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Issue date | Title | Topic | |
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ML20199K833 | 21 November 1997 | Ro:On 960528,detected Abnormal Metallic Impact Sounds.Caused by Confirmed Loose Part in Sg.Removed SG 4 Hot Leg Manway & Found Loose Metal Object Inside,Performed Engineering Evaluation & Performed Insp of Guide Tube Support Pins | |
ML20148F090 | 29 May 1997 | Special Rept:On 970513,CR Personnel Began Receiving Intermittent Alarms from Digital Metal Impact Monitoring Sys Annunciator.Monitoring of Impact Continuing & Search for Object & Insp for Damage Will Be Performed at Next Outage | |
ML20128P215 | 10 October 1996 | Special Rept 2-96-2:on 960921,start Attempt of Maint Run of DG2A Was Made But Engine Did Not Start.Caused by Loose Voltage Regulator Integrated Circuit Boards.Loose Boards Were Removed,Contacts Adjusted & Returned to Sockets | |
ML20129F873 | 1 October 1996 | Special Rept 2-96-1:on 960908,DG 2A Started But Tripped. Investigation Found Six Main Bearing Temp Sensor Venting Pressure.Defective Main Bearing Sensor Replaced | |
ML20112H007 | 10 June 1996 | Ro:On 960528,detected Abnormal Metallic Impact Sounds. Caused by Confirmed Loose Part in Steam Generator. Engineering Evaluation Performed & Repairs & Modifications Scheduled for Next Refueling Outage | |
ML20101N049 | 2 April 1996 | Special Rept 1-96-2:on 960310 & 23,non-valid DG Failures Occurred.Rocker Arm Clearances Adjusted & DGs Restarted & Operated Successfully | |
ML20092B628 | 7 September 1995 | Special Rept:On 950816,non-valid DG Failure Occurred Due to Circuits Not Properly set.Post-maint Surveillance Testing Discovered Problem Prior to DG Return to Svc | |
ML20087D621 | 7 August 1995 | Special Rept:On 950720,total of 33 3/4 Gallons of Grease Had Been Lost from Tendon.Horizontal Tendon H120 Was Detensioned & Strand Was Removed for Visual Exam & Tensile Testing | |
ML20086S264 | 26 July 1995 | Special Rept:On 950628,generator Output Voltage Dropped Below Normal Rated Value.Caused by Malfunctioning Transformer T3.Voltage Regulator 2 Replaced,Tested & Returned to Svc on 950629 | |
ML20086L948 | 14 July 1995 | Special Rept:On 950517,operators Experienced Difficulties W/Excitation of Generator in Form of Voltage Swings When Utilizing Each of Two Voltage Regulators | |
ML20086B892 | 29 June 1995 | Special Rept 2-95-3:on 950607,three non-valid DG2A Failures Occurred Due to Malfunctioning Automatic Min Excitation Limiter.Malfunctioning Automatic Min Excitation Limiter Removed from Service | |
ML20086H131 | 16 June 1995 | Special Rept:On 950517,operators Experienced Difficulties W/Excitation of Generator in Form of Voltage Swings When Utilizing Each of Two Voltage Regulators | |
ML20084M717 | 2 June 1995 | Special Rept:On 950517,operators Experienced Difficulties W/Excitation of Generator in Form of Voltage Swings When Utilizing Each of Two Voltage Regulators.Caused by Oxidation of Potentiometer Contact Surface.Surface Wiped Clear | |
ML20082F028 | 4 March 1995 | Special Rept 2-95-1 Re Invalid DG Failures.Test Frequency for DGs Remains at Once,Per 31 Days,W/Requirements of TS Table 4.8-1 | |
ML20149G122 | 23 September 1994 | Special Rept 1-94-2:on 940918,discovered That Seismic Monitor Inoperable for More than 30 Days.Seismic Switch Removed & Seismic Trigger Installed on 940918 & Seismic Monitor Returned to Svc | |
