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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20199K8331997-11-21021 November 1997 Ro:On 960528,detected Abnormal Metallic Impact Sounds.Caused by Confirmed Loose Part in Sg.Removed SG 4 Hot Leg Manway & Found Loose Metal Object Inside,Performed Engineering Evaluation & Performed Insp of Guide Tube Support Pins ML20148F0901997-05-29029 May 1997 Special Rept:On 970513,CR Personnel Began Receiving Intermittent Alarms from Digital Metal Impact Monitoring Sys Annunciator.Monitoring of Impact Continuing & Search for Object & Insp for Damage Will Be Performed at Next Outage ML20128P2151996-10-10010 October 1996 Special Rept 2-96-2:on 960921,start Attempt of Maint Run of DG2A Was Made But Engine Did Not Start.Caused by Loose Voltage Regulator Integrated Circuit Boards.Loose Boards Were Removed,Contacts Adjusted & Returned to Sockets ML20129F8731996-10-0101 October 1996 Special Rept 2-96-1:on 960908,DG 2A Started But Tripped. Investigation Found Six Main Bearing Temp Sensor Venting Pressure.Defective Main Bearing Sensor Replaced ML20112H0071996-06-10010 June 1996 Ro:On 960528,detected Abnormal Metallic Impact Sounds. Caused by Confirmed Loose Part in Steam Generator. Engineering Evaluation Performed & Repairs & Modifications Scheduled for Next Refueling Outage ML20101N0491996-04-0202 April 1996 Special Rept 1-96-2:on 960310 & 23,non-valid DG Failures Occurred.Rocker Arm Clearances Adjusted & DGs Restarted & Operated Successfully ML20092B6281995-09-0707 September 1995 Special Rept:On 950816,non-valid DG Failure Occurred Due to Circuits Not Properly set.Post-maint Surveillance Testing Discovered Problem Prior to DG Return to Svc ML20087D6211995-08-0707 August 1995 Special Rept:On 950720,total of 33 3/4 Gallons of Grease Had Been Lost from Tendon.Horizontal Tendon H120 Was Detensioned & Strand Was Removed for Visual Exam & Tensile Testing ML20086S2641995-07-26026 July 1995 Special Rept:On 950628,generator Output Voltage Dropped Below Normal Rated Value.Caused by Malfunctioning Transformer T3.Voltage Regulator 2 Replaced,Tested & Returned to Svc on 950629 ML20086L9481995-07-14014 July 1995 Special Rept:On 950517,operators Experienced Difficulties W/Excitation of Generator in Form of Voltage Swings When Utilizing Each of Two Voltage Regulators ML20086B8921995-06-29029 June 1995 Special Rept 2-95-3:on 950607,three non-valid DG2A Failures Occurred Due to Malfunctioning Automatic Min Excitation Limiter.Malfunctioning Automatic Min Excitation Limiter Removed from Service ML20086H1311995-06-16016 June 1995 Special Rept:On 950517,operators Experienced Difficulties W/Excitation of Generator in Form of Voltage Swings When Utilizing Each of Two Voltage Regulators ML20084M7171995-06-0202 June 1995 Special Rept:On 950517,operators Experienced Difficulties W/Excitation of Generator in Form of Voltage Swings When Utilizing Each of Two Voltage Regulators.Caused by Oxidation of Potentiometer Contact Surface.Surface Wiped Clear ML20082F0281995-03-0404 March 1995 Special Rept 2-95-1 Re Invalid DG Failures.Test Frequency for DGs Remains at Once,Per 31 Days,W/Requirements of TS Table 4.8-1 ML20149G1221994-09-23023 September 1994 Special Rept 1-94-2:on 940918,discovered That Seismic Monitor Inoperable for More than 30 Days.Seismic Switch Removed & Seismic Trigger Installed on 940918 & Seismic Monitor Returned to Svc ML20065J5871994-04-11011 April 1994 Special Rept 1-94-1:on 940202,pressurizer Pressure Transmitter Swung on Mounting Bolt & Touched Handle of Isolation Valve for Sensing Line,Causing Valve to Open Momentarily.Valve Was Closed & Unit Stabilized ML20059B8321993-10-25025 