ML20148S200

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Insp Rept 50-285/87-24 on 870901-30.Violations & Deviations Noted.Major Areas Inspected:Ler Followup,Operational Safety Verification,Plant tours,safety-related Sys Walkdowns & Monthly Maint & Surveillance Observations
ML20148S200
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 01/22/1988
From: Harrell P, Hunter D, Reis T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20148S078 List:
References
50-285-87-24, NUDOCS 8802020359
Download: ML20148S200 (23)


See also: IR 05000285/1987024

Text

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APPENDIX C-

U.S.LNUCLEAR REGULATORY COMMISSION

REGION IV

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, NRC Inspection' Report: 50-285/87-24 Operating License: DPR-40:

Docket: 50-285

Licensee: Omaha Public Power District (0 PPD)

3623 Harney Street

Omaha, Nebraska 68102

Facility Name: Fort Calhoun Station (FCS)

Inspection At: Fort Calhoun Station, Blair, Nebraska

Inspection Conducted: September 1-30, 1987

Inspector: OR C / 88

P. II. Harrell, Sen'ior Resident Reactor Date

Inspector

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b yi L A , ,---

T. Reis, Resident Reactor Inspector

Iktle8

Date

Approved: OlbJM

D. R. Hunter, thief, Technical Support Staff

l[LL/88

Date

Division of Reactor Projects

Inspection Summary

Inspection Conducted September 1-30, 1987 (Report 50-285/87-24)

Areas Inspected: Routine, unannounced inspection including followup on

,previously identified items, licensee event report followup, operational safety

verification, plant tours, safety-related system walkdowns, monthly maintenance

observations, monthly surveillance observations, radiological protection

observations, in-office review of periodic and special reports, review of

10 CFR Part 21 program, and followup on IE Information Notices and IE Bulletins

issued for information only.

8802020359 880125

$DR ADOCK 05000285

PDR

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-Results: Within the 11 areas inspected, 6 violations ~(failure to properly

' store compressed gas cylinders.;in the auxiliary building, paragraph 5; failure

to establish a procedure for controlling the~ erection.of temporary scaffolding.

in areas containing-safety-related equipment, paragraph-5; failure to post:

up-to-date 10 CFR Part 21 documentation, paragraph 12) and l' deviation (failure

to implement. interim measures for control of fire-barriers, paragraph 2.m) were

identified.

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DETAILS j

1. Persons Contacted

  • R..Andrews, Division Manager, Nuclear Production i
  • W. Gates, Plant Manager l
  • C. Brunnert, Supervisor, Operations Quality Assurance l
  • H. Core, Supervisor, Maintenance
  • T.- Dexter, Supervisor, Security
  • J. Fisicaro, Supervisor, Nuclear Regulatory and Industry Affairs

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J. Foley, Supervisor, I&C and Electrical Field Maintenance

H. Faulhaber, Manager, Electrical Engineering, Generating Station

Engineering

  • J. Gasper, Manager, Administrative and Training Services
  • L. Gundrum, Plant Licensing Engineer
  • R. Jaworski, Section Manager, Technical Services

J. Kecy, Acting Reactor Engineer

R. Kellogg, Technical Services Engineer

M. Klanderud, Licensing Engineer '

L. Kusek, Supervisor, Operations-

O. Hunderloh, Plant Licensing Engineer

  • T. McIvor, Supervisor, Technical

R. Mueller, Plant Engineer

  • A. Richard, Manager,-Quality Assurance

G. Roach, Supervisor, Chemical and Radiation Piotection

  • R. Scofield, Supervisor, Outage Projects
  • D. Trausch, Nuclear Production Engineer

S. Willrett,' Supervisor, Administrative Services and Security

  • Denotes attendance at the monthly exit' interview.

The.NRC inspectors also contacted other plant personnel, including operators,

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technicians, and administrative personnel.

2. Followup on Previously Identified Items

a. (Closed) Open Item 285/8623-03: Modification of Exhaust Piping on

the Security Diesel Generator - This item was related to the failure

of the security emergency diesel generator while supplying power to

security equipment. A review by the licensee determined that the

diesel stopped because the air intake filter had become clogged due

to exhaust gasses entering the fresh air intake.

Initially, the licensee indicated that a review would be performed to

determine if a modification to the diesel exhaust piping should be

made. The licensee subsequently determined that a preventive

maintenance (PM) instruction would be issued to require the air

intake filter to be changed monthly. PM EE-24 was issued and

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performed on September 29, 1986, to' change the filter. The licensee

has changed the filter monthly since initiating the PM.

The NRC inspector reviewed the actions taken by the licensee. .It.

appears that the actions taken by the licensee will ensure that the

security diesel will be available when needed. The NRC inspector

noted that the licensee had tested the security diesel weekly since

the event and no further problems were encountered and that during

sustained diesel operations, the licensee personnel have been

instructed to routinely check the condition of the air intake filter.

b. (Closed) Severity Level IV Violation 285/8522-II.F.1.1

(Deficiency 85-22/2.1-8): Incorrect Information on Flow Diagram for

the Main Steam System - This violation noted that Drawing M-252

incorrectly represented the piping arrangement associated with'the

bypass valves and the auxiliary feedwater steam warm-up lines.

In response to this violation, the licensee revised and reissued

Drawing M-252 to correctly represent all lines associated with the

main steam system.

The NRC inspector reviewed and performed a walkdown of the main steam

system to verify that Drawing M-252 accurate.y reflected the plant

as-built conditions. No problems were noted.

