IR 05000483/2024002

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And Independent Spent Fuel Storage Installation Integrated Inspection Report 05000483/2024002 and 07201045/2024001
ML24198A046
Person / Time
Site: Callaway  
Issue date: 07/18/2024
From: Greg Werner
NRC/RGN-IV/DORS/PBB
To: Diya F
Ameren Missouri
References
IR 2024002, IR 2024001
Download: ML24198A046 (28)


Text

July 18, 2024

SUBJECT:

CALLAWAY PLANT AND INDEPENDENT SPENT FUEL STORAGE INSTALLATION - INTEGRATED INSPECTION REPORT 05000483/2024002 AND 07201045/2024001

Dear Fadi Diya:

On June 30, 2024, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at the Callaway Plant. On July 10, 2024, the NRC inspectors discussed the results of this inspection with K. Scott, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. These findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at the Callaway Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at the Callaway Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Gregory E. Werner, Chief Reactor Projects Branch B Division of Operating Reactor Safety Docket Nos. 05000483, 07201045 License No. NPF-30

Enclosure:

As stated

Inspection Report

Docket Number:

05000483 and 07201045

License Number:

NPF-30

Report Number:

05000483/2024002 and 07201045/2024001

Enterprise Identifier:

I-2024-002-0008 and I-2024-001-0015

Licensee:

Ameren Missouri

Facility:

Callaway Plant and Independent Spent Fuel Storage Installation

Location:

Steedman, MO

Inspection Dates:

April 1 to June 30, 2024

Inspectors:

B. Baca, Health Physicist

L. Brookhart, Senior Spent Fuel Storage Inspector

N. Brown, Resident Inspector

J. Freeman, Spent Fuel Storage Inspector

J. Melfi, Project Engineer

D. Proulx, Senior Project Engineer

S. Schwind, Senior Resident Inspector

E. Simpson, Nuclear Systems Scientist

Approved By:

Gregory E. Werner, Chief

Reactor Projects Branch B

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at the Callaway Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Provide Adequate Work Instructions for Performing Maintenance on the Standby Diesel Generator Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000483/2024002-01 Open/Closed

[H.1] -

Resources 71111.15 The inspectors reviewed a self-revealed Green finding and associated non-cited violation of Technical Specification 5.4.1.a for the licensees failure to have an adequate maintenance procedure as required by Regulatory Guide 1.33, Quality Assurance Program Requirements, revision 2, February 1978. Specifically, licensee work instruction PM1000121, revision 1, did not adequately provide the level of detail required to ensure jacket water bolting was torqued to the correct value during restoration from maintenance in refueling outage 25 resulting in the bolts being found loose during a January 2024 maintenance outage.

Failure to Take Timely Corrective Action for Nonconservative Technical Specifications Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000483/2024002-02 Open/Closed

[H.1] -

Resources 71152A The inspectors identified a finding and associated Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the licensees failure to promptly correct a condition adverse to quality regarding technical specification surveillance acceptance criteria. Specifically, from 2006 to June 2024, Technical Specification 3.8.1, AC Sources - Operating, and Technical Specification 3.8.2, AC Sources - Shutdown, contained surveillance acceptance criteria for diesel generator steady state frequency that were not justified by analysis.

Additional Tracking Items

None.

PLANT STATUS

The Callaway Plant began the inspection period at rated thermal power and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of high temperatures for the ultimate heat sink cooling tower and control building heating ventilation and air conditioning systems on June 27, 2024.

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from impending thunderstorms on May 7, 2024.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)diesel-driven fire pumps on April 22, 2024 (2)safety injection system train A partial alignment on April 23, 2024

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the control room envelope on June 24, 2024.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1)diesel-and electric-driven fire pumphouse on April 23, 2024 (2)essential service water pumphouse, fire areas UNPH and USPH, on April 24, 2024 (3)engineered safety features A switchgear room number 1, fire area C-9, on April 2, 2024 (4)engineered safety features B switchgear room number 2, fire area C-10, on April 2, 2024 (5)component cooling water pump and heat exchanger area A, room 1406, on June 20, 2024

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill on April 9, 2024.

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1)train B class 1E switchgear room air conditioning unit essential service water heat exchanger SGK05B on April 15, 2024

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during surveillance testing and routine operations on June 20, 2024.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated staff crew A emergency preparedness drill and exercise performance indicator scenario on May 23, 2024.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1)safety injection train B system on April 24, 2024

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1)diesel-driven fire pump A and electric-driven fire pump outage on April 22, 2024 (2)risk mitigation activities during increased turbine trip risk activities on April 30, 2024 (3)planned maintenance on emergency diesel generator train A and essential service water train A on May 9, 2024 (4)turbine-driven auxiliary feedwater pump maintenance outage on June 13, 2024

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (3 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1)component cooling water isolation valve EGHV0069B on April 11, 2024 (2)emergency diesel generator A operability on April 30, 2024 (3)valve EGHV0016, train B component cooling water supply/return isolation valve flange bolts not torqued to required value on May 22, 2024

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)temporary power installed in 480 volt load center for fire pumphouse on April 22-23, 2024

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (4 Samples)

(1)emergency diesel generator B post-maintenance test after exhaust leak repairs on April 4, 2024 (2)480 VAC NGO1 breakers on April 10, 2024 (3)essential service water train B post-maintenance test on April 4, 2024 (4)emergency diesel generator A testing following maintenance on May 9, 2024

Surveillance Testing (IP Section 03.01) (4 Samples)

(1)emergency diesel generator A monthly surveillance on April 10, 2024 (2)control rod partial movement on May 3, 2024 (3)residual heat removal pump B on June 14, 2024 (4)safety injection trains A and B signal slave relay testing on June 20, 2024

Inservice Testing (IST) (IP Section 03.01) (1 Sample)

(1)essential service water pump A inservice test on April 23,

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated how the licensee identifies the magnitude and extent of radiation levels and the concentrations and quantities of radioactive materials and how the licensee assesses radiological hazards.

