IR 05000456/2007005

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IR 05000456-07-005, on 05000457/2007005; 07/01/2007 - 09/30/2007 for Braidwood Station, Units 1 & 2; Refueling and Other Outage Activities
ML073170645
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 11/13/2007
From: Richard Skokowski
Region 3 Branch 3
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
FOIA/PA-2010-0209 IR-07-005
Download: ML073170645 (44)


Text

November 13, 2007Mr. Christopher M. CranePresident and Chief Nuclear Officer Exelon Nuclear Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555SUBJECT:BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTIONREPORT 05000456/2007005; 05000457/2007005

Dear Mr. Crane:

On September 30, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed anintegrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection results, which were discussed on October 11, 2007, with Mr. T. Coutu and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, one NRC-identified finding of very low safetysignificance was identified. The finding involved a violation of NRC requirements. However, because of its very low safety significance, and because the issue was entered into your corrective action program, the NRC is treating the issue as a Non-Cited Violation in accordance with Section VI. A. of the NRC Enforcement Policy.If you contest the subject or severity of a finding, you should provide a response within 30 daysof the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood Station.

C. Crane-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and itsenclosure will be made available electronically for public inspection in the NRC PublicDocument Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/Richard A. Skokowski, ChiefBranch 3 Division of Reactor ProjectsDocket Nos. 50-456; 50-457License Nos. NPF-72; NPF-77Enclosure:Inspection Report 05000456/2007005;and 05000457/2007005 w/Attachment: Supplemental Informationcc w/encl:Site Vice President - Braidwood StationPlant Manager - Braidwood Station Regulatory Assurance Manager - Braidwood Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director Licensing Manager Licensing - Braidwood and Byron Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer Chairman, Illinois Commerce Commission

SUMMARY OF FINDINGS

IR 05000456/2007005, 05000457/2007005; 07/01/2007 - 09/30/2007; Braidwood Station,Units 1 & 2; Refueling and Other Outage Activities.This report covers a three-month period of inspection by resident inspectors and announcedbaseline inspections by regional inspectors. One Green finding was identified by the inspectors. The finding was considered a Non-Cited Violation of NRC regulations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Barrier Integrity

Green.

A finding of very low safety significance and associated Non-Cited Violation ofTechnical Specification 5.4.1 was identified by the inspectors for failure to have and follow procedures, which met the surveillance requirements of Technical Requirements Manual (TRM), Section 3.9.d.1. Specifically to verify that both the spent fuel pool crane electrical interlocks and physical stops were operable, with the purpose to prevent crane travel with loads greater than 2000 pounds over fuel assemblies. This was required to be completed within seven days prior to crane use. The inspectors identified that loads greater than 2000 pounds were regularly moved with the crane with the electrical interlocks bypassed and the physical stops removed.The finding was greater than minor because, if left uncorrected, it could have becomemore significant as additional heavy loads were moved with no interlocks in place. The finding affected the attribute of maintaining functionality of spent fuel cladding in the Barrier Integrity cornerstone. Using the SDP Phase 1 Screening Worksheet of IMC 0609, the inspectors determined that the finding screened as Green because it only affected the fuel barrier. The licensee entered the issue into its corrective action program, temporarily suspended crane operation, and modified its procedures and practices to meet the TRM. The finding had a cross-cutting aspect in the area of Human Performance in the work practices component. Personnel failed to follow the TRM because implementing procedures did not require both the electrical interlocks and physical stops to be in place within seven days prior to crane use (H.4(b)).

(Section 1R20)

B.Licensee-Identified Violations

None.

2

REPORT DETAILS

Summary of Plant StatusUnit 1 was operated at or near full power until September 15, 2007, when a gradual powercoastdown was initiated in preparation for a refueling outage. On September 30, 2007, Unit 1 was shutdown from about 94 percent power and the generator taken off line for the refueling outage.Unit 2 was operated at or near full power until a manual reactor trip was initiated due to loss ofcondenser vacuum on August 23, 2007. The unit was brought critical on August 24 and synchronized to the grid on August 25. Unit 2 reached full power on August 28, 2007, and remained at or near full power for the rest of the inspection period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01)Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

The inspectors monitored and reviewed the licensee's overall preparations forimpending severe thunderstorm, high wind, and hot temperature conditions that occurred several times during the inspection period. The inspectors conducted several walkdowns of the offsite power transformers and onsite transmission tower areas, monitored cooling lake temperature and level, and reviewed licensee procedures for coping with the conditions. The inspectors also monitored the daily scheduling of surveillance and other work activities to ensure that the additional risk from pending severe weather was taken into account. The inspectors verified that minor issues identified during the inspection were entered into the licensee's corrective action program. Documents reviewed during this inspection are listed in the Attachment.This inspection constituted one sample of the inspection requirement for site readinessfor impending adverse weather conditions.

b. Findings

No findings of significance were identified.

31R04Equipment Alignment (71111.04).1Partial Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the accessible portions of risk-significantsystem trains during periods when the train was of increased importance due to redundant trains or other equipment being unavailable. The inspectors utilized the valve and electric breaker checklists to determine whether the components were properly positioned and that support systems were aligned as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to determine whether there were any obvious deficiencies. The inspectors reviewed Issue Reports (IRs) associated with the train to determine whether those documents identified issues affecting train function. The inspectors used the information in the appropriate sections of the Technical Specifications (TS) and the Updated Final Safety Analysis Report (UFSAR) to determine whether the licensee had maintained the functional requirements of the system. The inspectors also reviewed the licensee's identification of and controls over the redundant risk-related equipment required to remain in service. The inspectors verified that minor issues identified during the inspection were entered into the licensee's corrective action program. Documents reviewed during this inspection are listed in the Attachment.The inspectors completed three samples of the quarterly requirement by walkdowns ofthe following trains:*1B containment spray (CS) system train in preparation for a 1A CS work window;*1A safety injection (SI) system train in preparation for a 1B SI work window; and

  • 2B diesel generator (DG) during emergent work on the 2A DG.

b. Findings

No findings of significance were identified..2Complete Walkdown

a. Inspection Scope

The inspectors performed a complete walkdown of the Unit 2 essential service water(SX) system. The SX system was chosen due to its high risk significance at Braidwood Station. In addition to walkdowns, the inspectors reviewed the following documentation to verify that the system was properly maintained in accordance with design basis documents:*selected operating procedures regarding system configuration;*the UFSAR, system drawings, and other selected design bases documentsregarding the system; and*IRs for the system initiated within the last year.

