ML18227A406

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Attached October, 1976 Operating Status Reports for Turkey Point Unit Nos. 3 & 4 and St. Lucie Unit No. 1
ML18227A406
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 11/08/1976
From: Schmidt A
Florida Power & Light Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML18227A406 (12)


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FLOHIOA POWER 8c LIGHT COi%1PANY November 8, 1976 Office of Management Information .

and Program Controls U.'. Nuclear Regulatory Commission Washington, D. C. '0555 Gentlemen:

Attached are the October, 1976 Operating Status Reports for Turkey Point Unit Nos. 3 and 4 and St. Lucie Unit No. l. ~I jq,qy Very truly yours, 1t j

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~1 VTC/DDC Attachments cc: Mr. Norman C. Moseley Jack R. Newman, Esquire 6/

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44

APPENDIX B AVERAGE DAILY UNIT POWER LEVEL t

DOCKET NO. 50 250 UNIT Turkey Point Unit No. 3 DATE Nov. 5, 1976 COMPLETED BY V- T. Chi1son TELEPHONE (305) 552-3830 MONTH October 1 76 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (M!fe-Net) (MWe-Net) 650 17 643 658 18 628 3 657 19 64S 655 20 656 656 21 654 652 22 659 651 23 667 630 24 663 596 25 651 10 643 26 642 640 27. '647 12 639 28 649 13 620 29 654 14 578 30 660 15 648 31 655 16 651

APPENDIX C 6

OPERATING DATA REPORT DOCXn NO. 50 - 250 UNIT Turkey Point Unit No. 3 REPORT MONTH October. 1976 DATE Nouo 5 ~ 1976 LETED By V. T. Chilson OPERATING STATUS TELEPHONE (305) 552-3830 lo 2.

THROUGH CURRENTLY 2400~7 I~'0 REPORTING PERIOD 0001 76 YAUTHORZZED POWER LEVEL NAE.DEPEND. CAPAC111 (IINA Nee):

01 GROSS (MWt):

HOURS

~66 IN REPORTING PERIOD 745.0*

DESIGN ELECTRICAL RATING (MWe-Net): 93 3~ POWER LEVEL TO WHICH RESTRICTED"(IF ANY) (MWe-Net): NONE

4. REASONS FOR RESTRICTION (IF ANY):

THIS MONTH YEAR TO DATE CUMULATIVE

5. NUMBERS OF HOURS REACTOR WAS 6

CRITICAL. ~ ... 745.0* 6 446.1 '27 726.2 60 REACTOR RESERVE SHUTDOWN HOURS ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 64.2 67.4

7. HOURS GENERATOR ON LINE.. ~........,.. ~..., 745.0* 6 355.6 26 725.6 8 UNIT RESERVE SHUTDOWN HOURS. ~ ~ ~ ~ ~ ~ .. ...

~ ~ . 0 0 0.0 85.0

9. GROSS THERMAL ENERGY GENERATED (MWH)...... 1 614 694 13 733 282 51 045 542
10. CROSS ELEC1RICAL EIIERDE CENERAEEO (NIIN)... 505 740 4 340 645 16 355 881 ll. NET ELECTRICAL ENERGY CENERATED (AAH). ~ ~ .. 480 673 4 119 351 1~5475
12. REACTOR SERVICE FACTOR............'........ 100.0 88.1 80.9 I
13. REACTOR AVAILABILITYFACTOR.. ~ ~ ~ ~ ~ .~~~.~~. 100.0 . 88.9 81.1
14. UNIT SERVICE FACTOR.... ~ ... .... ...,...,

~ ~ ~ 100,0 86.8 78.0

15. UNIT AVAILABILITYFACTOR,...,.......... ~ .. 100.0 86.8 78.2
16. EDIT CAPACITY PACTOR (Using (MDC)... ~ 84.5 68.8
17. UNIT CAPACITY FACTOR (Using Design MWe)... 81.2 65.2 18 'NIT FORCED OUTAGE RATEo ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 0.0 0.1 3.0 19 SHUTDOWNS. SCHEDULED OVER NEXT 6 MONTHS (TYPES DATES AND DURATION OF EACH)

