ML18227A414

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Attached July, 1977 Operating Status Reports for Turkey Point Unit Nos. 3 & 4 and St. Lucie Unit No. 1
ML18227A414
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 08/05/1977
From: Schmidt A
Florida Power & Light Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML18227A414 (14)


Text

U.S. NUCLEAR REGULATORY MMISSION D KET NUMBE NHC;FORM 195 12-76) c

/ FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL M NTHL FROM: DATE OF DOCU NT TO:

NRC Florida Power G Light Co. 8577 Miami, FL 33101 DATE R Ec EI V E D A.D. Schmidt 8 12 77 ETTE R ONOTORIZED PAOP INPUT FORM NUMBEA OF COPIES RECEIVED RIG INAL COPY

/fan N C LASS I F I E D / S/q~ro DESCAIPTION ENCLOSURE

'I Letter trans the foll:ng: Monthly Report for July 1977 Plant 5 Component Operability 8c Availability.

This Report to be used in preparing Gray Book by Planh 8e Operations.

qQ lIl;QSI PLANT NAME: (1-P) (ll-P)

VT'/13/77 Turkey Point Units 3 G 4; St. Lucie Unit 1 Cc I

FOR ACTION/INFORMATION CYS R CT N INTERNAL D ISTRI BUTION nc e c ss EXTERNAL DISTRIBUTION CONTROL NUMBER C e e ~

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'7224003 NAC FOAM 195 I2 7$ 1

P 0 8OX 013100 MIAMI FL 33>0I FLORIDA POWER Br LIGHT COMPANY August 5, 1977 Office of Management Information / .Rf.g/gp and Program Controls ~ ~ lg77~

U. S. Nuclear Regulatory Commission Washington, D. C. '0555 r Gentlemen:

Attached are the July, 1977, Operating Status Reports for Turkey Point Unit Nos. 3 and 4 and St. Lucie Unit No. l.

I Very truly yours, A. D. Schmidt Vice President i

Power Resources VTC/DDC cc: Mr. Norman C. Moseley Robert Lowenstein, Esquire

'722AQ' EOP LE... SERVING P EOP LE

APPEÃ)IZ B AVERAGE DAlLY MiET POVER LEVEL DOCKET NO. 50 250 UNITUnit No. 3 DATEAugust 5, 1977 COMiLETED BY V. T. Chil son TEKEPHOiiE (305) S52-3769

- MONTH JULY, 1977 (MWe-Net)

DAY AVERAGE DAlLY POMZR LEVEL DAY AVERAGE DAiLY POL'Pr'R LEVEL (KVe-Net) 643 17 658 645 18 314 645 19 292 646 20 644 21 646 22 25 649 23 227 642 467 641 25 647 10 639 26 643 636 27 640 12 639 28 638 13 639 29 637 14 640 30 643 as 640 31 639 16 652

APPENDIX C OPERATLfG DATA REPORT Domm HO. 50 - 250 ur ey o nt Unit No. 3 REPORT ifONTH JULY, 1977 DATF August 5, 1977 CONPLE~M BY V. T. Chilson TcCEPHONE (305) 552-3769 OP~TI'VG STATUS

1. REPORTZifG PERIOD: 0001077 07001 GROSS HOURS I.'i REPORTLfG PERIOD: 744.0 TBROUCH 2400
2. CUKKZLY AUTHORIZE) POWER LEVEL (i%Sit): 2200 NAZ D&KRfD. CAPACITY (Ifie-Net): 666 DESIGN ELECTRXCAL RATE'.fG (444e-Het): 693
3. PO~r LEVEL TO fsEIXCH RESTRICT%) (IF A."fY) ('Sie-Net): NONE
4. RL4SONS FOR RESTRICTION (ZF A!iY):

THIS NONTH YEAR TO DATE CiDPJLAT~iT 5 ~ NfSMiERS OF HOURS REACTOR WAS CRITICAL..... 670.9 4 514.7 32 554.8 6~ ~r CTOR RESERVE SHUTDOWi HOURS ~ ~ ~ ~ . ~ ...... ~ 4.8 4.8 72.2 7 ~ HOURS CLRfERATOR ON LiifE. .

