IR 05000456/2020010

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Biennial Problem Identification and Resolution Inspection Report 05000456/2020010 and 05000457/2020010
ML20086G679
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 03/25/2020
From: Hironori Peterson
NRC/RGN-III
To: Bryan Hanson
Exelon Generation Co
References
IR 2020010
Download: ML20086G679 (22)


Text

March 25, 2020

SUBJECT:

BRAIDWOOD GENERATING STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000456/2020010 AND 05000457/2020010

Dear Mr. Hanson:

On February 28, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Braidwood Generating Station and discussed the results of this inspection with Ms. M. Marchionda-Palmer, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

No findings or violations of more than minor significance were identified during this inspection. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Hironori Peterson, Chief Branch 3 Division of Reactor Projects

Docket Nos. 50-456 and 50-457 License Nos. NPF-72 and NPF-77

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000456 and 05000457

License Numbers:

NPF-72 and NPF-77

Report Numbers:

05000456/2020010 and 05000457/2020010

Enterprise Identifier: I-2020-010-0033

Licensee:

Exelon Generation Company, LLC

Facility:

Braidwood Generating Station

Location:

Braceville, IL

Inspection Dates:

February 03, 2020 to February 28, 2020

Inspectors:

L. Cender, Health Physicist

G. Hausman, Senior Reactor Inspector

N. Shah, Project Engineer

P. Smagacz, Resident Inspector

J. Weigandt, Reactor Engineer

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Braidwood Generating Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000456/2019-001-00 LER 2019-001-00 for Braidwood Station, Unit 1,

Unit Trip on Low Steam Generator Level Due to Failure of a Controller on a Feedwater Regulating Valve 71153 Closed

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program (CAP), use of operating experience, self-assessments and audits, and safety conscious work environment.
  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a 5-year review of the Units 1 and 2 125 Vdc systems.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

71153 - Followup of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) Licensee Event Report (LER) 05000456/2019-001-00, "Unit Trip on Low Steam Generator Level Due to Failure of a Controller on a Feedwater Regulating Valve,"

(ADAMS Accession No. ML19324D929). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors did not identify a violation of NRC requirements.

INSPECTION RESULTS

Assessment 71152B Review of Corrective Action Program:

Based on the samples reviewed, the team determined that the licensees' performance in each of these areas adequately supported nuclear safety.

Effectiveness of Problem Identification:

Overall, the station was effective at identifying issues at a low threshold and properly entering them into the CAP as required by station procedures. The team determined that the station was effective at identifying negative trends that could potentially impact nuclear safety. The team interviewed personnel, reviewed documents, walked down portions of the plant, and assessed licensee problem identification.

One item of note, while observing surveillance testing, the NRC resident inspectors noted that the flow gauge for the 2B residual heat removal pump was not responding properly. The licensee staff did not capture this issue in the CAP, in part, due to the belief that this was a low-level concern. However, after prompting by the inspectors, the licensee recognized that this gauge also controls the position of the downstream flow valve, which could impact pump operability. Although the licensee later verified the pump was operable, the initial lack of sensitivity potentially resulted in a more significant issue being missed. The licensee documented this issue as AR 4322053

Effectiveness of Prioritization and Evaluation of Issues:

ln-depth reviews of a risk-informed sampling of Action Request (ARs), work orders (WOs),and cause evaluations were completed, including a 5-year time period for the 125 Vdc. The team determined that the licensee had established a low threshold for entering issues into the CAP, that the issues were generally being appropriately prioritized and evaluated for resolution, and that the corrective actions (CAs) were implemented to mitigate the risk of issues occurring that could affect overall system operability and/or reliability.

The inspectors noted that the licensee had identified potential degradation of the feedwater check valves (AR 4291137), as a contributing cause to a Unit 1 reactor trip documented in AR 4281429. As part of the trip evaluation, the licensee decided to continue operating with the valves in the degraded condition; however, the inspectors noted that there was no assigned action to assess and document the risk impact of this decision. The inspectors noted that while the licensee had done some risk assessment and had proposed actions to address the issue, these actions were not subject to the normal station management review/challenge process, since they were not tied to a formal CAP action. The inspectors subsequently concluded that the licensees justification for continued operation was reasonable and did not identify any open safety concern. However, the licensees decision to not assign a formal CAP action and therefore bypass the normal management review process was documented as AR 4322046.

The inspectors also noted that while issue evaluations were generally sound, there were several examples where additional research was needed to understand the technical basis, primarily due to a lack of clear documentation. This theme had previously been identified in earlier licensee self-assessments and CAP audits and continued to be a concern.

The licensee documented this observation as AR 4322045.

