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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217N8911999-10-15015 October 1999 Forwards Rept of Changes,Tests & Experiments at Pilgrim Nuclear Power Station for Period of 970422-990621,IAW 10CFR50.59(b).List of Changes Effecting Fsar,Encl ML20217D3951999-10-13013 October 1999 Forwards Request for Addl Info Re Util 990806 Submittal on USI A-46, Implementation Methodology Used at Pilgrim Nuclear Power Station, Per GL 87-02 ML20217E1581999-10-0808 October 1999 Forwards Insp Rept 50-293/99-05 on 990726-0905.Three Violations Noted & Being Treated as Ncvs.Violations Include Failure to Assure That Design Bases Correctly Translated Into Specifications ML20217C3151999-10-0606 October 1999 Forwards Scenario Package for Pilgrim Nuclear Power Station Nrc/Fema Evaluated Exercise Scheduled for 991207.Without Encl ML20217D5591999-10-0505 October 1999 Documents Pilgrim Nuclear Power Station Five Yr Survey of Main Breakwater.Survey Has Determined That Pilgrim Main Breakwater Is Intact & Remains Adequately Constructed to Perform Designed Safety Function ML20217C8051999-10-0505 October 1999 Forwards Proprietary Results of Audiologic Evaluations for Jp Giar,License SOP-10061-3.Attachment Clearly Shows Requirements for Operator Hearing Ability Are Met. Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML20212J8301999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Pilgrim Nuclear Power Station.Staff Conducts Reviews for All Operating NPPs to Integrate Performance Info & to Plan Insp Activities at Facility Over Next Six Months ML20216J9961999-09-29029 September 1999 Forwards Resume of Person Identified as Acting RPM in Licensee to NRC Re Notification That Person Named in License Condition 11 of 20-07626-02,is No Longer Employed at Pilgrim Station.Resume Withheld,Per 10CFR2.790 ML20212F7871999-09-24024 September 1999 Advises That Util 990121 Application for Amend Being Treated as Withdrawn.Proposed Changes Would Have Modified Facility UFSAR Pertaining to Values for post-accident Containment Pressure Credited in Pilgrim Net Positive Head Analyses ML20212H1381999-09-23023 September 1999 Submits Info in Support of Request Filed on 990730 to Grant one-time Exemption from 10CFR50,App E,Authorizing Biennial Full Participation Emergency Preparedness Exercise to Be Conducted in 2002 Instead of 2001 ML20212H1441999-09-23023 September 1999 Withdraws 990121 Request for License Change Re Emergency Core Cooling Sys Net Positive Suction Head,Due to Incorrect Datum Preparation ML20216F3451999-09-16016 September 1999 Forwards Summary Rept Providing Results of ISI Conducted at PNPS on-line & Refueling Outage (RFO 12) ML20212C2861999-09-16016 September 1999 Forwards SER Accepting Licensee 981123 Request for Relief RR-E1,RR-E5,RR-E6 Pursuant to 10CFR50.55a(a)(3)(i) & Request for Relief RR-E2,RR-E3 & RR-E4 Pursuant to 10CFR50.55a(a)(3)(ii) ML20216E7111999-09-0909 September 1999 Forwards License Renewal Application Including Form NRC-398 & Form NRC-396 for Jp Giar,License SOP-10061-3.Without Encls ML20216E5891999-09-0707 September 1999 Forwards Copy of Pilgrim Station Organization Structure. Encl Refelcts Changes in Upper Mgt Level Structure.Changes Were Effective 990901 ML20211M4501999-09-0303 September 1999 Informs That Pilgrim Nuclear Power Station Plans to Conduct Full Participation Emergency Preparedness Exercise with Commonwealth of Ma on 991207,IAW 10CFR50,App E,Section IV.F.2 ML20211M9161999-08-31031 August 1999 Submits Review & Correction of Info in Reactor Vessel Integrity Database (Rvid),Version 2,re Pilgrim Station ML20211J8391999-08-30030 August 1999 Forwards Rev 1 to Provisional Decommissioning Trust Agreement for Plant,Changing Portions of Agreement to Permit Up to Two Distributions & Clarify Formula for Distribution ML20211H5701999-08-27027 August 1999 Forwards Insp Rept 50-293/99-04 on 990610-0725.Two Violations Identified Being Treated as non-cited Violations ML20211C3381999-08-19019 August 1999 Provides semi-annual LTP Update,Including Schedule, Commitment Descriptions,Progress Since Last Update & Summary of Changes.Rev Bars Indicate Changes in Status Since Last Submittal ML20210U5761999-08-18018 August 1999 Responds to Opposing Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts. Informs That for Sale,Nrc Responsible for Only Ensuring That Entergy Technically & Financially Qualified to Operate NPP ML20210U6691999-08-18018 August 1999 Forwards from Massachusetts State Senator T Murray Opposing Merger Between Bec Energy & Commonwealth Energy Systems ML20210U7521999-08-18018 August 1999 Forwards from Massachusetts State Senator T Murray Opossing Merger Between Bec Energy & Commonwealth Energy Systems ML20210U5151999-08-17017 August 1999 Forwards Notice of Withdrawal of Application for Approval of Indirect Transfer of FOL for Pilgrim in Response to .Approval No Longer Needed Since Beco Sold Interest in Pilgrim to EOI on 990713 ML20211B3841999-08-16016 August 1999 Forwards Response to NRC Second RAI Re Pressure Locking & Thermal Binding of SR power-operated Gate Valves ML20210U4831999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data Sheets for Period of 990101-0630,per 10CFR26.71(d) ML20210S0891999-08-0909 August 1999 Forwards Amend 11 to Indemnity Agreement B-48 Signed by Boston Edison Co & Entergy Nuclear Generation Co ML20210R6251999-08-0606 August 1999 Provides Supplementary Info on USI A-46 Implementation Methodology at Pilgrim Station,To Enable NRC to Perform Evaluation & Issuance of Plant Specific SER for Plant ML20210M9411999-08-0202 August 1999 Requests That NRC Treat Pending Actions Requested by Beco Prior to 990713,as Requests Made by Entergy.Ltr Requests That Minor Administrative Changes to License Amend 182 & Associated Ser, ,reflect 990713 Transfer ML20210H8761999-07-30030 July 1999 Requests That NRC Grant Exemption from Requirements of 10CFR50,App E,Section IV F,Which Would Authorize Rescheduling of 2001 Biennial Full Participation Emergency Preparedness Exercise for Pilgrim Station to 2002 ML20210H8661999-07-29029 July 1999 Provides Revised Response to GL 96-06 & Addresses NRC Insp Concern for Containment Penetration X-12.Info Submitted to Facilitate NRC Review & Closeout of Subject GL for Plant ML20216E2321999-07-26026 July 1999 Discusses GL 92-01,rev 1,suppl 1, Rv Structural Integrity. NRC Revised Info in Rvid & Releasing as Rvid Version 2 ML20216D4131999-07-22022 July 1999 Informs