~ ~ ~ .. ~ ~ ......,... 652.6 4 345.0 31 384.1 S. UNIT IIESERUE S!1UTUUUN "OURS............... 85.0

9. GROSS THEBIfAL ERKRGY CF'KRATED (RfWH)...... 1 387 483 9 313 286 ~61 041 I
10. GROSS ELECTRICAL KRIERGY CLRKRATED (IGHH). ~ . 424 265 2 979 151 19 549 602 I
11. NET ELECTRICAL ENERGY GENERATED (IffiH)..... 401 801 2 828 518 I~S04 4
12. REACTOR SERVECE FACTOR. 90.2 88.7 79.7
13. REACTOR AVAILABH.XTYFACTOR.. ~ ~ ~... ~..., .. 90.8 88.8 79.9 14 UNIT SERVECE FACTOR . ~ . . ~ , ~ , , 87.7 85.4 76.9
15. UiNIT AVAILABILITY FACTOR...,.....,....,... 87.7 85.4 77.1 16 'WET CAPACITY PACXOR (Uelng (44DC).......... 81.1 83.5 68.1
17. UNIT CAPACITY FACZOR (Using Design 'Sfie)... 80.2 65.4
18. UNIT FORCED OUTACE RATE. ~ ............... ~ 12.3 3.2 3.0
19. SHUTDO'vPifS SCIKDULED OVER 444T 6 .fOÃTHS (TYPE, DATE, A4%) DURATXON OF EACH):

Stean Generator Inspection - August 16 - Septenber 12, 1977

20. XF SHUTDOffN AT EHD OF ~ORT PERIOD, ESTLfATED DATE OF STARTJP:

214 UNXTS Li TEST STATUS (PRIOR TO CO. fERCEAL OPERATION): FORECAST ACHZaVED LNZTEAL CRITZCALXZY LIITZAL ELECTRICITY COMKRCZAL OPERATEO'.f

.) REASON APPEHDIX D DOCKET HO. 50 - 250 A: EQUIPHENT FAILURE (EXPLAIN) Turkey Point B: HAINT. OR TEST UNIT SIIUTDOWNS AHD POWER REDUCTIONS UNIT NAHE Unit No. 3 C: REFUEI.IHC D: RECULATORY RESTRICTION DATE Au ust 5 1977 E: l)PERATOR TRAIHINC AND LICENSE EXAHIHATIOH COMPLETED BY V. T. Chilson F: ADHIHISTRATIVE 0: TELEPIIONE (305) 552- 3769 OPERATIONAL ERROR (EXPLAIN) REPORT HOHTH JULY'977 H: OTIIER (EXPLAIN)

PACE 1 OF 2

) HETIIOD 1: HAHUAL . HETIIOD OF 2: .HANUAL SCRAM TYPE SIIUTTINC DOWN 3: AUTOHATIC SCRAH F: FORCED DURATION TIIE REACTOR OR 4: OIIIER (EXPLAIN) NO. DATE S: SCIIEDULED 010URS) REASOH(1) REDUCINC POWER(2) CORRECTIVE ACTIONS/COHHENTS 17 77-07-18 10.7 Unit No. 3 Mas manually tripped due to oil leak in generator seal oil system that could not be isolated.

Corrective actions included replacing failed seal oil system filter. (Non-nuclear system) 18 77-07-19 71.3 Unit No. 3 was removed from service to locate and repair condenser tube leak. (Non-nuclear system) 19 77-07-22 Load reduction to locate and repair condenser tube leak. (Non-nuclear system) 20 77-07-23 1.7 Unit No. 3 was tripped by spurious operation of a relay in the reactor protection system. (Nuclear system)

REASOII APPEHDIX D DOCKET NO. 50 250

)

A: EI)UIPHEIIT FAILURE (EXPLAIN) Turkey Point B: HAINT. OR TEST UHIT SIIUTDOIINS AND POWER REDUCTIOtIS UNIT NhtlC Unit No. 3 C: REFUEI.ING D: IIECULATORY RESTRICTION DATE Au ust 5, 1977 E: Ol'ERATOR TRAIHING AHD LICENSE EXAtlIHATIOH COHPLETED BY V. T. Chilson F: ADIIINISTRATIVE -

G: OPERATIONAI. ERROR (EXPLAIH) TELEPIIOHL'305) 552 3769 H:, OTHER (EXPLAIII)

