05000348/LER-1982-010: Difference between revisions

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| document report number = LER-82-010-03L, LER-82-10-3L, NUDOCS 8204160428
| document report number = LER-82-010-03L, LER-82-10-3L, NUDOCS 8204160428
| package number = ML20054B205
| package number = ML20054B205
| document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 1
| page count = 1
}}
}}

Latest revision as of 15:11, 15 March 2020

LER 82-010/03L-0:on 820304,during RCS Leakage Test, Unidentified RCS Leak Rate Exceeded Tech Spec Limit.Caused by Packing Leak from Flow Control Valve FCV 122.Packing Adjusted
ML20054B243
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 04/02/1982
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20054B205 List:
References
LER-82-010-03L, LER-82-10-3L, NUDOCS 8204160428
Download: ML20054B243 (1)


LER-2082-010,
Event date:
Report date:
3482082010R00 - NRC Website

text

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' o l 2 l l At 1035 on 3/04/82 during the performance of FNP-1-STP-9.0 (RCS Leakage Test) , it was

! y I a I l determined that the unidentified RCS leak mrate (2_,34_gpA exceeded the tech,Jge_q,__ limit.

ioI.iI LTech.__ Spec. 3.4.6.2_, in p_ art, requires the unidentified RCS leakage _to be less than io Isl t 1 gpm. Tech. Spec. 3.4.6.2 action statement requirements were met. Health / safety of i 5 JT] l the public was not affected.

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! i I t> l i This event was caused by a packing leak from flow control valve FCV 122. The packing _

[ i l i ) } was adj usted and upon satisfactory completion of FNP-1-STP-9.0 the leak rate (.74 gp.m)_

t, ; , i l was determined to be within the tech. spec. limits at 1400 on 3/04/82. Following i i

' l i l ] additional adj ustments to the packing the unidentified RCS leak rate was determined _to_,

, i 1.i ; [ be .19 gpm on 3/07/82. _.

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