4The inspectors verified that minor issues identified during the inspection were enteredinto the licensee's corrective action program. Documents reviewed during the inspection are listed in the Attachment. This inspection represented one sample of the semiannual requirement.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05).1Quarterly Inspection

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events. Also reviewed was the revised Individual Plant Examination of External Events, which contained additional insights on selected fire areas that impact equipment potentially causing plant transients, or adversely affecting safe shutdown capability. The inspectors used the Fire Protection Report, Revision 22, to determine: that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.The inspectors completed eight samples of the quarterly inspection requirement duringthe following walkdowns:*Unit 1 auxiliary feedwater tunnel (Zone 18.3-1);*Unit 1 auxiliary building 451 and 467 foot elevations (Zone 11.7-1);

  • Unit 2 auxiliary building 451 and 467 foot elevations (Zone 11.7-2);
  • Unit 1 auxiliary building 383 foot elevation (Zone 11.4-1);
  • Unit 2 auxiliary building 383 foot elevation (Zone 11.4-2);
  • Unit 1 upper cable spreading room (Zone 3.3A-1,2);
  • Unit 2 upper cable spreading room (Zone 3.3B-1,2); and
  • fuel handling building (Zone 12.1-0).The inspectors verified that minor issues identified during the inspection were enteredinto the licensee's corrective action program. Documents reviewed during this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

5.2Annual Inspection of Fire Brigade Performance

a. Inspection Scope

The inspectors observed the licensee's fire brigade response to several simulated firesin conjunction with the 2007 Threat Based Scenario Full Scale Exercise. The fire drill portion of the scenario included fighting multiple fires, coordination with multiple offsite fire departments and other responders, and coordination with the licensee's Emergency Response Organization. The scenario also included use of the alternate fire brigade equipment area outside of the power block, simulated use of alternate fire suppression water supplies, and simulated use of fire protection equipment for supplemental spent fuel pool cooling. The inspector's evaluation included the following criteria:*proper number of fire brigade members, including a brigade leader, responded;*protective equipment, including self-contained breathing apparatus, was donnedproperly;*adequate fire fighting equipment was brought to the scene;

  • command and control, communications, and procedure usage was appropriate;
  • checks for victims and fire propagation were conducted;
  • attacks on the fire were conducted in accordance with training and procedures;
  • drill objectives were met; and
  • a critique was conducted in which any deficiencies identified by the inspectorswere also identified and discussed by the licensee evaluators or participants.The inspectors verified that minor issues identified during this inspection were enteredinto the licensee's corrective action program. This inspection constituted one sample of the annual requirement. Documents reviewed as part of this inspection are listed in the

.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06)External Flood Protection Features

a. Inspection Scope

The inspectors reviewed Braidwood's flood analysis and design basis documents toidentify design features important to flood protection, and flood protection measures in place to prevent or mitigate effects of external flooding. For this sample, the inspectors focused on areas susceptible to ground water intrusion following a significant rain event, in particular the 377 foot elevation of the steam tunnels, and the 346 foot elevation residual heat removal and CS pump rooms in the auxiliary building. The inspectors examined the room walls and ceilings, leak detection sumps, normal sumps, and the effectiveness of the auxiliary building floor drains. This review represented one annual inspection sample. Documents reviewed during this inspection are listed in the

.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors observed flow measurement, setting, and flushing of service water to theUnits 1 and 2 component cooling heat exchangers and safety-related cubicle coolers.

This testing was completed in accordance with the licensee's Generic Letter 89-13 program. The inspectors determined whether there were any significant flow degradations or adverse trends in performance of the heat exchangers observed. This inspection was completed during a time of high heat sink temperature due to a period of hot summer weather. The inspectors also reviewed the most recent surveillance which measured the depth of the SX cooling basin (ultimate heat sink) to determine whether it still met the original design depth assumed in the UFSAR. Documents reviewed during this inspection are listed in the Attachment. This inspection represented two annual

samples.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11).1Facility Operating History

a. Inspection Scope

The inspectors reviewed the plant's operating history from July 2005 through July 2007to identify operating experience that was expected to be addressed by the Licensed Operator Requalification Training (LORT) program. The inspectors assessed whether the identified operating experience had been addressed by the facility licensee in accordance with the station's approved Systems Approach to Training (SAT) program to satisfy the requirements of 10 CFR 55.59(c), "Requalification Program Requirements." bFindingsNo findings of significance were identified..2Licensee Requalification Examinations

a. Inspection Scope

The inspectors performed a biennial inspection of the licensee's LORT test/examinationprogram for compliance with the station's SAT program which would satisfy the requirements of 10 CFR 55.59(c)(4), "Evaluation." The inspectors reviewed operating examination material consisted of seven operating tests, each containing two or four 7dynamic simulator scenarios (as appropriate) and ten job performance measures(JPMs). The seven written examinations reviewed consisted of a Section A, Plant and Control Systems, administered using a static simulator, and a Section B, Administrative Controls/Procedure Limits, administered in a classroom. The Section A consisted of 15 questions, and Section B, 20 questions. The senior reactor operator (SRO)