October 1993 Special Rept 2-93-3:on 931001,DG 2B Invalid Failure Occurred When DG Failed to Attain Rated Voltage & Frequency in Required Time & on 931002,DG 2A Invalid Failure Occurred When DG Tripped on Overspeed ML20057F5481993-10-11011 October 1993 Special Rept:On 930917,invalid Failure of DG 2A Occurred. Investigation of Leak Revealed Blown Gasket.Gasket Replaced & Engine Restarted ELV-03986, Special Rept:On 920819,discovered That Voltage Meter Did Not Respond Until 28 After Being Tapped Several Times. Caused by Erratic Meter Indications.Operators Advised of Proper Timing Method & Voltage Meter Replaced1992-08-28028 August 1992 Special Rept:On 920819,discovered That Voltage Meter Did Not Respond Until 28 After Being Tapped Several Times. Caused by Erratic Meter Indications.Operators Advised of Proper Timing Method & Voltage Meter Replaced ELV-03929, Special Rept 2-92-5:on 920709-12,temp in Room 122 of Equipment Bldg Exceeded Max Normal Temp of 115 F for More than 8 H.Periods of Plant Operation W/Higher than Normal Temps Had No Effect on Continued Operability of Equipment1992-07-31031 July 1992 Special Rept 2-92-5:on 920709-12,temp in Room 122 of Equipment Bldg Exceeded Max Normal Temp of 115 F for More than 8 H.Periods of Plant Operation W/Higher than Normal Temps Had No Effect on Continued Operability of Equipment ELV-03825, Rev 1 to Special Rept 2-92-1,reclassifying 920205 DG Failure from Valid to Nonvalid.Area Exists within Kvar Range in Which Voltage Regulator Will Not Function Due to Power Transformers.Operation of Generator in Range Limited1992-06-25025 June 1992 Rev 1 to Special Rept 2-92-1,reclassifying 920205 DG Failure from Valid to Nonvalid.Area Exists within Kvar Range in Which Voltage Regulator Will Not Function Due to Power Transformers.Operation of Generator in Range Limited ELV-03601, Rev 1 to Special Rept 2-91-1:on 910521,mechanical Governor Oil Level Appeared Low After Dropping to Bottom of Sight Glass Due to Small Span of Governor Oil Level Sight Glass. Change Made to DG Standby Status Mode Checklist1992-05-11011 May 1992 Rev 1 to Special Rept 2-91-1:on 910521,mechanical Governor Oil Level Appeared Low After Dropping to Bottom of Sight Glass Due to Small Span of Governor Oil Level Sight Glass. Change Made to DG Standby Status Mode Checklist ELV-03687, Special Rept:On 920331,K1 Relay to Latch in Closed Position & Short Generator Field.Caused by Spring Load Collar Not Fully Returning to Normal Position.Appropriate Procedures Will Be Changed by 920615 to Ensure Collar Is Checked1992-04-27027 April 1992 Special Rept:On 920331,K1 Relay to Latch in Closed Position & Short Generator Field.Caused by Spring Load Collar Not Fully Returning to Normal Position.Appropriate Procedures Will Be Changed by 920615 to Ensure Collar Is Checked ELV-03632, Special Rept 2-92-2:on 920317,dust & Debris Observed Settling in Vicinity of Generator End of Diesel.Caused by Large Piece of Fireproofing Insulation Falling Into Lead Termination Box.Power Termination Box Repaired1992-04-0909 April 1992 Special Rept 2-92-2:on 920317,dust & Debris Observed Settling in Vicinity of Generator End of Diesel.Caused by Large Piece of Fireproofing Insulation Falling Into Lead Termination Box.Power Termination Box Repaired ELV-03627, Special Rept:On 920320 & 21,invalid Failures of DG 2A Occurred Due to Inadequate Fuel in Supply Lines & Governor Speed Increased Too Slowly.On 920322,DG High Vibration Trip Occurred Due to Defective Sensor.Sensor Replaced1992-04-0909 April 1992 Special Rept:On 920320 & 21,invalid Failures of DG 2A Occurred Due to Inadequate Fuel in Supply Lines & Governor Speed Increased Too Slowly.On 