Instructions to Workers (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated how the licensee instructs workers on plant-related radiological hazards and the radiation protection requirements intended to protect workers from those hazards.

Contamination and Radioactive Material Control (IP Section 03.03) (2 Samples)

The inspectors observed/evaluated the following licensee processes for monitoring and controlling contamination and radioactive material:

(1)radiation workers exiting the radiologically controlled area and monitoring personal items with the tool equipment monitors (2)demobilizing and packaging equipment from the dry spent fuel campaign under radiation work permit (RWP) 24DFSDEMOBE, "Demobilize Dry Fuel Storage Equipment," revision 0

Radiological Hazards Control and Work Coverage (IP Section 03.04) (4 Samples)

The inspectors evaluated the licensee's control of radiological hazards for the following radiological work:

(1)decontamination of dry spent fuel tools, equipment, and components under RWP CEC03CLOSE, "2024 Dry Fuel Storage Campaign-CEC03: Remove HI-TRAC from cask loading pit, decontaminate, close & prepare multipurpose canister (MPC)for movement CEC-03," revision 0 (2)demobilizing and packaging equipment from the dry spent fuel campaign under RWP 24DFSDEMOBE, "Demobilize Dry Fuel Storage equipment," revision 0 (3)dry spent fuel canister closure which included welding under RWP CEC03CLOSE, "2024 Dry Fuel Storage Campaign-CEC03: Remove HI-TRAC from cask loading pit, decontaminate, close & prepare MPC for movement CEC-03," revision 0 (4)dry spent fuel canister transfer to the UMAX storage under RWP CEC03TRAN, "2024 Dry Fuel Storage Campaign-CEC03: Move loaded HI-TRAC from Cask Wash Down Pit to Hi-Storm UMAX, Including Download CEC-03," revision 0 High Radiation Area and Very High Radiation Area Controls (IP Section 03.05) (5 Samples)

The inspectors evaluated licensee controls of the following high radiation areas (HRAs) and very high radiation areas:

(1)containment personnel hatch - locked HRA (2)radwaste drumming station (room 7213) - locked HRA (3)radwaste valve room (room 7220) - locked HRA (4)cask washdown pit containing MPC - HRA (5)radioactive material (spent resin) locked storage container - HRA Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 03.06) (1 Sample)

(1) The inspectors evaluated radiation worker and radiation protection technician performance as it pertains to radiation protection requirements.

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated licensee performance as it pertains to radioactive source term characterization.

External Dosimetry (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated how the licensee processes, stores, and uses external dosimetry.

Internal Dosimetry (IP Section 03.03) (1 Sample)

The inspectors evaluated the following internal dose assessments:

(1) six personnel contamination events since the previous inspection period

Special Dosimetric Situations (IP Section 03.04) (2 Samples)

The inspectors evaluated the following special dosimetric situations:

(1)three dose assessments for workers declared pregnant (2)nine extremity dose assessment evaluation for multipack dosimetry assignments made for RWP R26CAVDECON, "Cavity Decontamination Activities"

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04)===

(1) April 2023 through March 2024

MS08: Heat Removal Systems (IP Section 02.07) (1 Sample)

(1) April 2023 through March 2024

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) July 1 through March 31, 2023 PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)
(1) July 1 through March 31, 2023

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1)damaged hypoid gear in actuator for valve EMHV8821A (condition report 202401656)

(2)nonconservative values in Technical Specifications (TSs) 3.8.1 and 3.8.2 (condition report 200603324)

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

(1) The inspectors performed a review of the negative trend in the quality assurance records program.

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Follow Up (IP Section 03.01)

(1) The inspectors evaluated the automatic turbine-driven auxiliary feedwater pump actuation on March 29, 2024.
(2) The inspectors evaluated the invalid actuation of automatic turbine-driven auxiliary feedwater pump on March 29,

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

===60855 - Operation of an ISFSI The inspectors performed a review of the licensees independent spent fuel storage installation (ISFSI) activities to verify compliance with requirements of the Certificate of Compliance 72-1040, license amendment 0, the HI-STORM UMAX FSAR revision 2, and HI-STORM FW FSAR revision 3. The inspectors reviewed selected procedures, corrective action reports, and records to verify ISFSI operations were compliant with the certificate's TSs, requirements in the Final Safety Analysis Report, and NRC regulations.

Operation Of An ISFSI===

(1) The inspectors evaluated the licensees dry cask storage operations, from May 13 through May 17, 2024, during an on-site inspection. The Callaway ISFSI is located within the Part 50 reactor's protected area. The UMAX ISFSI vault was designed to hold 48 MPCs, each with 37 spent fuel assemblies (MPC-37). At the time of the routine loading inspection, the Callaway UMAX ISFSI contained a total of 36 canisters, and the licensee was in the process of loading and processing the 37th canister in the spent fuel building.