That J Conlon,License OP-11040-1,terminated Employment with Beco on 990703,per 10CFR50.74.Individual Will Not Participate in Util Licensed Operator Requalification Training Program ML20210E2231999-07-20020 July 1999 Discusses Arrangements Made by Dennis & M Santiago During 990615 Telephone Conversation for NRC to Inspect Licensed Operator Requalification Program at Pilgrim During Wk of 991004 ML20210C4151999-07-19019 July 1999 Informs That Util Intends to Submit Approx Eight Licensing Actions in FY00 & Eight in FY01,in Response to Administrative Ltr 99-02.Actions Are Not Expected to Generate Complex Reviews ML20210F3711999-07-14014 July 1999 Informs NRC That Effective 990713,listed Pilgrim Station Security Plans Have Been Transferred from Boston Edison to Entergy & Are Still in Effect ML20210A9441999-07-14014 July 1999 Responds to Re Changes to Pilgrim Nuclear Power Station Physical Security Plan Identified as Issue 2,rev 14, Addendum 1,respectively.No NRC Approval Is Required IAW 10CFR54(p) ML20209G2251999-07-0909 July 1999 Forwards Insp Rept 50-293/99-03 on 990419-0609.Five Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations,Consistent with App C. Several Individual Tagging Errors Occurred ML20209C4661999-07-0707 July 1999 Forwards SE Accepting Addendum on Proposed Change in Corporate Ownership Structure Involving Entergy Nuclear Generation Co ML20209C7761999-07-0606 July 1999 Submits Annual Summary Rept of Changes Made to QAP Description as Described in QA Manual,Vol Ii.Rept Covers Period of Jul 1998 Through June 1999.No Changes Made During Period ML20209C3851999-07-0606 July 1999 Forwards Redacted Draft of Decommissioning Trust Agreement Re Transfer of PNPS & NRC Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generating Co ML20196J7251999-07-0101 July 1999 Informs of Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, for Pilgrim Nuclear Power Station ML20209B9411999-06-30030 June 1999 Discusses Deferral of IGSCC Welds to RFO 13.Deferral of Welds to Refueling Outage 13 Does Not Impact Acceptable Level of Quality & Safety Per 10CFR50.55(a)(3)(i) Since Plant in Compliance W/Exam Percentage Requirements ML20209B9431999-06-30030 June 1999 Provides Formal Notification That Closing Date for Sale & Transfer of Pilgrim Station Scheduled to Occur on 990713. a Wang Will Be Verbally Notified of Time of Sale Closing ML20209B9791999-06-29029 June 1999 Forwards Rev 13A to Pilgrims COLR for Cycle 13,IAW TS 5.6.5 Requirements.Rev 13A Provides cycle-specific Limits for Operating Pilgrim During Remainder of Cycle 13 ML20196H2381999-06-29029 June 1999 Forwards SER Denying Licensee 980820 Request for Alternative Under PRR-13,rev 2 for Use of Code Case N-522 During Pressure Testing of Containment Penetration Piping ML20209A8761999-06-28028 June 1999 Forwards SER Authorizing Licensee 990317 Relief Request to Use ASME Code Case N-573 as Alternative to ASME Code Section XI Article IWA-4000 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209A8701999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant,Reporting Status of Facility Y2K Readiness Encl ML20210U5901999-06-25025 June 1999 Opposes Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts.Expresses Skepticism Re Claim by Companies That Consumers Will Benefit from Proposed Consolidation & four-year Freeze in Base Rates ML20209C3431999-06-22022 June 1999 Forwards Addendum 1,Rev 14 to Pilgrim Station Security Plan,Iaw 10CFR50.54(p)(2).Changes Proposed Have Been Implemented & Constitute Increase in Plant Defense Plan Commitments.Encl Withheld,Per 10CFR73.21 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N8911999-10-15015 October 1999 Forwards Rept of Changes,Tests & Experiments at Pilgrim Nuclear Power Station for Period of 970422-990621,IAW 10CFR50.59(b).List of Changes Effecting Fsar,Encl ML20217C3151999-10-0606 October 1999 Forwards Scenario Package for Pilgrim Nuclear Power Station Nrc/Fema Evaluated Exercise Scheduled for 991207.Without Encl ML20217C8051999-10-0505 October 1999 Forwards Proprietary Results of Audiologic Evaluations for Jp Giar,License SOP-10061-3.Attachment Clearly Shows Requirements for Operator Hearing Ability Are Met. Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML20217D5591999-10-0505 October 1999 Documents Pilgrim Nuclear Power Station Five Yr Survey of Main Breakwater.Survey Has Determined That Pilgrim Main Breakwater Is Intact & Remains Adequately Constructed to Perform Designed Safety Function ML20216J9961999-09-29029 September 1999 Forwards Resume of Person Identified as Acting RPM in Licensee to NRC Re Notification That Person Named in License Condition 11 of 20-07626-02,is No Longer Employed at Pilgrim Station.Resume Withheld,Per 10CFR2.790 ML20212H1441999-09-23023 September 1999 Withdraws 990121 Request for License Change Re Emergency Core Cooling Sys Net Positive Suction Head,Due to Incorrect Datum Preparation ML20212H1381999-09-23023 September 1999 Submits Info in Support of Request Filed on 990730 to Grant one-time Exemption from 10CFR50,App E,Authorizing Biennial Full Participation Emergency Preparedness Exercise to Be Conducted in 2002 Instead of 2001 ML20216F3451999-09-16016 September 1999 Forwards Summary Rept Providing Results of ISI Conducted at PNPS on-line & Refueling Outage (RFO 12) ML20216E7111999-09-0909 September 1999 Forwards License Renewal Application Including Form NRC-398 & Form NRC-396 for Jp Giar,License SOP-10061-3.Without Encls ML20216E5891999-09-0707 September 1999 Forwards Copy of Pilgrim Station Organization Structure. Encl Refelcts Changes in Upper Mgt Level Structure.Changes Were Effective 990901 ML20211M4501999-09-0303 September 1999 Informs That Pilgrim Nuclear Power Station Plans to Conduct Full Participation Emergency Preparedness Exercise with Commonwealth of Ma on 991207,IAW 10CFR50,App E,Section IV.F.2 ML20211M9161999-08-31031 August 1999 Submits Review & Correction of Info in Reactor Vessel Integrity Database (Rvid),Version 2,re Pilgrim Station ML20211J8391999-08-30030 August 1999 Forwards Rev 1 to Provisional Decommissioning Trust Agreement for Plant,Changing Portions of Agreement to Permit Up to Two Distributions & Clarify Formula for Distribution ML20211C3381999-08-19019 August 1999 Provides semi-annual LTP Update,Including Schedule, Commitment Descriptions,Progress Since Last Update & Summary of Changes.Rev Bars Indicate Changes in Status Since Last Submittal ML20211B3841999-08-16016 August 1999 Forwards