IR 05000483/2024001
ML24102A027 | |
Person / Time | |
---|---|
Site: | Callaway |
Issue date: | 04/16/2024 |
From: | Greg Werner NRC/RGN-IV/DORS/PBB |
To: | Diya F Ameren Missouri |
Proulx D | |
References | |
EPID L-2024-001-0000 IR 2024001 | |
Download: ML24102A027 (13) | |
Text
April 16, 2024
SUBJECT:
CALLAWAY PLANT - INTEGRATED INSPECTION REPORT 05000483/2024001
Dear Fadi Diya:
On March 31, 2024, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at the Callaway Plant. On April 10, 2024, the NRC inspectors discussed the results of this inspection with John Beck, Vice President of Nuclear Engineering, and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Gregory E. Werner, Chief Reactor Projects Branch B Division of Operating Reactor Safety Docket No. 05000483 License No. NPF-30
Enclosure:
As stated
Inspection Report
Docket Number: 05000483
License Number: NPF-30
Report Number: 05000483/2024001
Enterprise Identifier: I-2024-001-0000
Licensee: Ameren Missouri
Facility: Callaway Plant
Location: Steedman, MO
Inspection Dates: January 1 to March 31, 2024
Inspectors: N. Brown, Acting Senior Resident Inspector S. Schwind, Technical Assistant
Approved By: Gregory E. Werner, Chief Reactor Projects Branch B Division of Operating Reactor Safety
Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at the Callaway Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
The Callaway plant began the inspection period at rated thermal power. On February 15, 2024, a turbine trip occurred, followed by a reactor trip. A faulted unit auxiliary transformer surge capacitor bushing was found and replaced. The unit was brought critical February 18 and entered Mode 1. On February 19 while bringing the main turbine online it experienced high vibrations and operators had to manually trip the main turbine. Operators maintained the unit at approximately 8 percent power until the main turbine was brought online February 21 at which point operators began power ascension and reached rated thermal power on February 22. The unit operated at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) containment spray train A on January 17, 2024
- (2) essential service water train A on March 13, 2024
- (3) train B swing inverter NN18 on March 11, 2024
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) fire area D-2 emergency diesel generator B, room 5201 on January 2, 2024
- (2) fire area A-16 component cooling water A and B and heat exchanger area, rooms 1401 and 1406, on January 8, 2024
- (3) fire areas A-17 and A-18, electrical penetration rooms A and B, rooms 1409 and 1410, on January 8, 2024
- (4) fire area A-1, auxiliary building general area 1974', rooms 1101, 1102, 1120, 1121, 1122 and 1130 on February 26, 2024
- (5) fire area A-2, safety injection and charging pump rooms A, rooms 1113 and 1114, on February 26, 2024
71111.06 - Flood Protection Measures
Flooding Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated internal flooding mitigation protections in the auxiliary building on January 18, 2024.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the control room during surveillance testing and routine operations on March 19, 2024.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated emergency action level exercises on March 7, 2024.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:
- (1) component cooling water pump discharge check valve EGV0016 D on January 8, 2024
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) emergency diesel generator A exhaust leak troubleshooting on January 17, 2024
- (2) essential service water B strainer on January 26, 2024
- (3) through-wall leak in component cooling water A heat exchanger essential service water drain line, February 6, 2024
- (4) plant trip and emergent issues on February 18, 2024
- (5) essential service water B maintenance risk informed completion time on February 29, 2024
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) component cooling water A minimum wall thickness on January 8, 2024
- (2) emergency diesel generator A jacket water bolting on January 19, 2024