During each inspection period, the NRC inspector walks down a

selected safety-related system to verify that the plant drawings

accurately reflect plant as-built conditions. During recent system

walkdowns, the NRC inspector occasionally found errors between the

drawings and the as-built plant, but the errors were of an editorial

nature and did not affect the safe operation of the plant or the

operability of the system. After each walkdown, the licensee

corrected the minor errors noted by the NRC inspector.

c. (Closed) Severity Level IV Violation 285/8529-II.A.2

(Deficiency 85-29/2.2-1): Installation of Temporary Lead Shielding

Without an Engineering Evaluation.- This violation described a

problem where the licensee was installing temporary lead shielding on

safety-related piping without performing an engineering evaluation to

determine if the piping could withstand the stresses caused by the

additional weight of the lead.

The licensee analyzed all locations where lead shielding had been

installed and a documented engineering evaluation was not available

for review at the time tha violation was identified. In each case

reviewed by the licensee, no cases were noted where the installed

piping had been ovec stressed due to the weight of the shielding. In

four of the locations, the licensee opted to leave the shielding

installed. The licensee performed appropriate calculations to verify

that no piping degradation existed. In addition, the licensee

securely attached the shielding to ensure that the shielding would

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not shift or move on the piping. The weight of the attachments was

considered in the engineering evaluations.

The. licensee has established a program through the issuance of-

Procedure 50-G-57, "Installation of Temporary. Lead Shielding," to

. ensure that a proper engineering evaluation was performed and

. documented prior to the. installation of any lead shielding. The

program required that an independent review be performed to verify

that the-required analysis and safety evaluation were completed prior

to approving installation.

The NRC inspector reviewed a selected number of evaluations to verify

that the shielding installed without a documented engineering

evaluation did not affect piping integrity, reviewed the evaluations

and actual installation for the four locations where the shielding

was left installed to verify proper installation, and reviewed

. Procedure 50-G-57 to verify that the licensee had established an

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appropriate program for control of shielding installation.

During the 1987 refueling outage, the NRC inspector reviewed the

installation of temporary lead shielding on several occasions to

verify that an engineering evaluation had been performed and that the

shielding was installed in accordance with the installation

instructions. For each case reviewed, the licensee had properly

installed the shielding.

Based on the review performed by the NRC' inspector, it appeared that

the licensee had performed evaluations for installed shielding and

had established a program to adequately control future shielding

installations,

d. (Closed) Severity Level IV Violation 285/8529-II.A.3

(Deficiency 85-29/2.2-2): Swagelok Fitting Installed Through Fire

Barrier at the Entrance to Room 17 - This item invcived the

installation of a stainless steel Swagelok fitting through a fire

barrier. The licensee could not produce documentation to indicate

that the installation of the fitting was performed in accordance with

an approved plant engineering field change.

The licensee, prior to startup from the 1985 refueling outage,

performed an evaluation and determined that the installation of the

fitting did not degrade the fire barrier. The review of this portion

of the followup on this violation is documented in NRC Inspection

Report 50-285/86-03.

The licensee revised and upgraded Procedure 50-G-58, "Fire Barrier

Protection," to include requirements for identification and

evaluation of all existing fire barrier penetrations. A program for

identification was completed and the evaluations performed on the

penetrations indicated some penetrations were inadequate. The

licensee repaired the inadequate penetrations. The barrier

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containing the stainless steel fitting identified by this violation

was replaced with a new fire door.

The NRC inspector reviewed Procedure 50-G-58 to verify that the

-licensee had establishrd.an adequate program to ensure an evaluation

was performed prior to installing a penetration. It appeared that

the program was adequate. In addition, the NRC inspector performed

numerous plant tours to identify any penetrations that had been

installed without prior approval. No penetrations were identified

during the tours.

e. (Closed) Severity Level IV Violation 285/8529-II.A.4

(Deficiency 85-29/2.2-3): Safety Evaluations for Installation of

Temporary Jumpers had not been Performed - This violation was related

to the. failure of the licensee to perform evaluations.for electrical

and mechanical jumpers and blocks installed in safety-related

systems. It was noted during the inspection that some jumpers had

been installed greater than 18 months.

The licensee performed a review of all electrical and mechanical

jumpers installed at the time of the inspection to verify none of the

jumpers adversely affected the operation of a safety-velated system.

No problems were noted. The li:ensee also revised Procedure 50-0-25,

"Electrical and Mechanical Jumpers and Block Control," to include

requirements previously unaddressed in Procedure 50-0-25. The new

requirements included performance of a documented safety evaluation

prior to installation of a jumper or block, review of jumpers and

blocks for initiation of a design change to make long-term temporary

system changes into permanent system modifications, and

implementation of a tracking system to ensure the design changes are

implemented in a timely manner.

The NRC inspector reviewed the jumper and lifted lead log to verify

that all temporary modification activities performed on

safety-related systems received an evaluation prior to installation

of the modification. During review of the log, the NRC inspector

noted no problems with the performance of evaluations. There were

two temporary modifications that had been installed in systems for

greater than 18 months. In both cases, the licensee had initiated

and scheduled system design changes to make the temporary

modifications permanent. A review of the log also indicated tnat the

Supervisor, I&C and Electrical Maintenance and the Plant Engineer

reviewed the temporary modification log each month to verify that all

installed jumpers and blocks were necessary. The NRC inspector

performed a review of Procedure 50-0-25 to verify that the procedure

appropriately implemented a program that provided adequate control of

temporary jumpers and blocks. Based on the various reviews

performed, it appeared that the licensee had established and

implemented an acceptable program for control of temporary

modifications.

