was dependent on the workers training to know how to use drawings included with the package to properly verify the amperage of the cubicle. The workers instead depended on incorrect system knowledge to determine the amperage. A specific qualification is required to operate and install the ground and test device (T67.2021 Q),however, the qualification standard does not have a specific requirement to demonstrate the ability to determine the proper amperage of a cubicle before installing the device.
As immediate corrective action, the rosettes were replaced and the breaker and pump retested satisfactorily.
Analysis.
The performance deficiency associated with this finding was the licensees failure to install the correctly configured ground and test device into the NB0101 cubicle of the NB01 switchgear. This finding is more than minor because it is associated with the human performance attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
Specifically, improper maintenance caused the A train safety-related switchgear to become unavailable. Because no fuel was in the vessel at the time of the event, the inspectors referred the issue to a Region IV senior reactor analyst for the significance determination. The analyst used NRC Inspection Manual 0609, Appendix G, Shutdown Operations Significance Determination Process, to evaluate the significance of the finding. Appendix G applies when the residual heat removal entry conditions begin and ends when the licensee exits the residual heat removal operational conditions and heats up the reactor. Appendix G defines a shutdown operation as an operational mode where more than one fuel assembly is in the reactor vessel and the decay heat removal system is in operation. However, all of the fuel had been removed from the vessel.
Therefore, there was no potential for core damage (the delta-CDF was zero). This finding is of very low safety significance (Green). It has a cross-cutting aspect in the area of human performance associated with the resources component in that the licensee failed to ensure training of maintenance personnel was adequate to assure nuclear safety H.2(b).
Enforcement.
Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criteria V, "Procedures," requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Contrary to the above, on October 26, 2011, maintenance workers installing a ground device in the train A switchgear, an activity affecting quality, failed to accomplish this task in accordance with the instructions, procedures, and drawings. Specifically, workers did not use the approved drawings to determine the appropriate amperage of the safety related breaker cubicle and as a result, installed the wrong ground and test device causing damage to the switchgear for residual heat
removal pump A. Because this finding is of very low safety significance and was entered into the licensee's corrective action program as Callaway Action Request 201109122, this violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000483/2011005-05, Improper Ground and Test Device Damages Residual Heat Removal Pump Switchgear.
1R20 Refueling and Other Outage Activities
a. Inspection Scope
The inspectors reviewed the outage safety plan and contingency plans for planned Refueling Outage 18, conducted between October 15 and November 30, 2011, to confirm that licensee personnel had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense in depth. During the refueling outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below.
- Configuration management, including maintenance of defense in depth, is commensurate with the outage safety plan for key safety functions and compliance with the applicable technical specifications when taking equipment out of service
- Clearance activities, including confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing
- Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error
- Status and configuration of electrical systems to ensure that technical specifications and outage safety-plan requirements were met, including controls over switchyard activities (Specifically the October 21, 2011, loss of offsite power feed to bus NB01 was selected for additional event follow-up. See Section 4OA3)
- Monitoring of decay heat removal processes, systems, and components
- Verification that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system
- Reactor water inventory controls, including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss (Specifically the November 1, 2011, loss of steam generator B hot leg drain plug integrity that necessitated draining the reactor cavity to near mid-loop level was selected for additional event follow-up. See Section 4OA3.)