Effectiveness of Corrective Actions:

The team concluded that the licensee was generally effective in developing CAs that were appropriately focused to correct the identified problem and to address the root and contributing causes for significant issues in order to preclude repetition. The licensee generally completed CAs in a timely manner and in accordance with procedural requirements commensurate with the safety significance of the issue. For NRC identified issues, the team determined that the licensee generally assigned CAs that were effective and timely.

During a walk down of the Unit 1 feedwater system, the inspectors identified an open deficiency tag on the Unit 1 Main Feedwater Regulating Valve Control Panel Display (panel 1PL1001). This panel was not safety-related. Specifically, the display was not receiving data or displaying valve position. The inspectors noted that the issue was identified in July 2019 under AR 4263048. In this AR, the licensee had noted that this panel was needed for an Adverse Condition Monitoring Plan. Subsequently, AR 4294972 was initiated in November 2019, as the display had not been repaired. After checking the CAP database and querying the licensee, the inspectors determined that both ARs were closed to a work order, which was then closed with no action taken. Subsequently, the inspectors determined that this display was not needed for indications or trending, but was used as a back-up indication by the control room. The licensee documented the failure to fix this issue as AR 4321854.

No violations or findings were identified.

Assessment 71152B 5-year Review of Units 1 and 2 125V DC Systems:

The inspectors performed an expanded 5-year review of the Units 1 and 2 125 Vdc system; specifically, by performing system walk-downs and evaluating condition reports, engineering changes, and work orders. The inspectors also interviewed the system engineer responsible for this system. Overall, the inspectors determined that the licensee was effectively managing issues associated with this system.

Since 2014, the licensee has observed intermittent grounds on both the Units 1 and 2 DC bus systems (i.e., buses 111, 112, 211 and 212). These grounds were primarily attributed to equipment issues (bus 111) and potential water intrusion due to wet weather (buses 112, 211 and 212). These grounds were documented in the CAP and the NRC resident inspectors had been reviewing them through the baseline inspection program. Because of the intermittent and/or short-lived nature of the grounds, the location of the grounds was difficult to discern.

The inspectors identified no operability or other immediate safety concerns with these grounds and concluded that the licensee had taken proactive actions to find and correct the cause of the grounds.

No violations or findings were identified.

Assessment 71152B Operating Experience, Self-Assessment and Audits:

The inspectors reviewed operating experience (OpE) captured in the CAP and sampled OpE from NRC, industry, vendors, and third-party groups. Overall, for the samples selected, the licensee was generally performing the appropriate assessments for station applicability.

Through interviews and observations at selected station meetings, the inspectors also concluded that OpE was being appropriately used in daily plant activities.

The inspectors determined that the licensee was adequately performing self-assessments and audits in accordance with licensee procedures and implementing corrective actions as needed. Of note, the inspectors observed that the overall conclusions of the licensees self-assessment and Nuclear Oversight audit of the CAP program done prior to this NRC inspection, was consistent with the inspectors observations.

No violations or findings were identified.

Assessment 71152B Review of Safety Conscious Work Environment:

The inspectors observed various station meetings, including those in which new CAP items were reviewed, and interviewed a representative cross-section of station personnel, both individually and small groups. Additionally, the inspectors interviewed the Employee Concerns Program (ECP) Coordinator, reviewed recent case logs and case files and inquired about the program during interviews with station personnel.

During interviews, several licensee staff stated a lack of confidence in the licensee's ability to correct low level issues. This was primarily based on issues taking a significant time to resolve and/or being closed without any apparent action being taken. This perception caused some interviewees to state that they likely wouldn't continue to document these concerns in the CAP. The inspectors determined that much of this was due to the lack of clear feedback on what actions were being taken to address the issue and understanding of what certain CAP actions (such as "closed to trend") actually meant. The inspectors also determined that the interviewees would not hesitate to raise a concern if they believed that plant or worker safety was potentially involved. This concern was discussed with the licensee, who documented it as AR 4322027.

Overall, inspectors found no evidence of challenges to the licensee's safety conscious work environment (SCWE). Licensee's employees were willing to raise nuclear safety concerns through at least one of several means available. Workers expressed favorable opinions of the ECP during interviews, and those that had utilized it had no concerns regarding the overall outcome. The inspectors noted that the licensee had generally addressed potential SCWE issues in the ECP and identified no significant trends with documented issues within the last two-years.

No violations or findings were identified.

Observation: LER closeout observation 71152B Review of Root Cause of Unit 1 Trip on Low Steam Generator Level:

The inspectors performed a detailed review of LER 2019-01-00, Unit 1 Trip on Low Steam Generator Level Due to Failure of a Controller on a Feedwater Regulating Valve. A root cause evaluation for this issue was performed under AR 4281429. As part of this evaluation, the licensee reviewed a previous root cause evaluation for a 2018 Unit 1 reactor trip, also caused by a feedwater controller malfunction, documented in AR 4144070. Although the feedwater system is non-safety related, it is a system important to plant risk.