During the on-site inspection, the inspectors evaluated and observed the following activities:

  • walk-down of the ISFSI haul path
  • welding and non-destructive testing of the lid-to-shell weld
  • processing of the spent nuclear fuel for storage, including bulk water removal, forced helium dehydration, and helium backfill operations
  • final sealing of the canister, including welding of the vent and port cover plates, non-destructive testing, and helium leak-testing
  • heavy load lifts using the cask handling crane to remove the transfer cask with the loaded canister from the canister processing area to the HI-PORT
  • transportation of the 37th canister on the vertical cask transporter from the spent fuel building to the ISFSI using the HI-PORT
  • heavy load lifts to transfer the MPC-37 from the transfer cask to the vertical ventilated module The inspectors reviewed and evaluated the following documentation during the inspection:
  • fuel selection evaluations for the canisters loaded since the last NRC ISFSI inspection, the inspectors reviewed the contents of canisters 26-37 against the license's TSs for approved contents
  • radiation surveys for dose at the owner-controlled boundary to verify compliance with the requirements of 10 CFR 72.104 for calendar years 2021, 2022, and 2023
  • selected ISFSI related condition reports issued since the last NRC ISFSI inspection (April 2021)
  • quality assurance program implementation, including recent quality assurance audits, surveillances, receipt inspection, and quality control activities related to ISFSI operations
  • compliance to TSs for operational surveillance activities and Final Safety Analysis Report required annual maintenance activities
  • documentation of annual maintenance activities for the sites cask handling crane, vertical cask transporter, and special lifting devices
  • selected licensee design changes and program changes to the ISFSI performed under the site's 10 CFR 72.48 program
  • changes made by the licensee in the site's 10 CFR Part 72.212 evaluation report from revision 5 to revision

INSPECTION RESULTS

Failure to Provide Adequate Work Instructions for Performing Maintenance on the Standby Diesel Generator Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000483/2024002-01 Open/Closed

[H.1] -

Resources 71111.15 The inspectors reviewed a self-revealed Green finding and associated non-cited violation of TS 5.4.1.a for the licensees failure to have an adequate maintenance procedure as required by Regulatory Guide 1.33, Quality Assurance Program Requirements, revision 2, February 1978. Specifically, licensee work instruction PM1000121, revision 1, did not adequately provide the level of detail required to ensure jacket water bolting was torqued to the correct value during restoration from maintenance in refueling outage 25 resulting in the bolts being found loose during a January 2024 maintenance outage.

Description:

On January 18, 2024, during a maintenance window, a worker identified three loose bolts on the train A standby diesel generator jacket water cooling system piping flange.

The standby diesel generator jacket water cooling system is designed to provide cooling to the diesel cylinders and turbo chargers to ensure proper operation during the diesel generators 7-day mission time following a design basis accident.

The licensee stopped work, reinstalled the bolts, and performed an extent of condition walkdown on the train A and B standby diesel generators looking for loose bolting on the jacket water cooling piping. The walkdown did not identify any other loose bolts on the train A or B generators. A review of previously performed surveillance tests did not identify any leakage from the jacket water flange. The licensees review of the plant computer point associated with the jacket water makeup valve, KJZ0067, which would have actuated should there have been a leak in the jacket water cooling system, did not show any actuation since coming out of refueling outage 26 during the fall of 2023.

The licensee initiated condition report 202400391 and investigated how the bolts could have backed out. They identified that the last time the bolts were manipulated during maintenance was during refueling outage 25 in the spring of 2022. A review of the work instruction, PM1000121, Change Upper & Lower WTR HDR O-Rings & Jumper O-Rings, revision 1, found that the bolts were torqued to wrench tight. The Fairbanks Morse Generator Manual, M-018-00309, revision 155, contains a torque table for various metric thread diameters.

Based on the size of the bolting, M 12 x 1.75, the correct torque value for the bolts was 30-35 ft. lbs. The licensee identified that the lack of actual torque values in work instruction PM1000121 was the probable cause of the bolts backing out of the threaded fasteners.

Corrective Actions: The licensee reinstalled the bolts with thread locking compound, as allowed by Bolting Manual, revision 20, and torqued the bolts to the value specified in vendor manual M-018-00309. A revision to work instruction PM1000121, Change Upper & Lower WTR HDR O-Rings & Jumper O-Rings, was also made to include the torque values from the vendor manual and the use of thread locking compound.

Corrective Action References: The licensee entered these issues into the corrective action program with condition report 202400391.

Performance Assessment:

Performance Deficiency: The failure to provide adequate work instructions for performing maintenance on the standby diesel generator A was a performance deficiency.

Screening: The inspectors determined that the performance deficiency was more than minor because it was associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to include the vendor specified torque value for the standby diesel generator jacket water cooling bolts resulted in the bolts disengaging.

Significance: The inspectors assessed the significance of the finding using IMC 0609 appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined the finding impacted mitigating systems and used exhibit 2 to evaluate the condition. The finding was determined to be of very low safety significance (Green)because it

(1) was not a deficiency affecting design or qualification of a mitigating system,
(2) does not represent a loss of the probability risk analysis (PRA) function of a single train TS system for greater than allowed outage time,
(3) does not represent a loss of PRA function of one train of a multi-train TS system for greater than its allowed outage time,
(4) does not represent a loss of the PRA function of two separate TS systems for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,
(5) does not represent a loss of PRA system and/or function as defined by the plant risk information e-book or the licensees PRA for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and
(6) does not result in the loss of a high safety-significant, non-TS train for greater than 3 days.