Refueling, r)aintenances and insPections

20. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION): FORECAST ACHIEVED INITIAL CHITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION NOTE<
  • Changed from DST to EST on Octobor'1, 1976

I) REASON APPENDIX D DOCKET NO A: EQUIPMENT FAILURE (EXPLAIN)

B: MAINT. OR TEST UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Turkey Point Unit No..3 C REFlKLING D- REGULATORY RESTRICTIOH DATE Nov. 5, 1976 E: OP~TOR TRAINING AND LICENSE EXAMINATION COMPLETED BYV. T. Chilson P. ADMINISTRATIVE G OPFZATIONAL ERROR (EXPLAIN) REPORT MONTH October TELEPHONE (305) 552-3830 1976 H: OTHER (EXPLAIN)

') ?KID raLUAL METHOD OP 2: MANUAL SCRAM TYPE SHUTTING DOWN 3: AUTOMATIC SCRAM Ft FORCED DURATION THE REACTOR OR DIPL (EXPLAIN) NO. S: SCHEDULED (HOURS) REASON(l) REDUCING POWER(2) CORRECTIVE ACTIONS/COHHENTS 20 76-10-08 8 N/A Load reduction to perform periodic test of turbine main steam stop, reheat stop> and reheat intercept valves. (Non-nuclear system)

SU7RARY: Unit No. 3 operated at approximately 1002 R.P. 'during month except for load reduction on October 8, 1976 to perform periodic test of turbine main steam stop, reheat stop, and reheat intercept valves.

APPENDIX B AVERAGE DAILY UNIT POWER LEVEL t

DOCKET NO. 50 251 UNIT Turke Point Unit No. 4 .

'ATE Nov. 5, 1976 COMPLETED BY V. T. Chilson TELEPHONE (305) 552-3830

'MONTH October 1976 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 666 17 674 676 18 673 3 676 19 596 673 20 630 675 21 675 6 667 22 683 666 23 683 663 24 685 610 25 562 10 26 620

.27 621 12 28 13 29 14 65 30 15 =

664 31 16 679 NOTE; Daily average power level greater than 666MWe due to cooler condenser water.

APPENDIX C OPERATINC DATA REPORT DOCYZT NO. 50 - 251 UNITTL2rke Point Unit No 4 REPORT MONTH October 1976 DATENov. 5, 1976 CO.PLETED BY V. T. Chilson

~ XELEPHONE (305) 552 3830 1 REPORTING PERIOD: 0001.76 10 01 CROSS HOURS IN REPORTING PERIOD:

  • THROUGH 2400
2. CURRENTLY AUTHORIZED POWER LEVEL (MWt):

MAX DEPEND. CAPACITY (MWe-Net):

3; POWER LEVEL TO WHICH RESTRICTED (IF ANY) (AAWe-Net): NO 46 REASONS FOR RESTRICTION (IF ANY):

THIS MONTH YEAR TO DATE CUMULATIVE

5. IIUHEERS OF HOIIIIS REACTOR'UAS CRZTZCAL..... 536.2 5 357.6 2~100 6, REACTOR RESERUE SHUTUOIIE HOIIIIS......... 0.0 0.0 ~ZZT 7~ HOURS GENERATOR ON LINE, ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~

527 ' 5 159 ' 20 434 0

8. UNIT RESERVE SHUTDOWN HOURS... ~ ..... ~ ,'.. ~ ~

0.0 0.0 0.0 r

9. GROSS THERMAL BARGY GBKRATED (MWH)...,, 1 134 444 10 957 697 41 606 333 10 CROSS ELECTRICAL DIRECT CEIIERATEU {HIIHZ... 365 550 ~gggO ~2LSKL.

