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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
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~CATEGORY REGULATORY INFORMATION DISTRIBUTION SYSTEM (BIDS)ACCESSION NBR: 9710160056 DOC.DATE: 97/10/08 NOTARIZED:
NO FACIL: 50-250 Turkey Point Plant>Unit 3 Flor ida Power and Light C AUTH.NA:>PE AUTHOR AFF ILI AT I ON MOWREY>C.L.Flor ida Power~>c Light Co.HOVEY>P..J.Florida Power 5 Light Co.REC IP.NAME REC IP I ENT AFF IL I AT I ON DOCKET¹05000250
SUBJECT:
LER 97-008-00:
on 970909>containment sump debris screens outside design basis due to stress damage was discovered.
Caused bg inadequate procedural'uidance Kc personnel error.Discrepancies found on screens'orrected.
w/971008 ltr.DISTRIBUTION CODE: IEEST COp IES RECEI'JED:
LTR l ENCL (SIZE: TITLE: 50.73/50.9 Licensee Event Report,(LER)
>Incident Rpt>etc.NOTES: REC IP I ENT ID CODE/NAME PD2-3 PD COPIES LTTR ENCL 1 REC IP I ENT ID CODE/NAME CPOTEAU>R COP I ES LTTR ENCL 1 0 INTERNAL: AEOD/S AB NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 2 1 1 1 1 1 1 1 AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HI CB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DET/EIB D EXTERNAL: L ST LOBBY NARD NOAC POORE>W.NRC PDR LITCO BRYCE>J H NOAC QUEENER>DS NUDOCS FULL TXT E N NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTETH TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COP I S REQUIRED: LTTR 0 ENCL 24 OCT 08 1997 L-97-250 10 CFR 50.73 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Re: Turkey Point Units 3 and 4 Docket Nos.50-250/251 Reportable Event: 97-00S Date of Event: September 9, 1997 Containment Sum Debris Screens Outside Desi n Basis Due to Screen Dama e The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.Sincerely, R.J.Hovey Vice President Turkey Point Plant CLM Attachment cc: Regional Administrator, USNRC Region II Senior Resident Inspector, USNRC, Turkey Point Plant 97i0i60056 97i008 PDR ADOCK 05000250 S PDR an FPL Group company llllllllllllllllllflllllllflflf fuff f f f LICENSEE EVENT REPORT (LER)FACIIITY NAME)I)TURKEY POINT UNITS 3&4 DOCKET NUMBER)2)05000250 PACE LT)1 OF 9 TITLE<<)Containment Sum Debris Screens Outside Desi n Basis Due To Screen Dama e EVENT DATE)5)DAY 9 9 97 YR 97 R)08 00 LER NUMBER(6)SEO)RPT DATE)2)HON DAY 10 08 97 OTHER FACILITIES INV.<8 FACILITY NAMES TURKCY POINT UNIT 6 DOCKET e (S)05000251 OPERATINC NODE{9)1/5 POKER LEVEL)10)100/0 LICENSEE CONTACT F'R THIS LER (12)C.L.MOWREY, COMPLIANCE SPECIALIST Tele hone Number (305)246-6204 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT HANUFACTURER NPRDS2 CAUSE SYSTEM COHP0 KENT MANUFACTURER NPRDS2 SUPPLEMENTAL REPORT EXPECTED{14)NO YES CI III Yee, coeplete EXPECTED SUBMISSION DATC)CXPECTED SUBMISSION DATE{15)DAY YEAR ABSTRACT (16)On September 9, 1997, Turkey Point Unit 4 was in Mode 5 in preparation for a refueling.
Inspection of the containment recirculation sumps revealed several gaps and a hole in the sump screens which were in excess of the design requirements.
On September 11, a similar condition was found on Unit 3 while in Mode 1.The gaps would allow debris larger than 3/8 inch to enter the flow stream to the containment spray nozzles, during the recirculation phase following a loss of coolant accident.Therefore, the screen damage resulted in both units operating outside the design basis.The causes of this event were inadequate procedural guidance, and personnel error (utility non-licensed personnel).
The Unit 3 screen was repaired on the spot'.The Unit 4 screens have also been repaired.FPL is clarifying the containment recirculation sump screen design basis.Additional procedural guidance is being developed to verify containment recirculation sump screen design details.Discussion of the event will be incorporated into the continuing training program at Turkey Point.