- Controls over activities that could affect reactivity
- Refueling activities, including fuel handling and heavy load lifts associated with reactor vessel assembly/disassembly
- Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the containment to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing
- Licensee identification and resolution of problems related to refueling outage activities Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one refueling and other outage activity inspection sample as defined in Inspection Procedure 71111.20-05.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the Final Safety Analysis Report, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:
- Preconditioning
- Evaluation of testing impact on the plant
- Acceptance criteria
- Test equipment
- Procedures
- Jumper/lifted lead controls
- Test data
- Testing frequency and method demonstrated technical specification operability
- Test equipment removal
- Restoration of plant systems
- Fulfillment of ASME Code requirements
- Updating of performance indicator data
- Engineering evaluations, root causes, and bases for returning tested systems, structures, and components not meeting the test acceptance criteria were correct
- Reference setting data
- Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
- September 26, 2011, routine surveillance emergency diesel train B 24-hour run with hot restart, Job 10507159
- September 29, 2011, routine surveillance of turbine-driven auxiliary feedwater pump valve, Surveillance OSP-AL-V001C, Job 11508034
- October 13, 2011 in-service test of main steam safety valve lift setpoints
- October 15, 2011, routine surveillance, shutdown margin calculation for Refueling Outage 18
- October 16, 2011, routine surveillance, diesel generator train A and sequencer testing
- November 9, 2011, routine surveillance to test the boron dilution mitigation system response, Job 10507555
- November 16, 2011, in-service test of the reactor vessel head vent valves, Job 10509161
- November 19, 2011, routine surveillance to verify containment closeout for Mode 4, Job 10509175
- November 19, 2011, routine surveillance, containment personnel hatch door and shaft seal leak rate test
- November 19, 2011, in-service test of auxiliary feedwater pump discharge check valves
- November 21, 2011, containment isolation valve surveillance testing associated with Procedure ESP-ZZ- SM01001, containment leakage rate testing program, Job 11513180
- November 22, 2011, in-service test of main feedwater isolation valves, Job 10508187
- November 22, 2011, routine surveillance to maintain reactor coolant system heat-up limitations
- November 23, 2011, routine surveillance to determine the estimated critical position for Refueling Outage 18 startup, Job 10509408 Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of a total of fourteen surveillance testing inspection samples, specifically nine routine, one containment isolation valve, and four in-service test surveillances as defined in Inspection Procedure 71111.22-05.
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstone: Occupational and Public Radiation Safety
2RS0 1 Radiological Hazard Assessment and Exposure Controls
a. Inspection Scope
This area was inspected to:
- (1) review and assess licensees performance in assessing the radiological hazards in the workplace associated with licensed activities and the implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures,
- (2) verify the licensee is properly identifying and reporting Occupational Radiation Safety Cornerstone performance indicators, and
- (3) identify those performance deficiencies that were reportable as a performance indicator and which may have represented a substantial potential for overexposure of the worker.
The inspectors used the requirements in 10 CFR Part 20, the technical specifications, and the licensees procedures required by technical specifications as criteria for determining compliance. During the inspection, the inspectors interviewed the radiation protection manager, radiation protection supervisors, and radiation workers. The inspectors performed walkdowns of various portions of the plant, performed independent radiation dose rate measurements and reviewed the following items:
- Performance indicator events and associated documentation reported by the licensee in the Occupational Radiation Safety Cornerstone
- The hazard assessment program, including a review of the licensees evaluations of changes in plant operations and radiological surveys to detect dose rates, airborne radioactivity, and surface contamination levels
- Instructions and notices to workers, including labeling or marking containers of radioactive material, radiation work permits, actions for electronic dosimeter alarms, and changes to radiological conditions
- Programs and processes for control of sealed sources and release of potentially contaminated material from the radiologically controlled area, including survey performance, instrument sensitivity, release criteria, procedural guidance, and sealed source accountability
- Radiological hazards control and work coverage, including the adequacy of surveys, radiation protection job coverage, and contamination controls; the use of electronic dosimeters in high noise areas; dosimetry placement; airborne radioactivity monitoring; controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools; and posting and physical controls for high radiation areas and very high radiation areas
- Radiation worker and radiation protection technician performance with respect to radiation protection work requirements
- Audits, self-assessments, and corrective action documents related to radiological hazard assessment and exposure controls since the last inspection Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.01-05.
b. Findings
No findings were identified.