Cross-Cutting Aspect: Human Performance, H.1 - Resources: Leaders ensure that personnel, equipment, procedures, and other resources are available and adequate to support nuclear safety. Specifically, the licensees procedure was inadequate to ensure the jacket water flange bolts did not back out.

Enforcement:

Violation: Technical Specification 5.4.1.a, Procedures, states in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures listed in Regulatory Guide 1.33, Quality Assurance Program Requirements, revision 2, appendix A, February 1978. Regulatory Guide 1.33, revision 2, appendix A, section 9, Procedures for Performing Maintenance, requires, in part, that maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. The licensee established work instruction, PM1000121, Change Upper &

Lower WTR HDR O-Rings & Jumper O-Rings, Revision 1, in part, to meet this requirement.

Contrary to the above, work instruction PM1000121 which was performed on, April 27, 2022, failed to include adequate instructions for the torquing of the train A standby diesel generator jacket water cooling flange bolts. As a result, the bolts were found loose during maintenance in January 2024.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with section 2.3.2 of the Enforcement Policy.

Failure to take Timely Corrective Action for Nonconservative Technical Specifications Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000483/2024002-02 Open/Closed

[H.1] -

Resources 71152A The inspectors identified a finding and associated Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the licensees failure to promptly correct a condition adverse to quality regarding technical specification surveillance acceptance criteria. Specifically, from 2006 to June 2024, Technical Specification 3.8.1, AC Sources - Operating, and Technical Specification 3.8.2, AC Sources - Shutdown, contained surveillance acceptance criteria for diesel generator steady state frequency that were not justified by analysis

Description:

In 1993, Westinghouse issued Nuclear Safety Advisory Letter NSAL 93-1907 to inform licensees that the standard TSs for diesel generator test frequencies in TS 3.8.1 (i.e. 58.8 to 61.2 Hz) were just reference values and were not justified by analysis. The NSAL noted that the lower end of the limit, 58.8 Hz, was not sufficient to support assumed flowrates of safety-related equipment powered by the diesel generators, and recommended this TS be changed to require frequencies from 60-61.2 Hz. When the licensee received this letter, they scheduled a periodic preventive maintenance item to verify diesel generator frequencies were greater than 60 Hz and closed the issue. The TS was not amended, and the periodic surveillance procedures were not revised to reflect the new criteria.

On April 27, 2006, the licensee received an operating experience notification concerning another facility that identified that the diesel generator surveillance frequency limits specified in the TS were nonconservative because they also used the reference values of 58.8 to 61.2 Hz rather than having acceptance criteria justified by analysis. It was also noted that the vendor had recommended acceptance criteria greater than 60 Hz to meet the assumed flowrates of the safety analysis. The licensee initiated condition report 200603324 to place this item into the corrective action program.

The licensees initial response was to follow the guidance of Administrative Letter 98-10, Dispositioning of Technical Specifications that are Insufficient to Assure Plant Safety, which was applicable at the time. This guidance stated that upon discovery that a TS was not sufficient to assure plant safety, the licensee should immediately impose administrative limits in plant procedures to assure safety as an interim measure, then promptly submit a license amendment request (LAR) to correct the condition in accordance with 10 CFR Part 50, appendix B, criterion XVI. The administrative letter gave two examples where licensees had inadequate responses to a nonconservative TS, in which the licensees took over an operating cycle (18 months) to resolve the deficient TS.

The licensee noted that TS surveillance requirement (SR) 3.8.1.2 (monthly surveillance),

TS SR 3.8.1.11 (18 months) and TS SR 3.8.1.19 (18 months) required the licensee to verify that the diesel generators maintain steady state frequencies of 58.8 to 61.2 Hz following fast starts. The licensee took action to revise procedure OSP-SA-2413A[B], Train A [B] Diesel Generator and Sequencer Testing, the 18-month surveillance tests, to include the administrative limits for frequency prescribed by the vendor of 60 to 61.2 Hz. The licensee did not revise the monthly surveillance procedure since it required the diesel generator to be synchronized to and follow grid frequency which would not indicate health of the diesel generator. The licensee took the position that the TS SR limits on steady state frequency only applied to the fully loaded condition when synchronized to the grid, and not when unloaded.

After imposing administrative controls, the licensee drafted LAR OL-1271 to correct TS SRs 3.8.1.2, 3.8.1.11, and 3.8.1.19 to implement the more restrictive acceptance range of diesel generator frequency to 60 to 61.2 Hz. During a meeting with operations, engineering, licensing, and quality assurance management to review the LAR, the licensee determined not to submit the LAR due to concerns about potential operability issues and/or the increased potential for TS noncompliance that could be introduced by changing the minimum required steady-state frequency to greater than or equal to 60 Hz. There was no discussion as to whether the current TS represented safe operation. Engineering was directed to find an alternate approach. In 2009, the licensee closed the corrective action to revise the TS because inadequate diesel generator TS was considered an industry issue. No additional actions were taken until 2015, when the licensee reopened the corrective action to amend the nonconservative TS.

In 2015, the licensee noted that Westinghouse had developed WCAP-17398-NP in 2012, which included a calculation methodology to precisely calculate the acceptable voltage and frequency to maintain adequate emergency core cooling flows post-accident. The NRC provided a safety evaluation report in February 2016. The licensee further delayed implementation of an amendment to TS 3.8.1 until Westinghouse was ready to issue a generic TS frequency change for diesel generators, and thus did not develop an LAR.