~=r LXCENSEE EVENT REPORT (LER)TEXT CONTXNUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.I.BACKGROUND INFORMATION The Emergency Core Cooling System (ECCS)containment recirculation sumps[NH:rvr]at Turkey Point Units 3 and 4 are collecting reservoirs provided to supply water to the Containment Spray (CS)[BE]and Safety Injection (SI)[BQ]Systems for long term recirculation following a Loss of Coolant Accident.Turkey Point Units 3 and 4 each have two containment recirculation sumps designated as the north and south sumps.The sumps are'hysically separated by reinforced concrete barriers, as shown in the attached sketch.Each sump provides the source of water, through its respective 14 inch pump suction line, to the Residual Heat Removal (RHR)pumps[BP:p], and includes a debris screen[BP:scn].The debris screen consists of 1/2 inch mesh overlaid with 1/4 inch mesh screen, both tied to and supported by a structural steel frame.II.DESCRIPTION OF THE EVENT On September 9, 1997, Turkey Point Unit 4 was in Cold Shutdown (Mode 5)in preparation for a refueling.
During an inspection of the ECCS containment recirculation sump, the sump screens were found to be inconsistent with design requirements.
Specifically, during an inspection of the containment recirculation sump area (performed in light of recent events at St.Lucie Unit 2 and with regard to industry activity concerning containment recirculation sumps), FPL identified a 1 inch diameter hole in the top of the south sump screen and gaps at the screen/floor interface on both sumps.The two largest gaps found were 13 inches long with a varying gap up to 5/8 inch, and 19 inches long with a varying gap up to 1/2 inch.Inspection of the north sump also revealed small gaps around a pipe penetrating the screen mesh.Although these gaps were relatively small, they exceeded the 1/4 inch mesh design requirement.
The condition was immediately brought to management attention and a condition report was generated for evaluation.
Since Unit 4 was in Mode 5, and since the containment recirculation sumps are not required in Mode 5, there was no immediate Unit 4 operability concern.However, immediate consideration was given to the issue of operability for Unit 3, which at the time was operating at full power.Since the particular activities causing the gaps in the Unit 4 sump screens were unknown and could have resulted from routine personnel activity in the sump screen area, FPL was concerned that similar conditions could exist on the operating
LICENSEE EVENT REPORT (LER)TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.unit.On September 10, 1997, FPL decided to perform a containment entry at power to inspect the Unit 3 containment recirculation sump screens.On September 10 and 11, 1997, preparations were made to perform on the spot repairs should any gaps be observed during the inspection.
A tailboard session was held among the participating personnel to ensure that each aspect of Unit 3 containment entry and inspection was understood.
On September 11, 1997, the at-power entries and inspections were made on the north and south sumps.No holes or gaps were found on the north sump screen.On the south sump screen no holes were found;however, a narrow gap (24 inches long with a varying gap up to 3/8 inch)was found at the floor/screen interface, similar to those gaps found on Unit 4.The Unit 3 gap was repaired immediately in accordance with prescribed instructions.
III.CAUSE OF THE EVENT The causes of this event were inadequate procedural guidance, and personnel error (utility non-licensed personnel).
Procedures Inadequate procedural guidance contributed to a delay in identifying the gaps associated with the containment recirculation sump screens.Specifically, the surveillance requirements in procedure O-SMM-051.3, Containment Closeout Inspection, did not provide sufficiently detailed inspection guidance for the sump screen enclosure to ensure compliance with the Turkey Point Updated Final Safety Analysis Report (UFSAR)design basis.The sump screen design and performance capability were evaluated in 1990 in response to NRC Information Notice 89-77,"Debris in Containment Emergency Sumps and Incorrect Screen Configuration" (November 21, 1989).Non-conformance reports were generated based on walkdown'inspections, and indicated discrepancies between as-built sump screen dimensions and those described in a UFSAR figure.The evaluation of these discrepancies concluded that available NPSH exceeds pump required NPSH even for the extreme conditions postulated, and that screen approach velocitie's are low, reducing the likelihood of debris accumulation.
Plant drawings were updated, and O-SMM-051.3 was revised to provide additional inspection criteria.