920322,DG High Vibration Trip Occurred Due to Defective Sensor.Sensor Replaced ELV-03602, Special Rept:On 920219,revealed That Microchip Failed on Circuit Card Resulting in Channels in Upper Reactor Vessel Being Declared Inoperable.Installation Will Be Completed & Inoperable Channels Will Be Restored to Svc by 9204151992-03-26026 March 1992 Special Rept:On 920219,revealed That Microchip Failed on Circuit Card Resulting in Channels in Upper Reactor Vessel Being Declared Inoperable.Installation Will Be Completed & Inoperable Channels Will Be Restored to Svc by 920415 ELV-03478, Special Rept 2-92-1:on 920205,DG 2B Declared Inoperable Due to Negative Reactive Power.Cause Undetermined.Engine Being Tested Each Wk While Monitoring Equipment Connected to Capture Any Info Useful in Investigation of Cause1992-03-0202 March 1992 Special Rept 2-92-1:on 920205,DG 2B Declared Inoperable Due to Negative Reactive Power.Cause Undetermined.Engine Being Tested Each Wk While Monitoring Equipment Connected to Capture Any Info Useful in Investigation of Cause ELV-03217, TS Special Rept 1-91-6:on 911019 & 20,maint Start of Diesel Generator 1A Made for Functional Testing Purposes.Caused by Engine Speed Dropping Too Low & Low Turbocharger Lube Oil Pressure.Exhaust Gasket for Cylinder Head Replaced1991-11-12012 November 1991 TS Special Rept 1-91-6:on 911019 & 20,maint Start of Diesel Generator 1A Made for Functional Testing Purposes.Caused by Engine Speed Dropping Too Low & Low Turbocharger Lube Oil Pressure.Exhaust Gasket for Cylinder Head Replaced ELV-03200, Special Rept 1-91-5:on 911008,discovered That Amount of Grease Injected Into Vertical Tendon V10-102 Significantly Larger than Amount of Grease Removed from Tendon.Caused by Voids in Tendons.Tendon Retensioned1991-11-0707 November 1991 Special Rept 1-91-5:on 911008,discovered That Amount of Grease Injected Into Vertical Tendon V10-102 Significantly Larger than Amount of Grease Removed from Tendon.Caused by Voids in Tendons.Tendon Retensioned ELV-03184, Special Rept 1-91-4:on 911001,DG 1B Was Shut Down Due to Oil Leak from Supply Line to Rocker Arms.Caused by Connection Not Being Sufficiently Retightened.Tap Setting Change Made for Unit 1 a Rat.Wiring Discrepancy for 140 Relay Corrected1991-10-30030 October 1991 Special Rept 1-91-4:on 911001,DG 1B Was Shut Down Due to Oil Leak from Supply Line to Rocker Arms.Caused by Connection Not Being Sufficiently Retightened.Tap Setting Change Made for Unit 1 a Rat.Wiring Discrepancy for 140 Relay Corrected ELV-03155, Special Rept 50-425/1991-003:on 910912,vent Valve on Grease Can for Horizontal Tendon H-96 at Butress 2 Found Broken Off & Grease Leaked from 15 Locations on Exterior Surface. No Degradation Occurred in Tendons or Containment1991-10-0808 October 1991 Special Rept 50-425/1991-003:on 910912,vent Valve on Grease Can for Horizontal Tendon H-96 at Butress 2 Found Broken Off & Grease Leaked from 15 Locations on Exterior Surface. No Degradation Occurred in Tendons or Containment ELV-03109, Special Rept:On 910821,valid Diesel Generator Failure of DG 2B Occurred,Troubleshooting Revealed K-1 Exciter Shutdown Relay Was Latched in Shutdown Position W/Reset.Caused by Component Failure1991-09-20020 September 1991 Special Rept:On 910821,valid Diesel Generator Failure of DG 2B Occurred,Troubleshooting Revealed K-1 Exciter Shutdown Relay Was Latched in Shutdown Position W/Reset.Caused by Component Failure ELV-03009, Special Rept:On 910708,invalid Diesel Generator Failure Occurred During Maint Run to Verify Balance of Silicon Control Rectifier Firing Waveforms.Provisions Implemented to Require Review Determining Need for Isolation