II. NET ELECTRICAL ENERGY GENERATED (MWH)..... 346 662 3 317 972 1~27 12 'EACTOR SERVICE PACTOR... ~ ........,'... ~ i ,

~

. 72.0

13. REACTOR AVAILABILITYPACTOR. ~ ~ ~ -~ AORS ~ ~ ~ 73.2 75.5
14. UNIT SERVICE FACTOR. ~ . ...... ~ . ~ ~ .. ...

~ ~ ~ . 70.8 70.5 73.0 15 'NIT AVAILABILITY PACTOR ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 70.5 73.0

16. 'UNIT CAPACITY FACTOR (Using (MDC)...... 69 9 68.1 69.3
17. UNIT CAPACITY FACTOR (Using Design MWe)... 67-1 65.4
18. UNIT FORCED OUTAGE RATE. .. . .. ~ . ~ 4.1 3.6 19 'HUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):
20. IP SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION): FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION NOTEt
  • Changed DST to EST on October 31, 1976 (1) Corrected-to-date

REASON APPENDIX D DOCKET NO. 50 - 251 A: EQUIPMENT FAILURE (EXPLAIN)

B: MAINT. OR TEST UNIT SHUTDOWNS AHD POWER REDUCTIONS UNIT NAME Turke Point Unit No. 4 C: REFUELING D: RECULATORY RESTRICTION DATE Nov..5, 1976 E: OPERATOR TRAINING AND LICENSE, EXAMINATION COMPLETED BY V. T. Chilson F: ADMINISTRATIVE C: OPERATIONAL ERROR (EXPLAIN) REPORT MONTH October, 1976 TELEPHONE 305 '552 3830 OTHER (EXPLAIN)

PACE ONE OF TWO 1: MANUAL METHOD OF 2: MAhUAL SCRAM TYPE SHUTTINC DOWN 3'AUTOMATIC SCP&! Ft FORCED DURATION THE REACTOR OR 4r OIHER (EXPLAIN) NO. DATE S: SCHEDULED (HOURS) REASON(1) REDUCINC POWER(2) CORRECTIVE ACTIONS/COMMEhTS 25 76-10-09 115.7 A- Unit No. 4 was removed from service to locate and repair tube leak in steam generator Ho. 4B. There were no significant quantities of radioactive material released as a result of this small leak. Corrective action was to plug the leaking tube. (Nuclear System) 26 76-10-19 Reactor was tripped by steam generator ho. 4A pro-tection system when the feedwater regulator was closed by failure of a solenoid valve. Corrective action was to replace the failed solenoid. (Non-nuclear System) 27 76-10-19 1.7 3 Unit No. 4 was triPped by actuation of the 1oss of field relay caused by malfunction of the generator voltage regulator system. (Non-nuclear System)

l) REASON APPENDIX D DOCKET NO. 50 - 251

~ A: EQUIPMENT FAILURE (EXPLAIN) 8: MAINT. OR TEST UHIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Turkey Point Unit No. 4 C: REFUELING D: REGULATORY RESTRICTION DATE Nov. 5; 1976 E: OPERATOR TRAINING AND LICENSE EXAMINATION COMPLpgg) DY V T Chilson F: ADMINISTRATIVE G: OPERATIONAL ERROR (EXPLAIH) REPORT MONTH October, TELEPHONE (305) 552-3830 1976 H: OTHER (FsXPLAIN)

PAGE TWO OF TWO METHOD OF 2: MANUAL SCRAM TYPE SHUTTING DOWN 3: AUROMATIC SCRAM Fs FORCED DURATION THE REACTOR OR 4: DINER (EXPLAIN) NO. DATE S: SCHEDULED (HOURS) REASON(1) REDUCING POWER(2) CORRECTIVE ACT ION8/CQDKNTS 27 76-10-19 2.3 Unit No. 4 vas tripped by actuation of generator over-excitation relay caused by malfunction of voltage regulator system. Corrective action included repairs to one of the tvo solid tstate pover supply units in the voltage regulator control section. (Nonnuclear System) 28 76-10-28 96.5 Unit No. 4 vas removed from service for steam generator tube inspection program. (Nuclear System) u o,

gllHHARY: Vnit Ho. 4 operated at sppro ital*y 1001 R 9 dri 9 n.th., *capt for outages n Oct. 9 to 14 snd Oct. 19, til Oct. 10, 1916, hen the nit uas ramrod fro ser ic to perforn ste generator tube inspection.