Response to NRC Second RAI Re Pressure Locking & Thermal Binding of SR power-operated Gate Valves ML20210U4831999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data Sheets for Period of 990101-0630,per 10CFR26.71(d) ML20210S0891999-08-0909 August 1999 Forwards Amend 11 to Indemnity Agreement B-48 Signed by Boston Edison Co & Entergy Nuclear Generation Co ML20210R6251999-08-0606 August 1999 Provides Supplementary Info on USI A-46 Implementation Methodology at Pilgrim Station,To Enable NRC to Perform Evaluation & Issuance of Plant Specific SER for Plant ML20210M9411999-08-0202 August 1999 Requests That NRC Treat Pending Actions Requested by Beco Prior to 990713,as Requests Made by Entergy.Ltr Requests That Minor Administrative Changes to License Amend 182 & Associated Ser, ,reflect 990713 Transfer ML20210H8761999-07-30030 July 1999 Requests That NRC Grant Exemption from Requirements of 10CFR50,App E,Section IV F,Which Would Authorize Rescheduling of 2001 Biennial Full Participation Emergency Preparedness Exercise for Pilgrim Station to 2002 ML20210H8661999-07-29029 July 1999 Provides Revised Response to GL 96-06 & Addresses NRC Insp Concern for Containment Penetration X-12.Info Submitted to Facilitate NRC Review & Closeout of Subject GL for Plant ML20216D4131999-07-22022 July 1999 Informs That J Conlon,License OP-11040-1,terminated Employment with Beco on 990703,per 10CFR50.74.Individual Will Not Participate in Util Licensed Operator Requalification Training Program ML20210C4151999-07-19019 July 1999 Informs That Util Intends to Submit Approx Eight Licensing Actions in FY00 & Eight in FY01,in Response to Administrative Ltr 99-02.Actions Are Not Expected to Generate Complex Reviews ML20210F3711999-07-14014 July 1999 Informs NRC That Effective 990713,listed Pilgrim Station Security Plans Have Been Transferred from Boston Edison to Entergy & Are Still in Effect ML20209C3851999-07-0606 July 1999 Forwards Redacted Draft of Decommissioning Trust Agreement Re Transfer of PNPS & NRC Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generating Co ML20209C7761999-07-0606 July 1999 Submits Annual Summary Rept of Changes Made to QAP Description as Described in QA Manual,Vol Ii.Rept Covers Period of Jul 1998 Through June 1999.No Changes Made During Period ML20209B9411999-06-30030 June 1999 Discusses Deferral of IGSCC Welds to RFO 13.Deferral of Welds to Refueling Outage 13 Does Not Impact Acceptable Level of Quality & Safety Per 10CFR50.55(a)(3)(i) Since Plant in Compliance W/Exam Percentage Requirements ML20209B9431999-06-30030 June 1999 Provides Formal Notification That Closing Date for Sale & Transfer of Pilgrim Station Scheduled to Occur on 990713. a Wang Will Be Verbally Notified of Time of Sale Closing ML20209B9791999-06-29029 June 1999 Forwards Rev 13A to Pilgrims COLR for Cycle 13,IAW TS 5.6.5 Requirements.Rev 13A Provides cycle-specific Limits for Operating Pilgrim During Remainder of Cycle 13 ML20209A8701999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant,Reporting Status of Facility Y2K Readiness Encl ML20210U5901999-06-25025 June 1999 Opposes Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts.Expresses Skepticism Re Claim by Companies That Consumers Will Benefit from Proposed Consolidation & four-year Freeze in Base Rates ML20209C3431999-06-22022 June 1999 Forwards Addendum 1,Rev 14 to Pilgrim Station Security Plan,Iaw 10CFR50.54(p)(2).Changes Proposed Have Been Implemented & Constitute Increase in Plant Defense Plan Commitments.Encl Withheld,Per 10CFR73.21 ML20195G3721999-06-0707 June 1999 Informs That Proposed Indicators Failed QA Assessments for Digital Verification,Validation & Control of Software. Proposed Mod Can Be Completed on-line ML20195B5021999-05-27027 May 1999 Provides Suppl Info to 990203 Request of Beco That NRC Consent to Indirect Transfer of Control of Util Interest in License DPR-35.Request Described Proposed Merger of Bec Energy with Commonwealth Energy Sys ML20207D4681999-05-24024 May 1999 Provides Addl Info to That Included in Beco Ltr 98-123 Dtd 981001,addressing NRC Concerns Described in GL 96-06, Concerning Waterhammer in Reactor Bldg Closed Cooling Water Sys ML20195B9051999-05-20020 May 1999 Forwards Completed Renewal Applications for Listed Operators.Without Encls ML20206J4901999-05-0606 May 1999 Forwards Completed License Renewal Application,Including Forms NRC-398 & 396 for Sc Power,License OP-6328-3 ML20206P0711999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Exam by Facility Licensee, for K Walz,License SOP-10886-1.Encl Withheld IAW 10CFR2.790(a)(6) ML20206D3621999-04-27027 April 1999 Informs NRC That Final Five Sys self-assessments Required to Fulfill Commitment Made in 980828 Response to Insp Rept 50-293/98-04 Were Completed on 990422.Completion Was Delayed by High Priority Refueling Outage 12 Preparatory Work ML20205R9871999-04-21021 April 1999 Forwards Affidavit of JW Yelverton of Entergy Nuclear Generation Co Supporting Request for Withholding Info from Rept on Audit of Financial Statements for Year Ended 971231. Pages 16 & 18 of Subj Rept Also Encl ML20207B0891999-04-20020 April 1999 Forwards e-mail Message from Constituent,J Riell Re Y2K Compliance of Nuclear Power Plant in Plymouth,Massachusetts. Copy of Article Entitled Nuke Plants May Not Be Y2K Ready Also Encl ML20206A2741999-04-16016 April 1999 Dockets Encl Ltr Which Was Sent to AL Vietti-Cook Re Condition of Approval of Transfer of License & License Condition for DPR-35.Encl Resolves Issues Between Attorney General of Commonwealth of Massachusetts & Applicants ML20205P9131999-04-16016 April 1999 Submits Applicant Consent to Listed Condition of Approval of Transfer of License & License Condition for License DPR-35 & Affirmatively Request That NRC Adopt Listed Language in Order ML20205P9271999-04-16016 April 1999 Withdraws Motion for Leave to Intervene & Petition for Summary Or,In Alternative,For Hearing.Requests That NRC Adopt Condition of Approval of Transfer of License & License Condition Agreed to Beco & Entergy Nuclear Generation Co ML20205Q9231999-04-15015 April 1999 Forwards Proprietary & non-proprietary Addl Info in Support of Request to Transfer of Plant FOL & Matls License to Entergy Nuclear Generation Co.Proprietary Info Withheld,Per 10CFR2.790 ML20205P9631999-04-15015 April 1999 Provides Attachments a & B in Support of Request for Transfer of Plant Operating License & NRC Matl License from Beco to Entergy Nuclear Generation