- (3) north electrical penetration room cooler SGL15A on February 1, 2024
- (4) safety injection accumulator C check valve BB8948C on February 28, 2024
- (5) door seal gap DSK 36092 on March 11, 2024
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)
The inspectors evaluated the following temporary or permanent modifications:
- (1) essential service water pipe replacement on January 8, 2024
- (2) safety related cooler/fan modifications on February 26, 2024
71111.24 - Testing and Maintenance of Equipment Important to Risk
The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:
Post-Maintenance Testing (PMT) (IP Section 03.01) (5 Samples)
- (1) feedwater isolation valve D rupture disk replacement on January 4, 2024
- (2) emergency diesel generator A exhaust leak troubleshooting on January 18, 2024
- (3) control room air conditioning system B SGK04B on January 26, 2024
- (4) essential service water B strainer on January 26, 2024
- (5) through-wall leak repair in the component cooling water A heat exchanger essential service water drain line, February 6, 2024
Surveillance Testing (IP Section 03.01) (2 Samples)
- (1) monthly testing of emergency diesel generator B on January 3, 2024
- (2) control room A air conditioning 18-month surveillance test on February 8, 2024
71114.06 - Drill Evaluation
Additional Drill and/or Training Evolution (2 Samples)
The inspectors evaluated:
- (1) team 4 emergency response organization training drill on January 11, 2024
- (2) team 5 emergency response organization training drill on January 18,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS06: Emergency AC Power Systems (IP Section 02.05)===
- (1) January 2023 through December 2023
MS10: Cooling Water Support Systems (IP Section 02.09) (1 Sample)
- (1) January 2023 through December 2023
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)
- (1) January 2023 through December 2023
BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)
- (1) January 2023 through December 2023
71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issue:
- (1) check valve BB8948C failed to seat during OSP-BB-VL006, on March 31, 2024
71153 - Follow Up of Events and Notices of Enforcement Discretion Personnel Performance (IP Section 03.03)
- (1) The inspectors evaluated turbine and reactor trip response on February 15, 2024.
Reporting (IP Section 03.05) (1 Sample)
The inspectors evaluated the 50.72 event report of the following issue:
- (1) turbine-driven auxiliary feedwater pump auto start on March 28,
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On April 10, 2024, the inspectors presented the integrated inspection results to John Beck, Vice President of Nuclear Engineering, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.04 Corrective Action Condition Reports 202401749
Documents
71111.04 Procedures OTN-EF-00001, Normal Valve Lineup Essential Service Water Pump House 32
CL0003 Train A
71111.04 Procedures OTN-EN-00001, Containment Spray System Normal Valve Lineup 13
CL0002
71111.04 Procedures OTN-NN-00002, NN18 B Train Inverter In Service Verification 0
Addendum 2
71111.05 Calculations KC-150 Fire Safety Analysis Calculation: KC-150 Fire Area: D-2 2
Diesel Generator B, Diesel Generator Building
Elevation 2000
71111.05 Engineering KC-52 Detailed Fire Modeling Report Fire Compartment: A-17 3
Evaluations Electrical Penetration Room B, Auxiliary Building,
Elevation 2026'
71111.05 Engineering KC-53 Detailed Fire Modeling Report Fire Compartment: A-18 4
Evaluations Electrical Penetration Room A, Auxiliary Building,
Elevation 2026'
71111.05 Fire Plans Fire Preplan 43
Manual
71111.05 Procedures OTO-KC-00001, Auxiliary Building 1974' - General Area 1
Addendum A-01
71111.05 Procedures OTO-KC-00001, Auxiliary Building 2026' - General Area 1
Addendum A-16
71111.05 Procedures OTO-KC-00001, Auxiliary Building 2026' - South Electrical Penetration Room 1
Addendum A-17
71111.05 Procedures OTO-KC-00001, Auxiliary Building 2026' - North Electrical Penetration Room1
Addendum A-18
71111.05 Procedures OTO-KC-00001, Diesel Generator Building 2000' - 'B' Diesel Generator Room1
Addendum D-02