PAGE 2 OF 2

) HETHOD 1: tIAHllhl. . IIETHOD OF 2: )IAIIUAI, SCRAH TYPE SIIUTTIIIG DOWII 3: AUTOHATIC SCRAH F: FORCbl) DU RATIOtl THE REACTOR OR 4: 0)IIER (EXPLAIN) HO. DATE S: SCHEDULED (IIOURS) REASON(1) REDUCING POltER(2) CORRECTIVE ACTIOIIS/CO)IHENTS 21 77-07-23 7.6 Unit No. 3 @as tripped when the second of two generator breakers'opened while nanually opening a transmission system breaker during a switching operation. Corrective actions included repairing a saalfunctioning generator breaker. (Hon-nuclear systen)

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SUIIHARY) Unit Ho. 3 operated at approxinatcly IOOZ R.P. except for load reduction on July 22, 1977, and outages of July lg, 19-22, 22, and 23> 1977.

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APPEIKLX B AVERAGE DAILY UNIT POWER LEVEL DOCKET NG. 50 251 Turkey Point UNIT Unit No.

DATE Au ust 5 1977 COMPLE~ BY V. T. Chilson HONE (305) 552-3769 MONTH (MWe-Net)

Y DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 17 18 3 19 20 21 6 22 23 24 25 10 26 27 12 28 13 29 30 15 31 16

APPENDL(

DATA REPORT C'PERA";XNG DOCKET NO. 50 - 251 Tur ey Point

. UNIT Unic No. 4 REPORT HONTH JULY, 1977 DA~ August 5, 1977 I

COMPLETED BY V* T. Chilson TELEPHONE (305) 552 3769 OPERATING STATUS

1. REPORTXilG PERIOD: 0001,77 07 01 GROSS HOUPS XN REPORTING PERIOD: 744.0 THROUGH 2400 77
2. CURRENTLY AU HORXEED PQllER LEVEL (AOlc): 2200 6%ZZ DEPEND. CAPACZTY (RDle-Net): 666 DESIGN ELECTRICAL RATING (Nile-N(Ec): 93
3. PO~E LEVEL TO 4HICH RESTRICTED (IF ANY) (A(Ne-Nec): NONE 4.

5 6.

7

~

~

~~ONS FOR RESTRXCTION (XF AZMIESS 87 HOURS REAC OR HAS REACTOR RESERVE SHUTDO'lN HOURS HOURS GENERATOR ON A'lY):

CRZZZCAL.....

~ ~ ~ ~ ~ ~

LINK...................

~ 2~

. THIS HONTH

-0 0 0 2 YEAR TO

-0 496.7 DATAE- ClÃULATXVE

~I

~138.

23 038.8 8 ~ UNiIT RESERVE SHUTDOMA HOURS. ~.......... ~ .. 9. GROSS LLL.'lAL ENERGY GENERATED (.'M!)...... W- 5 424 235 48 483 605

18. CROSS El "CZRZCAL LUEROZ.OLU RII ~" (HHH)... 1 768 385 '~5726 8 8
11. HE ~CZRZCAL LUSRCZ OEIERAZEO (will).....- 3 615 .

2~675 2 6 ~OIRHRg

12. REACTOR SERVICE PACTOR...... 0.2 49.6 70.2
13. REACTOR AVAZLABILZTYFACTOR.... 0.2 49.6 70.6 14 ~ UANIT-SERVICE FACTOR. 0.0 49.1 66.7 15 .lIT AVAILABILITYFACTOR....... ~ . ~ ~ ~ .. ..

~ ~ 0.0 49.1 66.7

16. WZT CAPACITY FA~AR (Using QSC) ... ~ . ~.... 0.0 49.4 64.8
17. UNIT CAPACITY FACTOR (Using Design HNe)... 0.0 47.5
18. UNXT FORCED OUTAGE RATE. ...... ... .. ...