Section A examination contained a minimum of one SRO level question, and the Section B examination, three SRO level questions. The inspectors reviewed the annual requalification operating test and biennial written examination material to evaluategeneral quality, construction, and difficulty level. The inspectors assessed the level of examination material duplication from week-to-week during the current year operating test. The examiners assessed the amount of written examination material duplication from week-to-week for the written examination administered in 2006. The inspectors reviewed the methodology for developing the examinations, including the LORT program two year sample plan, probabilistic risk assessment insights, previously identified operator performance deficiencies, and plant modifications.

b. Findings

No findings of significance were identified..3Licensee Administration of Requalification Examinations

a. Inspection Scope

The inspectors observed the administration of a requalification operating test toassess the licensee's effectiveness in conducting the test to ensure compliance with 10 CRF 55.59(c)(4), "Evaluation." The inspectors evaluated the performance of two crews in parallel with the facility evaluators during four dynamic simulator scenarios.

The inspectors also evaluated various licensed crew members concurrently with facility evaluators during the administration of several JPMs. The inspectors assessed the facility evaluators' ability to determine adequate crew and individual performance using objective, measurable standards. The inspectors observed the training staff personnel administer the operating test, including conducting pre-examination briefings, evaluations of operator performance, and individual and crew evaluations upon completion of the operating test. The inspectors evaluated the ability of the simulator to support the examinations. A specific evaluation of simulator performance was conducted and documented under Section 1R11.8, "Conformance With Simulator Requirements Specified in 10 CFR 55.46," of this report.

b. Findings

No findings of significance were identified..4Examination Security

a. Inspection Scope

The inspectors observed and reviewed the licensee's overall licensed operatorrequalification examination security program related to examination physical security 8(e.g., access restrictions and simulator considerations) and integrity (e.g., predictabilityand bias) to verify compliance with 10 CFR 55.49, "Integrity of Examinations and Tests."

The inspectors also reviewed the facility licensee's examination security procedure, any corrective actions related to past or present examination security problems at the facility, and the implementation of security and integrity measures (e.g., security agreements, sampling criteria, bank use, and test item repetition) throughout the examination process.

b. Findings

No findings of significance were identified..5Licensee Training Feedback System

a. Inspection Scope

The inspectors assessed the methods and effectiveness of the licensee's processes forrevising and maintaining its LORT Program up to date, including the use of feedback from plant events and industry experience information. The inspectors reviewed the licensee's quality assurance oversight activities, including licensee training department self-assessment reports. The inspectors evaluated the licensee's ability to assess the effectiveness of its LORT program and their ability to implement appropriate corrective actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c),

"Requalification Program Requirements" and the licensee's SAT program.

b. Findings

No findings of significance were identified..6Licensee Remedial Training Program

a. Inspection Scope

The inspectors assessed the adequacy and effectiveness of the remedial trainingconducted since the previous biennial requalification examinations and the training fromthe current examination cycle to ensure that they addressed weaknesses in licensed operator or crew performance identified during training and plant operations. The inspectors reviewed remedial training procedures and individual remedial training plans. This evaluation was performed in accordance with 10 CFR 55.59(c), "Requalification Program Requirements" and with respect to the licensee's SAT program.

b. Findings

No findings of significance were identified.

9.7Conformance With Operator License Conditions

a. Inspection Scope

The inspectors reviewed the facility and individual operator licensees' conformance withthe requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's program for maintaining active operator licenses and assessment of compliance with 10 CFR 55.53(e) and (f). The inspectors reviewed the licensee's procedural guidance and process for tracking on-shift hours for licensed operators, and which control room positions were granted watch-standing credit for maintaining active operator licenses.

The inspectors reviewed the facility licensee's LORT program to assess compliance with the requalification program requirements as described by 10 CFR 55.59(c). In addition, medical records for ten licensed operators were reviewed for compliance with 10 CFR 55.53 (i).

b. Findings

No findings of significance were identified..8Conformance with Simulator Requirements Specified in 10 CFR 55.46

a. Inspection Scope

The inspectors assessed the adequacy of the licensee's simulation facility (simulator) foruse in operator licensing examinations and for satisfying experience requirements as prescribed in 10 CFR 55.46, "Simulation Facilities." The inspectors also reviewed a sample of simulator performance test records (i.e., transient tests, malfunction tests, steady state tests, and core performance tests), simulator discrepancies, and the process for ensuring continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy process to ensure that simulator fidelity was maintained. Open simulator discrepancies were reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator actions as well as on nuclear and thermal hydraulic operating characteristics. The inspectors conducted interviews with members of the licensee's simulator staff about the configuration control process and completed the Inspection Procedure 71111.11, Appendix C, checklist to evaluate whether or not the licensee's plant-referenced simulator was operating adequately as required by 10 CFR 55.46(c) and (d).

b. Findings

No findings of significance were identified..9Annual Operating Test Results and Biennial Written Examination Results

a. Inspection Scope

The inspectors reviewed the pass/fail results of the 2006 individual biennial writtenexaminations, and the annual operating tests (required to be given annually per 10 CFR 55.59(a)(2)) administered by the licensee during calendar year 2007. The 10overall written examination and operating test results were compared with thesignificance determination process in accordance with NRC Manual Chapter 0609, Appendix I, "Operator Requalification Human Performance Significance Determination

Process."Sections 1 through 9 discussed above together constituted one sample of the biennialinspection requirement.

b. Findings

No findings of significance were identified..10Quarterly Review of Testing/Training Activity

a. Inspection Scope

The inspectors observed operating crew performance during a graded out-of-the-boxsimulator set. Details of the scenarios used are withheld due to exam security considerations.The inspectors evaluated crew performance in the following areas:

  • clarity and formality of communications;*ability to take timely actions in the safe direction;
  • prioritization, interpretation, and verification of alarms;
  • procedure use;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • group dynamics.Crew performance in these areas was compared to licensee management expectationsand guidelines.The inspectors verified that the crew completed the critical tasks listed in the simulatorguide. The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed the licensee evaluators to determine whether they also noted the issues and discussed them in the critique at the end of the session. Documents reviewed are listed in the Attachment.