Transformers1991-07-31031 July 1991 Special Rept:On 910708,invalid Diesel Generator Failure Occurred During Maint Run to Verify Balance of Silicon Control Rectifier Firing Waveforms.Provisions Implemented to Require Review Determining Need for Isolation Transformers ELV-02901, Special Rept 1-91-2:on 910522,operator at Diesel Generator Panel Observed Fluctuation in Field Voltage.On 910524,when Diesel Generator Tied to Grid,Field Voltage & Amps Spiked. Caused by Failure of Voltage Regulator.Regulator Replaced1991-06-17017 June 1991 Special Rept 1-91-2:on 910522,operator at Diesel Generator Panel Observed Fluctuation in Field Voltage.On 910524,when Diesel Generator Tied to Grid,Field Voltage & Amps Spiked. Caused by Failure of Voltage Regulator.Regulator Replaced ELV-02900, Special Rept 2-91-1:on 910521,operator Noticed Mechanical Governor Oil Level Low When Level Dropped to Bottom of Sight Glass.Caused by Small Span of Governor Oil Level Sight Glass.Governor Drain Connection Tightened1991-06-17017 June 1991 Special Rept 2-91-1:on 910521,operator Noticed Mechanical Governor Oil Level Low When Level Dropped to Bottom of Sight Glass.Caused by Small Span of Governor Oil Level Sight Glass.Governor Drain Connection Tightened ELV-02753, Special Rept Re Listed Invalid Diesel Generator Failures. Causes & Corrective Actions Listed1991-06-0404 June 1991 Special Rept Re Listed Invalid Diesel Generator Failures. Causes & Corrective Actions Listed ELV-02255, Special Rept 1-90-7 Re Invalid Diesel Generator Failure on 901025.Caused by Operator Using Improper Timing Method to Time Event.Diesel Generator 1B Restarted Using Proper Timing Method & Required Frequency Range Reached within Time Limit1990-11-15015 November 1990 Special Rept 1-90-7 Re Invalid Diesel Generator Failure on 901025.Caused by Operator Using Improper Timing Method to Time Event.Diesel Generator 1B Restarted Using Proper Timing Method & Required Frequency Range Reached within Time Limit ELV-02215, Special Rept 2-90-04:on 901009,invalid Diesel Generator Failure Occurred1990-11-0808 November 1990 Special Rept 2-90-04:on 901009,invalid Diesel Generator Failure Occurred ELV-02165, Special Rept 2-90-03:on 900914,invalid Diesel Generator Failure Occurred Due to Crack in Fuel Line Tubing.New Tubing Installed & Bent Appropriately1990-10-15015 October 1990 Special Rept 2-90-03:on 900914,invalid Diesel Generator Failure Occurred Due to Crack in Fuel Line Tubing.New Tubing Installed & Bent Appropriately ELV-02112, RO 1-90-06:on 900829,valid Diesel Generator (DG) Failure Occurred.Investigation Begun & Troubleshooting DG Run Made1990-09-24024 September 1990 RO 1-90-06:on 900829,valid Diesel Generator (DG) Failure Occurred.Investigation Begun & Troubleshooting DG Run Made ELV-01995, Special Rept 1-90-05:on 900711,valid Diesel Generator Failures Occurred.Caused by Initial Mfg Process.Starting Air Valves on Each of Four Diesel Generators Tested & Polished to Provide Adequate Clearance Between Pistons & Caps1990-08-0707 August 1990 Special Rept 1-90-05:on 900711,valid Diesel Generator Failures Occurred.Caused by Initial Mfg Process.Starting Air Valves on Each of Four Diesel Generators Tested & Polished to Provide Adequate Clearance Between Pistons & Caps ELV-00929, Special Rept:On 890902,area Max Normal Temp Limit Exceeded for More than 8 H.Caused by Erroneous Reading Taken by Plant Equipment Operator.Temp Excursion Had No Adverse Effect on Qualified Life of safety-related Equipment in Room1989-10-0303 October 1989 Special Rept:On 890902,area Max Normal Temp Limit Exceeded for More than 8 H.Caused by Erroneous Reading Taken by Plant Equipment Operator.Temp Excursion Had No Adverse Effect on Qualified Life of safety-related Equipment in Room ELV-00909, Revised Special Rept Re Valid Diesel Generator Failure on 890719.