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f. (Closed) Unresolved Item 85-29/2.5-2 of NRC Inspection

Report.50-285/85-29: No Documentation Available for Replacement of

0-rings in Foxboro Transmitters .This unresolved item identified

that the licensee could not produce documentation for replacement of

the-'0-rings.in Foxboro transmitters following instrument calibration.

The calibration procedures used by the licensee required 0-ring

repla_ cement in order to maintain the equipment qualification of the

transmitters.

The licensee replaced the 0-rings in all Foxboro transmitters prict

to plant startup from the 1985 refueling outage. Each 0-ring

replacement was documented by an informal notation in the calibration

procedure for each instrument and by completion of a Form FC-198

"Electrical Equipment Qualification / Qualified Life Program

Information Sheet." In addition, the licensee made changes to all ,

affected calibration procedures to require that formal entries be

made to record the part and purchase order numbers for the 0-ring

used, and a verification sign-off that the transmitter cap was

torqued to the proper value. By including this information in each

calibration procedure, the licensee established a method for easily

retrievable documentation for verification of 0-ring replacement.

The NRC inspector reviewed a selected sample of completed calibration

procedures that were performed during the 1985 refueling outage to

verify that documented evidence existed to indicate that the 0 rings

were properly replaced. The NRC inspector also reviewed selected

calibration procedures to verify that changes had been made to

require documentation of 0-ring replacement in each calibration

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procedure. No problems were noted.during the reviews.

g. (Closed) Severity Level IV Violation 285/8529-II.F.1.b

(Deficiency 85-29/2.8-1): Failure to Properly Perform a Battery

Charger Test - This. violation was related to the failure of the

licensee to perform an adequate test of Battery Charger 3. The test

did not require that data be taken at specific time intervals;

therefore, no evidence existed that the battery charger could meet

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the established acceptance criteria.

In response to this violation, the licensee reperformed the test on

the battery charger during the 1987 refueling outage in accordance

with Maintenance Order (MO) 871643. The M0 provided specific

instructions for testing that included the concerns identified by the

inspection team. The concerns were starting time of test, initial

float and equalizing voltages, voltage values recorded at regular

intervals, final float and equalizing voltages at test completion,

and completion time of test. The licensee reviewed the test results

and determined that the battery charger was capable of meeting its

intended safety function.

The NRC inspector reviewed MO 871643 to verify that the licensee had

established an appropriate test for the battery charger. The review

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included verification that the appropriate data was taken, the

acceptance criteria were clearly established, and tne test results

verified that the battery charger was capable of performing its

operational requirements. Based on the results of the review

performed, it appeared that the licensee had taken appropriate

actions to verify proper operation of the charger.

h. (Closed) Severity Level IV Violation 285/8529-II.I.4, II.I.5, and

II.I.6 (Deficiency 85-29/2.9-1): Failure to Properly Store Material

in Temporary Critical Quality Element (CQE) Storage Areas - This

violation involved the failure of the licensee to. ensure only

properly designated CQE material was stored in temporary CQE storage

areas. CQE storage areas were erected inside the plant to provide

storage for items that had received quality assurance (QA) inspection

and required segregated storage in accordance with ANSI standards.

In response to this violation, the licensee revised

Procedure 50-G-22, "Storage of Critical Element and Radioactive

Material Packaging, Fire Protection Material, and Calibration

Equipment." The procedure revision established new requirements for

placing or storing parts and materials in the temporary CQE storage

areas. The procedure required that an entry on a storage area log

sheet be made and verification established to ensure that the

material was CQE prior to placement in the storage area.

The NRC inspector reviewed Procedure 50-G-22 to verify that the

procedure had properly implemented requirements to prevent storage of

non-CQE material in temporary CQE storage areas. During the past

12 months, the NRC inspector also performed an inspection of various

temporary CQE storage areas located in the plant. During the

reviews, the NRC inspector verified that the material stored in the

areas was CQE material; the material was properly identified; the

material was properly stored with respect to cleanliness control, as

appropriate; and no non-CQE material was stored in the area. No

problems were noted with the procedure revision or storage of

material in the temporary CQE areas.

i. (Closed) Severity Level IV Violation 285/8529-II.I.3

(Deficiency 85-29/2.9-3): Failure to Perform Surveillances of

Temporary CQE Storage Areas This violation was related to the

failure of the quality control (QC) department to perform

surveillances of temporary CQE storage areas. The monthly

surveillance reqJirements Were established by Proceduro S0-G-22 and

no documentation existed to indicate the surveillances were being

performed.

The licensee revised Procedure S0-G-22 to establish a program for

tracking the surveillances performed to verify the adequacy of

temporary CQE storage areas. The revision to the procedure

implemented Form FC-1068 that provided a historical .ecord for

surveillance performance for each storage area. Form FC-1068

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required a surveillance of each storage area monthly during plant

operations and weekly during the high activity period of a refueling

outage.

The NRC inspector reviewed Procedure S0-G-22 to verify that an

appropriate surveillance program for storage areas had been

established. The NRC inspector also reviewed Form FC-1068 to verify

that surveillances had been performed on a monthly or. weekly

frequency, as appropriate. During review of Procedure 50-G-22 and

Form FC-1068, no problems were noted. It appeared that the licensee

had established and implemented an acceptable program for the

surveillance of temporary CQE storage areas.

j. (Closed) Severity Level IV Violation 285/8529-II.J.1

(Deficiency 85-29/2.10-1): A Program for Installation of Temporary

Lead Shielding had not been Established - This violation documented

the failure of the licensee to establish a program for installation

of temporary lead shielding on safety-related systems.