2RS0 2 Occupational ALARA Planning and Controls
a. Inspection Scope
This area was inspected to assess performance with respect to maintaining occupational individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors used the requirements in 10 CFR Part 20, the technical specifications, and the licensees procedures required by technical specifications as criteria for determining compliance. During the inspection, the inspectors interviewed licensee personnel and reviewed the following items:
- Site-specific ALARA procedures and collective exposure history, including the current 3-year rolling average, site-specific trends in collective exposures, and source-term measurements
- ALARA work activity evaluations/postjob reviews, exposure estimates, and exposure mitigation requirements
- The methodology for estimating work activity exposures, the intended dose outcome, the accuracy of dose rate and man-hour estimates, and intended versus actual work activity doses and the reasons for any inconsistencies
- Records detailing the historical trends and current status of tracked plant source terms and contingency plans for expected changes in the source term due to changes in plant fuel performance issues or changes in plant primary chemistry
- Radiation worker and radiation protection technician performance during work activities in radiation areas, airborne radioactivity areas, or high radiation areas
- Audits, self-assessments, and corrective action documents related to ALARA planning and controls since the last inspection Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.02-05.
b. Findings
No findings were identified.
OTHER ACTIVITIES
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
4OA1 Performance Indicator Verification
.1 Data Submission Issue
a. Inspection Scope
The inspectors performed a review of the performance indicator data submitted by the licensee for the third quarter 2011 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, Performance Indicator Program.
This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.
b. Findings
No findings were identified.
.2 Mitigating Systems Performance Index - High Pressure Injection Systems (MS07)
a. Inspection Scope
The inspectors sampled licensee submittals for the mitigating systems performance index - high pressure injection systems performance indicator for the period from the fourth quarter 2010 through the third quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of October 2010 through September 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance.
The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of one mitigating systems performance index -
high pressure injection system sample as defined in Inspection Procedure 71151-05.
b. Findings
No findings were identified.
.3 Mitigating Systems Performance Index - Residual Heat Removal System (MS09)
a. Inspection Scope
The inspectors sampled licensee submittals for the mitigating systems performance index - residual heat removal system performance indicator for the period from the fourth quarter 2010 through the third quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of October 2010 through September 2011 to validate the accuracy of the submittals. The inspectors
reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance.
The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of one mitigating systems performance index -
residual heat removal system sample as defined in Inspection Procedure 71151-05.
b. Findings
No findings were identified.
.4 Occupational Exposure Control Effectiveness (OR01)
a. Inspection Scope
The inspectors reviewed performance indicator data for the first quarter 2011 through the third quarter 2011. The objective of the inspection was to determine the accuracy and completeness of the performance indicator data reported during these periods. The inspectors used the definitions and clarifying notes contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, as criteria for determining whether the licensee was in compliance.
The inspectors reviewed corrective action program records associated with high radiation area (greater than 1 rem/hr) and very high radiation area non-conformances.
The inspectors reviewed radiological controlled area exit transactions greater than 100 mrem. The inspectors also conducted walkdowns of high radiation areas (greater than 1 rem/hr) and very high radiation area entrances to determine the adequacy of the controls of these areas.
These activities constitute completion of the occupational exposure control effectiveness sample as defined in Inspection Procedure 71151-05.
b. Findings
No findings were identified.
.5 Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual
Radiological Effluent Occurrences (PR01)
a. Inspection Scope
The inspectors reviewed performance indicator data for the first quarter 2011 through the third quarter 2011. The objective of the inspection was to determine the accuracy and completeness of the performance indicator data reported during these periods. The
inspectors used the definitions and clarifying notes contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, as criteria for determining whether the licensee was in compliance.
The inspectors reviewed the licensees corrective action program records and selected individual annual or special reports to identify potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose.
These activities constitute completion of the radiological effluent technical specifications/offsite dose calculation manual radiological effluent occurrences sample as defined in Inspection Procedure 71151-05.
b. Findings
No findings were identified.
4OA2 Identification and Resolution of Problems
.1 Routine Review of Identification and Resolution of Problems
a. Inspection Scope
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
b. Findings
No findings were identified.
.2 Daily Corrective Action Program Reviews
a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.
The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
b. Findings
No findings were identified.
.3 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on repetitive equipment issues, but also considered the results of daily corrective action item screening discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human performance results. The inspectors nominally considered the 6-month period of July 2011 through December 2011 although some examples expanded beyond those dates where the scope of the trend warranted.
