IR 05000282/2002008: Difference between revisions

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{{IR-Nav| site = 05000282 | year = 2002 | report number = 008 | url = https://www.nrc.gov/reactors/operating/oversight/reports/prai_2002008.pdf }}
{{Adams
| number = ML023040324
| issue date = 10/30/2002
| title = IR 05000282-02-008, IR 05000306-02-008, on 07/01/02 - 09/30/02, Prairie Island, Maintenance Effectiveness and Identification and Resolution of Problems
| author name = Riemer K
| author affiliation = NRC/RGN-III/DNMS
| addressee name = Nazar M
| addressee affiliation = Nuclear Management Co, LLC
| docket = 05000282, 05000306
| license number = DPR-042, DPR-060
| contact person =
| document report number = IR-02-008
| document type = Inspection Report, Letter
| page count = 36
}}
 
{{IR-Nav| site = 05000282 | year = 2002 | report number = 008 }}
 
=Text=
{{#Wiki_filter:ber 30, 2002
 
==SUBJECT:==
PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 50-282/02-08; 50-306/02-08
 
==Dear Mr. Nazar:==
On September 30, 2002, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on September 27, 2002, with you and members of your staff.
 
This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
Based on the results of this inspection, the NRC identified two issues of very low safety significance (Green). One of the issues was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it has been entered into your corrective action program, the NRC is treating the issue as a Non-Cited Violation, in accordance with Section VI.A.1 of the NRCs Enforcement Policy.
 
If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 801 Warrenville Road, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Prairie Island Nuclear Generating Plant.
 
In response to the terrorist attacks on September 11, 2001, the NRC issued an Order and several threat advisories to commercial power reactors to strengthen licensees capabilities and readiness to respond to a potential attack. The NRC established a deadline of September 1, 2002, for licensees to complete modifications and process upgrades required by the order. To confirm compliance with this order, the NRC issued Temporary Instruction 2515/148 and over the next year, the NRC will inspect each licensee in accordance with this Temporary Instruction. The NRC continues to monitor overall security controls and may issue additional temporary instructions or require additional inspections should conditions warrant.
 
In accordance with 10 CFR 2.790 of the NRC's Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,
/RA/
Kenneth Riemer, Chief Branch 5 Division of Reactor Projects Docket Nos. 50-282; 50-306 License Nos. DPR-42; DPR-60
 
===Enclosure:===
Inspection Report 50-282/02-08; 50-306/02-08
 
REGION III==
Docket Nos: 50-282; 50-306 License Nos: DPR-42; DPR-60 Report No: 50-282/02-08; 50-306/02-08 Licensee: Nuclear Management Company, LLC Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2 Location: 1717 Wakonade Drive East Welch, MN 55089 Dates: July 1 through September 30, 2002 Inspectors: J. Adams, Senior Resident Inspector D. Karjala, Resident Inspector R. Daley, Reactor Engineer R. Walton, Operations Specialist Approved by: Kenneth Riemer, Chief Branch 5 Division of Reactor Projects
 
=SUMMARY OF FINDINGS=
IR 05000282-02-08, 05000306-02-08; Nuclear Management Company, LLC; on 07/01 -
 
9/30/02, Prairie Island Nuclear Generating Plant, Units 1 & 2. Maintenance Effectiveness and Identification and Resolution of Problems.
 
This report covers a 3-month period of baseline resident inspection. The inspection was conducted by Region III inspectors and the resident inspectors. Two findings of significance were identified. The significance of most findings is indicated by their color (Green, White,
Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
 
A.      Inspection Findings
 
===Cornerstone: Initiating Events===
: '''Green.'''
A finding of very low safety significance was identified by the inspectors investigating the repeat failures of the external circulating water intake screen bypass gates to fully open and to latch in the open position. The finding resulted from performance deficiencies associated with the establishment of an appropriate maintenance rule safety significance classification of the external circulating water intake screen bypass gates. The bypass gates were classified as low safety significant components, not as low safety significant standby components as specified by industry maintenance rule guidance.
 
This finding was more than minor because it increased the likelihood of a reactor trip event due to a loss of circulating water. The finding was of very low safety significance because it did not contribute to the likelihood of a primary or secondary system loss of coolant accident, did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available, and did not increase the likelihood of a fire or internal/external flood. A violation determination could not be completed until appropriate maintenance rule performance criteria have been established and will be tracked by an Unresolved Item. (Section 1R12.1)
 
===Cornerstone: Mitigating Systems===
: '''Green.'''
A finding of very low safety significance was identified by the inspectors during a review of licensee corrective action taken to address concerns documented in Licensee Event Report (LER) 1-98-15 pertaining to Appendix R potential flow diversion paths.
 
The primary cause of this finding was related to a failure to correct or implement appropriate compensatory actions to address potential flow diversion paths that had existed since 1999.
 
This finding is more than minor because, if left uncorrected, the finding would become a more significant safety concern. Failure to resolve fire protection non-compliance items and failure to establish appropriate compensatory measures could potentially affect the availability, reliability, and capability of fire protection safe shutdown equipment and response efforts. The inspectors determined that the finding was not suitable for SDP analysis. However, the finding was determined to be of very low safety significance because the probability of having a fire event in the affected areas such that the fire would cause more than one valve to reposition to cause a flow diversion was very low.
 
This was determined to be a Non-Cited Violation (NCV) of 10 CFR Part 50, Appendix B,
Criterion XVI. (Section 4OA2.1)
 
===Licensee-Identified Violations===
 
A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and corrective action tracking numbers are listed in Section 4OA7 of this report.
 
=REPORT DETAILS=
 
===Summary of Plant Status===
 
Unit 1 was operated at or near full power for the entire inspection period. Unit 2 was operated at or near full power for the entire inspection period.
 
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R04}}
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
===.1 Partial Walkdowns===
 
====a. Inspection Scope====
The inspectors performed partial walkdowns of accessible portions of trains of risk-significant mitigating systems equipment during times when the trains were of increased importance due to the redundant trains or other related equipment being unavailable.
 
The inspectors utilized the valve and electric breaker checklists listed at the end of this report to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders (WOs) and Corrective Action Program (CAP) Action Requests (ARs) associated with the trains to verify that those documents did not reveal issues that could affect train function. The inspectors used the information in the appropriate sections of the Updated Safety Analysis Report (USAR) to determine the functional requirements of the systems.
 
The inspectors verified the alignment of the following trains:
* D1 emergency diesel generator during the unavailability of the D2 emergency diesel generator on July 29, 2002;
* 12 safety-related cooling water pump and 121 safety-related traveling screen during the unavailability of the 22 safety-related cooling water pump and 122 safety-related traveling screen on July 30, 2002; and
* 22 and 121 safety-related cooling water pumps following the emergent failure of the 12 safety-related cooling water pump on August 15, 2002.
 
The inspectors reviewed the ARs listed at the end of this report to verify that the licensee was identifying issues at an appropriate threshold and entering them into their corrective action program. The inspectors also reviewed ARs to verify that minor deficiencies identified during these inspections were entered into the licensees corrective action system.
 
====b. Findings====
No findings of significance were identified. {{a|1R05}}
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
===.1 Area Walkdowns===
 
====a. Inspection Scope====
The inspectors conducted fire protection walkdowns that were focused on the availability and accessibility of fire protection equipment, the condition of fire fighting equipment, the control of transient combustibles, and the condition and operating status of installed fire barriers as described in fire hazards analysis and pre-fire plans. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events (IPEEE); their potential to impact equipment which could initiate a plant transient; or their impact on the plants ability to respond to a security event. The inspectors reviewed the as-found condition of fire doors, dampers, penetration seals, fire detectors, sprinklers, fire hoses and extinguishers, comparing the as-found conditions to the configuration described in fire hazards analysis and pre-fire plans. The inspectors also reviewed equipment to verify that it was in its appropriate location, was available for immediate use, and was not obstructed. The as-found transient combustible loading was also reviewed to verify that it was within the analyzed limits. The inspectors reviewed the ARs listed at the end of this report to verify that the licensee was identifying fire protection issues at an appropriate threshold and entering them into their corrective action program.
 
The inspectors assessed the following areas:
* Fire Area 13, Unit 1 and 2 Control Room on July 13, 2002;
* Fire Area 18, Unit 1 and 2 Cable Spreading and Relay Rooms on July 11, 2002;
* Fire Area 35, 21 Battery Room on July 10, 2002;
* Fire Area 36, 22 Battery Room on July 11, 2002;
* Fire Area 69, Turbine Ground Floor and Mezzanine;
* Fire Area 101, D5 Emergency Diesel Generator Room; and
* Fire Area 102, D6 Emergency Diesel Generator Room.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Fire Brigade Drills===
 
====a. Inspection Scope====
The inspectors observed the performance of a fire brigade drill in the Unit 1 electrical bus 150/160 room on July 19, 2002. This area was considered risk significant because a fire could cause a unit trip initiating event. The inspectors observed the initial response of the fire brigade leader, the fire brigade, security personnel, and the duty Emergency Medical Technician. The inspectors observed establishment of communications with the control room, the brigade response strategy briefing, and the brigades response to the simulated fire. The inspectors used the NRC inspection procedure listed above and the documents listed at the end of this report to evaluate the drill. At the conclusion of the drill, the inspectors observed the licensees drill critique to ensure that any weaknesses noted during the drill were addressed.
 
====b. Findings====
No findings of significance were identified. {{a|1R11}}
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
 
====a. Inspection Scope====
On September 10, 2002, the inspectors observed an operating crew during a requalification examination on the simulator. The inspectors evaluated crew performance in the areas of:
* clarity and formality of communications;
* ability to take timely, appropriate, and safe actions;
* prioritization, interpretation, and verification of alarms;
* procedure use;
* control board manipulations;
* oversight and direction from supervisors; and
* group dynamics.
 
The inspectors compared crew performance in the above areas to the critical tasks listed in the exercise guide at the end of this report. The inspectors also compared simulator configurations with actual control room board configurations. The inspectors attended the post-examination critique to verify that the licensee evaluators noted the same weaknesses observed by the inspectors and discussed them during the critique.
 
====b. Findings====
No findings of significance were identified. {{a|1R12}}
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
===.1 External Circulating Water Intake Screen Bypass Gate Repeat Failures===
 
====a. Inspection Scope====
On August 20, 2002, while investigating the repeat failures of the external circulating water intake screen bypass gates, the inspectors identified that the maintenance rule safety significance classification of the external circulating water intake screen bypass gates was inappropriate.
 
====b. Findings====
The inspectors identified a Green finding associated with the inappropriate maintenance rule safety significance classification of the external circulating water intake screen bypass gates. The bypass gates were classified as low safety significant components, contrary to the NRC-endorsed, industry guidance of NUMARC 93-01.
 
On June 19, 2002, the sequential loss of external circulating water intake traveling screens caused a low intake bay level. In response to the intake bay low level, operators initiated the opening of the intake bypass gates by isolating power to the bypass gates. This action simulated a loss of power to the traveling screens and should have caused the bypass gates to open hydraulically. However, the 121 intake bypass gate failed to open and the 122 only partially opened. The partial opening of 122 gate allowed sufficient makeup to the intake bay to prevent a loss of circulating water and reactor trip.
 
The inspectors conducted a historical evaluation of the intake bypass gates performance. The inspectors noted a history of problems with the failure of the intake gates to fully open and to latch in the open position. Based on the number of repeat failures documented in the licensees corrective action program, the inspectors evaluated whether the intake bypass gate were scoped in accordance with the maintenance rule, 10 CFR 50.65; whether the intake bypass gates had been assigned the proper safety significance classification; whether the established performance criteria was appropriate; whether the performance problems associated with intake bypass gates constituted maintenance rule functional failures or repeat maintenance rule functional failures; and whether the intake bypass gates were properly classified as (a)(1) or (a)(2).
 
The inspectors determined that the bypass gates were properly included in the scope of the maintenance rule, but found that the licensee had inappropriately classified the bypass gates as low safety significant components. The licensee should have recognized the bypass gates as low safety significant standby components since their function was to open automatically on loss of power to the external circulating water intake traveling screens, or on a high differential level across the external circulating water intake traveling screens. Since the bypass gates were improperly classified, the licensees performance criteria were also inappropriate and bypass gate failures were not properly evaluated for maintenance preventable functional failures. The licensee entered this condition into their corrective action program with AR CAP 024744. A list of documents reviewed during this inspection is included at the end of this report.
 
The inspectors determined that the inappropriate maintenance rule safety significance classification of the intake bypass gates was a performance deficiency warranting a significance evaluation in accordance with Inspection Manual Chapter IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on April 29, 2002. The inspectors determined that the finding was more than minor because it:
: (1) involved the equipment performance attribute of the Initiating Events cornerstone, and
: (2) affected the cornerstone objective of limiting the likelihood of those events that upset plant stability during power operations.
 
The inspectors determined that the finding could be evaluated in accordance with IMC 0609, Significance Determination Process, because the finding was associated with an increase in the likelihood of an initiating event. For the Phase 1 screening, the inspectors determined that the finding did not contribute to the likelihood of a primary or secondary system loss of coolant accident, did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available, and did not increase the likelihood of a fire or internal/external flood. This finding (FIN 50-282/306/02-08-01), screened out of the Phase 1 SDP, was determined to be of very low safety significance.
 
The inspectors discussed the potential of a violation of NRC maintenance rule requirements with Region III, Division of Reactor Safety inspectors. Based on that discussion, the inspectors concluded that a violation determination could not be completed until appropriate performance criteria for the low safety significant standby safety significance classification were first established by the maintenance rule expert panel. Following the establishment of appropriate performance criteria, a maintenance rule functional failure evaluation of all bypass gate failures for the previous 2 years can be performed. If the results of that evaluation show that the intake bypass gates should have been classified as (a)(1) based on their performance and were not, a violation may exist. This is an Unresolved Item (URI 50-282/306/02-08-02).
 
===.2 Repeat Failures of the Containment Fan Cooling Unit Cooling Water Return Orifice===
 
Bypass Valve, CV 39201
 
====a. Inspection Scope====
On August 13, 2002, the inspectors reviewed AR CAP 023812 that identified a repeat failure of the containment fan cooling unit cooling water return orifice bypass valve, CV 39201. The proper operation of CV 39201 supports the performance of the safety-related maintenance rule function of providing cooling water to the containment fan cooler Units 11 and 13 and was within the scope of the maintenance rule.
 
The inspectors performed an in-office review of work orders and corrective action program documents associated with the failures of CV 39201. The inspectors compared the licensees maintenance documentation to the requirements contained in the administrative work instruction (AWI) procedures for the performance of nuclear maintenance, investigation, and troubleshooting. The documents reviewed are listed at the end of this report. The inspectors also conducted an extent-of-condition assessment by searching the licensees corrective action program database for similar failures of valves in redundant containment fan cooling unit trains.
 