This violation is discussed in paragraph 2.c of this inspection

report. Based on the discussion, this violation is considered

closed.

k. (Closed) Severity Level IV Violation 285/8614-01: Failure to

Maintain Cable and Cable Tray Installations in Accordance with Design

Documents - This violation was related to the failure of the licensee

to maintai.) the installation of safety releted cable and cable trays

in accordance with the design documents that originally installed the

cable and trays. The proble.ns noted in this violation were the

failure to maintain cable tray covers properly installed and

overfilling of a tray with power cables.

The licensee took actions to ensure that the installation of

safety-related cable trays complied with design documentation. The

actions taken by the licensee included a walkdown of all trays to

ensure all covers were properly installed. The walkdown was

performed in accordance with the instructions provided by MO 862038.

The licensee established a computerized system for the cable and

conduit schedule. Using the computerized schedule, the licensee

established that the cables installed in Tray Section 21S were

satisfactory. The cables were determined to be satisfactory based on

cable derating factors. Prior to establishment of a computerized

schedule, the licensee used a criteria based on cable and tray

cross-sectional area. The licensee also revised the appropriate

sections of the Updated Safety Analysis Report (USAR) Figure 8.5-1 to

reflect the change to the computerized system. Drawing 11405-E-151

provided instructions for installation of cable trays. This drawing

has been deleted and USAR Figure 8.5-1 has been implemented for cable

tray installation instructions.

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The NRC inspector-reviewed the actions taken by the licensee to

verify that they were appropriate. The items reviewed are listed

below:

. Reviewed'the calculation performed by the licensee and' verified

that the cables installed in Tray 215 did not exceed the limits

specified for cable derating.

. . Reviewed USAR Figure 8.5-1-to verify that the licensee had

changed the figure to reflect the newly established computerized

conduit and cable schedule.

. Walked down various cable trays in the auxiliary building and in

containment to verify that covers were properly installed, no

loose objects were in the trays, divider plates were securely

fastened, and' cables were tied down.

Based on the reviews performed, it appeared that the licensee had

taken appropriate actions to ensure cables and cable trays were

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installed in accordance with design requirements and had taken

actions to ensure the cables and cable trays were maintained in a

satisfactory condition.

1. (Closed) Open Item 285/8702-05: Review of the Audit Performed by the

Licensee in the Area of 10 CFR Part 21 Activities - This open item is

related to an audit performed by the licensee in the area of Part 21

activities. During an inspection performed by the NRC inspector in

January 1987 the inspector noted various problems with the licensee's

implementation of their Part 21 activities. The NRC inspector noted

that the licensee's QA department had found the same problems during

an audit performed in December 1986.

The NRC inspector reviewed the close out of the deficiencies

identified by the licensee. The review was performed to verify that

the QA department had addressed the specific problem noted and had

ensured that adequate action had been taken to prevent recurrence.

The deficiencies noted by the QA department were a systematic and

generic problem with issuance and control of procedures and

instructions related to Part 21 reporting responsibilities, and a

systematic and generic problem related to training of parsonnel in

each individual's responsibilities for reporting Part 21

deficiencies. Based on the review, it appeared that the QA

department performed adequate close out of the audit findings.

m .~ (0 pen) Severity Level V Violation 285/8710-01: Failure to Provide a t

Continuous or Hourly Fire Watch for Nonfunctional Fire Barriers -

This violation identified a problem where the licensee failed to

provide a fire watch for a nonfunctional fire barrier. The failure

to provide a fire watch was a violation of TS 2.19(7).

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In response-to the viol'ation, the licensee stated that

Procedures SCP-14, "Patrol Procedures," used to define

responsibilities of the security guard during plant tours, and

150-0-38,'"Firewatch Duties and Turnover Procedures," used for the

. establishment of_ fire watches, would be revised to ensure that an

effective program was implemented. The licensee revised

Procedure 50-0-38, but had not completed implementation of corrective

actions due to Procedure SCP-14 not being revised.

In response to this violation, tSe licensee also stated that a memo

would be issued to all personnel with unescorted access as an interim

measure. The purpose of the memo was to make each individual aware of

his/her individual responsibilities in maintaining fire barriers

fully functional. The interim measure was to be taken until changes

could be made to the appropriate procedures to establish permanent

corrective action.

In followup on this violation, the NRC inspector noted that the

licensee had not yet issued the memo. The failure to issue the memo

that provided interim measures for ensuring nonfunctional fire

barriers were provided appropriate attention is an apparent deviation

from a commitment made to the NRC. (285/8524-01)

As detailed in NRC Inspection Report 50-285/87-20, the licensee has

continued to experience problems in maintaining fire barriers in a

functional status. These problems were discussed with licensee

management during the exit interview.

n .- (0 pen) Unresolved Item 285/8710-05: Performance of a Calculation to

Verify Sufficient Trisodium Phosphate Dodecahydrate (TSP) is Stored

in Containment - This unresolved item was related to the performance

of a calculation for verification that sufficient TSP was inplace in

containment. The calculation was to be performed to evaluate the

discrepancy between the TS and the USAR as to the quantity of TSP

needed in containment in the event that containment recirculation was

initiated. Prior to plant startup in June 1987 the NRC inspector

reviewed a preliminary calculction that verified the proper amount of

TSP was stored in containment. At the time of the review, licensee

personnel stated that a formal calculation would be completed in the

near future (i.e., 2 or 3 weeks). The NRC inspector has requested at

various times since review of the preliminary calculation, to review

the final calculation; the licensee has not yet completed the formal

calculation to verify the TSP in containment was adequate. This item

remains open pending completion of the formal calculation by the

licensee and a review of the results by NRC personnel.