LICENSEE EVENT REPORT (LER)TEXT CONTINUATION FACZLITY NAME DOCKET NUMBER LER NUMBER'AGE NO.On December 3, 1993, Supplement 1 to Information Notice 89-77 was issued.FPL reviewed the supplement and determined that the new information had been adequately addressed in the 1990 effort.Nevertheless, this supplement was included in the January 1994 training reports.On February 24, 1995, O-SMM-51.3 was revised to add more specific inspection criteria including the 1/4 inch mesh requirement and an inspection hold point.This revision was initiated partly as the result of a 10CFR50.72 notification by another utility regarding sump screen configuration (later retracted by that utility).Even so, methods for ensuring strict conformance to the 1/4 inch mesh requirement
'were not effectively conveyed.The opportunity for earlier detection was missed, despite the substantial efforts associated with addressing the industry experience.
More recent generic communications, e.g., NRC Bulletin 93-02,"Debris Plugging of Emergency Core Cooling Suction Strainers," and Information Notice 96-10,"Potential Blockage By Debris of Safety System Piping Which Is Not Used During Normal Operation Or Tested During Surveillance," have focused on sump clogging and debris blockage rather than sump screen configuration.
FPL's response to these was directed toward minimizing debris in containment.
The lack of sufficient procedural guidance to ensure compliance with the UFSAR design basis was'not recognized.
Personnel The 1 inch hole found on the Unit 4 south sump screen may have been made to allow insertion of a drain hose.A similar hole found in the north sump screen in 1993 was determined to have been made to allow for a hose to pump water out of the sump.Specific causes for the gaps in the Unit 4 north and south sump screens and the Unit 3 south sump screen are unknown.These gaps may have been caused by running hoses under the screen or by incidental impact from personnel activity in the area.Personnel were not aware of the significance of maintaining sump screen configuration integrity.
Both sump screens are in highly contaminated, high radiation areas.There is no permanent lighting at either sump.The south sump is recessed several feet back under the refueling cavity, and there is le'ss than four feet of vertical clearance between the containment floor and the underside of the refueling cavity.Because of these dose concerns, contamination concerns, and physical impediments, previous inspections of the screens were performed from several feet away using flashlights.
These inspections were adequate to determine the presence of debris, and to detect major signs of degradation, structural distress or LICENSEE EVENT REPORT (LER)TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE No.abnormal corrosion.
However, these inspections were not adequate to detect small gaps or holes in the screen mesh.lV.ANALYSlS OF THE EVENT The Turkey Point Units 3 and 4 containment recirculation sump screens are designed to prevent all debris larger than that screened by 1/4 inch mesh from entering the RHR pumps and containment spray nozzles[BE:nzl]during the recirculation phase of a Loss of Coolant Accident.Since the screens are required to filter debris larger than 3/8 inch (see Design Basis discussion below), the presence of the hole and gaps placed the Turkey Point sump screen configurations outside the design basis as stated in the UFSAR.However, the gaps.~ere relatively small and not considered to create a hazard that would have compromised the ability of the ECCS or the Containment Spray system to perform their respective safety related functions.
The safety significance of the as-found conditions were evaluated and the results are summarized below.Design Basis The Turkey Point Units 3 and 4 UFSAR, Section 6.2.2 states,"Filtration of the water entering the residual heat removal pump suction piping is accomplished by screens located over the sumps which remove all debris 1/4 inch or larger." Section 6.4.2 of the UFSAR states,"During spray recirculation operation, the water is screened through a 1/4 inch mesh before leaving the containment recirculation sump.The spray nozzles are bronze and have a 3/8 inch diameter orifice." As such, the 1/4 inch filtration is nominal based on screen design, and is necessary to prevent debris from clogging the containment spray nozzle 3/8 inch opening.Therefore, the design basis for the screen is actually to prevent passage of rigid particles larger than 3/8 inch.This is accomplished by the 1/4 inch mesh since the diagonal is less than 3/8 inch.Section 6.2.2 of the UFSAR goes on to state,"In the unlikely event that one sump is 100%clogged and the other sump is 50%clogged, required circulation flow can still be maintained." Additionally, this section states,"Recirculation may start with a water depth of 2.93 feet on the containment floor at elevation 14 feet 0 inches.This is equivalent to 249,000 gallons of water at 283 degrees Fahrenheit.
The maximum velocity of approach to the screens is less than 0.5 foot/second."