The inspectors reviewed the licensees implementation of the maintenance rule for the repeat failures of CV 39201 by comparing their actions to the requirements contained in the Maintenance Rule, 10 CFR 50.65, and Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, NUMARC 93-01. The inspectors evaluated whether the CV 39201 was scoped in accordance with the maintenance rule; whether the performance problems associated with CV 39201 constituted maintenance rule functional failures; whether the cooling water system had been assigned the proper safety significance classification; whether the system was properly classified as (a)(1) or (a)(2); and whether appropriate performance criteria and/or goals were established. The above aspects were evaluated using the maintenance rule scoping and report documents listed at the end of this report. For each structure, system and component reviewed, the inspectors also reviewed the significant work orders (WO) and ARs listed at the end of this report to verify that failures were properly identified, classified, and corrected, and that unavailable time had been properly calculated.
 
====b. Findings====
No findings of significance were identified. {{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
 
====a. Inspection Scope====
The inspectors reviewed the licensees management of plant risk during emergent maintenance activities and during activities where more than one risk significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety significant mitigating equipment. The inspection was conducted to verify that evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate. Inspectors reviewed the licensees daily configuration risk assessment records, observed shift turnover meetings, observed daily plant status meetings, and reviewed risk assessment documents listed at the end of this report to verify that the equipment configurations were properly listed, that protected equipment was identified and controlled, and that significant aspects of plant risk were communicated to the necessary personnel. The inspectors discussed daily and emergent risk assessments with risk assessment engineers and operators.
 
The inspectors reviewed the following emergent and planned maintenance activities associated with maintenance rule risk significant systems:
* Repair of the 22 safety injection (SI) pump while Unit 2 was in a yellow risk situation because the 22 residual heat removal (RHR) pump and heat exchanger were out-of-service for preventive maintenance;
* Testing of the 22 turbine-driven auxiliary feedwater (AFW) pump while Unit 2 was in a yellow risk situation because the 125 air compressor was out-of-service for repair;
* Testing of the 22 turbine-driven auxiliary feedwater (AFW) pump while the 122 control room chiller was out-of-service for repair;
* Quarterly check valve testing on the 21 motor-driven AFW pump while the train A inadequate core cooling monitor was out-of-service;
* Emergent work due to failure of the 12 diesel-driven cooling water pump (DDCLP);
* The 12 motor-driven AFW pump failed a surveillance test due to sluggish operation of the outboard motor slinger ring; and
* Unit 1 in yellow risk configuration while D2 diesel generator, 18 inverter, 11 charging pump, and the 12 motor-driven AFW pump were out-of-service for maintenance.
 
The inspectors reviewed several ARs to verify that problems associated with plant risk assessment were identified at an appropriate threshold, and that corrective actions commensurate with the significance of the issue were identified and implemented. A detailed list of the documents reviewed during this inspection is included at the end of the report.
 
====b. Findings====
No findings of significance were identified. {{a|1R14}}
==1R14 Personnel Performance Related to Non-Routine Plant Evolutions and Events==
{{IP sample|IP=IP 71111.14}}
 
====a. Inspection Scope====
On August 23, 2002, the inspectors completed their review of licensee personnel performance during a June 19, 2002, transient that resulted in a decreasing intake bay level. The level decrease was caused by the loss of intake traveling screens and a failure of the intake bypass gates to open. The inspectors compared operator performance to the applicable response procedures. The inspectors reviewed plant data and operator logs to determine if the plant responded as designed. The inspectors also reviewed the licensees root cause evaluation to verify that noted deficiencies were recognized and entered in their corrective actions program. The documents reviewed during this inspection are listed at the end of this report.
 
====b. Findings====
No findings of significance were identified. {{a|1R15}}
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}
 
====a. Inspection Scope====
The inspectors evaluated plant conditions, selected ARs, and CAP documents for risk significant components and systems in which operability issues were questioned on the dates that appear in the list below. These conditions were evaluated to determine whether the continued operability of the components and systems was justified. The inspectors compared the component or systems function and design criteria in the applicable sections of the Technical Specifications (TSs) and USAR to the licensees evaluations in order to verify that the components and systems were operable. The inspectors verified that compensatory measures necessary to maintain operability were in place, functioned as intended, and were properly controlled. A detailed list of the documents reviewed during this inspection is included at the end of the report.
 
The inspectors evaluated the following conditions:
* 12 and 22 diesel-driven cooling water pump speed oscillations on July 10, 2002;
* The hot chemical laboratory ventilation in the auxiliary building draws air from the turbine building at a flow rate sufficient to prevent the auxiliary building special ventilation system from achieving a negative pressure with the doors to the hot chemical laboratory open on July 15, 2002;
* The Unit 2 reactor missile shield was weighed during the 2002 refueling outage and found to weigh more than listed in the USAR on July 16, 2002;
* Operation of the 21 AFW pump with insufficient packing leakoff on August 12, 2002;
* 22 containment fan cooling unit high vibrations on August 22, 2002;
* System grid voltage dropped to the point where the Grid Security Analysis for the Prairie Island Two Unit Trip Contingency failed on August 26, 2002; and
* Inadequate thread engagement on 22 SI pump suction flange bolts September 24, 2002.
 
====b. Findings====
No findings of significance were identified. {{a|1R16}}
==1R16 Operator Workarounds (OWA)==
{{IP sample|IP=IP 71111.16}}
===.1 Review of Selected Workarounds===
 
====a. Inspection Scope====
On August 7, 2002, the inspectors reviewed OWAs associated with the 12 station battery charger. During an accident or transient that results in a safety injection, the 12 station battery charger may require manual restarting. The inspectors verified that the functional capability of the system, human reliability in responding to an initiating event, or the ability of operators to implement abnormal or emergency operating procedures was not significantly affected. The inspectors reviewed the applicable sections of USAR and TSs and discussed the OWAs with control room operators. A detailed list of the documents reviewed during this inspection is included at the end of the report.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Cumulative Effects of OWAs===
 
====a. Inspection Scope====
On August 12, 2002, the inspectors reviewed the cumulative effect of all identified OWAs to determine whether the cumulative conditions had a significant impact on plant risk or on the operators ability to respond to a transient or an accident. The inspectors used the NRC inspection procedure listed above and the documents listed at the end of this report to evaluate the list of OWAs.
 
====b. Findings====
No findings of significance were identified. {{a|1R19}}
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}
 
====a. Inspection Scope====
The inspectors reviewed post-maintenance testing activities associated with maintenance on important mitigating, barrier integrity, and support systems to ensure that the post-maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. The inspectors reviewed the appropriate sections of the TSs, the USAR, and maintenance documents to determine the systems safety functions and the scope of the maintenance. In addition, the inspectors reviewed ARs to verify that minor deficiencies identified during these inspections were entered into the licensees corrective action system. A detailed list of the documents reviewed during this inspection is included at the end of the report.
 
The inspectors observed and evaluated the post-maintenance activities for the following:
* Refueling water storage tank (RWST) to SI pumps header isolation valve MV-32182 following modification to the control circuit on July 29, 2002;
* D2 6-month inspection on July 30, 2002;
* 22 diesel-driven cooling water pump following replacement of a jacket water heater, starting air compressor preventive maintenance (PM), and pump bearing seal water filter change and line flush on July 31, 2002;
* 21 RHR pump following annual PM on August 8, 2002;
* 122 control room chiller and air handler PM, and chilled water pump seal replacement on August 26, 2002; and
* 22 RHR pump following annual PM on September 19, 2002.
 
====b. Findings====
No findings of significance were identified. {{a|1R22}}
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
 
====a. Inspection Scope====
The inspectors observed selected surveillance tests and/or reviewed test data to verify that the equipment performance met Surveillance Procedure (SP) acceptance criteria.
 
The inspectors verified that the tested equipment was capable of performing its intended safety functions as described in TSs and the USAR. The inspectors verified that the testing met the required TS frequency; that the tests were conducted in accordance with the applicable procedures; that operators met prerequisites and established the proper plant conditions; and that the results of the tests were properly reviewed and recorded.
 
In addition, the inspectors reviewed several ARs to verify that the licensee was identifying surveillance problems at an appropriate threshold, and that corrective actions commensurate with the significance of the issue were identified and implemented. A detailed list of the documents reviewed during this inspection is included at the end of the report.
 
The following tests were observed and/or evaluated:
* SP 2102, 22 Turbine-Driven AFW Pump Monthly Test on July 24, 2002;
* SP 1093, D1 Diesel Generator Monthly Slow Start Test on September 9, 2002;
* SP 1106A, 12 Diesel Cooling Water Pump Monthly Test on September 12, 2002;
* SP 2307, D6 Diesel Generator 6-Month Fast Start Test on September 16, 2002; and
* SP 2295, D5 Diesel Generator 6-Month Fast Start Test on September 30, 2002.
 
====b. Findings====
No findings of significance were identified.
 
==SAFEGUARDS==
 
===Cornerstone: Physical Protection===
 
3PP3 Response to Contingency Events (71130.03)
 
====a. Inspection Scope====
The Office of Homeland Security developed a Homeland Security Advisory System (HSAS) to disseminate information regarding the risk of terrorist attacks. The HSAS implements five color-coded threat conditions with a description of corresponding actions at each level. NRC Regulatory Information Summary (RIS) 2002-12a, dated August 19, 2002, NRC Threat Advisory and Protective Measures System, discusses the HSAS and provides additional information on protective measures to licensees.
 
On September 10, 2002, the NRC issued a Safeguards Advisory to reactor licensees to implement the protective measures described in RIS 2002-12a in response to the Federal government declaration of threat level Orange. Subsequently, on September 24, 2002, the Office of Homeland Security downgraded the national security threat condition to Yellow and a corresponding reduction in the risk of a terrorist threat.
 
The inspectors interviewed licensee personnel and security staff, observed the conduct of security operations, and assessed licensee implementation of the threat level Orange protective measures. Inspection results were communicated to Region III and Headquarters security staff for further evaluation.
 
====b. Findings====
No findings of significance were identified.
 
==OTHER ACTIVITIES==
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
 
====a. Inspection Scope====
The inspectors reviewed the performance indicator data submitted by the licensee for completeness and accuracy, and to verify that the licensee had reported data in accordance with the guidance provided by the Nuclear Energy Institute (NEI). The inspectors reviewed documents listed at the end of this report for performance indicator data for initiating events, mitigating systems, and barrier integrity cornerstones. The inspectors reviewed the following performance indicators from the 3rd quarter 2001 through the 2nd quarter 2002:
* Safety system functional failures on July 31, 2002;
* Reactor coolant system specific activity on August 2, 2002; and
* Unplanned power changes on August 26, 2002.
 
====b. Findings====
No findings of significance were identified. {{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
===.1 Failure to Correct Deficiencies Involving Potential Flow Diversion Paths===
 
====a. Inspection Scope====
On August 6, 2002, during a selected issues followup inspection of corrective actions to address potential Appendix R flow diversion paths concerns, the inspectors identified that specified corrective action to implement modifications and/or administrative controls to resolve flow diversion issues were not completed.
 
====b. Findings====
The inspector identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI, for failure to correct deficiencies adverse to quality involving potential flow diversion paths.
 
These deficiencies had existed since 1999, but had not been corrected. Additionally, no compensatory actions had been established to address these flow diversion paths.
 
The licensee issued Condition Report (CR) 19982008 and LER 1-98-15 to identify and report concerns associated with the effects of potential spurious opening of the Unit 1 and Unit 2 containment sump B to RHR motor-operated valves. Specifically, it was noted that if any pair of the valves were to spuriously open during a fire, the RWST would drain to the containment sump leaving a less than required volume of borated water available for make-up. In fire protection terminology, this type of issue is referred to as a flow diversion issue, since the diversion of flow may potentially affect safe shutdown capability in the event of a fire.
 
As a result of the LER, the licensee issued two specific corrective action items to address generic concerns associated with this issue. The first action item required the licensee to review the Appendix R safe shutdown list against the appropriate flow diagrams to ensure that all other flow paths vulnerable to diversion were included in the Safe Shutdown
 
=====Analysis.=====
The second action item was to implement modifications and/or administrative controls to resolve this issue (and any other flow diversion issues identified subsequent to the LER). The second action item had not been completed as of August 6, 2002.
 
The first action item was completed and closed in 1999. The results of the review of flow diversion pathways was documented and issued as calculations GEN-PI-034, 035, 036, 037, 038, and 040. These calculations identified a large number of safe shutdown required flow diversion components. However, the calculations ambiguously stated in their Conclusion sections, Those components not previously identified are indicated with a note in the attached table. Subsequent analysis may show that some of the components can be eliminated from the Appendix R component list. The calculations were extremely conservative and identified all potential flow diversion paths. Because of this, compensatory measures were never established for the potential flow paths. Since the engineering staff knew that the calculations were extremely conservative, the licensee decided to wait and perform the second action item to implement modifications and/or administrative controls to resolve this issue (and any other flow diversion issues identified subsequent to the LER) as specific flow paths were identified.
 
Since the calculations identified required flow diversion paths, the NRC inspector asked the licensee why compensatory actions were not in place. As a result of this questioning, the licensee documented this issue in their corrective action program as AR CAP 024536. In AR CAP 024536, the licensee stated that the calculations were potentially misleading and do not meet the original intention behind their issuance, they should be canceled. Subsequently, all six calculations were canceled.
 
The flow diversion review committed to in LER 1-98-15 was to identify if any flow diversion paths existed. An additional corrective action document was initiated by the licensee, AR CAP 024537, which documented that this LER action item was inappropriately closed, since the calculations did not fully address the LER commitment.
 
Also, AR CAP 024537 recommended that the action item either be reopened or a new action item be entered to track the eventual completion of this commitment.
 
As a result, subsequent to the NRC identifying these issues, the licensee performed another review of flow diversion paths. While this review was again conservative, the licensee had procedure actions and guidance that would address spurious operations in these flow diversion paths in the event of a fire.
 
Criterion II of 10 CFR Part 50, Appendix B, requires that the licensee establish a quality assurance program. It states, This program shall be documented by written policies, procedures, or instructions and shall be carried out throughout plant life in accordance with those policies, procedures, or instructions.
 
The Prairie Island Quality Assurance Plan Appendix C implements Quality Assurance requirements for the Fire Protection Program. Section 12.2 states that work control process procedures shall be used to correct equipment failure, malfunctions, deficiencies, and defective components of fire protection systems.
 
In 10 CFR Part 50, Appendix B, Criterion XVI, it states that Measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to Criterion XVI of 10 CFR Part 50, Appendix B, deficiencies adverse to quality involving potential flow diversion paths were known to exist since 1999, but were not corrected. Additionally, no compensatory measures for these deficiencies were established to address these flow diversion paths.
 
This finding is more than minor because, if left uncorrected, the finding would become a more significant safety concern. Failure to resolve fire protection non-compliance items and failure to establish appropriate compensatory measures could potentially affect the availability, reliability, and capability of fire protection safe shutdown equipment and response efforts. This finding was not suitable for SDP analysis. However, this issue has very low safety significance (Green) because the probability of having a fire event in the affected areas such that the fire would cause more than one valve to reposition to cause a flow diversion was very low. Since the licensee entered this finding into their corrective action program with AR CAP 024536 and AR CAP 024537, this violation is being treated as an NCV in accordance with VI.A.1 of the NRCs Enforcement Policy (NCV 50-282/306/02-08-03) .
 