The inspectors also included issues documented outside the normal corrective action program in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.
The inspectors compared and contrasted their results with the results contained in the licensees corrective action program trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.
These activities constitute completion of one semi-annual trend inspection sample as defined in Inspection Procedure 71152-05.
b. Findings
The inspectors found that the licensee identified the following trends of significance:
- Callaway Action Request 201103255, trend in consequential errors in maintenance
- Callaway Action Request 201105601, boric acid corrosion control program health score is declining
- Callaway Action Request 201107725, adverse trend in security human performance
- Callaway Action Requests 201110229, 201110462, and 201110566, safety injection accumulator A leakage to fill lines causing potential void concerns
- Callaway Action Request 201110817, licensee personnel fitness-for-duty work-hour violations The resident inspectors concurred with these items as being noteworthy trends needing additional corrective actions.
An additional inspector-identified adverse trend was:
- Callaway Action Requests 201109569 and 201110526, unanalyzed fire barriers associated with essential service water piping features (specifically the high density polyethelene piping entering room 3101 and the rubber expansion joints in the essential service water piping to the emergency diesels were unanalyzed fire barriers)
The licensee has entered these issues into their corrective action program.
.4 Selected Issue Follow-up Inspection
a. Inspection Scope
During a review of items entered in the licensees corrective action program, the inspectors recognized corrective action items documenting:
- October 6, 2011, potential vulnerability to air ingestion at the turbine-driven auxiliary feedwater pump during certain accidents, Callaway Action Request 199700957
- November 5, 2011, impact of essential service water system water hammer event, Callaway Action Request 201109422
- November 18, 2011, licensee generated list of degraded, nonconforming conditions requiring resolution for mode changes
- December 12, 2011, cumulative review of operator workarounds These activities constitute completion of four in-depth problem identification and resolution samples as defined in Inspection Procedure 71152-05.
b. Findings
No findings were identified.
4OA3 Event Follow-up
a. Event Response On September 26, 2011, at 11:06 a.m., with the plant at full power, the supply breaker to inverter NN11 opened unexpectedly causing 120 VAC safety related bus NN01 to transfer to its alternate power supply. The licensee entered Technical Specification 3.8.7.a, a 24-hour shutdown action. Four hours later, the normal power supply was restored.
On October 21, 2011, at 1:21 p.m., with the plant in Mode 6, Callaway Plant operators responded to a loss of one of the two incoming offsite power feeds to the plant due to an unplanned opening of safeguards transformer B output breaker 52-3 during relay testing.
On November 1, 2011, at 8:15 a.m., with the reactor defueled and the refueling pool level 23 feet above the reactor vessel flange, steam generator B bowl drain plug became dislodged. Plant operators operated residual heat removal pumps to drain the pool to mid-loop level as immediate corrective action for the unisolable leak. An estimated 4000 gallons of reactor coolant system water leaked onto the containment floor inside the bioshield area. The cause determination for the steam generator bowl drain plug failure was ongoing at the conclusion of this inspection.
On December 21, 2011, at 10:02 a.m., while running emergency diesel generator B for a routine surveillance, a fire was reported in the diesels jacket water heater. Operators secured the diesel and extinguished the fire within 10 minutes. The cause was traced to a loose screw in the jacket water heater breaker starter housing. No damage to the diesel engine occurred, however, the jacket water heater and heater breaker were replaced.
In each case, NRC resident inspectors responded to the plant to review plant status, communicate the event to supervision, evaluate performance of mitigating systems and ensure proper licensee actions, event classification, and notifications to the NRC and state/county governments.
b. Findings
===.1
Introduction.
The inspectors reviewed a Green self-revealing non-cited violation of===
Technical Specification 5.4.1.a, Procedures, involving the licensees failure to take action to appropriately isolate an electrical power supply during maintenance on control room air conditioning unit, train A.
Description.
On September 23, 2011, a current surge resulted in the power supply breaker to safety related instrument inverter NN11 opening. Inverter NN11 is the normal power supply to the safety related 120 VAC bus NN01. As designed, the inverter shifted
to its alternate supply and the bus did not lose power. This caused an unplanned entry into a 24-hour shutdown action statement per Technical Specification 3.8.7.a.