This review constituted one sample of this inspection requirement.

b. Findings

No findings of significance were identified.

111R12Maintenance Effectiveness (71111.12)Routine Inspection

a. Inspection Scope

The inspectors reviewed the licensee's overall maintenance effectiveness for selectedplant systems. This evaluation consisted of the following specific activities:*observing the conduct of planned and emergent maintenance activities where possible;*reviewing selected IRs, open work orders, and control room log entries in orderto identify system deficiencies;*reviewing licensee system monitoring and trend reports;

  • attending various meetings throughout the inspection period where the status ofmaintenance rule activities were discussed;*conducting partial walkdowns of the selected system; and
  • interviewing appropriate system engineers.The inspectors also reviewed whether the licensee properly implemented MaintenanceRule, 10 CFR 50.65, for the affected systems. Specifically, the inspectors determined whether:*the system was scoped in accordance with 10 CFR 50.65;*performance problems constituted maintenance rule functional failures;
  • the system had been assigned the proper safety significance classification;
  • the system was properly classified as (a)(1) or (a)(2); and
  • the goals and corrective actions for the system were appropriate.The above aspects were evaluated using the maintenance rule program and otherdocuments listed in the Attachment. The inspectors also verified that the licensee was appropriately tracking reliability and/or unavailability for the systems. Documents reviewed in this inspection are listed in the Attachment.The inspectors completed two samples in this inspection requirement by reviewing thefollowing systems and equipment performance issues:*main steam system [(a)(1) system]; and*feedwater system [(a)(1) system].

b. Findings

No findings of significance were identified.

121R13Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's management of plant risk during emergentmaintenance activities or during activities where more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety-significant equipment. The inspectors verified that the evaluation, planning, control, and work in progress met the requirements of 10 CFR 50.65, "Maintenance Rule." Specifically, the inspectors verified that the equipment was identified and controlled where appropriate, work was being conducted properly, and significant aspects of plant risk were being communicated to the necessary personnel.Documents reviewed during this inspection are listed in the Attachment.

The inspectors completed six samples by reviewing the following activities:

  • emergent work for leak on 15B feedwater heater shell drain tank relief;*emergent work for Unit 1 control rod urgent failure;
  • emergent work due to a trip on the 1B DG with severe weather in the vicinity;
  • planned work on 1B SI pump with the Unit 0 service air compressor out ofservice;*emergent work due to 2A DG slow start; and
  • emergent work due to Unit 1 containment emergency hatch local leak rate test(LLRT) failure.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors evaluated plant conditions and selected IRs for risk-significantcomponents and systems in which operability issues were questioned. These conditions were evaluated to determine whether the operability of components was justified. The inspectors compared the operability and design criteria in the appropriate section of the UFSAR to the licensee's evaluations presented in the IRs and other documents to verify that the components or systems were operable. The inspectors also conducted interviews with the appropriate licensee system engineers and conducted plant walkdowns, as necessary, to obtain further information regarding operability questions. Documents reviewed as part of this inspection are listed in the

.The inspectors completed four samples by reviewing the following operabilityevaluations and conditions:

13*refueling water storage tank vortexing concerns;*steam generator relief valve capacity to maintain margin-to-overfill during asteam generator tube rupture casualty; *2B DG field flash problem; and

  • non-conservatism in steam generator tube rupture methodology regarding decayheat.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17)Annual Review.1Unit 1 Digital Electro-Hydraulic Main Turbine Controls

a. Inspection Scope

The inspectors continued with design reviews and limited observations of the Unit 1Digital Electro-Hydraulic Controls upgrade project during this inspection period. The inspection activities during this inspection period consisted mainly of attendance at aPlant Operating Review Committee meeting where operating characteristics were reviewed and observing operators use the new controls on the simulator. Cable termination and system testing will be completed during future inspection periods and the NRC inspection activities will continue. This activity was not considered a completed inspection sample. Documents reviewed as part of this inspection are listed in the

.

b. Findings

No findings of significance were identified..2Installation of the 500,000 Gallon Radwaste Storage Tank

a. Inspection Scope

The inspectors observed various phases of the construction of a new 500,000 gallonradwaste storage tank designed to reduce the amount of tritiated water to be released to the environment. The inspection activities included construction observations, drawing and safety evaluation reviews and attendance at several Plant Operating Review Committee meetings where the tank was discussed. Although the project was not quite finished by the end of the inspection period, the activity is considered a complete inspection sample. Documents reviewed as part of this inspection are listed in the

.

b. Findings

No findings of significance were identified.