In 2017, the licensee updated condition report 200603324 to further extend the completion of revising the TS, with the statement that there was a risk that the next NRC comprehensive design basis inspection may identify the issue. Further entries indicated that licensee was waiting for an industry solution to the issue.

On April 25, 2024, while reviewing the morning leadership package, the inspectors noted that the licensee had an entry under open operability determinations titled Technical Specifications 3.8.1 and 3.8.2 are Nonconservative, referencing condition report 200603324 with a forecast closure date of 2026. The inspectors noted that Regulatory Guide 1.239, Licensee Actions to Address Nonconservative Technical Specifications, states the following:

Occasionally, licensees have determined that the TS may be nonconservative. Examples include, but are not limited to, an improper or inadequate TS value, required action, or completion time. When this occurs, in the interim, licensees typically enter the nonconservative TS into their corrective action program, conduct an evaluation, and, if necessary, institute administrative controls that instruct the operators to maintain a more restrictive value for a particular parameter or to take a more conservative action. Following the implementation of such administrative controls, most licensees have properly considered reporting under 10 CFR 50.72, 10 CFR 50.73, or both and have promptly submitted a license amendment request to correct the TS. However, some licensees have failed to comply with NRC reporting requirements, significantly delayed submitting a license amendment request to correct the TS, or improperly concluded that a license amendment request was unnecessary if administrative controls are implemented.

Regulatory Guide 1.239 also superseded Administrative Letter 98-10 and endorsed the guidance of NEI 15-03 Licensee Actions to Address Nonconservative Technical Specifications. The guidance of NEI 15-03 repeated the actions of NRC Administrative Letter 98-10, that, upon identification of a nonconservative TS, licensees should implement administrative controls on a short-term interim basis, and promptly submit a license amendment. It also states that the generic nature of a nonconservative TS does not alleviate the licensees responsibility to promptly correct their TS. The NEI guidance also contains an example of a violation of 10 CFR Part 50, appendix B, criterion XVI, in which a licensee waited 5 years to correct a nonconservative TS related to diesel generator frequency.

Since the licensee had not corrected the diesel generator TS 3.8.1 frequency range for over 18 years, the inspectors concluded that was not timely corrective action, and thus a violation of 10 CFR Part 50, appendix B, criterion XVI.

Corrective Actions: The licensee initiated a condition report to enter this item into the corrective action program and plan to submit a license amendment request in the last quarter of 2024.

Corrective Action References: Condition Report 200603324.

Performance Assessment:

Performance Deficiency: The licensees failure to promptly correct a condition adverse to quality was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency was associated with failure to correct nonconservative TSs that would allow diesel generator operation outside the bounds of the safety analysis.

Significance: The inspectors assessed the significance of the finding using IMC 0609 appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined the finding impacted mitigating systems and used exhibit 2 to evaluate the condition. The finding was determined to be of very low safety significance (Green)because it was a deficiency affecting the design of a mitigating system and the emergency diesel generator maintained its probabilistic risk assessment functionality.

Cross-Cutting Aspect: H.1 - Resources: Leaders ensure that personnel, equipment, procedures, and other resources are available and adequate to support nuclear safety.

Specifically, the licensee did not commit the resources to promptly correct the inadequate TSs. Although the initial performance deficiency occurred greater than three years prior, the condition continues until the TSs are corrected.

Enforcement:

Violation: Title 10 of CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected.

Contrary to the above, from April 14, 2006, to June 30, 2024, a condition adverse to quality was not promptly corrected. Specifically, in April 2006, the licensee was informed that TS SRs 3.8.1.2, 3.8.1.11 and 3.8.1.19 were nonconservative because the acceptance criteria of 58.8 to 61.2 Hz for diesel generator frequency was not justified by analysis and should be 60 to 61.2 Hz. However, the licensee had not taken action to correct the nonconservative TSs as of June 2024.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observation: The inspectors performed a review of the negative trend in the quality assurance records program.

71152S The inspectors performed a review of the of potential adverse trends in the licensees corrective action program with emphasis on the implementation of the licensees quality assurance record program. Inspectors sampled a population of condition reports during the period of January 1 through June 30, 2024. Based on the samples reviewed, the inspectors identified a negative trend in the quality assurance records program associated with 11 condition reports regarding missing or incomplete records, improper record storage, and missing timeliness deadlines for record retention. The inspectors discussed this trend with the licensee, and they initiated condition report 202404599 to address the negative trend.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On July 10, 2024, the inspectors presented the integrated inspection results to K. Scott, Site Vice President, and other members of the licensee staff.
  • On June 27, 2024, the inspectors presented the occupational radiation safety inspection results to K. Scott, Site Vice President, and other members of the licensee staff.
  • On May 16, 2024, the inspectors presented the ISFSI inspection results to W. Witt, Senior Director Nuclear Operations, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