Based on the results of the 2018 evaluation, the licensee revised the 2019 evaluation to include additional information regarding performance issues with the feedwater check valves.

Specifically, these valves would occasionally not fully open (AR 4165777), resulting in partial flow restrictions in the feedwater system. Although the licensee had taken corrective action, this issue remained a concern and was a contributor in the 2019 Unit 1 reactor trip.

In the 2019 evaluation, the licensee elected to continue operating with these valves in a degraded condition; however, there was no formal CAP action initiated to assess the potential operational risk of this decision. The inspectors noted that the licensee had opened an Adverse Condition Monitoring Plan (ACMP) to monitor the check valve performance and had developed a white paper to evaluate the operational risk and offer several recommendations to improve operating reliability. However, because these actions were not formally tied back to AR 4281429, they were not subject to management review through the normal CAP screening processes or other means. Therefore, these documents did not constitute a formal decision and/or risk assessment to justify continued operation with the degraded check valves.

After reviewing the white paper, ACMP and discussing the issue with plant engineers, the inspector concluded the licensee could reasonably justify continued operation with the degraded check valves. Additionally, inspectors noted this issue was being tracked in the U1 system health report and the Plant Health Committee approved replacement of the existing valves with a new style of valve. These actions were being tracked in the CAP under AR 4291137.

The inspectors concluded that although the licensee had not taken a formal CAP action to justify continued operation with the degraded Unit 1 feedwater check valves, the implemented controls were appropriate to manage the risk until the issue was corrected. Therefore, no violations or findings were identified. The licensee documented the failure to assign a formal action in AR

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On February 28, 2020, the inspectors presented the biennial problem identification and resolution inspection results to Ms. M. Marchionda-Palmer, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective Action

Documents

2448240

Westinghouse NSAL-15-1. FQ(Z) Tech Spec Surveillance

2/05/2015

2567071

OSP-A-CT--Exciter Stator Phase Banding Is Loosening

10/07/2015

2589930

Root Cause Report: Severe Corrosion and Degraded

Coating Observed on Line 0SXH2AA-6

2/29/2015

2589930

Heavy General Corrosion on 0SXH2AA 6" in 0SX165A Pit

11/19/2015

270540

DC System Trend IR (January 2014 - July 2019)

08/08/2019

3993342

Request Formal OPEX Review for ICES 407278

04/03/2017

4066205

Braidwood Station OPEX Level 3 Review - NRC IN 2017-06

10/24/2017

4071655

Preparation for NRC Problem Identification and Resolution

Inspection

06/01/2018

4074647

Ops Effectiveness Review of ATV Actions Self-Assessment

11/14/2017

4081071

Level 3 OPEX Review Needed--Unusual Event Hydrogen

Leak

2/05/2017

4083304

DC System Short Circuit Calculation Update

2/12/2017

4086455

Green NCV - Errors in Analysis of Record for MS Line HELB

2/21/2017

4107379

Security 24 HR Loggable SY-AA-103-500 Procedure Not

Followed

2/23/2018

4110095

PI&R Deficiency (OBJ 2H): Shift Review Bypassed

03/01/2018

4110095

PI&R Deficiency: Shift Review Bypassed

03/01/2018

4110536

PI&R Deficiency Inappropriate NCAP IR

03/02/2018

4115813

Failed Gasket of 2B AF PP Gearbox Oil Cooler

03/16/2018

23789

PI&R Deficiency: Aging Management Program

04/06/2018

24952

RCS Pressure Transient During 7300 TCP Mod

04/10/2018

26942

Level 2 C&T Event--Work Stopped on 1PA08J and 1PA09J

04/15/2018

28714

OSP-A Loss of ESF Bus 141 During 1A EDG Sequencer

Testing

04/19/2018

29240

OSP-X 1RC01R NDE Results for 1RV-03-002 Reactor Head

Weld

06/19/2020

4131031

EC 620239 Poorly Written Lacks Operational Experience

04/26/2018

4132550

Root Cause Report: Unit 1 A1R20 Turbine Trip

06/22/2018

4143493

PI&R Deficiency: Untimely IR Generation Review

06/01/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4143518

PI&R Deficiency: Corrective Action Investigations

06/01/2018

4144070

U1 Manual Rx Trip

06/04/2018

4144695

Unit 1 DG-1 Maintenance Rule a(1) Determination

06/06/2018

4145161

Trend--THU Behaviors

06/07/2018

4146837

LORT TSA Failure (Isolate WS Flooding)