ML20065J587 | 11 April 1994 | Special Rept 1-94-1:on 940202,pressurizer Pressure Transmitter Swung on Mounting Bolt & Touched Handle of Isolation Valve for Sensing Line,Causing Valve to Open Momentarily.Valve Was Closed & Unit Stabilized | |
ML20059B832 | 25 October 1993 | Special Rept 2-93-3:on 931001,DG 2B Invalid Failure Occurred When DG Failed to Attain Rated Voltage & Frequency in Required Time & on 931002,DG 2A Invalid Failure Occurred When DG Tripped on Overspeed | |
ML20057F548 | 11 October 1993 | Special Rept:On 930917,invalid Failure of DG 2A Occurred. Investigation of Leak Revealed Blown Gasket.Gasket Replaced & Engine Restarted | |
ELV-03986, Special Rept:On 920819,discovered That Voltage Meter Did Not Respond Until 28 After Being Tapped Several Times. Caused by Erratic Meter Indications.Operators Advised of Proper Timing Method & Voltage Meter Replaced | 28 August 1992 | Special Rept:On 920819,discovered That Voltage Meter Did Not Respond Until 28 After Being Tapped Several Times. Caused by Erratic Meter Indications.Operators Advised of Proper Timing Method & Voltage Meter Replaced | |
ELV-03929, Special Rept 2-92-5:on 920709-12,temp in Room 122 of Equipment Bldg Exceeded Max Normal Temp of 115 F for More than 8 H.Periods of Plant Operation W/Higher than Normal Temps Had No Effect on Continued Operability of Equipment | 31 July 1992 | Special Rept 2-92-5:on 920709-12,temp in Room 122 of Equipment Bldg Exceeded Max Normal Temp of 115 F for More than 8 H.Periods of Plant Operation W/Higher than Normal Temps Had No Effect on Continued Operability of Equipment | |
ELV-03825, Rev 1 to Special Rept 2-92-1,reclassifying 920205 DG Failure from Valid to Nonvalid.Area Exists within Kvar Range in Which Voltage Regulator Will Not Function Due to Power Transformers.Operation of Generator in Range Limited | 25 June 1992 | Rev 1 to Special Rept 2-92-1,reclassifying 920205 DG Failure from Valid to Nonvalid.Area Exists within Kvar Range in Which Voltage Regulator Will Not Function Due to Power Transformers.Operation of Generator in Range Limited | |
ELV-03601, Rev 1 to Special Rept 2-91-1:on 910521,mechanical Governor Oil Level Appeared Low After Dropping to Bottom of Sight Glass Due to Small Span of Governor Oil Level Sight Glass. Change Made to DG Standby Status Mode Checklist | 11 May 1992 | Rev 1 to Special Rept 2-91-1:on 910521,mechanical Governor Oil Level Appeared Low After Dropping to Bottom of Sight Glass Due to Small Span of Governor Oil Level Sight Glass. Change Made to DG Standby Status Mode Checklist | |
ELV-03687, Special Rept:On 920331,K1 Relay to Latch in Closed Position & Short Generator Field.Caused by Spring Load Collar Not Fully Returning to Normal Position.Appropriate Procedures Will Be Changed by 920615 to Ensure Collar Is Checked | 27 April 1992 | Special Rept:On 920331,K1 Relay to Latch in Closed Position & Short Generator Field.Caused by Spring Load Collar Not Fully Returning to Normal Position.Appropriate Procedures Will Be Changed by 920615 to Ensure Collar Is Checked | |
ELV-03632, Special Rept 2-92-2:on 920317,dust & Debris Observed Settling in Vicinity of Generator End of Diesel.Caused by Large Piece of Fireproofing Insulation Falling Into Lead Termination Box.Power Termination Box Repaired | 9 April 1992 | Special Rept 2-92-2:on 920317,dust & Debris Observed Settling in Vicinity of Generator End of Diesel.Caused by Large Piece of Fireproofing Insulation Falling Into Lead Termination Box.Power Termination Box Repaired | |