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework on Module Completed & Circuit Returned to Svc1989-09-25025 September 1989 Revised Special Rept Re Valid Diesel Generator Failure on 890719.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework on Module Completed & Circuit Returned to Svc ELV-00790, Special Rept 1-89-02:on 890717,observed Valid Diesel Generator Failure.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework in Progress & Scheduled for Completion by 8908141989-08-14014 August 1989 Special Rept 1-89-02:on 890717,observed Valid Diesel Generator Failure.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework in Progress & Scheduled for Completion by 890814 ELV-00562, Special Rept 89-002:on 890318,while Performing Procedure Re Unit Heatup to Normal Operating Temp & Pressure,Handswitches Opened & Safety Injection Occurred.Approx 2,900 Gallons of Water Injected Into Rcs.Safety Injection Signal Reset1989-05-30030 May 1989 Special Rept 89-002:on 890318,while Performing Procedure Re Unit Heatup to Normal Operating Temp & Pressure,Handswitches Opened & Safety Injection Occurred.Approx 2,900 Gallons of Water Injected Into Rcs.Safety Injection Signal Reset ELV-00431, Special Rept 89-001 Re Positive Moderator Temp Coefficient Measured During Low Power Physics Testing.Calculations Performed to Determine Control Rod Withdrawal Limits & Duration of Effect Time1989-04-0606 April 1989 Special Rept 89-001 Re Positive Moderator Temp Coefficient Measured During Low Power Physics Testing.Calculations Performed to Determine Control Rod Withdrawal Limits & Duration of Effect Time ELV-00028, Special Rept 88-008:on 881026,diesel Generator Train B Did Not Reach Rated Voltage & Frquency within Required Time,Per Reg Guide 1.108,Section C.2.E.2.Caused by Lack of Fuel in Line Upon Diesel Start Due to Personnel Error1988-11-23023 November 1988 Special Rept 88-008:on 881026,diesel Generator Train B Did Not Reach Rated Voltage & Frquency within Required Time,Per Reg Guide 1.108,Section C.2.E.2.Caused by Lack of Fuel in Line Upon Diesel Start Due to Personnel Error ML20206E8231988-11-14014 November 1988 Special Rept:On 881013,during Troubleshooting of Diesel Generator Train A,Mvar Meter Was Reading Offscale High. Investigation Showed That Rewiring Led to Meter Malfunction. Wiring Corrected ML20206B5631988-11-0707 November 1988 Special Rept 88-007:on 881022,following Inservice Insp, Completed on 881022,one Tube in Steam Generator 1 Plugged ML20205G6721988-10-24024 October 1988 Special Rept 88-005:on 880923,high Lube Oil Temp Trip Occurred When Start 1-88-0076,diesel Generator Train B Being Run to Prove Operability Following Routine Maint.Diesel Restarted to Verify High Lube Oil Temp 1997-05-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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GM t;ta Power C:vnpany e 40 tmtmes.s Center Pcv4 Aay Pmt Once B.n t?)5 ti " arn Adama362U1
. !penN. ,e 205 t /7 7 ? ??
m C.K.McCoy ($C()[()l{}
L f()\yOf v4 N sk-l.N o se won rwei October 8, 1991 ve u" men"cn+m ELV-03155 ,
i 1148 Docket No. 50-425 U. S. Nuclear Regulatory Commission ATTN: Document Cont ol Desk Washington, D. C. 20555 Gentlemen:
V0GTLE ELECTRIC GENERATING PLANT SPECIAL REPORT CONTAINMENT TENDON SVRV_LILLANCE DEFICLLNCIES In accordance with the rcquirements of Vogtle Electric Generating Plant Technical Specification 3.6.1.6, action statement b, Georgia Power Company submits the enclosed Special Report concerning containment tendon surveillance deficiencies.