71111.05 Procedures OTO-KC-0001, Auxiliary Building - 1974' Train 'A' ECCS Pump Rooms 1
Addendum A-02
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.06 Corrective Action Condition Reports 201402680, 202400404
Documents
71111.06 Miscellaneous ULDBD-FLOOD-Topical Area - Internal Flooding 1
001
71111.11Q Miscellaneous T61.0810 8 EAL Exercises 02/09/2024
71111.11Q Procedures APA-ZZ-00003 Shift Relief and Turnover 30
71111.11Q Procedures ODP-ZZ-00001, Annunciator Response 38
Addendum 1
71111.12 Corrective Action Condition Reports 202202985
Documents
71111.12 Miscellaneous Bolting Manual 20
71111.12 Miscellaneous OQCM Operational Quality Control Manual 35
71111.12 Work Orders Jobs 20201934
71111.13 Corrective Action Condition Reports 202001790, 202307764, 202400556, 202400664,
Documents 202400845, 202401065, 202401089, 202401134,
2401145, 202401164, 202401177, 202401213,
2401217, 202401255, 202401258
71111.13 Miscellaneous Summary of the Weekly Schedule 01/11/2024
71111.13 Miscellaneous RICT-2024-01 ESW Strainer RICT 0
71111.13 Miscellaneous RICT-2024-0226 ESW RICT 0
71111.13 Procedures APA-ZZ-00315, Risk Informed Completion Time (RICT) Program 2
Appendix D
71111.13 Work Orders Jobs 18001654, 24000408
71111.15 Corrective Action Condition Reports 202302380, 202400119, 202400391, 202000586,
Documents 202400593, 202400602, 202400673, 202400788
2400915, 202401634
71111.15 Drawings M-018-00309 Emergency Diesel Generator System 154
71111.15 Procedures APA-ZZ-00750 Hazard Barrier Program 30
71111.15 Procedures EDP-ZZ-01121 Raw Water System Predictive Performance Program 27
71111.15 Work Orders Jobs 22506696, 18001654, 23503549
71111.18 Corrective Action Condition Reports 202307723, 202400566
Documents
71111.18 Engineering MP 21-0011 RFR 210038 - Modification Request for Speed Changes for 1
Changes Safety Related Belt Driven Fans
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.18 Engineering MP 23-0039 Replace Section of EF-7-HBC Spool 4 with Stainless Steel 0
Changes
71111.18 Engineering EF-5069-SCD Essential Service Water (EF) System Categorization 1
Evaluations Document
71111.18 Procedures APA-ZZ-05069 10 CFR 50.69 Program Categorization and Alternative 30
Treatment
71111.18 Work Orders Jobs 23002810
71111.24 Corrective Action Condition Reports 202400373, 202400391, 202400409, 202400469,
Documents 202400497, 202400556, 202400939
71111.24 Miscellaneous Summary of the Weekly Schedule 01/11/2024
71111.24 Procedures APA-ZZ-00322, Post-Maintenance Test Program 38
Appendix E
71111.24 Procedures APA-ZZ-00661 Administration of Welding 22
71111.24 Procedures MSE-GK-0004A Refrigeration Cycle and Air Flow for SGK04A 7
71111.24 Procedures MSM-ZZ-QV004 Rupture Disc Replacement for FWIV and MSIV 2
71111.24 Procedures OSP-NE-0001A Standby Diesel Generator A Periodic Tests 71
71111.24 Procedures OSP-NE-0001B Standby Diesel Generator B Periodic Tests 70
71111.24 Work Orders Jobs 19507350, 18001654, 24000408, 22509342, 20512567,
23514351, 23002086, 22508560
71114.06 Miscellaneous 2024 EP WRO Training Drill Scenario
71151 Miscellaneous Cooling Water Systems Performance Indicator Data for
January 2023 through December 2023
71151 Miscellaneous Reactor Coolant System Specific Activity Performance
Indicator Data for January 2023 through December 2023
71151 Miscellaneous Reactor Coolant System Leakage Performance Indicator
Data for January 2023 through December 2023
71151 Miscellaneous Emergency AC Power Systems Performance Indicator Data
for January 2023 through December 2023
71152A Corrective Action Condition Reports 202203677, 202203737, 202307958, 202308035,
Documents 202308066, 202308073, 202308090, 202308108,
2308132, 202308194, 202308302, 202308315,
2308831, 202308855, 202308977, 202309098
Inspection Type Designation Description or Title Revision or
Procedure Date
71153 Corrective Action Condition Reports 202001790, 202301129, 202307764, 202400816,
Documents 202401065, 202401089, 202401134, 202401137,
2401145, 202401164, 202401177, 202401213,
2401217, 202401255, 202401258, 202402078,
2402247
71153 Procedures OTG-ZZ-00008 Normal Unit Recovery Guideline Following Reactor Trip 24
11