60855

Corrective Action

Documents

2300487

Regarding Holtec Certificate of Compliance (CoC) 1040

Amendment 0, Revision 1

60855

Engineering

Changes

2.48-1597

Aluminum basket shim for HI-STORM FW

60855

Engineering

Changes

2.48-1608

Change in HI-STORM UMAX FSAR computer model

program

60855

Miscellaneous

CFR 72.212

Evaluation Report

Callaway Plant,

Unit 1

Dry Fuel Storage System for Spent Nuclear Fuel Docket

Number 72-1045

60855

Miscellaneous

HGMPC0001

Loading Plan

Loading plan for Canister HGMPC0001

60855

Miscellaneous

HI-STORM FW

FSAR

Final safety analysis report for FW system

60855

Miscellaneous

Holtec 1040 HI-

STORM UMAX

FSAR

Final safety analysis report for HI-STORM UMAX

60855

Miscellaneous

Holtec 1040

UMAX License

Certificate of Compliance No. 1040 for the HI-STORM

UMAX cask storage system

60855

Procedures

HSP-366

HI-TRAC Lift Lugs inspection

60855

Procedures

HSP-720

Inspection of Horizontal Lift beam, lift links, and downloader

components for ASME B30.2 requirements

60855

Procedures

OSP-ZZ-00001

Control Room Shift and Daily Log Readings and Channel

Checks

60855

Procedures

Vent Surveillance

Documentation of Technical Specification requirements for

requested dates

60855

Radiation

Surveys

ISFSI Pad Survey

Survey CA-M-20240222-4 Semi Annual ISFSI Pad Survey

60855

Radiation

Surveys

ISFSI Posted

OSL Data

Verify compliance with 10 CFR 72.104 requirements.

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

60855

Self-Assessments

Dry Cask Storage

Surveillance

SP23005 Letter to

File

QA surveillance

60855

Self-Assessments Nuclear Oversight

Audit of Dry Fuel

Storage AP21005

Dry Fuel Storage program QA audit

60855

Work Orders

JOB 21500410-

500

Annual inspection of large overhead cask handling crane

meeting ASME B30.2 requirements

2/14/2023

71111.01

Corrective Action

Documents

Condition Reports

2400283, 202402233, 202402961

71111.01

Procedures

APA-ZZ-00322,

Appendix B

Work Week Schedule and Execution

71111.01

Procedures

OTO-ZZ-00012

Severe Weather

71111.01

Procedures

PDP-ZZ-00027

Seasonal Readiness Program

71111.01

Work Orders

Jobs

17001890, 17004923, 19003303, 19004768

71111.04

Corrective Action

Documents

Condition Reports

202207673, 202208438, 202302688, 202307412,

2401673, 202403710

71111.04

Procedures

APA-ZZ-00703

Fire Protection Operability Criteria and Surveillance

Requirements

71111.04

Procedures

EDP-ZZ-01012

Control Room Envelope Habitability Program

71111.04

Procedures

EDP-ZZ-04107

HVAC Pressure Boundary Control

71111.04

Procedures

OTN-EM-00001

Safety Injection System

71111.04

Procedures

OTN-EM-00001,

CL0002

Safety Injection System Outside Containment Valve Lineup

71111.05

Calculations

KC-51

Detailed Fire Modeling Report, Fire Compartment A-16

71111.05

Calculations

KC-96

Fire Safety Analysis Calculation, Fire Area A-16

71111.05

Miscellaneous

Fire Preplan Manual

71111.05

Miscellaneous

T210.0001

Training Scenario Fire Drill Number 24-1

71111.05

Procedures

OTO-KC-00001,

Addendum C-10

Control Building South Engineered Safety Features

Switchgear Room

71111.05

Procedures

OTO-KC-00001,

Addendum C-9

Control Building North Engineered Safety Features

Switchgear Room

71111.07A

Corrective Action

Condition Reports

2302663, 202303127, 202304836, 202309038,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