The licensee determined that an arc was observed while landing power leads on electrical cabinet GK198A associated with control room air conditioning unit SGK04A during maintenance. This caused the current surge which opened the inverters normal power supply breaker. The lead inside the cabinet was supposed to have been deenergized by the Workmans Protection Assurance isolation lockout tagout prior to commencing work.
Unit SGK04A was identified to be removed as interference for a weld repair on an adjacent pipe. The reactor operators Workman's Protection Assurance review of associated drawings failed to identify and isolate all of the power to the cabinet. The primary drawing used (E-23GK02B) contained no clear reference to the power supply.
Subsequent investigation determined that one of the additional drawings, E-23GK02C, did reference the power supply.
As a result of the missed isolation, the maintenance workers who initially de-terminated the leads to remove the cabinet experienced an unexpected electrical arc. However, the workers failed to properly notify their supervisor and isolate the source of power. The workers taped the ends and proceeded with the work. After the work was complete, different workers were assigned to re-terminate the leads to reinstall the cabinet. These workers were unaware that there were live leads that would be connected and did not perform Live-Dead-Live voltage checks as required. They noted the wires with the taped ends and believed they could be energized but still did not verify or question this before reconnecting them. When the leads were re-terminated, they grounded the bus through the cabinet causing the protective relays in inverter NN11 to open the normal supply breaker on overcurrent.
As immediate corrective action the licensee restored normal power to inverter NN11 within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and exited the technical specification action statement. Callaway Action Request 201107612 was initiated to evaluate the cause and extent-of-condition and specify corrective actions.
Analysis.
Failure to stop work when a lockout tagout isolation for maintenance was discovered to be inadequate was a performance deficiency. This finding is more than minor because it is associated with the configuration control attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, inverter NN11 was rendered less reliable by improper maintenance. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this finding was of very low safety significance because it did not create a loss of system safety function of a single train for greater than the technical specification allowed outage times, and did not affect seismic, flooding, or severe weather initiating events. This finding has a cross-cutting aspect in the area of human performance associated with the work practices component because
licensee personnel failed to stop in the face of uncertainty or unexpected circumstances
Enforcement.
Technical Specification 5.4.1.a, Procedures, requires that written procedures be established, implemented and maintained covering the activities specified in Appendix A, Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality Assurance Program Requirements, February 1978. Appendix A, Item 1.c, requires procedures for equipment control (e.g., locking and tagging).
Callaway Procedure APA-ZZ-00310, Workmans Protection Assurance, Revision 45, Step 4.11.4, states that IF it is determined that the WPA Tagging is NOT adequate for a particular JobSTOP work on the associated Job until adequate WPA Tagging is placed. Contrary to the above, on September 23, 2011, the licensee's procedures for equipment control were not implemented for activities specified in Appendix A of Regulatory Guide 1.33. Specifically, maintenance workers failed to notify operations and continued to work when the energized wires were discovered. Subsequently, grounding of the live lead caused an excessive current which opened the normal breaker for the 120 VAC inverter NN11. Because this finding is of very low safety significance and was entered into the licensee's corrective action program as Callaway Action Request 201107612, this violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000483/2011005-06, Failure to Isolate Control Room Air Conditioning Unit SGK04A for Maintenance.
===.2
Introduction.
The inspectors reviewed a Green self-revealing non-cited violation of===
Technical Specification 5.4.1.a, Procedures, involving the licensees failure to ensure compliance with relay test maintenance procedures and associated job task guidance in the electrical switchyard.
Description.
On October 21, 2011, Callaway Plant was in Mode 6 with switchyard activities in progress to test transfer trip and lockout relay devices associated with switchyard bus A and safeguards transformer A. Emergency diesel generator A and undervoltage start circuitry for the emergency diesel generator A bus were out of service. At 1:21 p.m. the control room operators received several annunciators indicating that the diesel generator A bus had become deenergized and was in a lockout condition. Safeguards transformer B breaker 52-3 had opened and the other bus feeder breakers were also open. Without power to the bus, all the bus loads became unavailable, including residual heat removal pump A.