Sincerely, L
C. K. McCoy CKM/JAE/NJS/gmb
Enclosure:
Special Report 50-425/1991-003 xc: 9_torcia Power Company Mr. W. B. Shipman Mr. M. Sheibani NORMS U. S. Nuclear Reaulatory Commission Mr. S. D. Ebneter, Regional Administrator Mr. D. S. Hood, Licensing Project Manager, NRR Mr. B. R. Bonser, Senior Resident Inspector, Vogtle
,/ ~
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l
V0GTLE ELECTRIC GENERATING FLANT - UNIT 2 SPECIAL REPORT NO. 50-425/1991-003 A. RE0VIREMENT FOR REPORT This report is submitted pursuant to Technical Specification 3.6.1.6, action statement b. This action ctatement contains the following requirements:
"With the indicated abnormal degradation of the structural integrity other than ACTION a at a level below the acceptance criteria of Specification 4.6.1.6, restore the containment (s) to the required level of integrity or verify that containment integrity is maintained within 15 days; perform an engineering evaluation of the containment (s) and provide a Special P.eport to the Commission within 30 days in accordance with Specification 6.9.2 or be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />, lhe provisions of Specification 3.0.4 are not applicable."
During the performance of the combined Unit I fifth year / Unit 2 third year tendon surveillance, two deficiencies were discovered which necessitated entry into the above action requirements. The first deficiency involved the discovery of free water in the grease can of Unit 2 horizontal tendon H-96 due to a broken vent valve. The second deficiency involved the discovery of tendon grease leakage inside the auxiliary and fuel handling buildings on the exterior surface of the Unit 2 containment cylindrical shell. It was determined that these deficiencies do not meet the acceptince criteria of Specification 4.6.1.6.1.d, which, in part, require that the operability of the sheathing filler grease be assured by verifying the following:
- 1. There are no changes in the presence or physical appearance of the sheathing filler grease, including the presence of free water.
- 2. During general visual examination of the containment exterior surface, grease leakage that could affect containment integrity is not present.
B.
SUMMARY
OF CONTAINMENT VISUAL INSPECTION A visual examination was performed on all of the exposed surfaces of the containment cylindrical shell per the requirements of Technical Specification 4.6.1.6.1.d(4) and 4.6.1.6.3, including the portion which is enclosed within the auxiliary and fuel hanJ11ng buildings. During this inspection, the vent valve on horizontal tendon H-96 was found to be broken.
Also, shrinkage cracks with small quantities of grease leakage were found at 15 locations along the bottom of the containment cylindrical shell (just above the junction of the containment base slab and cylinder).
-C. QUAL.L5 0F THE DISCOVERED DEFICIENCIES
- 1. Water in the Crease Can for Horizontal Tendon H-96 l On September 12, 1991, the vent valve on the grease can for Unit 2 horizontal tendon H-96 at buttress no. 2 was found to be broken off, it l
l
was decided to replace the broken valve and to pump grease into the grease can through a valve in the trumpet area of the tendon to determine if any water had entered the grease can while the vent valve was broken / missing.
Da September 13, 1991, with the vent valve open, grease was pumped into the trumpet area cf tendon H-96 at buttress no. 2. Appioximately I cup of water discharged out of the grease can vent valve soon after the pumping operations commenced. This was followed by grease. No additional water was discharged after the grease started flowing from the grease can. Due to the presence of water, it was decided to remove the grease can and perform a complete visual inspection of the tendon end anchorage.
On September 16, 1991, the grease can was removed from tendon H-96 ct buttress no. 2, and a complete visual examination of the end anchorage was performed. Approximately 2 tablespoons of free water were found in the grease can, and the inspection revealed that a small area of the anchor head was of reddish brown color. However, there was no evidence of pitting or active oxidation, and this was determined to be an acceptable condition.
Following inspection of the tendon end anchorage, the grease inside the can was removed and replaced with new Visconorust 2090 P-4 material.
The tendon end anchorage was stripped of the existing grease and was hand coated with new grease. The grease can was reinstalled, and new Visconorust 2090 P-4 material was pumped into the tendon trumpet area and the grease can,
- 2. Grease Leakage Through Containment Cylindrical Shell Concrete Prior to performing any regressing for the Unit 2 tendon surveillance, a {
visual examination of the exterior surface of the containment cylindrical shell was performed. It was discovered that grease had leaked from 15 locations on the exterior surface. Four of these locations are in the_ fuel handling building encapsulation vessel rooms.