ELV-03627, Special Rept:On 920320 & 21,invalid Failures of DG 2A Occurred Due to Inadequate Fuel in Supply Lines & Governor Speed Increased Too Slowly.On 920322,DG High Vibration Trip Occurred Due to Defective Sensor.Sensor Replaced | 9 April 1992 | Special Rept:On 920320 & 21,invalid Failures of DG 2A Occurred Due to Inadequate Fuel in Supply Lines & Governor Speed Increased Too Slowly.On 920322,DG High Vibration Trip Occurred Due to Defective Sensor.Sensor Replaced | |
ELV-03602, Special Rept:On 920219,revealed That Microchip Failed on Circuit Card Resulting in Channels in Upper Reactor Vessel Being Declared Inoperable.Installation Will Be Completed & Inoperable Channels Will Be Restored to Svc by 920415 | 26 March 1992 | Special Rept:On 920219,revealed That Microchip Failed on Circuit Card Resulting in Channels in Upper Reactor Vessel Being Declared Inoperable.Installation Will Be Completed & Inoperable Channels Will Be Restored to Svc by 920415 | |
ELV-03478, Special Rept 2-92-1:on 920205,DG 2B Declared Inoperable Due to Negative Reactive Power.Cause Undetermined.Engine Being Tested Each Wk While Monitoring Equipment Connected to Capture Any Info Useful in Investigation of Cause | 2 March 1992 | Special Rept 2-92-1:on 920205,DG 2B Declared Inoperable Due to Negative Reactive Power.Cause Undetermined.Engine Being Tested Each Wk While Monitoring Equipment Connected to Capture Any Info Useful in Investigation of Cause | |
ELV-03217, TS Special Rept 1-91-6:on 911019 & 20,maint Start of Diesel Generator 1A Made for Functional Testing Purposes.Caused by Engine Speed Dropping Too Low & Low Turbocharger Lube Oil Pressure.Exhaust Gasket for Cylinder Head Replaced | 12 November 1991 | TS Special Rept 1-91-6:on 911019 & 20,maint Start of Diesel Generator 1A Made for Functional Testing Purposes.Caused by Engine Speed Dropping Too Low & Low Turbocharger Lube Oil Pressure.Exhaust Gasket for Cylinder Head Replaced | |
ELV-03200, Special Rept 1-91-5:on 911008,discovered That Amount of Grease Injected Into Vertical Tendon V10-102 Significantly Larger than Amount of Grease Removed from Tendon.Caused by Voids in Tendons.Tendon Retensioned | 7 November 1991 | Special Rept 1-91-5:on 911008,discovered That Amount of Grease Injected Into Vertical Tendon V10-102 Significantly Larger than Amount of Grease Removed from Tendon.Caused by Voids in Tendons.Tendon Retensioned | |
ELV-03184, Special Rept 1-91-4:on 911001,DG 1B Was Shut Down Due to Oil Leak from Supply Line to Rocker Arms.Caused by Connection Not Being Sufficiently Retightened.Tap Setting Change Made for Unit 1 a Rat.Wiring Discrepancy for 140 Relay Corrected | 30 October 1991 | Special Rept 1-91-4:on 911001,DG 1B Was Shut Down Due to Oil Leak from Supply Line to Rocker Arms.Caused by Connection Not Being Sufficiently Retightened.Tap Setting Change Made for Unit 1 a Rat.Wiring Discrepancy for 140 Relay Corrected | |
ELV-03155, Special Rept 50-425/1991-003:on 910912,vent Valve on Grease Can for Horizontal Tendon H-96 at Butress 2 Found Broken Off & Grease Leaked from 15 Locations on Exterior Surface. No Degradation Occurred in Tendons or Containment | 8 October 1991 | Special Rept 50-425/1991-003:on 910912,vent Valve on Grease Can for Horizontal Tendon H-96 at Butress 2 Found Broken Off & Grease Leaked from 15 Locations on Exterior Surface. No Degradation Occurred in Tendons or Containment | |