06/13/2018

4147583

1PI-AF105 Inlet Pressure Reads Lower Than Outlet Gauge

06/15/2018

4149089

BYR OPEX: U2 DEHC Drop 2 in Failure Mode

06/21/2018

4154913

NER NC-18-015 Yellow Adverse Trend in Fleet Fuel

Performance

07/10/2018

4156368

Potential Inventory Loss for Ultimate Heat Sink

07/17/2018

4158520

NRC ID'D - Support on 1B DG Lube OIl - Not Fret Protected

07/24/2018

4158523

NRC ID'D - 5 Missing Shroud Bolts - Top of 1B DG

07/24/2018

4160763

PI&R: UFSAR Revision Not Tracked Properly

08/01/2018

4167984

2Q18 Green NCV--Inadequate Maintenance Work

Instructions

08/28/2018

4167985

2Q18 Green Finding--Work Instruction Error Caused RCS

Issue

08/28/2018

4182698

OSP-X 2B SI Pump Recirculation Flow Anomaly

10/11/2018

4182783

OSP-A 2B SI Pump Recirculation Line Restriction

10/12/2018

4183593

Inspection Results of 2B SI Pump Recirculation Line FME

10/15/2018

4186040

NRC ID During Mode 4 Containment Walk Down

10/21/2018

4188177

FME Identified in K-14 RCCA Assembly

10/26/2018

4190621

NRC Green LIV - Security Inspection

11/01/2018

4190742

Digital FRV Controlling with Integral Function

11/01/2018

4193552

Notification Part 21 Framatome RFM Manipulator Gripper

11/09/2018

4197712

OPS Focus, Monitoring Plant Conditions Closely

11/26/2018

4198029

Foreign Material Exclusion (FME) - Declining Trend

2/22/2019

203982

2B SI Pump Low Recirculation Flow Rate

03/21/2019

210285

Source of FME ins 2B SI System

01/11/2019

216119

Level 3 OPEX Review Requested

01/31/2019

217023

DBAI: HELB Manual Actions

2/10/2014

217133

DBAI: Global Effects of Missile Impact on RWST Hatch

Cover

2/04/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

217715

Self-Assessment: Ops Mid-Cycle with OJT/TPE/Inst/SMEs

2/06/2019

217716

Self-Assessment: Ops 71111.11

2/06/2019

217944

Level 3 OPEX Review--ICES 449343

04/24/2019

22716

Loose Conduit Nut on 1B AF Pump

2/22/2019

24262

DG Temperature Switch - Part 21 Evaluation

2/27/2019

29548

Potential Part 21 Applicability on Battery Charger 111

10/17/2019

232818

FME: 2TO5337A Inspection Revealed FM

08/10/2019

233266

Two DEP Failures of an Evaluated Simulator Scenario

03/26/2019

235177

FME: Metal Tag Cable Created I/A Leak on 1LC-ES086

04/01/2019

236442

NOS ID RCR 4145161 Contained Descripencies: CA Not

Classified

04/04/2019

254840

2BWOA RCP-2 Entry

06/06/2019

256355

Self Assessment FME

06/12/2019

261661

One ILT SRO-I Preliminary Denied License By NRC

07/03/2019

263659

Scaffold Tie Off to Structure Broke--Div 12 ESF Room

07/12/2019

265036

DC Bus 212 Ground (2DC06E - 125 Vdc ESF - Distribution

Center Bus 212)

07/18/2019

265545

Unexpected Annunciator 1-21-D6. DC Bus 111 Ground

(1DC05E 125 Vdc ESF Dist. Cent 111 Assembly)

07/19/2019

266244

Perform OPEX Review of 2019 INPO FME AFIs

09/24/2019

267116

DC Bus 212 Ground (2DC06E - 125 Vdc ESF Dist. Cent 212

Assembly)

07/26/2019

268875

Station Vulnerability Issue Due to Ginna OPEX 458342

08/01/2019

268944

NOS ID 2018 Bioassay Prgm Periodic Measuremt Not

Performed

08/01/2019

269225

Efficiency Impact Seen With Lake Softening

07/25/2019

269360

DC Bus 212 Ground (2DC06E - 125 Vdc ESF Dist. Cent 212

Assembly)

08/03/2019

270275

+96 Vdc Ground on DC 111

08/07/2019

270893

2TO5337A Inspection Revealed FM

08/10/2019

272759

Pilot Cell 19 at 91F (>90F Admin Limit) 2DC01E (2DC01E -

ESF Battery 211 Assembly)