3. Licensee Event Report (LER) Followup

Through direct observation, discussions with licensee personnel, and

review of records, the following event reports were reviewed to atitennine

that reportability requirements were fulfilled, immediate corrective

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action was accomplished, and corrective action to prevent recurre. ice had

been accomplished in accordance with TS.

The LERs listed below are closed:

-87-005 Unplanned actuation of the ventilation isolation actuation

system (VIAS) via Radiation Monitor RM-061

87-006 Unplanned initiation of the containment pressure high

signal (CPHS) during surveillance testing

87-020 Unplanned actuation of the VIAS via Radiation Monitor RM-050

-A discussion of the closeout of each LER is provided below:

a. LER 87-005 reported inadvertent actuation of the. VIAS during

calibration of Radiation Monitor RM-061. The VIAS was initiated when

the technician pushed RM-061 back into the monitor cabinet and a

loose screw caused a momentary loss of signal. The loss of the

signal caused initiation of the VIAS. All appropriate systems

functioned normally. The technician tightened the screw.and the VIAS

cleared.

The licensee issued MO 871159 to check and tighten the screw

terminations on the other process monitors. No other screws were

found that were loose. In addition,-during routine calibration

activities, technicians verify that all connections are tight.

The NRC inspector reviewed the actions taken by the licensee. Based

on the review, it appeared that the licensee had taken appropriate

actions to correct the cause of the event and to prevent recurrence.

b. LER 87-006 reported the initiation of the containment pressure high

signal (CPHS) during performance of a local leak rate test for the

containment pressure sensing penetration. All appropriate safety

equipment functioned normally. CPHS was initiated due to a contract

technician error during performance.of the pressure test. The

technician inadvertently opened the sensor isolation valve prior to

bleeding the test pressure off the sensing line. The technician

failed to follow all notes and steps contained in the procedure being

used. Upon becoming aware of the event, the technician bled the

pressure off the sensing line to clear the CPHS.

The licensee instructed all contract and licensee technicians of the

importance of ensuring all notes and steps of procedures were

followed. The licensee committed in Violation 285/8710-04, which was

related to an error in performance of a local leak rate surveillance

test, to conduct training for contract and licensee personnel

performirg leak rate testing. This training should ensure that tests

are performed properly during the next refueling outage.

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The NRC inspector reviewed Procedure ST-CONT-3, "Type C Local Leak

Rate Test," to verify that'the proper instructions had been provided

to the technicians. No problems were noted. The NRC inspector

reviewed the actions taken by the licensee.and it appeared that the

actions W re appropriate for correcting the problems related to this

event and that the proposed training will prevent recurrence.

c. LER 87-020 reported the unplanned actuation of the VIAS during plant

startup. The VIAS was initiated due to a containment radiation high

signal that was caused by an alarm on Radiation Monitor RM-050. All

appropriate systems functioned normally during the VIAS. .The

licensee took immediate action and verified no particulate radiation

was present in containment and no release occurred.

The licensee reviewed the cause of the initiation of the VIAS and

noted that the setpoints for RM-050 had not been reset from the

shutdown value to the operating value prior to commencing plant

startup. To ensure that the setpoints were reset at the appropriate

point during plant startups in the future, the licensee made a

procedure change to require resetting of the setpoints.at a reactor

coolant system temperature of 395 F, the minimum temperature at which

the hydrostatic test of the reactor coolant system may be performed-

during startup.

The NRC inspector reviewed the actions taken by the licensee and it

appeared that appropriate actions were taken to ensure that no

particulate radiation was released to the atmosphere. The NRC

inspector reviewed Procedure 01-RC-3, "Reactor Coolant System

Startup," and verified that a change had been. issued to require t e

setpoints to be raised from the shutdown to operating values at

395 F. Based on the review performed by the NRC inspector, it

appeared that the licensee had taken actions to prevent recurrence of

L this event.

d. In May 1987, the licensee identified problems with the welds on the

emergency feedwater storage tank (EFWST). In May 1987, a conference

j. was held in the Region IV offices to discuss the problems associated

with the EFWST welds and the licensee's planned corrective actions.

Four days after the meeting, the NRC inspector requested that an LER

be submitted to the NRC detailing the problems found with the EFWST.

Licensee personnel stated that an LER would be sent.

In September 1987, the NRC inspector requested a copy of the LER on

the EFWST. Licensee personnel stated that the LER had not yet been

issued. In addition, licensee personnel stated that the problems

with the welds on the EFWST were not reportable under the

requirements of 10 CFR Part 50.73; therefore, an LER was not issued

within the 30-day requirement specified in Part 50.73. Subsequently,

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the licensee issued LER 87-022, dated September 25, 1987, detailing

the problems identified with the EFWST. The LER was issued as a

voluntary report by the licensee.

When the NRC inspector reviewed'the circumstances associated with

this. event, it appeared that a 30-day event report should have been

initiated by the licensee. This item remains unresolved pending a

review of the licensee's LER program to verify that.the program

. properly implements the reporting requirements of 10 CFR Part 50.73.

(285/8724-02)

No violations or deviations were identified.

4. Operational Safety Verification

The NRC inspectors conducted reviews and observations of selected

activities to verify that facility operations were performed in

conformance with.the-requirements established under 10 CFR, administrative

procedures, and the TS. The NRC inspectors made several control room

observations to verify the following:

. _ Proper shift staffing

. Operator adherence to approved procedures and TS requirements

. Operability of reactor protective system and engineered safeguards

equipment

. Logs, records, recorder traces, annunciators, panel indications, and

switch positions complied with the appropriate requirements

. Proper return to service of components

. H0s initiated for equipment in.need of maintenance-

. Appropriate conduct of control room and other licensed operators

. Management personnel toured the control room on a regular basis

No violations or deviations were identified.