ELV-03109, Special Rept:On 910821,valid Diesel Generator Failure of DG 2B Occurred,Troubleshooting Revealed K-1 Exciter Shutdown Relay Was Latched in Shutdown Position W/Reset.Caused by Component Failure | 20 September 1991 | Special Rept:On 910821,valid Diesel Generator Failure of DG 2B Occurred,Troubleshooting Revealed K-1 Exciter Shutdown Relay Was Latched in Shutdown Position W/Reset.Caused by Component Failure | |
ELV-03009, Special Rept:On 910708,invalid Diesel Generator Failure Occurred During Maint Run to Verify Balance of Silicon Control Rectifier Firing Waveforms.Provisions Implemented to Require Review Determining Need for Isolation Transformers | 31 July 1991 | Special Rept:On 910708,invalid Diesel Generator Failure Occurred During Maint Run to Verify Balance of Silicon Control Rectifier Firing Waveforms.Provisions Implemented to Require Review Determining Need for Isolation Transformers | |
ELV-02901, Special Rept 1-91-2:on 910522,operator at Diesel Generator Panel Observed Fluctuation in Field Voltage.On 910524,when Diesel Generator Tied to Grid,Field Voltage & Amps Spiked. Caused by Failure of Voltage Regulator.Regulator Replaced | 17 June 1991 | Special Rept 1-91-2:on 910522,operator at Diesel Generator Panel Observed Fluctuation in Field Voltage.On 910524,when Diesel Generator Tied to Grid,Field Voltage & Amps Spiked. Caused by Failure of Voltage Regulator.Regulator Replaced | Temporary Modification |
ELV-02900, Special Rept 2-91-1:on 910521,operator Noticed Mechanical Governor Oil Level Low When Level Dropped to Bottom of Sight Glass.Caused by Small Span of Governor Oil Level Sight Glass.Governor Drain Connection Tightened | 17 June 1991 | Special Rept 2-91-1:on 910521,operator Noticed Mechanical Governor Oil Level Low When Level Dropped to Bottom of Sight Glass.Caused by Small Span of Governor Oil Level Sight Glass.Governor Drain Connection Tightened | |
ELV-02753, Special Rept Re Listed Invalid Diesel Generator Failures. Causes & Corrective Actions Listed | 4 June 1991 | Special Rept Re Listed Invalid Diesel Generator Failures. Causes & Corrective Actions Listed | |
ELV-02255, Special Rept 1-90-7 Re Invalid Diesel Generator Failure on 901025.Caused by Operator Using Improper Timing Method to Time Event.Diesel Generator 1B Restarted Using Proper Timing Method & Required Frequency Range Reached within Time Limit | 15 November 1990 | Special Rept 1-90-7 Re Invalid Diesel Generator Failure on 901025.Caused by Operator Using Improper Timing Method to Time Event.Diesel Generator 1B Restarted Using Proper Timing Method & Required Frequency Range Reached within Time Limit | |
ELV-02215, Special Rept 2-90-04:on 901009,invalid Diesel Generator Failure Occurred | 8 November 1990 | Special Rept 2-90-04:on 901009,invalid Diesel Generator Failure Occurred | |
ELV-02165, Special Rept 2-90-03:on 900914,invalid Diesel Generator Failure Occurred Due to Crack in Fuel Line Tubing.New Tubing Installed & Bent Appropriately | 15 October 1990 | Special Rept 2-90-03:on 900914,invalid Diesel Generator Failure Occurred Due to Crack in Fuel Line Tubing.New Tubing Installed & Bent Appropriately | |
ELV-02112, RO 1-90-06:on 900829,valid Diesel Generator (DG) Failure Occurred.Investigation Begun & Troubleshooting DG Run Made | 24 September 1990 | RO 1-90-06:on 900829,valid Diesel Generator (DG) Failure Occurred.Investigation Begun & Troubleshooting DG Run Made | |
ELV-01995, Special Rept 1-90-05:on 900711,valid Diesel Generator Failures Occurred.Caused by Initial Mfg Process.Starting Air Valves on Each of Four Diesel Generators Tested & Polished to Provide Adequate Clearance Between Pistons & Caps | 7 August 1990 | Special Rept 1-90-05:on 900711,valid Diesel Generator Failures Occurred.Caused by Initial Mfg Process.Starting Air Valves on Each of Four Diesel Generators Tested & Polished to Provide Adequate Clearance Between Pistons & Caps | |