08/18/2019

272834

DC 112 Specific Gravity Deviation High (1DC02E - ESF

08/18/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Battery 112 Assembly)

273460

OP-AA-105-102, Att 1 Not Complete for First Qtr 2019

08/20/2019

273637

Crew Learning for LORT Scenario

08/22/2019

277166

DC Bus 211 Ground (2DC05E - 125 Vdc ESF Dist. Center

Bus 211 Assembly)

09/06/2019

277356

Unexpected Alarm 1-21-E8 125 Vdc Batt Charger 111

Trouble

09/06/2019

278172

Part 21 Closure Actions Inadequate

10/10/2019

278351

DPM JW Leak 1B EDG--1DG01KB

09/11/2019

278530

Proactive Inspection to Prevent Grounds 1AP01E (1AP01E -

Unit Aux. Power Transformer 141-1)

09/11/2019

278534

Proactive Inspection to Prevent Grounds 2AP70E (2AP70E -

Unit Aux. Power Transformer 241-2)

09/11/2019

278536

Proactive Inspection to Prevent Grounds 1AP02E (1AP02E -

Transformer, System Aux Trans 142-1)

09/11/2019

278539

Proactive Inspection to Prevent Grounds 1AP71E (1AP71E -

System Aux Transformer 142-2)

09/11/2019

278540

Proactive Inspection to Prevent Grounds 2AP02E (2AP02E -

System Aux. Power Transformer 242-1)

09/11/2019

278544

Proactive Inspection to Prevent Grounds 2AP71E (2AP71E -

System Aux. Power Transformer 242-2)

09/11/2019

278548

Proactive Inspection to Prevent Grounds 1SY01E (1SY01E -

SAT 142-1 E.O. Disc Switch)

09/11/2019

278549

Proactive Inspection to Prevent Grounds 1SY02E (1SY02E -

SAT 142-2 E.O. Disc Switch)

09/11/2019

278551

Proactive Inspection to Prevent Grounds 2SY01E (2SY01E -

SAT 242-1 E.O. Disc Switch)

09/11/2019

278557

Proactive Inspection to Prevent Grounds 1FP01EA

(1FP01EA - Outside FP Alarm Horn for Transformer Area)

09/11/2019

278558

Proactive Inspection to Prevent Grounds 1FP01EB

(1FP01EB - Inside FP Alarm Horn for Transformer Area)

09/11/2019

278559

Proactive Inspection to Prevent Grounds 2FP01EA

(2FP01EA - Alarm Horn Outdoor Transformer Area)

09/11/2019

278561

Proactive Inspection to Prevent Grounds 2FP01EB

09/11/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

(2FP01EB - Alarm Horn Outdoor Transformer Area)

281258

1ER-DC05E Positive Ground Pushed Is > Rounds Maximum

(1ER DC05E DC Bus 111 Ground Voltage Recorder)

09/22/2019

282020

DC ESF Bus 112 Ground Alarm Received (1DC06E - 125

Vdc ESF Dist. Cent 112 Assembly)

09/25/2019

282409

NOS ID'D: 1 of 10 LORT JPM Score Sheets was Incomplete

09/26/2019

283427

FME: Foreign Material Found During Disassembly of

1PS124A

09/30/2019

283868

20 Pre-NRC Problem Identification and Resolution

Inspection

01/17/2020

285090

1B AF Pump Flow Lower Than Acceptable Flow

10/04/2019

285470

2-OSP-F Unexpected Alarm DC 112 Ground

10/06/2019

285532

-122 Vdc 112 Ground

10/07/2019

286018

2 DC Ground

10/08/2019

286217

05-OSP-X Received Unexpected ALM 1-21-E8, 111 Battery

Charger Trouble (1DC03C Battery Charger 111)

10/09/2019

287611

FME - Metal Shavings Found in ES Piping

10/14/2019

288186

10-OSP-R T/S Multiple Spurious Alarms on DC 111 Charger

(1DC03E 125 Vdc Battery Charger 111)

10/16/2019

288445

11-OSP-R Intermittent DC Bus 112 Ground (1DC06E - 125

Vdc ESF Dist. Cent 112)

10/16/2019

289894

Unexpected Alarm 1-22-D6 DC Bus 112 Ground

10/21/2019

295309

1ER-DC05E Reads > 75 V (1ER-DC05E - DC Bus 111

Ground Voltage Recorder)

11/07/2019

298533

DC Bus 212 Ground Detector Is Degraded (2ER-DC06E -

DC Bus 212 Ground Voltage Recorder)

11/19/2019

298558

25 Vdc Battery Charger 111 Alarm Received After Ground

Check (1ER-DC05E DC Bus 111 Ground Voltage

Recorder)