141R19Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed post-maintenance testing activities associated with importantmitigating systems, barrier integrity, and support systems to ensure that the testing adequately demonstrated system operability and functional capability. The inspectors used the appropriate sections of the TS and UFSAR, as well as work orders for work performed, to evaluate the scope of the maintenance and to determine whether the post-maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. The inspectors determined whether the tests were conducted in accordance with licensee procedures, including establishing the proper plant conditions and prerequisites, that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. The activities were selected based on their importance in demonstrating mitigating systems capability and barrier integrity. The inspectors verified that minor issues identified during the inspection were entered into the licensee's corrective action program. Documents reviewed as part of this inspection are listed in the Attachment.Six samples were completed by observing post-maintenance testing of the followingcomponents:*Exelon pond pump operation following flow totalizer repair;*1A CS pump following planned maintenance;

  • 1B DG following repair of control air line leak;
  • 0B diesel-driven fire pump following planned maintenance;
  • 2A reactor containment fan cooler following planned maintenance; and
  • 2A DG following governor actuator replacement.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20)

a. Inspection Scope

The inspectors observed several activities associated with receipt, inspection, andstorage of new fuel in preparations for the Unit 1 refueling outage scheduled for October 2007. The inspectors verified that minor issues identified during the inspection were entered into the licensee's corrective action program. Documents reviewed as part of this inspection are listed in the Attachment. This inspection covered only refueling preparations and the remainder of the refueling activities will be inspected in the next quarter. Thus, this inspection does not represent a completed sample.

b. Findings

Introduction:

The inspectors identified a Non-Cited Violation (NCV) of TS having a verylow safety significance (Green) for the licensee reactor services personnel failing to 15have and follow procedures, which met the requirements of the Technical RequirementsManual (TRM) to verify that crane interlocks and physical stops prevent spent fuel building crane travel with loads greater than 2000 pounds over fuel assemblies.Description: On July 16, 2007, the inspectors observed licensee reactor servicespersonnel perform 0BwOS TRM 3.9.d.1, a procedure that implemented TRM surveillance requirement 3.9.d.1 to test the spent fuel building crane electrical interlocks and mechanical stops within seven days prior to crane use. The inspectors noted that the personnel did not complete the entire procedure before moving loads, which included loads greater than 2000 pounds. The inspectors later discussed the observation with the fuel handling supervisor and others and ascertained that:*the crane's electrical interlocks were installed in a position that prevented thecrane from traveling from the new fuel canister unloading mezzanine to the new fuel storage vaults;*in order to move new fuel to the new fuel storage vaults, the personnel regularlyoperated with the electrical crane interlocks bypassed;*the electrical interlocks were usually bypassed continuously when performingnew fuel operations, even when moving loaded fuel shipping canisters weighinggreater than 2000 pounds;*the crane's mechanical stops, which would prevent crane movement over allexcept a small portion of the spent fuel pool, had been removed for several years; and*licensee procedures were written to allow operation of the crane withoutinterlocks and stops, contrary to the requirements in the TRM.Thus, loads of greater than 2000 pounds were being moved in the spent fuel building bythe crane with neither the electrical interlocks or mechanical stops in place. In addition to being required by the TRM, the interlocks and stops were described in the UFSAR and the licensee's response to NUREG 0612, "Control of Heavy Loads at Nuclear Power Plants."Licensee corrective actions included temporarily suspending crane operations in thespent fuel pool building, conducting a thorough review of the licensing and design basis for the various interlocks and heavy loads control program, installing the physical crane stops, and suspending the practice of moving the loaded new fuel shipping containers with the electrical crane interlocks bypassed. The licensee also changed the TRM to allow movement of heavy loads, with the exception of fuel casks, with only one of the motion control methods in place. These and other corrective actions were being tracked by IR 651354.Analysis: Although the inspectors did not observe the personnel actually move anyheavy loads over the spent fuel pool, operating the crane without the interlocks and stops could increase the probability of an accident involving damage to spent fuel due to a crane malfunction or human error. The inspectors concluded that the issue was a performance deficiency involving a challenge to barrier integrity warranting a significance evaluation. The finding was greater than minor because, if left uncorrected, it could have become more significant as additional heavy loads were moved with no interlocks in place. The finding affected the attribute of maintaining functionality of 16spent fuel cladding in the Barrier Iintegrity cornerstone. Using the SDP Phase 1Screening Worksheet of Inspection Manual Chapter (IMC) 0609, the inspectors determined the finding screened as Green because it only affected the fuel barrier. The finding had a cross-cutting aspect in the area of Human Performance in the work practices component. Personnel failed to follow the TRM because implementing procedures did not require both the electrical interlocks and physical stops to be in place within seven days prior to crane use (H.4(b)). For example, Procedures 0BwOS TRM 3.9.d.1, OU-AP-200, and BwMP 3300-024 all had steps and acceptance criteria that allowed either the interlocks or stops to be operable, but not necessarily both. In addition, even though procedures required at least one of the two control methods be operable, it was the practice of the fuel handlers to operate the crane, including lifting heavy loads, with neither operable.Enforcement: Technical Specification 5.4.1 required that written procedures beestablished, implemented, and maintained covering the areas recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Section 2.k of Appendix A of the Guide required procedures for preparation for refueling and refueling equipment operation. This requirement was partially implemented by TRM Surveillance Requirement 3.9.d.1, which required that the licensee verify that crane interlocks and physical stops prevent crane travel with loads greater than 2000 pounds over spent fuel assemblies. Contrary to this, on July 16, 2007, and on numerous instances before that date, the licensee operated the spent fuel building crane with loaded fuel shipping canisters weighing greater than 2000 pounds without verifying that interlocks and physical stops were in place. In fact, the interlocks were bypassed and the physical stops were not installed. TRM Section 1.5.c stated that violations of the surveillance requirements shall be treated the same as plant procedure violations. Because this violation was of very low safety significance and it was entered into the licensee's corrective action program, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000456/2007005-01; 05000457/2007005-01).

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed surveillance testing activities associated with importantmitigating systems, barrier integrity, and support systems to ensure that the testing adequately demonstrated system operability and functional capability. The inspectors used the appropriate sections of the TS and UFSAR to determine whether the surveillance testing was performed adequately and that operability was restored. The inspectors determined whether the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. Activities were selected based on their importance in demonstrating Mitigating Systems Capability, Barrier Integrity and the Initiating Events cornerstones. Documents reviewed as part of this inspection are listed in the Attachment.