===.2 Routine Review of Identification and Resolution of Problems===
 
====a. Inspection Scope====
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action system at an appropriate threshold, that corrective actions were performed in a timely manner, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action system as a result of inspectors observations are generally denoted in the report.
 
====b. Findings====
No findings of significance were identified. {{a|4OA3}}
==4OA3 Event Followup==
{{IP sample|IP=IP 71153}}
(Closed) LER 1-02-01: Condition Prohibited by TSs Due to Potential for Auxiliary Building Special Vent Zone Boundary Degradation.
 
The LER concerns a modification during plant construction in 1973 to the hot chemistry lab ventilation, which was within the auxiliary building special ventilation zone (ABSVZ).
 
The modification supplied ventilation to the lab from the turbine building. If the lab doors were open during an accident that generated a safety injection signal, the lab supply booster fans, which do not receive a trip signal on a safety injection, would continue to supply air, affecting the ability of the ABSVZ system to perform its required functions to maintain a negative pressure. Technical Specification 3.6.E.2 requires that openings in the ABSVZ be under direct administrative control and be reduced to less than 10 square feet within 6 minutes following an accident. Contrary to the above, the hot chemistry lab doors were not under direct administrative control. The licensee entered this condition into their corrective action program with AR CAP 024185. The inspectors reviewed this licensee-identified finding and determined that it met the criteria to be considered a NCV of TS 3.6.E.2 (see Section 4OA7). The finding was screened by the inspectors using the SDP and determined to be of very low safety significance since the finding only represents a degradation of the radiological barrier function provided for the auxiliary building. No new significant issues were identified during the review of the LER.
 
Inspectors verified that the licensee implemented immediate actions to place the hot chemistry lab doors under direct administrative control by adding them into the ABSVZ boundary control log.
 
{{a|4OA5}}
==4OA5 Other Activities==
 
===.1 Review of Institute of Nuclear Power Operations Report===
 
On September 13, 2002, the inspectors completed a review of the final report, dated July 2002, for the Institute of Nuclear Power Operations, November 2001 Evaluation.
 
{{a|4OA6}}
==4OA6 Meeting(s)==
 
===.1 Exit Meeting===
 
The resident inspectors presented the inspection results to Mr. M. Nazar and other members of licensee management at the conclusion of the inspection on September 27, 2002. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
 
{{a|4OA7}}
==4OA7 Licensee-Identified Violation==
 
The following violation of very low significance was identified by the licensee and is a violation of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.
 
===Cornerstone: Reactor Safety===
 
Technical Specification 3.6.E.2 states that openings in the ABSVZ are permitted provided they are under direct administrative control and can be reduced to less than 10 square feet within 6 minutes following an accident. As described in AR CAP 024185 and LER 1-02-01, on July 16, 2002, the licensee identified that there were no direct administrative controls associated with the hot chemistry lab doors. A 1973 design change to the hot chemistry lab ventilation could affect the ability of the ABSVZ system to perform its required functions to maintain a negative pressure with these doors open.
 
The finding was determined to be of very low safety significance since the finding only represented a degradation of the radiological barrier function provided for the auxiliary building.
 
KEY POINTS OF CONTACT Licensee T. Amundson, Manager Business Support P. Huffman, Manager of System Engineering B. Jefferson, Director Site Operations J. Jensen, Production Planning Manager A. Johnson, General Superintendent Radiation Protection and Chemistry J. Kivi, Licensing Engineer R. Lingle, Operations Manager M. McKeown, Manager of Design Engineering L. Meyer, General Superintendent Plant Maintenance M. Nazar, Site Vice President S. Northard, Director of Engineering J. Waddell, Superintendent Security M. Werner, Plant Manager R. Womack, Manager of Engineering Programs LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened 50-282/306/02-001-00      LER    Condition Prohibited by TSs Due to Potential for Auxiliary Building Special Vent Zone Boundary Degradation (Section 4OA3)50-282/306/02-08-01      FIN    Inappropriate Maintenance Rule Safety Significance Classification of the External Circulating Water Intake Screen Bypass Gates (Section 1R12.1)50-282/306/02-08-02      URI    Maintenance Rule Functional Failure Evaluation of Bypass Gate Failures (Section 1R12.1)50-282/306/02-08-03      NCV    Failure to Correct Deficiencies Adverse to Quality Involving Potential Flow Diversion Paths (Section 4OA2.1)
Closed 50-282/306/02-001-00      LER    Condition Prohibited by TSs Due to Potential for Auxiliary Building Special Vent Zone Boundary Degradation (Section 4OA3)50-282/306/02-08-01      FIN    Inappropriate Maintenance Rule Safety Significance Classification of the External Circulating Water Intake Screen Bypass Gates (Section 1R12.1)50-282/306/02-08-03      NCV    Failure to Correct Deficiencies Adverse to Quality Involving Potential Flow Diversion Paths (Section 4OA2.1)
Discussed None.
 
LIST OF ACRONYMS USED ABSVZ Auxiliary Building Special Ventilation Zone ACE  Apparent Cause Evaluation ADAMS Agencywide Documents Access and Management System AFW  Auxiliary Feedwater AR    Action Request AWI  Administrative Work Instruction CAP  Corrective Action Program CE    Condition Evaluation CFR  Code of Federal Regulations CR    Condition Report DBD  Design Bases Document DDCLP Diesel-Driven Cooling Water Pump FIN  Finding HSAS  Homeland Security Advisory System IMC  Inspection Manual Chapter INPO  Institute of Nuclear Power Operations IPEEE Individual Plant Examination of External Events IR    Inspection Report LCO  Limiting Conditions for Operation LER  Licensee Event Report MOV  Motor Operated Valve NCV  Non-Cited Violation NEI  Nuclear Energy Institute OOS  Out-of-service OPR  Operability Recommendation OWA  Operator Workaround PARS  Publicly Available Records PINGP Prairie Island Nuclear Generating Plant PM    Preventive Maintenance RHR  Residual Heat Removal RIS  Regulatory Information Summary RWST  Refueling Water Storage Tank SDP  Significance Determination Process SI    Safety Injection SP    Surveillance Procedure TS    Technical Specification USAR  Updated Safety Analysis Report NRC  U.S. Nuclear Regulatory Commission WO    Work Order LIST OF
 