~ ~ ~ 0.0 0.0 19 'HUTDOllNS SCHIZlULED OVER NK:P' HONTHS (TYPE, DATE, AND DURATION OF EACH):

20. ZF SHUTDOQll AT KND OP REPORT PERIOD, KST~AWM DATE OP STA(l~JP: Au st 3 1977
21. UNITS XN I"ST STATUS (PRIOR TO COEKRCXAL OPTATION): FORECAST ACHIZPci)

IiNITIAL CRITXCALZ Y INITIAL ELECTRICITY COi%lKRCLQ. OPERATION

.) REASOII APPENDIX D DOCKET NO. 50 - 251 h: E"<UIPIIENT FAII.URE (EXP Lhltl)

Turkey Point D: Hhitt'T. OR TEST UtIIT SIIUTD(httIS AHU POHER REDUCTIONS UtIIT NAHF. Unit No. 4 C: REFUEI.IHG nt REOULATORY RESTRICTION DATE August 5, 1977 E: OPFRATOR TRAINING AND l.ICEHSE EXAHIHATIOH COtIPLETED DY V. T. Chilson F: ADIIINISTRATIVE TELEPUOIIE (305) 552-3769 G: OPERATIONAL ERROR (EXPLAIN) REPORT tIOtml JULY 1977 Il: OTII FR (EXP IXIII)

) HETIIOD 1: tlhHUAI. . HETHOD OF 2: tlhNUAI. SCRAH TYPE SIIUTTIHC DOMH 3: AUTOtlhTIC SCRAH F: FORCED DURATION THE REACTOR OR 4: OIIIER (EXPLAIH) NO. DATE S: SCIIEDULED (NOUNS) REASON(1) REDUCIHC POWER(2) CORRECTIVE ACTIONS/CO..IHEHTS 77-05-09 7414. 0 Unit llo. 4 uas removed from service for refueling, maintenance, and inspections. {Continued from previous month) (Nuclear and non-nuclear systems)

SUIIHARY- Unit Ho. 4 was out of service for entire month for refueling, maintenance, and inspect'ions.

APPENDIX B AVERAGE DAILY UNXT POWER LEVEL DOCKET NO. 50 -'35 St. Lucie PilIT Unit No. 1 DATE August. 5, 1977 COMPLETED BY V. T. Chilson TELEPHONE (305) 552-3769 MONTH JULY 1977 DAY AVERAGE DAILY POWER LEVEL DAY AVKULGE DAILY POWER L"VEL (Kfe-Net) (MWe-Net) 769 17 779 774 18 779 779 19 780 752 20 783 454 783 773 22 783 780 23 778 270 778 778 25 741 10 600 26 772 524 27 763 12 698 ,28 773 13 481 29 631

'73 30 229 15 722 768 16 758 NOTE Average daily power greater than 777 ice due to cooler condenser cooling water. /

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APPENDS C OPERATZ'.lG DATA R~~ORT DOCKET NO. 50 - 335 t ~ ncie Unit No. 1 REPORT HONZH JULY9 1977 DATE Angst 5, 1977 CONPLETED BY V. T. ChiIson TELEPHONE (305) 552 3769 OPERATX4NG STATUS

1. REPORTING PERIOD: 0001077907901 GROSS HOURS Zil REPORTI.lG PERIOD: 744.0 OUGH 2400 77 0 2~ CURR2'9fTLY Al42THORZZED P09~q LEVEL (989gt) . 2560 DESIGN ELECTRICAL RATING (HWe-Net): '802
3. POWaR LEVEL TO 'riHZCH RESTRICic9 (XF AilY) (94Ãe-Het): NONE REASONS FOR RESTRICTION {IF <Vr):

THIS 4HONTH YEAR TO DATE CUNULATZVE

5. NU44BERS OF HOURS BM~CTOR WAS CRITICAL...,, 735 ~ 3 4 344.4 ~4 HOURS............ 8.7 ~0

~...