ELV-00929, Special Rept:On 890902,area Max Normal Temp Limit Exceeded for More than 8 H.Caused by Erroneous Reading Taken by Plant Equipment Operator.Temp Excursion Had No Adverse Effect on Qualified Life of safety-related Equipment in Room | 3 October 1989 | Special Rept:On 890902,area Max Normal Temp Limit Exceeded for More than 8 H.Caused by Erroneous Reading Taken by Plant Equipment Operator.Temp Excursion Had No Adverse Effect on Qualified Life of safety-related Equipment in Room | |
ELV-00909, Revised Special Rept Re Valid Diesel Generator Failure on 890719.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework on Module Completed & Circuit Returned to Svc | 25 September 1989 | Revised Special Rept Re Valid Diesel Generator Failure on 890719.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework on Module Completed & Circuit Returned to Svc | |
ELV-00790, Special Rept 1-89-02:on 890717,observed Valid Diesel Generator Failure.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework in Progress & Scheduled for Completion by 890814 | 14 August 1989 | Special Rept 1-89-02:on 890717,observed Valid Diesel Generator Failure.Caused by Remote Gate Firing Module on Bridge Circuit 1.Rework in Progress & Scheduled for Completion by 890814 | |
ELV-00562, Special Rept 89-002:on 890318,while Performing Procedure Re Unit Heatup to Normal Operating Temp & Pressure,Handswitches Opened & Safety Injection Occurred.Approx 2,900 Gallons of Water Injected Into Rcs.Safety Injection Signal Reset | 30 May 1989 | Special Rept 89-002:on 890318,while Performing Procedure Re Unit Heatup to Normal Operating Temp & Pressure,Handswitches Opened & Safety Injection Occurred.Approx 2,900 Gallons of Water Injected Into Rcs.Safety Injection Signal Reset | |
ELV-00431, Special Rept 89-001 Re Positive Moderator Temp Coefficient Measured During Low Power Physics Testing.Calculations Performed to Determine Control Rod Withdrawal Limits & Duration of Effect Time | 6 April 1989 | Special Rept 89-001 Re Positive Moderator Temp Coefficient Measured During Low Power Physics Testing.Calculations Performed to Determine Control Rod Withdrawal Limits & Duration of Effect Time | |
ELV-00028, Special Rept 88-008:on 881026,diesel Generator Train B Did Not Reach Rated Voltage & Frquency within Required Time,Per Reg Guide 1.108,Section C.2.E.2.Caused by Lack of Fuel in Line Upon Diesel Start Due to Personnel Error | 23 November 1988 | Special Rept 88-008:on 881026,diesel Generator Train B Did Not Reach Rated Voltage & Frquency within Required Time,Per Reg Guide 1.108,Section C.2.E.2.Caused by Lack of Fuel in Line Upon Diesel Start Due to Personnel Error | |
ML20206E823 | 14 November 1988 | Special Rept:On 881013,during Troubleshooting of Diesel Generator Train A,Mvar Meter Was Reading Offscale High. Investigation Showed That Rewiring Led to Meter Malfunction. Wiring Corrected | |
ML20206B563 | 7 November 1988 | Special Rept 88-007:on 881022,following Inservice Insp, Completed on 881022,one Tube in Steam Generator 1 Plugged | |
ML20205G672 | 24 October 1988 | Special Rept 88-005:on 880923,high Lube Oil Temp Trip Occurred When Start 1-88-0076,diesel Generator Train B Being Run to Prove Operability Following Routine Maint.Diesel Restarted to Verify High Lube Oil Temp |