5. Plant Tours

The NRC inspectors conducted plant tours at various times to assess plant

and equipment conditions. The following items were observed during the

tours:

. General plant conditions, including operability of standby equipment,

were satisfactory.

l

1

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.

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.

. Equipment was being maintained in proper condition, without fluid

leaks and excessive vibration.

. Plant hous'ekeeping and cleanliness practices were observed, including

no fire hazards-and the control of combustible material.

. Performance of work activities was in accordance with approved

procedures.

. Portable gas cylinders were properly stored to prevent possible

missile hazards.

. Tag out of equipment was performed properly.

. Management personnel toured the operating spaces on a regular basis.

. The auxiliary feedwater pumps were not steam bound.

During plant tours, the NRC inspector noted the following:

. A seismic support for a safety-related cable tray.in Room 81 had been

removed and not reattached. The support was attached to the tray but

was not affixed to a structural member. The NRC inspector requested

the licensee provide a drawing that would indicate whether or not the

tray support should be' installed to maintain seismic qualification of

the tray. The licensee stated that a drawing showing.the location of

tray seismic supports did not exist. The licensee could not

establish, prior to the end of this inspection period, whether or not

the support was required for the cable tray. This item remains

unresolved pending a review by the licensee to determine if the tray

support is required and to establish why no drawing exists that shows

the location of seismic supports for safety-related cable trays.

(285/8724-03)

. During a tour cf the auxiliary building on September 21, 1987, the

NRC inspector identified a problem where two large nitrogen

compressed gas cylinders had been secured to a support for a

safety-related pipe snubber. The snubber was attached to the

-

recirculation line for the safety injection and containment spray

pumps. The NRC inspector also noted that a large nitrogen bottle

pressurized to 1600 psig was attached to a handrail, in the vicinity

of safety-related equipment, with a 3/8-inch nylon rope; that 4 gas

cylinders were tied in a group to a cylinder storage rack with a

3/8-inch nylon rope; and a welding cart containing an oxygen and

acetylene compressed gas cylinder, without caps, was stored,

unsecured in an area with safety-related equipment.

Criterion V of Appendix B to 10 CFR Part 50 states, in part, that

activities affecting quality shall be prescribed by documented

' procedures of a type appropriate to the circumstances and shall-be

accomplished in accordance with these procedures.

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Paragraph 1.0 of Section 6.4, "Housekeeping;" of the licensee's

Quality Assurance Plan (QAP) states, in part, that this plan section

specifies the quality assurance requirements for housekeeping

controls'for protection of equipment. Paragraph 4.5 of QAP

Section 6.4 states, in part, that. instructions which implement this

plan section shall be contained in the station standing orders.

Standing Order (50) G-6, "Housekeeping," was issued to implement the

requirements of QAP Section 6.4. Paragraph 3.3.4 of 50-G-6 states,

in part, that gas cylinders shall be properly stored in the auxiliary

building, with caps installed, unless in use or use is intended

within a short period of time.

Contrary to the above, the licensee failed to properly store gas

cylinders in the auxiliary building, as noted by the four examples

discussed above, in that cylinders were secured to a safety-related

seismic support; cylinders were secured using a 3/8-inch nylon rope,

an unapproved storage method; and cylinders were left. uncapped and

unsecured in the auxiliary building. This is an apparent violation.

(285/8724-04)

As documented in past inspection reports issued by the NRC resident

inspector, the licensee has continued, over the last 6 months, to

encounter problems with storage of gas cylinders in the auxiliary

building. Early in this inspection period, the licensee issued a

memo to the appropriate personnel to alert the individuals of the

problems previously experienced with the storage of gas cylinders.

It appears that issuance of the memo did not provide adequate

corrective action to prevent recurrence of this problem. The

licensee, upon notification by the NRC inspector, took actions to

properly secure the gas cylinders.

. Housekeeping in the auxiliary building continued to require

additional licensee attention. Bags of miscellaneous material were

stored in various locations. Room 59 was noted to have a large

accumulation of bagged material.

. During a tour of the plant on September 9, 1987, the NRC noted that

the licensee had erected two temporary scaffolding sections adjacent

to the EFWST. One section of scaffolding was a free-standing

structure and the other section was attached to the EFWST

instrumentation lines. The NRC inspector requested a copy of the

safety evaluation that addressed the affect of the nonseismically

installed scaffolding on the EFWST, should a seismic event occur.

The: licensee stated that a safety evaluation had not been performed

and that no procedure existed to require an evaluation be done when

erecting temporary scaffolding in safety-related areas.

The scaffolding was erected to facilitate work on the nitrogen supply

line for the EFWST in accordance with Modification

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Request (MR) FC-86-56. MR-FC-86-56 stated that scaffolding should be

erected, as needed, to perform the modification work.

l

Criterion V of Appendix B to 10 CFR Part 50 states, in part, that

activities affecting quality shall be prescribed by procedures of a

type appropriate to U4e circumstances.

Paragraph 4.7.2 of Section 5.1, "Control of Plant Design and

Modification," of the licensee's QAP states, in part, that

appropriate procedures shall be used for modification activities.

Contrary to the above, the licensee failed to implement a procedure

for control of the erection of temporary scaffolding in areas

containing safety-related equipment; therefore, no evaluation was

performed to address the potential affect of nonseismically installed

scaffolding on safety-related equipment during a seismic event. This

is an apparent violation. (285/8724-05)

The NRC inspector notified the licensee of the existence of the

scaffolding on September 9, 1987. The licensee completed removal of

the scaffolding on September 14, 1987.