=DOCUMENTS REVIEWED=
 
1R04 Equipment Alignment
Cooling Water System
TS 3.3-7                Cooling Water System                      Revision 131
USAR 10.4.1              Cooling Water System                      Revision 22
Plant Procedure B35      Cooling Water System                      Revision 5
Integrated Checklist    Cooling Water System                      Revision 21
C1.1.35-3
Operating Procedure C35  Cooling Water System                      Revision 48
WO 0203427              Remove T Mod 00T076                      April 3, 2002
AR CAP 000060            121 CLP Bearing Seal Water Filter Changes March 27, 2002
AR CAP 023610            Bearing Water Flow to Lineshaft and      May 27, 2002
Suction Bell Less than 50%
AR CAP 023779            Unable to Make Bearing Water Flow        June 10, 2002
Adjustments on DDCLP Flows
AR CAP 024661            12 DDCLP Declared Inoperable              August 15, 2002
AR CAP 024393            High Risk Work Not Complete As            August 31, 2002
Scheduled
D1 Emergency Diesel
Generator
Integrated Checklist    D1 Diesel Generator Valve Status          Revision 19
C1.1.20.7-1
Integrated Checklist    D1 Diesel Generator Auxiliaries and Room  Revision 8W
C1.1.20.7-2              Cooling Local Panels
Integrated Checklist    Diesel Generator D1 Main Control Room    Revision 13
C1.1.20.7-3              Switch and Indicating Light Status
Integrated Checklist    D1 Diesel Generator Circuit Breakers and  Revision 11
C1.1.20.7-4              Panel Switches
TS 3.7                  Auxiliary Electrical Systems              Revision 110
USAR Section 8.4        Plant Standby Diesel Generator Systems    Revision 23
AR CAP 024968            Pressure Indicator 11079, 21 Heater Drain August 30, 2002
Tank Pump Discharge Pressure Indicator
Was Isolated During WO 0205739
1R05 Fire Protection
Area Walkdowns
Plant Safety Procedure    Fire Strategies for Fire Areas 13, 18, 35, 36, Revision 7
F5, Appendix A            69, 101, and 102
IPEEE NSPLMI-96001        Internal Fires Analysis                        Revision 2
Appendix B
Plant Safety Procedure    Fire Hazard Analysis for Fire Areas 13, 18,    Revision 16
F5, Appendix F            35, 36, 69, 101, and 102
AR CAP 024122              Transient Combustibles Stored In Safety-      July 11, 2002
Related Area, Repeat Occurrence
AR CAP 025395              Pressure Switch Communication Failure          September 23,
With Fire Panel                                2002
Fire Brigade Drill
Plant Safety Procedure    Fire Drills                                    Revision 8
F5, Appendix J
Plant Safety Procedure    Fire Detection Zone 83                        Revision 8
F5, Appendix A
1R011 Licensed Operator Requalification Program
USAR 14.5.4                Steam Generator Tube Rupture                  Revision 22
Procedure 1E-0            Reactor Trip or Safety Injection              Revision 21
NRC Inspection Report      Prairie Island Nuclear Generating Plant        January 17, 2002
NRC Inspection Report 50-282/01-18;
50-306/01-18
AR CAP 000232              November 2001 INPO [Institute of Nuclear      December 18,
Power Operations] Evaluation                  2001
Simulator Team            Simulator Team Evaluation                      September 4,
Evaluation PITCQ-83                                                      2002
1R12 Maintenance Rule Implementation
Repeat Failure of External
Circulating Water Intake
Bypass Gates
Root Cause Investigation  Decreasing Intake Canal Level Due to          Revision 0
Report 000171              Failure of the Intake Traveling Screens
Plant Procedure H24        Prairie Island Nuclear Generating Plant        Revision 4
Maintenance Rule Program
Prairie Island Nuclear Generating Plant    Revision 3
Maintenance Rule System Specific Basis
Document, External Circulating Water
Section
Prairie Island Nuclear Generating Plant
Maintenance Rule Scope Determination and
Performance Criteria Spreadsheet
Prairie Island Nuclear Generating Plant
Quarterly Equipment Performance Report,
2nd Quarter 2002
AR CAP 023908        Decreasing Intake Bay Levels Due to Loss    June 19, 2002
of Intake Screens
AR MRE 000014        Maintenance Rule Evaluation of Intake      June 20, 2002
Screens and Bypass Gates
AR CAP 023958        121 Bypass Gate Failed to Open with Loss    June 24, 2002
of Control Power
AR CAP 023959        122 Bypass Gate Failed to Open with Loss    June 24, 2002
of Control Power
AR CAP 009179        Need Acceptance Criteria for Operability of September 3,
Intake Bypass and Screens                  2001
AR CAP 024744        Maintenance Rule Performance Criteria for  August 20, 2002
Screenhouse Bypass Gates Not In
Accordance With the Guidance of
NUMARC 93-01
AR ACE 008543        Apparent Cause Evaluation of CAP 024744    August 22, 2002
AR CAP 024391        Unsatisfactorily Completed Test            August 30, 2002
Procedure 2537
AR CAP 025146        Failure of Test Procedure 2537              September 11,
2002
Failure of CV 39201,
11/13 Containment Fan
Cooling Unit Cooling
Water Return Bypass
Control Valve
5AWI 3.2.10          Investigation and Troubleshooting          Revision 7
5AWI 3.12.0          Nuclear Plant Maintenance                  Revision 10
USAR, Section 10.4.1  Cooling Water System                        Revision 22
Flow Diagram          Unit 1 Cooling Water - Auxiliary Building  Revision R
NF-39216-3
AR CAP 023812            CV 39201, 11/13 Containment Fan Cooling    June 12, 2002
Unit Cooling Water Return Bypass Control
Valve Found Open
AR MRE 000010            Maintenance Rule Evaluation of CV-39201    June 13, 2002
Failure
AR CE 000405              Condition Evaluation of CAP 023812        June 13, 2002
WO 0205407                Investigate and Repair CV 39201            June 13, 2002
WO 0108187                Investigate and Repair CV 39201            July 9, 2001
WO 0107267                Investigate and Repair CV 39201            May 14, 2002
Prairie Island Nuclear Generating Plant    Revision 3
Maintenance Rule System Specific Basis
Document, Cooling Water Section
1R13 Maintenance Risk Assessments and Emergent Work Control
SI Pump with 22 RHR
Pump and Heat
Exchanger Out-of-service
TS 3.3.A                  Safety Injection and Residual Heat Removal Revision 161
Systems
TS 4.2                    Inservice Inspection and Testing of Pumps  Revision 60
and Valves Requirements
WO and Work Plan          22 SI Pump Has a Leak on the Pump Head    September 9,
202701                                                              2002
10CFR50.59 Screening      NMC Standard 10 CFR 50.59 Screening        Revision 0
No. 1567
ENG-ME-525                Calculation                                Revision 0
Unit 2 Configuration Risk Assessment      September 17,
2002
Turbine-Driven AFW
Pump Surveillance with
25 Air Compressor Out-
of-service
Unit 2 Configuration Risk Assessment      September 17,
2002
Turbine-Driven AFW
Pump Testing with 122
Control Room Chiller Out-
of-service
Plant Procedure H24.1    Assessment and Management of Risk          Revision 4
Associated with Maintenance Activities
Risk Assessment for Work Week 2B33        August 20, 2002
Motor-Driven AFW
Pump Check Valve
Testing with Train A ICCM
Out-of-service
Unit 2 Configuration Risk Assessment    July 10, 2002
DDCLP Emergent
Work
Operation Log Entries                    August 14, 2002
Plant Status Report                      August 15, 2002
Open Limiting Conditions for Operation  August 15, 2002
                            (LCO) Log
Motor-Driven AFW
Pump Failed Surveillance
Operation Log Entries                    August 30, 2002
Plant Status Report                      August 30, 2002
Open LCO Log                            August 30, 2002
AR CAP 024946              12 Motor-Driven AFW Pump Failed SP 1000 August 30, 2002
Due to Sluggish Motor Slinger Ring
Operation
AR CAP 024956              12 Motor-Driven AFW Pump Made            August 30, 2002
Unavailable When in an Indeterminate
Condition
D2 Diesel Generator, 18
Inverter, 11 Charging
Pump, and 12 Motor-
Driven AFW Pump Out-
of- Service
Operations Log Entries                  August 26, 2002
Open LCO Log                            August 25, 2002
Unit 1 Configuration Risk Assessment    August 25, 2002
1R14 Non-Routine Evolutions
Root Cause Investigation  Decreasing Intake Canal Level Due to    Revision 0
Report 000171              Failure of the Intake Traveling Screens
AR CAP 023908              Decreasing Intake Bay Levels Due to Loss June 19, 2002
of Intake Screens
AR CAP 023958              121 Bypass Gate Failed to Open with Loss June 24, 2002
of Control Power
AR CAP 023959              122 Bypass Gate Failed to Open with Loss June 24, 2002
of Control Power
Operations Control Room Logs                  June 19, 2002
Plant Procedure C41.5      Emergency Response Computer System            Revision 16
Operating Procedure Alarms, Displays, and
Responses, Computer Alarm 26
Plant Procedure C25        Circulating Water System                      Revision 23
C91802                      Annunciator Response Procedure for            Revision 1
External Circulating Water Remote
Panel 91802, High Traveling Screen
C47501                      Annunciator Response Procedure for            Revision 22
Control Room Panel 47501, Alarm 47501-
0101, Intake Screenhouse Traveling Screen
High Differential Pressure
1R15 Operability Evaluations
Unit 2 Reactor Missile
Shield Weight
USAR 12.2, Table 12.2-      Loads Handled Over Safety Related            Revision 23
Components, Components Required for
Plant Shutdown or Decay Heat Removal
Plant Procedure D58        Heavy Loads Program                          Revision 30
AR CAP 023549              U2 Reactor Missile Shield Weight Measured May 19, 2002
74,500 Pounds Versus SAR Listed Weight
of 56, 200 Pounds
AR CE 000266                Determine Extent of Condition Regarding      May 30, 2002
the Weight of the U2 Reactor Missile Shield
Auxiliary Building Special
Ventilation Boundary
TS 1.0 and 3.6.E            Auxiliary Building Special Ventilation Zone  Revision 111 and
Integrity                                    91
USAR 10.3.4                Auxiliary Building Special Ventilation System Revision 23
Plant Procedure B19        Containment Systems                          Revision 6
Plant Procedure D54        Control of Openings in the Auxiliary Building Revision 13
Special Ventilation Zone Boundary
AR CAP 024185              ABSVZ Boundary at Hot Chem Lab                July 16, 2002
AR OPR 000324              Operability Recommendation for Auxiliary      July 17, 2002
Building Special Vent Zone Boundary Issue
and 22 DDCLP
Oscillations
USAR, Section 10.4.1        Cooling Water System                          Revision 22
TS 3.3-7                    Cooling Water System                          Revision 131
Operating Procedure C35    Cooling Water System                        Revision 48
Plant Procedure B35        Cooling Water System                        Revision 5
DBD SYS-35                Design Basis Document for the Cooling      Revision 4
Water System
AR CAP 024010              Sluggish Governor Response on 22 Diesel    June 28, 2002
Driven Cooling Water Pump
AR CE 000500              Condition Evaluation of AR CAP 024010      July 1, 2002
AR ACE 008426              Apparent Cause Evaluation                  June 13, 2002
Operation of the 21 AFW
Pump with Insufficient
Packing Leakoff
USAR Section 11.9.2.2      Auxiliary Feedwater System                  Revision 23
XH-258-24                  Auxiliary Feedwater Technical Manual
Condition Report Notebook Issue #
20000592
AR CAP 024541              No Seal Leakage During Run of SP 2100,      August 8, 2002
Auxiliary Feedwater Pump
Containment Fan
Cooling Unit High
Vibrations
AR CAP 024294              Containment Fan Cooling Unit Vibration in  July 23, 2002
Alert Range at 5 Mils in Fast Speed
AR CE 000637              Condition Evaluation of AR CAP 024294      July 25, 2002
AR OPR 000327              Operability Recommendation of              July 25, 2002
AR CAP 024294
Containment Fan Cooling Unit Inspection    August 7, 2002
Summary
USAR, Section 6.3.2        Containment Air Cooling System Design      Revision 22
and Operation
Grid Security Analysis for
the Prairie Island Two
Unit Trip Contingency
Failed
AR CAP 024732              Low Grid Voltage, Security Analysis Failure August 19, 2002
to Satisfy Two Unit Trip Contingency
AR OPR 000330              Operability Recommendation of              August 20, 2002
AR CAP 024732
AR CAP 023977              Guidance for Response to Security Analysis June 25, 2002
Alarm Needs Improvement
TS 3.7                    Auxiliary Electrical Systems                Revision 110
USAR, Section 8.2          Transmission System                        Revision 23
Inadequate Thread
Engagement on 22 SI
Pump Suction Flange
Bolts
AR CAP 025410              22 Safety Injection Pump Suction Flange    September 24,
Bolts Do Not Meet D63 Requirements          2002
Plant Procedure D63        Installation Guidelines for Threaded        Revision 9W
Fasteners (Studs or Bolts)
Calculation ENG-CS-080    Acceptable Thread Engagement
1R16 OWAs
Station Battery
Charger
Operator Workarounds                        August 7, 2002
CR 19971622                Intermittent Operation During SP 1083      December 5, 1997
CR 19991958                Intermittent Operation During SP 1083      June 6, 1999
Safety Evaluation 534      Station Battery Charger Current Limit      Revision 0,
Setpoint Change                            April 12, 1999
Safety Evaluation 534      Station Battery Charger Current Limit      Revision 1,
Setpoint Change                            August 10, 1999
SP 1083                    Integrated SI Test With a Simulated Loss of Revision 26W
Offsite Power
Cumulative Effects of
OWAs
5AWI 3.10.8                Equipment Problem Resolution Process        Revision 0
Prairie Island Nuclear    Minutes #2714                              August 7, 2002
Generating Plant (PINGP)
Operation Committee
Meeting Minutes
1R19 Post Maintenance Testing
Diesel-Driven Cooling
Water Pump
TS 3.3.D                  Cooling Water Systems                      Revision 131
USAR 10.4.1                Cooling Water System                        Revision 22
Plant Procedure B35        Cooling Water System                        Revision 5
SP 1106B                22 Diesel Cooling Water Pump Monthly Test Revision 58
WO 0202848              SP 1106B 22 Diesel Cooling Water Pump      July 29, 2002
Monthly
RWST to SI Header
Isolation Valve MV-32182
TS 3.3.A.2.d            Safety Injection and Residual Heat Removal Revision 161
Systems
USAR 6.2                Safety Injection System                    Revision 22
Plant Procedure B18A    Safety Injection System                    Revision 4
WO 0110007              Refueling Water to Safety Injection Pumps  July 29, 2002
Header Isolation Motor Valve A
RHR Pump
TS 3.3.A                Safety Injection and Residual Head          Revision 161
Removal Systems
USAR 6.2.2.2.4          Safety Injection and Residual Heat Removal Revision 22
Pumps
Plant Procedure H10.1    ASME Inservice Testing Implementing        Revision 12
Program
Plant Procedure B15      Residual Heat Removal System                Revision 7
WO 0202361              P3124-1-21 21 RHR Pump Annual              July 16, 2002
Inspection
WO 0204146              SP 2089AL Light Verification During        August 7, 2002
SP 2089A
WO 0204145              SP 2089A RHR Pump and Suction Valves        August 7, 2002
from the RWST
2 Control Room Chiller
and Air Handler
WO 0100313              Replace Mechanical Seals and Inspect
Chilled Water Pump
WO 0111036              122 Control Room Chiller Electrical Breaker
15-Year PM
WO 0202368              122 Control Room Chiller Annual Inspection
WO 0202370              6-Month Inspection of Control Room Air
Handling Unit
WO 0202371              12-Month Inspection of Control Room Air
Handling Unit
WO 0202635              Leak Check 122 Control Room Chiller
WO 0203915              Control Room Train B Chilled Water Pump
Test
WO 0203943              Alternating In-Service Control Room Chillers
WO 9406919              Change Wire Codes at Pump Push Button
Station
Drawing NF-39603-1      Admin Bldg, Screen House, and Control        Revision AL
Room Flow Diagram
Drawing NF-40890-3      External Connections Motor Control Center    Revision N
1T
TS 3.13                  Control Room Air Treatment System            Revision 91
TS 4.14                  Control Room Air Treatment System Tests      Revision 91
USAR 10.3.3              Control Room Ventilation System              Revision 23
D2 Diesel Generator 6-
Month Inspection
PM 3001-2-D2            D2 Diesel Generator 18-Month Inspection      Revision 17
PM 3001-4-D2            D2 Diesel Generator Inspection Electrical    Revision 5
SP 1306                  D2 Diesel Generator 18-Month Relay          Revision 6
Functional Test
SP 1307                  D2 Diesel Generator 6-Month Fast Start      Revision 22
Test
TS 3.7                  Auxiliary Electrical Systems                Revision 110
TS 4.6                  Periodic Testing of the Emergency Power      Revision 91
System
1R22 Surveillance Testing
Turbine-Driven AFW
Pump Monthly Test
TS 3.4.B                Auxiliary Feedwater System                  Revision 123
TS 4.8.A                Auxiliary Feedwater System                  Revision 116
USAR 1.9                Condensate, Feedwater and Auxiliary          Revision 23
Feedwater Systems
Plant Procedure B28B    Auxiliary Feedwater System                  Revision 5
SP 2102                  22 Turbine-Driven AFW Pump Monthly Test Revision 69
D1 Diesel Generator
Monthly Slow-Start Test
TS 3.7                  Auxiliary Electrical Systems                Revision 110
TS 4.6                  Periodic Testing of Emergency Power          Revision 147
System
Plant Procedure B38A    Unit 1 Diesel Generators                    Revision 5
SP 1093                D1 Diesel Generator Monthly Slow Start    Revision 73
Test
Diesel Cooling Water
Pump Monthly Test
TS 3.3.D                Cooling Water System                      Revision 131
TS 4.2                  Inservice Inspection and Testing of Pumps Revision 60
and Valves Requirements
TS 4.5.B.1.b            Component Test, Pumps                    Revision 161
USAR 10.4.1            Cooling Water System                      Revision 22
Plant Procedure B35    Cooling Water System                      Revision 5
SP 1106A                12 Diesel Cooling Water Pump Monthly Test Revision 61
AR CAP 025178          12 Diesel Driven Cooling Water Pump      September 12,
2002
AR CAP 025186          12 DDCLP Fell in the Performance Curve    September 12,
Alert Range During 9/12/02 Run            2002
D6 Diesel Generator 6-
Month Fast-Start Test
TS 4.6.A.2              Periodic Testing of Emergency Power      Revision 113
System
Operating Procedure    D5/D6 Fuel Oil System                    Revision 16
2C38
SP 2307                D6 Diesel Generator 6 Month Fast Start    Revision 17
Test
AR CAP 025281          Positive Glycol Test D5 Engine 2          September 18,
2002
AR CAP 025334          WO to Fill D6 Coolant Expansion Tanks    September 20,
Issued While Monthly Diesel Run In        2002
Progress
AR CAP 025241          Discrepancy Between SP 2305 and          September 16,
SP 2307 for 2LI-6011A for Acceptance      2002
Criteria
D5 Diesel-Driven
Generator 6-Month Fast-
Start Test
TS 3.7                  Auxiliary Electrical Systems              Revision 110
TS 4.6.A.2              Periodic Testing of Emergency Power      Revision 113
System
Plant Procedure B38C    Unit 2 Diesel Generators                  Revision 2
SP 2295                D5 Diesel Generator 6-Month Fast Start    Revision 23
Test
WO 0206045                  SP 2295 D5 Diesel Generator 6-Month Fast      September 30,
Start Test                                    2002
AR CAP 025506                D5 Generator Stator Temperature              September 30,
Channel 3 Failed                              2002
AR CAP 025507                SP 2295 D5 Fast Start Scheduled When D5 September 30,
1B Was Scheduled OOS [Out-of-service]        2002
AR CAP 025515                D5 2A Air Dryer Dust Filter Drain Plugged    October 1, 2002
4OA1 Performance Indicator Verification
Safety System Functional Failure
LER 1-01-02                  Auto Activation of Unit 1 4160 Volt          Revision 0
Safeguards Bus 16 Source Sequencer
Following Grid Disturbance Caused by
Severe Weather
LER 1-01-03                  Plant In Unanalyzed Condition Due To          Revision 0
Flood Panel Deficiencies
LER 1-01-03                  Plant In Unanalyzed Condition Due to Flood Revision 1
Panel Deficiencies
LER 1-01-04                  Water Intrusion Into a Control Rod Electrical Revision 0
Cabinet Results in Dropped Rods Causing a
Negative Flux Reactor Trip
LER 1-01-05                  Fault and Fire in Non-Safeguards Circuit      Revision 0
Breaker Results in Reactor Trip and
Auxiliary Feedwater Actuation
LER 1-01-06                  Security Responders Out of Position Due to    Revision 0
Plant Fire
LER 2-01-01                  Failure to Meet TS Limiting Condition for    Revision 0
Operation Verification Within Eight Hour
Limit Due to Personnel Error
LER 2-01-02                  Emergency Diesel Generator Out-of-service Revision 0
Longer Than TS Allowed Outage Time
LER 2-01-03                  Technical Specification Required Shutdown    Revision 0
of Unit 2 Due to Declared Inoperability of
Both Emergency Diesel Generators
LER 2-01-03                  Technical Specification Required Shutdown    Revision 1
of Unit 2 Due to Declared Inoperability of
Both Emergency Diesel Generators
LER 2-01-03                  Technical Specification Required Shutdown    Revision 2
of Unit 2 Due to Declared Inoperability of
Both Emergency Diesel Generators
LER 2-01-04            Manual Turbine Trip/Reactor Trip Due to    Revision 0
High Differential Condenser Backpressure
LER 2-01-05            Manual Reactor Trip on Unit 2, Initiated in Revision 0
Response to a High Differential Pressure
Between the Turbine Steam Condensers,
Caused By an Inadvertent Venting of One
Condenser While Isolating a Steam Leak
Operator Logs from April 1, 2001, to
March 31, 2002
NEI 99-02              Regulatory Assessment Performance          Revision 2
Indicator Guideline
Prairie Island Nuclear Generating Plant    2nd Quarter 2001
Quarterly Equipment Performance Report
Prairie Island Nuclear Generating Plant    3rd Quarter 2001
Quarterly Equipment Performance Report
Prairie Island Nuclear Generating Plant    4th Quarter 2001
Quarterly Equipment Performance Report
Prairie Island Nuclear Generating Plant    1st Quarter 2002
Quarterly Equipment Performance Report
Plant Procedure H33    Performance Indicator Reporting            Revision 5
Plant Procedure H33.3  Safety System Functional Failure            Revision 0
Performance Indicator Reporting
Instructions
PINGP Form 1318C      Performance Indicator-Safety System        2nd Quarter 2001
Functional Failure
PINGP Form 1318C      Performance Indicator-Safety System        3rd Quarter 2001
Functional Failure
PINGP Form 1318C      Performance Indicator-Safety System        4th Quarter 2001
Functional Failure
PINGP Form 1318C      Performance Indicator-Safety System        1st Quarter 2002
Functional Failure
Reactor Coolant System
Specific Activity
TS 3.1-10              Maximum Coolant Activity                    Revision 147
SP 1057                Unit 1 Reactor Coolant Monthly              Revision 17
Radiochemical Analysis
Unit 1 Radiochemistry Report                July 1, 2001 to
May 31, 2002
Unit 2 Radiochemistry Report                July 1, 2001 to
May 31, 2002
NEI 99-02                  Regulatory Assessment Performance            Revision 2
Indicator Guideline
Unplanned Power
Changes
NEI 99-02                  Regulatory Assessment Performance            Revision 2
Indicator Guideline
Plant Procedure H33.2,    Data Sheets 3rd Quarter 2001 to 2nd Quarter  Revision 3
Figure 1                  2002
PINGP Form 1318A          Data Sheets 3rd Quarter 2001 to 2nd Quarter  Revision 0
2002
4OA2 Identification and Resolution of Problems
LER 1-98-15                Containment to RHR MOVs [Motor              10/26/98
Operated Valves] Appendix R Safe
Shutdown Analysis Issues
CR 19982008                FPFI [Fire Protection Functional Inspection] 9/25/98
Question FP-I072: Sump B to RHR MOVs
Not on SSEL [Safe Shutdown Equipment
List]. Can NPSH [Net Positive Suction
Head] be obtained if these MOVs spuriously
open due to a fire?
GEN-PI-034                Appendix R Equipment List Review - Decay    3/30/99
Heat Removal Function
GEN-PI-035                Appendix R Equipment List Review - RCS      5/25/99
                            [Reactor Coolant System] Inventory Control
Function
GEN-PI-036                Appendix R Equipment List Review - Safe      5/25/99
Shutdown Support Function
GEN-PI-037                Appendix R Equipment List Review -          5/25/99
Process Monitoring Function
GEN-PI-038                Appendix R Equipment List Review -          7/9/99
Electrical Power Supply Function
GEN-PI-039                Appendix R Equipment List Review -          7/9/99
Containment Integrity Function
AR CAP 024536              Appendix R Equipment List Evaluations        8/7/02
Should Be Canceled
AR CAP 024537              Appendix R Commitment Closed                8/7/02
Prematurely
G
4OA3 Event Followup
AR CAP 024536        Appendix R Equipment List Evaluations      8/7/02
Should Be Canceled
LER 1-02-01          Condition Prohibited by TS Due to Potential September 16,
for Auxiliary Building Special Vent Zone    2002
Boundary Degradation
AR CAP 024185        ABSVZ Boundary at Hot Chem Lab              July 16, 2002
AR OPR 000324        Operability Recommendation for Aux          July 16, 2002
Building Special Vent Zone Boundary Issue
Plant Procedure D54, Control of Openings in the Aux Building    July 25, 2002
Temporary Change    Special Ventilation Zone Boundary
Notice 2002-1367
Log Entry            Category 1 Special Vent Zone Report        September 8,
2002
35
}}