Co as Submitted in Ref 1. Info Provided in Response to Request at 990413 Meeting ML20205H9281999-04-0707 April 1999 Requests Withdrawal of Uwua Locals 369 & 387 Unions Joint Intervention in Listed Matter ML20205F3731999-04-0202 April 1999 Submits Addl Info Provided in Support of Request for Transfer of Pilgrim Nuclear Power Station Operating License & Matls License.State of Ma Order Authorizing Divestiture & Copy of Financial Arrangement Encl ML20204H3771999-03-26026 March 1999 Informs That Local 387,Utility Workers Union of America,AFL- Cio Voted to Approve New Contract with Entergy Nuclear Generation Co & Voted to Accept Boston Edison Divestiture Agreement ML20205D4231999-03-24024 March 1999 Forwards Decommissioning Funding Rept for Pilgrim Nuclear Power Station,In Accordance with 10CFR50.75(f)(1) 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARBECO-90-108, Forwards Anticipated Operator Licensing Exam Schedule Requested by Generic Ltr 90-07, Operator Licensing Natl Exam Schedule,1990-09-12012 September 1990 Forwards Anticipated Operator Licensing Exam Schedule Requested by Generic Ltr 90-07, Operator Licensing Natl Exam Schedule, ML20059D6641990-08-30030 August 1990 Forwards Revised Emergency Plan Implementing Procedures,Per 10CFR50,App E,Section V.W/O Encl ML20059D6791990-08-30030 August 1990 Notifies That Two Remaining Actions for Implementation of SPDS at Plant Complete,Per .Spds Procedures Modified,Identifying Sampling Panel C-19 Return Valves to Operator BECO-90-100, Advises That Valve MO-1001-50 Cannot Be Shown to Meet 30-day Mission for PASS in post-accident Environ Due to Elevated Radiation Dose Rates.Util Currently Developing Solution to Allow PASS to Meet 30-day Availability Requirement1990-08-27027 August 1990 Advises That Valve MO-1001-50 Cannot Be Shown to Meet 30-day Mission for PASS in post-accident Environ Due to Elevated Radiation Dose Rates.Util Currently Developing Solution to Allow PASS to Meet 30-day Availability Requirement BECO-90-102, Forwards Fitness for Duty Program Performance Data for Jan- June 19901990-08-23023 August 1990 Forwards Fitness for Duty Program Performance Data for Jan- June 1990 BECO-90-095, Informs That Kn Taylor Permanently Reassigned to Nuclear Training Dept as of 900717.Taylor Will Remain in Position Which Does Not Require License Certification1990-08-0808 August 1990 Informs That Kn Taylor Permanently Reassigned to Nuclear Training Dept as of 900717.Taylor Will Remain in Position Which Does Not Require License Certification BECO-90-092, Forwards, Decommissioning Funding Rept, Per 10CFR50.33(k) & 50.75(b)1990-07-26026 July 1990 Forwards, Decommissioning Funding Rept, Per 10CFR50.33(k) & 50.75(b) ML20044B3111990-07-11011 July 1990 Responds to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. Corrective Actions Include Replacement of Transmitters Identified in Suspect Lots & Implementation of Surveillance Program ML20044A7891990-06-19019 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Table Listing Status of Each Issue Encl ML20043D7181990-05-31031 May 1990 Advises That Response to NRC 900426 Safety Evaluation Re Util 880804 & 890619 Responses to Generic Ltr 88-01 Will Be Sent on 901115 ML20043A8211990-05-15015 May 1990 Notifies of Change of Senior Operator Status for Cj Martin, Per 10CFR50.74.CJ Martin Will No Longer Participate in Licensed Operator Requalification Training Program ML20042F2211990-05-0101 May 1990 Advises That Scheduled Completion of SPDS Human Factors Validation Activities Scheduled for 900630 & Sys Availability Test by 900731 ML20043B3881990-05-0101 May 1990 Responds to Violations Noted in Insp Rept 50-293/90-05. Corrective actions:82 Excess Flow Check Valves Installed & Operability of Valves Verified by Performing Surveillance Testing ML20012F5601990-04-0202 April 1990 Responds to Generic Ltr 89-13 Re Svc Water Sys Problems Affecting safety-related Equipment.Util Instituted Biofouling Control Program in 1982 & Program Has Been Effectively Implemented at Plant & Complies W/Generic Ltr ML20012F3631990-03-30030 March 1990 Requests Temporary Waiver of Compliance from Requirements of Tech Spec Table 3.2.C-1, APRM Upscale Rod Block in Startup & Refuel Modes to Avoid Unnecessary Delay in Critical Path Surveillance Testing ML20012C6501990-03-15015 March 1990 Responds to Generic Ltr 90-01 Re Request for Voluntary Participation in NRC Regulatory Impact Survey.Completed Questionnaire for Applicable Areas Delineated in Survey Encl ML20012D1931990-03-15015 March 1990 Forwards Proposed Scope & Objectives of Annual Exercise 90-04-B Scheduled for 900618 Per Lazarus 890609 Ltr, Emergency Exercise Objective & Scenerio Guidelines. Exercise Will Test & Evaluate Util EPIPs ML20012C7191990-03-14014 March 1990 Forwards Explanation of Errors in 890707 Application Re Corrective Action Plan & Advises That Errors Do Not Affect Technical Basis on Which Exemption Granted.Util Corrective Action Plan Remains Unchanged ML20011F5381990-02-26026 February 1990 Responds to Violations Noted in Insp Rept 50-293/89-12 on 891002-1119.Corrective Actions:On 891109,operations Personnel Directed,Via Night Orders,To Be More Diligent W/ Tagout Documentation & Boundary Tagging Clarified ML20011F2301990-02-23023 February 1990 Notifies of Change in Status of Senior Licensed Operator. DW Gerlits Terminated Senior Reactor Operator License on 900201 But Will Retain Position as Senior Sys & Safety Analysis Engineer ML20006G1411990-02-23023 February 1990 Advises That Tj Mcdonough Reassigned Effective 900126. Individual Will No Longer Participate in Licensed Operator Requalification Training Program ML20011F6521990-02-21021 February 1990 Forwards Inservice Insp Plan for 1990 mid-cycle Spring Outage for Facility.Augmented Insp Will Be Performed for Three IGSCC Category a Welds Using Guidance in Generic Ltr 88-01 & Criteria in NRC Bulletin 88-08,Suppl 3 ML20011F4481990-02-20020 February 1990 Forwards Revised Operability Evaluation of Salt Svc Water Pumps for Plant.Evaluation Concludes That Salt Svc Water Pumps Operable & Requirements of Tech Spec 3.5.B.1 for Pumps Met ML20006G0051990-02-20020 February 1990 Forwards Update to long-term Plan,In Accordance W/Section V.A of Plan for Long-Term Program. Util Implementing Plant Betterment Mods & Activities ML20011E7551990-02-0909 February 1990 Requests Temporary Relief from Tech Spec 4.7.A.2.b.1.d, Limiting Condition for Operation. ML19354E7661990-01-23023 January 1990 