6. REACTOR RESERVE ShODOWN 101. 8
7. HOURS Gc~RATOR ON LLlE.. ~... ~ 689.4 4 137.9 4 401 9 8- UNZT RESERVE SHUTDOWN HOURS. ~ ~ - ~ ~ ~ ~ ~ ~ ~ ~ ~ . ~ -0 9. GROSS THERl8~ ENERGY G~ci 2 TlU) (HllH) ~..... 1 705 667
10. GROSS ELECTRICAL ENERGY Gc lERATED (944H)...
11. NET ELECTRICAL ENERGY GESF'lATED (iSHH)...,. 518 560 2 823 148 2~92
12. ACTOR SERVICE FACTOR. 98.8 85.4 86.1
13. REACTOR AVAZLABILZTY FACTOR......,........ 100. 0 87.4 14 'Ni XT SERVICE FACTOR. 92. 7 81.3 15 ~ UNIT AVAILABILITYFACTOR...,.....,,....... 92.7 81. 3
16. lD{IT CAPACZT FACTOR (Using,(NDC) ........ 89 ' 71.4 70.3
17. UNIT CAPACITY FACTOR {Using Design HWe)... 86.9 69.2 18 'NXT FORCED OUTAGE RATE. . ~ ~ ~ ~ ~ ~ ~ ~ 1.6 16.8 16.0 19 ~ SHUTDOWN48 SCHEDULED OVER NEET 6 HONTHS ('JJPE 9 DAT 9 AND DURATXON OF EACH)

Warzanty Inspection - Septet2ber 26 to October 10, 1977. 'zelininary

20. iF SHUTDOWNi AT RQ OF REPORT PERIOD> ESTZQTED DATE OF STARTUP:

21 ~ UNITS Dl T.ST STATUS (PRIOR TO CO48rr'lCZAL OPMATIO4Q: FORECAST ACHIEVED ZiXTZAL CRXTICALITY INITIAL ELECTRICIT CO4 lERCL4L OPERATION

.) REASON APPENDIX D DOCKET NO. 50 - 335 h: EQUIPHF&f FAILURE (EXPLAIN) St. Lucio D: NAINT. OR TEST UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT HANE Unit No.

C: REFUELllt0 D: REGULATORY RESTRICTION DATE Au ust 5 197 E: OPERATOR TRAIHIHC AHD I.ICENSE EXAHIHATIOH COllPLETED DY V. T. Chilson F: AlkllNISTRATIVE G: OPERATIOHhl. ERROR (EXPLAIN) TELEPHONE 305 552-3769 H: OTHER (EXPLAIN)

PAGE 1 OF 2

') IIETIBD I: MANUAL . NETilOD OF 2: HANUAf. SCRAH TYPE SIIUTTINC DOWN 3: AUTOHATIC SCRAN F: FORCED DURATION TIIE REACTOR OR 4: OIIIER (EXPLAIN) NO. DATE S: SCHEDULED (I10URS) REASON(1) REDUCIHC POWER(2) CORRECTIVE ACTIONS/COHNENTS 26 77-07-04 8.1 Unit was removed from service to repair packing leak on pressurizer spray valve. (Nuclear system) 27 77-07-08 11.0 Unit was removed from service to repair failed pres-surizer spray valves. (Nuclear system) 28 77-07-10 10. 1 Unit was removed from service for maintenance of pres-surizer spray vplve. (Nuclear system)

.) RFJlSON APPENDIX D DOCKET HO. 50 - 335 h: EqUIPMENT Fhll.URP. (EXPIAIN) St. Lucie 8: MAIHT. OR TEST UNIT SHUTDOWNS AND POWER REDUCTIONS WHIT HAIIE Unit No. 1 C: REFUL'l.l NC D: REGULATORY RESTRICTIOH DATE August 5, 1977 E: 01'ERATOR TRAININC AND I.ICFNSE EXAMINATION COHPLETED BY V. T. Chilson F: ADMINISTRATIVE C: OPERATIONAl. ERROR (EXPLAIN) TELEPllOHE 305 552-3769 Il: OTHER (EXPLAIN)

PACE 2 OF 2

) METIIOD I: IIANUhl. . METllOD OF 2: .MANUhl, SCRAM TYPE SIIUTTINC DOWN 3: AUTOHATIC SCRAM F: FORCED DURATION TNE REACTOR OR 4: OIIIER (EXPLAIN) NO. DATE S: SCHEDULED (lIOURS) REASON(1) REDUCINC POWER(2) CORRECTIVE ACTIONS/COMMENTS 29 77-07-12 8.1 Unit was removed from service to install the repaired alternate pressurizer spray valve. (Nuclear system) 30 77-07-29 17. 2 Unit uas removed from service to install modified pressurizer spray valve assembly. (Nuclear system)

SUMllhRY: Unit operated at approximately IOOX R.P. except for outages of July 4-5, 8, 10-11, 12-13, and 29-30, 1977.

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