Latest revision as of 02:35, 25 March 2020

IR 05000282-02-008, IR 05000306-02-008, on 07/01/02 - 09/30/02, Prairie Island, Maintenance Effectiveness and Identification and Resolution of Problems
ML023040324
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 10/30/2002
From: Kenneth Riemer
Division of Nuclear Materials Safety III
To: Nazar M
Nuclear Management Co
References
IR-02-008
Download: ML023040324 (36)


Text

ber 30, 2002

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 50-282/02-08; 50-306/02-08

Dear Mr. Nazar:

On September 30, 2002, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on September 27, 2002, with you and members of your staff.

This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, the NRC identified two issues of very low safety significance (Green). One of the issues was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it has been entered into your corrective action program, the NRC is treating the issue as a Non-Cited Violation, in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 801 Warrenville Road, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Prairie Island Nuclear Generating Plant.

In response to the terrorist attacks on September 11, 2001, the NRC issued an Order and several threat advisories to commercial power reactors to strengthen licensees capabilities and readiness to respond to a potential attack. The NRC established a deadline of September 1, 2002, for licensees to complete modifications and process upgrades required by the order. To confirm compliance with this order, the NRC issued Temporary Instruction 2515/148 and over the next year, the NRC will inspect each licensee in accordance with this Temporary Instruction. The NRC continues to monitor overall security controls and may issue additional temporary instructions or require additional inspections should conditions warrant.

In accordance with 10 CFR 2.790 of the NRC's Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief Branch 5 Division of Reactor Projects Docket Nos. 50-282; 50-306 License Nos. DPR-42; DPR-60

Enclosure:

Inspection Report 50-282/02-08; 50-306/02-08

REGION III==

Docket Nos: 50-282; 50-306 License Nos: DPR-42; DPR-60 Report No: 50-282/02-08; 50-306/02-08 Licensee: Nuclear Management Company, LLC Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2 Location: 1717 Wakonade Drive East Welch, MN 55089 Dates: July 1 through September 30, 2002 Inspectors: J. Adams, Senior Resident Inspector D. Karjala, Resident Inspector R. Daley, Reactor Engineer R. Walton, Operations Specialist Approved by: Kenneth Riemer, Chief Branch 5 Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000282-02-08, 05000306-02-08; Nuclear Management Company, LLC; on 07/01 -

9/30/02, Prairie Island Nuclear Generating Plant, Units 1 & 2. Maintenance Effectiveness and Identification and Resolution of Problems.

This report covers a 3-month period of baseline resident inspection. The inspection was conducted by Region III inspectors and the resident inspectors. Two findings of significance were identified. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspection Findings

Cornerstone: Initiating Events

Green.

A finding of very low safety significance was identified by the inspectors investigating the repeat failures of the external circulating water intake screen bypass gates to fully open and to latch in the open position. The finding resulted from performance deficiencies associated with the establishment of an appropriate maintenance rule safety significance classification of the external circulating water intake screen bypass gates. The bypass gates were classified as low safety significant components, not as low safety significant standby components as specified by industry maintenance rule guidance.

This finding was more than minor because it increased the likelihood of a reactor trip event due to a loss of circulating water. The finding was of very low safety significance because it did not contribute to the likelihood of a primary or secondary system loss of coolant accident, did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available, and did not increase the likelihood of a fire or internal/external flood. A violation determination could not be completed until appropriate maintenance rule performance criteria have been established and will be tracked by an Unresolved Item. (Section 1R12.1)

Cornerstone: Mitigating Systems

Green.

A finding of very low safety significance was identified by the inspectors during a review of licensee corrective action taken to address concerns documented in Licensee Event Report (LER) 1-98-15 pertaining to Appendix R potential flow diversion paths.

The primary cause of this finding was related to a failure to correct or implement appropriate compensatory actions to address potential flow diversion paths that had existed since 1999.

This finding is more than minor because, if left uncorrected, the finding would become a more significant safety concern. Failure to resolve fire protection non-compliance items and failure to establish appropriate compensatory measures could potentially affect the availability, reliability, and capability of fire protection safe shutdown equipment and response efforts. The inspectors determined that the finding was not suitable for SDP analysis. However, the finding was determined to be of very low safety significance because the probability of having a fire event in the affected areas such that the fire would cause more than one valve to reposition to cause a flow diversion was very low.

This was determined to be a Non-Cited Violation (NCV) of 10 CFR Part 50, Appendix B,

Criterion XVI. (Section 4OA2.1)

Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and corrective action tracking numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 was operated at or near full power for the entire inspection period. Unit 2 was operated at or near full power for the entire inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment

.1 Partial Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of accessible portions of trains of risk-significant mitigating systems equipment during times when the trains were of increased importance due to the redundant trains or other related equipment being unavailable.

The inspectors utilized the valve and electric breaker checklists listed at the end of this report to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders (WOs) and Corrective Action Program (CAP) Action Requests (ARs) associated with the trains to verify that those documents did not reveal issues that could affect train function. The inspectors used the information in the appropriate sections of the Updated Safety Analysis Report (USAR) to determine the functional requirements of the systems.

The inspectors verified the alignment of the following trains:

  • 12 safety-related cooling water pump and 121 safety-related traveling screen during the unavailability of the 22 safety-related cooling water pump and 122 safety-related traveling screen on July 30, 2002; and
  • 22 and 121 safety-related cooling water pumps following the emergent failure of the 12 safety-related cooling water pump on August 15, 2002.

The inspectors reviewed the ARs listed at the end of this report to verify that the licensee was identifying issues at an appropriate threshold and entering them into their corrective action program. The inspectors also reviewed ARs to verify that minor deficiencies identified during these inspections were entered into the licensees corrective action system.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Area Walkdowns

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on the availability and accessibility of fire protection equipment, the condition of fire fighting equipment, the control of transient combustibles, and the condition and operating status of installed fire barriers as described in fire hazards analysis and pre-fire plans. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events (IPEEE); their potential to impact equipment which could initiate a plant transient; or their impact on the plants ability to respond to a security event. The inspectors reviewed the as-found condition of fire doors, dampers, penetration seals, fire detectors, sprinklers, fire hoses and extinguishers, comparing the as-found conditions to the configuration described in fire hazards analysis and pre-fire plans. The inspectors also reviewed equipment to verify that it was in its appropriate location, was available for immediate use, and was not obstructed. The as-found transient combustible loading was also reviewed to verify that it was within the analyzed limits. The inspectors reviewed the ARs listed at the end of this report to verify that the licensee was identifying fire protection issues at an appropriate threshold and entering them into their corrective action program.

The inspectors assessed the following areas:

  • Fire Area 13, Unit 1 and 2 Control Room on July 13, 2002;
  • Fire Area 18, Unit 1 and 2 Cable Spreading and Relay Rooms on July 11, 2002;
  • Fire Area 35, 21 Battery Room on July 10, 2002;
  • Fire Area 36, 22 Battery Room on July 11, 2002;
  • Fire Area 69, Turbine Ground Floor and Mezzanine;

b. Findings

No findings of significance were identified.

.2 Fire Brigade Drills

a. Inspection Scope

The inspectors observed the performance of a fire brigade drill in the Unit 1 electrical bus 150/160 room on July 19, 2002. This area was considered risk significant because a fire could cause a unit trip initiating event. The inspectors observed the initial response of the fire brigade leader, the fire brigade, security personnel, and the duty Emergency Medical Technician. The inspectors observed establishment of communications with the control room, the brigade response strategy briefing, and the brigades response to the simulated fire. The inspectors used the NRC inspection procedure listed above and the documents listed at the end of this report to evaluate the drill. At the conclusion of the drill, the inspectors observed the licensees drill critique to ensure that any weaknesses noted during the drill were addressed.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

On September 10, 2002, the inspectors observed an operating crew during a requalification examination on the simulator. The inspectors evaluated crew performance in the areas of:

  • clarity and formality of communications;
  • ability to take timely, appropriate, and safe actions;
  • prioritization, interpretation, and verification of alarms;
  • procedure use;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • group dynamics.

The inspectors compared crew performance in the above areas to the critical tasks listed in the exercise guide at the end of this report. The inspectors also compared simulator configurations with actual control room board configurations. The inspectors attended the post-examination critique to verify that the licensee evaluators noted the same weaknesses observed by the inspectors and discussed them during the critique.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 External Circulating Water Intake Screen Bypass Gate Repeat Failures

a. Inspection Scope

On August 20, 2002, while investigating the repeat failures of the external circulating water intake screen bypass gates, the inspectors identified that the maintenance rule safety significance classification of the external circulating water intake screen bypass gates was inappropriate.

b. Findings

The inspectors identified a Green finding associated with the inappropriate maintenance rule safety significance classification of the external circulating water intake screen bypass gates. The bypass gates were classified as low safety significant components, contrary to the NRC-endorsed, industry guidance of NUMARC 93-01.

On June 19, 2002, the sequential loss of external circulating water intake traveling screens caused a low intake bay level. In response to the intake bay low level, operators initiated the opening of the intake bypass gates by isolating power to the bypass gates. This action simulated a loss of power to the traveling screens and should have caused the bypass gates to open hydraulically. However, the 121 intake bypass gate failed to open and the 122 only partially opened. The partial opening of 122 gate allowed sufficient makeup to the intake bay to prevent a loss of circulating water and reactor trip.

The inspectors conducted a historical evaluation of the intake bypass gates performance. The inspectors noted a history of problems with the failure of the intake gates to fully open and to latch in the open position. Based on the number of repeat failures documented in the licensees corrective action program, the inspectors evaluated whether the intake bypass gate were scoped in accordance with the maintenance rule, 10 CFR 50.65; whether the intake bypass gates had been assigned the proper safety significance classification; whether the established performance criteria was appropriate; whether the performance problems associated with intake bypass gates constituted maintenance rule functional failures or repeat maintenance rule functional failures; and whether the intake bypass gates were properly classified as (a)(1) or (a)(2).

The inspectors determined that the bypass gates were properly included in the scope of the maintenance rule, but found that the licensee had inappropriately classified the bypass gates as low safety significant components. The licensee should have recognized the bypass gates as low safety significant standby components since their function was to open automatically on loss of power to the external circulating water intake traveling screens, or on a high differential level across the external circulating water intake traveling screens. Since the bypass gates were improperly classified, the licensees performance criteria were also inappropriate and bypass gate failures were not properly evaluated for maintenance preventable functional failures. The licensee entered this condition into their corrective action program with AR CAP 024744. A list of documents reviewed during this inspection is included at the end of this report.

The inspectors determined that the inappropriate maintenance rule safety significance classification of the intake bypass gates was a performance deficiency warranting a significance evaluation in accordance with Inspection Manual Chapter IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on April 29, 2002. The inspectors determined that the finding was more than minor because it:

(1) involved the equipment performance attribute of the Initiating Events cornerstone, and
(2) affected the cornerstone objective of limiting the likelihood of those events that upset plant stability during power operations.

The inspectors determined that the finding could be evaluated in accordance with IMC 0609, Significance Determination Process, because the finding was associated with an increase in the likelihood of an initiating event. For the Phase 1 screening, the inspectors determined that the finding did not contribute to the likelihood of a primary or secondary system loss of coolant accident, did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available, and did not increase the likelihood of a fire or internal/external flood. This finding (FIN 50-282/306/02-08-01), screened out of the Phase 1 SDP, was determined to be of very low safety significance.

The inspectors discussed the potential of a violation of NRC maintenance rule requirements with Region III, Division of Reactor Safety inspectors. Based on that discussion, the inspectors concluded that a violation determination could not be completed until appropriate performance criteria for the low safety significant standby safety significance classification were first established by the maintenance rule expert panel. Following the establishment of appropriate performance criteria, a maintenance rule functional failure evaluation of all bypass gate failures for the previous 2 years can be performed. If the results of that evaluation show that the intake bypass gates should have been classified as (a)(1) based on their performance and were not, a violation may exist. This is an Unresolved Item (URI 50-282/306/02-08-02).

.2 Repeat Failures of the Containment Fan Cooling Unit Cooling Water Return Orifice

Bypass Valve, CV 39201

a. Inspection Scope

On August 13, 2002, the inspectors reviewed AR CAP 023812 that identified a repeat failure of the containment fan cooling unit cooling water return orifice bypass valve, CV 39201. The proper operation of CV 39201 supports the performance of the safety-related maintenance rule function of providing cooling water to the containment fan cooler Units 11 and 13 and was within the scope of the maintenance rule.

The inspectors performed an in-office review of work orders and corrective action program documents associated with the failures of CV 39201. The inspectors compared the licensees maintenance documentation to the requirements contained in the administrative work instruction (AWI) procedures for the performance of nuclear maintenance, investigation, and troubleshooting. The documents reviewed are listed at the end of this report. The inspectors also conducted an extent-of-condition assessment by searching the licensees corrective action program database for similar failures of valves in redundant containment fan cooling unit trains.