LICENSEE EVENT REPORT (LER)TEXT CONTINUATION EACILZTY NAME DOCKET NUMBER LER NUMBER PAGE NO.Analysis of Safety Significance The Turkey Point Units 3 and 4 containment recirculation sumps are protected against debris resulting from a postulated Loss of Coolant Accident (LOCA)by screens.The hole and gaps in the containment recirculation sump screens could have allowed larger than design basis particles to pass into the Containment Spray system.The containment spray nozzles are capable of passing rigid particles of up to 3/8 inch.The spray nozzles would also be expected to pass larger, compressible particles without clogging.The Containment Spray system is designed to aid in reducing containment temperature and pressure following a postulated LOCA.The peak temperature and pressure occur about 20 seconds in the design basis LOCA scenario.Most of the cooling and pressure reduction of the containment atmosphere by containment spray occurs during the injection phase of the LOCA event, long before suction is transferred to the containment recirculation sump from the refueling water storage tank[BP:tk](about one hour after a design basis LOCA).Further, the containment spray cooling function is supplemented by the emergency containment coolers[BK:clr], which function regardless of the condition of the containment recirculation sump screens.The containment floor is relatively level, with no channels leading to the sumps.Flow into the sumps initially results from spillover during the flooding stage of the LOCA.Actual induced flow does not begin until recirculation operation is initiated, well after the initial blowdown subsides.By this time, most of the heavy debris is expected to have dispersed and settled out before nearing the sumps.Any debris entrainment onto the screens during blowdown is expected to be incidental with relatively little accumulation.
Therefore, very little debris is available to pass through any gaps or holes in the screens.The generated debris would be materials in the vicinity of the postulated pipe break which are dislodged by pipe whip or jet impingement forces.Since leak-before-break considerations are part of the Turkey Point design basis (NRC Safety Evaluation Report dated June 23, 1995), the dynamic effects of a main loop pipe break need not be considered in the design basis.As such, the postulated effects of pipe whip and jet impingement are from a smaller pipe in the reactor coolant pressure boundary and would significantly reduce the quantity of debris generated from a LOCA.Incidental transient materials are considered negligible and are not potential debris sources due to the current housekeeping practices and provisions for post-maintenance inspection and cleanup.
LICENSEE EVENT REPORT (LER)TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.The following is a summary of the supporting rationale regarding the type of debris expected during a LOCA and the effects of that debris on the containment recirculation sump screens: The screens are protected from internal missiles, pipe whip and jet impingement by major intervening structures.
Dynamic effects of a primary loop pipe break are not postulated based on leak-before-break considerations.
Therefore, the next largest credible pipe breaks are in the 12 inch pressurizer surge line and the 14 inch RHR hot leg connections.
Of the two, a surge line break is expected to generate more debris because of the double-ended jet effects near the break.The free-flow path of rising water to the sumps is arduous and hindered by intervening equipment, steel pipe supports and concrete structures.
Water is expected to approach the sumps as spreading, wide, open-channel flow as opposed to directed flow.As such, the debris, transport mechanisms of turbulence and fl'ow velocity are relatively low.Most of the debris is expected to be from thermal insulation:
reflective metal, asbestos, calcium silicate, and blanket insulation.
Reflective metal is likely to settle before reaching the sumps.Some of the asbestos and calcium silicate insulation would enter into suspension and pass harmlessly through the screens and spray nozzles.The larger pieces of insulation would become saturated and, along with its lagging, likely settle before reaching the sumps.The smaller particles of blanket insulation would be suspended in the recirculation fluid, and the portion of insulation remaining in larger sections would either settle or be hung up by obstructions approaching the sumps.Based on the preceding rationale, most of the generated debris is not likely to reach the sumps during the blowdown phase and will have settled out before nearing the screens.When the recirculation mode is initiated, the screens are expected to be relatively clean.Under these screen conditions, coupled with normal system alignment, approach velocities would be less than 0.2 foot per second, which is lower than velocities required in open-channel flow to initiate movement and transport of most settled debris.More likely the debris approaching the sump screen's will be metal foil, fine solid particles, and suspended calcium silicate and other materials having specific gravities slightly greater than one.As such the potential for large particles to reach the screens, to pass through the relatively
LICENSEE EVENT REPORT (LER)TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.small hole and gaps and to block the containment spray nozzles, is extremely low.Therefore, the as-found discrepancies are considered to be of low safety significance and would not compromise the ability of the ECCS and the Containment Spray system from performing their safety functions.