11/20/2019

298558

25 Vdc Battery Charger 111 Alarm Received After Ground

Check

11/20/2019

4300007

DC 112 Ground During FP RTS (1FP02J - Fire Protection

Cabinet 1FP02J)

11/26/2019

4301635

Clearance & Tagging Annual Audit Deficiency - Ops

2/04/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4302464

Unexpected Alarms 1-21-D6 and 1-21-E8 (1DC05E 125

Vdc ESF Dist. Cent 111 Assembly)

2/09/2019

4302464

Unexpected Alarms 1-21-D6 and 1-21-E8

2/09/2019

4304503

Erratic Negative Ground Volt Reading When Depressed DC

2

2/17/2019

4304938

Level 3 Config Control: Zero d/p Indicated on 0PDI-VC058

2/19/2019

4308125

Battery 212 Charger Circuit Card Issue (2DC04E - 125 Vdc

Battery Charger 212 Assembly)

01/05/2020

4308795

Unexpected Annunciator: 1-21-E8 (1DC03E 125 Vdc

Battery Charger 111)

01/08/2020

Corrective Action

Documents

Resulting from

Inspection

21466

NRC ID: Issue With Rigging Restraint

2/25/2020

21854

NRC ID'd Deficiency on 1PL100J With No Open WR/WO

2/27/2020

Drawings

20E-1-4030DC05

Schematic Diagram, 125 Vdc ESF Distribution Center, Bus

111, Part 1, 1DC05E

X

20E-1-4030DC06

Schematic Diagram, 125 Vdc ESF Distribution Center, Bus

111, Part 2, 1DC05E

P

AC-7

AC One Line Diagram, January 6, 2015 (For Training Use

Only)

DC-1

25 Vdc System (For Training Use Only)

DC-2

250 Vdc System (For Training Use Only)

Engineering

Changes

25953

Evaluate Impact on Safety Analyses due to As-Found ECCS

Flow Rates

10/20/2018

BR-19-002

Surveillance Test Interval (STI) Evaluation: Revise The 125

Vdc ESF Battery Bank and Charger Operability Weekly

Surveillance Frequency from Once per 7-days to Once per

31-days

BRW-15-006

Surveillance Test Interval (STI) Evaluation: Change the STI

for Service Test (SR 3.8.4.3) to an 18-month Staggered Test

Basis

Engineering

Evaluations

2541232-46-01

ICES 318417, Sequoyah Unit 1 Trip Due to Loss of Vital

Inverter Power Board

05/19/2016

2683598-83

ICES 323906, Prairie Island Diesel Driven Fire Pump Failed

09/22/2016

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

to Start

28714

Multiple Losses of ESF Bus 141 during 1A Diesel Generator

Sequence Testing in A1R20

06/08/2018

4190742

Feedwater Regulating Valve Oscillations During Power

Ascension

01/17/2019

4192903

2018 Equipment Reliability Evaluation

2/10/2018

ATI 02541232-46-

ICES 318417, Sequoyah Unit 1 Trip Due to Loss of Vital

Inverter Power Board

05/19/2016

ATI 02683598-83

ICES 323906, Prairie Island Diesel Driven Fire Pump Failed

to Start

09/22/2016

ATI 03969265-82

ICES 407851, Palo Verde Unit 2 Inverter Failed to Transfer

to Emergency Power

No Date

Given

ATI 03993342-02

ICES 407278, Catawba Battery System Cell Failure

04/04/2017

ATI 04008241-33

ICES 408139, Fermi Unit 2 Uninterruptible Power Supply

Inverter Failed to Start

No Date

Given

ATI 04048975-28

ICES 420726, Fermi Unit 2 Balance of Plant Battery Charger

Failed to Charge

09/27/2017

ATI 04048975-96

ICES 426149, Byron Unit 2 Battery Charger Input Breaker

Tripped Open

No Date

Given

ATI 04066205-02

NRC IN 2017-06: Battery and Battery Charger Short-Circuit

Current Contributions to a Fault on the Direct Current

Distribution System

2/13/2017

ATI 04242973-53

IRIS 460461, Quad Cities Unit 1 24/48 Vdc Charger Tripped

10/30/2019

Miscellaneous

2018 ECP Logs

2019 ECP Logs

2019 ECP Files

Plant Health Committee Agenda

2/24/2020

Braidwood Management Review Committee Agenda

2/11/2020;

2/13/2020;

2/24/2020

Station Ownership Committee Package

2/10/2020;

2/12/2020;

2/13/2020;

2/24/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Station Trend Report

November

2019

Station Trend Report

December

2019

--

Final Safety Evaluation for PWROG Topical Report WCAP-

17661, Rev. 1, "Improved RAOC and CAOC FQ Surveillance

Technical Specifications,"