The inspectors reviewed the licensees implementation of the maintenance rule for the repeat failures of CV 39201 by comparing their actions to the requirements contained in the Maintenance Rule, 10 CFR 50.65, and Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, NUMARC 93-01. The inspectors evaluated whether the CV 39201 was scoped in accordance with the maintenance rule; whether the performance problems associated with CV 39201 constituted maintenance rule functional failures; whether the cooling water system had been assigned the proper safety significance classification; whether the system was properly classified as (a)(1) or (a)(2); and whether appropriate performance criteria and/or goals were established. The above aspects were evaluated using the maintenance rule scoping and report documents listed at the end of this report. For each structure, system and component reviewed, the inspectors also reviewed the significant work orders (WO) and ARs listed at the end of this report to verify that failures were properly identified, classified, and corrected, and that unavailable time had been properly calculated.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensees management of plant risk during emergent maintenance activities and during activities where more than one risk significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety significant mitigating equipment. The inspection was conducted to verify that evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate. Inspectors reviewed the licensees daily configuration risk assessment records, observed shift turnover meetings, observed daily plant status meetings, and reviewed risk assessment documents listed at the end of this report to verify that the equipment configurations were properly listed, that protected equipment was identified and controlled, and that significant aspects of plant risk were communicated to the necessary personnel. The inspectors discussed daily and emergent risk assessments with risk assessment engineers and operators.

The inspectors reviewed the following emergent and planned maintenance activities associated with maintenance rule risk significant systems:

  • Repair of the 22 safety injection (SI) pump while Unit 2 was in a yellow risk situation because the 22 residual heat removal (RHR) pump and heat exchanger were out-of-service for preventive maintenance;
  • Testing of the 22 turbine-driven auxiliary feedwater (AFW) pump while Unit 2 was in a yellow risk situation because the 125 air compressor was out-of-service for repair;
  • Testing of the 22 turbine-driven auxiliary feedwater (AFW) pump while the 122 control room chiller was out-of-service for repair;
  • Quarterly check valve testing on the 21 motor-driven AFW pump while the train A inadequate core cooling monitor was out-of-service;
  • Emergent work due to failure of the 12 diesel-driven cooling water pump (DDCLP);
  • The 12 motor-driven AFW pump failed a surveillance test due to sluggish operation of the outboard motor slinger ring; and
  • Unit 1 in yellow risk configuration while D2 diesel generator, 18 inverter, 11 charging pump, and the 12 motor-driven AFW pump were out-of-service for maintenance.

The inspectors reviewed several ARs to verify that problems associated with plant risk assessment were identified at an appropriate threshold, and that corrective actions commensurate with the significance of the issue were identified and implemented. A detailed list of the documents reviewed during this inspection is included at the end of the report.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance Related to Non-Routine Plant Evolutions and Events

a. Inspection Scope

On August 23, 2002, the inspectors completed their review of licensee personnel performance during a June 19, 2002, transient that resulted in a decreasing intake bay level. The level decrease was caused by the loss of intake traveling screens and a failure of the intake bypass gates to open. The inspectors compared operator performance to the applicable response procedures. The inspectors reviewed plant data and operator logs to determine if the plant responded as designed. The inspectors also reviewed the licensees root cause evaluation to verify that noted deficiencies were recognized and entered in their corrective actions program. The documents reviewed during this inspection are listed at the end of this report.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors evaluated plant conditions, selected ARs, and CAP documents for risk significant components and systems in which operability issues were questioned on the dates that appear in the list below. These conditions were evaluated to determine whether the continued operability of the components and systems was justified. The inspectors compared the component or systems function and design criteria in the applicable sections of the Technical Specifications (TSs) and USAR to the licensees evaluations in order to verify that the components and systems were operable. The inspectors verified that compensatory measures necessary to maintain operability were in place, functioned as intended, and were properly controlled. A detailed list of the documents reviewed during this inspection is included at the end of the report.

The inspectors evaluated the following conditions:

  • 12 and 22 diesel-driven cooling water pump speed oscillations on July 10, 2002;
  • The hot chemical laboratory ventilation in the auxiliary building draws air from the turbine building at a flow rate sufficient to prevent the auxiliary building special ventilation system from achieving a negative pressure with the doors to the hot chemical laboratory open on July 15, 2002;
  • The Unit 2 reactor missile shield was weighed during the 2002 refueling outage and found to weigh more than listed in the USAR on July 16, 2002;
  • Operation of the 21 AFW pump with insufficient packing leakoff on August 12, 2002;
  • 22 containment fan cooling unit high vibrations on August 22, 2002;
  • System grid voltage dropped to the point where the Grid Security Analysis for the Prairie Island Two Unit Trip Contingency failed on August 26, 2002; and
  • Inadequate thread engagement on 22 SI pump suction flange bolts September 24, 2002.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds (OWA)

.1 Review of Selected Workarounds

a. Inspection Scope

On August 7, 2002, the inspectors reviewed OWAs associated with the 12 station battery charger. During an accident or transient that results in a safety injection, the 12 station battery charger may require manual restarting. The inspectors verified that the functional capability of the system, human reliability in responding to an initiating event, or the ability of operators to implement abnormal or emergency operating procedures was not significantly affected. The inspectors reviewed the applicable sections of USAR and TSs and discussed the OWAs with control room operators. A detailed list of the documents reviewed during this inspection is included at the end of the report.

b. Findings

No findings of significance were identified.

.2 Cumulative Effects of OWAs

a. Inspection Scope

On August 12, 2002, the inspectors reviewed the cumulative effect of all identified OWAs to determine whether the cumulative conditions had a significant impact on plant risk or on the operators ability to respond to a transient or an accident. The inspectors used the NRC inspection procedure listed above and the documents listed at the end of this report to evaluate the list of OWAs.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance testing activities associated with maintenance on important mitigating, barrier integrity, and support systems to ensure that the post-maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. The inspectors reviewed the appropriate sections of the TSs, the USAR, and maintenance documents to determine the systems safety functions and the scope of the maintenance. In addition, the inspectors reviewed ARs to verify that minor deficiencies identified during these inspections were entered into the licensees corrective action system. A detailed list of the documents reviewed during this inspection is included at the end of the report.

The inspectors observed and evaluated the post-maintenance activities for the following:

  • Refueling water storage tank (RWST) to SI pumps header isolation valve MV-32182 following modification to the control circuit on July 29, 2002;
  • D2 6-month inspection on July 30, 2002;
  • 22 diesel-driven cooling water pump following replacement of a jacket water heater, starting air compressor preventive maintenance (PM), and pump bearing seal water filter change and line flush on July 31, 2002;
  • 21 RHR pump following annual PM on August 8, 2002;
  • 122 control room chiller and air handler PM, and chilled water pump seal replacement on August 26, 2002; and
  • 22 RHR pump following annual PM on September 19, 2002.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed selected surveillance tests and/or reviewed test data to verify that the equipment performance met Surveillance Procedure (SP) acceptance criteria.

The inspectors verified that the tested equipment was capable of performing its intended safety functions as described in TSs and the USAR. The inspectors verified that the testing met the required TS frequency; that the tests were conducted in accordance with the applicable procedures; that operators met prerequisites and established the proper plant conditions; and that the results of the tests were properly reviewed and recorded.

In addition, the inspectors reviewed several ARs to verify that the licensee was identifying surveillance problems at an appropriate threshold, and that corrective actions commensurate with the significance of the issue were identified and implemented. A detailed list of the documents reviewed during this inspection is included at the end of the report.

The following tests were observed and/or evaluated:

  • SP 2102, 22 Turbine-Driven AFW Pump Monthly Test on July 24, 2002;
  • SP 1093, D1 Diesel Generator Monthly Slow Start Test on September 9, 2002;
  • SP 1106A, 12 Diesel Cooling Water Pump Monthly Test on September 12, 2002;
  • SP 2307, D6 Diesel Generator 6-Month Fast Start Test on September 16, 2002; and
  • SP 2295, D5 Diesel Generator 6-Month Fast Start Test on September 30, 2002.

b. Findings

No findings of significance were identified.

SAFEGUARDS

Cornerstone: Physical Protection

3PP3 Response to Contingency Events (71130.03)

a. Inspection Scope

The Office of Homeland Security developed a Homeland Security Advisory System (HSAS) to disseminate information regarding the risk of terrorist attacks. The HSAS implements five color-coded threat conditions with a description of corresponding actions at each level. NRC Regulatory Information Summary (RIS) 2002-12a, dated August 19, 2002, NRC Threat Advisory and Protective Measures System, discusses the HSAS and provides additional information on protective measures to licensees.

On September 10, 2002, the NRC issued a Safeguards Advisory to reactor licensees to implement the protective measures described in RIS 2002-12a in response to the Federal government declaration of threat level Orange. Subsequently, on September 24, 2002, the Office of Homeland Security downgraded the national security threat condition to Yellow and a corresponding reduction in the risk of a terrorist threat.

The inspectors interviewed licensee personnel and security staff, observed the conduct of security operations, and assessed licensee implementation of the threat level Orange protective measures. Inspection results were communicated to Region III and Headquarters security staff for further evaluation.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

a. Inspection Scope

The inspectors reviewed the performance indicator data submitted by the licensee for completeness and accuracy, and to verify that the licensee had reported data in accordance with the guidance provided by the Nuclear Energy Institute (NEI). The inspectors reviewed documents listed at the end of this report for performance indicator data for initiating events, mitigating systems, and barrier integrity cornerstones. The inspectors reviewed the following performance indicators from the 3rd quarter 2001 through the 2nd quarter 2002:

  • Safety system functional failures on July 31, 2002;

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Failure to Correct Deficiencies Involving Potential Flow Diversion Paths

a. Inspection Scope

On August 6, 2002, during a selected issues followup inspection of corrective actions to address potential Appendix R flow diversion paths concerns, the inspectors identified that specified corrective action to implement modifications and/or administrative controls to resolve flow diversion issues were not completed.

b. Findings

The inspector identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI, for failure to correct deficiencies adverse to quality involving potential flow diversion paths.

These deficiencies had existed since 1999, but had not been corrected. Additionally, no compensatory actions had been established to address these flow diversion paths.

The licensee issued Condition Report (CR) 19982008 and LER 1-98-15 to identify and report concerns associated with the effects of potential spurious opening of the Unit 1 and Unit 2 containment sump B to RHR motor-operated valves. Specifically, it was noted that if any pair of the valves were to spuriously open during a fire, the RWST would drain to the containment sump leaving a less than required volume of borated water available for make-up. In fire protection terminology, this type of issue is referred to as a flow diversion issue, since the diversion of flow may potentially affect safe shutdown capability in the event of a fire.

As a result of the LER, the licensee issued two specific corrective action items to address generic concerns associated with this issue. The first action item required the licensee to review the Appendix R safe shutdown list against the appropriate flow diagrams to ensure that all other flow paths vulnerable to diversion were included in the Safe Shutdown

Analysis.

The second action item was to implement modifications and/or administrative controls to resolve this issue (and any other flow diversion issues identified subsequent to the LER). The second action item had not been completed as of August 6, 2002.

The first action item was completed and closed in 1999. The results of the review of flow diversion pathways was documented and issued as calculations GEN-PI-034, 035, 036, 037, 038, and 040. These calculations identified a large number of safe shutdown required flow diversion components. However, the calculations ambiguously stated in their Conclusion sections, Those components not previously identified are indicated with a note in the attached table. Subsequent analysis may show that some of the components can be eliminated from the Appendix R component list. The calculations were extremely conservative and identified all potential flow diversion paths. Because of this, compensatory measures were never established for the potential flow paths. Since the engineering staff knew that the calculations were extremely conservative, the licensee decided to wait and perform the second action item to implement modifications and/or administrative controls to resolve this issue (and any other flow diversion issues identified subsequent to the LER) as specific flow paths were identified.

Since the calculations identified required flow diversion paths, the NRC inspector asked the licensee why compensatory actions were not in place. As a result of this questioning, the licensee documented this issue in their corrective action program as AR CAP 024536. In AR CAP 024536, the licensee stated that the calculations were potentially misleading and do not meet the original intention behind their issuance, they should be canceled. Subsequently, all six calculations were canceled.

The flow diversion review committed to in LER 1-98-15 was to identify if any flow diversion paths existed. An additional corrective action document was initiated by the licensee, AR CAP 024537, which documented that this LER action item was inappropriately closed, since the calculations did not fully address the LER commitment.

Also, AR CAP 024537 recommended that the action item either be reopened or a new action item be entered to track the eventual completion of this commitment.

As a result, subsequent to the NRC identifying these issues, the licensee performed another review of flow diversion paths. While this review was again conservative, the licensee had procedure actions and guidance that would address spurious operations in these flow diversion paths in the event of a fire.

Criterion II of 10 CFR Part 50, Appendix B, requires that the licensee establish a quality assurance program. It states, This program shall be documented by written policies, procedures, or instructions and shall be carried out throughout plant life in accordance with those policies, procedures, or instructions.

The Prairie Island Quality Assurance Plan Appendix C implements Quality Assurance requirements for the Fire Protection Program. Section 12.2 states that work control process procedures shall be used to correct equipment failure, malfunctions, deficiencies, and defective components of fire protection systems.

In 10 CFR Part 50, Appendix B, Criterion XVI, it states that Measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to Criterion XVI of 10 CFR Part 50, Appendix B, deficiencies adverse to quality involving potential flow diversion paths were known to exist since 1999, but were not corrected. Additionally, no compensatory measures for these deficiencies were established to address these flow diversion paths.

This finding is more than minor because, if left uncorrected, the finding would become a more significant safety concern. Failure to resolve fire protection non-compliance items and failure to establish appropriate compensatory measures could potentially affect the availability, reliability, and capability of fire protection safe shutdown equipment and response efforts. This finding was not suitable for SDP analysis. However, this issue has very low safety significance (Green) because the probability of having a fire event in the affected areas such that the fire would cause more than one valve to reposition to cause a flow diversion was very low. Since the licensee entered this finding into their corrective action program with AR CAP 024536 and AR CAP 024537, this violation is being treated as an NCV in accordance with VI.A.1 of the NRCs Enforcement Policy (NCV 50-282/306/02-08-03) .

.2 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action system at an appropriate threshold, that corrective actions were performed in a timely manner, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action system as a result of inspectors observations are generally denoted in the report.

b. Findings

No findings of significance were identified.

4OA3 Event Followup

(Closed) LER 1-02-01: Condition Prohibited by TSs Due to Potential for Auxiliary Building Special Vent Zone Boundary Degradation.

The LER concerns a modification during plant construction in 1973 to the hot chemistry lab ventilation, which was within the auxiliary building special ventilation zone (ABSVZ).

The modification supplied ventilation to the lab from the turbine building. If the lab doors were open during an accident that generated a safety injection signal, the lab supply booster fans, which do not receive a trip signal on a safety injection, would continue to supply air, affecting the ability of the ABSVZ system to perform its required functions to maintain a negative pressure. Technical Specification 3.6.E.2 requires that openings in the ABSVZ be under direct administrative control and be reduced to less than 10 square feet within 6 minutes following an accident. Contrary to the above, the hot chemistry lab doors were not under direct administrative control. The licensee entered this condition into their corrective action program with AR CAP 024185. The inspectors reviewed this licensee-identified finding and determined that it met the criteria to be considered a NCV of TS 3.6.E.2 (see Section 4OA7). The finding was screened by the inspectors using the SDP and determined to be of very low safety significance since the finding only represents a degradation of the radiological barrier function provided for the auxiliary building. No new significant issues were identified during the review of the LER.