FPL also believes that the flow path from the sump screens to the fuel is not likely to be degraded significantly by debris.Large or heavy debris is unlikely to reach the sump screens, as demonstrated above.Debris which does have the potential to reach and pass through the gaps and holes discovered is not considered to have the capability to negatively impact the RHR, SI, or CS pumps (all large centrifugal pumps).Nevertheless, should credible debris reach the fuel, core damage is still unlikely.Due to the reduced decay heat at the time ECCS flow is established, core cooling flow requirements are only about 300 gpm.The decay heat and the associated fuel rod temperatures remain low enough that forced convective heat removal is not required.The ECCS flow serves to remove decay heat to prevent core uncovery.In this situation, redistribution of flow at the inlet, from blocked channels to different fuel channels, is of little importance as long as the active fuel remains covered, and there is no major blockage in the upper regions to prevent water circulation to all fuel channels.The trapping of debris at the lower spacer gri'ds will result in channels in the active fuel region remaining unblocked, and thus not jeopardize ECCS performance requirements.
Therefore, the fuel will not experience any adverse effects from credible sump debris.Based on the above assessment of Turkey Point's design basis (containment spray nozzles), and other potentially affected items (ECCS pumps, fuel), FPL has concluded that this condition did not represent a significant impact to the operation of components required for accident mitigat-'on.
Therefore, the protection of the public health and safety was not adversely affected by this event.V.CORRECTIVE ACTIONS 1)The discrepancies found on the Unit 4 containment recirculation sump screens have been corrected.
The repairs included enhancements to prevent inadvertent screen deformation due to activities in the area.
LICENSEE EVENT REPORT (LER)TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.2)The discrepancy found on the Unit 3 containment recircu-lation sump screen was corrected on the spot.Enhancements included during the Unit 4 repair to prevent inadvertent screen deformation will be implemented on Unit 3 during the next refueling outage, presently scheduled for Fall, 1998.3)4)To,augment current surveillance instructions, additional procedural guidance is being developed to verify containment recirculation sump screen design details.FPL is cl'arifying'the design basis requirements for the Turkey Point Units 3 and 4 containment recirculation sump screens in the UFSAR.Additionally, design documents will provide more containment recirculation sump screen design details.5)Training Information Bulletin No.97-44 was issued to inform all personnel of the restrictions when working in and around the containment recirculation sumps.6)This event report will be incorporated into the c'ontinuing training program at Turkey Point.7)FPL is evaluating the use of foreign material exclusion covers, to be placed over the sump screens during refueling outages.8)Personnel assigned to perform containment recirculation sump inspections will receive training on inspection criteria specific to the sumps.VI.ADDITIONAL INFORMATION There have been no other similar events previously reported at Turkey Point.EIIS Codes are shown in the format[EIIS SYSTEM: IEEE component function identifier, second component identifier (if appropriate)].
A simplified sketch of the Unit 4 containment building (basement elevation) is attached.
P EL.14'-0" REGEN.HEAT EXCHANGER 4E200 4'I UNIT 4 a,'ONTAINMENT 8c REACTOR COMMON OIL COLLECTION TANK\\I GENITOR 4E210B 4P2009 LOOP B REACTOR COOLANT PUMP~'r PLATFORM El 25'-10+0/<c'/>, i(y~dg INCOR E INSTRUMENTATION
,4 dr/I PRESSURIZER (ABOVE)4 ST GEN JRTOR 4E-210C p//././..'EACTOR COOIANT PUMP LOWER 4P200C REACTOR 4T237 4 LOOP C LOOP A STEAM GENERATO 4E-210A 4P200A/I 4 4~'ANOING.EL.21'-4 CONTAINMENT SOUTH SUMP~4 EXCESS LETDOWN EAT EXCH.~~c EL21'-6~I J;8'-6" 4E202 UPPER INTERNALS d STORACE EL.14'-0" CONTAINMENT NORTH SUMP',d ATTACHMENT To LER 97-008-00 SIMPLIFIED SKETCH OF UNIT 4 CONTAINMENT BUILDING IBASEMENT ELEVATION)