2018 ECP Files

IEEE-450

Standard

IEEE Recommended Practice for Maintenance, Testing, and

Replacement of Vented Lead-Acid Batteries for Stationary

Applications

1995

ML052350494

NUREG-0800, Standard Review Plan, 8.3.2 D-C Power-

Systems

ML122130601

IN 2013-05; Battery Expected Life and Its Potential Impact on

Surveillance Requirements

03/19/2013

PI-AA-125-1006,

Att 20

Performance Analysis 04281548-06

10/30/2019

PI-AA-3

Exelon Nuclear Policy: Nuclear Safety Culture

2/05/2015

PORC Meeting:

18-025

PORC Topic: Surveillance Test Interval (STI) BRW-15-006 -

Change the STI for Service Test (SR 3.8.4.3) To An 18-

Month Staggered Test Basis

09/20/2018

STS428.TG

NRC Inspection Manual, Part 9900: Technical Guidance,

Standard Technical Specifications, Section 4.2.8.X.X.

Surveillance Requirements - 125 Volt Battery Bank

10/01/1979

Operability

Evaluations18-001

2B SI Pump Low Recirc Flow Rate

Procedures

1BwHSR 3.8.4.2-

111

Unit One 125 Volt ESF Battery Charger 111 Capacity Test

1BwHSR 3.8.4.2-

2

Unit One 125 Volt ESF Battery Charger 112 Capacity Test

1BwHSR 3.8.4.3-

111

Unit One 125 Volt ESF Battery Bank 111 Service Test

1BwHSR 3.8.4.3-

2

Unit One 125 Volt ESF Battery Bank 112 Service Test

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1BwHSR 3.8.6.6-

111

Unit One 125 V ESF Battery Bank 111 Modified Performance

Test

1BwHSR 3.8.6.6-

2

Unit One 125 V ESF Battery Bank 112 Modified Performance

Test

1BwOSR 3.8.6.1-

Unit One 125 Vdc ESF Battery Bank and Charger 111

Operability Surveillance

1BwOSR 3.8.6.1-

Unit One 125 Vdc ESF Battery Bank and Charger 112

Operability Surveillance

1BwOSR 3.8.6.5-

Unit One 125 Vdc ESF Battery Bank 111 Operability

Surveillance

1BwOSR 3.8.6.5-

Unit One 125 Vdc ESF Battery Bank 112 Operability

Surveillance

2BwHSR 3.8.4.2-

211

Unit Two 125 Volt ESF Battery Charger 211 Capacity Test

2BwHSR 3.8.4.2-

2

Unit Two 125 Volt ESF Battery Charger 212 Capacity Test

2BwHSR 3.8.4.3-

211

Unit Two 125 Volt ESF Battery Bank 211 Service Test

2BwHSR 3.8.4.3-

2

Unit Two 125 Volt ESF Battery Bank 212 Service Test

2BwHSR 3.8.6.6-

211

Unit Two 125 V ESF Battery Bank 211 Modified Performance

Test

2BwHSR 3.8.6.6-

2

Unit Two 125 V ESF Battery Bank 212 Modified Performance

Test

2BwOSR 3.8.6.1-

Unit Two 125 Vdc ESF Battery Bank and Charger 211

Operability Surveillance

2BwOSR 3.8.6.1-

Unit Two 125 Vdc ESF Battery Bank and Charger 212

Operability Surveillance

2BwOSR 3.8.6.5-

Unit Two 125 Vdc ESF Battery Bank 211 Operability

Surveillance

2BwOSR 3.8.6.5-

Unit Two 125 Vdc ESF Battery Bank 212 Operability

Surveillance

AD-AA-3000

Nuclear Risk Management Process

71152B

Procedures

BwHS TRM

25 Volt Battery Bank Surveillance

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

3.8.C.4

BwHS TRM

3.8.C.4S1

25 Volt ESF Battery Bank and Rack Surveillance Data

Sheet for Battery 111

BwHS TRM

3.8.C.4S2

25 Volt ESF Battery Bank and Rack Surveillance Data

Sheet for Battery 112

BwHS TRM

3.8.C.4S3

25 Volt ESF Battery Bank and Rack Surveillance Data

Sheet for Battery 211

BwHS TRM

3.8.C.4S4

25 Volt ESF Battery Bank and Rack Surveillance Data

Sheet for Battery 212

BwOP DC-5-111

25 Vdc ESF Battery 111 Equalization

BwOP DC-5-112

25 Vdc ESF Battery 112 Equalization

BwOP DC-5-211

25 Vdc ESF Battery 211 Equalization

BwOP DC-5-212

25 Vdc ESF Battery 212 Equalization

ER-AA-2001

Plant Health Committee

ER-AA-320-1004

Maintenance Rule 18-10 - Performance Monitoring and

Dispositioning Between (a)(1) and (a)(2)