Inspectors verified that the licensee implemented immediate actions to place the hot chemistry lab doors under direct administrative control by adding them into the ABSVZ boundary control log.

4OA5 Other Activities

.1 Review of Institute of Nuclear Power Operations Report

On September 13, 2002, the inspectors completed a review of the final report, dated July 2002, for the Institute of Nuclear Power Operations, November 2001 Evaluation.

4OA6 Meeting(s)

.1 Exit Meeting

The resident inspectors presented the inspection results to Mr. M. Nazar and other members of licensee management at the conclusion of the inspection on September 27, 2002. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violation

The following violation of very low significance was identified by the licensee and is a violation of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.

Cornerstone: Reactor Safety

Technical Specification 3.6.E.2 states that openings in the ABSVZ are permitted provided they are under direct administrative control and can be reduced to less than 10 square feet within 6 minutes following an accident. As described in AR CAP 024185 and LER 1-02-01, on July 16, 2002, the licensee identified that there were no direct administrative controls associated with the hot chemistry lab doors. A 1973 design change to the hot chemistry lab ventilation could affect the ability of the ABSVZ system to perform its required functions to maintain a negative pressure with these doors open.

The finding was determined to be of very low safety significance since the finding only represented a degradation of the radiological barrier function provided for the auxiliary building.

KEY POINTS OF CONTACT Licensee T. Amundson, Manager Business Support P. Huffman, Manager of System Engineering B. Jefferson, Director Site Operations J. Jensen, Production Planning Manager A. Johnson, General Superintendent Radiation Protection and Chemistry J. Kivi, Licensing Engineer R. Lingle, Operations Manager M. McKeown, Manager of Design Engineering L. Meyer, General Superintendent Plant Maintenance M. Nazar, Site Vice President S. Northard, Director of Engineering J. Waddell, Superintendent Security M. Werner, Plant Manager R. Womack, Manager of Engineering Programs LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened 50-282/306/02-001-00 LER Condition Prohibited by TSs Due to Potential for Auxiliary Building Special Vent Zone Boundary Degradation (Section 4OA3)50-282/306/02-08-01 FIN Inappropriate Maintenance Rule Safety Significance Classification of the External Circulating Water Intake Screen Bypass Gates (Section 1R12.1)50-282/306/02-08-02 URI Maintenance Rule Functional Failure Evaluation of Bypass Gate Failures (Section 1R12.1)50-282/306/02-08-03 NCV Failure to Correct Deficiencies Adverse to Quality Involving Potential Flow Diversion Paths (Section 4OA2.1)

Closed 50-282/306/02-001-00 LER Condition Prohibited by TSs Due to Potential for Auxiliary Building Special Vent Zone Boundary Degradation (Section 4OA3)50-282/306/02-08-01 FIN Inappropriate Maintenance Rule Safety Significance Classification of the External Circulating Water Intake Screen Bypass Gates (Section 1R12.1)50-282/306/02-08-03 NCV Failure to Correct Deficiencies Adverse to Quality Involving Potential Flow Diversion Paths (Section 4OA2.1)

Discussed None.

LIST OF ACRONYMS USED ABSVZ Auxiliary Building Special Ventilation Zone ACE Apparent Cause Evaluation ADAMS Agencywide Documents Access and Management System AFW Auxiliary Feedwater AR Action Request AWI Administrative Work Instruction CAP Corrective Action Program CE Condition Evaluation CFR Code of Federal Regulations CR Condition Report DBD Design Bases Document DDCLP Diesel-Driven Cooling Water Pump FIN Finding HSAS Homeland Security Advisory System IMC Inspection Manual Chapter INPO Institute of Nuclear Power Operations IPEEE Individual Plant Examination of External Events IR Inspection Report LCO Limiting Conditions for Operation LER Licensee Event Report MOV Motor Operated Valve NCV Non-Cited Violation NEI Nuclear Energy Institute OOS Out-of-service OPR Operability Recommendation OWA Operator Workaround PARS Publicly Available Records PINGP Prairie Island Nuclear Generating Plant PM Preventive Maintenance RHR Residual Heat Removal RIS Regulatory Information Summary RWST Refueling Water Storage Tank SDP Significance Determination Process SI Safety Injection SP Surveillance Procedure TS Technical Specification USAR Updated Safety Analysis Report NRC U.S. Nuclear Regulatory Commission WO Work Order LIST OF

DOCUMENTS REVIEWED

1R04 Equipment Alignment

Cooling Water System

TS 3.3-7 Cooling Water System Revision 131

USAR 10.4.1 Cooling Water System Revision 22

Plant Procedure B35 Cooling Water System Revision 5

Integrated Checklist Cooling Water System Revision 21

C1.1.35-3

Operating Procedure C35 Cooling Water System Revision 48

WO 0203427 Remove T Mod 00T076 April 3, 2002

AR CAP 000060 121 CLP Bearing Seal Water Filter Changes March 27, 2002

AR CAP 023610 Bearing Water Flow to Lineshaft and May 27, 2002

Suction Bell Less than 50%

AR CAP 023779 Unable to Make Bearing Water Flow June 10, 2002

Adjustments on DDCLP Flows

AR CAP 024661 12 DDCLP Declared Inoperable August 15, 2002

AR CAP 024393 High Risk Work Not Complete As August 31, 2002

Scheduled

D1 Emergency Diesel

Generator

Integrated Checklist D1 Diesel Generator Valve Status Revision 19

C1.1.20.7-1

Integrated Checklist D1 Diesel Generator Auxiliaries and Room Revision 8W

C1.1.20.7-2 Cooling Local Panels

Integrated Checklist Diesel Generator D1 Main Control Room Revision 13

C1.1.20.7-3 Switch and Indicating Light Status

Integrated Checklist D1 Diesel Generator Circuit Breakers and Revision 11

C1.1.20.7-4 Panel Switches

TS 3.7 Auxiliary Electrical Systems Revision 110

USAR Section 8.4 Plant Standby Diesel Generator Systems Revision 23

AR CAP 024968 Pressure Indicator 11079, 21 Heater Drain August 30, 2002

Tank Pump Discharge Pressure Indicator

Was Isolated During WO 0205739

1R05 Fire Protection

Area Walkdowns

Plant Safety Procedure Fire Strategies for Fire Areas 13, 18, 35, 36, Revision 7

F5, Appendix A 69, 101, and 102

IPEEE NSPLMI-96001 Internal Fires Analysis Revision 2

Appendix B

Plant Safety Procedure Fire Hazard Analysis for Fire Areas 13, 18, Revision 16

F5, Appendix F 35, 36, 69, 101, and 102

AR CAP 024122 Transient Combustibles Stored In Safety- July 11, 2002

Related Area, Repeat Occurrence

AR CAP 025395 Pressure Switch Communication Failure September 23,

With Fire Panel 2002

Fire Brigade Drill

Plant Safety Procedure Fire Drills Revision 8

F5, Appendix J

Plant Safety Procedure Fire Detection Zone 83 Revision 8

F5, Appendix A

1R011 Licensed Operator Requalification Program

USAR 14.5.4 Steam Generator Tube Rupture Revision 22

Procedure 1E-0 Reactor Trip or Safety Injection Revision 21

NRC Inspection Report Prairie Island Nuclear Generating Plant January 17, 2002

NRC Inspection Report 50-282/01-18;