Responds to NRC Bulletin 89-002, Stress Corrosion Cracking of High Hardness Type 410 Stainless Steel Bolting in Anchor Darling.... Review Determined That No Subj Anchor Darling Swing Check Valves or Similar Valves Installed at Facility ML20011F4441990-01-19019 January 1990 Forwards Operability Evaluation Re Salt Svc Water Pumps P208 B,C,D & E,Per 900117 Telcon.Evaluation Concluded That Salt Svc Water Pumps P208 B,C,D & E Operable & Tech Spec 3.5.B.1 Requirements Met ML20006A0761990-01-15015 January 1990 Forwards Executed Amend 10 to Indemnity Agreement B-48 ML20006A2591990-01-15015 January 1990 Responds to Generic Ltr 89-10, Safety-Related Motor- Operated Valve Testing & Surveillance. Util Will Develop Program to Enhance Maint,Analysis & Testing Already Conducted on motor-operated Valves ML20005G7701990-01-11011 January 1990 Discusses Revised Schedule for Operability & Availability of Spds,Per 891221 Notification to Nrc.Rev Necessitated by Software Problems Affecting 891231 Schedule Projected in Util 890710 Ltr ML20005G7451990-01-11011 January 1990 Provides Bases for Environ Qualification of Instrumentation Monitoring Effluent Radioactivity & Status of Standby Power Per Reg Guide 1.97,Rev 3 & Generic Ltr 82-33 ML20005G8061990-01-11011 January 1990 Advises That Commitment to Complete Enhancements of Control Panels as Part of Dcrdr,Per NUREG-0737,Item I.D.1 by Oct 1989 Not Met.All Three Panels at Simulator Enhanced & Installation of Revised Meter Scales in Progress ML20005F0761990-01-0404 January 1990 Forwards Revised Inservice Test Program in Response to Generic Ltr 89-04.List of Inservice Test Program Relief Requests Previously Submitted & Acceptable,Per Generic Ltr 89-04,encl ML20005E5601989-12-29029 December 1989 Certifies That Util Has Established Fitness for Duty Program That Meets Requirements of 10CFR26.Drug & Alcohol Level Screening Match Rule Imposition & Implementation Will Be Effective on 900103 ML20042D4821989-12-26026 December 1989 Responds to Violations Noted in Insp Rept 50-293/89-10. Corrective Action:Radiological Section Standing Order 89-09 Issued Allowing Only Radiological Supervisors to Exercise Locked High Radiation Area Door & Key Control ML20011D6851989-12-14014 December 1989 Forwards Response to Generic Ltr 89-21, Request for Info Re Status of Implementation of USI Requirements. ML20011D1631989-12-14014 December 1989 Forwards Pilgrim Nuclear Plant Station Final Assessment Rept, Summarizing Results of self-assessments & Evaluations Conducted Throughout Implementation of Plant Restart Plan & Power Ascension Program ML19325F2751989-11-10010 November 1989 Responds to NRC Bulletin 88-010,Suppl 1, Nonconforming Molded-Case Circuit Breakers. Util Installed H2/02 Analyzers Procured in 1980 & Therefore Exempt from Bulletin Requirements ML19327C0911989-11-0606 November 1989 Forwards Response to Suppl 3 to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs. Since cyclic- Thermal Heatup/Cooldown Not Present in Piping,Failure Due to Cyclic Thermal Fatigue Will Not Occur ML19325E8581989-11-0101 November 1989 Discusses Litigation Before FERC Re Plant.Util Will Undertake Review of Matls Developed by Opposing Parties in Proceedings.Required Repts Will Be Submitted to NRC After Reportability Has Been Determined ML19325E5251989-10-27027 October 1989 Responds to Generic Ltr 88-20,Suppl 1,describing Plan for Completing Individual Plant Exam for Severe Accident Vulnerabilities.Performance of Level 1 PRA Based on Current Plant Design & Operation Intended ML19325E5661989-10-27027 October 1989 Response to Generic Ltr 89-04, Guidance on Developing Acceptable Inservice Testing Programs. Revised Inservice Testing Program Which Will Include Statement of Conformance to Technical Positions Will Be Submitted by 891215 ML19324B8191989-10-25025 October 1989 Informs That C Leonard & J Stokes Reassigned to Positions Which Do Not Require License Certification Effective 891003 & 891020,respectively ML19327B2291989-10-20020 October 1989 Responds to Generic Ltr 89-07 Re Power Reactor Safeguards Contingency Planning for Surface Vehicle Bombs.Changes Made to Contingency Plan,Per 10CFR50.54.Plan Withheld (Ref 10CFR73.21) ML19325E0981989-10-20020 October 1989 Responds to NRC Re Violations Noted in Insp Rept 50-293/89-07.Corrective Actions:Terminal Block Replaced, post-work Functional Test of Ref Temp Switches Performed & Procedure Tp 88-78 Revised to Correct Relay Numbers BECO-89-142, Responds to NRC Re Violations & Proposed Imposition of Civil Penalty from Insp Rept 50-293/89-95. Corrective Action:Two Responsible Util Operators Suspended Because Breakers Incorrectly Positioned for Test1989-09-22022 September 1989 Responds to NRC Re Violations & Proposed Imposition of Civil Penalty from Insp Rept 50-293/89-95. Corrective Action:Two Responsible Util Operators Suspended Because Breakers Incorrectly Positioned for Test BECO-89-144, Requests Interim Approval for Relief from Testing of RHR Sys Valves 63 & 64 Until Refueling Outage 8 Scheduled for 9103151989-09-22022 September 1989 Requests Interim Approval for Relief from Testing of RHR Sys Valves 63 & 64 Until Refueling Outage 8 Scheduled for 910315 BECO-89-135, Forwards Util Anticipated OL Exam Schedule,Per 890706 Generic Ltr 89-12 Request1989-09-11011 September 1989 Forwards Util Anticipated OL Exam Schedule,Per 890706 Generic Ltr 89-12 Request BECO-89-131, Forwards Tech Spec Figures 6.2-2 & 6.2-1,replacing Title of Director of Nuclear Engineering W/Title of Station Director & Adding New Title of Vice President of Nuclear Engineering1989-09-0505 September 1989 Forwards Tech Spec Figures 6.2-2 & 6.2-1,replacing Title of Director of Nuclear Engineering W/Title of Station Director & Adding New Title of Vice President of Nuclear Engineering BECO-89-129, Submits Addl Info Re 890707 Request for Exemption from Certain Containment Leakage Testing Requirements of 10CFR50. Plant mid-cycle Maint Outage,Previously Scheduled for Oct 1989,has Been Rescheduled for Spring 19901989-09-0101 September 1989 Submits Addl Info Re 890707 Request for Exemption from Certain Containment Leakage Testing Requirements of 10CFR50. Plant mid-cycle Maint Outage,Previously Scheduled for Oct 1989,has Been Rescheduled for Spring 1990 1990-09-12
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.- l Mi 10CFR50.59 l sosuwsusow
- Pilgrim Nuclear Power station Rocky Hdi Road Plymouth, Massachusetts 02360 l
Ralph G. Bird senior Vice President - Nuclear .