IP 71152

NRC Problem Identification and Resolution Inspection

Procedure

01/01/2015

MA-AA-716-017

Station Rework Reduction Program

MA-AA-721-1001

Station Battery Testing Strategies

NO-AA-210-1002

Nuclear Oversight Audit Templates

PI-AA-101-1001

Performance Monitoring and Analysis Manual

PI-AA-101-1003

Performance Gap Resolution

PI-AA-115

Operating Experience Program

PI-AA-115-1001

Processing of Level 1 and Level 2 OPEX Evaluations

PI-AA-115-1002

Processing of Level 2 OPEX Evaluations

PI-AA-115-1003

Processing of Level 3 OPEX Evaluations

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program Procedure

PI-AA-125-1003

Corrective Action Program Evaluation Manual

71152B

Self-Assessments

Braidwood Station Maintenance Rule Periodic a(3)

Assessment

December 1,

2017 to

January 19,

2019

4074648

Simulator Management Compliance (per TQ-AA-306)

11/14/2017

M1C-4

NOS Objective Evidence Report Maintenance Functional

Area Audit - Battery Maintenance and Testing (AR 2608396-

17)

2/03/2016

NOSA-BRW-16-

Braidwood Station Maintenance Audit Report 01/19/2016 to

01/29/2016 (AR2608396)

2/03/2016

NOSA-BRW-16-

Braidwood Station Engineering Programs and Station

Blackout Audit Report 03/28/2016 to 04/08/2016

(AR2637791)

04/13/2016

NOSA-BRW-18-

Braidwood Station Maintenance Functional Area Audit

Report 02/19/2018 to 03/2/2018 (AR4090567)

03/08/2018

NOSA-BRW-18-

Braidwood Station Emergency Preparedness Audit Report

03/26/2018 to 04/06/2018 (AR4113152)

04/11/2018

NOSA-BRW-18-

Braidwood Station In-service Inspection, In-service Testing,

and Appendix J Audit Report 08/20/2018 to 08/31/2018

(AR4161245)

09/07/2018

NOSA-BRW-19-

Braidwood Station Corrective Action Program Audit Report

03/25/2019 to 04/05/2019 (AR4224677)

04/10/2019

NOSA-BRW-19-

Braidwood Station Radiation Protection Audit Report

07/22/2019 to 08/02/2019 (AR4254882)

08/07/2019

PI-AA-126-1001-

F-01

2018 Employee Concerns Program Performance and

Effectiveness Review

PIIM 2019-0242

2019-0242 System and Component Monitoring

06/07/2019

71153

Corrective Action

Documents

4144070

Unit 1 Manual Reactor Trip Due to Lowering Steam

Generator Level - Root Cause Investigation Report

2/12/2020

4165777

1FW079B Check Valve Further Closed than 1FW079A, C, &

D

08/20/2018

25240

Review of Byron IR 4185973 FW Reg Valv Travel

Transducers

03/01/2019

251835

1PL100J Windows Operating System Crashed

05/26/2019

263048

1PL100J Screen Illegible

07/10/2019

281429

Unit 1 Reactor Trip on 1FW520 Valve Closure

289400

15-OSP-R U1&2 FRV Positioner ByP Reg Handwheel

10/20/2019

291137

1FW530 Full Open Following Power Ascension

10/25/2018

294972

1PL100J Screen is Fuzzy

11/06/2019

296357

A1R21LL - Valve Team Lessons Learned

11/11/2019

4303483

Troubleshooter Requested for FW Performance Hardening

2/12/2019

699328

1FW079B Check Valve Further Closed than Expected

11/14/2007

2428

Modify 1FW520 LOOP to Allow Living with FW Line

Restriction

11/21/2007

Engineering

Evaluations

-

Braidwood Unit 1 Feedwater Line C Hydraulic Resistance

Imbalance RELAP5 Study

October

2019

Miscellaneous

Adverse

Condition

Monitoring and

Contingency Plan

U1 Feedwater Regulating Valve (FRV) Position

10/25/2019

Adverse

Condition

Monitoring and

Contingency Plan

U2 Feedwater Regulating Valve DVC Health

10/29/2019

Procedures

PI-AA-125-1001

ROOT CAUSE ANALYSIS MANUAL

Work Orders

29232

1FW079B Check Valve Further Closed than 1FW079A,

C, & D

2/01/2019

4989927

Troubleshooter Requested for FW Performance Hardening

2/15/2019