The remaining 11 are located in or adjacent to the encapsulation vessel rooms in the auxiliary building. All of the leaks occurred at vertical cracks in the concrete just above the junction of the containment base slab and cylindrical shell. The location of the leaks, concrete crack width, quantity of grease collected at each location, and other observations are shown in table 1.
A containment entry was not made to inspect the liner plate for the following reasons:
- a. Regreasing of tendons inspected for the Unit 2 tendon surveillance had not been started.
- b. None of the cracks are located near the tendons which were inspected and regreased during the Unit 2 first year surveillance in November l 1989.
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'l Therefore, there is no possibility of existing damage to the liner plate due to the grease pumping process. The concrete surfaces at all of the 15 grease leakage locations have been cleaned and will be monitored for further leakage.
D. [NGINEERING EVALUATION
- 1. Water in the Grease Can for Horizontal Tendon H-96 The procedure used by the Georgia Power Company (GPC) Construction Department for installing the tendons ensured a high degree of corrosion protection for the tendons. The tendons were hand corted with Visconorust 2090 P-4 material as they were pulled intc the sheathing.
Additionally, the tendons were hand coated at the fcctory with a
- temporary corrosion preventive material. During the greasing procedure, i vents were opened to allow the release of air bubbles. Hot grease was pumped until a clear-flow of grease was observed exiting the appropriate vent. Inspections were made to identify any grease leakage from the tendon duct. This process ensured that the tendons originally received a thorough coating of grease.
Visconorust 2090 P-4 material, which is manufactured by the Viscosity 011 Com.oany, provides an effective barrier to moisture and air which retards the effect of a corrosive atmosphere. The grease provides a protective film which is not easily penetrated by free water and which has a reserve alkalinity for long-term acid neutralization. The film l
aids in retarding corrosion introduced by water soluble ions from (
l chlorides, nitrates, and sulfides. Samples of grease were taken from i the grease can of horizontal tendon H-96 in which a cup of free water t was found during the surveillance, as well as from the grease which leaked out of the cracks in the exterior surface of the containment shell. These samples-are being tested to determine the reserve alkalinity of the grease. Test results are expected by the end of October 1991. If the test results are not satisfactory, a supplemental report will be submitted to the NRC.
Approximately I cup of water had infiltrated into the grease can of L horizontal tendon H-96 through a broken vent valve. However, visual l inspection determined that this small amount of water did not cause any damage to the tendon end anchorage components. A small area of the anchor head was found to be of reddish brown color. It appears that
' this anchor head was initially installed in this condition during construction since the anchor head surface displayed no evidence of active oxidation or pitting. The broken vent valve has now been replaced, and the end anchorage components have been recoated with new grease. In addition, the grease in the grease can has been replaced with new Visconorust 2090 P-4 material. These actions will ensure that horizontal tendon H-96 will perform its intended design function.
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A visual examination of. the grease cans for all other tendons.in the Unit 2 containmerit-has been performed, and no other broken vent valves have been found.: Therefore, it can be concluded that the end anchorages
'of all tendons in the. Unit 2 containment are not subjected to a corrosive environment. -
2,: Grease Leakage Through Containment Cylindrical Shell Concrete ,
t Based upon the location'of the leakage and the quantity of grease that has leaked into the fuel handling and auxiliary buildings as listed in table 1,-it is likely that this grease is leaking from the taped joints of the sheathing for several vertical tendons. The leakage has occurred through vertical cracks in the exterior surface of the containment shell located just above the base mat. This location is where the hydraulic -
head of the grease is at-its highest for vertical tendons'along the cylindrical shell. In addition, no horizontal tendons are located in
-this area of the containment shell which would be beneficial in sealing shrinkage _ cracks that normally occur in concrete structures. Since the j
-tendon sheathing is. not designed to be leak tight, the reduced flow l resistance caused by high summer temperatures has apparently allowed the grease, driven byL a high hydraulic head, to-leak from the taped joints into the' hairline cracks in the concrete adjacent to the tendons.