2 BECo 88- 113 U. S. Nuclear Regulatory Commission t Document Control Desk l
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Hashington, DC 20555 License DPR-35 !
Docket 50-293 i i
- REPORT OF CHANGES, TESTS ..;L ta ERIMENTS PERFORMED AT PILGRIM NUCLEAR POWER STATION
Dear Sir:
In accordance with 10CFR50.59(b), Boston Edison submits this report of the changes, tests, and experiments performed at Pilgrim Nuclear Power Station for the period of January 22, 1987 through January 21, 1988. t Attachment A is a list of changes completed in the-reporting period. Each ,
listing contains a brief description of the changes, a reference to the l 11evant Final Safety Analysis Report (FSAR) section, and a reference to !
the Safety Evaluation (s) that supports each change.
1 Attachment B contains a brief description of changes made to the plant l prior to 1987.
There were no reportable tests or experiments conducted in the report period. ;
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GGW/amm/2236 !
Attachments: A) Changes Completed in 1987 B) Changes Hade Prior to 1987 3
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- See Next Page '
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RMe9gfCM05000293 17 ano722 ., b PNU l
BOSTON EDISON COMPANY July 22, 1988
,U. S. Nuclear Regulatory Commission Page 2 cc: Mr. D. Mcdonald, Project Manager Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Mail Station P1-137 Hachington, DC 20555 U. S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Senior NRC Resident Inspector Pilgrim Nuclear Power Station
ATTACHMENT A tt BECO LETTER NO. 88- 113(5 pages)
CHANGES COMPLETED IN 1987 The following changes and related Safety Evaluations were reviewed and recommended for approval by the Operations Review Committee. The safety evaluations concluded that these changes did not involve an unreviewed safety quest *on as defined in 10CFR50.59(a).
YN ae_ndix e "R" Related Modifications Evaluation No. 1623 ce: FSAR Section 8.9 5., modification was broken up into six separate PDC packages as follows:
- 1. PDC 84-03A; Ductline Installation for Rerouting 65 Cables
- 2. PDC 84-03B; In plant raceway installation
- 3. PDC 84-03D; ADS System Relocation (Panel C157)
- 4. PDC 84-03E; Cable Installations
- 5. PDC 84-03F; Diesel Generator Alternate Shutdown Panel Modifications
- 6. PDC 84-03C; (This PDC was voided)
The changes were required for the plant to be in compliance with the requirements of 10CFR50, Appendix "R".
Reactor Buildina Secondary Containment Isolation Damoers Reolacement Safety Evaluation No. 2032
Reference:
FSAR Section 5.3.4, 5.3.3.3 This modification replaced the secondary containment isolation dampers.
The old dampers were commercial grade and experienced a high failure rate.
The replacement dampers are of sturdier construction and are fabricated with metal linkages for positive closure.
Add an_ Alarin to Mor,itor Position of Diesel Generator Jacket Water Pressure Relays Safety Evaluation No. 1866
Reference:
FSAR Section 8.5.4 This modification added an alarm to monitor the position of the diesel generator jacket water pressure relays when the diesels are in standby mode. Monitoring the position of control relays in the starting logic of the diesels is not safety related, and does not impact diesel generator performance. The alarm will increase reliability by providing the operators with advanced warning that parts of the diesel generator starting logic are inoperable, preventing the engines from starting.
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s Ultrasonic Flow M0nitor for Standbv Liquid _ Control System Safety Evaluation N0. 1858 (RI)
Reference:
FSAR Figure 3.8-1 This PDC installed an ultrasonic flow monitor on the SLC System d % charge piping for determining pump capacity during surveillance testit.g.
10CFR50.62 required an increase in SLC pump capacity. In order to measure the increased flow rate the externally mounted ultrasonic flow monitor was mounted on the discharge piping of the SLC pumps.
Shif t Suoervisor's Console - Communications Modules Safety Evaluation No. 1988
Reference:
FSAR Section 10.15-3 This change installed communications modules in the shift supervisor's new console. All communication functions previously provided are now provided in the new console with new equipment. The arrangement is organized to support operator and shift supervisor use. Additional capabilities (intercom and State Police line) are provided to resolve Human Engineering Discrepancies and improve emergency response.
Joa Open Feature for RHCU Valve 1201-2 Safety Evaluation No.1900
Reference:
FSAR Figures 4.9-1 and 7.3-20 This change will enable operators to jog open MOV 1201-2. There is no change to the control circuit to close the valve. The jog opening feature reduces the pressure transient experienced during start up of the RWCU system. H0V 1201-2 is a primary containment system valve. The automatic closure of the valve upon receiving a containment isolation signal is not affected by this change.
Refuelina Bridae Reolacement Safety Evaluation No. 2044
Reference:
FSAR Section 7.6 Due to degradation and obsolescence, the original refueling bridge was replaced with the exception of the refueling mast. The new bridge and I
attachments were analyzed against design basis accidents that could place a load on the bridge to ensure this Class II component will not degrade any Class I equipment, i
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Install Pressure Gauces on RHR System Safety Evaluation No. 1962 (Rev. 1)
Reference:
FSAR Figure 4.8-1, Figure 4.8-2 This modification provides indications to assist plant personnel in trending the leakage rate past the Residual Heat Removal System isolation valves. This will result in more efficient plant operation and an increase in plant safety. To achieve this, 4 additional pressure indicators were added and a controlled leakage bypass around the RHR discharge check valves was provided. In addition, temperature indicating tape was added to the process lines outboard of M01001-29A&B.
Deletion of Modulatina Controls for Diesal Generator Rooms Ventilation Damoers V207(A&B)
Safety Evaluation No. 2082
Reference:
FSAR Section 10.9-10 This modification deletes the modulating temperature controls for ventilation dampers in the diesel generator rooms. The requirements for these controls have been eliminated by the addition of a separate ventilation system consisting of two shutdown cooling fans. The ventilation dampers will open when the DG starts and will close when the DG is secured. The shutdown cooling fans operate whenever the DG is secured and the area temperature exceeds 90*F.