The switchyard transfer trip work was approved prior to the outage and was performed per Job 09511787, which referred the electrical worker to Procedure MPE-ZZ-QY054, "Inspection, Test, Calibration of Protective Instantaneous Overcurrent Relay, GE type.
The lockout relay testing per Job 09511798 and Procedure MPE-ZZ-NY161, Operational Test Sequence of 345 kV Safeguards Transformer A Circuit Breakers, was not approved for the outage. It was submitted during the outage on outage add form 4589 but was disapproved.
The corporate office relay test workers convinced the onsite engineering group that resources and test setup were similar for both of these jobs. Thus, engineering supported addition of just the actuation steps from Job 09511798 to the end of the
Job 09511787 work instructions. The additional steps in the job were performed just after the transfer trip procedure had been completed. The relay test engineer incorrectly assumed that safe working conditions for the transfer trip setup still existed. Step 7.1.14 of lockout relay test Procedure MPE-ZZ-NY161 required manually operating the lockout relay to simulate a breaker 52-3 lockout. Instead, the technician electrically operated the lockout relay, which unintentionally opened breaker 52-3. The technician failed to realize that steps 7.2.4 and 8.10 of Procedure MPE-ZZ-QY054 had been completed earlier during transfer trip testing. These steps opened and then closed all test switches for the transfer trip function of the lockout relays. Had the Procedure MPE-ZZ-QY054 tripping sequence test been started at the beginning, bus NB01 would not have been deenergized. The inadvertent loss of bus NB01 resulted in a loss of one of the two residual heat removal pumps, but not residual heat removal flow. Immediate corrective action was to stop all switchyard work and determine the cause of the bus lockout. The issue was entered into the licensee's corrective action program as Callaway Action Request 201108691.
Analysis.
Failure to establish the safe working conditions per the transfer trip procedure and failure to operate the lockout relay in the manner specified by the lockout relay procedure were performance deficiencies. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the availability of one of the two offsite power feeds to the plant was lost and the capability of shutdown cooling was reduced. Using Manual Chapter 0609, Appendix G, Attachment 1, Checklist 4 - PWR Refueling Operation: RCS level > 23 OR PWR Shutdown Operation with Time to Boil >2 hours And Inventory in the Pressurizer, this finding was of very low safety significance because it did not increase the likelihood of a loss of reactor coolant system inventory, did not degrade the ability to terminate a leak path or add reactor coolant system inventory when needed, and did not degrade the ability to recover decay heat removal, if lost. This finding has a cross-cutting aspect in the area of human performance associated with the work controls component because the electrical relay test technicians, onsite engineering, and work control staff failed to adequately maintain interfaces to communicate and safely coordinate significant switchyard activities to assure proper human performance H.3(b).
Enforcement.
Technical Specification 5.4.1.a, Procedures, requires that written procedures be established, implemented and maintained covering the activities specified in Appendix A of Regulatory Guide 1.33, Quality Assurance Program Requirements, February 1978. Appendix A, Item 9.a, required procedures for maintenance testing.
Procedure MPE-ZZ-QY054, "Inspection, Test, Calibration of Protective Instantaneous Overcurrent Relay, GE type, Revision 6, and Procedure MPE-ZZ-NY161, "Operational Test Sequence of 345 kV Safeguards Transformer A Circuit Breakers, Revision 5,were maintenance test procedures. Contrary to the above, on October 21, 2011, the licensee failed to correctly implement a written procedure covering an activity specified in Appendix A of regulatory Guide 1.33. Specifically, electrical relay test personnel did not manually operate the lockout relay per Step 7.1.14 of test Procedure MPE-ZZ-NY161
device 86-3. The relay technicians also failed to perform step 7.2.4 of Procedure MPE-ZZ-QY054 to open all applicable test switches for the lockout relays.