At the worst leakage location, the quantity of grease leakage to date is less than 1.0 percen: of the net duct volume of any vertical tendons in the area. - This is well within the acceptance limit of 5 percent of the net duct volume as specified by Technical Specification 4.6.1.6.1.d. At the other leakage locations, the quantity of grease leakage to date is .
insignificant in comparison to the net duct volume of any vertical i tendons in the area of those leaks. Therefore, no'immediate action is L -necessary. . All leakage locations will be monitored, and additional grease will be injected if the cumulative leakage at any location approaches the grease void acceptance limit of 5 percent of the net duct volume, n The width ~ of the crack at' the worst leakage location in the concrete
shell is 0.020 inch or less. At the other 14 leakage locations, the maximum width of the crack in the concrete is no more'than-0.010 inch.
All concrete structures, including prestressed concrete structures,- are subject to shrinkage cracking. -The crack widths found at the leakage L locations do not pose any threat to:the structural integrity of the concrete structure.- In addition; visual examination of the concrete surfaces did not-identify any spalling, scaling, D-cracking, or surface deterioration or disintegration. Therefore, the structural integrity of the Unit 2 containment has not been affected by the grease leakage L
-occurring'through these cracks.
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To prevent further grease leakage and any possible surface deterioration or disintegration, some repairs may be required to seal'the concrete' L cracks which are leaking grease. Details for sealing the cracks will be l- developed-if the data. collected from monitoring the grease; leakage at the 15 leakage-locations indicate that such repairs are warranted.
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E, [0NCLUS10N Based upon the inspections performed for corrosion, characteristics of the grease, the construction process used to initially fill the ducts, quantity of grease leakage, and width of the surface cracks, it can be concluded that the grease is providing adequate corrosion protection and no abnormal degradation has occurred in the tendons or the concrete containment. The structural integrity of the Unit 2 containment has not been affected by the discovered discrepancies.
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.+ a-TABLE 1 GREASE LEAKS IN THE EXTERIOR SURFACE OF UNIT 2 CONTAINMENT CYLINDRICAL SHELL ANGLE IN CRACK WIDTH QUANTITY Of GREASE PLAN FROM .
(INCHES) COLLECTED N0. BLDG ROOM NO. PLANT NORTH +
1 FUEL R-001 2460 0.010 To 0.020 4 GALLONS
- 2 FUEL R-C01 2480 0.010 NEGLIGIBLE **
3 FUEL R-C02 2310 0.005 TO 0.010 NEGLIGIBLE **
4 FUEL R-C02 2340 0.010 1 QUART 4+
5 AUX R-Cl29 1460 < 0.005 1 QUART 6 -AUX R-Cl29 1510 < 0.005 NEGLIGlBLE**
7 AUX R-Cl28 1550 0.005 TO 0.010 NEGLIGIBLE **
8 AUX R-Cl28 1650 0.005 TO 0.010 1 QUART 9 AUX R-Cl24 1690 < 0.010 NEGLIGIBLE **
10 AUX R-Cl24 1710 < 0.010 NEGLIGIBLE **
11 AuA R-Cl24 1750 < 0.010 NEGLIGlBLE** i 12 AUX R-Cl24 1760 < 0.010 NEGLIGIBLE **
13 AUX R-Cl24 1790 < 0.010 NEGLIGIBLE **
i l 14 AUX R-Cl24 1830 < 0.010 NEGLIGIBLE **
15 AUX R-Cl24 1860 < 0.010 NEGLIGIBLE **
2 GALLONS OF GREASE WERE COLLECTED DURING THE 1989 SURVEILLANCE AS REPORTED IN SPECIAL REPORT 50-424/1989-003 (ref.: GPC letter ELV-01105, dated i November 29, 1989). THE REMAINING 2 GALLONS LEAKED BETWEEN NOVEMBER OF 1989 I AND SEPTEMBER OF 1991.
- LEAKAJE AT THESE POINTS IS VERY SMALL. A TOTAL-0F 1 PINT OF GREASE WAS COLLECTED FROM POINTS 9 THROUGH 15.
+ ANGLE IS MEASURED ALONG CONTAINMENT SHELL CYLINDRICAL SURFACE IN A COUNTERCLOCKWISE DIRECTION.
++ THE 1 QUART COLLECTED WAS DURING THE 1989 SURVEILLANCE. ONLY NEGLIGIBLE LEAKAGE WAS OBSERVED DURING THE CURRENT SURVEILLANCE.