. During a plant tour on September 25, 1987, the NRC inspector noted

that licenseo personnel had stored tool boxes, large cabinets, small

parts cabinets, and a small crane in the safety-related east and west

switchgear rooms. In discussions with licensee personnel, it was

determined that the electrical shop was being moved so the current

shop facility could be expanded. When the move occurred,

electricians had stored their tools and parts in the switchgear

rooms. Upon notification by the NRC inspector, licensee personnel

immediately removed all tools and parts from the switchgear rooms.

The NRC inspector discussed the need to ensure that unsecured objects

were not stored in any safety-related areas witt. licensee management

at the exit meeting.

6. Safety-Related System Walkdowns

The NRC inspector walked down accessible portions of the following

safety-related emergency diesel generator 1 and 2 systems to verify system

operability. Operability was determined by verification of selected valve

and switch positions. The systems were walked down using

Procedures 0I-DG-1, Revision 22; 01-DG-2, Revision 22; and the drawings

noted below:

. Fuel oil system (Drawing M-262, Revision 23)

. Air start system (Drawing B120F07001, Revision 4)

. Lubricating oil system (Drawing B120F03001, Revision 4)

. Jacket cooling water system (Drawing B120F04002, Revision 1)

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During the walkdowns, the NRC inspector noted that valves designated by

procedure did not correspond correctly with the system drawings. Due to

the nature of the errors, system safety and operability were not degraded;

however, the NRC inspector expressed concern to the licensee that the

errors were not internally found with 22 revisions existing to the

operating procedures. Licensee personnel verified the errors and had them

corrected immediately.

'

No violations or deviations were identified.

7. Monthly Maintenance Observations

The NRC inspectors reviewed and/or observed selected station maintenance

activities on safety-related systems and components to verify the

maintenance was conducted in accordance with approved procedures,

regulatory requirements, and _ the TS. The following items were considered

during the reviews and/or observations:

. The TS limiting conditions for operation were met while systems or

components were removed from service.

. Approvals were obtained prior,to initiating the work.

. Activities were accomplished using approved M0s and were inspected,

as applicable.

. Functional testing and/or calibrations w'ere performed prior to

returning components or systems to service.

. Quality control records were maintained.

. Activities were accomplished by qualified personnel.

. Parts and materials used were properly certified.

. Radiological and fire prevention controls were implemented.

The NRC inspectors reviewed and/or observed the following :paintenance

activities:

. Installation of Fire Door 1007-11 (M0 853356)

. Troubleshooting of high temperature trip on Emergency Diesel

Generator (EDG) No.2

. Repair of pilot valve for radiator exhaust damper on EDG No. 2

(M0 874509)

. Repair of the emergency diesel fuel oil storage tank level indicator

(M0 874516)

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. Testing of a battery charger (M0 871643)

No violations or deviations were identified.

8. Monthly Surveillance Observations

The NRC inspectors observed selected portions of the performance of and/or

reviewed completed documentation for the TS-required surveillance testing

on safety-related systems and components. The NRC inspectors verified the

following items during the testing:

. Testing was performed by qualified personnel using approved

procedures.

'

. Test instrumentation was calibrated.

. The TS limiting conditions for operation were met.

. Removal and restoration of the affected system and/or component were

accomplished.

. Test results conformed with TS and procedure requirements.

. Test results were reviewed by personne? other than the individual

directing the test.

. Deficiencies identified during the testing were properly reviewed and

resolved by appropriate management personnel.

The NRC inspectors observed and/or reviewed the documentation for the

following surveillance test activities. The procedures used for the test

activities are noted in parenthesis.

. Monthly test of an emergency diesel generator (ST-EST-6-F.2)

~

. Local leak detection test of the personnel air lock (ST-CONT-2-F.1)

. Pressurizer pressure channel check (ST-ESF-1-F.2)

. Recirculation actuation logic test (ST-ESF-13-F.2)

. Auxiliary feedwater valve alignment check (ST-FW-1-F.1)

. Reactor coolant system low flow trip check (ST-RPS-3-F.2)

No violations or deviations were identified.

9. Radiological Protection Observations

The NRC inspectors verified that selected activities of the licensee's

radiological protection program were implemented in conformance with the

, facility policies and procedures and in compliance with regulatory

requirements. The activities listed below were observed and/or reviewed:

. Health physics (HP) supervisory personnel conducted plant tours to

check on activities in progress.

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. ~ Radiation work permits contained the appropriate information to

. ensure work was performed in a safe and controlled manner.

. Personnel in radiation controlled areas (RCA) were wearing the

required personnel monitoring equipment and protective clothing.

. Radiation and/or contaminated areas were properly posted and

controlled based on the activity levels within the area.

. Personnel properly frisked prior to exiting an RCA.

During a plant tour on September 11, 1987, the NRC inspector found a door

to a very high radiation area unlocked. This matter was referred to a

Region IV health physics specialist. The details of this item are

provided in NRC Inspection Report 50-285/87-21.

No violations or deviations were identified.

10. In-office Review of Periodic and Special Reports

In-office review of periodic and special reports was performed by the NRC

resident inspectors and/or the Fort Calhoun project inspector to verify

the following, as appropriate:

. Reports included the information required by appropriate NRC

requirements.

. Test results and supporting information were consistent with design

predictions and specifications.

. Determination that planned corrective actions were adequate for

resolution of identified problems.

. Determination as to whether any information contained in the report

should be classified as an abnormal occurrence.

The NRC inspectors reviewed the following:

. Refueling outage inservice inspection results, dated August 31, 1987

. Cycle 10 fuel performance report, dated September 2, 1987 <

. Refueling outage Type B and C local leak rate test summary, dated

September 3, 1987

. Monthly Operations Report, undated

. August Monthly Operating Report, dated September 14, 1987

No violations or deviations were identified.