17Five samples were completed by observing and evaluating the following surveillance tests:*1A auxiliary feedwater pump American Society of Mechanical Engineers test(inservice test);*2A DG monthly surveillance (routine);

  • Unit 1 solid state protective system bi-monthly surveillance (routine);

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the installation of temporary modifications that could affect theoperability of risk significant equipment, the probability of an initiating event, or an unauthorized radioactive material discharge. For each temporary modification, the inspectors reviewed the associated design change documentation, performed a walkdown of the installation, and reviewed the affected TS and UFSAR sections. The inspectors also reviewed the licensee's plans and schedules for removing the temporary modification or making it permanent. Documents reviewed during this inspection are listed in the Attachment. This review constituted two samples of this inspection requirement. The following modifications were reviewed:*Engineering Change 366773; Gag Closed Relief Valve 1DV021B and Lock OpenValve 1HD014B - allow inflatable plug to be installed in 0TE63AB-6; and*leakrate monitoring collar installation on 2SX27DA-10 (SX piping).

b. Findings

No findings of significance were identified.Cornerstone: Emergency Preparedness1EP6Drill Evaluation (71114.06)

a. Inspection Scope

The inspector observed the licensee performance during an operations crewout-of-the-box examination scenario on the simulator. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-drill critiques for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the drill performance and ensure that the licensee evaluators noted the same issues and entered them into the corrective 18action program.

As part of the inspection, the inspectors reviewed the scenariopackage and other documents listed in the Attachment. This review represented one inspection sample.

b. Findings

No findings of significance were identified.2.RADIATION SAFETYCornerstone: Public Radiation Safety 2PS1Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems (71122.01)Review of Blowdown Line Operations and Tritium Remediation Efforts

a. Inspection Scope

The inspectors continued to monitor the licensee's activities resulting from previousinadvertent leaks of tritiated liquid from the blowdown line to the Kankakee River. The inspection activities included the following:*periodic inspections of all vacuum breaker vaults;*periodic inspections of remediation system pump operations at the Exelon Pondand vacuum breaker 1;*installation of a third remediation system on the west side of the turbine building;

  • efforts to reduce tritium concentrations in secondary plant systems; and
  • participation in Community Information Meetings.In addition, the inspectors instituted a program to accompany licensee employees andcontractors during their collection of water samples at 23 monitoring locations of interest. The inspectors verified by direct observation that the water samples were being taken from the locations specified, that proper sampling protocols were followed, and that split samples were properly obtained and labeled. The inspectors took direct custody of the split samples and maintained a chain of custody as the samples were sent to the U.S. Government's contract laboratory in Oak Ridge, Tennessee. The inspectors also reviewed the results of earlier split samples to ensure that the results from the licensee's and NRC's contract laboratories matched within normal statistical variance.The inspectors verified that minor issues identified during these inspection activitieswere entered into the licensee's corrective action program. Documents reviewed are listed in the Attachment. This inspection did not represent a completed inspection

sample.

b. Findings

No findings of significance were identified.

192PS3Radiological Environmental Monitoring Program (REMP) and Radioactive MaterialControl Program (71122.03).1

Inspection Planning

a. Inspection Scope

The inspectors reviewed the most current annual Radiological Environmental Operating Report (REMP), dated May 14, 2007, and licensee assessment results to evaluate if the REMP was implemented as required by the Radiological Effluent Technical Specifications (RETS) and the Offsite Dose Calculation Manual (ODCM). The inspectors reviewed the report for changes to the ODCM with respect to environmental monitoring and commitments in terms of sampling locations, monitoring and measurement frequencies, land use census, interlaboratory comparison program, and data analysis.

The inspectors reviewed the ODCM to identify environmental monitoring stations and evaluated licensee self-assessments, audits, licensee event reports, and inter-laboratory comparison program results. The inspectors reviewed the UFSAR for information regarding the environmental monitoring program and meteorological monitoring instrumentation. The inspectors also reviewed the scope of the licensee's audit program to determine if it met the requirements of 10 CFR 20.1101(c). This review represented one sample. Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified..2Onsite Inspection

a. Inspection Scope

The inspectors walked down selected air sampling stations (greater than 20 percent) andapproximately five percent of the thermoluminescent dosimeter monitoring stations to determine whether they were located as described in the ODCM and to determine the equipment material condition.The inspectors observed the collection and preparation of a variety of environmentalsamples including drinking water, surface water, and air. The environmental sampling program was evaluated to determine if it was representative of the release pathways as specified in the ODCM and if sampling techniques were performed in accordance with station procedures.The inspectors evaluated the condition of the meteorological instruments, using observations and record reviews, and assessed whether the equipment was operable, calibrated, and maintained in accordance with guidance contained in the UFSAR, NRC Safety Guide 23, and licensee procedures. The inspectors assessed whether the meteorological data readout and recording instruments, including computer interfaces and data loggers that measure and record wind speed, wind direction, delta temperature, and atmospheric stability measurements, were available on the licensee's computer system and whether this information was available in the control room.

20The inspectors reviewed each event documented in the Radiological EnvironmentalOperating Report that involved missed samples, inoperable samplers, lost thermoluminescent dosimeters, or anomalous measurements for the cause and corrective actions.The inspectors reviewed the ODCM for significant changes that resulted from land usecensus modifications, or sampling station changes made since the last inspection.