This resulted in a loss of train A components. Because this finding is of very low safety significance and was entered into the licensee's corrective action program as Callaway Action Request 201108691, this violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy:
NCV 05000483/2011005-07, Failure to Correctly Implement Plant Maintenance Procedures.
.3 (Closed) Licensee Event Reports 2010-009-00, 2010-009-01, and 2010-009-02: High-
Energy Line Break (HELB) Program Deficiencies On December 1, 2010, the licensee Nuclear Oversight audit of engineering programs identified deficiencies in the Callaway Plant high-energy line break barrier program.
Subsequent evaluation of these issues revealed three failures to maintain the operability of equipment located in the train A electrical penetration room following a potential high-energy line break in nonseismically analyzed auxiliary steam piping. Specifically, the harsh environment from a high-energy line break had the potential to impact safety related motor control center NG01B. The licensee identified five areas with deficient high-energy line break barrier controls. These instances involved inadequate control of high-energy line break barrier impairments and inadequate analysis of the high-energy line break hazards in engineering evaluations. License Event Reports 2010-009-00, 2010-009-01, and 2010-009-02 were submitted pursuant to 10 CFR 50.73(a)(2)(i)(B)and 10 CFR 50.73(a)(2)(ii)(B) as a condition prohibited by technical specifications and an unanalyzed condition that significantly degraded plant safety because plant equipment that would have been required to respond to a postulated high-energy line break event may not have been available. The resident inspectors and a Region IV senior risk analyst reviewed the licensee's most recent submittal and determined that the report adequately documented the issue, including the potential safety consequences and necessary corrective actions. Enforcement aspects associated with these license event reports are discussed in Section 40A7. No additional violations were identified during the inspectors' review. These license event reports are closed.
4OA6 Meetings
Exit Meeting Summary
On October 21, 2011, the inspectors presented the results of the radiation safety inspections to Mr. C. Reasoner, Vice President, Engineering, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
On June 24, 2011, the inspectors discussed the results of the licensed operator requalification program inspection with Mr. C. Reasoner, Vice President Engineering, and other members of the licensee's staff. The lead inspector obtained the final biennial examination results and telephonically exited with Mr. R. Barton, Manager, Training, on November 30, 2011. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any
materials examined during the inspection should be considered proprietary. No proprietary information was identified On October 28, 2011, the inspectors presented the inspection results of the review of in-service inspection activities to Mr. R. Barton, Manager, Training, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
On January 3, 2012, the resident inspectors presented the inspection results to Mr. F. Diya, Vice President Nuclear Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
4OA7 Licensee-Identified Violations
The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC Enforcement Policy for being dispositioned as non-cited violations. Documents reviewed in this inspection are listed in the attachment.
- Title 10 of the Code of Federal Regulations, Section 55.49, requires, in part, that facility licensees shall not engage in any activity that compromises the integrity of any application, test, or examination required by this part. The integrity of a test or examination is considered compromised if any activity, regardless of intent, affected, or, but for detection, would have affected the equitable and consistent administration of the test or examination. This includes activities related to the preparation, administration, and grading of the tests and examinations required by this part. Contrary to the above, during the 2010 annual operating exam cycle, the licensee engaged in an activity that compromised the integrity of a test required by 10 CFR Part 55. Specifically, training personnel administered JPMs to licensed operators on their operating tests that had been used for previous exams in excess of 50 percent. Administering an operating test with greater than 50 percent overlap from previously administered operating tests is considered a compromise of the integrity of the test in that it is a practice that, but for detection, would affect the equitable and consistent administration of the these tests.
The finding was more than minor because it adversely impacted the human performance attribute of the mitigating systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Additionally, if left uncorrected, the performance deficiency could have become more significant in that allowing licensed operators to return to the control room without valid demonstration of appropriate knowledge and abilities on the annual operating exams could be a precursor to a significant event if undetected performance deficiencies develop. The licensee has entered this issue into their corrective action program as Callaway Action Request 201009333. The finding was determined to have very low safety significance because, although the finding resulted in a compromise of the integrity of operating test components (JPMs) and compensatory
actions were not immediately taken when the compromise should have been discovered in 2010, the equitable and consistent administration of the test was not actually impacted by this compromise.