Reolacement of Offgas SJAE Flow Transmitter Safety Evaluation No. 85-30
Reference:
FSAR Figure 11.4-1 This modification replaced the Fischer and Porter SJAE flow transmitter with a qualified Rosemount transmitter. The installed Fischer and Porter transmitter failed in the field. Fischer and Porter no longer manufactures this unit. The Rosemount replacement is used in similar applications at PNPS and is functionally identical and only minor installation changes were required.
Replacement of Moisture Elements Safety Evaluation No. 84-99
Reference:
FSAR Figure 5.4-1 Obsolete moisture elements in the drywell have been replaced with new, smaller units, with no change in function. The elements are und to detect moisture in the drywell, and provide no trip function, only 9ndication.
They are also used during the ILRT.
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,' Drvwell Parsonnel Air Lock Modification (TH 84-251 Safety Evaluation No. 2011
Reference:
FSAR Figure L.2-24 The Drywell lock / closing mechanism was modified using the manufacturer's rebuild kit. Improved materials and replacement-in-kind components were recommended by the original equipment manufacturer. The rebuild / upgrade of the locking / closing mechanism for the drywell personnel air lock improves the reliability and operability of the equipment without changing the original design function.
RCIC Valve Annunciation Circuit Modification Safety Evaluation No. 83-22
Reference:
FSAR Figure 4.7-6 This modification eliminated the 15 second time delay relay in the RCIC trip valve annunciation circuit. The trip valve requires manual reset; therefore, this modification provides the operator with immediate indication of the system condition.
RBCCH Pressure Gauges Installation Safety Evaluation No. 2086
Reference:
FSAR Figure 10.7-1 This modification installed pressure gauges at exiting pressure test taps located on the salt water inlet and outlet nozzles for both RBCCH heat exchangers. Administrative limits for containment cooling subsystem operability require assessment of RBCCH heat exchanger heat transfer capability. To aid in surveillance in support of these limits, a means of pressure indication is required to show pressure differential between the heat exchanger tube inlet and outlet.
Repla_ cement of Fuses in the 23KV Supolv to the Shutdown Transformer Safety Evaluation No. 2068
Reference:
FSAR Figure 8.2-1 This modification replaced the fuse holders and links in the 23KV switchyard with 250 ampere links and new holders. This is the non-class 1E supply to transformer X13 (Shutdown Transformer). The fuses originally specified for protection of the Shutdown Transformer were type 'E' power fuses. The replacement fuse is the same basic type with an increase in size to 250 amp to provide transformer protection and acceptable coordination with downstream protective devices.
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Rgolacement of the Seal Helded Yoke to Adapter Plate on Mqior Opprator 1400-4A and B Safety Evaluation No. 2132
Reference:
FSAR Figure 7.4-8 This modification to Core Spray MOVs 1400-4 A&B, replaces a yoke design with a seal welded adapter plate with a yoke which has an integral adapter plate. The seal welded plate was a modification made to the original yoke design to eliminate an overstress condition. The replacement yoke has been manufactured specifically to accommodate the SMB-00 Limitorque operator.
As part of this change, the motor operator torque switch is also adjusted to limit the closing force thereby limiting stresses in the yee. This modification was made to strengthen the yoke to motor connection, improving valve reliability.
"B" RHR Heat Exchanger Floatina Head Drain Modification Safety Evaluation No. 2130
Reference:
FSAR Section 10.5-1 This modification removed the defective "B" RHR Heat Exchanger (E-2078) floating head drain line ball valve and replaced it with a threaded pipe cap. This change will decrease maintenance and improve the reliability of the heat exchanger by eliminating a potential leakage problem. The RHR Heat Exchanger is an interface between the RHR and RBCCH system. The floating head drain is used to drain the tube side (RBCCH side). This modification does not ef fect the operation of either system.
Raolacement of Valve A0-7011 A Safety Evaluation No. 2244 Reference FSAR Figure L.2-24 This modification replaced containment isolation valve A0-7011A (drywell equipment drain sump discharge) on the Radwaste Collection System. Only the valve was changed. The existing operator, limit uwitches and air supply is retained.
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.' ATTACHMENT B TO BECO LETTER NO. 88- 113(5 pages) l CHANGES MADE PRIOR TO 1987 This attachment describes changes made prior to 1987. They were identified this period as a result of improvements to our 50.59 reporting process.
Administrative / Shoo Buildina Service System Tie-ins Safety Evaluation No. 0667
Reference:
FSAR Figure 10.6-1 Connections with isolation valves were provided on existing PNPS Unit 1 systems (service / instrument air, plant heating, fire protection, potable water, and TBCCH). These connections were to be used when PNPS Unit 2 was built. The expanded buildings were cancelled with Unit 2 cancellation. The tie-ins were completed and remain unused or were u;ad for other plant modifications. The connections were designed to permit future tie-ins without affecting Unit 1 plant operations.
Miscellaneous Air Comoressor Chanaes Safety Evaluation No. 80-SE-13
Reference:
FSAR Sections F10.ll-1 and F11.9-1 This modification made the following changes to increase system reliability:
- 1. Installation of 1/2" copper piping from the demineralized water source to the two low pressure service air blowers (K105 A&B) seals.
- 2. Installation of a 1/2" bypass with manual block valve around the low pressure air compressor seal water solenoids (for maintenance purposes).
- 3. Addition of a 3/4" drain line from the K-111 compressor to the radwaste floor drain hub.
- 4. Addition of a drain / vent valve to the K-105B Kahn Air Dryer after filter (X-112F).
EA_SS and2 H 02 Monitoring System Electrical Installation Safety Evaluation Nos. 1112, 1018
Reference:
FSAR Sections 10.19 and F10.19.1 This modification provided the electrical installation details for the Post Accident Sampling System and the Primary Containment H2 /02 Monitoring System.
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Reagent and Calibrati 9n Gas Sucolv Subsystem for Containment 2H IO2jinniton Safety Evaluation No. 1237 I
Reference:
FSAR Section 10.19 This modification provided each H2 /02 analyzer panel with a reagent gas subsystem which provides commercially pure oxygen and hydrogen gas. A calibration gas subsystem common to both panels is also provided which supplies 4% hydrogen and 7% oxygen gas for calibration proposes. The gas subsystems are supplied by compressed gas cylinders located in racks on the 74'3" elevation of the Reactor Building.