.

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11. Review of-10 CFR Part 21 Program

A review of the licensee's program established to meet the requirements of-

10.CFR Part 21 was performed. The review included the following elements:

. Procedures have been. established and are adequate to ensure proper

implementation of 10 CFR Part 21 requirements.

. Documentation required by 10 CFR Part 21 has been posted in areas

where safety-related work activities are conducted.

. Specification of the application of 10 CFR Part 21 requirements in

applicable procurement documents.

. Evaluation of self-identified deviation, condition, or circumstance

was performed by the licensee for determination of reportability

under the requirements of 10 CFR Part 21.

. Evaluation by the licensee of a condition, deviation, or circumstance

reported by vendors or suppliers to determine the affect of safe

operation of the facility.

. Verification that facility modifications were performed when the

licensee's evaluation indicated that a modification was appropriate.

The NRC inspector reviewed the procedures established by the licensee to

implement the requirements of 10 CFR Part 21. The. documentation reviewed

included Procedure 50-G-42, "Reporting of Defects and Noncompliance to the

Nuclear Regulatory Commission," Revision 7; Procedure H-2, "Report of

Defects and Noncompliance to the Nuclear Regulatory Commission,"

~

Revision 1; and Procedure QADP-19, "10 CFR 21, Reporting. Defects and

Noncompliances," Revision 3. Procedure 50-G-42 provides reporting

instructions for individuals working in the Omaha offices, and

Procedure QADP-19 provides the quality assurance department instructions

for reporting defects. Based on the review of these procedures, it

appeared that they adequately implement the evaluation and reporting

requirements of 10 CFR Part 21.

The NRC inspector reviewed the postings required by 10 CFR Part 21 to

verify the appropriate documents of the latest revision had been posted.

The review included verification of postings at the plant site, Jones

Street offices, and at the Brandeis building. The NRC inspector noted

that the posting of 10 CFR Part 21 and the implementing Procedure (H-2) at

the Brandeis building were not the current revision. The NRC inspector

also noted that Section 206 of the Energy Reorganization Act of 1974 was

not posted. During the previous review performed by the NRC inspector in

January 1987, as documented in NRC Inspection Report 50-285/87-02, it was

also noted that the material required to be posted by Part 21 was out of

date. The licensee stated at that time that all posting would be updated.

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Section 21.6 of 10 CFR Part 21 states, in part, that each entity subject

to the regulations of this part, shall post current. copies of the

following documents where activities subject to this part are conducted.

The documents include the regulations in this part, Section 206 of the

Energy Reorganization Act (ERA) of 1974, and procedures adopted pursuant

to the regulations in this part.

Section 7.6.2 of Procedure H-2, "Reporting of Defects and Noncompliance to

the Nuclear Regulatory Commission," states, in part, that the following

documents shall be posted in conspicuous places at the Fort Calhoun

Station, Jones Street Station, and Generating Station Engineering offices:

10 CFR Part 21, Section 206 of the ERA of 1974, and Procedure H-2.

Contrary to the above, the licensee failed to post the latest revision of

the Part 21 regulations and the licensee's implementing procedure, and

failed to post Section 206 of the ERA at the Brandeis building (the

Generating Station Engineering offices). This is an apparent violation.

(285/8724-06)

The review performed in this area was not completed prior to the end of

the inspection period. Tht review will be continued during a future

inspection.

12. Followup on IE Information Notices and IE Bulletins Issued for Information

Only

The NRC inspector reviewed the licensee's system established for

processing IE Information Notices and IE Bulletins issued for information

only. This review was perfonned to verify that the licensee had received

the notices and bulletins; the notices and bulletins were distributed to

the appropriate personnel for review; and that any actions determined to

be appropriate during the review, had been taken.

The NRC inspector reviewed selected notices and bulletins issued during

the latter part of 1986 and 1987 to verify appropriate action had been

taken. No problems were noted by the inspector for those items reviewed.

No violations or deviations were identified.

13. Unresolved Item

An unresolved item is a matter about which more information is required in

order to determine whether it is acceptable, a violation, or a deviation.

Two unresolved items are discussed in paragraphs 2.d and 5.

1

Item Paragraph Subject l

285/8724-02 3.d Review of licensee's program to

implement reporting requirements

of 10 CFR Part 50.73

l

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285/8724-03 5 *

. Improperly installed seismic

support for a safety-related

cable tray

14. Diesel Generator Shutdown and Water Ingress Into the Instrument Air System.

On September 23, 1987, Diesel Generator No. 2 (DG-2) shutdown due to high

coolant temperature. Licensee investigation revealed that the air

operated exhaust damper for the diesel generator radiator did not appear

to hade fully opened as designed. The cause of damper malfunction appears

to be the presence of a sticky lime like residue which cause the air pilot

valve to stick. It is significant that on July 6,.1987, water was-

introduced into the instrument air system flooding that portion of the

system below the auxiliary building elevation 1025 feet. A separate

inspection was conducted by the Region IV Resident Inspectors in

preparation for an enforcement conference concerning both the DG-2 failure

and the introduction of a significant quantity of water in the instrument

air system. For further detail see NRC Inspectior Report 50-285/87-27 and

License Event-Report 05000285-025.

15. Exit Interview

The NRC inspectors met with Mr. R. L. Andrews (Division Manager, Nuclear

Production) and other members of the licensee staff at the end of this

inspection. At this meeting, the NRC inspectors summarized the scope of

the inspection and the findings.

.