APPENDIX B AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

UNIT St. L'ucie Unit No. 1 DATE Nov. 5, 1976 COMPLETED BY V. T. Chilson TELEPHONE (305) 552-3830 MONTH October, 1976 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 17 18 3 19 20 21

.22 23 24 10 26 27 12 28 13 29 14 30 15 16

APPENDIX C OPERATING DATA REPORT DOCXET NO. 50 - 335 UNIT St. Lucia Unit No. 1 REPORT MONTH October 1976 DATE Nov. 5, 1976 COMPLETED BY V. T. Chilson TELEPHONE (305) 552-3830 OPERATING STATUS THROUGH 24

2. CURRENTLY AUTHORIZED POWER LEVEL (MWt):

DESIGN ELECTRICAL RATING (MWe-Net): 802

3. POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net): 722 46 REASONS FOR RESTRICTION (IF ANY):

"Temporary 902 restriction pending Reactor Coolant Flov Analysis" THIS MONTH YEAR TO DATE CUMULATIVE 56 NUMBERS OF HOURS REACTOR WAS CRITICAL. ~ ~ .. -0 1 366.6 1 366.6 A(1) N/A(1) N/A(1) 69 REACTOR RESERVE SHUTDOWN HOURS.. ~ .. ~

N

7. HOURS GKKRATOR ON LINE ,... . . . ..

~

1 121.9 1 121.9

8. UNIT RESERVE SHUTDOWN HOURS. .......* . ..

~ ~ ~

N A(1) N/A(1) N/A (1)

9. GROSS THERMAL ENERGY GF9iERATED (MWH)...... 0- 1 495 088 1 495 088 10 GROSS ELECTRICAL ENERGY GRKRATED (MWH) -0 418 670 418 670 116 NET ELECTRICAL ENERGY GENERATED (MWH) ~ ~ ~ ~- 374. 180 374 180 12, REACTOR SERVICE FACTOR. ~ ~ ~ ~ ~ 9 6 ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 0.0 31.8 31.8 I
13. REACTOR AVAILABILITYFACTOR. ~ ~ ~ ~ ~ ~ ~ ~ ~ '6 0.0 31.8 31.8
14. UNIT SERVICE FACTOR...... ~ ... ...... ...

~ . 0.0 26.4 26.4

15. UNIT AVAILABILITYtACTOR, ~ ~ ~ ~ ~ ~ ~ ~, ~ ~...,, . 0 0 26.4 26.4
16. IDiIT CAPACITY FACTOR (Using (MDC) ........., 0.0 11.0 11.0
17. UNIT CAPACITY FAC1OR (Using Design MWe)... 11.0 11.0
18. UNIT FORCED OUTAGE RATE.................. ~ 72.3 72.3 19 ~ SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE ~ DATE 9 AA%l DURATION OF EACH)

N/A(1) 206 IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

21. UNITS Oi TEST STATUS (PRIOR TO COMMERCIAL OPERATION): FORECAST ACHIEVED INITIAL CRITICALITY Arrll 22, 1976 INITIAL ELECTRICITY 72IL" 7~76 COMMERCIAL OPERATION NOTEi (1) Unit in test status Changed from DST to EST on October,31, 1976,

ql

) REASON APPENDIX D DOCKET NO+ 50 335 h: EQUIPMENT FAILURE (EXPLAIN)

B: MAIHT. OR TEST UHIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME St. Lucio Unit No 1 C: REFUELING D: DATE Hov. 5, 1976 REGULATORY RESTRICTION E: OPERATOR TRAINIHG AND V. T. Chilson LICENSE EXAHINATION F: ADMIHISTRATIVE C: TELEPHONE OPERATIONAL ERROR (EXPLAIN) REPORT MONTH October 1976 H: OTHER (FAP IAIN)

) METHOD MANUAL METHOD OF MANUAL SCRAM TYPE SHUTTIHC DOWN AUTOMATIC SCRAM F: FORCED DURATION THE REACTOR OR 4: DINER (EXPLAIN) NO. DATE S: SCHEDULED (HOURS) REASON(l) REDUCINC POWER(2) CORRECTIVE ACTIONS/COMMENTS 16 76-07-10 745.0>> Unit yas reaeved froa service for reactor tests and inspection. (Nuclear Systen)

SUMMARY

Unit No. 1 reactor inspection continued during conth.

NOTEt

  • Changed fron DST to EST on October 31, 1976