50-306/01-18

AR CAP 000232 November 2001 INPO [Institute of Nuclear December 18,

Power Operations] Evaluation 2001

Simulator Team Simulator Team Evaluation September 4,

Evaluation PITCQ-83 2002

1R12 Maintenance Rule Implementation

Repeat Failure of External

Circulating Water Intake

Bypass Gates

Root Cause Investigation Decreasing Intake Canal Level Due to Revision 0

Report 000171 Failure of the Intake Traveling Screens

Plant Procedure H24 Prairie Island Nuclear Generating Plant Revision 4

Maintenance Rule Program

Prairie Island Nuclear Generating Plant Revision 3

Maintenance Rule System Specific Basis

Document, External Circulating Water

Section

Prairie Island Nuclear Generating Plant

Maintenance Rule Scope Determination and

Performance Criteria Spreadsheet

Prairie Island Nuclear Generating Plant

Quarterly Equipment Performance Report,

2nd Quarter 2002

AR CAP 023908 Decreasing Intake Bay Levels Due to Loss June 19, 2002

of Intake Screens

AR MRE 000014 Maintenance Rule Evaluation of Intake June 20, 2002

Screens and Bypass Gates

AR CAP 023958 121 Bypass Gate Failed to Open with Loss June 24, 2002

of Control Power

AR CAP 023959 122 Bypass Gate Failed to Open with Loss June 24, 2002

of Control Power

AR CAP 009179 Need Acceptance Criteria for Operability of September 3,

Intake Bypass and Screens 2001

AR CAP 024744 Maintenance Rule Performance Criteria for August 20, 2002

Screenhouse Bypass Gates Not In

Accordance With the Guidance of

NUMARC 93-01

AR ACE 008543 Apparent Cause Evaluation of CAP 024744 August 22, 2002

AR CAP 024391 Unsatisfactorily Completed Test August 30, 2002

Procedure 2537

AR CAP 025146 Failure of Test Procedure 2537 September 11,

2002

Failure of CV 39201,

11/13 Containment Fan

Cooling Unit Cooling

Water Return Bypass

Control Valve

5AWI 3.2.10 Investigation and Troubleshooting Revision 7

5AWI 3.12.0 Nuclear Plant Maintenance Revision 10

USAR, Section 10.4.1 Cooling Water System Revision 22

Flow Diagram Unit 1 Cooling Water - Auxiliary Building Revision R

NF-39216-3

AR CAP 023812 CV 39201, 11/13 Containment Fan Cooling June 12, 2002

Unit Cooling Water Return Bypass Control

Valve Found Open

AR MRE 000010 Maintenance Rule Evaluation of CV-39201 June 13, 2002

Failure

AR CE 000405 Condition Evaluation of CAP 023812 June 13, 2002

WO 0205407 Investigate and Repair CV 39201 June 13, 2002

WO 0108187 Investigate and Repair CV 39201 July 9, 2001

WO 0107267 Investigate and Repair CV 39201 May 14, 2002

Prairie Island Nuclear Generating Plant Revision 3

Maintenance Rule System Specific Basis

Document, Cooling Water Section

1R13 Maintenance Risk Assessments and Emergent Work Control

SI Pump with 22 RHR

Pump and Heat

Exchanger Out-of-service

TS 3.3.A Safety Injection and Residual Heat Removal Revision 161

Systems

TS 4.2 Inservice Inspection and Testing of Pumps Revision 60

and Valves Requirements

WO and Work Plan 22 SI Pump Has a Leak on the Pump Head September 9,

202701 2002

10CFR50.59 Screening NMC Standard 10 CFR 50.59 Screening Revision 0

No. 1567

ENG-ME-525 Calculation Revision 0

Unit 2 Configuration Risk Assessment September 17,

2002

Turbine-Driven AFW

Pump Surveillance with

25 Air Compressor Out-

of-service

Unit 2 Configuration Risk Assessment September 17,

2002

Turbine-Driven AFW

Pump Testing with 122

Control Room Chiller Out-

of-service

Plant Procedure H24.1 Assessment and Management of Risk Revision 4

Associated with Maintenance Activities

Risk Assessment for Work Week 2B33 August 20, 2002

Motor-Driven AFW

Pump Check Valve

Testing with Train A ICCM

Out-of-service

Unit 2 Configuration Risk Assessment July 10, 2002

DDCLP Emergent

Work

Operation Log Entries August 14, 2002

Plant Status Report August 15, 2002

Open Limiting Conditions for Operation August 15, 2002

(LCO) Log

Motor-Driven AFW

Pump Failed Surveillance

Operation Log Entries August 30, 2002

Plant Status Report August 30, 2002

Open LCO Log August 30, 2002

AR CAP 024946 12 Motor-Driven AFW Pump Failed SP 1000 August 30, 2002

Due to Sluggish Motor Slinger Ring

Operation

AR CAP 024956 12 Motor-Driven AFW Pump Made August 30, 2002

Unavailable When in an Indeterminate

Condition

D2 Diesel Generator, 18

Inverter, 11 Charging

Pump, and 12 Motor-

Driven AFW Pump Out-

of- Service

Operations Log Entries August 26, 2002

Open LCO Log August 25, 2002

Unit 1 Configuration Risk Assessment August 25, 2002

1R14 Non-Routine Evolutions

Root Cause Investigation Decreasing Intake Canal Level Due to Revision 0

Report 000171 Failure of the Intake Traveling Screens

AR CAP 023908 Decreasing Intake Bay Levels Due to Loss June 19, 2002

of Intake Screens

AR CAP 023958 121 Bypass Gate Failed to Open with Loss June 24, 2002

of Control Power

AR CAP 023959 122 Bypass Gate Failed to Open with Loss June 24, 2002

of Control Power

Operations Control Room Logs June 19, 2002

Plant Procedure C41.5 Emergency Response Computer System Revision 16

Operating Procedure Alarms, Displays, and

Responses, Computer Alarm 26

Plant Procedure C25 Circulating Water System Revision 23

C91802 Annunciator Response Procedure for Revision 1

External Circulating Water Remote

Panel 91802, High Traveling Screen

C47501 Annunciator Response Procedure for Revision 22

Control Room Panel 47501, Alarm 47501-

0101, Intake Screenhouse Traveling Screen

High Differential Pressure

1R15 Operability Evaluations

Unit 2 Reactor Missile

Shield Weight

USAR 12.2, Table 12.2- Loads Handled Over Safety Related Revision 23

Components, Components Required for

Plant Shutdown or Decay Heat Removal

Plant Procedure D58 Heavy Loads Program Revision 30

AR CAP 023549 U2 Reactor Missile Shield Weight Measured May 19, 2002

74,500 Pounds Versus SAR Listed Weight

of 56, 200 Pounds

AR CE 000266 Determine Extent of Condition Regarding May 30, 2002

the Weight of the U2 Reactor Missile Shield

Auxiliary Building Special

Ventilation Boundary

TS 1.0 and 3.6.E Auxiliary Building Special Ventilation Zone Revision 111 and

Integrity 91

USAR 10.3.4 Auxiliary Building Special Ventilation System Revision 23

Plant Procedure B19 Containment Systems Revision 6

Plant Procedure D54 Control of Openings in the Auxiliary Building Revision 13

Special Ventilation Zone Boundary

AR CAP 024185 ABSVZ Boundary at Hot Chem Lab July 16, 2002

AR OPR 000324 Operability Recommendation for Auxiliary July 17, 2002

Building Special Vent Zone Boundary Issue

and 22 DDCLP

Oscillations

USAR, Section 10.4.1 Cooling Water System Revision 22

TS 3.3-7 Cooling Water System Revision 131

Operating Procedure C35 Cooling Water System Revision 48

Plant Procedure B35 Cooling Water System Revision 5

DBD SYS-35 Design Basis Document for the Cooling Revision 4

Water System

AR CAP 024010 Sluggish Governor Response on 22 Diesel June 28, 2002

Driven Cooling Water Pump

AR CE 000500 Condition Evaluation of AR CAP 024010 July 1, 2002

AR ACE 008426 Apparent Cause Evaluation June 13, 2002

Operation of the 21 AFW

Pump with Insufficient

Packing Leakoff

USAR Section 11.9.2.2 Auxiliary Feedwater System Revision 23

XH-258-24 Auxiliary Feedwater Technical Manual

Condition Report Notebook Issue #

20000592

AR CAP 024541 No Seal Leakage During Run of SP 2100, August 8, 2002

Auxiliary Feedwater Pump

Containment Fan

Cooling Unit High

Vibrations

AR CAP 024294 Containment Fan Cooling Unit Vibration in July 23, 2002

Alert Range at 5 Mils in Fast Speed

AR CE 000637 Condition Evaluation of AR CAP 024294 July 25, 2002

AR OPR 000327 Operability Recommendation of July 25, 2002

AR CAP 024294

Containment Fan Cooling Unit Inspection August 7, 2002

Summary

USAR, Section 6.3.2 Containment Air Cooling System Design Revision 22

and Operation

Grid Security Analysis for

the Prairie Island Two

Unit Trip Contingency

Failed

AR CAP 024732 Low Grid Voltage, Security Analysis Failure August 19, 2002

to Satisfy Two Unit Trip Contingency

AR OPR 000330 Operability Recommendation of August 20, 2002

AR CAP 024732

AR CAP 023977 Guidance for Response to Security Analysis June 25, 2002

Alarm Needs Improvement

TS 3.7 Auxiliary Electrical Systems Revision 110

USAR, Section 8.2 Transmission System Revision 23

Inadequate Thread

Engagement on 22 SI

Pump Suction Flange

Bolts

AR CAP 025410 22 Safety Injection Pump Suction Flange September 24,

Bolts Do Not Meet D63 Requirements 2002

Plant Procedure D63 Installation Guidelines for Threaded Revision 9W

Fasteners (Studs or Bolts)

Calculation ENG-CS-080 Acceptable Thread Engagement

1R16 OWAs

Station Battery

Charger

Operator Workarounds August 7, 2002

CR 19971622 Intermittent Operation During SP 1083 December 5, 1997

CR 19991958 Intermittent Operation During SP 1083 June 6, 1999

Safety Evaluation 534 Station Battery Charger Current Limit Revision 0,

Setpoint Change April 12, 1999

Safety Evaluation 534 Station Battery Charger Current Limit Revision 1,

Setpoint Change August 10, 1999

SP 1083 Integrated SI Test With a Simulated Loss of Revision 26W

Offsite Power

Cumulative Effects of

OWAs

5AWI 3.10.8 Equipment Problem Resolution Process Revision 0

Prairie Island Nuclear Minutes #2714 August 7, 2002

Generating Plant (PINGP)

Operation Committee

Meeting Minutes

1R19 Post Maintenance Testing

Diesel-Driven Cooling

Water Pump

TS 3.3.D Cooling Water Systems Revision 131

USAR 10.4.1 Cooling Water System Revision 22

Plant Procedure B35 Cooling Water System Revision 5

SP 1106B 22 Diesel Cooling Water Pump Monthly Test Revision 58

WO 0202848 SP 1106B 22 Diesel Cooling Water Pump July 29, 2002

Monthly

RWST to SI Header

Isolation Valve MV-32182

TS 3.3.A.2.d Safety Injection and Residual Heat Removal Revision 161

Systems

USAR 6.2 Safety Injection System Revision 22

Plant Procedure B18A Safety Injection System Revision 4

WO 0110007 Refueling Water to Safety Injection Pumps July 29, 2002

Header Isolation Motor Valve A

RHR Pump

TS 3.3.A Safety Injection and Residual Head Revision 161

Removal Systems

USAR 6.2.2.2.4 Safety Injection and Residual Heat Removal Revision 22

Pumps

Plant Procedure H10.1 ASME Inservice Testing Implementing Revision 12

Program

Plant Procedure B15 Residual Heat Removal System Revision 7

WO 0202361 P3124-1-21 21 RHR Pump Annual July 16, 2002

Inspection

WO 0204146 SP 2089AL Light Verification During August 7, 2002

SP 2089A

WO 0204145 SP 2089A RHR Pump and Suction Valves August 7, 2002

from the RWST

2 Control Room Chiller

and Air Handler

WO 0100313 Replace Mechanical Seals and Inspect

Chilled Water Pump

WO 0111036 122 Control Room Chiller Electrical Breaker

15-Year PM

WO 0202368 122 Control Room Chiller Annual Inspection

WO 0202370 6-Month Inspection of Control Room Air

Handling Unit

WO 0202371 12-Month Inspection of Control Room Air

Handling Unit

WO 0202635 Leak Check 122 Control Room Chiller

WO 0203915 Control Room Train B Chilled Water Pump

Test

WO 0203943 Alternating In-Service Control Room Chillers

WO 9406919 Change Wire Codes at Pump Push Button

Station

Drawing NF-39603-1 Admin Bldg, Screen House, and Control Revision AL

Room Flow Diagram

Drawing NF-40890-3 External Connections Motor Control Center Revision N

1T

TS 3.13 Control Room Air Treatment System Revision 91

TS 4.14 Control Room Air Treatment System Tests Revision 91

USAR 10.3.3 Control Room Ventilation System Revision 23

D2 Diesel Generator 6-

Month Inspection

PM 3001-2-D2 D2 Diesel Generator 18-Month Inspection Revision 17

PM 3001-4-D2 D2 Diesel Generator Inspection Electrical Revision 5

SP 1306 D2 Diesel Generator 18-Month Relay Revision 6

Functional Test

SP 1307 D2 Diesel Generator 6-Month Fast Start Revision 22

Test

TS 3.7 Auxiliary Electrical Systems Revision 110

TS 4.6 Periodic Testing of the Emergency Power Revision 91

System

1R22 Surveillance Testing

Turbine-Driven AFW

Pump Monthly Test

TS 3.4.B Auxiliary Feedwater System Revision 123

TS 4.8.A Auxiliary Feedwater System Revision 116

USAR 1.9 Condensate, Feedwater and Auxiliary Revision 23

Feedwater Systems

Plant Procedure B28B Auxiliary Feedwater System Revision 5

SP 2102 22 Turbine-Driven AFW Pump Monthly Test Revision 69

D1 Diesel Generator

Monthly Slow-Start Test

TS 3.7 Auxiliary Electrical Systems Revision 110

TS 4.6 Periodic Testing of Emergency Power Revision 147

System

Plant Procedure B38A Unit 1 Diesel Generators Revision 5

SP 1093 D1 Diesel Generator Monthly Slow Start Revision 73

Test

Diesel Cooling Water

Pump Monthly Test

TS 3.3.D Cooling Water System Revision 131

TS 4.2 Inservice Inspection and Testing of Pumps Revision 60

and Valves Requirements

TS 4.5.B.1.b Component Test, Pumps Revision 161

USAR 10.4.1 Cooling Water System Revision 22

Plant Procedure B35 Cooling Water System Revision 5

SP 1106A 12 Diesel Cooling Water Pump Monthly Test Revision 61

AR CAP 025178 12 Diesel Driven Cooling Water Pump September 12,

2002

AR CAP 025186 12 DDCLP Fell in the Performance Curve September 12,

Alert Range During 9/12/02 Run 2002

D6 Diesel Generator 6-

Month Fast-Start Test

TS 4.6.A.2 Periodic Testing of Emergency Power Revision 113

System

Operating Procedure D5/D6 Fuel Oil System Revision 16

2C38

SP 2307 D6 Diesel Generator 6 Month Fast Start Revision 17

Test

AR CAP 025281 Positive Glycol Test D5 Engine 2 September 18,

2002

AR CAP 025334 WO to Fill D6 Coolant Expansion Tanks September 20,

Issued While Monthly Diesel Run In 2002

Progress

AR CAP 025241 Discrepancy Between SP 2305 and September 16,

SP 2307 for 2LI-6011A for Acceptance 2002

Criteria

D5 Diesel-Driven

Generator 6-Month Fast-

Start Test

TS 3.7 Auxiliary Electrical Systems Revision 110

TS 4.6.A.2 Periodic Testing of Emergency Power Revision 113

System

Plant Procedure B38C Unit 2 Diesel Generators Revision 2

SP 2295 D5 Diesel Generator 6-Month Fast Start Revision 23

Test

WO 0206045 SP 2295 D5 Diesel Generator 6-Month Fast September 30,

Start Test 2002

AR CAP 025506 D5 Generator Stator Temperature September 30,

Channel 3 Failed 2002

AR CAP 025507 SP 2295 D5 Fast Start Scheduled When D5 September 30,

1B Was Scheduled OOS [Out-of-service] 2002

AR CAP 025515 D5 2A Air Dryer Dust Filter Drain Plugged October 1, 2002

4OA1 Performance Indicator Verification

Safety System Functional Failure

LER 1-01-02 Auto Activation of Unit 1 4160 Volt Revision 0

Safeguards Bus 16 Source Sequencer

Following Grid Disturbance Caused by

Severe Weather

LER 1-01-03 Plant In Unanalyzed Condition Due To Revision 0

Flood Panel Deficiencies

LER 1-01-03 Plant In Unanalyzed Condition Due to Flood Revision 1

Panel Deficiencies

LER 1-01-04 Water Intrusion Into a Control Rod Electrical Revision 0

Cabinet Results in Dropped Rods Causing a

Negative Flux Reactor Trip

LER 1-01-05 Fault and Fire in Non-Safeguards Circuit Revision 0

Breaker Results in Reactor Trip and

Auxiliary Feedwater Actuation

LER 1-01-06 Security Responders Out of Position Due to Revision 0

Plant Fire

LER 2-01-01 Failure to Meet TS Limiting Condition for Revision 0

Operation Verification Within Eight Hour

Limit Due to Personnel Error

LER 2-01-02 Emergency Diesel Generator Out-of-service Revision 0

Longer Than TS Allowed Outage Time

LER 2-01-03 Technical Specification Required Shutdown Revision 0

of Unit 2 Due to Declared Inoperability of

Both Emergency Diesel Generators

LER 2-01-03 Technical Specification Required Shutdown Revision 1

of Unit 2 Due to Declared Inoperability of

Both Emergency Diesel Generators

LER 2-01-03 Technical Specification Required Shutdown Revision 2

of Unit 2 Due to Declared Inoperability of

Both Emergency Diesel Generators

LER 2-01-04 Manual Turbine Trip/Reactor Trip Due to Revision 0

High Differential Condenser Backpressure

LER 2-01-05 Manual Reactor Trip on Unit 2, Initiated in Revision 0

Response to a High Differential Pressure

Between the Turbine Steam Condensers,

Caused By an Inadvertent Venting of One

Condenser While Isolating a Steam Leak

Operator Logs from April 1, 2001, to

March 31, 2002

NEI 99-02 Regulatory Assessment Performance Revision 2

Indicator Guideline

Prairie Island Nuclear Generating Plant 2nd Quarter 2001

Quarterly Equipment Performance Report

Prairie Island Nuclear Generating Plant 3rd Quarter 2001

Quarterly Equipment Performance Report

Prairie Island Nuclear Generating Plant 4th Quarter 2001

Quarterly Equipment Performance Report

Prairie Island Nuclear Generating Plant 1st Quarter 2002

Quarterly Equipment Performance Report

Plant Procedure H33 Performance Indicator Reporting Revision 5

Plant Procedure H33.3 Safety System Functional Failure Revision 0

Performance Indicator Reporting

Instructions

PINGP Form 1318C Performance Indicator-Safety System 2nd Quarter 2001

Functional Failure

PINGP Form 1318C Performance Indicator-Safety System 3rd Quarter 2001

Functional Failure

PINGP Form 1318C Performance Indicator-Safety System 4th Quarter 2001

Functional Failure

PINGP Form 1318C Performance Indicator-Safety System 1st Quarter 2002

Functional Failure

Reactor Coolant System

Specific Activity

TS 3.1-10 Maximum Coolant Activity Revision 147

SP 1057 Unit 1 Reactor Coolant Monthly Revision 17

Radiochemical Analysis

Unit 1 Radiochemistry Report July 1, 2001 to

May 31, 2002

Unit 2 Radiochemistry Report July 1, 2001 to

May 31, 2002

NEI 99-02 Regulatory Assessment Performance Revision 2

Indicator Guideline

Unplanned Power

Changes

NEI 99-02 Regulatory Assessment Performance Revision 2

Indicator Guideline

Plant Procedure H33.2, Data Sheets 3rd Quarter 2001 to 2nd Quarter Revision 3

Figure 1 2002

PINGP Form 1318A Data Sheets 3rd Quarter 2001 to 2nd Quarter Revision 0

2002

4OA2 Identification and Resolution of Problems

LER 1-98-15 Containment to RHR MOVs [Motor 10/26/98

Operated Valves] Appendix R Safe

Shutdown Analysis Issues

CR 19982008 FPFI [Fire Protection Functional Inspection] 9/25/98

Question FP-I072: Sump B to RHR MOVs

Not on SSEL [Safe Shutdown Equipment

List]. Can NPSH [Net Positive Suction

Head] be obtained if these MOVs spuriously

open due to a fire?

GEN-PI-034 Appendix R Equipment List Review - Decay 3/30/99

Heat Removal Function

GEN-PI-035 Appendix R Equipment List Review - RCS 5/25/99

[Reactor Coolant System] Inventory Control

Function

GEN-PI-036 Appendix R Equipment List Review - Safe 5/25/99

Shutdown Support Function

GEN-PI-037 Appendix R Equipment List Review - 5/25/99

Process Monitoring Function

GEN-PI-038 Appendix R Equipment List Review - 7/9/99

Electrical Power Supply Function

GEN-PI-039 Appendix R Equipment List Review - 7/9/99

Containment Integrity Function

AR CAP 024536 Appendix R Equipment List Evaluations 8/7/02

Should Be Canceled

AR CAP 024537 Appendix R Commitment Closed 8/7/02

Prematurely

G

4OA3 Event Followup

AR CAP 024536 Appendix R Equipment List Evaluations 8/7/02

Should Be Canceled

LER 1-02-01 Condition Prohibited by TS Due to Potential September 16,

for Auxiliary Building Special Vent Zone 2002

Boundary Degradation

AR CAP 024185 ABSVZ Boundary at Hot Chem Lab July 16, 2002

AR OPR 000324 Operability Recommendation for Aux July 16, 2002

Building Special Vent Zone Boundary Issue

Plant Procedure D54, Control of Openings in the Aux Building July 25, 2002

Temporary Change Special Ventilation Zone Boundary

Notice 2002-1367

Log Entry Category 1 Special Vent Zone Report September 8,

2002

35