- Technical Specification 3.8.9, Distribution Systems - Operating, required, in part, that any applicable inoperable distribution subsystem be restored within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Technical Specification 3.8.9, Required Action D.1, required Mode 3 entry within 6 additional hours.
Contrary to the above, in the three years prior to December 1, 2010, the licensee identified three failures to maintain the operability of equipment located in the electrical penetration room, train A, following a potential high-energy line break in nonnuclear, nonseismically analyzed auxiliary steam piping to the boric acid batching tank.
Specifically, the harsh environment from a high-energy line break had the potential to impact safety related motor control center NG01B located in room 1410 for greater than the allowed 8 plus 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Additionally the licensee identified five areas with deficient high-energy line break barrier controls. The details of these deficient barrier controls were documented in License Event Report 05000483/2010-009-02. This finding is greater than minor because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this finding required a Phase 3 significance determination to evaluate the cumulative risk of the multiple high-energy line break deficient barrier controls.
The Region IV senior reactor analyst evaluated each case separately. For each area the approximate steam pipe break frequency was determined to be 2.5E-11/ft-hour.
Each initiating event frequency was adjusted by the exposure period to obtain the initiating event frequency on a per year basis. Thus the event frequencies were 2.5E-11*Length*Exposure time/year. The analyst used the Callaway Standardized Plant Analysis Risk model to calculate the conditional core damage probabilities. The Standardized Plant Analysis Risk analysis assumed that the steam line break occurred and that the affected component failed and was not recoverable. The analyst determined that the five cases total change in core damage frequency was less than 2.3E-8/year. Because the delta core damage frequency was less than 1E-6 and the finding was not a significant contributor to the large early release frequency, the finding was of very low safety significance (Green). This finding was entered in the licensees corrective action program as Callaway Action Request 201102329.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- R. Barton, Manager, Training
- K. Blair, Steam Generator Engineer
- J. Cortez, Assistant Manager, Operations Training
- J. Doughty, Inservice Inspection Program Owner
- K. Gilliam, Supervisor, Radiation Protection
- L. Graessle, Director, Plant Support
- J. Little, Regulatory Affairs, Supervisory Engineer
- A. Lord, Supervising Engineer, Simulator
- D. Neterer, Plant Director
- S. Petzel, Consulting Engineer, Licensing
- C. Reasoner, Vice President Engineering
- A. Schnitz, Engineer, Licensing
- C. Smith, Manager, Radiation Protection
- D. Stepanovic, Project Manager, Maintenance
- D. Thompson, Health Physicist
- R. Tiefenauer, Senior Training Supervisor
- L. Wilhelm, Operations Supervisor, Operations Training
LIST OF ITEMS
OPENED AND CLOSED
Opened and Closed
- 05000483/2011005-01 NCV Failure to Ensure Separation of Stainless Steel and Carbon Steel Hand Files and Wire Brushes (Section 1R08.1)
- 05000483/2011005-02 NCV Failure to Maintain Simulator Fidelity (Section 1R11.2.b.1)
- 05000483/2011005-03 FIN Failure to Conduct Simulator Testing In Accordance With ANSI/ANS 3.5-1998 (Section 1R11.2.b.2)
- 05000483/2011005-04 NCV Failure to Adequately Assess and Manage Outage Risk Associated with Significant Switchyard Work (Section 1R13)
- 05000483/2011005-05 NCV Improper Ground and Test Device Damages Residual Heat Removal Pump Switchgear (Section 1R19)
- 05000483/2011005-06 NCV Failure to Isolate Control Room Air Conditioning Unit SGK04A for Maintenance (Section 4OA3.b.1)
- 05000483/2011005-07 NCV Failure to Correctly Implement Plant Maintenance Procedures (Section 4OA3.b.2)
Attachment 1
Closed
- 05000483-2010-009-00 LER High Energy Line Break (HELB) Program Deficiencies
- 05000483-2010-009-01 (Section 4OA3)
- 05000483-2010-009-02