2402779

71111.07A

Miscellaneous

Heat Exchanger Inspection Report

04/15/2024

71111.07A

Procedures

EDP-ZZ-01112

Heat Exchanger Predictive Performance Manual

71111.07A

Work Orders

Jobs

251680, 235000870

71111.11Q

Miscellaneous

Emergency Preparedness LOCT cycle 24-3 DEPI on

May 23, 2024

05/06/2024

through

06/21/2;024

71111.11Q

Procedures

APA-ZZ-00003

Shift Relief and Turnover

71111.11Q

Procedures

ODP-ZZ-00001,

Addendum 1

Annunciator Response

71111.11Q

Procedures

ODP-ZZ-000011

Control Room Decorum

Procedures

OSP-EM-V001B

Safety Injection System Train B Valve Inservice Test

71111.12

Work Orders

Jobs

20505514, 23002819, 21505329, 18504363, 22511757,

2004100, 205106820

71111.13

Miscellaneous

Daily Site Risk Assessment

6/11/2024

through

6/13/2024

71111.13

Miscellaneous

Shift Managers Operational Focus Items

6/11/2024

through

6/13/2024

71111.13

Miscellaneous

Shift Managers Operational Focus Items

04/30/2024

71111.13

Miscellaneous

Daily Site Risk Assessment

04/30/2024

71111.13

Miscellaneous

2050029

Risk Assessment for Fire Pump Outage

04/23/2024

71111.13

Miscellaneous

Requests for

Resolution

06316A, 014080B, 240111

71111.13

Procedures

APA-ZZ-00315

Risk Management Programs

71111.13

Procedures

APA-ZZ-00315

Appendix B

Technical Specification Risk Assessments

71111.13

Procedures

APA-ZZ-00315

Appendix C

Risk Management Actions

71111.13

Procedures

APA-ZZ-00315,

Appendix A

Configuration Risk Management Program - Online

and 4

71111.13

Procedures

APA-ZZ-00750

Hazard Barrier Program

71111.13

Work Orders

Jobs

18001564, 22512274

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.15

Corrective Action

Documents

Condition Reports

2401648, 202403190, 202403496

71111.15

Procedures

APA-ZZ-00801

Foreign Material Exclusion

71111.15

Procedures

CTP-SJ-01102

Auxiliary Building Sample Station (SJ-143) Operation

71111.15

Procedures

KDP-ZZ-00013

Emergency Response Facility and Equipment Evaluation

71111.18

Procedures

APA-ZZ-00605

Temporary System Modifications

045

71111.18

Work Orders

Job

20500029.270

Install Temporary Power to CPKC1002A AND CPKC1002B

71111.18

Work Orders

WPA 115357

Install Temporary Power to CPKC 1002A and CPKC 1002B

04/18/2024

71111.24

Corrective Action

Documents

Condition Reports

2402529, 202402598, 202402599, 202402614,

2404220

71111.24

Procedures

ITM-SF-00006

CRD Current Trace Testing

71111.24

Procedures

ODP-ZZ-00008

Nitrogen Monitoring Required in Both A and B Emergency

Diesel Generator Rooms While Diesel Running

71111.24

Procedures

OSP-EJ-P001B

RHR Train B Inservice Test - Group A

71111.24

Procedures

OSP-NE-0001A

Standby Diesel Generator A Periodic Tests

71111.24

Procedures

OSP-SA-0014A

Train A SIS Slave Relay Test

71111.24

Procedures

OSP-SA-0014B

Train B SIS Slave Relay Test

71111.24

Procedures

OSP-SF-00002

Control Rod Partial Movement

71111.24

Procedures

OTS-SF-00001

Control Road Repositioning

71111.24

Work Orders

Jobs

24502791, 19507533, 19507535, 22513159, 24500629,

24500650, 24503681, 24504110, 18001654.911, 18004031,

20505498, 21000903, 22510721, 22512340, 23001676,

24501210

71124.01

ALARA Plans

24-ISFSI Project

24 Dry Fuel Storage Campaign ALARA Plan

3/11/2024

71124.01

Procedures

HDP-ZZ-01200

Radiation Work Permits

71124.01

Procedures

HDP-ZZ-01500

Radiological Postings

71124.01

Procedures

HDP-ZZ-03000

Radiological Survey Program

71124.01

Procedures

HDP-ZZ-03000

APPB

Performing Radiation Surveys

71124.01

Procedures

HDP-ZZ-03000

APPC

Performing Contamination Surveys

71124.01

Procedures

HDP-ZZ-03000

Spent Fuel Storage Cask Surveys

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

APPH

71124.01

Procedures

HDP-ZZ-06000

Contamination Control and Alpha Monitoring Program

71124.01

Radiation

Surveys

CA-M-20240513-

24 DFS CEC 01 MPC 317 Survey Moving to Cask

Washdown Pit

05/13/2024

71124.01

Radiation

Surveys

CA-M-20240513-

24 DFS CEC 01 MPC 317 Decon/Downpost CA of Hi-

Trac/MPC in Cask Washdown Pit

05/13/2024

71124.01

Radiation

Surveys

CA-M-20240513-

24 DFS CEC 01 MPC 317 Annulus Technical

Specification

05/13/2024

71124.01

Radiation

Surveys

CA-M-20240513-

24 DFS CEC 01 MPC 317 Cask Washdown Pit MPC/Hi-

Trac Lower Pit Pre/Post Decon Survey

05/13/2024

71124.01

Radiation

Surveys

CA-M-20240514-

24 DFS Fuel Building 2026-foot Cask Washdown Pit Post

Blowdown Survey (CEC 01 MPC 317)

05/14/2024

71124.01

Radiation

Surveys

CA-M-20240514-

24 DFS ROVA Removal/Post Shielding Removal (CEC 01

MPC 317)