This included a review of technical justifications for changed sampling locations. The inspectors assessed whether the licensee performed reviews required to ensure that the changes did not affect their ability to monitor the impacts of radioactive effluent releases on the environment.The inspectors reviewed the calibration and maintenance records for eight air samplersto evaluate operating parameters. The inspectors reviewed results of the vendor's inter-laboratory comparison program and quality assurance programs to assess the adequacy of environmental sample analyses performed by the licensee.The inspectors reviewed quality assurance audit results of the REMP to determinewhether the licensee met the TS/ODCM requirements. Documents reviewed are listed in the Attachment. These reviews represent six samples.

b. Findings

No findings of significance were identified..3Unrestricted Release of Material From the Radiologically Restricted Area

a. Inspection Scope

The inspectors observed the access control location where the licensee monitoredpotentially contaminated material leaving the radiologically controlled area and inspected the methods used for control, survey, and release of material from this area.

The inspectors observed the performance of personnel surveying and releasing material for unrestricted use to verify that the work was performed in accordance with plant procedures.The inspectors evaluated whether the radiation monitoring instrumentation wasappropriate for the radiation types present and was calibrated with appropriate radiation sources that represented the expected isotopic mix. The inspectors reviewed the licensee's criteria for the survey and release of potentially contaminated material and verified that there was guidance on how to respond to an alarm indicating the presence of licensed radioactive material. The inspectors evaluated the licensee's equipment to determine if radiation detection sensitivities were consistent with the NRC guidance contained in IE Circular 81-07 and IE Information Notice 85-92 for surface contamination and Health Physics Position-221 for volumetrically contaminated material.

21The inspectors reviewed the licensee's procedures and records to verify that the radiationdetection instrumentation was used at its typical sensitivity level based on appropriate counting parameters, such as counting times and background radiation levels. The inspectors assessed whether the licensee had established a "release limit" by altering the instrument's typical sensitivity through such methods as raising the energy discriminator level or locating the instrument in a high radiation background area.These reviews represent two samples.

b. Findings

No findings of significance were identified..4Identification and Resolution of Problems

a. Inspection Scope

The inspectors reviewed the licensee's self-assessments, audits, condition reports, andspecial reports related to the radiological environmental monitoring program since the last REMP inspection to determine if identified problems were entered into the corrective action program for resolution. The inspectors also assessed whether the licensee's self-assessment program was capable of identifying and addressing repetitive deficiencies or significant individual deficiencies that were identified by the problem identification and resolution process.The inspectors also reviewed selected corrective action documents related to the REMPthat affected environmental sampling and analysis and meteorological monitoring instrumentation. Staff members were interviewed and documents were reviewed to determine if the following activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk:*Initial problem identification, characterization, and tracking;*Disposition of operability/reportability issues;

  • Evaluation of safety significance/risk and priority for resolution;
  • Identification of repetitive problems;
  • Identification of contributing causes;
  • Identification and implementation of effective corrective actions;
  • Resolution of NCVs tracked in the corrective action system; and
  • Implementation/consideration of risk significant operational experience feedback.This review represented one sample.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1Mitigating System Performance Indexes (MSPIs) Performance Indicators (PIs)

a. Inspection Scope

Cornerstone: Mitigating SystemsThe inspectors sampled the licensee's MSPI and PI submittals for the periods listedbelow. The inspectors used MSPI and PI definitions and guidance contained in Nuclear Energy Institute Document 99-02; "Regulatory Assessment Performance Indicator Guideline," Revision 5, to verify the accuracy of the data. The following MSPIs and PIs were reviewed for a total of six samples:Unit 1*safety system functional failures PI;*high pressure injection system MSPI; and

  • emergency AC [alternating current] power system MSPI.Unit 2*safety system functional failures PI;*high pressure injection system MSPI; and
  • emergency AC power system MSPI.The inspectors reviewed licensee IRs, electronic logs, and other records for the periodfrom July 1, 2006, through June 30, 2007, for each area specified above. The inspectors independently re-performed calculations where applicable. The inspectors compared the information acquired for each MSPI and PI to the data reported by the licensee. The inspectors verified that minor issues identified during the inspection were entered into the licensee's corrective action program. Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.Cornerstones: Barrier Integrity, Occupational Radiation Safety, and PublicRadiation Safety.2Radiation Safety Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed, at a minimum, the most recent 12 months of licensee eventreports, licensee data reported to the NRC, plant logs, and NRC inspection reports to verify the following performance indicators reported by the licensee for the 2 nd Quarterof 2007:

23*reactor coolant system (RCS) activity, Units 1 and 2;*occupational exposure control effectiveness; and

  • RETS/ODCM radiological effluent occurrence.The inspectors verified that the licensee accurately reported performance as defined bythe applicable revision of Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5.These performance indicator reviews constituted four inspection samples. Documentsreviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.4OA2Identification and Resolution of Problems (71152).1Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed screening of all items entered into the licensee's corrective action program. This screening was accomplished by reviewing the description of each new IR and attending selected daily management review committee meetings. Documents reviewed are listed in the Attachment to this report. Minor issues entered into the licensee's corrective action program as a result of the inspectors' observations are generally denoted in the Attachment. These activities were part of normal inspection activities and were not considered separate samples.

b. Findings

No findings of significance were identified..2Annual Review of Operator Workarounds

a. Inspection Scope

The inspectors reviewed the licensee's operator workaround program. Since there wereno current formalized operator workarounds, the inspectors also reviewed operator challenges, control room distractions, standing orders, leakage catch basins, and selected IRs to verify that none of those issue rose to the level of an operator workaround which could cause an impact on the operators' ability to implement abnormal and emergency operating procedures. This activity represented one inspection sample of the selected issue follow-up inspection requirement. In particular, it completed the annual requirement for a review of operator workarounds. The inspectors verified that minor issues identified during the inspection were entered into the licensee's corrective 24action program. Documents selected for a more detailed review are listed in theAttachment.