Reactor Pressure Boundarv Leak Detection System Panel C-19 Safety Evaluation Nos. 1095/1079/1136/1161
Reference:
FSAR Sections 4.10.3.2, T7.3-1, T5.2-4, T5.2-5, F4.10-1 The Reactor Pressure Boundary Leak Detection System (RPBLDS) was modified by adding isolation valves to isolate (on receipt of a LOCA signal) non-Q piping. Sample return lines and containment isolation valves 'or the RPBLDS sample panel C-19 were also installed. The revised lear, detection system takes samples from two of the existing sample locations. These samples will be routed to separate locations at elevation 23' in the Reactor Building Secondary Containment. Sample return lines from each location are routed to a common return penetration with two series isolation valves.
Replace PT-1001-601 A and B Rosemount Absolute Transmitters with Rosemount Gauge Transmitters Safety Evaluation No. 1818
Reference:
FSAR Figures 4.8-1 and 7.4-11 This modification replaced an absolute pressure monitoring transmitter with a gauge pressure transmitter. Both types of transmitters are Rosemount. The FSAR Figure change is a P&ID update to note the supplier. Mounting and elet trical configuration are similar for both types of transmitter. Therefore, there is no change to safety significance. This is essentially an in-kind replacement.
Modification to Neutralizina Sump
( Safety Evaluation No. 83-13 4
Reference:
FSAR Section 10.10.3.7 and Figure 10.10-1 This modification removed the PH meter on the recirculation line of the
. Demineralizer and make-up systems neutralizing sump pumps and replaced it l with a bucket strainer to filter out resin beads.
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I Salt Service Water Cb_lorination Pioina Safety Evaltation No. 84-16
Reference:
FSAR Figure 10.07-1 This modification replaced corroded portions of the Salt 3ervice Hater chlorination piping with PVC piping. The change was performed on a Class II. system. This modification does not affect the ability of other safety systems from performing their safety function.
Remove Packing Leak-Off Valve on Core Sorav Valve H0-1400-4A Safety Evaluation No. 84-86
Reference:
FSAR Figure 7.4-8 This modification, to Core Spray Valve H01400-4A, replaced the packing leak-off valve and pipe with a 1/2" diameter section of stainless steel pipe and end cap. The evaluation concluded that no adverse safety condition would be created by this change.
Removal of the Gland Seal Leak-off Valve on RHR H0V-1001-29B Safety Evaluation No. 1747
Reference:
FSAR Figure 4.8-1 This modification removed a leak-off valve on RHR valve H0-1001-298. The leak-off line and valve interfered with the removal of the valve bonnet during normal valve maintenance. A 1/2" diameter stainless steel section of pipe with an end cap was welded into the opening created by removal of the leak-off valve. This modification does not affect the operability of the valve to perform its intended safety function nor does it degrade the Class I pressure boundary.
Installation of a Filter on the Discharae of the Sodium Hvoochlorite Tank Safety Evaluation No.84-104
Reference:
FSAR Figure 10.7-1 This modification installed a filter in parallel with an existing section of one inch PVC pipe down stream of the sodium hypochlorite tank isolation valve. Particulate debris (corrosion products from the tank) had been clogging downstream flow meters, valves, etc. The filter was added to remove the debris. All affected system and piping are non-safety related, Class II. This modification does not affect the ability of other safety systems from performing their safety function.
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Replace Pine in Sodium Hvoochlorite System Safety Evaluation No.84-117
Reference:
FSAR Figure 10.7-1 This modification replaced 3 sections of original piping with PVC pipe to determine the condition of the remaining original pipe. The chlorination system is non-safety related, Class II. This modification does not affect the ability of other safety systems from performing their safety function.
Egolace Oriainal 304SS Pipe Piece Hith 316SS in the RWCU System Safety Evaluation No. 1800
Reference:
FSAR Figure 4.3-2 This modification replaced a pipe piece of 304SS in the line from the bottom reactor vessel drain line to the RBCCH drain line. This installation will result in stresses within code allowable limits and will help mitigate IGSCC thereby enhancing safety.
New Trash Comoaction Facility Safety Evaluation No. 1630
Reference:
FSAR Sections 9.5, 9.2.4.1, 9.2.4.2.1, 9.2.4.2.2, 911, and 12.2.2.5 This safety evaluation addressed the radiological concerns associated with the new Trash Compaction Facility (TCF). The TCF is located outside the protected area, and is used to collect, prepare, package, and provide temporary storage for dry compactable trash prior to shipment offsite for disposal. No equipment in the TCF is related to any safe shutdown consequences. Radiological releases from the TCF, under normal operations, shall be within 10CFR20 limits. The operating procedures, storage cells and contaminated trash containers of the TCF are designed to reduce radiation levels ALARA.
Plua Leakina Tubes in the "B" TBCCH Heat Exchanaer (E-122 B)
Safety Evaluation No. 1648
Reference:
FSAR Section 10.6.3 This safety evaluation allows a revision to the heat exchanger seawater temperature parameter referenced in the FSAR. The evaluation assumes a maximum seawater temperature of 72*F whereas, the FSAR reference is 75'F. Actual operating experience has shown that the seawater temperature stays at or below 70*f. The safety evaluation concludes it is acceptable to plug a total of 141 tubes and still retain adequate heat transfer capability. Tube plugging is a normal maintenance activity.
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," ."- Change HPCI Start Time From 25 Seconds To 90 SecnM i Safety Evaluation No. 1830
Reference:
FSAR Sections 6.4.1, 7.4.3.2.4, 7.4.3.2.5 The purpose of this safety evaluation was to determine the impact of a potentially extended HPCI response time from the current ncminal 25 seconds to 90 seconds. The evaluation concluded that no significant change in the safety margins of the Pilgrim Nuclear Power Station for HPCI system response times ranging from 30 to 90 seconds would occur.
Cold. starts of the HPCI system have resulted in turbine trips followed by a rapid restart of the system to rated flow in-less than 90 seconds. The ECCS performance of PNPS with an assumed HPCI response time as long as 90 seconds was evaluated over the full range of postulated LOCAs. This safety evaluation did not involve any physical change to the HPCI system.
Exoand Allowable Cycle Time Limit for M0-1400-25 Valves A and B (Core Sorav Injection Valves)
Safety Evaluation No. 1914
Reference:
FSAR 7.4.3.4.4 This safety evaluation provides for changing the allowable cycle time limit for opening or closing M0-1400-25 valves A and B from 18 to 20 seconds. The slightly longer cycle time has a negligible impact on the containment isolation function of this valve. The revised cycle time is referenced in the FSAR. No physical change was made to the plant.
Diesel Oil Storage and Transfer Safety Evaluation No. 2084
Reference:
FSAR Figure 8.5-1 This safety evaluation documented the acceptability of as-built field conditions which are now reflected in the latest FSAR revision. The installed valve 38-H0-III was determined to be a 1/2" gate valve rather than a 1/2" stop cock as indicated on plant documentation. The replacement of the stop cock with a gate valve does not increase the risk of Diesel Fire Pump inoperability or increase the risk of an oil spill.
Gate valves are notably more durable and have superior stem packing than stop cock valves.
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