05/14/2024

71124.01

Radiation

Surveys

CA-M-20240515-

24 DFS Technical Specification (CEC 01 MPC 317)

05/15/2024

71124.01

Radiation

Surveys

CA-M-20240515-

24 DFS CEC 01 MPC 317 Technical Specification

05/15/2024

71124.01

Radiation

Surveys

CA-M-20240515-

24 DFS CEC 01 MPC 317 ISFSI Mating Device

05/15/2024

71124.01

Radiation

Surveys

CA-M-20240520-

24 DFS CEC 02 MPC 318 Survey Moving to Cask

Washdown Pit

05/20/2024

71124.01

Radiation

Surveys

CA-M-20240520-

24 DFS CEC 02 MPC 318 Post Blowdown/Gross Dewater

Survey

05/21/2024

71124.01

Radiation

Surveys

CA-M-20240520-

24 DFS CEC 02 MPC 318 Annulus Technical

Specification

05/20/2024

71124.01

Radiation

Surveys

CA-M-20240520-

24 DFS CEC 02 MPC 318 Decon/Downpost CA of Hi-

Trac/MPC in Cask Washdown Pit

05/20/2024

71124.01

Radiation

Surveys

CA-M-20240522-

24 DFS CEC 02 MPC 318 Hi-Trac Top View-RVOA

Removal

05/22/2024

71124.01

Radiation

Surveys

CA-M-20240523-

24 DFS CEC 02 MPC 318 Technical Specification

05/22/2024

71124.01

Radiation

Surveys

CA-M-20240523-

24 DFS CEC 02 MPC 318 Technical Specification

05/23/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.01

Radiation

Surveys

CA-M-20240523-

24 DFS CEC 02 MPC 318 - ISFSI Mating Device/Hi-Trac

Lid

05/23/2024

71124.01

Radiation

Surveys

CA-M-20240526-

24 DFS CEC 03 MPC 319 Decon/Downpost CA of Hi-

Trac/MPC in Cask Washdown Pit

05/26/2024

71124.01

Radiation

Surveys

CA-M-20240527-

24 DFS CEC 03 MPC 319 Survey Moving to Cask

Washdown Pit

05/27/2024

71124.01

Radiation

Surveys

CA-M-20240527-

24 DFS CEC 03 MPC 319 Annulus Technical

Specification

05/27/2024

71124.01

Radiation

Surveys

CA-M-20240528-

24 DFS CEC 03 MPC 319 Cask Washdown Pit Post

Blowdown Survey

05/27/2024

71124.01

Radiation

Surveys

CA-M-20240528-

24 DFS Technical Specification CEC 03 MPC 319

05/28/2024

71124.01

Radiation

Surveys

CA-M-20240529-

24 DFS CEC 03MPC 319 ROVA Removal/Post Shielding

Removal

05/29/2024

71124.01

Radiation Work

Permits (RWPs)

24DFSDEMOBE

Demobilize and store DFS equipment which includes

disassembly, decontamination support, RP coverage and

storage activities

71124.01

Radiation Work

Permits (RWPs)

24DFSHCA

Decon activities on HI-TRAC Annulus Area

71124.01

Radiation Work

Permits (RWPs)

CEC01CLOSE

24 DRY FUEL STORAGE CAMPAIGN CEC-01: Remove

HI-TRAC from cask loading pit, decontaminate, close &

prepare MPC for movement CEC-01

71124.01

Radiation Work

Permits (RWPs)

CEC02CLOSE

24 DRY FUEL STORAGE CAMPAIGN CEC-02: Remove

HI-TRAC from cask loading pit, decontaminate, close &

prepare MPC for movement CEC-02

71124.01

Radiation Work

Permits (RWPs)

CEC03CLOSE

24 DRY FUEL STORAGE CAMPAIGN CEC-03: Remove

HI-TRAC from cask loading pit, decontaminate, close &

prepare MPC for movement CEC-03

71124.04

Calibration

Records

NA

Fast Scan Calibration Check Count

Multiple

71124.04

Calibration

Records

NA

Fast Scan Background Check QA Count

Multiple

71124.04

Calibration

Records

NA

Whole Body Counter Calibration Check Count

Multiple

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.04

Calibration

Records

NA

Whole Body Counter Background Check QA Count

Multiple

71124.04

Corrective Action

Documents

Condition Reports

2204651, 202206786, 202302813, 202307061,

2307654, 202307679, 202308189, 202402537,

2404078, 202404415

71124.04

Procedures

HTP-ZZ-01302-

DTI-DPW

Response to Positive In Vivo Count for Declared Pregnant

Woman

71124.04

Procedures

HTP-ZZ-01302-

DTI-Medical

Admin

Response to a Medical Administration of Radioactive

Nuclides

71124.04

Procedures

HTP-ZZ-01433-

DTI-Multipack

Sentinel Multi-Pack Operations

71124.04

Procedures

HTP-ZZ-01480-

DTI-SRD

External Radiation Dose Evaluation SRD Related

71124.04

Procedures

HTP-ZZ-01489-

DTI-DLR

External Radiation Dose Evaluation DLR Related

71124.04

Procedures

HTP-ZZ-06009

Personnel Contamination Assessment and Decontamination

71124.04

Procedures

RP-DTI-EXT-

DOS-DLR-

Operations

DLR Operations

71124.04

Procedures

RP-DTI-EXT-

DOS-DLR-

Processing

Disposition of Dosimeter of Legal Record for Processing

71124.04

Procedures

RP-DTI-

FASTSCAN-OP

Operation of the Canberra FastScan

71124.04

Procedures

RP-DTI-In Vitro

Bioassay

In-Vitro Bioassay Sample Collection

71124.04

Procedures

RP-DTI-

VARSKIN-Use

VARSKIN Use

71124.04

Procedures

RP-STI-CHAIR-

OP

Whole Body Chair Operations

71124.04

Radiation Work

Permits (RWPs)

R26CAVDECON

Specific Radiation Work Permit

71151

Miscellaneous

Radiological controlled area greater than 100 mrem dose

05/28/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

accrued per entry summary

71151

Miscellaneous

Callaway Energy Center 2023 Annual Radioactive Effluent

Release Report

04/30/2024

71151

Miscellaneous

PM0911004

Dose Assessment from Liquid Effluents

03/31/2024

71151

Miscellaneous

PM0911009

Dose Assessment from Noble Gases

03/31/2024

71151

Miscellaneous

PM0911010

Dose Assessment from Radioiodines and Particulates

03/31/2024

71152A

Corrective Action

Documents

Condition Reports

200603324, 202402477

71152A

Miscellaneous

LTU 05-03

Flowserve Technical Update

71152A

Miscellaneous

LTU-05-02

FLowserve Technical Update

03/05/2009

71152A

Miscellaneous

NEI 15-03

Licensee Actions to Address Nonconservative Technical

Specifications

71152S

Corrective Action

Documents

Condition Reports

2400041, 202400891, 202400956, 202401387,

2401847, 202401986, 202402062, 202402123,

2403580, 202403696, 202403790, 202404131,

2404208, 202404599

71152S

Procedures

APA-ZZ-00220

Record Management

71153

Miscellaneous

Event Number 57043

Automatic Turbine-Driven Auxiliary Feedwater Pump

Actuation

71153

Miscellaneous

Event Number 57091

Invalid Actuation of Automatic Turbine-Driven Auxiliary

Feedwater Pump