b. Findings

No findings of significance were identified.4OA3 Followup of Events and Notices of Enforcement Discretion (71153).1Grid Electrical Disturbance

a. Inspection Scope

The inspectors reviewed the plant's response to a grid disturbance event on the eveningof August 4, 2007. The disturbance was the result of the loss of three Midwest fossil plants within a short period of time. Grid frequency dropped and, as a result, the output of both Braidwood units increased slightly. The inspectors observed control room activities, discussed the event with operators and reviewed control room logs. Operators rapidly noted the power increases and took prompt action to limit the power increase and return the units to less than 100 percent power. The inspectors verified that hourly and shiftly calorimetric power did not exceed licensed limits on either unit. Documents reviewed in this inspection are listed in the Attachment. This inspection represents one

sample.

b. Findings

No findings of significance were identified..2Increase in Unit 1 RCS Unidentified Leakage Indication

a. Inspection Scope

The inspectors reviewed the licensee's response to indications of increased RCSunidentified leakage on August 19-20, 2007. The inspectors verified that the licensee actions were in accordance with commitments detailed in the response to the NRC regarding inspection of Alloy 600/82/182 pressurizer butt welds. The inspectors observed that the unidentified leakage increase was not sustained for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and that the temporary increase was within the statistical expectations for the measurement techniques. Documents reviewed as part of this inspection are listed in the Attachment.

This inspection represented one sample of the inspection procedure.

b. Findings

No findings of significance were identified.

25.3Unit 2 Manual Reactor Trip Due To Loss of Condenser Vacuum

a. Inspection Scope

On the afternoon of August 23, 2007, during a period of sudden high winds, operatorsmanually tripped the Unit 2 reactor due to lowering condenser vacuum. Sudden winds in the cooling lake had apparently raised waves high enough to cause a high differential pressure across the circulating water pumps intake traveling screens. Two of the three operating circulating water pumps on Unit 2 tripped on high differential pressure and, although operators quickly began reducing power, condenser vacuum entered the "not acceptable" region of operating procedures and operators initiated a manual reactor trip.

The plant responded as designed. One NRC inspector was in the control room at the time of the trip and another responded a short time later. The inspectors verified that the expected automatic actions had taken place and that operators performed the actions required by their emergency procedures. The auxiliary feedwater pumps started as expected.Due to the high winds, electrical power was lost to several areas near the plant, includingnumerous emergency sirens. In accordance with 10 CFR 50.72 the licensee reported the manual reactor protection system actuation, the automatic actuation of the auxiliary feedwater system, and the loss of more than 25 percent of its emergency sirens to the NRC. Power to all of the sirens were restored by the evening of September 24, 2007.

Documents reviewed as part of this inspection are listed in the Attachment. This inspection represents one sample.

b. Findings

No findings of significance were identified..4(Closed) LER 05000456/2007001-00 Unit 1 Reactor Trip Following a 345 kV [kilovolts]Transmission Line Lightning StrikeThis event, which occurred on June 27, 2007, was previously discussed in InspectionReport 05000456/2007004; 05000457/2007004, Section 4OA3.1. The inspectors reviewed the LER and the root cause report for the trip. Although the direct cause of the trip was loss of the 1D reactor coolant pump due to the electrical transient from the lightning strike, the trip probably would not have happened had a fuse in the pump's protective circuit not have been defective. The licensee was aware of industry problems with that particular model of fuse and had instituted a program for their replacement.

However, this particular fuse had not been replaced because the licensee determined that the risk of replacing the fuse while online was greater than waiting until the next outage. During the shutdown, the licensee replaced this and similar fuses to address the industry issue.The inspectors determined that the licensee's actions were reasonable and did notconstitute a performance deficiency. As additional corrective actions, the licensee modified its procedures to monitor the integrity of this and similar fuses and they also intended to take other design or alternate actions to address potential reactor coolant 26pump protective circuit vulnerabilities. Documents reviewed as part of this inspection arelisted in the Attachment. This inspection represented one sample. This LER is closed.4OA6Meetings.1Exit MeetingThe inspectors presented the inspection results to Mr. T. Coutu, and other members oflicensee management at the conclusion of the inspection on October 11, 2007. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified..2Interim Exit MeetingsInterim exit meetings were conducted for:

  • Licensed Operator Requalification Training Program with Mr. M. Smith, ActingPlant Manager, on August 31, 2007.*Radiological Environmental Monitoring Program (REMP) and Radioactive MaterialControl Program Inspection with Mr. T. Koutu, Site Vice President on August 31, 2007.*Licensed Operator Requalification Training Annual Operating Test withMr. G. Dudek, Training Director, on September 6, 2007, via telephone.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Coutu, Site Vice President
L. Coyle, Plant Manager
K. Aleshire, Emergency Preparedness Manager
D. Burton, Licensed Operator Requalification Training Group Lead
S. Butler, Operations Training Manager
G. Dudek, Site Training Director
R. Gadbois, Maintenance Director
D. Gullott, Regulatory Assurance Manager
J. Knight, Nuclear Oversight Manager
T. McCool, Operations Director
J. Moser, Radiation Protection Manager
J. Petty, Licensing Engineer
M. Smith, Engineering Director
T. Tierney, Chemistry, Environmental, and Radioactive Waste ManagerNuclear Regulatory Commission
R. Skokowski, Chief, Reactor Projects Branch 3

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSEDOpened05000456/2007005-01;05000457/2007005-01NCVFailure to Meet TRM Requirements for Spent Fuel BuildingCrane Interlocks and Physical Stops (Section 1R20)

Closed

05000456/2007005-01;05000457/2007005-01NCVFailure to Meet TRM Requirements for Spent Fuel BuildingCrane Interlocks and Physical Stops (Section 1R20)05000456/2007-001-00LERUnit 1 Reactor Trip Following a 345 KV Transmission LineLightning Strike (Section 4OA3.4)

Discussed

None.

2

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection.

Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that